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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217N3541999-10-26026 October 1999 Informs That Effective 991026,TF Dragoun Inspector for Licensee Facility ML20217G1111999-10-18018 October 1999 Forwards Results of Operator Initial Exam Conducted at Univ of Michigan on 990719-21.Without Encls ML20217H8731999-10-14014 October 1999 Forwards Initial Exam Rept 50-002/OL-99-01 on 990719-21. NRC Administered Initial Exam to Employees of Facility Who Applied for License to Operate Univ of Michigan Reactor ML20212E1881999-09-22022 September 1999 Responds to 990914 Request for Approval of Alternate Route Plan for Transporting Spent Fuel from University of Michigan Ford Nuclear Reactor to Savannah River Plant,Aiken,Sc. Route in Encl 1 Meets Regulatory Requirements of 10CFR73.37 ML18066A7231999-09-13013 September 1999 Responds to 990616 & 0823 Requests for Approval of Route Plan for Transporting Spent Fuel from Univ of Michigan to Savannah River Plant,Aiken,Sc.Route Set Forth in Encl 1, Meets Regulatory Requirements of 10CFR73.37 ML20195D3951999-06-0707 June 1999 Informs That Author Made Arrangements with B Ducamp,For Administration of Operator Licensing Exams at Univ of Mi Reactor for Week of 990719 ML20195C4771999-05-27027 May 1999 Forwards Insp Rept 50-002/99-201 on 990503-06.No Violations Noted ML20195C0551999-05-25025 May 1999 Forwards Reactor License Application for P Simpson. Certification of Medical Exam by Facility Licensee Encl with License Application.Certification of Medical Exam Withheld ML20206P2891999-05-11011 May 1999 Forwards Revised Rept of Reactor Operation for Jan-Dec 1998 for Ford Nuclear Reactor Michigan Memorial - Phoenix Project Univ of Mi,Ann Arbor, Correcting Omission of Section 5.0 ML20204H6111999-03-24024 March 1999 Ack Receipt of 981214 Request for Approval of Route for Transporting Spent Fuel from Univ of Michigan Ford Nuclear Reactor to Savannah River Plan,Alken,South Carolina. Approval for Route Encl IR 05000002/19980031998-12-11011 December 1998 Submits Suppl to Insp Rept 50-002/98-03 Conducted on 981016-20.Inspectors Reviewed Operating Log Book Entries from 970304-0828,to Verify That Reactor Staffing Met Min Requirements of TSs ML20196A8831998-11-23023 November 1998 Forwards Insp Rept 50-002/98-203 on 981026-30.No Violations Noted.Insp Conducted to Determine Whether Activities Authorized by License Were Conducted Safely & IAW NRC Requirements ML20154E9021998-09-30030 September 1998 Informs That Jc Lee Has Assumed Duties of Interim Director of Michigan Memorial Phoenix Project (Mmpp) at Univ of Mi. All Future Correspondences & Notifications Re Ford Nuclear Fuel Should Now Be Directed to Jc Lee ML20153B9381998-09-18018 September 1998 Informs of Changes Re self-contained Breathing Apparatuses at Univ of Michigan Ford Nuclear Reactor.Changes Do Not Decrease Effectiveness of Emergency Plan Per 10CFR50.54(q) ML20151Z2561998-09-17017 September 1998 Forwards Amend 45 to License R-28,amend 13 to Indemnity Agreement E-24 & Se.Amend Adds License Condition to Allow Greater Flexibility in Receipt & Possession of Byproduct Matl Used to Support Research & Development within Facility ML20237D6691998-08-21021 August 1998 Forwards Ro/Sro License Certificates for Ek Sharp & MW Landis.W/O Encls ML20237B2251998-08-12012 August 1998 Forwards Inital Exam Rept 50-002/OL-98-01 Administered During Week of 980803,to Employees of Facility Who Applied for License to Operate Univ of Michigan Reactor.W/O Encl ML20237A7301998-08-12012 August 1998 Forwards Results of Operator Initial Exam Conducted at Univ of Michigan on 980804-05.W/o Encl ML20249C2321998-06-22022 June 1998 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Notice of Violation on 980513. Finds Corrective Actions Adequate & Have No Further Questions.C/A to Be Examined During Future Insp ML20249A6411998-06-13013 June 1998 Responds to NRC Re Violations Noted in Insp Rept 50-002/98-202.Corrective Actions:Nrc Issued Amend 44 on 980416 Which Puts Licensee in Full Compliance ML20248A4891998-05-26026 May 1998 Discusses Arrangements Made During Telcon Between W Eresian & B Ducamp for Administration of OL Exams Scheduled for Wk of 980803 at Univ of Michigan.Requests One Set of Ref Matl Listed in Enclosure 1 IR 05000002/19982021998-05-13013 May 1998 Discusses Insp Rept 50-002/98-202 on 980223-27 & Forwards Notice of Violation.Open Predecisional Enforcement Conference Conducted in Rockville,Maryland to Discuss Two Violations,Root Causes & Corrective Actions ML20236U0791998-05-0101 May 1998 Requests That Attachment to Indemnity Agreement E-34 Between Univ of Mi & Us Aec,Be Amended by Replacing,In Entirety, Language Under Item 3 - Location W/Listed Sentence,To Make Location Consistent w/R-28 Reactor License ML20217N9961998-04-27027 April 1998 Discusses Predecisional Enforcement Conference Held on 980422 Re Routine Safety Insp Rept 50-002/98-202 ML20217K5361998-04-24024 April 1998 Revised Ltr Forwarding Corrected First Page of SE for Amend 44 to License R-28.Dates in First & Second Paragraphs Has Been Changed to 970930 & Oct 1996.Ltr Revised to Correct Typo ML20217K8611998-04-23023 April 1998 Forwards Corrected First Page of Safety Evaluation for Amend 44.Date in First Paragraph Changed to 970930 & Date in Second Paragraph Changed to Oct 1996 ML20217E3901998-04-22022 April 1998 Responds to NRC Ltr Re Violations Noted in Insp Rept 50-002/98-202 on 980223-27.Corrective Actions:Temporary Operating Instruction to Lower Outlet Temperature Setpoint to 126 F Was Issued on 961008 ML20216J3181998-04-16016 April 1998 Forwards Amend 44 to License R-28 & Safety Evaluation.Amend Revises TSs to Add Coolant Inlet Temperature Rundown ML20217D5311998-03-24024 March 1998 Forwards Insp Rept 50-002/98-202 on 980223-27.Two Apparent Violations Noted & Being Considered for Escalated Enforcement Action.Nrc Concerned Because Violations Reflect Lack of Full Understanding of License Requirements ML20199F7861998-01-27027 January 1998 Ack Receipt of Re Rev 16 to Univ of Michigan Ford Nuclear Reactor Emergency Plan.Nrc Approval Not Required,Based on Determination That Changes Do Not Decrease Effectiveness of Subj Plan ML20199A1521998-01-16016 January 1998 Forwards Insp Rept 50-002/98-201 on 980106-07.No Violations Noted.Insp Consisted of Routine Secruity & Matl Control & Accountability Reviews ML20203B3111997-12-0303 December 1997 Responds to to T Burdick of NRC Re Licensing of by-product Matls Produced at Univ of Michigan Ford Nuclear Reactor in Support of Hssi Program.Suggests Identifying Areas Where Nuclear Matl Handled & Reviewing Emergency Plan ML20199F4141997-11-18018 November 1997 Forwards Certificates Issued to Rl Mvcue & Tj Hall for Becoming Newly Licensed Individuals at Facility ML20203A4941997-11-14014 November 1997 Requests List of Names & Mailing Addresses of State Governor Designees for Advance Notifications of Shipment of Irradiated Reactor Fuel.Univ Shipping Fuel to DOE Site in South Carolina in mid-summer of 1998 ML20211C9161997-09-17017 September 1997 Forwards Results of Operator Initial Exam Conducted at Univ of Michigan on 970818-19.W/o Encl ML20216E8971997-09-0202 September 1997 Forwards SRO Certificate for Weger,Newly Licensed Operator at Univ of Michigan.W/O Encl ML20217P3201997-08-22022 August 1997 Informs That Responsibility for Non-Power Reactor Insp Program Has Been Transferred from Nrr.All Related Repts, Correspondence & Inquires W/Docket Number Specified Should Be Directed to Listed Address ML20217Q8571997-08-14014 August 1997 Notifies of Change of Staff in HP Position at Fnr.Am Jackson Is Being Rotated to HP Position at Univ Hosp & Ht Downey Will Be Taking Over Pml/Fnr HP Position,Effective 970908 ML20196J4311997-07-0202 July 1997 Forwards Rev 16 to Ford Nuclear Reactor Emergency Plan. Rev Corrects Various Minor Typos & Revised Significant Radiation Exposures to Reflect Current 10CFR20 Guidance as Listed ML20148J8151997-06-12012 June 1997 Requests That Material Listed in Encl Be Submitted Including Applications Certifying That All Training Has Been Completed within 14 Days Before Exam ML20141G3571997-05-20020 May 1997 Forwards RO Certificates for MW Landis & Rl Mccue. Certificates Are in Addition to Actual License Issued & Later Renewed as Ltr.W/O Encl ML20137R8271997-04-0909 April 1997 Forwards SRO License Certificates for MW Landis & Rl Mccue. W/O Encl ML20137K3521997-03-25025 March 1997 Forwards Insp Rept 50-002/97-01 on 970224-28.No Violations Noted ML20135F9251997-03-12012 March 1997 Ack Receipt of Transmitting Rev 15 to Emergency Plan.Nrc Approval Not Required Based on Determination That Changes Do Not Decrease Overall Effectiveness of Emergency Plan ML20135F7881997-03-12012 March 1997 Forwards Results of Operator Initial Exam Conducted at Univ of Michigan on 970305.W/o Encl ML20135D9551997-02-28028 February 1997 Forwards Reactor Operator License Exams for R Mccue & M Landis.Exams Need Not Be Administered at Same Time.W/O Encl ML20135C1151997-02-24024 February 1997 Forwards Certificates for Newly Licensed Individuals at University of Michigan.W/O Encl ML20133A2381996-12-26026 December 1996 Forwards Copy of Results of 961209-12 Operator Initial Exam Conducted at Univ of Mi.W/O Encl ML20133B4181996-12-26026 December 1996 Discusses Initial Exams Administered During Wk of 961209 to Employees of Phoenix Memorial Lab Who Had Applied for License to Operate Univ of Michigan Reactor.W/Out Encls ML20134L7301996-11-18018 November 1996 Forwards Senior Operator License Certificate to JW Young.W/O Encl 1999-09-22
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20195C0551999-05-25025 May 1999 Forwards Reactor License Application for P Simpson. Certification of Medical Exam by Facility Licensee Encl with License Application.Certification of Medical Exam Withheld ML20206P2891999-05-11011 May 1999 Forwards Revised Rept of Reactor Operation for Jan-Dec 1998 for Ford Nuclear Reactor Michigan Memorial - Phoenix Project Univ of Mi,Ann Arbor, Correcting Omission of Section 5.0 ML20154E9021998-09-30030 September 1998 Informs That Jc Lee Has Assumed Duties of Interim Director of Michigan Memorial Phoenix Project (Mmpp) at Univ of Mi. All Future Correspondences & Notifications Re Ford Nuclear Fuel Should Now Be Directed to Jc Lee ML20153B9381998-09-18018 September 1998 Informs of Changes Re self-contained Breathing Apparatuses at Univ of Michigan Ford Nuclear Reactor.Changes Do Not Decrease Effectiveness of Emergency Plan Per 10CFR50.54(q) ML20249A6411998-06-13013 June 1998 Responds to NRC Re Violations Noted in Insp Rept 50-002/98-202.Corrective Actions:Nrc Issued Amend 44 on 980416 Which Puts Licensee in Full Compliance ML20236U0791998-05-0101 May 1998 Requests That Attachment to Indemnity Agreement E-34 Between Univ of Mi & Us Aec,Be Amended by Replacing,In Entirety, Language Under Item 3 - Location W/Listed Sentence,To Make Location Consistent w/R-28 Reactor License ML20217N9961998-04-27027 April 1998 Discusses Predecisional Enforcement Conference Held on 980422 Re Routine Safety Insp Rept 50-002/98-202 ML20217E3901998-04-22022 April 1998 Responds to NRC Ltr Re Violations Noted in Insp Rept 50-002/98-202 on 980223-27.Corrective Actions:Temporary Operating Instruction to Lower Outlet Temperature Setpoint to 126 F Was Issued on 961008 ML20203A4941997-11-14014 November 1997 Requests List of Names & Mailing Addresses of State Governor Designees for Advance Notifications of Shipment of Irradiated Reactor Fuel.Univ Shipping Fuel to DOE Site in South Carolina in mid-summer of 1998 ML20217Q8571997-08-14014 August 1997 Notifies of Change of Staff in HP Position at Fnr.Am Jackson Is Being Rotated to HP Position at Univ Hosp & Ht Downey Will Be Taking Over Pml/Fnr HP Position,Effective 970908 ML20196J4311997-07-0202 July 1997 Forwards Rev 16 to Ford Nuclear Reactor Emergency Plan. Rev Corrects Various Minor Typos & Revised Significant Radiation Exposures to Reflect Current 10CFR20 Guidance as Listed ML20129J0281996-10-28028 October 1996 Submits Rev 15 to Ford Nuclear Reactor Emergency Plan ML20057D2321993-09-30030 September 1993 Responds to NRC Re Violations Noted During Insp of Facility.Corrective Actions:Purchased New Model MGS0500 Mixed Gamma Std to Use for Germanium Detector Calibr,Per HP-105.Contests Part of Violation Re Fnr HP Procedures ML20057C5811993-09-15015 September 1993 Forwards Rev 3 of Page 5 of Requalification Program.Rev Makes Requalification Program Consistent W/Requirements of 10CFR55.53(F)(2) Re Extended Absence from Operation ML20056G3731993-08-27027 August 1993 Informs of Plans to Conduct Series of off-line Periods to Evaluate Reactor Sys,Procedures & Drawings,Evaluate Effluent Paths from Reactor Facility,Test Upgraded Equipment & Train Operators on Equipment & to Modify Procedures & Manuals ML20045C2091993-06-18018 June 1993 Forwards Response to Re Violations Noted in Insp of License R-28 & Payment of Proposed Civil Penalty. Corrective Actions:Shift Supervisor on Shift During Overpower Event Permanently Removed from Licensed Duties ML20045D2381993-06-16016 June 1993 Forwards Editorial Change to TS Table 3.2 to Be Included W/ Amend 39 to License R-28 & Ts,Changing Footnote B to Reflect Reduction in Number of Radiation Detectors in Radiation Monitoring Sys from Six to Five ML20035E7601993-04-15015 April 1993 Submits Changes to Amend 38 to License R-28,per 930414 & 15 Telcons W/Nrc.Changes Correct Shutdown Margin in Spec 3.1.5 to Read 0.10 Delta K/K Rather than 0.010 Delta K/K ML20034H0041993-03-0505 March 1993 Responds to Reactor Operator Exams Administered on 921215-16.Memo,distributed to Operations Staff Re Relationship Between Reactor Power Instrument Readings & Actual Reactor Power,Encl ML20044B8701993-03-0101 March 1993 Forwards Changes to Be Added to Amend 38 to TS Pages 5 & 44 Re Surveillance Time Intervals & RO Repts,Respectively,Per 930222 Telcon W/Nrc ML20126E6571992-10-29029 October 1992 Forwards Amend 38 to Ford Nuclear Reactor TS Redefining Specification 3.1,under License R-28 for Phoenix Project ML20126E7351992-10-27027 October 1992 Responds to Commitment to Evaluate Effects of Unanticipated Reactivity Insertions at Facility & to Conduct Thorough Review of Procedures & Ts.Info on Corrective Actions Planned & Completed Related Reportable Occurrence 15 Encl ML20055H1111990-07-18018 July 1990 Forwards, Requalification Program Ford Nuclear Reactor, in Response to NRC 900706 Request for Addl Info ML20055G3081990-07-17017 July 1990 Submits Info Re 10CFR50.33 & 50.75 Decommissioning Funds ML20042G2541990-05-0303 May 1990 Forwards Rev 2 to Ford Nuclear Reactor Requalification Program, for Review & Approval ML19332F8021989-12-0606 December 1989 Forwards Rev 2 to Requalification Program Ford Nuclear Reactor, for Review & Approval ML20248G2411989-09-20020 September 1989 Responds to NRC Questions Re Pool Leakage at Facility. Summary of Pool Water Makeup,Surface Evaporation & Leakage for Most Recent Two Quarters of 1989 & for Preliminary Measurement Conducted from 890915-18 Provided ML20244B1251989-05-30030 May 1989 Provides Correlation Between Rev Numbers & Content & Listing of Revs on Review Sheet of Emergency Plan ML20247F3101989-05-16016 May 1989 Forwards Revised Figure 6.1, Organization Chart for Ford Nuclear Reactor, Reflecting Reorganization of Health Physics Organization.Figure Should Be Included w/890508 Rev 1 to Tech Specs ML20245F0981989-04-20020 April 1989 Forwards Rev 5 to Emergency Plan Ford Nuclear Reactor. Changes Involve Time Limit on Ltrs of Agreement W/Ann Arbor Police Dept,Fire Dept & Ambulance Svc and Definition of Emergency Staff Members ML20196E7521988-11-0404 November 1988 Requests Approval of Alternate Routing for Shipment of Spent Triga Fuel from Cheyenne,Wy to Denver,Co ML20148D7571988-03-15015 March 1988 Forwards Revised Page 17 of Emergency Plan Re Modifying Section 3.2.1,per 880309 Request ML20244B1331988-01-15015 January 1988 Requests Listed Mods to Facility Emergency Plan ML20235Y9961987-10-13013 October 1987 Advises That on 871012,last High Enrichment U Fuel Shipped to Savannah River,Sc Site.Requests Issuance of Revised Security Plan Submitted on 860715 Reducing Security Requirements Re Low Enrichment U Fuel ML20237K9631987-08-14014 August 1987 Forwards Proposed Revs to Emergency Plan,Reflecting Reorganization of Facility Mgt.Reactor Operators Are Not Required to Be in Line of Succession for Emergency Director ML20237J1511987-08-0404 August 1987 Forwards Proposed Revs to Pages 13-15 of Emergency Plan, Reflecting Facility Mgt Reorganiztion Including Addition of Second Assistant Reactor Manager ML20212R1111987-04-15015 April 1987 Forwards Response to NRC Re Security Insp on 870316-19.W/o Encl ML20215K4671987-03-26026 March 1987 Requests Approval of Route to Be Used for Transport of Spent Reactor Fuel.Proposed Route Attached ML20210F9121987-02-0505 February 1987 Advises That 861203 Revs to Emergency Plan Implemented,Per NRC 870116 Approval ML20244B1311986-12-0303 December 1986 Provides Changes to Listed Sections of Plant Emergency Plan, for Review & Approval.Changes Result of Region III Emergency Preparedness Insp ML20211C9881986-10-16016 October 1986 Responds to Re Security Plan.Revised Plan,W/All Mods Delineated,Encl.Encl Withheld (Ref 10CFR2.790) ML20203P1101986-10-0808 October 1986 Advises That Changes to Emergency Plan Submitted on 860813 Fully Implemented ML20203F2711986-07-15015 July 1986 Forwards Security Plan,Amending License R-28,per 10CFR50.90. Revised Sections Provide Decreased Security Arrangements Due to Conversion to Low Enriched Fuel & Organization Changes. Plan Withheld (Ref 10CFR2.790) ML20214A7351986-01-28028 January 1986 Requests Approval of Route for Transporting Spent Reactor Fuel.Proposed Route Encl ML20136E6451986-01-0303 January 1986 Forwards Revised Pages 5.7 & 18 to QA Program,Reflecting Elimination of Supervisor of Reactor Operations.Assistant Reactor Manager Assumed Responsibilities Formerly Assigned to Position ML20137X0391985-12-0404 December 1985 Responds to NRC Re Noncompliance Noted in Safety Insp on 851120-22.Corrective Actions:License Amend Request Submitted on 851202 to Remove Position of Supervision of Reactor Operations from Tech Specs ML20136F5531985-11-0707 November 1985 Responds to NRC Re Violations Noted in Insp on 851002-04.Corrective Actions:Rubber Sealing Gasket on Final 5-micron Filter Replaced & Fourth Sentence in Section 5.10.3 of Retention Tank Dumping Procedure HP 115 Revised ML20138L4941985-08-17017 August 1985 FOIA Request for Records of Conversion from High to Low Enriched U Fuel,Including Safety Analyses,Empirical Test Data,Feasibility Studies & Studies Re Applicability of Conversion to Other Research Reactors ML20138L5891985-02-28028 February 1985 Forwards Revised Tech Specs & Safety Analysis as Part of OL Renewal Request,Including Page 5 of Section 1.0 Re Establishment of Surveillance Frequencies & Page 9 of Section 3.0 Re Shutdown Margin Requirements ML20024F0741983-08-22022 August 1983 Submits Public Version of Notice That 820729 Emergency Plan, as Amended by Jan 1983 Documents,Fully Implemented, Effective 830822 1999-05-25
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l MICHIGAN MEMORIAL -PHOENIX PROJECT PHOENIX MEMORIAL LABORATORY FORD NUCLEAR REACTOR g.g ANN ARBOR, MICHIGAN 48109-2100 own, at e, puu ww June 13,1998 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington D.C. 20555 Docket 50-2 License R-28 Re: REPLY TO A NOTICE OF VIOLATION dated May 13,1998.
Gentlemen:
The Notice of Violation refers to two distinct instances in which the requirements of our License were not followed:
- 1) The first violation involved failure to adequately perform a required 10 CFR 50.59 evaluation of Modification Request No.120 which installed a new primary cooling pump and motor and removed the pump discharge
[~
check valve internals in April 1996.
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- 2) The second violation involved failure to notify the NRC in writing within 30 days as required by Technical Specifications 6.6.2.b.2 following the discovery of the condition described previously on October 8,1996.
/ /'g o
Reasons for the Violations The reasons for the violations have been provided as follows:
- 1) Inspection Report No. 50-002/98202(DRPM) by Tom Burdick.
- 2) Presentation to the Enforcement Conference of April 22,1998, with attachments by Ronald F. Fleming.
9906180034 990613 9 PDR ADOCK 05000002 PDR Phone:(734) 7644213 Fam: (734) 763-7863 www.umich.edu/~mmpp/
t Cor'rective Steps Taken to Avoid Further Violations The Arrective actions taken fall into two categories, those involving technical aspects of our license and those involving the adequacy of our communication with the NRC. The technical issues with the license have been resolved by License Amendment No. 44, submitted on April 2,1998, and approved by the NRC on April 16,1998. These issues are discussed in detail in my Presentation to the Enforcement Conference of April 22,1998. The communication issues were also addressed at the April 22,1998 meeting and included dual approval lines as well as additional specific review by our Safety Review Committee.
Perhaps the best indication that these Corrective Steps have borne fruit is our
- Report of Non-routine Occurrence - Hot Demineralized Leak Causes 75 Gallon Loss of Pool Water to Radioactive Liquid Retention Tank System" dated June 3, 1998. I have included a copy of this Report with this Reply.
Date When Full Compliance Will Be Achieved We believe that we were in full compliance as of the approval date of Amendment 44, April 16,1998. We will continue to improve our license in terms of Safety Limits for Operation, and we will continue to improve out,Jrocess of review and communication. However, we are now in full compliance with the issues leading to these Violations.
Sincerely,
)
N-Ronald F. Fleming Director
- he Lmversity if Michigan
.icnigan Memorial Phoenix Project
- hice
- :..e Director
- 201 Ben: steel Boulevarc A.nn Aroor..'.lienigan 48109-200 June 3.1998 Docxet 50-2 License R-23 United States Nuclear Reculatorv C:mm:ssion Document Control Desx Washington. D.C. 20555 Re:
Report of Non routine Occurrence. Hot Demineralized Leak Causes 75 Gallon Loss of Pool Water to Radioactive Liquid Retention Tank System.
Summarv of Events On May 10.1998 at 0:50 reactor operators at the University of Michigan's Ford Nuclear Reactor discovered a leak in one of the two resin columns comprising the "B" Hot Demmeralizer (Hot DD system. Tne leak resuited in the loss of approximately 75 gallons of reactor pool water to tne factiity s radioactive liquid waste retention tank system (total textor pool water voiume is approximately 48.000 gallonsi. Hot DI "B" was isolated and
- Mw rextor operauon conunuca. Safe overanon of the reactor was not (Mr.w.eed at any time during this occurrence. No radioacuvity was released from the facility as a result of this occurrence. This report is bemg mace cecause the leak resulted from a failure in a component of the pnmary coolant boundarv.
The leak was discovered while the reactor eperators were investigating the case of an unusually large ooserved decrease m pooi water level amounung to one-half O/2) inch dunng the pnor two nours. The normal pooi water loss rate is about one and one-half i1-1/2)incnes per cay.
An automauc shutorf rais e tnat was installed with the most recent Hot DI system upgrade was not m service cecause of past erranc cenavior in its tiow sensor.
Hot DISystem The FNR Hot DI system consists to two sets of fiberglass reinforced resin tanks containing mixed canon and amon ion excnange resin ocads. The purpose of the Hot DI system is to mamtam the pH and concucuvity tne pnmary coolant water. The tanks are physically located in the basement of the reactor t'uilding. The Hot DI system taps off of the pnmary coolant retum piping civemng a smail fracuan t 14 gallons / minute) of pnmary coolant water to the Hot DI's. Nommal pnmary coolant : low rate is 1050 gallons / minute. Valves are installed that allow isciation of the Hot Di system from the pnmary coolant system. A check valve crevents eacx : low from ine reoi throuch the Hot Di rerum line. Most of the Hot DI syste'm has eeen switenec to Seneauie 50 chionnated polyvinyl chloride (CPVC) pipe fittings and valves. See tne two enciesed tigures.
ciW5%7TCt28
&fP
, Dunng nonnai operanon ene set et DI coiumns will be put on-line wnen concucuvity of the
- ooi water reacnes 2.5 w.no/cm. Arter tne conductivity has been brought down to 1.5
'amnoicm. tne DI's a tii ~r e cypasse:: unui :nauctivity a' gam reaches 2.! umno/cm.
Then tne on-line set ::::.umns :mer 3.
~
B"' is no ioneer effecuve tne otner set is
~
- ut
- nto semce. 2.e cut-et-sem:e set ci ::.umns are restorea after a suitaoie cecay
- enoa ov reunne tne utstream cc:umn.. v:ng tne cownstream column to tne uostream position.' ana replacmg tne.:ownstream cc:umn with a tanx containmg fresn ton exchange resms.
Safety Anairsis Testing conducted on Stay 13 dunng tne snutcown mamtenance period immediately following the event showea tnat tne maximum onmar; coolant loss rate throuen a cuillotine breax in the Hot DI piping is 15.9 gallons /mmtite. This loss rate would cause'a decrease in
- he water height above tne core at tne rate ci 6.4 incnes per hour (one inch of pool height is eaual to 150 gallons of wateri.
The water would flow into pits and floor crams in the reactor basement that drain to a pair cisumps. Sump pumps transfer tne water to tne 3000 gallon radioactive liquid retention tanks in the Phoerux 51emonal Lacoratorv rutiding. 29 gallons is pumped each time the sump pumps actuate. An alarm also annunc:ates in the reactor control room when the reactor control circtuts are energizea ano e:tner sump pump actuates. The normal frequency at which the sumps pump out ano alarm is acout once per eight hour shift.
Reactor Operatmg A worst case leak in tne Hot DI system wouid cause repeated sump alarms and would quickly be invesugated. ciscovereo and isoiatea by the reactor operators when the reactor is coeraung. This operator accon would take p:xe well before the low pool level alarm at nunus five inches or tne automanc reactor r:ndown at mmus 12 inches would occur. (Note:
the mmus 12 inch level corresoonas to tne reol water level LSSS of 19 feet above the core.
one foot aoove me safety iinut of 18 feet.) '
Reactor Secured Two poei level alarms are acuve wnen tne reactor is secured. A local alarm is actuated at a rooi level of about minus seven menes. The second alann, actuated by the same sensor inat gives the pool levei reactor rundown signal at minus 12 inches. is 'sent direcdy to the alarm panel at the Of Depanment of Public Safety which is statfed 24 hours per day.
The worst case Hot DI leak situanon u nen tne reactor is secured would occur if the local alarm actuates just after tne secunty guara nas passed through on his rounds. In this situation, knowledge that a proolem exists will probably not be known unul the minus 12 inch alarm actuates. Given a one nour response time between Public Safety contxting the On-Call Supemsor iOCS) and the OCS isciatme the Hot Di system. an additional 6.4 nenes wouid be iost frem tne cool. The pect iev'el wouid still be at least IS feet 5 inches
- cove tne core wnen tne
- e:K is isolatec.
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Raciation ievels at me sud=e ci me pool tould not be sigm6cantly aitered by a drop in pooi levei from 20 feet acove me cere to 15 feet 5 inenes. The intensity oidirect gamma ediation from the core would increase ey a factor of approximately 60 at the average f:ssion gamma enerzy oi 00 keE However the contnbution direct core gammas make to ne total dose rate at me coot sur:re :s msienincant as comoared to tne cose cue to nuvateo imounnes i:nmaruv 'U _4. in me rooi water. Die reactor nas ocerated with the rooi level lo'wereo chs mucn 5 :.ve :nenes'uncer special c:rcumstances.'No ciscemible I
~
ncrease m surface =atauon. '.e: t as cetec:ec at tne ume. Normal pooi surface radiation
.:veis are 10 to 15 mRihr.
Reactor pool water ieaxmg from tne Hot DI system would be captured by the facility's radioacuve licuid waste system. 2ere are no direct oatnways between the basement of the TNR building', where tne' dor Drs are located. and tinrestn'eted areas. Therefore. no cdioacuvity would be releasea to unrestnctea areas.
De conclusion is tnat a leak from tne Hot DI system will have no reactor safety signi5Cance.
?ossible Root Cause In the course of tesung the Hot DI system following this event, it was observed that a pamal vacuum could be drawn en tne resm columns depending on how the system's valves were operated. This causea an inward flexmg of the resm tank. Such flexing may have initiated the crack in the failed resm column.
lmmealate Actions Taicen Immediate xtions taken were: D :o isolate at,d secure Hot DI "B", and 2) to isolate and secure the entire Hot DI system cunng penoas when the reactor was not operating until d:rtner testing could be completec.
'.ane Term Acnons to Prevent a kcurrence The vendor who supplied the resm columns was contacted. The burst pressure was quoted
- o oe 250 psi. The maximum recommenced working pressure was said to be 100 psi. A
'00 psi pressure test will be performea on each DI resm column before it is put into servlCe.
A number of tests were performea on tne entire Hot DI system on May 18. 26 and June 2.
l
~he entire Hot DI system was isolated anc men pressurized and hydrostaucally leak tested
- t 85 psi for more inan one hour en Slay is. No leaks were found. The system was hydrostatically tested a secono ame on June 2. One 5tting containing a conductivity cell
- =cked at a pressure cetween 100 and 120 esi. The fitting was replaced by a CPVC pipe n:pple and the system was testea again at 1:0 psi. No further leaks were detected. The
.aximum operatmg pressure m me Hot DI system occurs in the piping immediately after l
ne return pump. The Hot DI retum pump is normally operated with a back pressure of 50 -
l
- 0 psi to prevent cr. vim: ton. Alax: mum pressure will occur when the pumps are running 1
l 1
L.
emme_.
ma :ne Hot DI re:um :soianon.aise :s snut. Under tnis conoition a pressure of 80 psi was ecserved on May. 3. i ne ;Lne..eax test snowed the Hot DI system piping is capaole of withstanding the nignest anucipatec coeraung pressure without failure.
A new auto-snutorf vaive =a now +ensor using a different cesien have oeen crocured and
~
nsta21ed. but are not yet wirec elec:..::uiy. This will maxe tne Hot DI system self-isolating
- n :se at a major ::2K.s nen :ne :ns:ananon is complete.
Operaune Procecure No. ;;;. :!ec Oreranne the Hot Demineralized Svstem has been
~
m'ooined to secure tne iniet anc outlet rumos enor to enancing valve line-uns in the system. This should eliminate unneceisaritlexing of the resiin tanks.
~
~
- Sigerely, f(' A f.
==
Ronald F. Flenung, Director
~
Michigan Memonai-Phoemx Project ene.: as stated
- c:
Theodore Michaels. USNRC Proiect Manager Thomas Burdick. USNRC Region III
~
- LTER e 3YPass
{
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- LTERS POOL CHECK 200L CONOUCTMTY
. BYPASS VALVE
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~~
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- 4ot Jemineraliser System m
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.Orzmat issue:. 0997 Revision i: :50398 OPERATING PROCEDL*RE NO. 211 U!C %R OEACTOR LtBORATORY
- Nuclear Reactor
- P.xna.\\!e=cnal Lacoratorv 2e il=versary of.\\licmgan Ann Aroor. Miciugan HII2 OPERATING TIE HOT DE.\\IINERM.I7FR SYSTEM (HOT DD l.
?URPOSE The purpose of this procedure is to provice a means to ensure the punty of the pnmary
- ooiant Dy removal ofimpunnes in tne form of nunerais, dissolved solids. and conosion prooucts.
3.
EOLUPMENTCOVERFD The hot DI pumps. cemmeralizer columns. tilters. as weil as valves and pipeg required to
- rculate pool water tmougn tne not DI system.
4 RESPONSIBILITIES 2.1 Shift Suoemsor The Shift Suoervisor will be a licensed senior reactor operator. S/he will supervise
- .nd authonze all acuvines relatec to the performance of this proceaure.
A; Shift Ooerator Se Shift Ocerator wiii be a licensed senior rextor operator. a licensed reactor
~
coerator, cr a person cualitied for on-shift dunes. Tlie Shift Operator will assist in me performance of tms crocecure uncer the supervision of the Shift Supervisor.
5.
PROCEDL*RE 5.1 Censole ocerator review Oceraung Procedure 211.
5.2 Normal cooi water concucuvity ts mamtained between 1.5 umho and 2.5 4mho.
Denuneralizer column "A" ("B'"i is piaced on line when conoucuviry is 22.5 mho.
When the concucuvity ei the pooi water is 51.5 pmho, the column that is on line is bypassed.
f.;
? LACING A HOT DEMINERAI 77CR ON LINE.
f.:.1 When pooi water condue::vity is 22.5 pmho. checic the Hot DI L~tilizatior.
- nput recera. ;cstec in== controi room. to determine which column is to be piacea on ime.
evi::n. 30398 O
- ..; - r -- M:: :::::5 f..3
- he:s cpen me :sotauen.aives for tne "A * '"B"i DI coiumns.
f.2.4. pen me vaive :aceiec "A ' "B"1 DI on me not DI mamfold.
l
^
f.2.5 ihut me.alve =e:ec "3. ass :n me not DI mamiold.
m f.:.5 z: ca Het CI;um:5.
f..7 2e x me pressure cut :: ne outlet pump, adjust tne clue oudet valve as eecca to mamtmn a 50-c0 psi back pressure.
f.2.3 ' form me Censoie 0;emtor mat "A" "B") DI is on line.
f.2.9 Conscie Orerator. upc:.te me Hot DI Utilizaucn Input recort. r.nd record i: ms enange m reactor.cg coor.
5.3 3YPASSING A HOTDEMDGpAU7FR.
3.3.1 When cooi water concucuvity is $1.5 umho, Check the Hot DI Unl 7arion l
- nput recora. posted in me co'ntrol room. to determme which coiumn is on
.:ne.
5.3.2 T;m off Hot DI pumps.
l f.3.3 Cren tne valve :abeled "3vpass cn the hot DI mamfold.
l 5.3.4 Shut me vaive iabelec "A * "B") DI on the hot DI manifold.
l
\\
l f.3.5 Tum on Hot DI pumps.
l f.3.6 Check de pressure out c:ie outlet pump, adjust the blue outiet valve as l
.eecca to mamtam a f 0-ed psi back pressure.
5.3.7 '-iorm tne Censoie 0:emtor that "A" ("B") DI is bvpassea.
l 5.3.S Consoie Operator. upcate tne Hot DI Utilization Input report. and record l
status change :n reacter:og book.
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