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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20211B8931999-08-17017 August 1999 Safety Evaluation Supporting Amend 143 to License NPF-2 ML20210T2161999-08-0606 August 1999 Draft SE Supporting Proposed Conversion of Current TS to ITS for Plant ML20206L4551999-05-10010 May 1999 Safety Evaluation Supporting Amends 142 & 134 to Licenses NPF-2 & NPF-8,respectively ML20206G7471999-05-0404 May 1999 Safety Evaluation Accepting Corrective Actions Taken by SNC to Ensure That Valves Perform Intended Safety Functions & Concluding That SNC Adequately Addressed Requested Actions in GL 95-07 ML20203J0631999-02-19019 February 1999 Safety Evaluation Supporting Amends 107 & 85 to Licenses NPF-2 & NPF-8,respectively ML20199D8611999-01-12012 January 1999 SER Accepting Relief Request for Inservice Insp Program for Plant,Units 1 & 2 ML20195E2281998-11-16016 November 1998 Safety Evaluation Authorizing Relief Request for Second 10-year ISI Program Relief Request 56 for Plant,Unit 1 ML20155E0271998-10-29029 October 1998 SER Approving & Denying in Part Inservice Testing Program Relief Requests for Plant.Relief Requests Q1P16-RR-V-3 & Q2P16-RR-V Denied Since Requests Do Not Meet Size Requirement of GL 89-04 NUREG-1407, Safety Evaluation Accepting IPEEE for Severe Accident Vulnerabilities,Per GL 88-20 & NUREG-14071998-10-0101 October 1998 Safety Evaluation Accepting IPEEE for Severe Accident Vulnerabilities,Per GL 88-20 & NUREG-1407 ML20154B6121998-10-0101 October 1998 Safety Evaluation Granting Second 10-year ISI Requests for Relief RR-13 & RR-49 Through RR-55 for Jm Farley NPP Unit 1 ML20237C5471998-08-20020 August 1998 Suppl to SE Re Amends 137 & 129 to Licenses NPF-2 & NPF-8, Respectively.Se Being Supplemented to Incorporate Clarifications/Changes & Revise Commitment for Insp of SG U-bends in Rows 1 & 2 for Unit 2 Only ML20236U6141998-07-23023 July 1998 Safety Evaluation Authorizing Use of Alternative Alloy 690 Welds (Inco 52 & 152) as Substitute for Other Weld Metal ML20236R8671998-07-0909 July 1998 Safety Evaluation Concluding That Southern Nuclear Operating Co USI A-46 Implementation Program Has Met Purpose & Intent of Criteria in GIP-2 & Staff SSER-2 on GIP-2 for Resolution of USI A-46 ML20236L2451998-07-0707 July 1998 Safety Evaluation Accepting Licensee Request for Exemption from Certain Requirements of 10CFR50.71(e)(4) Re Submittal of Revs to UFSAR for Facility Changes Made Under 10CFR50.59 for Plant,Units 1 & 2 ML20217P0571998-04-29029 April 1998 Safety Evaluation Supporting Amends 137 & 129 to Licenses NPF-02 & NPF-08,respectively ML20217D2591998-04-21021 April 1998 Safety Evaluation Accepting Licensee Proposed Alternative Re Augmented Exam of Reactor Vessel Shell Welds for Plant ML20217H3191998-03-31031 March 1998 Safety Evaluation Accepting Proposed Changes to Plant Matl Surveillance Programs ML20217D4081998-03-24024 March 1998 Safety Evaluation Accepting Proposed Changes to Maintain Calibration Info Required by ANSI N45.2.4-1972 ML20216H6731998-03-17017 March 1998 SER Accepting Quality Assurance Program Description Change for Joseph M Farley Nuclear Plant,Units 1 & 2 ML20203B4731998-02-0505 February 1998 Safety Evaluation Supporting Amends 135 & 127 to Licenses NPF-2 & NPF-8,respectively ML20203B7581998-02-0505 February 1998 Safety Evaluation Supporting Amends 134 & 126 to Licenses NPF-2 & NPF-8,respectively ML20199F8931998-01-23023 January 1998 Safety Evaluation Supporting Amends 133 & 125 to Licenses NPF-02 & NPF-08,respectively ML20199B0371998-01-22022 January 1998 SER Accepting Request for Relief (RR-27) for Plant,Units 1 & 2 from Certain Provisions of Section XI to ASME Boiler & Pressure Vessel Code.Relief Will Remove Insulation on ASME Code Class 1 Sys During Inservice Insp ML20198R5221997-10-29029 October 1997 Safety Evaluation Supporting Amends 132 & 124 to Licenses NPF-02 & NPF-08,respectively ML20212F4791997-10-23023 October 1997 Safety Evaluation Supporting Amend 131 to License NPF-2 ML20212A5711997-10-17017 October 1997 Safety Evaluation Supporting Amends 130 & 123 to Licenses NPF-2 & NPF-8,respectively ML20217E8501997-10-0101 October 1997 Safety Evaluation Supporting Amends 129 & 122 to Licenses NPF-2 & NPF-8,respectively ML20216G9521997-09-0404 September 1997 Safety Evaluation Authorizing Request for Relief for IEEE 279-1971,Section 4.7.3 Requirements Concerning Steam Generator Water Level Control ML20236N3331997-08-21021 August 1997 SER Re Request for Interpretation of EDG TS 4.8.1.1.2.e for Farley Nuclear Plant,Units 1 & 2 ML20140B8571997-06-0202 June 1997 Corrected Page 7 to Safety Evaluation Supporting Amend 124 to License NPF-2 ML20137E2951997-03-24024 March 1997 Safety Evaluation Supporting Amends 125 & 119 to Licenses NPF-2 & NPF-8,respectively ML20137B4371997-03-20020 March 1997 SER Accepting Request for Relief for 120-month Update of Facility Inservice Insp & Inservice Testing Programs & Code Addition & Addenda of Asme/Ansi Parts 6 & 10 ML20135E4811997-03-0404 March 1997 Safety Evaluation Accepting Implementation of 10CFR50.55a Requirements Related to Repair & Replacement Activities for Containment at Plant ML20056H1341993-08-23023 August 1993 Safety Evaluation Accepting Licensee 921217 Response to NRC 920917 SE Re Inservice Testing Program Relief Request ML20062D7001990-11-0909 November 1990 Safety Evaluation Supporting Util 881123 & 900917 Responses to Generic Ltr 88-11, NRC Position on Radiation Embrittlement of Reactor Vessel Matls & Its Effect on Plant Operations. Submittals Acceptable.Beltline Welds Discussed ML20245A8601989-06-13013 June 1989 Safety Evaluation Supporting Util 831104 & 850422 Responses to Generic Ltr 83-28,Item 4.5.3, Reactor Trip Sys Reliability for All Domestic Operating Reactors ML20247K6281989-05-19019 May 1989 Safety Evaluation Supporting Amends 81 & 73 to Licenses NPF-2 & NPF-8,respectively ML20247A8481989-05-0404 May 1989 Safety Evaluation Supporting Amends 80 & 72 to Licenses NPF-2 & NPF-8,respectively ML20195D5391988-10-31031 October 1988 Safety Evaluation Supporting ATWS Rule,10CFR50.62 ML20154C9651988-05-12012 May 1988 Safety Evaluation Re Flaw Indications in Reactor Pressure Vessel ML20147E2621987-11-16016 November 1987 Corrected Page 2 of Safety Evaluation Re Amends 74 & 66 to Licenses NPF-2 & NPF-8,respectively,deleting Ref to Quarterly Surveillance Testing on Staggered Test Basis ML20235D5061987-09-21021 September 1987 Safety Evaluation Supporting Amend 64 to License NPF-8 ML20235K4441987-07-0808 July 1987 Safety Evaluation Supporting Granting Licensee Relief from Volumetric Exam of Steam Generator Primary Side Noozles Inside Radiused Sections ML20216E7401987-06-23023 June 1987 Safety Evaluation Supporting Amend 71 to License NPF-2 ML20209E5981987-04-10010 April 1987 Safety Evaluation Supporting Amends 70 & 62 to Licenses NPF-2 & NPF-8,respectively ML20206G3561987-03-30030 March 1987 Safety Evaluation Supporting Amends 69 & 61 to Licenses NPF-2 & NPF-8,respectively ML20212E2241987-02-27027 February 1987 Safety Evaluation Accepting Util 831104 Response to Item 4.5.2 of Generic Ltr 83-28 Re on-line Functional Testing of Reactor Trip Sys,Including Independent Testing of Diverse Trip Features of Reactor Trip Breakers ML20211D5341987-01-0707 January 1987 Safety Evaluation Re Rev 1 to EGG-EA-6794, Conformance to Reg Guide 1.97,Joseph M Farley Nuclear Plant,Units 1 & 2 & Licensee Submittals.Response Acceptable ML20212F5101987-01-0707 January 1987 Safety Evaluation Accepting Licensee 831104 Response to Generic Ltr 83-28,Item 2.1 (Part 1), Equipment Classification (Reactor Trip Sys Components) ML20207J8931986-12-29029 December 1986 Safety Evaluation Granting Exemption from Technical Requirements of 10CFR50,App R,Section Iii.G for 16 Fire Areas 1999-08-06
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217P0761999-10-0606 October 1999 Non-proprietary, Farley Units 1 & 2 LBB Calculation Results Due to SG Replacement & SG Snubber Elimination Programs ML20217G0361999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20216E4941999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Jmfnp.With ML20212E7451999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Hcgs,Unit 1.With Summary of Changes,Tests & Experiments Implemented During Aug 1999.With ML20211B8931999-08-17017 August 1999 Safety Evaluation Supporting Amend 143 to License NPF-2 ML20210T2161999-08-0606 August 1999 Draft SE Supporting Proposed Conversion of Current TS to ITS for Plant ML20211B2011999-08-0404 August 1999 Informs Commission About Results of NRC Staff Review of Kaowool Fire Barriers at Farley Nuclear Plant,Units 1 & 2 & Staff Plans to Address Technical Issues with Kaowool & FP-60 Barriers ML20210R6031999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With 05000364/LER-1999-001-05, :on 990621,plant Was Manually Tripped Due to Decreasing Vacuum in Condenser.Caused by Broken Steam Dump Drain Line.Broken Section of Line Was Repaired & Licensee Will Implement Addl Design Change1999-07-0202 July 1999
- on 990621,plant Was Manually Tripped Due to Decreasing Vacuum in Condenser.Caused by Broken Steam Dump Drain Line.Broken Section of Line Was Repaired & Licensee Will Implement Addl Design Change
ML20196J3791999-06-30030 June 1999 Safety Evaluation of TR WCAP-14750, RCS Flow Verification Using Elbow Taps at Westinghouse 3-Loop Pwrs. Rept Acceptable L-99-267, Monthly Operating Repts for June 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20209G0661999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With 05000348/LER-1999-002-02, :on 990527,Unit 1 Reactor Trip Occurred Following Loss of 1A SG Feedwater Pump.Caused by Personnel Error.Unit Was Stabilized in Hot Standby.With1999-06-25025 June 1999
- on 990527,Unit 1 Reactor Trip Occurred Following Loss of 1A SG Feedwater Pump.Caused by Personnel Error.Unit Was Stabilized in Hot Standby.With
L-99-023, Monthly Operating Repts for May 1999 for Jfnp Units 1 & 2. with1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Jfnp Units 1 & 2. with ML20206L4551999-05-10010 May 1999 Safety Evaluation Supporting Amends 142 & 134 to Licenses NPF-2 & NPF-8,respectively ML20206G7471999-05-0404 May 1999 Safety Evaluation Accepting Corrective Actions Taken by SNC to Ensure That Valves Perform Intended Safety Functions & Concluding That SNC Adequately Addressed Requested Actions in GL 95-07 ML20206C9461999-04-30030 April 1999 1:Final Cycle 16 Freespan ODSCC Operational Assessment L-99-161, Monthly Operating Repts for Mar 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20204D4391999-03-31031 March 1999 Unit-1 1999 Voltage-Based Repair Criteria 90-Day Rept ML20204D7271999-03-15015 March 1999 ISI Refueling 15,Interval 2,Period 3,Outage 3 for Jm Farley Nuclear Generating Plant,Unit 1 ML20207M6421999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20203J0631999-02-19019 February 1999 Safety Evaluation Supporting Amends 107 & 85 to Licenses NPF-2 & NPF-8,respectively ML20203A2651999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With 05000348/LER-1998-008-01, :on 981223,reactor Vessel Support Concrete Design Bases Temperature Exceeded Due to Closed Cooling Damper.Caused by Personnel Error.Damper Opened & Secured in Position.With1999-01-18018 January 1999
- on 981223,reactor Vessel Support Concrete Design Bases Temperature Exceeded Due to Closed Cooling Damper.Caused by Personnel Error.Damper Opened & Secured in Position.With
ML20199D8611999-01-12012 January 1999 SER Accepting Relief Request for Inservice Insp Program for Plant,Units 1 & 2 ML20206C8081998-12-31031 December 1998 Alabama Power 1998 Annual Rept ML20199E6591998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Jm Farley Nuclear Plant,Units 1 & 2.With 05000348/LER-1998-007-02, :on 981106,found Several TSP Circumferential Indications & Several TSP Axial Indications Extending Just Beyond Edge of Tsp.Caused by Tube Defects.Sg Tubes Have Been Plugged or Repaired as Required1998-12-22022 December 1998
- on 981106,found Several TSP Circumferential Indications & Several TSP Axial Indications Extending Just Beyond Edge of Tsp.Caused by Tube Defects.Sg Tubes Have Been Plugged or Repaired as Required
05000348/LER-1998-006-03, :on 981124,PRF Sys Suction Damper Was Outside Design & Licensing Basis.Caused by 1976 Personnel Failure to Identify Noted Inconsistency.Scheduled Design Change in 1999 to Modify Dampers to Ensure Licensing Basis Are Met1998-12-18018 December 1998
- on 981124,PRF Sys Suction Damper Was Outside Design & Licensing Basis.Caused by 1976 Personnel Failure to Identify Noted Inconsistency.Scheduled Design Change in 1999 to Modify Dampers to Ensure Licensing Basis Are Met
ML20198K4091998-12-18018 December 1998 COLR for Jm Farley,Unit 1 Cycle 16 05000364/LER-1998-007-01, :on 981116,ESF Actuation Occurred During DG 1000 Kw Load Rejection Test.Caused by Poor Jumper Electrical Connection.Improved Jumpers Will Be Used on Appropriate Terminals in Load Rejection Test Procedures.With1998-12-11011 December 1998
- on 981116,ESF Actuation Occurred During DG 1000 Kw Load Rejection Test.Caused by Poor Jumper Electrical Connection.Improved Jumpers Will Be Used on Appropriate Terminals in Load Rejection Test Procedures.With
ML20198B2561998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20195E2281998-11-16016 November 1998 Safety Evaluation Authorizing Relief Request for Second 10-year ISI Program Relief Request 56 for Plant,Unit 1 05000348/LER-1998-005-03, :on 981021,automatic Start of B Train Penetration Room Filtration Occurred Due to Filling Sf Tc. Caused by Inadequate Procedure.Changed Procedure to Provide Specific Guidance for Filling SFP Tc.With1998-11-12012 November 1998
- on 981021,automatic Start of B Train Penetration Room Filtration Occurred Due to Filling Sf Tc. Caused by Inadequate Procedure.Changed Procedure to Provide Specific Guidance for Filling SFP Tc.With
ML20195C9681998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20155E0271998-10-29029 October 1998 SER Approving & Denying in Part Inservice Testing Program Relief Requests for Plant.Relief Requests Q1P16-RR-V-3 & Q2P16-RR-V Denied Since Requests Do Not Meet Size Requirement of GL 89-04 NUREG-1407, Safety Evaluation Accepting IPEEE for Severe Accident Vulnerabilities,Per GL 88-20 & NUREG-14071998-10-0101 October 1998 Safety Evaluation Accepting IPEEE for Severe Accident Vulnerabilities,Per GL 88-20 & NUREG-1407 ML20154B6121998-10-0101 October 1998 Safety Evaluation Granting Second 10-year ISI Requests for Relief RR-13 & RR-49 Through RR-55 for Jm Farley NPP Unit 1 ML20154H0121998-09-30030 September 1998 Submittal-Only Screening Review of Farley Nuclear Plant IPEEE (Seismic Portion) ML20154H6001998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20151V8341998-09-30030 September 1998 Non-proprietary Rev 2 to NSA-SSO-96-525, Jm Farley Nuclear Plant Safety Analysis IR Neutron Flux Reactor Trip Setpoint Change 05000348/LER-1998-004-03, :on 980909,turbine Trip & Consequent Reactor Trip Occurred.Caused by Reactor Protection Sys Card Failure. Failed Card Was Replaced & Unit 1 Returned to Power on 980910.With1998-09-28028 September 1998
- on 980909,turbine Trip & Consequent Reactor Trip Occurred.Caused by Reactor Protection Sys Card Failure. Failed Card Was Replaced & Unit 1 Returned to Power on 980910.With
05000348/LER-1998-003-04, :on 980816,determined That Wgdt Hydrogen & Oxygen Had Exceeded Concentration Limits,Per TS 3.11.2.5. Caused by Undetected Leak.Leak Was Identified & Isolated & Waste Gas Sys Was Returned to Svc on 980818.With1998-09-11011 September 1998
- on 980816,determined That Wgdt Hydrogen & Oxygen Had Exceeded Concentration Limits,Per TS 3.11.2.5. Caused by Undetected Leak.Leak Was Identified & Isolated & Waste Gas Sys Was Returned to Svc on 980818.With
05000348/LER-1997-003, :on 970315,determined That TS SR 4.5.3.2 Had Not Been Performed,Per Operating Procedure.Caused by Personnel Error.Verified That RHR Discharge to Charging Pump Suction MOVs 8706A & 8706B Were Closed.With1998-09-0808 September 1998
- on 970315,determined That TS SR 4.5.3.2 Had Not Been Performed,Per Operating Procedure.Caused by Personnel Error.Verified That RHR Discharge to Charging Pump Suction MOVs 8706A & 8706B Were Closed.With
05000348/LER-1998-005, :on 980315,failure to Perform Nuclear Instrumentation Surveillance Requirements Prior to Mode 2 & 3 Entry,Was Discovered.Caused by Personnel Error.Revised Applicable Procedures1998-09-0303 September 1998
- on 980315,failure to Perform Nuclear Instrumentation Surveillance Requirements Prior to Mode 2 & 3 Entry,Was Discovered.Caused by Personnel Error.Revised Applicable Procedures
05000348/LER-1998-002-05, :on 980816,SG Tube Leakage Investigation,Repair & Evaluation,Occurred.Caused by ODSCC in Two Locations on Same Tube.Operational Leak Rate Limit Requiring Plant Shutdown Has Been Administratively Reduced1998-09-0303 September 1998
- on 980816,SG Tube Leakage Investigation,Repair & Evaluation,Occurred.Caused by ODSCC in Two Locations on Same Tube.Operational Leak Rate Limit Requiring Plant Shutdown Has Been Administratively Reduced
ML20197C8991998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20237C5471998-08-20020 August 1998 Suppl to SE Re Amends 137 & 129 to Licenses NPF-2 & NPF-8, Respectively.Se Being Supplemented to Incorporate Clarifications/Changes & Revise Commitment for Insp of SG U-bends in Rows 1 & 2 for Unit 2 Only ML20237B1891998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Jm Farley Nuclear Plant,Units 1 & 2 ML20236Y1121998-07-31031 July 1998 Voltage-Based Repair Criteria 90-Day Rept 1999-09-30
[Table view] |
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SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION RELATED TO AMENDMENT NO.13iTO FACILITY OPERATING LICENSE NO. NPF-2 SQUIEIERN NUCLEAR OPERATING COMPANY. INC. ET AL.
JOSEPH M. FARI FY NUCLEAR PLANT. UNIT 1 DOCKET NO. 50-348 r
1.0 INTRODUCTION
i By letter dated September 3,1997 Southem Nuclear Operating Company (SNC, the licensee),-
' inc., et al., requested changes to the Technical Specifications for Joseph M. Farley Nuclear Plant, Unit 1. These changes would reduce the number of required incore detectors necessary for continued operation for the remainder of Cycle 15 only.
The Farley Unit 1 Movable incore Detection System (MIDS) contains a total of 50 instrumentation thimbles in the core. Technical Specification (TS) 3.3.3.2 requires that at least 75% of the detector thimbles be opereble with a minimum of two detector thimbles per quadrant when performing a flux map to ensure compliance with the peaking factor requirements of TS 3.2.2. The surveilbnce requirements of TS 3.2.2 require that the peaking factors must be ~
determined to be within limits at least once per 31 effective full power days. Due to the recent increase in incore detector thimble failures at Farley Unit i during Cyc'e 15 thus far, SNC has proposed a change that will allow plant operation with the number of operable detector thimbles
- reduced to a minimum of 50% with three detector thimbles per quadrant. To compensate for the increased uncertainty as the number of operable detector thimbles is reduced, the 4
measurement uncertainty for F"aH and F"o will be increased whenever the number of detectors t
~ is between 37 and 25.
I-During the Unit 1 Cycle 14 refueling outage, the incore thimbles were inspected and cleaned and additional work was performed on the moveable incore detector system. During the start-up of Cycle 15, numerous flux maps were run dth no unusual problems. A flux map attempt on July 8,1997, was unsuccessful because 16 incore thimbles would not allow the detector to a-complete its transit. Flux maps, since that time, have been completed with 38 or 39 thimbles.
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While the location of the detector thimbles that were unavailable has changed from map to i
map, the available detectors have remained distributed throughout the core and the thimble coverage has been adequate. Since SNC believes that this problem has the potential to
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L worsen throughout Cycle 15, there is concern about meeting the 75% requirement called for in the TS for future-required moveable incore detection system uses. Failure to have at least 75%
- of the thimbles accessible could result in a forced shndown.
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- 2.0 EVALUATION
- Essentially all pressurized water reactor (PWR) TSs contain a requiremert for operability of 75% of the incore detector locations for mapping of the core power distribution. On a number
- of occasions, for various reasons, failures of detector thimbles in operating PWRs have approached or sxceeded 25%, and relaxation of the 75% requirement has been permitted for the remainder of the affected operating cycle.
Incore detector data is used to _ calculate power peaking factors that are used to verify compliance with fuel performance limits. As the number of inoperable detector thimbles -
increases, the uncerta_Inties i_n the power distribution calculation increase. The requirement for maintaining 75% of the detector thimbles available provides for a reasonable number of failures -
of the incore detectors while encouraging licensees to strive for maintaining the system as near >
to 100% available as possible The proposed TS 3.3.3.2 allows continued use of the movable incore detector system with less than 75% of the thimbles available if the measurement error allowance due to incomplete flux mapping is appropriate. The licensee submitted an analysis performed by the vendor, Westinghouse, which assessed the impacts of a reduction to a minimum of 25 of the 50 movable detector thimbles for Farley Unit 1 Cycle 15. The analysis indicated that additional uncertainties of 1.5% for FN4H and 2% for F"o are appropriate when e
the number of instrumented assemblies is reduced from 38 to 25 The additional uncertainties should be applied linearly from below 75% to greater than 50% detector thimble locations. In addition, the Westinghouse analysis assumed random deletion of the thimbles. If the thimbles were systematically deleted from use, the calculated peaking factor uncertainties would not apply. Thus, there is an additional requirement that when the number of detector locations is less than 75%, there should be a minimum of three thimbles available per quadrant, where quadrant includes both horizontal-vertical quadrants and diagonally bounded quadrants (eight quadrants in all). This requirement improves the abihty to distinguish between random and -
systemic thimble deletion events and establishes the boLoos of applicability of the peaking factor uncertainties.
SNC has provided the results of core maps for Cycle 15. These show that there is currently approximately 10% margin to the F"aH TS limit and approximately 6% margin to the FN o
TS limit. Since the peaking factors normally tend to decrease with bumup, the staff would expect the margin to increase from now till the end of the cycle.
Another safety concem relating to degradation of incore mapping ability is the ability to detect
- anomalous conditions in the core. One of these is inadvertent loading of a feel assembly into an improper position. Since this is a loading problem, it is not of concem for the remainder of the operating cycle. Fu,thermore, review of the Cycle 15 startup physics test results showed very good agreement between predictions and measurements, thus, giving more assurance that the core is as designed. Other anomalous conditions are conceived to produce either an
- axial or radial effect, which would causu either a change in quadrant tilt ratio or axial offset ratio.
These are monitored by the excore detectors and would help identify problems not fully detectable with reduced incore mapping capability. Furthermore, the core exit thermocouples in the reactor provide a useful supplement to the incore detectors to detect problems.
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- 3-L Our review of the suitability of operation of the Farley Unit i reactor for the remainder of Cycle 15 with a reduced number of movable incore thimbles locations to as few as 50%
indicated adequate margin exists at this time in Cycle 15 and sufficiently increased uncertainty allowances have been made to ensure that TS peaking factor limits will be met. In addition, there are adequate supplementalindicators of anomalous conditions to preclude an unsafe condition from escaping detection in the absence of full incore detector mapping capability.
3.0 IECHNICAL SPECIFICATION CHANGES
. TSs 3.2.2.3.b,4.2.2.3, and 4.2.3.2 - The changes increase the measurement uncertainty by 2%
for F"o and 1.5% for F"6H when the number of operab!e incore detector thimbles is reduced to 50% (25) of the total number of duectors. The additional uncertainty is applied linearly from below 75% to greater than 50% detector thimble locations. The change in the uncertainty has been justified and is therefore acceptable.
TS 4.3.3.2 - The change adds a footnote which states that for Unit 1 Cycle 15 with greater than 50% and less than 75% detector thimbles available, three detector thimbles per quadrant are required where quadrant includes both the horizontal-vertical quadrant and four diagonally-bounded quadrants (eight individual quadrants in total). The proposed change was added to establish the bounds of applicability of the evaluation and is acesptable. The Bases have also been modified to incorporate the method for calculating the allowances for measuremant uncertainty with 25 to 37 operable detector thimbles.
On the basis of the staff's evaluation in Section 2.0 above, the staff concludes that adequate margin exists to ensure that TS peaking factors will be met for the remainder of Cycle 15.
Therefore, the proposed Technical Specification changes are acceptable. These changes are for the rema!nder of Cycle 15 only.
4.0 STATE CONSULTATION
- In accordance with the Commission's regulations, the State of Alabama official was notified of the proposed issuance of the amendments. The State official had no comments.
1
5.0 ENVIRONMENTAL CONSIDERATION
The amendment changes a requirement with respect to installation or use of a facility-component located within the restricted area as defined in 10 CFR Part 20 and changes surveillance requirements. The NRC staff has determined that the amendment involves no significant increase in the amounts, and no significant change in the types, of any effluents that may be released offsite, and that there is no significant increase in individual or cumulative Meu$ional radiation exposure. The Commission has previously issued a proposed finding i
that the amendment involves no significant hazards consideration, and there has been no
. public comment on such finding (62 FR 47695 dated September 10,1997). Accordingly, the smondment meets the eligibility criteria for categorical exclusion set forth in 10 CFR
--51.22(c)(9). Pursuant to 10 CFR 51.22(b) no environmental impact statement or environmental.
assessment need be prepared in connection with the issuance of the amendment.
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6.0 CONCLUSION
The Commission has concluded, based en the considerations discussed above, that (1) there is reasonable assurance that the health and safety of the public will not be endangered by-operation in the proposed mannst, (2) such activities will be coMucted in compliance with the
. Csmmission's regulations, and (3) the issuance of the amendmont will not be inimical to the common defense and security or to the health and safety of the public, g
PrincipalContributor: M. Chatterton
- Date:
October 23, 1997 P
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