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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20211B8931999-08-17017 August 1999 Safety Evaluation Supporting Amend 143 to License NPF-2 ML20210T2161999-08-0606 August 1999 Draft SE Supporting Proposed Conversion of Current TS to ITS for Plant ML20206L4551999-05-10010 May 1999 Safety Evaluation Supporting Amends 142 & 134 to Licenses NPF-2 & NPF-8,respectively ML20206G7471999-05-0404 May 1999 Safety Evaluation Accepting Corrective Actions Taken by SNC to Ensure That Valves Perform Intended Safety Functions & Concluding That SNC Adequately Addressed Requested Actions in GL 95-07 ML20203J0631999-02-19019 February 1999 Safety Evaluation Supporting Amends 107 & 85 to Licenses NPF-2 & NPF-8,respectively ML20199D8611999-01-12012 January 1999 SER Accepting Relief Request for Inservice Insp Program for Plant,Units 1 & 2 ML20198S4091999-01-0606 January 1999 Revised SE Supporting Amends 140 & 132 to Licenses NPF-2 & NPF-8,respectively.Page Contains Vertical Lines to Indicate Areas of Change ML20195E2281998-11-16016 November 1998 Safety Evaluation Authorizing Relief Request for Second 10-year ISI Program Relief Request 56 for Plant,Unit 1 ML20155H4801998-11-0303 November 1998 Safety Evaluation Supporting Amends 139 & 131 to Licenses NPF-2 & NPF-8,respectively ML20155E0271998-10-29029 October 1998 SER Approving & Denying in Part Inservice Testing Program Relief Requests for Plant.Relief Requests Q1P16-RR-V-3 & Q2P16-RR-V Denied Since Requests Do Not Meet Size Requirement of GL 89-04 ML20154B6121998-10-0101 October 1998 Safety Evaluation Granting Second 10-year ISI Requests for Relief RR-13 & RR-49 Through RR-55 for Jm Farley NPP Unit 1 ML20237C5471998-08-20020 August 1998 Suppl to SE Re Amends 137 & 129 to Licenses NPF-2 & NPF-8, Respectively.Se Being Supplemented to Incorporate Clarifications/Changes & Revise Commitment for Insp of SG U-bends in Rows 1 & 2 for Unit 2 Only ML20236U6141998-07-23023 July 1998 Safety Evaluation Authorizing Use of Alternative Alloy 690 Welds (Inco 52 & 152) as Substitute for Other Weld Metal ML20236R8671998-07-0909 July 1998 Safety Evaluation Concluding That Southern Nuclear Operating Co USI A-46 Implementation Program Has Met Purpose & Intent of Criteria in GIP-2 & Staff SSER-2 on GIP-2 for Resolution of USI A-46 ML20236L2451998-07-0707 July 1998 Safety Evaluation Accepting Licensee Request for Exemption from Certain Requirements of 10CFR50.71(e)(4) Re Submittal of Revs to UFSAR for Facility Changes Made Under 10CFR50.59 for Plant,Units 1 & 2 ML20217P0571998-04-29029 April 1998 Safety Evaluation Supporting Amends 137 & 129 to Licenses NPF-02 & NPF-08,respectively ML20217D2591998-04-21021 April 1998 Safety Evaluation Accepting Licensee Proposed Alternative Re Augmented Exam of Reactor Vessel Shell Welds for Plant ML20217H3191998-03-31031 March 1998 Safety Evaluation Accepting Proposed Changes to Plant Matl Surveillance Programs ML20217D4081998-03-24024 March 1998 Safety Evaluation Accepting Proposed Changes to Maintain Calibration Info Required by ANSI N45.2.4-1972 ML20216H6731998-03-17017 March 1998 SER Accepting Quality Assurance Program Description Change for Joseph M Farley Nuclear Plant,Units 1 & 2 ML20203B4731998-02-0505 February 1998 Safety Evaluation Supporting Amends 135 & 127 to Licenses NPF-2 & NPF-8,respectively ML20203B7581998-02-0505 February 1998 Safety Evaluation Supporting Amends 134 & 126 to Licenses NPF-2 & NPF-8,respectively ML20199F8931998-01-23023 January 1998 Safety Evaluation Supporting Amends 133 & 125 to Licenses NPF-02 & NPF-08,respectively ML20199B0371998-01-22022 January 1998 SER Accepting Request for Relief (RR-27) for Plant,Units 1 & 2 from Certain Provisions of Section XI to ASME Boiler & Pressure Vessel Code.Relief Will Remove Insulation on ASME Code Class 1 Sys During Inservice Insp ML20198R5221997-10-29029 October 1997 Safety Evaluation Supporting Amends 132 & 124 to Licenses NPF-02 & NPF-08,respectively ML20212F4791997-10-23023 October 1997 Safety Evaluation Supporting Amend 131 to License NPF-2 ML20212A5711997-10-17017 October 1997 Safety Evaluation Supporting Amends 130 & 123 to Licenses NPF-2 & NPF-8,respectively ML20217E8501997-10-0101 October 1997 Safety Evaluation Supporting Amends 129 & 122 to Licenses NPF-2 & NPF-8,respectively ML20216G9521997-09-0404 September 1997 Safety Evaluation Authorizing Request for Relief for IEEE 279-1971,Section 4.7.3 Requirements Concerning Steam Generator Water Level Control ML20236N3331997-08-21021 August 1997 SER Re Request for Interpretation of EDG TS 4.8.1.1.2.e for Farley Nuclear Plant,Units 1 & 2 ML20140B8571997-06-0202 June 1997 Corrected Page 7 to Safety Evaluation Supporting Amend 124 to License NPF-2 ML20140A8471997-05-29029 May 1997 Errata to Safety Evaluation Supporting Amends 123 & 118 to Licenses NPF-2 & NPF-8,respectively.Corrects Pp 2 of Subj Safety Evaluation ML20137D6961997-03-24024 March 1997 Safety Evaluation Supporting Amend 124 to License NPF-2 ML20137E2951997-03-24024 March 1997 Safety Evaluation Supporting Amends 125 & 119 to Licenses NPF-2 & NPF-8,respectively ML20137B4371997-03-20020 March 1997 SER Accepting Request for Relief for 120-month Update of Facility Inservice Insp & Inservice Testing Programs & Code Addition & Addenda of Asme/Ansi Parts 6 & 10 ML20135E4811997-03-0404 March 1997 Safety Evaluation Accepting Implementation of 10CFR50.55a Requirements Related to Repair & Replacement Activities for Containment at Plant ML20134F3721997-02-0303 February 1997 Safety Evaluation Supporting Amends 123 & 118 to Licenses NPF-2 & NPF-8,respectively ML20129K3781996-11-20020 November 1996 Safety Evaluation Supporting Amend 117 to License NPF-8 ML20129A9361996-10-11011 October 1996 Safety Evaluation Supporting Amend 115 to License NPF-8 ML20117H4861996-09-0303 September 1996 Safety Evaluation Supporting Amends 121 & 113 to Licenses NPF-2 & NPF-8,respectively ML20115J9481996-07-19019 July 1996 Safety Evaluation Supporting Amends 120 & 112 to Licenses NPF-2 & NPF-8,respectively ML20112B0741996-05-20020 May 1996 Safety Evaluation Supporting Amend 110 to License NPF-08 ML20095J2561995-12-0808 December 1995 Safety Evaluation Supporting Amends 118 & 109 to Licenses NPF-2 & NPF-8,respectively ML20092N1841995-09-28028 September 1995 Safety Evaluation Supporting Amends 116 & 108 to Licenses NPF-2 & NPF-8,respectively ML20084M0401995-05-22022 May 1995 Safety Evaluation Supporting Amends 115 & 107 to Licenses NPF-2 & NPF-8, Respectively ML20082G4311995-04-0707 April 1995 Safety Evaluation Supporting Amends 114 & 105 to Licenses NPF-2 & NPF-8,respectively ML20081H5101995-03-20020 March 1995 Safety Evaluation Supporting Amends 112 & 103 to Licenses NPF-2 & NPF-8,respectively ML20081J6481995-03-20020 March 1995 Safety Evaluation Supporting Amends 113 & 104 to Licenses NPF-2 & NPF-8,respectively ML20080N3461995-03-0101 March 1995 Safety Evaluation Supporting Amends 112 & 103 to Licenses NPF-2 & NPF-8,respectively ML20080D7111994-12-28028 December 1994 Safety Evaluation Supporting Amends 111 & 102 to Licenses NPF-2 & NPF-8,respectively 1999-08-06
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217P0761999-10-0606 October 1999 Non-proprietary, Farley Units 1 & 2 LBB Calculation Results Due to SG Replacement & SG Snubber Elimination Programs ML20217G0361999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20212E7451999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Hcgs,Unit 1.With Summary of Changes,Tests & Experiments Implemented During Aug 1999.With ML20216E4941999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Jmfnp.With ML20211B8931999-08-17017 August 1999 Safety Evaluation Supporting Amend 143 to License NPF-2 ML20210T2161999-08-0606 August 1999 Draft SE Supporting Proposed Conversion of Current TS to ITS for Plant ML20211B2011999-08-0404 August 1999 Informs Commission About Results of NRC Staff Review of Kaowool Fire Barriers at Farley Nuclear Plant,Units 1 & 2 & Staff Plans to Address Technical Issues with Kaowool & FP-60 Barriers ML20210R6031999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With 05000364/LER-1999-001-05, :on 990621,plant Was Manually Tripped Due to Decreasing Vacuum in Condenser.Caused by Broken Steam Dump Drain Line.Broken Section of Line Was Repaired & Licensee Will Implement Addl Design Change1999-07-0202 July 1999
- on 990621,plant Was Manually Tripped Due to Decreasing Vacuum in Condenser.Caused by Broken Steam Dump Drain Line.Broken Section of Line Was Repaired & Licensee Will Implement Addl Design Change
ML20209G0661999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20196J3791999-06-30030 June 1999 Safety Evaluation of TR WCAP-14750, RCS Flow Verification Using Elbow Taps at Westinghouse 3-Loop Pwrs. Rept Acceptable L-99-267, Monthly Operating Repts for June 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With 05000348/LER-1999-002-02, :on 990527,Unit 1 Reactor Trip Occurred Following Loss of 1A SG Feedwater Pump.Caused by Personnel Error.Unit Was Stabilized in Hot Standby.With1999-06-25025 June 1999
- on 990527,Unit 1 Reactor Trip Occurred Following Loss of 1A SG Feedwater Pump.Caused by Personnel Error.Unit Was Stabilized in Hot Standby.With
L-99-023, Monthly Operating Repts for May 1999 for Jfnp Units 1 & 2. with1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Jfnp Units 1 & 2. with ML20206L4551999-05-10010 May 1999 Safety Evaluation Supporting Amends 142 & 134 to Licenses NPF-2 & NPF-8,respectively ML20206G7471999-05-0404 May 1999 Safety Evaluation Accepting Corrective Actions Taken by SNC to Ensure That Valves Perform Intended Safety Functions & Concluding That SNC Adequately Addressed Requested Actions in GL 95-07 ML20206C9461999-04-30030 April 1999 1:Final Cycle 16 Freespan ODSCC Operational Assessment ML20204D4391999-03-31031 March 1999 Unit-1 1999 Voltage-Based Repair Criteria 90-Day Rept L-99-161, Monthly Operating Repts for Mar 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20204D7271999-03-15015 March 1999 ISI Refueling 15,Interval 2,Period 3,Outage 3 for Jm Farley Nuclear Generating Plant,Unit 1 ML20207M6421999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20203J0631999-02-19019 February 1999 Safety Evaluation Supporting Amends 107 & 85 to Licenses NPF-2 & NPF-8,respectively ML20203A2651999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With 05000348/LER-1998-008-01, :on 981223,reactor Vessel Support Concrete Design Bases Temperature Exceeded Due to Closed Cooling Damper.Caused by Personnel Error.Damper Opened & Secured in Position.With1999-01-18018 January 1999
- on 981223,reactor Vessel Support Concrete Design Bases Temperature Exceeded Due to Closed Cooling Damper.Caused by Personnel Error.Damper Opened & Secured in Position.With
ML20199D8611999-01-12012 January 1999 SER Accepting Relief Request for Inservice Insp Program for Plant,Units 1 & 2 ML20198S4091999-01-0606 January 1999 Revised SE Supporting Amends 140 & 132 to Licenses NPF-2 & NPF-8,respectively.Page Contains Vertical Lines to Indicate Areas of Change ML20199E6591998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20206C8081998-12-31031 December 1998 Alabama Power 1998 Annual Rept 05000348/LER-1998-007-02, :on 981106,found Several TSP Circumferential Indications & Several TSP Axial Indications Extending Just Beyond Edge of Tsp.Caused by Tube Defects.Sg Tubes Have Been Plugged or Repaired as Required1998-12-22022 December 1998
- on 981106,found Several TSP Circumferential Indications & Several TSP Axial Indications Extending Just Beyond Edge of Tsp.Caused by Tube Defects.Sg Tubes Have Been Plugged or Repaired as Required
05000348/LER-1998-006-03, :on 981124,PRF Sys Suction Damper Was Outside Design & Licensing Basis.Caused by 1976 Personnel Failure to Identify Noted Inconsistency.Scheduled Design Change in 1999 to Modify Dampers to Ensure Licensing Basis Are Met1998-12-18018 December 1998
- on 981124,PRF Sys Suction Damper Was Outside Design & Licensing Basis.Caused by 1976 Personnel Failure to Identify Noted Inconsistency.Scheduled Design Change in 1999 to Modify Dampers to Ensure Licensing Basis Are Met
ML20198K4091998-12-18018 December 1998 COLR for Jm Farley,Unit 1 Cycle 16 05000364/LER-1998-007-01, :on 981116,ESF Actuation Occurred During DG 1000 Kw Load Rejection Test.Caused by Poor Jumper Electrical Connection.Improved Jumpers Will Be Used on Appropriate Terminals in Load Rejection Test Procedures.With1998-12-11011 December 1998
- on 981116,ESF Actuation Occurred During DG 1000 Kw Load Rejection Test.Caused by Poor Jumper Electrical Connection.Improved Jumpers Will Be Used on Appropriate Terminals in Load Rejection Test Procedures.With
ML20198B2561998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20195E2281998-11-16016 November 1998 Safety Evaluation Authorizing Relief Request for Second 10-year ISI Program Relief Request 56 for Plant,Unit 1 05000348/LER-1998-005-03, :on 981021,automatic Start of B Train Penetration Room Filtration Occurred Due to Filling Sf Tc. Caused by Inadequate Procedure.Changed Procedure to Provide Specific Guidance for Filling SFP Tc.With1998-11-12012 November 1998
- on 981021,automatic Start of B Train Penetration Room Filtration Occurred Due to Filling Sf Tc. Caused by Inadequate Procedure.Changed Procedure to Provide Specific Guidance for Filling SFP Tc.With
ML20155H4801998-11-0303 November 1998 Safety Evaluation Supporting Amends 139 & 131 to Licenses NPF-2 & NPF-8,respectively ML20195C9681998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20155E0271998-10-29029 October 1998 SER Approving & Denying in Part Inservice Testing Program Relief Requests for Plant.Relief Requests Q1P16-RR-V-3 & Q2P16-RR-V Denied Since Requests Do Not Meet Size Requirement of GL 89-04 ML20154B6121998-10-0101 October 1998 Safety Evaluation Granting Second 10-year ISI Requests for Relief RR-13 & RR-49 Through RR-55 for Jm Farley NPP Unit 1 ML20154H6001998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20154H0121998-09-30030 September 1998 Submittal-Only Screening Review of Farley Nuclear Plant IPEEE (Seismic Portion) ML20151V8341998-09-30030 September 1998 Non-proprietary Rev 2 to NSA-SSO-96-525, Jm Farley Nuclear Plant Safety Analysis IR Neutron Flux Reactor Trip Setpoint Change 05000348/LER-1998-004-03, :on 980909,turbine Trip & Consequent Reactor Trip Occurred.Caused by Reactor Protection Sys Card Failure. Failed Card Was Replaced & Unit 1 Returned to Power on 980910.With1998-09-28028 September 1998
- on 980909,turbine Trip & Consequent Reactor Trip Occurred.Caused by Reactor Protection Sys Card Failure. Failed Card Was Replaced & Unit 1 Returned to Power on 980910.With
05000348/LER-1998-003-04, :on 980816,determined That Wgdt Hydrogen & Oxygen Had Exceeded Concentration Limits,Per TS 3.11.2.5. Caused by Undetected Leak.Leak Was Identified & Isolated & Waste Gas Sys Was Returned to Svc on 980818.With1998-09-11011 September 1998
- on 980816,determined That Wgdt Hydrogen & Oxygen Had Exceeded Concentration Limits,Per TS 3.11.2.5. Caused by Undetected Leak.Leak Was Identified & Isolated & Waste Gas Sys Was Returned to Svc on 980818.With
05000348/LER-1997-003, :on 970315,determined That TS SR 4.5.3.2 Had Not Been Performed,Per Operating Procedure.Caused by Personnel Error.Verified That RHR Discharge to Charging Pump Suction MOVs 8706A & 8706B Were Closed.With1998-09-0808 September 1998
- on 970315,determined That TS SR 4.5.3.2 Had Not Been Performed,Per Operating Procedure.Caused by Personnel Error.Verified That RHR Discharge to Charging Pump Suction MOVs 8706A & 8706B Were Closed.With
05000348/LER-1998-005, :on 980315,failure to Perform Nuclear Instrumentation Surveillance Requirements Prior to Mode 2 & 3 Entry,Was Discovered.Caused by Personnel Error.Revised Applicable Procedures1998-09-0303 September 1998
- on 980315,failure to Perform Nuclear Instrumentation Surveillance Requirements Prior to Mode 2 & 3 Entry,Was Discovered.Caused by Personnel Error.Revised Applicable Procedures
05000348/LER-1998-002-05, :on 980816,SG Tube Leakage Investigation,Repair & Evaluation,Occurred.Caused by ODSCC in Two Locations on Same Tube.Operational Leak Rate Limit Requiring Plant Shutdown Has Been Administratively Reduced1998-09-0303 September 1998
- on 980816,SG Tube Leakage Investigation,Repair & Evaluation,Occurred.Caused by ODSCC in Two Locations on Same Tube.Operational Leak Rate Limit Requiring Plant Shutdown Has Been Administratively Reduced
ML20197C8991998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20237C5471998-08-20020 August 1998 Suppl to SE Re Amends 137 & 129 to Licenses NPF-2 & NPF-8, Respectively.Se Being Supplemented to Incorporate Clarifications/Changes & Revise Commitment for Insp of SG U-bends in Rows 1 & 2 for Unit 2 Only ML20237B1891998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Jm Farley Nuclear Plant,Units 1 & 2 1999-09-30
[Table view] |
Text
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UNITED' STATES i
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NUCLEAR REGULATORY COMMISSION 3
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WASHINGTON, D.C. seeaHoot SAFETY EVALUATION SY THE OFFICE OF NUCLEAR REACTOR REGULATION RELATED TO REQUEST FOR RF1 IEF FOR lEEE 279-1971. SECTION 4.7.3 REQUIREMENTS - STEAM GENERATOR WATER LEVEL CONTROL UDB SOUTHERN NUCLEAR OPERATING COMPANY. INC.
JOSEPH M. FARI FY NUCI FAR PLANT. UNITS 1 AND 2 DOCKET NOS. 50-348 AflD 50-364 1.0 INTRODUCHQS
- By letter dated April 29,1997, and supplemented by letter dated July 25,1997, the Southem Nuclear Operating Company, Inc. (SNC), proposed an altemative to the requirements of 10 CFR 50.55a(h).~ Pursuant to 10 CFR 50.55a(h), the protection system must meet the requirements of IEEE 279-1971, Section 4.7.3, which states, "Where a single random failure can cause a control system action that results in a generating station condition requiring i
protective action and can also prevent proper action of a protection system channel designed to L
protect against the condition, the remaining redundant protection channels shall be capable of providing the protective action even when degraded by a second random failure." -
Section 50.55a(a)(3) states that altemativas to the requirements of paragraph (h) rnay be used, when authorized by the Director of the Office of Nuclear Reactor Regulation, if (i) the proposed
[4 attematives would provide an acceptable level of quality and safety or (ii) compliance with the specified requirements would result in hardship or unusual difficulty without a compeasat!ng
(
i increase in the level of quality and safety.
SNC has proposed interim administrative controls of steam generator water level control -
- (SGWLC) channels that provide reactor trip system actuation signals in conformance with the requirements of 10 CFR 50.55a(a)(3) to resolve the design deficiency idedified by the i
j Westinghouse Electric Corporation (Westinghouse) in Nuclear Safety Ad.s,ory Letter _(NSAL)-
96-004, dated August 14,1996. In NSAL 96-004, Westinghouse stated that a common
~
instrument tap for the SGWLC steam generator level and steam flow channels can fall, thereby L
' resulting in_an inability _to meet the single failure criterion as required in 10 CFR 50.55a(h).
l
- in License Amendment Nos.104 (Unit 1) and 97 (Unit 2), SNC eliminated the low feedwater flow reactor trip based on the addition of a median signal selector (MSS) system in the SGWLC.
The MSS was installed to select the median of the steam generator water level instrument channel input signals, so that the control system is prevented from acting on a single, failed 1
protection system instrument channel. In a letter dated December 29,1993, NRC approved the
- MSS change.
9709160097-970904 PDR-ADOCK.05000348
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i-In the present Farley plant design, each unit has three steam generator water level channels (1,11, and 111) per steam generator and two steam flow channels (lli and IV) per steam line. The i
Channel ill level transmitter reference leg instrument tap is shared with the Channel lil steam j
flow transmitter. A failure of that tap wiIl cause the associated instruments to fall high. Such a L
- failure will result in the feedwater flow being shut-off and will prevent initiation of the required 1
- reactor trip when a random failure is postulated in a second steam generator water level l
channel, per the requirements of IEEE 279-1971, Section 4.7.3. NSAL 96-004 notifed the Westinghouse NSSS plants that because of this common tap, the existing SGWLC system did
' not satisfy the requirements of IEEE 279-1971. Section 4.7.3. However, NSAL-96-004 stated that the probability of a tap / impulse line failure coupled with a failure in another level channel of
- the redundant set (Channel I or ll) is extremely low and is, therefore, not considered to be a i
substantial safety hazard. Furthermore, the NSAL stated that to meet the requirements of l
IEEE 279-1971, plants with an analog MSS must *ther remove the steam flow control signal 3
3
- selector switch and connect it directly to the steam flow transmitter that does not share the tap with a level transmitter used for protection functions, or include a statement in the TS Bases section stating that the steam flow selector switch must normelly select the steam flow i.
transmitter that does not share a tap connection with a narrow range steam generator water level transmitter. The Channel IV steam flow instrument tap is not shared with any water level protection channel.
2.0 EVALUATION NSAL 96-004 is applicable to the three-loop Farley units. As an interim measure,' SNC chose to use Channel IV steam flow for normal plant operation as recommended in NSAL 96-004.
However, under this administrative control, the Channel 111 steam flow will be used (selected) i when Channel IV is unavailable during quarterly functional testing, which will be less than 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> every quarter. The Farley Technical Specifications allow 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> for testing of reactor i
trip system and engineered safety feature actuation system analog channels. Further, when n
the Channel lli steam flow is selected, the associated Charne lil steam generator low-low level bistables will be placed in test within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> to initiate a partial trip signal.
On December 19,1996, the SNC's Plant Onsite Review Committee approved this administrative control procedure and an associated 10 CFR 50.59 Safety Evaluation to-
' implement this interim measure.- The 10 CFR 50.59 Safety Evaluation stated that the Farley plant-specific probabilistic risir assessment (PRA) indicated that the probability of a simultaneous failure of the common tap selected by the flow control signal selector switch for steam flow and narrow range steam generator _ water level and an additional level channel during quarterly functional test of Channel IV steam pressure'and steam flow instruments is on the order of 8.0E-09/ year. This initiating event frequency in the PRA was based on reliance on Channel lli to provide the protection function when it is selected for an assumed total time of 100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> per year when Channel IV is unavailable. Each Farley unit has a total of three Channel IV steam pressure channels and three Channel IV steam flow channels each of which is silotted 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> for a quarterly functional test, for a total of 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> per year, during which the channels are unavailable. Thus, with the above administrative control, Channel ill would normally be used for only 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> per year, which is below the 100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> per year assumed in the event frequency determination in the PRA.. The calculated event frequency of 8.05-09/ year a
- 7. _ _ _
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I L
3-is well below the guidelines of ANSI /ANS-51,1 1983, " Nuclear Safety Criteria for the Design of Stationefy Pressurized Water Reactor Plants," which states in Clause 3.2 that events with a best-estimate frequency of occurrence of less than 10E-6 per reactor year need not be considered for design.-
- SNC stated that in the unlikely event of a common tap failure when Channel 111 steam flow is selected, control room indications, control system response, and operating procedures will provide sufficient information and instructions to ensure that the affected unit is safely operated. Furthermore, SNC intends to rely on the interim administrative measures until -
l the Unit 1 16th refueling outage (spring 2000) and Unit 214th refueling outage (spring 2001).
Full compliance with IEEE 279-1971 requirements will be provided for the SGWLC channels before startup from these refueling outages. SNC stated that the interim measure will provide r
~ the necessary additional time to study design altematives prior to finalizing the required modification to meet IEEE 279-1971 requirements. In addition SNC has made the decision to replace the steam generators in Units 1 and 2 during the spring of 2000 and 2001 refueling
-outages, respectively. As a result, completing modifications twice, once for the current steam generators and once for the replacement steam generators, would result in hardship or unusual difficulty withcut a compensating increase in the level of quality and safety.
3.0 CONCLUSION
The staff has reviewed SNC's evaluation and justification to use administrative controls to
. correct the SGWLC design deficiency by selection of Channel IV as an interim measure for the SGWLC reactor trip function during normal plant operation, and use of Channel lli only for brief periods when Channel IV is unavailable due to surveillance tests. - Based on this review, the staff concludes that the proposed administrative controls are in accordance with Westinghouse NSAL g6-004 and provide sufficient plant safety measures due, to the low probability of event frequency for a limited time prior to restorir g the SGWLC to full compliance with the single failure requirements of IEEE 279-1971 during the 16th refueling outage (spring 2000) for Unit 1 and 14th refueling outage (spring 2001) for Unit 2. The staff authorizes the interim administrative controls as an attemative to the requirements of IEEE 279-1971 pursuant to 10 CFR 50.55a(s)(3)(ii), in that compliance would result in hardship or u, usual difficulty without
- a compensating increase in the level of quality and safety. The proposed interim administrative controls are authorized until the steam generator replacement outages, which are scheduled for spring 2000 for Unit 1 and spring 2001 for Unit 2.
Principal Contributors:
S. Mazumdar J. Zimmerman Date:-
September.4, 1997 1
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