Safety Evaluation Concluding That Insufficient Info Was Available for Staff to Perform Any Detailed Evaluation of Adequacy of Licensee New Strainer DesignML20199B202 |
Person / Time |
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Site: |
Hope Creek ![PSEG icon.png](/w/images/c/cc/PSEG_icon.png) |
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Issue date: |
10/31/1997 |
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From: |
NRC (Affiliation Not Assigned) |
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To: |
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Shared Package |
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ML20199B172 |
List: |
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References |
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IEB-96-003, IEB-96-3, NUDOCS 9711180243 |
Download: ML20199B202 (3) |
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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20211N5531999-09-0808 September 1999 Safety Evaluation Supporting Amend 121 to License NPF-57 ML20216D8331999-07-26026 July 1999 Safety Evaluation Concluding That Licensee IPEEE Complete Re Info Requested by Suppl 4 to GL 88-20 & That IPEEE Results Reasonable Given HCGS Design,Operation & History ML20210F3331999-07-22022 July 1999 Safety Evaluation Granting Relief Requests RR-B1,RR-C1,RR-D1 & RR-B3.Finds That Proposed Alternative for RR-B3 Provides Acceptable Level of Quality & Safety & Authorizes Alternative Pursuant to 10CFR50.55a(a)(3)(i) ML20206Q4731999-05-14014 May 1999 SER Accepting Response to GL 97-05, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant ML20206C8481999-04-22022 April 1999 SER Authorizing Pse&G Proposed Relief Requests Associated with Changes Made to Repair Plan for Core Spray Nozzle Weld N5B Pursuant to 10CFR50.55a(a)(3)(i) ML20205G6051999-03-19019 March 1999 SER Accepting Relief Request Re Acme Code Case N-567, Alternate Requirements for Class 1,2 & 3 Replacement Components,Section Xi,Div 1 ML20205F8911999-03-18018 March 1999 Safety Evaluation Authorizing Licensee Requests for Second 10-year Interval for Pumps & Valves IST Program ML20198H8121997-12-18018 December 1997 Corrected Safety Evaluation Supporting Amend 63 to License NPF-57,correcting Error Re Description of Min Core Thermal Power & Flow Conditions to Avoid Thermal Stratification ML20199C1441997-11-0606 November 1997 Safety Evaluation Supporting Amend 108 to License NPF-57 ML20198P3861997-10-31031 October 1997 Safety Evaluation Authorizing Licensee & Suppls & 1001,requesting Alternative to Perform RPV Circumferential Sheld Weld Exam Requirements of ASME Boiler & Pressure Vessel Code,Section XI,1993 Edition ML20199B2021997-10-31031 October 1997 Safety Evaluation Concluding That Insufficient Info Was Available for Staff to Perform Any Detailed Evaluation of Adequacy of Licensee New Strainer Design ML20212C4481997-10-17017 October 1997 SER Accepting Alternative to ASME Section XI Code Requirements to Use Code N-432 & N-504-1 for Weld Overlay Repair for Hope Creek Generating Station ML20217D8341997-09-25025 September 1997 Safety Evaluation Authorizing Licensee Request for Relief RR-C2 for Plant,First 10-yr Interval Insp Program Plan ML20198F9981997-08-0404 August 1997 Safety Evaluation Accepting Proposed Changes to Rev 8 of HCGS Qap,Submitted on 970516 & 970606 by PSEG ML20133N6491996-12-24024 December 1996 Safety Evaluation Denying Amend Request Re Plant Svc Water Sys & Ultimate Heat Sink ML20134L7181996-11-12012 November 1996 Safety Evaluation Accepting Relief Request V-20 ML20128G2761996-09-26026 September 1996 SER Accepting Continuation of 18-month Test Schedule for Drywell to Suppression Chamber Vacuum Breakers ML20058G5171993-11-29029 November 1993 Safety Evaluation Supporting Amend 60 to License NPF-57 ML20058N8311990-08-13013 August 1990 Safety Evaluation Granting Relief Until Next Scheduled Outage Exceeding 30 Days & No Later than Next Scheduled Refueling Outage ML20055D3361990-06-27027 June 1990 Safety Evaluation Re Util 881128,900308 & 0417 Responses to Generic Ltr 88-11.Proposed Pressure/Temp Limits for RCS for Heatup,Cooldown,Leak Test & Criticality Acceptable & May Be Incorporated Into Plant Tech Specs,Per Reg Guide 1.99 ML20195H6751988-11-22022 November 1988 Safety Evaluation Re Part 2 of Item 2.1 to Generic Ltr 83-28, Vendor Interface Programs - Reactor Trip Sys Components ML20151E2751988-04-11011 April 1988 SER Supporting Util Responses to Part 1,Item 2.1 of Generic Ltr 83-28, Required Actions Based on Generic Implications of Salem ATWS Events ML20148P6341988-01-19019 January 1988 Safety Evaluation Supporting Amend 14 to License NPF-57 ML20237B4611987-12-11011 December 1987 Safety Evaluation Granting Relief from Exams & Testing Requirements & Alternate Methods from First 10-yr Interval Inservice Insp Program ML20236V8151987-12-0101 December 1987 Safety Evaluation Supporting Program Existing for Identifying,Classifying & Treating Components Required for Performance of Reactor Trip Function as Safety Related. B&W Owners Group 870403 Internal Memo Also Encl ML20236U6151987-11-24024 November 1987 Safety Evaluation Supporting Amend 12 to License NPF-57 ML20236A8891987-10-14014 October 1987 Safety Evaluation Supporting Description of How Plant Alternate Rod Injection Sys,Atws Reactor Coolant Recirculation Pump Trip & Standby Liquid Control Sys Meet Requirements of ATWS Rule 10CFR50.62 ML20206G7201987-04-0909 April 1987 Safety Evaluation Supporting Util 861125 Rev 1 to Process Control Program ML20206G4001987-04-0707 April 1987 Safety Evaluation Supporting Amend 3 to License NPF-57 ML20206R0691986-06-25025 June 1986 Safety Evaluation Supporting Util 841217 Response to Generic Ltr 83-28,Items 3.1.1,3.2.1,3.2.2 & 4.5.1 Re Required Actions Based on Generic Implications of Salem ATWS Events ML20203N2221986-06-12012 June 1986 Safety Evaluation Accepting Util Responses to Generic Ltr 83-28,Items 3.1.1,3.1.2,3.2.1,3.2.2 & 4.5.1 ML20154S2081986-03-27027 March 1986 SER Supporting Util 860127 Request to Use Later ASME Code Editions for Design & Fabrication of Components & Supports. Proposed FSAR Changes in ASME Code Section III Requirements Acceptable ML20137R9191986-02-0404 February 1986 Safety Evaluation Accepting Applicant 850821,1004 & 17,1106 & 1209 Proposed Mods to Tests 24,28E,25,28D,3,11,16,1 & 32 of Power Ascension Test Program ML20151Z1081986-02-0303 February 1986 SER Supporting Util Response to Generic Ltr 83-28,Item 1.2 Re post-trip Review (Data & Info Capability) ML20151R2511986-01-22022 January 1986 Sser Supporting Power Ascension Test Program Acceleration. SALP Input Encl ML20137L7401986-01-22022 January 1986 SER Supporting Util 840330 Response to Generic Ltr 83-28, Items 1.1,3.1.3 & 3.2.3 Re post-trip Review (Program Description Procedure) & post-maint Testing ML20137M4001986-01-22022 January 1986 Safety Evaluation Accepting Power Ascension Program Proposed Test Mods ML20138M2421985-12-16016 December 1985 Sser Re Power Ascension Test Program Acceleration.Change Acceptable Except for Elimination of Testing at Test Condition 4.Justification for Deleting Testing at Test Condition 4 Insufficient ML20132A4481985-09-30030 September 1985 Safety Evaluation Supporting Elimination of Arbitrary Intermediate Pipe Breaks 1999-09-08
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217F1501999-10-12012 October 1999 Special Rept:On 990929,south Plant Vent (SPV) Range Ng Monitor Was Inoperable.Monitor Was Inoperable for More than 72 H.Caused by Electronic Noise Generated from Noise Suppression Circuit.Replaced Circuit ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML20217N6531999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Hope Creek Generating Station,Unit 1.With ML20217M0211999-09-20020 September 1999 Part 21 Rept Re Possible Deviation of NLI Dc Power Supply Over Voltage Protection Circuit Actuation.Caused by Electrical Circuit Conditions Unique to Remote Engine Panel. Travelled to Hope Creek to Witness Startup Sequence of DG ML20211N5531999-09-0808 September 1999 Safety Evaluation Supporting Amend 121 to License NPF-57 ML20211B3781999-08-13013 August 1999 Special Rept 99-002:on 990730,NPV Radiation Monitoring Sys Was Declared Inoperable.Caused by Voltage Induced in Detector Output by Power Cable to Low Range Sample Pump. Separated Cables & Secured in Place to Prevent Recurrence ML20210U4721999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Hope Creek Generating Station,Unit 1.With ML20216D8331999-07-26026 July 1999 Safety Evaluation Concluding That Licensee IPEEE Complete Re Info Requested by Suppl 4 to GL 88-20 & That IPEEE Results Reasonable Given HCGS Design,Operation & History ML20216D8721999-07-26026 July 1999 Review of Submittal in Response to USNRC GL 88-20,Suppl 4: 'Ipeees,' Fire Submittal Screening Review Technical Evaluation Rept:Hope Creek Rev 1:980518 ML20210F3331999-07-22022 July 1999 Safety Evaluation Granting Relief Requests RR-B1,RR-C1,RR-D1 & RR-B3.Finds That Proposed Alternative for RR-B3 Provides Acceptable Level of Quality & Safety & Authorizes Alternative Pursuant to 10CFR50.55a(a)(3)(i) ML20210C4731999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Hope Creek Generating Station,Unit 1.With ML20216D8901999-06-30030 June 1999 IPEEEs Technical Evaluation Rept High Winds,Floods & Other External Events ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML20196A1511999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Hope Creek Generating Station,Unit 1.With ML20206Q4731999-05-14014 May 1999 SER Accepting Response to GL 97-05, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant ML20206U1571999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Hope Creek Generating Station,Unit 1.With ML20216D8451999-04-30030 April 1999 Rev 1, Submittal-Only Screening Review of Hope Creek Unit 1 IPEEE (Seismic Portion). Finalized April 1999 ML20206C8481999-04-22022 April 1999 SER Authorizing Pse&G Proposed Relief Requests Associated with Changes Made to Repair Plan for Core Spray Nozzle Weld N5B Pursuant to 10CFR50.55a(a)(3)(i) LR-N990157, Special Rept 99-001:on 990315, C EDG Valid Failure Occurred During Surveillance Testing.Testing Resulted in Unsuccessful Loading Attempt,Due to Failure EDG Output Breaker to Close.Faulty Card Replaced1999-04-12012 April 1999 Special Rept 99-001:on 990315, C EDG Valid Failure Occurred During Surveillance Testing.Testing Resulted in Unsuccessful Loading Attempt,Due to Failure EDG Output Breaker to Close.Faulty Card Replaced ML20205R5901999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Hope Creek Generating Station,Unit 1.With ML20205G6051999-03-19019 March 1999 SER Accepting Relief Request Re Acme Code Case N-567, Alternate Requirements for Class 1,2 & 3 Replacement Components,Section Xi,Div 1 ML20205F8911999-03-18018 March 1999 Safety Evaluation Authorizing Licensee Requests for Second 10-year Interval for Pumps & Valves IST Program ML20204F7951999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Hope Creek Generating Station,Unit 1.With ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML20202F6861999-01-26026 January 1999 Engine Sys,Inc Part 21 (10CFR21-0078) Rept Re Degradation of Synchrostat Model ESSB-4AT Speed Switches Resulting in Heat Related Damage to Power Supply Card Components.Caused by Incorrect Sized Resistor.Notification Sent to Customers ML18107A1871998-12-31031 December 1998 PSEG Annual Rept for 1998. ML20199E7271998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Hope Creek Generating Station,Unit 1.With ML18107A1881998-12-31031 December 1998 PECO 1998 Annual Rept. LR-N980580, Monthly Operating Rept for Nov 1998 for Hope Creek Generating Station,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Hope Creek Generating Station,Unit 1.With ML20198N4161998-11-12012 November 1998 MSIV Alternate Leakage Treatment Pathway Seismic Evaluation LR-N980544, Monthly Operating Rept for Oct 1998 for Hcgs,Unit 1. with1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Hcgs,Unit 1. with ML20155J9861998-10-31031 October 1998 Non-proprietary TR NEDO-32511, Safety Review for HCGS SRVs Tolerance Analyses LR-N980491, Monthly Operating Rept for Sept 1998 for Hope Creek Generating Station,Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Hope Creek Generating Station,Unit 1.With ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils LR-N980439, Monthly Operating Rept for Aug 1998 for Hope Creek Generating Station Unit 1.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Hope Creek Generating Station Unit 1.With LR-N980401, Monthly Operating Rept for July 1998 for Hope Creek Generating Station,Unit 11998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Hope Creek Generating Station,Unit 1 ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps LR-N980354, Monthly Operating Rept for June 1998 for Hope Creek Generating Station,Unit 11998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Hope Creek Generating Station,Unit 1 ML20236E9491998-06-30030 June 1998 Rev 0 to non-proprietary Rept 24A5392AB, Lattice Dependent MAPLHGR Rept for Hope Creek Generating Station Reload 7 Cycle 8 ML18106A6821998-06-24024 June 1998 Revised Charting Our Future. ML18106A6681998-06-17017 June 1998 Charting the Future. LR-N980302, Monthly Operating Rept for May 1998 for Hope Creek Generating Station,Unit 11998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Hope Creek Generating Station,Unit 1 ML20248C7381998-05-22022 May 1998 Rev 0 to Safety Evaluation 98-015, Extension of Allowed Out of Service Time for B Emergency Diesel Generator LR-N980247, Monthly Operating Rept for Apr 1998 for Hope Creek Station, Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Hope Creek Station, Unit 1 LR-N980196, Monthly Operating Rept for Mar 1998 for Hope Creek Generating Station,Unit 11998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Hope Creek Generating Station,Unit 1 ML20217D5701998-03-20020 March 1998 Part 21 Rept 40 Re Governor Valve Stems Made of Inconel 718 Matl Which Caused Loss of Governor Control.Control Problems Have Been Traced to Valve Stems Mfg by Bw/Ip.Id of Carbon Spacer Should Be Increased to at Least .5005/.5010 ML18106A5851998-03-0303 March 1998 Emergency Response Graded Exercise,S98-03. Nuclear Business Unit Salem,Hope Creek Emergency Preparedness, 980303 1999-09-08
[Table view] |
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SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION RELATED TO NRC BULLETIN 96-03 PUBLIC SERVICE ELECTRIC & GAS COMPANY ATLANTIC CITY ELECTRIO COMPANY HOPE CREEK GENERATING STATION DOCKET NO. 50-354
1.0 INTRODUCTION
By letters dated November 4, 1996, and May 20, 1997 Public Service Electric and Gas Company (the licensee) submitted their response to NRC Bulletin (NRCB) 96-03, " Potential Plugging of Emergency Core Cooling Suction Strainers by Debris in Boiling Water Reactors" (NRCB 96-03), for Hope Creek Generating Station. In a NRC 970617 e-mail & During 970619 Telcon|letter dated July 18, 1997]], the licensee submitted a supplemental response providing licensee responses to staff questions. The purpose of the May 20, 1997, submittal was to provide the NRC staff with the sizing criteria the licensee intends to use for sizing their new emergency core cooling system (ECCS) suction strainers (specifically, the low pressure coolant injection (LPCI) and the low pressure core spray (CS) systems) being installed in response to NRCB 96-03. The May 20, 1997, letter requested NRC staff review and approval of the licensee's sizing criteria. This Safety Evaluation providos the NRC staff's evaluation of the licensee's criteria for sizing the new LPCI and CS suction strainers.
2.0 DISCUSSION The NRC staff's contractor, Science and Engineering Associates, Inc. (SEA),
performed a technical evaluation of the licensee's submittals and their responses to the NRC staff's requests for additional information. The contractor's evaluation results are documented in the attached Technical Evaluation Report (TER). The staff has evaluated the contractor's findings and agrees with the conclusions in the TER.
3.0 CONCLUSION
S I
Based on the NRC staff's evaluation of the licensee's submittals, the l contractor's TER, and all other relevant information, the staff concludes the t
following:
- 1. In performing its plant-specific analysis, the licensee calculated the l strainer debris loadings based upon pipe break locations specified in l Section 3.6.2 of the Hope Creek Updated Final Safety Analysis Report j
I 9711190243 971031 ?
PDR ADOCK 05000354 ?
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= (UFSAR). This led to some break locations being screened out of the .
analysis because they were non-credible. This analysis is not
- acceptable to the staff unless the licensee perfoms an analysis which demonstrates that the "non-credible" breaks which they initially screened out of their plant-specific evaluation would not be more limiting in terns of head loss across the strainer than the breaks included in the initial evaluation by the licensee. The licensee committed to performing this evaluation in their response of July 18, -
i 1997. The staff notes that NRCB 96-03 was sent to licensees to ensure compliance with the ECCS rule, 10 CFR Part 50, Section 50.46, not General Design Criterion 4 (GDC 4) of Appendix A to 10 CFR Part 50. The ,
licensing basis that the licensee refers to in Section 3.6.2 of their UFSAR is for demonstrating compliance with GDC 4, not 10 CFR 50.46. GDC 4 requires that licensees protect equipment important to safety from the i
dynamic and environmental effects of a postulated pipe rupture. Hope Creek's licensing basis for GDC 4 described in Section 3.6 of the UFSAR does not discuss compliance with 10 CFR 50.46,-nor does the Ho>e Creek '
Safety Evaluation Report (NUREG-1048, October 1984) indicate t1at _
Sectien 3.6 of the UFSAR is adequate for compliance with 10 CFR 50.46.
The requirements of 10 CFR 50.46-do not provide guidance which allows screening out of "non-credible" breaks. The rule states that a licensee must evaluate "a number of postulated loss-of-coolant accidents of different: sizes, locations, and other properties sufficient to provide 4
assurance that the most severe postulated loss-of-coolant accidents are calculated. " Hope Creek's licensing basis for compliance with 10 CFR 50.46 is clearly stated on page 6.3-1 of their UFSAR. The UFSAR states,
. " Protection is provided for any RCPB (Roactor Coolant Pressure Boundary]
line failure up to, and including, the guillotine failure of the largest line." The licensee's current analysis as described in their May 20, 1997, submittal may not be sufficient in scope to meet the intent of 10 CFR 50.46.
- 2. Insufficient data and calculations were provided by the licensee for the staff to determine the adequacy of the strainer design to handle the calculated debris loadings. Specifically, the head loss across the new strainers with the calculated debris loadings, the basis for the estimated head loss across the new strainers (e.g., the head loss correlation, supporting test data, head loss caiculations, and test data scaling analysis), and the calculated net positive suction head (NPSH) margin with the new strainers were not made available for staff review.
As a result, the staff is unable to draw any specific conclusions as to the adequacy of the strainer design to perform its function with-the calculated debris loadings. However, the staff believes that the new strainers will result in an improvement in NPSH margin due to the increase in strainer size, and the corresponding decrease in strainer pressure drop. Since the licensee is conducting this modification under 10 CFR 50.59, the staff will evaluate the adequacy of their design during a post-implementation inspection. _;
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- 3. The staff also notes that adding additional margin for potential foreign material in the suppression pool is a conservative practice and will assist the licensee in minimizing potential operability concerns should they find foreign material in the suppression pool. The staff also believes allowing margin for potentially degraded or in)roperly applied coatings to be transported to the strainers would also >e prudent. The staff notes that the licensee chose not to allow margin for foreign material or degraded coatings. However, the staff wants to make it clear that increasing the margin in the strainer size does not in any way reduce the licensee's responsibility to maintain an effective foreign material exclusion program, and to take all steps necessary to minimize the amount of material that can accumulate in the suppression pool, vent pipes, vent header, downcomers, drywell and in any other system or component that communicates with the torus.
- 4. The issue of whether or not Technical Specification Surveillances are needed will be addressed generickily with the Boiling Water Reactor ,
Owners' Group. The strainer / suppression pool maintenance and inspection I program will be evaluated during the staff's post-implementation program.
Base u)on the above, the NRC staff concludes that insufficient information was availa)1e for the staff to perform any detailed evaluation of the adequacy of the licensee's new strainer design.
Principal contributor: Rob Elliott
Attachment:
TER Date: October 31, 1997 l
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