ML20134L674
ML20134L674 | |
Person / Time | |
---|---|
Site: | Three Mile Island |
Issue date: | 08/26/1985 |
From: | Conte R NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
To: | |
Shared Package | |
ML20134L645 | List: |
References | |
RTR-NUREG-0737, RTR-NUREG-737, TASK-1.A.1.2, TASK-1.A.1.3, TASK-1.C.3, TASK-1.C.6, TASK-2.B.3, TASK-2.D.3, TASK-2.E.1.1, TASK-2.E.4.2, TASK-2.F.2, TASK-2.G.1, TASK-TM 50-289-85-20, NUDOCS 8509030375 | |
Download: ML20134L674 (30) | |
See also: IR 05000289/1985020
Text
.
.
U.S. NUCLEAR REGULATORY COMMISSION
REGION I
Report Nc. 50-289/85-20
Docket No. 50-289
License No. DPR-50 Priority -- Category C
Licensee: GPU Nuclear Corporation
Post Office Box 480
Middletown, Pennsylvania 17057
Facility At: Three Mile Island Nuclear Station, Unit 1
Inspection At: Middletown, Pennsylvania
Inspection Conducted: June 28, 1985 - August 2, 1985
Inspectors: D. Haverkamp, Technical Assistant for TMI-1
Restart, Region I
R. Urban, Reactor Engineer, Region I
P. Wen, Reactor Engineer, Region I
F. Young, Resident Inspector (TMI-1), Region I
Approved By: M~ // b % f/Jc /rs'
r p R. Conte, TMI I Restart Manager Date
TMI-1 Restart Staff
Division of Reactor Projects
Inspection Summary:
Routine safety inspection (180 hours0.00208 days <br />0.05 hours <br />2.97619e-4 weeks <br />6.849e-5 months <br />) of hot shutdown plant activities in
preparation for TMI-1 restart; licensee action in response to events occurring
at other reactor facilities including emergency feedwater (EFW) system steam
binding and mispositioned control rods; operability of TMI task action plan
equipment modifications; modification control program improvements including
updated status on EFW modifications; tube plugging in steam generators; pres-
surized thermal shock flux reduction program; licensee action on 10 CFR 21
reports; examination security; control room habitability ventilation system
test; licensee action on previous inspection findings; and overall restart
readiness.
8509030375 850827289
PDR ADOCK O pg
G
.
.
Inspection Results:
Licensee upper management continued their detailed involvement in site activi-
ties. Personnel properly implemented facility procedures for hot shutdown
evaluations and testing. Licensee personnel took appropriate actions through
testing, procedural changes, and training in response to events at other
reactor facilities, i.e., steam binding in the emergency feedwater (EFW) system
and mispositioned control rods. The installed TMI Action Plan equipment was
operable although some discrepancies existed with Technical Specification
covering this equipment. The licensee continued to implement initiatives to
improve the modification control program. Reasonable progress continued on
modification work to upgrade the EFW system to full safety grade status. The
licensee design documents reflected restart hearing-imposed safety design
objectives. The licensee took appropriate action on issues addressed in an NRC
safety evaluation; various 10 CFR 21 reports, and previous inspection findings
including two violation responses. The plant remains physically ready for
restart, however, the reliability of one of two source range channels for
nuclear instrumentation needs to be evaluated as to its impact on a safe
restart of TMI-1.
.
.
DETAILS
1.0 Introduction
At the beginning of this inspection period on June 28, 1985, the plant was
at normal hot shutdown conditions (about 530 F and 2150 psig) to complete
licensed operator familiarization training, pending further action by the
U.S. Court of Appeals for the Third Circuit in Philadelphia, Pennsylvania.
As discussed in NRC Region Inspection Report Number 50-289/85-19, the
Court of Appeals on June 7,1985, stayed the Commission Restart Order
(CLI-85-09). No further court action has been taken and the facility
remained at hot shutdown for the remainder of the inspection period.
Inspection coverage was provided by the resident inspector and support
staff components of the NRC TMI-1 Restart Staff.
2.0 Plant Operations During Hot Shutdown '
2.1 Routine Review
The resident inspectors periodically inspected the facility to deter-
mine the licensee's compliance with general operating requirements of
Section 6 of the Technical Specifications (TS) in the following
areas:
--
review of selected plant parameters for abnormal trends;
--
plant status from a maintenance / modification viewpoint including
plant housekeeping and fire protection measures;
--
control of ongoing ard special evolutions, including control
room personnel awareness of these evolutions;
--
control of documents including log-keeping practices;
--
implementation of radiological controls; and,
--
implementation of the security plan including access control,
boundary integrity and badging practices.
The inspectors focused on the following areas:
--
control room operations during regular and backshift hours
including frequent observation of activities in progress and
periodic reviews of selected sections of the shift foreman's log
and control room operator's log and selected sections of other
control room daily logs;
,
--
areas outside the control room; and,
l
l
l
l
I
_
.. . - _ .
.
.
3
--
selected licensee planning meetings.
The inspectors identified no conditions adverse to nuclear safety or
inconsistent with regulatory requirements.
2.2 Summary of Findings
Overall, personnel stationed in the control room exhibited control of
daily activities, including problem areas that needed resolution.
Licensee planning meetings stressed attentiveness to proceed safely
,
'
with daily activities, including surveillance and maintenance and to
resolve any inter-departmental interface problems. Licensee upper
management continued their detailed involvement in site activities.
3.0 Licensee Actions in Response to IE Information Notices
The inspector reviewed the licensee's action associated with IE Informa-
l tion Notice (IN) 84-06, " Steam Binding of Auxiliary Feedwater Pumps," and
l IN 83-75, "Mispositioned Control Rods." The inspector also reviewed the
corresponding Institute of Nuclear Power Operations (INPO) Significant
Operating Experience Reports (SOER).
3.1 Steam Binding in Emergency Feedwater System
l The inspector reviewed the licensee's current methodology on identi-
I fying steam back-leakage into the emergency feedwater (EFW) system.
! The inspector noted, at the beginning of the inspection period, that
l the licensee was training their auxiliary operators in a general
manner to determine if there were any abnormal plant conditions in
the intermediate building. It was not apparent how the specific
problem of back-leakage in the EFW system was addressed in training
sessions.
Licensee representatives initially indicated that if steam back-leakage
- into the EFW system occurred, this would probably be noticed during
l the monthly surveillance check of the EFW pumps. Prior to this time,
! the licensee had performed a one-time test during the last hot
I
functional test (HFT) in April 1985 to determine if such back-leakage
( occurred. Temperature readings at specific EFW piping locations were
! taken over an eight hour period. These test results indicated no
! back-leakage into the system. In addition, the licensee inspected
certain EFW valves prior to this HFT and they found no significant
, wear or wastage of valve internals.
After discussion of the problem with the inspector, the Plant Opera-
tions Manager initiated a procedure change request (PCR) that added a
'
requirement to auxiliary operator shift logs to check for back-
leakage into the EFW system. In addition, he wrote a shift briefing
sheet to re-emphasize the safety concern about steam binding.
Operations personnel reviewed the shift briefing sheet.
1
-
I
w -- v - , . .-. - - - - - - - . . , - . - - . - ~ -- - - - - - r
.
.
4
The inspector concluded that the licensee actions were adequate
measures to detect back-leakage into the EFW system if it occurred.
3.2 Mispositioned Control Rods
Based on discussions with the TMI-1 lead nuclear engineer, the
inspector reviewed the licensee's actions regarding rod misposi-
tioning and how they would recover from this type of problem. The
inspector discussed the rod misalignment event that occurred at ANO-1
to ensure that the lessons learned from that event were incorporated
into station procedures. The engineer demonstrated how their
procedures addressed this concern.
The licensee conducted specific simulator training that addressed
mispositioning of a control rod. A review of the lecture guides and
other training material showed that there were specific and defined
methods on how to recover a misaligned or dropped rod. The inspector
also reviewed the licensee's training plans used during simulator
training and, independently, reviewed applicable station procedures.
The inspector concluded that information presented was detailed
enough that an operator could develop a working knowledge of the core
physics aspects of a misaligned rod. Review of station proce-
dures indicated that necessary guidance was reflected in the appli-
cable procedures.
4.0 Operability of TMI Task Action Plan Equipment Modifications
The purpose of this review was to assess, on a sampling basis, the opera-
bility status of completed TMI Action Plan (TAP) required equipment and
procedural controls modifications specified in NUREG 0737. The review
consisted of evaluating the present status of installed plant equipment,
modifications, and any program / procedure requirements to determine if the
TAP requirement was met on a continuing basis. The TAP items reviewed
included I.A.l.2, I.C.3, I.C.6, I.A.l.3, II.B.3, II.D.3, II.F.2, II.E.1.1,
II.E.4.2 and'II.G.l.
As part of this review, the inspectors referred to NUREG 0660, "NRC
Action Plan De'veloped as a Result of the TMI-2 Accident;" NUREG 0737,
" Classification of TMI Action Plan Requirements," TMI Unit 1 Tech-
nical Specifications (TS); and the NRC resident office files related
to TAP correspondence.
The inspectors determined which TAP items were applicable and if any
<
plant equipment, modifications, or TS changes were made as a result
of each TAP item. All TS associated with the TAP items were reviewed
for adequacy and completeness.
,
'
.
.
-
-- - - -
.w m
. _ -
.
.
5
The inspectors also walked down various systems throughout the plant
such as emergency feedwater equipment, controls and indication, and
inadequate core cooling instrumentation.
The inspectors identified no conditions adverse to nuclear safety or
inconsistent with regulatory requirements. The licensee completed
modifications and related technical specification (TS) changes (approved
by NRR) in accordance with NRC staff requirements and guidelines. The
inspectors identified certain existing TS that might be improved by
additional changes in wording and/or format; but, in all instances, the
inspectors considered the TS to be enforceable in assuring operability of
related equipment. Further, the TS, as approved, were consistent with
applicable NRC staff generic letter guidelines. The inspectors'
suggested TS improvements will be reviewed by Region I for generic
applicability and forwarded to NRR, if applicable.
5.0 Modification Control Program - Selected Aspects
At the corporate office (Parsippany, New Jersey), the resident inspector
reviewed selected aspects of the modification control program. He also
obtained a statui on the upgrade modifications for the emergency feedwater
system.
5.1 Modification Task Force Improvements
The licensee responded to the latest NRC Systematic Assessmen; of
Licensee Performance (SALP) (NRC Inspection Report 50-289/85-99) by
letter dated May 7,1985, from H. Hukill, Director, TMI-1, to
T. Murley, Region I Regional Administrator, and specifically
addressed improvements in the Design, Engineering, and Modification
functional area. They reported that the Office of the President
approved the GPUN Modification Task Force (Task Force) recommenda-
tions discussed in the SALP. During this inspection period, the
inspector discussed the status of the Task Force recommendations with
the GPUNC Director of Engineering, Director of Licensing, and Manager,
TMI-1 Long Range Planning.
The inspector learned that a documented update to these recommenda-
tion was to be prepared and he determined that reasonable progress is
being made to resolve the concerns embodied in the Task Force report.
Of particular interest to the inspector were actions related to the
Task Force observation that too much work (beyond resource capability)
was planned for a given outage period.
The inspector determined that licensee management took direct steps
for better outage planning. They created two new planning positions
that now report to the Vice President of Technical Functions (for
Oyster Creek and TMI-1). Modification items were placed on a
computerized list which was to identify the regulatory source organi-
zation (such as NRR, IE), the particular outage and cycle during
which they planned to implement the item, responsible engineer, and
estimates of ALARA exposure in addition to staff-hour estimates for
l
- _ ._-
.
-.
6
.
engineering and construction. The computerized list for TMI-1 was to
receive inputs from various GPUNC divisions for complete planning
information and assurance that regulatory and corporate schedule ob-
jectives were met. Overall, the inspector concluded that these posi-
tive licensee initiatives, if properly and fully implemented, could
serve to enhance reactor safety. These measures would assure a
methodical outage implementation with the avoidance of last minute
engineering changes for safety-related system modifications.
Further, during the above discussions, the inspector determined that
licensee management planned to issue a consistent set of engineering
specifications, installation standards, and inspection standards to
assure an up-front and consistent engii. ering implementation, and
verification of regulatory requirements and industrial standards for
all modifications including those affecting safety systems. This is
a long-term improvement item.
5.2 Preliminary Engineering Design Review
The inspector reviewed Technical Functions Procedure 5000-ADM-7311.03
(EMP-014), Revision 1-00, effective April 12, 1985, " Project Reviews"
as it related to the conduct of Preliminary Engineering Design
Reviews (PEDR) meetings. At the site, on July 18, 1985, the inspec-
tor monitored a PEDR (second meeting for operations department repre-
sentatives) on modifications for 10 CFR 50, Appendix R. Also, at the
corporate office on July 24, 1985, the inspector monitored a PEDR
(the last in the series of several PEDRs) on modifications to install
an engineered safety features ventilation system for the fuel handling
building.
On a sampling basis, the inspector verified proper implementation of
EMP-014 with respect to PEDR requirements. Licensee attendees pro-
vided their expertise and experience to pose thoughtful and challeng-
ing questions to the design engineers. Various company disciplines
were represented including site plant engineering, site radiological
engineering, site maintenance and construction planning, in addition
to corporate engineering and quality assurance representatives. The
PEDR chairman controlled the meeting and ensured that safety concerns,
regulatory requirements, industrial standards, and practical site-
specific concerns were adequately addressed in licensee design docu-
ments (primarily system design descriptions and safety evaluations).
Overall,'the meetings showed continued implementation of this
resource-intensive licensee initiative and appeared to be focused
toward producing quality products that directly enhance plant safety.
F
i
.-
9res--r , - -- - - - - - - " - --r-- -
q-
,9 9 ,,, y- ,-,-,i+. m y- - - - , - - --- -4 3--w+-- - -- ,- ---
.
r
7 l
5.3 Emergency Feedwater System Upgrade
5.3.1 Introduction
As a result of the TMI-2 accident, the NRC ordered TMI-1 shut
- down because it did not have "...the requisite reasonable as-
surance that the same licensee's Three Mile Island Unit I can
be operated without endangering the health and safety of the
public" (Commission Order, dated July 2,1979). In a Commission
Order, dated August 9, 1979, the Commission specified that the
following licensee actions must be taken with respect to the
emergency feedwater (EFW) system:
--
upgrade the timeliness and reliability of the EFW-in accor-
dance with licensee proposed actions, in letter dated June
28, 1979;
--
develop _and implement operating procedures for initiating
and controlling EFW independent of integrated control
system (ICS);
--
complete analysis of potential small breaks, and develop
and implement instructions to define operator actions; and,
--
provide reasonable assurance of the safety of long term
operation with outstanding category B items of NUREG 0578
(later became Task Action Plan Items II.E.1 and II.E.1.2 of '
NUREG 0737). ,
The short term licensee actions were verified as a part of the
staff's restart certification process to the Commission (SECY
85-192, May 29, 1985). Additional licensee actions taken were
as a result of Union of Concerned Scientist (UCS) 2.206 Petition
in early 1984. The NRC staff reviewed and verified these actions
as noted in NRR Director Decisions 84-12, dated April 27, 1984,
and 84-22, dated September 25, 1984; and NRC Inspection Reports
50-289/84-21, 84-22, and 84-38. The long-term licensee actions
with respect to upgrading the EFW system to full safety grade
status are summarized in paragraph 5.3.3.
5.3.2 Scope of Review
The purpose of this review was to update the status of EFW long-
term modifications and verify that the licensee incorporated
NRC-imposed design objectives into licensee design packages /
documents for subsequent plant installation. The inspector
reviewed applicable licensing and appeal board decisions and
related staff safety evaluations to identify the outstanding
long term items. He also reviewed applicable licensee letters
and licensee internal design documents.
l -
-
r
c
.
,
l
8
,
5.3.3 Detailed Status
Listed below are the applicable design documents for various EFW
upgrade modifications /or licensee evaluation along with status
of construction and testing.
5.3.3.1 Mechanical System Modifications
5.3.3.1.1 Add cavitating venturis (and vibration supports) in
EFW discharge piping (289/83-BC-16)
References
(1) Atomic Safety and Licensing Board (ASLB)
Partial Initial Decision (PID),on the Restart
Hearing, dated 12/14/81, paragraph 1037, item
No. 1
(2) NUREG 0680, NRC Staff TMI-1 Restart Safety
Evaluation Report and Supplement 3, Order Item
8-2.1.7.(a), Item No. 1
(3) System Design Description (SDD)-1-424B,
Division (Div) 1, Revision (Rev.) 4, Item
1.1.1
(4) Licensee Letter (LL) (5211-85-2057), dated
April 19, 1985, from H. Hukill, TMI-1, to
J. Stolz, NRC, Enclosure (Encl.) 1, Item 1.3.1
This was completed for restart and verified in NRC
Inspection Reports 50-289/82-26, 83-01, 83-12, 83-14,
and 84-01. This was considered by the staff to be a
long-term modification but it was relied upon by the
staff to limit EFW flow to an affected once through
steam generator (OTSG) on main steam /feedwater line
rupture to resolve an ASLB concern. The concern was
that inadvertent actuation of the then non-safety grade
portion of the steam line rupture detection system would
,
'
isolate EFW. The isolation function was removed by the
licensee and it was verified in NRC Inspection Report
50-289/83-01, thereby resolving this concern.
5.3.3.1.2 Provide redundant safety grade EFW control and
block valves (289/83-BC-01 and 03) ,
References
(1) sASLB PID, dated 12/14/81, paragraph 1036
(2) NUREG 0680, and Supplement 3, Order Item
8-2.1.7.a(2)
(3) SDD-424B, Revision 4, Item 1.1.2
(4) LL of April 19, 1985, Enclosure 1, Item 1.3.2
i
- - - , - - , - - , - - . _ - , _ , - - _ _ , - - - _ . , , , - - . , - -
.. - , - __ . _ - . _ _.
, .
.
!
i
9
,
The mechanical portion of this modification is
complete. Electrical work is controlled by the
installation of the heat sink protection panel,
~
the status of which is addressed in paragraph
5.3.3.5 of this report.
5.3.3.2 Structural Modifications
References
l (1) SDD-4248, Div. 1, Rev. 4, Items 1.2.1, .2, .3
(2) LL of April 29, 1985, Encl. 1, Items 1.3.3,
.4, and .5
(3) LL of February 13, 1985, from B, Hukill,
GPUNC, to J. Stolz, NRC, Correction to NRC
Inspection Report 50-289/84-37
'
These modifications were: upgrade of EFW pumps recirculation
lines to Seismic Category I (as described in reference (3)); up-
grade vent stacks for safety valve and atmospheric dumps to
Seismic Category I; and provide increased flood protection in the
intermediate building for a main feedwater line break. These modi-
fications were completed and were verified by NRC Region I in
response to the USC 2.206 Petition of 1984 and subsequent NRR
Director Decisions.
5.3.3.3 Electrical Modifications
5.3.3.3.1 Provide a safety grade power supply to valves
C0-V111 A/B and upgrade cable routing for power
supply to valve CO-V V14 A/B
'
Reference
'
(1) LL 83-232, dated August 23, 1983, in response
to TAP II.E.1.1 (Section IV.B.1, page 5)
(2) SDD-4248, Div. 1, Rev. 4, Item 1.3.1
- (3) LL of April 29, 1985, Encl. 1, Item 1.3.6
These valves have the safety function of isolating a damaged
condensate storage tank (CST) (C0-Villa /B) or isolating non-
safety systems from the EFW system (C0-V14A/B). This work is
related to the extensive cable and conduit work required
for meeting safety grade criteria and meeting 10 CFR 50,
Appendix R. The status of the cable and conduit effort is
addressed in paragraph 5.3.3.5 of this report.
5.3.3.3.2 Delete cross connect between electrical busses that
allows an operator to load both EFW electric driven
pumps on a single diesel generator
_ _ _ -. _
~
- _ _. _ ._ _ _ _ _ _ ___.. _ .- _ _ ._. . .. . . _ _ . . _ .
.
.
10
References-
(1) LL 83-232, dated August 23, 1983, in response
to TAP II.E.1.1 (Section IV.B.2, page 16)
(2) SDD-4248, Div. 1, Rev. 4, Item 1.3.8
- (3) LL of April 29, 1985, Encl. 1,' Item 1.3.18
Reference 1 reported this item complete from a human factors
viewpoint, that is, operator error causing a diesel generator
overload. In a later design document (reference (2)) the-
licensee relied on this modification to fulfill electrical
separation criteria for redundant electrical systems. The
licensee completed this modification prior to the restart hear-
ing in 1980 by Engineering Change Memorandum S-225. The
inspector reviewed licensee records on this modification and he
examined control room panels for the control of EFW electric-
driven pumps. The inspector concluded that the licensee
properly deleted the subject power cross-connect function from
EFW pump control.
5.3.3.3.3 Review of diesel generator bus loadings to assure
no overload situation exists as a result of system
modifications
References
(1) LL 83-232, dated August 23, 1983, in response
to TAP II.E.1.1 (Section IV.B.3, page 6)
(2) LL 84-2304, dated January 11, 1984, on
computer program for diesel generator bus
loadings
As committed to in reference (1), reference (2) documented the
satisfactory results of the licensee's computer analysis of
diesel generator bus loadings as a result of modifications made
to the facility. The licensee concluded that no overload situ-
ation would exist.
These documents will be reviewed by NRR as a part of TAP
II.E.1.1 and .2 reviews.
5.3.3.4 Instrument and Control Modifications
! 5.3.3.4.1 Deletion of the main steam line rupture detection i
system (MSLRDS) signal to emergency feedwater '
control valves (289/83-BC-10)
l References
(1) ASLB PID, dated 12/14/81, paragraph 1064
[L (2) ALAB 729, dated 5/26/83, pages 35 and 176
I (3) LL 82-153, dated August 2, 1982
i (4) NRC letters (NRR), dated November 10, 1982 and
( August 30, 1983
1
-se-.
m-y%e,---q.- -
-w--.gr--* emaw gw- -. p-- . ep w+---g p p %---w 9--
.
.
11
(5) Commission Memorandum and Order CLI 84-11,
dated July 26, 1984
(6) NRC Inspection Report 50-289/83-01
(7) SDD-423B, Div. 1, Rev. 4, Item 1.3.2
(8) LL of April 29, 1985, Encl. 1, Item 1.3.17
In reference (1), the ASLB raised the concern of the non-safety
grade MSLRDS inadvertently isolating EFW. In reference (2) the
ALAB noted that the licensee's proposed resolution (deletion of
the MSLRDS signal to EF-V 30A/B) should be reviewed by the
Commission after NRC staff review. Reference (3) documented
the licensee's proposed resolution. In reference (4) NRC staff
accepted the licensee's proposed resolution and forwarded their
review to the Commission. In reference (5) the Commission also
accepted the licensee's resolution of the ASLB concern. The NRC
staff verified completion of licensee action as documented in
reference (6). References (7) and (8) incorporated the design
objectives into licensee design documents.
5.3.3.4.2 Provide safety-grade automatic initiation and
control of EFW (289/83-BC-01 and 06)
References
{1) ASLB PID, dated 12/14/81, paragraph 1036
(2) SDD-4238, Div. 1, Rev. 4, Items 1.3.3, 1.3.4
and 1.3.5
(3) LL of April 29, 1985, Enc 1. 1, Items 1.3.9,
1.3.11,.1.3.14, and 1.3.16
The EFW auto initiation restart modifications were to be
retained and these modifications included auto initiation of EFW
on loss of both main feedwater pumps or on loss of all four
reactor coolant pumps. Planned modifications were automatic
initiation of EWF on high containment pressure and low steam
generator water level.
The controlling work in these planned modifications is the
installation of the heat sink protection system panels which
contain the logic actuation sub-systems for EFW initiation.
Licensee design requirements include safety grade criteria for
the initiation system. The status of the HSPS installation is
addressed in paragraph 5.3.3.5 of this report.
The control functions will remain similar to that committed to
in the restart hearing, that is, EF-V 30A/B actuation to main-
tain level in the OTSG startup range with reactor coolant pumps
on or in the operating range (higher level) on loss of reactor
- coolant pumps to assure natural circulation. The safety grade
j redundant block and control valves for each OTSG will be
controlled by the HSPS logic system.
,
__
, - . - , - - , , . . - . . . , - . . - - . . . . ~ , . , , _ . - - . - . - , , . - - - , . - ~ , , - . , , - - . , , . , - - -
. - _ - -
.
.
i
12
5.3.3.4.3 Provide safety grade OTSG level instrumentation
with signal to initiate EFW and isolate MFW on high
,
water level in the OTSG (289/83-BC-08 and 18) ,
References s
-
(1) ASLB PID, dated 12/14/81, paragraph 1037, Item
'
No. 4
(2) NUREG 0680 and Supplement 3, Order Item
8-2.1.7.a(3)
-
(3) SDD-4248, Div. 1, Rev. 4, Item 13.4
(4) LL of April 29, 1985, Encl. 1, Item 1.3.10
Instrument transmitters are installed and the remaining work is
being accomplished with HSPS installation.
Licensee design documents (references (3) and (4)) reflect
design objectives as noted in references (1) and (2).
5.3.3.4.4 Upgrade MSLRDS to safety grade to assure isolation
of MFW and prevent a potential overpressurization
of containment on steam line break in containment
(289/83-BC-09)
References
(1) ASLB PID, dated 12/14/81, paragraph 1037, Item
i No. 5
(2) ALAB, 7-29, dated 5/26/83, page 36
(3) SDD-4248, Div. 1, Rev. 4, Item 1.3.6
(4) LL of April 29, 1985, Encl. 1, Item 1.3.12
Safety grade logic actuation is provided by HSPS panels. The
HSPS and related cable and conduit installation is addressed in
paragraph 5.3.3.5. The design objectives, as noted in refer-
ences (1) and (2), are incorporated into licensee design docu-
ments, references (3) and (4).
5.3.3.4.5 Provide safety grade condensate storage tank level
installation and low water level alarm
(289/83-BC-07 and 19)
References
(1) ASLB PID, dated 8/14/81, paragraph 1037, Item
No. 2
(2) NUREG 0680 and Supplement 3, Order Item
8-2.1.7.a, Item No. 5
, (3) SDD-4248, Div. 1, Rev. 4, Item No. 1.3.7
(4) LL of April 29, 1985, Encl. 1, Item No. 1.3.13 ,
. , -. =-.
. . - .. -- . _ _. __
...
.
.
.t
13
This work is part of the cable and conduit effort. The design
objectives of references (1) and (2) are incorporated into the
licensee's design documents (references (3) and (4)).
5.3.3.4.6 Provide safety grade OTSG high level alarm
(289/83-BC-13)
References
(1) ASLB PID, dated 8/14/81, paragraph 1037, Item
No. 3
(2) NUREG 0680 and Supplement 3, Order Item No.
8-2.7.1.a, Item No. 7
(3) SDD-424B, Div. 1, Rev. 4, Item No. 1.3.4
(4) LL of April 29, 1985, Encl. 1, Item No. 1.3.10
The design objectives were incorporated into the design of new
OTSG water level instrumentation as noted in paragraph 5.3.3.4.3
above.
5.3.3.4.7 Other licensee proposed modifications / actions
References
(1) SDD-424B, Div. 1, Rev. 4, Items-1.3.9.10,
1.5.3
(2) LL of April 29, 1985, Encl. 1, Items, 1.3.7,
.8, .20
The following additional modifications were proposed and are
being implemented by the licensee:
--
overspeed trip alarm for the turbine-driven EFW pumps;
I , --
safety grade pit level (flood detection) alarm for inter-
mediate building and control grade condenser hotwell low
l level alarm; and,
--
evaluate performance of electric and instrument control
!
'
cables in the event of flooding in the intermediate
building.
These proposals are under review by the NRC staff in conjunction
with SER development for TAP II.E.1.2, Auto Initiation of EFW.
o
,
5.3.3.5 Summary and Conclusion
,
The controlling work effort is cable and conduit installation
~
along with HSPS cabinet installation and wire termination. This
work involves extensive resources and is delayed, in part, for
.
'
procurement and receipt of qualified material. Extensive
preoperational and startup testing is planned. If TMI-1
restarts, then system tie-ins and testing will be delayed.
_ , _ _ _ _ _ _ ___ _ _ __ _ _ . . _ _ __ __ __ . _ . _ _ _ _ .
.
.
14
However, the cycle 6 startup (first refueling after restart)
commitment to the NRC should be met.
Based on the above review, the inspector concluded that NRC-
imposed safety design objectives, as a result of the restart
hearing, were properly incorporated into licensee design docu-
ments.
The proper implementation of the safety grade design require-
ments is unresolved pending completion of licensee action and
- subsequent NRC Region I review (289/85-20-01).
~
6.0 Operation of TMI-1 with 2,000 Plugged Steam Generator Tubes
In NUREG 1019, the NRC staff evaluated the licensee's analyses on the
effects of operating TMI-1 once through steam generators (CTSG) with 1,500
tubes plugged. The staff found that transient and accident consequences
resulting from operation with 1,500 tubes plugged were bounded by the FSAR
analyses, and therefore subsequent operation was acceptable.
To date, a total of 1,542 OTSG tubes have been plugged. To support this
additional plugging, the licensee provided to the NRC resident irspector,
TDR No. 674, Revision 1, " Comparison of Steam Generator Tube Plugging with
the TMI-1 Design Basis." This document stated that plugging up to 2,000
tubes will not adversely affect plant operation and is still bounded by
the FSAR. The licensee plans to officially submit TDR No. 674 (current
revision) to the NRC.
At the request of NRC Region I, the NRC Office of Nuclear Reactor
Regulation (NRR) reviewed and evaluated the licensee's analysis. The NRR
staff's safety evaluation (SE), attached to this report, confirmed that
operation with up to 2,000 plugged tubes does not involve an unreviewed i
safety question and the conclusions in NUREG 1019 remain valid for up to
2,000 tubes. In addition, the SE stated that the upper number of 2,000
tubes was acceptable as long as the plugging ratio between OTSGs does not
exceed a 3 to 1 ratio.
The inspector discussed the SE with appropriate licensee representatives.
The inspector stated that if the licensee, at a later date, was required
to plug in excess of 2,000 tubes or exceed the 3 to 1 plugging ratio, an
additional evaluation would be required to be performed per 10 CFR 50.59
in order to return the unit to operation. No further licensee action
regarding this matter is required at this time.
7.0 Pressurized Thermal Shock Flux Reduction Program
A concern on the capability of pressurized water reactor pressure vessels
to withstand a severe pressurized thermal shock (PTS) without compromising
reactor vessel integrity was under intensive examination by the NRC. A
neutron flux reduction program was proposed by the licensee to reduce
neutron-induced radiation embrittlement of the reactor vessel. The NRC
reviewed the licensee's flux reduction program and concluded in its safety
. - - , - - _ - _ - . . -__ __ - _ - . . _ - . ._
.
. .
15
evaluation that the licensee adequately addressed this issue (NRC letter
dated March 14, 1985, from J. F. Stolz, NRC to H. D. Hukill, GPUNC). The
NRC's conclusion was based on the licensee's plan to implement a low-
leakage fuel loading scheme in future cycles of operation.
~
Based on discussions with the site lead nuclear engineer and later
confirmed by a GPU Headquarters nuclear fuel engineer (through telephone
conversation), the inspector noted that the low-leakage fuel loading scheme
(in-out-in strategy) is planned for Cycle 6 reload. However, due to the
long delay in Cycle 5 restart, the actual Cycle 6 fuel design was not
initiated. The proper design and implementation of the flux reduction
scheme for Cycle 6 reload is unresolved pending completion of licensee
action and subsequent NRC Region I review (289/85-20-02).
8.0 Part 21 Report Followup
The inspector reviewed the below noted 10 CFR 21 and 10 CFR 50.55(e)
Reports to ascertain the nature of the problems (deficiencies) as related
to TMI-1. Subsequently, he reviewed licensee corrective actions to ascer-
tain if the licensee received complete and appropriate information from
the applicable vendor and if licensee corrective actions were adequate to
resolve the deficiency consistent with vendor recommendations.
8.1 Small Break Operating Guidelines (SB0G)
Reference
B&W letter from J. H. Taylor to R. C. DeYoung, dated
July 29, 1983 (Part 21 Report)
The original SB0G did not deal to any great extent with the
pressurized thermal shock issue. As a result, it is possible to have
misused or misinterpreted a statement contained in the SB0G. The
reference letter clarified the ambiguities, specifically the repres-
surization restriction following the RCS cooldown below 500 F not to
exceed a rate greater than 100 F/hr. The inspector reviewed the
Abnormal Transient Procedure 1210-10, Figure 1, and noted that the
PTS concerns and proper RCS cooldown rates were clearly included in
the procedure. The inspector had no further questions.
8.2 HPI Throttle Valves
References
(1) Letter from G. R. Westafer (Florida Power Corpora-
tion) to J. P. O'Reilly (NRC Region II), dated June
27, 1983 (Part 21 Report)
(2) IE Information Notice No. 80-48 and Supplement 1
The failure of throttling HPI valves and similar failures involving
Rockwell International globe valves were reported to the NRC. The
licensee uses 2 1/2" Rockwell International globe valves in the HPI
_
. .
.
16
lines at TMI-1 for throttling purposes (MU-V 16 A through D). The
,
inspector discussed this subject with the licensee mechanical engine-
ering representative and he learned that the licensee was aware of
the problem encountered at the other sites. This is evidenced in the
completion of the licensee's Licensing Action Item No. 84-9519.
As a result of the licensee's evaluation, a procedure note cautions
against backseating valves with torque switches set in accordance
with Corrective Maintenance Procedure 1420-LTQ-1, "Limitorque Opera-
tor, Limit Switch Adjustment," Revision 8. The inspector further
reviewed the machinery history report for MU-V 16A through D, and found
no similar deficiencies were ever recorded in the plant history. The
inspector also reviewed the hign pressure injection flow test results
(SP 1303-11.8) performed on April 11-12, 1985, and noted that no un-
acceptable conditions were identified. The inspector concluded that
the licensee either had or had taken reesonable measures to assure
operability of the HPI throttling valves.
8.3 D.C. Batteries
Reference
Letter from W. P. Murphy (Vermont Yankee Nuclear Power
l Corporation) to T. E. Murley (NRC, Region 1), dated June
- 29, 1984 (Part 21 Report)
.
A potential deficiency involving corrosion in the lead posts of the
I batteries supplied by Exide Corporation was reported for Vermont
( Yankee. Through discussions with the licensee's cognizant representa-
- tive, the inspector learned that the station batteries were supplied
! by C&D Corporation. Appropriate preventive maintenance has been
implemented to ensure the operability of the station batteries. The
inspector physically walked down the 'A' and 'B' battery rooms and
,_ noted that battery posts were clean with no crud buildup, and no
i
cracking or negative plate discoloration. The licensee had previously
- noted cell cracking at TMI-1 but reasonable measures are in place to
j assure the timely detection of cracks before they would affect the
i operability of the battery bank. Battery bank replacements are
,
planned for a future refueling outage.
8.4 Hydrogen Recombiner
8.4.1 References
(1) Letter from D. C. Empey (Rockwell
International) to U. Potapovs
(NRC, Vendor Inspection Brarch), dated
December 15, 1981
(2) Letter from D. C. Empey to J. Collins
(NRC, Region IV), dated May 5, 1983 (Part
21 Report)
. - - . -_-..
_ _ -
- _
, c, . -
2
, m. h
'
, ., .f 's
.n 1
17
, ,
9, n -
,
,
,. .g.
"
. - +
y .
'
c 8
'(3) LettdrfromD.C.Em'eytoJ. Collins,
'
p '
-
dated Ma'y 27, 1983 '
(Part 2h Report)
s (4) Letter f rom D. C. Empey.19, 1983 ,to J. Collins,
dated December '
. (Part 21 Report) ~
,'(5) IE Information Notice No. 85-08, Item 3 ,
u
-
(6) IE Information Notice No. 83-72, Items >17 & 18 '
~
. .
1
8.4.'2 A . Review / Findings
. 3
l
i
's
As a result of environmental qualification testing exper-
,
(s
- N'
i
ifence, sdveral concerns related to the hydrogen recombiner.' '
coOpon'ents were reported by'Rockwell International
'(Energy Systems Group). The following d'escribes each -
concern and the licensee's' response / action: - '
8.4.2.1 Viton Seals '
s
'
d ton seals were used at the recombiner inlet and outlet
piph-to-blower housing flanges, and at the blower flowmeter'. :
The material's sealing capability may be degraded due to
exposure to radiation, levated temperature, and steam
envi ronments'.- The licensee has evaluated this problem
(Pemorandum'frem S. U. Zaman to D. Shovlin/R. Knight," dated
May 24, 1985). .As"a result, new qualified seals have,been
s ordered and the replacement s has been scheduied on an annual
'
'bisis. N' s 'T' %.
8.4.2.2 LeadwireInshl'atinn !
., 1 , s -
- - t
3 t cl %.
s s ,' I I
'
The o\righ al h ater'leadwire' routing areas may reach
temperatures higher than the leadwire insulation design
l rating (194 F). 'fluring the iccidqnt conditions, this may .
result in a reduced service for t.he leadwire insulation.
The licensee corrected this probler by installing a new g
qualified leadwire per job ticket No. CA075 on January. 24,
1983.
'
. ,
8.4.2.3 Time Delay Rilay and Circuit Breaker
'
-
The subject components failed the vendor's environmental
'
.
qualification, test. However, these components at TMI-1 are
-Icceted Jithin"the intermediatetbuilding and are not
exsosehto a' postulated LOCA coddition. The test results
'
3
werenot9pplicabletothequalificationofthesecompon-
'
s
ents.
l.
s .
I
s
I
..,
.,
-
R
s
'* .
{
. _ _ _ _ _ _ _ _ _ _
.
18
8.5 Conclusion
The licensee has taken proper corrective action in response to
the various 10 CFR 21 Reports, IE Information Notices, and
Industrial Experience Reports noted above.
9.0 Security of TMI-1 Operator Examinations
Additional review of the subject matter was conducted as a result of Three
Mile Island Alert's (TMIA) appeal to the Atomic Safety and Licensing
Appeal Board subsequent to the issuance of NRC Inspection 50-289/85-12.
The incident involved the discovery of a microfiche copy of a TMI-1
auxiliary operator examination in the TMI-2 parking lot. Subsequent
investigation determined it to be a record of a completed examina-
tion that had been administered about a year prior to its discovery.
In accordance with the licensee's procedures, examination security
requirements for Category 1 examination materials applies to the
period of time when an exaniination is prepared, administered and
graded. Once this process is completed, the materials become a
record and are not considered to be Category I materials.
Based on discussions with licensee personnel and a review of applicable
procedures, the inspector determined that completed examinations are
i controlled until the administration of examinations to all operators is
completed. Copies of the examinations are subsequently decontrolled and
made available to the operators if requested.
Previously administered examinations are produced from an examination
question bank and the requirements for the selection of questions from the
bank are such that the contents of a new examination are not identical to
any previous examination. This assures that the potential for any par-
ticular examination containing a substantial number of the same questions
as a previous examination is extremely remote. Nothing would preclude an
operator, once in receipt of a graded examination, from generally
distributing it. A parallel of this process is the program for NRC-
administered licensed operator examinations in that, although exams to be -
administered are secured, once they have been administered and graded
they, along with the answer key, become a public record.
In summary, the licensee met its procedural requirements for the
control of examinations and thereby continued to implement the com-
mitments made to the licensing board.
10.0 Control Room Habitability Test
During this inspection period, the resident inspector accompanied an NRR
systems engineer in witnessing portions of Startup and Test Procedure
(STP) 141/3, " Control Building (dP) Test with Single Mode Failure." The
inspector found the STP to be detailed and specific enough to ensure that
the tes; met the scope or stated objective of the test. The test results
__ ___
.
.
l
l 19
l
l
l
indicated areas within the control building that were at a lower pressure
than adjacent areas. The NRR systems engineer discussed the test results
, with the licensee's representatives and stated that their submittal to the
! NRC would have to demonstrate that these low pressure areas would not have
!
an adverse affect on the habitability of the control room. The inspector
had no further questions regarding this test.
11.0 Licensee Action on Previous Inspection Findings
'The following items were reviewed to assure that the licensee took ade-
quate corrective action in a timely manner and/or met their commitments as
stated in applicable inspection reports.
11.1 (CLOSED) Inspector Follow Item (289/83-BC-02): Instal-
lation of Engineering Safety Features (ESF) Ventilation
System for the Fuel Handling Building (FHB)
The NRC staff TMI-1 Restart Safety Evaluation Report (NUREG 0680,
Supplemant 3, page 19) accepted licensee plans to install the ESF
Ventilation System for the FHB in accordance with Regulatory Guide
1.52, Revision 2. By Partial Initial Decision, dated December 14,
1981, paragraph 1265 and Order, dated April 5, 1982, the TMI-1
-Restart ASLB accepted these plans for a commitment of prior to TMI-I
fuel movement from the reactor core for Cycle 6 refueling.
The inspector monitored a licensee preliminary engineering design
review at the corporate office (paragraph 5.2). The inspector
verified that the safety design objectives as a result of the TMI-1
restart hearings were incorporated into licensee design documents
specifically or by reference to Regulatory Guide 1.52, Revision 2.
Inspector Follow Item 289/83-BC-02 is considered closed. However,
proper implementation of the design requirements is unresolved
pending completion of licensee action and subsequent NRC Region I
review (289/85-20-03).
11.2 (CLOSED) Inspector Follow Item (289/83-BC-01, 03, 06, '
07, 08, 09, 13, 18, and 19): Various modification
commitments to upgrade the emergency feedwater system to
safety grade
Additional details for each of the items is addressed in paragraph
5.3.3. The inspector verified that the safety design objectives are
incorporated into licensee design documents. The proper implementa-
tion of these design requirements to meet safety grade criteria is
unresolved (paragraph 5.3.3.5) pending completion of licensee actions
i
and subsequent NRC Region I review.
l
. . _ _ _ _- _ J
.
i
.
20
11.3 (CLOSED) Inspector Follow Item (289/84-11-02): Update
RM-L6 Alarm Response Procedure
In NRC Inspection Report 50-289/84-11, the inspector noted that the
alarm response procedure (C-2-1 alarm procedure) for the plant liquid
release radiation monitor, RM-L6, lacked specific guidance on how
many times the monitor could be backflushed if the monitor alarmed.
The procedure did not address when sampling was required in conjunc-
tion with backflushing. The inspector noted that the alarm response
procedure was inconsistent with the licensee's approach to other
radiation monitoring alarms. Because the RM-L6 alarm signal is used
to terminate a plant release when the monitor exceeds a certain
radiation level, the inspector questioned the adequacy of management
guidance to shift personnel.
Subsequently, the licensee revised the C-2-1 alarm procedure. The
revised procedure stated that the monitor may be backflushed once
before a sample must be taken and analyzed. If the monitor did trip
after the backflush, the operator was to investigate the cause before
re-establishing the release. Based on the inspector's review, the
revised procedure is now consistent with the intent of the applicable
corresponding emergency and radiological control procedures.
11.4 (CLOSED) Violation (289/84-16-04): Failure to Properly
Follow Radiation Work Permit (RWP)
As described in NRC Inspection Report 50-289/84-16, the inspector, I
while witnessing the demonstration of post-accident chemistry analysis,
noted on two occassions the failure on the part of a chemistry
technician to wear an alarming dosimeter when entering the Nuclear
Sample Room. The applicable RWP required that a "Xetex" alarming
dosimeter.be worn by each individual. The licensee held a critique
to determine the cause of the violation. The licensee's review noted
that the chemistry technicians indicated that they were unaware that
the Xetex had to be worn by at least one person in the laboratory or
sample room when occupied. The technicians indicated that leaving
the dosimeter on a laboratory bench gave no less representative
exposure reading for technicians not assigned a Xetex than if the
dosimeter was being carried by a single technician in the group. The
licensee concluded the cause of the incident was the failure of
health physics personnel to properly communicate Xetex use require- ,
'
ments to the chemistry technicians.
GPU responded to this notice of violation in a letter (5211-84-2223),
dated August 30, 1984, to NRC Region I. The licensee stated that
corrective actions taken were:
--
a critique was held on the day of the incident. Radiological
Investigative Report No.84-009 details the actions and con-
clusions of this critique;
.
.
21
--
a memorandum detailing the requirements for use of a Xetex
instrument has been reissued to all TMI-1 departments; and,
--
all chemistry technicians have been instructed or otherwise
informed as to the requirements for use of the Xetex dosimeter.
The inspector reviewed the applicable licensee records that docu-
mented the above corrective action. The inspector also discussed the
corrective action with a plant chemistry foreman to ensure that the
use of alarming dosimeters was understood and discussed the cause
and corrective measures with station health physics personnel.
During this review the inspector noted that part of the root cause
also stemmed from a lack of familiarity by certain personnel on their
individual responsibilities associated with personnel radiation
, protection and as low as reasonably achievable (ALARA) concepts. The
inspector stated that these facts should be emphasized in the general
employee radiation training. However, the inspector noted that this
training was strongly emphasizing that if you had a " Rad Con" problem,
station health physics personnel were there to solve the problem.
Apparently, some general employees had translated this idea into the
belief that the Radiological Controls (Rad Con) Department was
responsible for assuring their protection in the area of radiation
exposure.
The Rad Con Manager restated that it was both the individuals' and
station health physics personnel responsibility. The licensee's
training representative stated they would review the training to
ensure proper emphasis on individual responsibilities. The Rad Con
Manager also stated that he was meeting with operation and mainte-
nance personnel to reemphasize items such as this. The inspector
determined that the licensee's corrective and preventive measures
were appropriate for this violation, and that individual misunder-
standings did not result in a radiological controls programmatic
breakdown.
4
11.5 (CLOSED) Unresolved Item (289/84-24-01): Licensee to
review job ticket for short form release to maintenance
for its completion
NRC Inspection Report 50-289/84-24 described an inconsistency on
how shift foremen were signing off the release of equipment to main-
tenance. This occurred when work was being performed on important to
safety equipment. Maintenance procedure 1407-1 did not provide
proper guidance on when shift foremen signatures are required to
commence work.
. _ - _ - - - - - _ - _ _ ._. _ _ - .. . ___. _ -_ ,-
.
.
22
The inspector reviewed Maintenance Procedure 1407-1, Revision 23,
dated January 31, 1985. The inspector determined that adequate
guidance was now incorporated in this procedure. The inspector
reviewed package C-964, " Minor Maintenance on Various Components in
the Reactor Building," dated February 8,1985, and determined that
various job tickets were now being completed consistently.
11.6 (CLOSED) Violation (289/84-24-02): Failure to determine
the adequacy of minor maintenance work form to meet ANSI
18.7-1976
NRC Inspection Report 50-289/84-24 indicated that Maintenance Proce-
dure 1407-1, " Unit 1 General Corrective Maintenance," Revision 16,
dated August 23, 1984, was not reviewed, in part, for adequacy.
Specifically, for minor maintenance, the work form was not adequate
in that it did not provide for: 1) documented release of important
to safety system equipment to maintenance by the operations depart-
ment, 2) traceability of materials / parts, 3) documented use of
maintenance procedures, and 4) specified post-maintenance test
procedures including test acceptance criteria.
In a letter, dated December 5, 1984 (H. Hukill, GPUN to T. Murley,
NRC) the licensee responded to the above Appendix A, Notice of
Violation. Region I Inspection Report 50-289/84-38, described the
licensee's response to this violatien. The licensee's corrective
actions were acceptable as stated in an NRC Region I letter dated
March 13, 1985. However, the licensee was requested to provide a
supplemental response to more fully address the root cause and
corrective actions taken or planned to avoid further violations of
this type. A letter, dated April 12, 1985, (H. Hukill, GPUN to T.
Murley, NRC) provided the licensee's supplemental response.
The inspector reviewed Maintenance Procedure 1407-1, Revision 23,
dated January 31, 1985. The four items identified in the notice of
violation were adequately addressed in Revision 23; therefore, the
corrective steps taken by the licensee were acceptable. The correc-
tive actions to prevent further violations of this type was to pro-
vide guidance to all safety reviewers in the TMI-1 division. This
was accomplished by an internal licensee memorandum dated April 9,
1985, (Nelson, GPUN, to PORC Members, 3200-85-9016). The inspector
determined that this memorandum was a reasonable measure to pre-
vent similar violations in the future. The effectiveness of these
measures will be routinely reviewed by the resident inspectors.
11.7 (CLOSED) Inspector Follow Item (289/84-37-01):
Inservice Testing (IST) Program Stroke Timing Requirements
NRC Region I Inspection Report 50-289/84-37 indicated that the river
water supply to emergency feedwater system suction check valve EF-V3
l was only partially stroke tested in the in-service testing (IST) program.
Also, stroke timing for turbine driven EFW pump steam supply line valves
l MSV-10A and MSV-108 was not included in the surveillance procedure.
l
-
1
L
r
.
.
23
By various letters to the NRC the licensee sought IST relief for
EF-V3 to conduct partial stroke testing in lieu of full stroke
testing as required by the ASME Code,Section XI. However, this
request was denied (NRC letter from J. F. Stolz to H. D. Hukill,
dated October 23,1984). As an alternate proposal, the licensee
plans to remove the internals of the check valve. The licensee is
now in the process of evaluating the safety impact of this action.
The inspector will review the results of the evaluation during a
subsequent inspection (289/85-20-04).
The inspector reviewed the surveillance procedure 1300-3K, "IST of
Valves During Shutdown and Remote Indication Check," Revision 13,
and noted that the stroke timing for MSV-10A and MSV-10B was
incorporated in the procedure.
12.0 Restart Readiness
The NRC Inspection Report 50-289/85-19 documented the TMI-1 Restart Staff
conclusion that there were no adverse conditions that would affect the
safe restart of TMI-1. During this inspection period, the resident
inspector continued to monitor plant status from a viewpoint oriented
toward major equipment operability problems. Based on this review, the
inspector concluded that there still was no adverse condition that would
affect the safe restart of TMI-1 except for sporadic inoperability periods
for one of two channels of source range nuclear instrumentation. This
. problem needs further evaluation prior to restart. Prior to any restart
authorization, the TMI-1 Restart Staff will conduct another review of all
open licensea and NRC issues similar to the restart readiness reviews
previously documented.
13.0 Exit Interview
The inspectors discussed the inspection scope and findings with licensee
management at the exit interview conducted on August 2, 1985. The follow-
ing personnel attended the final exit meeting:
--
J. Colitz, Plant Engineering Director, TMI-1
--
W. County, Quality Assurance Lead Auditor, Nuclear
Assurance Division
--
E. Eisen, Project Engineer, Technical Functions Division
(TFD)
--
D. Hassler, Licensing Engineer, TFD
--
S. Otto, Licensing Engineer, TFD
As discussed at the meeting, the inspection results are summarized in the
cover page of the inspection report. The licensee representatives indi-
cated that none of the subject matter discussed contained proprietary
information. The inspector noted that there were no obstacles (physical
or administrative) to the safe restart of the unit, however, the
potentially unreliable channel of source range instrumentation requires
further evaluation prior to restart.
. . . - - - - - . . . .- - . -
.
.
i
l 24
l
l. Unresolved Items are matters about which information is required in order
! to ascertain whether they are acceptable items, violations or deviations.
[ Unresolved item (s), discussed during the exit meeting, are documented in
l paragraphs 5.3.3.5, 7.0, 11.1, and 11.5.
Inspector Follow Items are matters which were established to administra-
tively follow open issues based on licensee or staff commitments from the
TMI-1 restart hearing. Inspector follow item (s), discussed during the
, exit meeting, are documented in paragraphs 5.3.3, 11.1, 11.2, 11.3, and
!
11.7.
i
l
l~
l
i
I
<
$
1
.
'
$
i
__
J
v w ss- - , , . - --,n-- - -..-. . .,, - . _ . -_ , , , ,.,,--c.,,.,,n--.,., -. u ..,,,.w,,n , , , - --.,.7, ,., , ,,,,, , , , ,,,._r. g, --e.~,+.-
.
-
ATTACHMENT TO REGION I INSPECTION REPORT N0. 50-289/85-20
+
[Q MQ UMTED STATES
E ~. c NUCLEAR REGULATORY COMMISSION .
E .I WASHINGTON, D. C. 20555
.....
OFFICE OF NUCLEAR REACTOR REGULATION .
EVALUATION OF OPERATION OF TMI-1 WITH UP TO
2000 PLUGGED STEAM GENERATOR TUBES
1. Introduction
In the staff's Safety Evaluation Report related to steam generator tube
i repair and return to operation of TMI-1, NUREG-1019, we examined the
effects of plugging up to 1500 steam generator tubes on TMI-1 reactor
thermal and hydraulic considerations and on various transients and
accidents. We concluded that the thermal-hydraulic consequences of such
operation were acceptable, and that accident consequences were bounded
by the FSAR analysis or meet appropriate criteria and were therefore
acceptable.
Since that time, additional tubes have been plugged and the total now
is 1542. The licensee submitted its safety evaluation TDR No. 674,
i Comparison of Steam Generator Tube Plugging with the TMI-1 Design Basis, -
- in which it also concluded that plugging 3000 tubes would have no adverse
affect on performance of the steam generators or on licensing basis analyses
- for transients and accidents. However, in order to assure conformance with
'
present Technical Specifications, the licensee in Revision 1 to TDR No.
!
674, limited the applicability of that document to 2000 tubes. The
licensee also concluded that plugging up to 2000 tubes does not involve ,
i an unreviewed safety question as defined in 10 CFR 50.59. '
We have reviewed TDR No. 674 to verify the licensee's conclusions. Our
evaluation is sumarized below.
'
2.0 Evaluation
2.1 Core Thermal-Hydraulic Design
The existing TMI-1 safety analysis for Cycle 5 operation is based on a
power level of 2568 ht and a reactor cgolant system (RCS) flow of
106.5% of the design flow of 131.3 x 10 lbm/hr. The licensed TMI-1
power level is 2535 h t and the measured four pump flow is reported to
be 109.5% of the design flow, with 1.5% flow calibration uncertainty,
Plugging of steam generator tubes increases the RCS flow resistance and
results in flow degradation. The licensee has calculated that RCS flow
reduction of 2.0% would result from the plugging of 3000 tubes. Thus,
considering flow uncertainty, this case could result in an actual flow
of 106.0% which is slightly below the existing safety analysis and
Technical Specification limit of 106.5% for four pump operation. We
have considered.the impact of this reduced flow on reactor protection
-
system trip limits and capability for full power (2535 Nt) operation,
as discussed below.
-
_- . - - _ - _ . . - - - . - _ . _ . - . . .-- - _
.
.
ATTACHMENT TO REGION I INSPECTION REPORT N0. 50-289/85-20
-2-
'
Even though tube plugging results in reduced RCS flow, the flux / flow
<
trip function in the TMI-1 plant protection system provides necessary
protection with respect to overpower at reduced flow. This trip
function is specified in the TMI-1 Technical Specifications where the
power level trip setpoint is dependent on the RCS flow rate and power
,
imbalance. Flow reduction reduces the power level trip and associated
reactor power / reactor power-imbalance boundaries by 1.08% for a one
percent flow reduction. This is based on the sensitivity of DNBR margin
to power and flow changes and prevents a DNBR of less than 1.3 (limit
value) if a low flow condition should exist due to any malfunction.
For the licensed power level of 2535 Mwt. the safety analysis DNBR
margin and protection system setpoint bases would be preserved for
reduced flow to 105.3% of design flow based on the power / flow versus
DNBR sensitivity relationship. Thus, the existing setpoint for overpower
, protection (105.5%) could be justified for actual flow as low as 105.3%.
However, the flow is limited by current Technical Specifications to a
minimum value of 106.5%. We have also reviewed the licensee's
statements that up 40 2000 tubes could be plugged without reducing flow
below the TS figure, and we concur with that conclusion.
, The licensee has also evaluated the plugging of 3000 tubes with a plugging
ratio of 3:1, i.e., 2250 tubes in OTSG "A" and 750 tubes in OTSG "B". '
The licensee's calculation has determined that this plugging 4
' * configuration would result in loop "A" flow rate approximately 2.5%
smaller than loop B. However, the licensee also states that field data -
during the last cycle had shown that A loop had typically about 3% more
flow than B loop. As a result, the net flow difference due to 3:1 plugging
configuration would be approximately 0.5%, and therefore, the 3:1 plugging e
configuration is acceptable.
In summary, existing reactor protection system setpoints provide DNBR
protection for power operation at 2535 Mwt with flow reduced to 105.3%
even though the flow is limited to a low value of 106.5% by current
- Technical Specifications. We conclude that TMI-1 can be operated
within the TS limits on RCS flow with up to 2000 tubes plugged. As part
of the power escalation test program, the licensee will verify by flow
! calibration that the RCS flow remains above existing Technical ;
, Specification limits.
~
2.2 Transient and Accident Analysis
i'
.
The effect of plugging up to 3000 steam generator tubes on the
consequences of design basis transients and accidents will be minimal.
The steam generator tubes account for less than 25% of the total RCS
, pressure drop. Plugging 3000 out of a total of more than 30,000 tubes
!
would cause the pressure drop through the steam generator tubes to
increase. As discussed above, this increase in pressure drop would
cause the total coolant flow to decrease by approximately 2% as
'
r
l
l
_ _ _ _ - _ . _ - . _ _ , . _ _ ,._____ _ .__ ___.__.s,___.__.-..___ _ _ _ _ _ _ _ - _ . _ - _ . . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
<
.
.
'
i ATTACHNENT TO REGION I INSPECTION REPORT NO. 50-289/85-20
!
-3-
. calculated by the licensee. For transients and accidents involving loss
i of forced coolant flow the effect of the tube plugging on flow coast
down and natural circulation flow would also be of little significance,
because the stalled coolant pumps introduce a large flow resistance in
the coolant loops that is substantially greater than the flow resistance
imposed by tube plugging. The effect of the plugged tubes on the ability
of the steam generators to remove heat would also be minimal. During
power operation, secondary system water level would be adjusted upward
as needed to provide for reactor system heat removal. Following reactor
trip the heat transfer surface would be more than adequate to remove
core decay heat.
'
The licensee evaluated the consequences of design basis transients and
accidents and concluded that the evaluations previously submitted in
support of the original license application would still be bounding.
The design basis loss of coolant accidents for TMI-1 were evaluated for
a generic B&W Plant with lowered loops having a power level 9% higher
than that of TMI-1 using approved 10 CFR Appendix K models. The most
severe small break LOCA was detennined to be a 0.07ftr cold leg break.
i This break size would be sufficient to remove decay heat so that steam
generator heat removal would not be required. Uncovery of a region at
i the top of the core was calculated to occur between 1350 seconds and -
1750 seconds. At this time the steam generators would be acting as a
heat source and not be aiding in core cooling. Loss of steam generator
'
.
heat transfer surface from tube plugging would not affect the
consequences of this accident.
.
One class of small break LOCA depends on steam generator heat removal
for event recovery. Break sizes of 0.01ft8 and smaller would be unable to
,
remove reactor decay heat solely through the break and would require
i steam generator heat removal in the boiler-condenser mode. Previous
'
j analyses of small breaks in this size range without tube plugging have
demonstrated that the consequences would not be bounding and that
neither core heatup nor core uncovery would occur. The boiler-condenser
mode of decay heat removal involves condensation of steam generated by
i the core on condensing surface in the steam generators. The
'
the outennost tubes and the action of the operator to raise the steam
generator water level to 95% on the operating range, which is well above
the top of the core. The establishment of an adequate condensing
surface above the top of the core is important to provide for reactor
I system depressurization which increases high pressure injection flow
! preventing core uncovery. The staff has concluded that at the 95% level
l an. adequate condensing surface would be available to remove all decay
'
heat, with a considerable margin. The plugging of 3000 tubes would
remove 10% of this condensing surface. However, the remaining surface
'
would still be more than adequate to remove all decay heat. The staff
j concludes that core uncovery would not occur for breaks in the size range
of 0.01fte and smaller if up to 3000 tubes are plugged.
'
,
_ _ _ _ _ _ .
.
'
!
e
ATTACHMENT TO REGION I ItiSPECTION REPORT NO. 50-289/85-20
!
! -4-
i
,
For large break LOCA analysis, a critical feature for some plants is the
resistance of steam flow through the reactor coolant loops and steam
generators during reflood. For TMI-I the peak cladding temperature was
calculated to occur during the reflooding period. The analysis did not
i take credit for flow in the reactor coolant loops including the steam
generators during this period and assumed they were completely blocked
by water in the cold legs. Relief of steam from the core was assumed
only through the core barrel vent valves. This assumption would be
- unaffected by steam generator tube plugging. The staff concludes that
i the consequences of a large break LOCA would not be affected by plugging
up to 3000 steam generator tubes.
The licensee also evaluated the consequences from non-LOCA transients
- and accidents. The reactor system flow coast down curve in the FSAR for
- loss of forced flow events was detemined to be still bounding for the
case of 3000 plugged tubes. This detemination was made using the B&W
'
PUMP computer code which has been approved by the NRC staff. After the
,
coolant pumps were stopped, natural circulation flow would continue
'
through the core. The natural circulation flow was calculated to be
negligibly affected by tube plugging.
'
, ,
The licensee has previously comitted to confim the adequacy of natural
- circulation flow in tests at low power during power escalation. This
action is included in the restart license conditions.
Since steam generator secondary side water inventory will increase in
'
>
,
order to compensate for the reduced heat transfer surface following tube
i plugging, the licensee evaluated the revised inventory in comparison to
! that assumed in the FSAR for steam line break analysis. The FSAR
i inventory assumption of 55,000 lbs was detemined to bound the revised
steam generator water mass by a considerable margin.
1 In the event of loss of feedwater or a main feedwater line break, the
, increase in inventory would provide an additional heat sink until EFW
! could be actuated. More time would be available before steam generator
l dryout could occur. The FSAR analyses would therefore be bounding for
! events of this type.
Although the analysis of a locked _ reactor coolant pump rotor is included
in the FSAR, the licensee did not evaluate the consequences of a
'
locked rotor accident accounting for plugging 3000 tubes. The licensee
has stated that the design basis locked rotor analysis, which assumed no
plugged tubes, also assumed very conservative values for loop
resistance, core power peaking, and core flow bypass. Because of these
factors and the small change that tube plugging produces on reactor
3
coolant flow, the staff does not expect that the consequences from ,
- accidents of this type would be significantly affected. The licensee
j should, however, analyze this event to confim this conclusion.
'
i
!
1
!_- _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
.
9
.
ATTACHMENT TO REGION I INSPECTION REPORT N0. 50-289/85-20
-5-
The licensee evaluated other design basis events including boron
dilution, coolant pump startup, loss of electric power and steam ;
l
generator tube failure. The licensee concluded that these events would
not be significantly affected by plugging up to 3000 tubes. The staff
agrees with these conclusions. The effect of the plugged steam generator
tubes on reactivity initiated transients and accidents has been reviewed.
The reductions in flow and heat transfer are not large enough to affect
uncompensated operating reactivity changes, CRA withdrawal events from
startup or power conditions, misaligned or dropped CRA events, fuel
handling events or the rod ejection accident. The FSAR analyses for
these events, therefore, remain bounding.
3.0 Conclusions
Based on our review as summarized above, we find that our earlier
conclusions in NUREG-1019 regarding the effects of plugged steam
generator tubes remain valid for up to 2000 tubes. We agree with the
licensee's conclusion that operation with up to 2000 plugged tubes does
not involve an unreviewed safety question as defined in 10 CFR 50.59.
.
O
e
F