ML20129J377

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Insp Rept 50-483/96-09 on 960901-1012.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support
ML20129J377
Person / Time
Site: Callaway Ameren icon.png
Issue date: 10/12/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20129J360 List:
References
50-483-96-09, 50-483-96-9, NUDOCS 9611060232
Download: ML20129J377 (18)


See also: IR 05000483/1996009

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ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION l

REGION IV i

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Docket No.: 50-483

License No.: NPF-30

Report No.: 50-483/96-09

Licensee: Union Electric Company

Facility: Cal laway Plant

Location: Junction Hwy. CC and Hwy. O

Fulton, Missouri

Dates: September 1 through October 12,1996

Inspectors: D. G. Passehl, Senior Resident inspector

F. L. Brush, Resident inspector

Approved By: W. D. Johnson, Chief, Projects Branch B

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ATTACHMENT: Supplemental information

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9611060232 961031

gDR ADOCK 05000483

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EXECUTIVE SUMMARY

Callaway Plant

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NRC Inspection Report 50-483/96-09

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Operations

  • The licensee identified that an operator had inadvertently closed a nitrogen

accumulator outlet valve which rendered inoperable the power operated relief valve

for Steam Generator C and the auxiliary feedwater flow path from the turbine-driven

auxiliary feedwater pump to Steam Generator C. Plant operators did not adequately

review this activity prior to performance. The failure to utilize a procedure or

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guidance appropriate to the circumstances was identified as a noncited violation

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(Section 04.1).

e Plant operators responded well to an unplanned isolation of low pressure Heater

String C. The inspectors identified that there was no off-normal procedure to guide

operator actions in response to unplanned automatic isolation of low pressure

feedwater heater strings (Section 04.2).

  • The inspectors found that the licensee's program for minimizing shutdown safety

risk was good. Use of the simulator to practice the heatup and cooldown indicated '

good preparation and planning (Section 07.1).

Maintenance

  • The licensee met its goals on outstanding corrective maintenance work requests

prior to the start of Refueling Outage 8. The goal was to have less than

200 corrective maintenance work requests prior to the start of Refueling Outage 8.

There were 104 corrective maintenance work requests outstanding. Additionally,

there was a goal of no more than 30 corrective maintenance work requests greater

than six months old. There were 23 corrective maintenance work requests greater

i than six months old (Section M2.1).

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Enaineerina

  • The inspectors identified a violation involving failure to maintain proper configuration

control during a modification to a hydrogen recombiner. The inspectors found that

the licensee's use of the " Request For Resolution" process to implement

modifications did not have a feedback loop to ensure that procedures, drawings, or

other documents affected by the modification were changed (Section E1.1).

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Report Details

Summarv of Plant Status -

The reactor began this inspection period at 100 percent power. The reactor remained at

fuil power for most of the inspection period. On October 6,1996, plant operators oegan a

gradual reduction of reactor power to support planned activities for Refueling Outage 8.

On October 12,1996, operators opened the main generator output breaker to commence ,

the refueling outage.

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1. ODerations

01 Conduct of Operations

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01.1 General Comments (71707)

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Using Inspection Procedure 71707, the inspectors conducted frequent reviews of l

ongoing plant operations. In general, the conduct of operations was professional  :

and safety-conscious. Plant status, operating problems, and work plans were )

appropriately addressed during daily turnover and plan-of-the-day meetings. Plant j

testing and maintenance requiring control room coordination were properly I

controlled.

02 Operational Status of Facilities and Equipment

O 2.1 Enaineered Safetv Feature System Walkdowns (71707)

The inspectors used Inspection Procedure 71707 to walk down accessible portions

of the following Engineered Safety Feature systems:

  • Component Cooling Water Train A; and

Equipment operability, material condition, and housekeeping were acceptable.

Several minor discrepancies were brought to the licensee's attention and were

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corrected.

02.2 Review of Eauioment Taaouts (71707)

The inspectors walked down the following tagouts for the Residual Heat Removal j

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System Train B planned maintenance outage:

, Worker Protection Assurance 20312 Component Cooling Water to Residual

. Heat Removal Heat Exchanger B isolation

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Worker Protection Assurance 20357 Residual Heat Removal Pump B

Worker Protection Assurance 20358 Residual Heat Removal Pump B Suction

Valve From the Refueling Water Storage ,

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Worker Protection Assurance 20359 Residual Heat Removal Pump B Minimum -

Flow Control Valve

Worker Protection Assurance 20360 Residual Heat Removal Pump B Room

Cooler

The inspectors did not identify any discrepancies. All tags were on the correct

devices and the devices were in the position prescribed by the tags.

04 Operator Knowledge and Performance

04.1 Inadvertent Closure of Nitroaen Accumulator Outlet Valve KAC0637

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a. Insoection Scoce (71707)

The inspectors reviewed the licensee's response to an inadvertent closure of

nitrogen accumulator Outlet Valve KAV0637. Closure of this valve rendered the

main steam to atmosphere power operated relief valve for Steam Generator C and

the auxiliary feedwater flow path from the turbine-driven auxiliary feedwater pump

to Steam Generator C inoperable,

b. Observations and Findinas

On September 18,1996, the system engineer for the compressed air system

requested operations department personnel to close four nitrogen accumulator tank

valves to obtain leak rate data for trending. The accumulators serve as a backup

gas system to supply compressed gas to the four steam generator main steam to

l atmosphere power operated relief valves and the four auxiliary feedwater flow

l control valves at the discharge of the turbine-driven auxiliary feedwater pump.

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The system engineer gave operations personnel a marked-up copy of the associated

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piping and instrument drawing with the valves to be closed. While intending to

mark Accumulator Tank TKA03 Inlet Valve KAV0636, the system engineer

mistakenly marked Accumulator Tank TKA03 Outlet Valve KAV0637. The shift and

control room supervisors reviewed the drawing and erroneously concurred on the

valves to be closed, f ailing to realize an incorrect valve was marked. The shift

supervisor assigned an equipment operator to close the valves indicated on the

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drawing. Closing Valve KAV0637 made two components inoperable: Steam

Generator C main steam to atmosphere power operated relief Valve ABPV0003, and

turbine-driven auxiliary feedwater pump to Steam Generator C discharge

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Valve ALHV0012. Because of persistent questioning by the equipment operator,

approximately 3.3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> later, senior operators and the system engineer realized the

mistake and had Valve KAV0637 reopened.

The licensee convened an Event Review Team to investigate the facts and causes

surrounding this event. The shift supervisor realized he had misread the marked-up

l drawing. In addition, the licensee identified the folhwing:

l There was no procedural guidance or work request directing this activity. A

plant engineer voided a preventive maintenance task that performed this

activity in June 1995 because it was viewed as no longer needed. The basis

was that the preventive maintenance task was effectively accomplished in a

separate surveillance procedure. The surveillance procedure placed the

nitrogen accumulator system in the accident lineup and checked leakage

from each accumulator in accordance with the Technical Specifications.

Plant operators did not perform an adequate review of the drawing prior to

allowing the marked valves to be closed. One reason was that control room

l personnel were busy covering several different activities at the time. This

l included routine and nonroutine activities for the upcoming refueling outage.

The licensee lessened the amount of control room activity by rescheduling

l many activities for off-hours.

The inspectors found:

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  • The licensee's basis for deleting the preventive maintenance task was

inaccurate. The established lineup for the preventive maintenance task

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air from the nitrogen system during normal plant operations. The Technical

l Specification surveillance procedure established a different lineup that could

j not check for leakage past these check valves.

  • The equipment operator performed the requested lineup and immediately

informed the control room supervisor that all requested valves were closed.

The equipment operator specifically pointed out to the control room

l supervisor that he had closed a nitrogen accumulator tank outlet valve while

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closing inlet valves for the other accumulator tanks. Still the control room

supervisor did not realize a problem existed.

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  • The equipment operator showed a strong questioning attitude in following up

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his question with the system engineer.

  • Use of a controlled drawing in lieu of a reviewed and approved work

document to reposition the accumulator valves was minimally acceptable.

The licensee agreed and stated that a reviewed and approved work

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document would be used if there is a future need to test the check valves for

leakage.

The licensee was still evaluating whether the preventive maintenance task for the

check valves would be re-established. This was because the check valves were

recently replaced with little evidence of leakage.

The Technical Specification Action Statement under 3.7.1.2.d allowed 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> for

Valve ALHV0012 to be inoperable since it disabled one of the flow paths from the

turbine-driven auxiliary feedwater pump to the steam generators. Valve ABPV0003

l being inoperable did not require entry into any Technical Specification Action

l Statement since the other three main steam to atmosphere power operated relief

l valves remained operable. The duration of Accumulator Tank TKA03 Outlet

Valve KAV0637 being closed did not exceed the 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> limit.

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The failure to provide procedural guidance or work document to direct this activity,

and the subsequent use of a controlled drawing with the incorrect component

l identified for operation is a violation of 10 CFR 50, Appendix B, Criterion V, in that

the guidance provided was inappropriate for the circumstances. Given that the

condition was licensee identified, :.c Tachnical Specification Action requirements

were exceeded, and the response to the v'ent was prompt and comprehensive, this

violation is being treated as a noncited vic.ation consistent with Section Vll.B.1 of

the NRC Enforcement Policy (483/9609-0 ?).

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c. Conclusions

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l The inspectors found that the licensee did not utilize a procedure or guidance

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engineer. The need for a formal review was evident in that the consequence of the

error was inadvertent entry into a Technical Specification Limiting Condition for

! Operation. The lack of formal review was a weakness that contributed to the

I occurrence of this event.

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04.2 Unolanned Isolation of Condensate Flow to a low Pressure Feedwater Heater Strina

a. Inspection Scope (93702)

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The inspectors observed the licensee's response to an unplanned isolation of low

pressure Heater String C.

l b. Observations and Findinos

, On September 27,1996, an unplanned isolation of condensate flow to low pressure

Heater String C occurred. Plant operators responded appropriately per plant

procedures to minimize the effects of the transient on the primary and secondary

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systems. The licensee held an Event Review Team to investigate the causes and

develop an action plan for corrective and preventive actions.

l The licensee found the probable cause was inadvertent bumping of the hi-hilevel

switch for low pressure feedwater Heater 2C. Investigatiori showed that bumping

of this switch would have resulted in the transient by causing the inlet and outlet

condensate isolation valves for the low pressure Heater String C to close. At the

j time of the event, contractors were removing insulation in the vicinity of the hi-hi

i level switch and may have inadvertently bumped or otherwise contacted the switch.

The licensee identified a list of proposed corrective and preventive actions. This

included re-emphasizing good work practices with contract personnel and assigning

additionallicensee personnel to observe field activities. Also, the licensee was

investigating ways to identify sensitive balance-of-plant instrumentation which

might cause unplanned activation of plant equipment.

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The inspectors found that plant operators responded well to this event. The

operator immediately recognized the feedwater heater string had isolated by visual

l indication of a digital alarm on the main control board computer console. The alarm

f ailed to sound. The licensee later performed troubleshooting on the alarm and

could not identify a cause for the alarm not sounding since the alarm functioned

properly during troubleshooting.

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l The inspectors reviewed plant procedures and identified that there was no off-

normal procedure to guide operator actions in response to unplanned automatic  ;

isolation of low pressure feedwater heater strings. The guidance was contained in l

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multiple places in existing procedures for normal planned removal of low pressure

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heater strings. The licensee also recognized this and began to evaluate issuing an

l off-normal procedure for this type of event.

Overall, the inspectors iound good teamwork by plant operations, maintenance, and

engineering personnel in responding to this event. Licensee management

l appropnately monitored and assisted in the recovery effort.

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c. Conclusions

The inspectors concluded that licensee's overall response to this event was good.

05- Operator Training and Qualification

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05.1 Refuelino Outaae Trainina for Licensed Ooerators

The inspectors observed a refueling training seminar held for plant operators. The

seminar covered topics such as refueling outage work scope, schedule, lessons

learned from the previous refueling outage, safety, and testing. The licensee

required all licensed ope.ators attend one of two seminars.

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Licensee management presented a majority of the topics. In addition to technical

discussions, management presented their expectations for operator performance.

There were open discussions on the various topics. The inspectors found the

outage training to be beneficial for plant operators in understanding outage work

scope and potential problems and contingencies.

05.2 Fire Briaade Trainina

The inspectors reviewed the licensee's fire brigade training and qualification tracking

program. The inspectors did not discover any problems in this area. The details are

discussed in Section F5 of this report.

07 Quality Assurance in Operations

07.1 Refuelina Outaae Shutdown Safety

a. inspection Scone (71707)  :

The inspectors reviewed the licensee's plans for ensuring that the plant meets all

Technical Specification and Final Safety Analysis Report requirements during the f

upcoming refueling outage. This included discussions with licensee management, '

attending one of the operator refueling outage training seminars, and reviewing

Procedure PDP-ZZ-00015, " Shutdown Safety Management", Revision O.

b. Observations and Findinas

Prior to the refueling outage, the licensee's Independent Safety Evaluation Group

reviewed the outage schedule to determine if there were any shutdown safety

problems. The group compared the planned equipment out-of-service schedule with

Technical Specification and Final Safety Analysis Report requirements. To assist in

the review, the group used a software package prepared by the Electric Power

Research Institute. The package used probabilistic shutdown safety assessment

models and various shutdown safety function assessment trees. The group

identified no significant concerns in this area.

The inspectors noted that all operator crews practiced the plant heatup and

cooldown on the plant simulator. Operators recommended some enhancements to

the procedures that were appropriately evaluated and included into the procedures.

The inspectors found that no outstanding issues needed to be resolved as a result

l of the shutdown safety review or from use of the procedures on the plant simulator.

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The inspectors found that during the outage, the operations shift supervisor

performs a formal risk assessment during each shift. Any maintenance schedule

changes are compared to the equipment out-of-service list. The shift supervisor

then presents the results of the risk assessment during the twice daily outage

schedule meetings. Any actual or potential problems concerning shutdown risk are

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resolved during the meeting. The licensee displays the updated outage risk j

assessment to ensure personnel are aware of the plant status. l

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c. Conclusions j

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The inspectors concluded that the licensee's program for minimizing shutdown

safety risk is good. In addition, use of the simulator to practice the heatup and j

cooldown indicated good preparation and planning. The inspectors did not identify

any concerns.

08 Miscellaneous Operations issues

08.1 (Closed) Violations 50-483/9508 01 and 50-483/9518-02: Failure of the Control

Room Operators to Review Control Room Narrative Loas Prior to Assumina the

Watch

in several instances the operators failed to read completed control room logs prior to 1

assuming the watch, in addition, the inspectors noted problems in the quality of

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shift turnovers.

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Since March 1996, the inspectors have observed numerous shift turnovers. The

inspectors did not identify any instances of a control room operator failing to read

the control room logs prior to assuming the watch.

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Additionally, the quality of the shift turnovers has improved. Prior to assuming the

watch, the operators discuss the plant status with the offgoing reactor operators,

walk down the control boards, and review the status of plant equipment. The

operators also review the current night orders to determine if there are any issues

that could affect plant operations. The inspectors have no further concerns in this

area and these violations are closed.

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11. Maintenance

M1 Conduct of Maintenance and Surveillance

M 1.1 General Comments - Maintenance  ;

a. Insoection Scoce (62707)

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The inspectors observed or reviewed all or portions of the following work activities: l

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  • Work Document W180963, Repair seat leakage on essential service water l

Train A to turbine-driven auxiliary feedwater pump Valve ALHV0032;

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Emergency Diesel Generator A room Supply Fan CGM 01 A;

sump heaters Train A;

sump heaters Train B; and

  • Work Document W179860, Rebuild nitrogen supply regulator for

turbine-driven auxiliary feedwater pump to Steam Generator C flow control

Valve ALHVOO12, and Steam Generator C ttmospheric relief

Valve ABPV0003.

b. Observations and Findinas

The inspectors found most work performed to be professional and thorough. All )

work observed was performed with the work packages present and in active use.  :

The inspectors frequently observed supervisors and system engineers monitoring job

progress, and quality control personno' were present when required. Housekeeping

and foreign material exclusien contro.s were satisfactory. Some minor weaknesses

were identified and discussed with appropriate licensee personnel.

M1.2 General Comments - Surveillance

a. Insoection Scope (61726)

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The inspectors observed or reviewed all or portions of the following test activities: I

  • Surveillance Procedure OSP-AL-P0002,"Section XI Turbine-Driven Auxiliary

Feedwater Pump Operability";  ;

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  • Surveillance Procedure OSP-AL-P0018,"Section XI Motor-Driven Auxiliary

Feedwater Pump B Operability"; and

  • Surveillance Procedure CTP4Z-01010," Sampling of Secondary Grab Sample

Points."

b. Observations and Findinas

Surveillance testing was performed satisfactorily.

in addition, see the specific discussions under Section M1.3 below.

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M1.3 Section XI Motor Driven Auxiliary Feed Pumo B Operability Test

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a. Inspection Scope (71707)

The inspectors observed the normally scheduled motor-driven auxiliary feedwater

Pump B pre-job briefing and operability test. In addition to the operability test,

mechanical maintenance personnel adjusted the pump's packing while the pump <

was running.

b. Observations and Findinas

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The control room supervisor conducted a thorough pre-job briefing. All personnel

involved in the effort were present. The briefing included an overview of the work

to be accomplished as well as potential problems and plant transients. The

communications between the control room operators and field personnel during the

test were good. Licensee management was also present for the briefing and pump  ;

run and reinforced their expectations on coordination and communications. The l

inspectors did not note any problems. i

M2 Maintenance and Material Condition of Facilities and Equipment i

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M 2.1 Review of Plant Material Condition  !

The inspectors reviewed licensee data on material condition of the plant. The

licensee's goal was to have less than 200 corrective maintenance work requests  !

prior to the start of Refueling Outage 8. The licensee met the goal, with

104 corrective maintenance work requests. Additionally, a goal of no more than l

30 corrective maintenance work requests greater than six months old was

established. The licensee met the goal, with 23 corrective maintenance work

requests greater than 6 months old. In all, the licensee started the cycle with 985

plant work requests, and ended the cycle with 495 work requests. Plant work

requests included corrective maintenance work requests but did not include work

activities performed on spare parts or in buildings outside the power block.

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l M8 Miscellaneous Maintenance issues l

M 8.1 (Closed) Insnection Followup item 483/9518-01: Ultimate Heat Sink Train B Sumo

Blocked with ice

On January 3,1996, while performing his daily sump inspection, a plant equipment

! operator found the ultimate heat sink Train B sump blocked with several inches of

ice. Plant operators declared the ultimate heat sink Train B sump inoperable. I

Workers immediately broke up the ice, returning the sump to an operable status.

The licensee found the formation of ice to be due to the failure of both temperature

switches in the ultimate heat sink Train B sump. As an immediate corrective action,

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the licensee implemented a temporary modification to jumper around the

temperature switches so that the heaters remained energized. As a long term 1

corrective action, plant engineers developed a permanent modification to increase

the reliability of the system.

The licensee removed the temporary modification and installed the permanent

modification as discussed in NRC Inspection Report 50-483/95-18. The inspectors

reviewed the modification package, observed functional testing of the Train B

heaters, and reviewed documentation on testing of the Train A heaters. The test.

results were satisfactory. The licensee has included annual testing of the heaters in

the preventive maintenance program.

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E1 Conduct of Engineering

E1.1 Installation of New Temperature indicator for Hvdroaen Recombiner Train B i

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a. Insoection Scope (37551)

l The inspectors reviewed a plant modification to install a like-kind replacement for an

l indicator to monitor containment hydrogen recombiner Train B temperature.

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b. Observations and Findinos

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l Instrument and control personnel replaced the old analog temperature indicator,

GSTl0029, for hydrogen recombiner Train B with a new digital indicator. The old

indicator was obsolete. The licensee termed the modification a " material

equivalency", and used the " Request For Resolution" process to approve and install

the replacement temperature indicator. The inspectors reviewed the modification

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package and saw no items of concern except that changes to operations

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department procedures affected by the modification were not made.

From September 17-18,1996, hydrogen recombiner Train B was inoperable for

installation of the new indicator. On September 19,1996, the inspectors found  !

l that procedures for operating and testing the recombiner were not changed. I

Specifically, Procedure OTN-GS-00001," Containment Hydrogen Control System", l

Rev. 5, contained instructions at Step 4.4 for placing the hydrogen recombiner in

service during post LOCA conditions. Step 4.4.9.2 required the operator to check

that temperatures of the hydrogen recombiner were increasing by reading i

temperatures from selected thermocouples. Step 4.4.9.2 also contained a " note"  !

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informing the operator to gently tap the " knurled setpoint ring" on Temperature

Indicator GSTl0029 when changing selected thermocouples to ensure a true

reading. Installation of the new indicator invalidated the note since there was no

knurled setpoint ring on the new indicator. The same note appeared in

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Procedure OSP-GS-00001," Containment Hydrogen Recombiner Functional Test",

Rev. 6., Step 6.2.

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l The licensee explained that procedure notes are for information only and are used to

l provide information that can help the procedure user in performing the procedure.

Although the inspectors agreed, it was evident that the licensee did not review

! proceoures affected by the modification to determine whether any changes were

i needed. The licensee changed the procedures to remove the note. The f ailure to l

update the operations department procedures was a violation of Technical  :

Specification 6.8.1(483/9609-02). -

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Upon further review, the inspectors found that the licensee's use of the " Request

For Resolution" process to implement modifications did not have a feedback loop to j

ensure that procedures, drawings, or other documents affected by the modification

were changed. The licensee agreed and issued a corrective action document to

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evaluate this concern. The inspectors will review of the results of the licensee's

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evaluation when the violation is closed.

The licensee supplied the inspectors with results of a recent audit by quality

assurance personnel. The audit sampled 16 modifications implemented using the

Request For Resolution process. The auditors identified no substantive concerns.

! c. Conclusions i

The licensee's overall configuration control process following plant modifications

was satisfactory. A violation was identified for one example of failing to maintain

proper configuration control.

E2 Engineering Support of Facilities and Equipment

E2.1 Review of Facility Conformance to Updated Final Safety Analysis Report i

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Commitments

A recent discovery of a licensee operating their facility in a manner contrary to the

Final Safety Analysis Report description highlighted the need for a special focused

review that compares plant practices, procedures, and/or parameters to the Final

Safety Analysis Report description. While performing the inspections discussed in

this report, the inspectors reviewed the applicable portions of the Final Safety

Analysis Report that related to the areas inspected. No inconsistencies were noted

between the wording of the Updated Safety Analysis Report and the plant practices,

procedures, and/or parameters observed by the inspectors.

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E8 Miscellaneous Engineering issues

E8.1 (Closed) Licensee Event Reoort 50-483/96002: One train of essential service water

inocerable due to revised accuracy of the butterfiv valve analysis and review test

system

in April 1996, Innovative Technology Incorporated notified the licensee that an error

assumption in calculating the setpoints for certain butterfly valve torque switches

was nonconservative. The license performed a reanalysis with the correct error

assumption for all affected safety related butterfly valves.

Following the reanalysis, the licensee determined that service water to essential

service water Isolation Valve EFHVOO25 could not be proven to close under all

design basis scenarios. The licensee processed a temporary modification to jumper

out the torque switch when the valve closes. The torques switches were used for

testing purposes only. A limit switch controls the actuator during stroking of the

valve.

As a long term corrective action, the licensee planned to jumper out the closing

torque switch contacts for all safety related butterfly valves. This modification

would preclude the valves from failing to close due to errors in torque switch

settings. The modifications are scheduled to be completed during routine

i maintenance on the valve actuators. The inspectors have no further concerns with

! this item and consider it closed.

IV. Plant Support

R1 Radiological Protection and Chemistry (RP&C) Controls

R1.1 Radioloaical Protection Proaram Observations

The inspectors toured various areas of the radiologically controlled areas of the

plant. Health physics personnel were observed routinely touring the radiologically

controlled areas. Pre-job briefs for work in radiological controlled areas were

satisfactory, with open discussions on radiological and personal safety. Licensee

personnel observed performing work in radiological control areas exhibited good

radiation worker practices. Contaminated areas and high radiation areas were

properly posted. Area surveys posted outside rooms in the auxiliary building were

current.

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F5 Fire Protection Staff Training and Qualification

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a. Insoection Scope (71750)

The inspectors reviewed the fire brigade training program and qualification tracking  ;

system. The inspectors also reviewed the program to determine if it was in

! compliance with the Final Safety Analysis Report requirements,

b. Observations and Findinas

The initial fire brigade program training is performed for all operators during initial  ;

licensed operator training and is described in the Final Safety Analysis Report site

addendum Section 9.5. The licensee's fire brigade training program is implemented

by Procedure FPP-ZZ-00009," Fire Protection Training Program," Revision O.

The training subject matter correlated to the requirements of the Final Safety j

Analysis Report. The fire brigade members attend on-going fire protection training.

The fire protection requalification classes were comprised of six modules that were

taught at least once every 2 years. These modules were taught as part of the

licensed operator requalification program. 3

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The fire brigade member qualification status was tracked using the licensee's

computerized training tracking program. This program lists each person's  ;

qualification and medical certification expiration dates. The inspectors reviewed this  !

status list and verified that all operators assigned to the fire brigade were qualified.

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c. Conclusions l

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The inspectors concluded that fire brigade training met the licensee's program 1

l requirements. The inspectors did not note any problems with the fire brigade

member qua!ification tracking program. The training program met the requirements

of the Final Safety Analysis Report.  ;

V. Manaaement Meetinas

X1 Exit Meeting Summary

The exit meeting was conducted on October 11,1996. The licensee expressed a position

on some of the inspection findings documented in this report:

  • During the discussion of the unplanned feedwater heater string isolation

i (Section 04.2), the licensee stated that an off-normal procedure would be developed 1

) to respond to an unplanned automatic isolation of a low pressure feedwater heater

l string.

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  • During the discussion of the installation of the new temperature indicator for the

hydrogen recombiner (Section E1.1), the licensee stated that failure to delete a note

in the hydrogen recombiner procedure did not rise to the level of significance to

warrant a violation.

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I ATTACHMENT

SUPPLEMENTAL INFORMATION '

l PARTIAL LIST OF PERSONS CONTACTED

Licensee

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R. D. Affolter, Manager, Callaway Plant

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J. D. Blosser, Manager, Operations Support

L H. D. Bono, Supervi::ing Engineer, Licensing Fuels and Site Licensing i

F. J. Forck, Quality Assurance, Scientist

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. J. M. Gloe, Superintendent, Maintenance

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G. A. Hughes, Supervising Engineer, independent Safety Engineering Group

K. W. Kuechenmeister, Superintendent, Design Engineering

C. D. Naslund, Manager, Nuclear Engineering 3

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D. W. Neterer, Shift Supervisor

! J. R. Peevy, Manager, Emergency Preparedness and

Organizational Support

l G. L. Raedolph, Vice President, Nuclear Operations

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L The above personnel attended the exit meeting. Ir. addition to these personnel, the

inspectors contacted other personnel during this inspection penod. l

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INSPECTION PROCEDURES USED

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lP 37551: Onsite Engineering

IP 61726: Surveillance Observations

IP 62707: Maintenance Observations

! IP 71707: Plant Operations

l~ IP 71750: Plant Support Activities

l lP 93702: Prompt Onsite Response to Events at Operating Power Reactors

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ITEMS OPENED, CLOSED, AND DISCUSSED

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Opened

9609-02 VIO Failure to change operating procedures following a modification.

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Ooened and Closed

9609-01 NCV Failure to provide guidance opportunities to the circumstances to l

perform evaluations requested by the system engineer. j

Closed i

9508-01 VIO Failure of control room operators to review logs prior to assuming ,

watch, i

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9518-02 VIO Failure to control room oeprators to review logs prior to assuming l

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watch. I

9518-01 IFl Ultimate heat sink Train B sump blocked with ice.

96002 LER Essential service water valve inoperable due to revised accuracy of j

butterfly valve analysis.

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Discussed

None.

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