ML20126A503

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Insp Rept 50-482/92-31 on 921011-1121.Violations Noted. Major Areas Inspected:Plant Status,Prompt Onsite Response to Events,Operational Safety Verification,Maint Observations, Surveillance Observations,Mgt Meeting & Followup
ML20126A503
Person / Time
Site: Wolf Creek Wolf Creek Nuclear Operating Corporation icon.png
Issue date: 12/09/1992
From: Howell A
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20126A488 List:
References
50-482-92-31, NUDOCS 9212210092
Download: ML20126A503 (29)


See also: IR 05000482/1992031

Text

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f- APPENDIX B

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

NRC Inspection Report: 50-482/92-31

Operating License No.: NPF-42

Docket No.: 50-482

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Licensee: Wolf Creek Nuclear OpeMing Corporation

P. O. Box 411

Burlington, Kansas 66839

Facility Name: Wolf Creek Generating Station

Inspection At: Coffey County, Burlington, Kansas

Inspection Conducted: October 11 through November 21, 1992

Inspectors: G. A. Pick, Senior Resident inspector

L. E. Myers, Resident Inspector

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Approved: M d Q. 12.l9f96

A. TQowell, Chief, ProjecQebon IF Date

Division orReR tor Projects

Inspection Summary

Areas Inspected: Routine, unannounced inspection including plant status,

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prompt onsite response to events, operational safety verification, maintenance

observations, surveillance observations, cold weather preparations, management

meeting, and followup.

Results:

o The licensee's overall response to the reactor trip was excellent.

However, during the response to the reactor trip, the inspectors

determined that operators did not use the repeat back technique in their

communications. Also, because operations personnel had not received

training on a change in the operation of the letdown radiation monitor,

they were suprised by the alarm entering the action range (Section 2).

e The licensee's implementation of their program to evaluate indeterminate

conditions was effectively implemented (Sections 3.3 and 3.6).

e The licensee's action to form a task team to identify a refueling water

storage tank low boron concentration condition was considered good.

9212210092

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However, the inspectors identified several weaknesses in that licensee

personnel failed to inform operations personnel about the altered

configuration, failed to review similar situations, and failed to

consider all contributing causes. The licensee failed to-revise an

inadequate alarm response procedure until prompted by the inspectors,

which resulted in a violation. The licensee also had previous

opportunities to correct a deficiency with the refueling water storage

tank drain line. The inspectors considered this to be an additional

example resulting from past problems associated with the corrective

action program (Section 3.2),

e The licensee conducted an excellent medical emergency preparedness drill

(Section 3.7).

e Generally, the licensee conducted maintenance in a thorough, well

controlled manner (Section 4). However, the inspectors identified

potential weaknesses in work controls related to heavy loads in the

spent fuel pool. This issue will be tracked by an unresolved item

(Section 4.3). The inspectors determined that inadequate

postmaintenance testing prevented the licensee from identifying a

misadjusted rotor immediately following maintenance activities, which

resulted in a violation. Also, the maintenance instructions provided

incorrect guidance to the maintenance worker. The instructions were

incorrect because an error occurred while transferring data from one

design document to another. This deficiency resulted in a noncited

violation for inadequate control of design information (Section 3.6).

The failure of craft personnel to identify an obvious component

deficiency is a weakness (Section 4.2).

e The knowledge level and deliberateness of a nonlicensed operator during

operator rounds indicated that nonlicensed personnel were sensitized to

the importance of proper logtaking (Section 5.1).

e The licensee expended considerable effort to protect the plant against

the effects of cold weather. The licensee's sensitivity to the problems

associated with cold weather was demonstrated by their efforts to make

operable an auxiliary steam feedwater pump. The licensee had a very

good program to protect against cold weather (Section 6),

e A violation occurred because of operator inattention to detail, which is

a continuing problem. There was a los:: of charging flow and a decrease

in letdown flow for approximately 20 seconds because a licensed operator

failed to follow a procedure (Section 8).

Summary of Inspection Findings:

e Violation 482/9231-01 was opened (Section 3.2).

e Violation 482/9231-02 was opened (Section 3.6).

  • Unresolved item 482/9231-03 was opened (Section 4.3).

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e Violation 482/9231-04 was opened (Section 8). l

  • Unresolved Item 482/9228-01 was closed (Section 8).

Attachments:

e Attachment 1 Simplified Diagram of the Refueling Water Storage Tank

e Attachment 2 - Persons Contacted and Exit Meeting.

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DETAILS

1 PLANT STATUS (71707)

At the beginning of the inspection period, the plant operated at 100 percent

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power. On November 10, 1992, the turbine tripped because of degraded grid ',

vol tage. Personnel at the Rose Hill substation, west of the plant, accidently l

shorted the secondary side of a 345 to 138 kilovolt transformer while

performing maintenance. Operators took the plant critical on November 11,

1992, and the unit achieved 100 percent power on November 13, 1992. At the

end of the inspection period, the plant was operating at 100 percent power. j

2 PROMPT ONSITE RESPONSE TO EVENTS (93702, 71707) l

2.1 Plant Trip

On November 10, 1992, at 11:05 a.m. the main generator tripped _because of

degraded grid voltage. The main generator trip caused a turbine trip that, by

design, caused the reactor trip. Subsequently, the_ licensee was notified that

troubleshooting activities at the Rose Hill substation created a line fault

that may have tripped the Wolf Creek Generating Station main generator.

Personnel working on a 345 to 138 kilovolt transformer inadvertently shorted

the 138 kilovolt side to ground. The licensee determined that 'a ground . fault

occurred when personnel made incidental contact between an overhead ground and

the energized portion of a 138 kilovolt transformer during implementation of a

clearance procedure. Annunciator 98C, " Response Spectrum OBE (Operating Basis

Earthquake) Exceeded," alarmed during the reactor trip. Following the seismic

alarm, the shift supervisor dispatched personnel to perform a plant walkdown,

including the containment, to look for equipment problems. At 2:10 p.m.,

chemistry reported that dose equivalent iodine (DEI) was measured to be

1.01 microcurie / milliliter (uCi/ml) of primary coolant, which exceeded the

Technical Specification (TS) limiting conditions for operation. -The

supervising operator promptly entered TS 3.4.8,'which required the primary

coolant to be sampled every 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> whenever the DEI exceeds 1.0 uCi/ml. The

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licensee entered Offnormal Procedure 0FN 00-006, Revision 1, "High Reactor

Coolant Activity," and verified the letdown flow rate to be 120-gallons per

minute as specified in the procedure. The licensee exited TS 3.4.8 and

Procedure 0FN 00-006 at 2:35 p.m. when DEI levels were meas ~ red at-

0.966 uCi/ml. The licensee conducted a walkdown of the switchyard, the main

generator exciter, and the main generator. -No problems were identified.

2.2 Posttrip Review and Shutdown Activities

Plant management conducted a meeting to determine: ~(1) the cause of the -

turbine trip, (2) the_ significance of anomalies or equipment failures,

(3) forced outage list work activities that must be completed prior to

starting the reactor, and (4) the approximate duration of the shutdown. The

licensee's forced outage work list identified two mandatory actions, which

involved replacing a failed rod control system power supply and performing a

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TS surveillance. The licensee replaced the rod control power supply restoring

the desired redundancy and completed TS required testing of the manual shunt

trip as committed when they received an emergency TS amendment on August 29,

1992 (refer to NRC Inspection Report 50-482/92-18).

The inspectors attended the posttrip review session conducted on November 10,

1992. Licensee personnel participating in the posttrip review had each

reviewed all the available information related to the plant trip. The plant-

walkdowns revealed no adverse equipment or pipe support conditions. Chemistry

personnel determined that under transient conditions with failed fuel. a spike

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in primary coolan, iodine activity, by a factor of 100, was not unusual-- From

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review of the electrical system design, instrumentation and control (l&C)

personnel determined that the Wolf Creek Generating Station switchyard

distance relaying was not designed to sense the line fault because it occurred

on'the secondary side of the offsite transformer. All safety-related and

nonsafety-re'ated equipment actuated as designed. The posttrip review team

classified the reactor trip as Condition I in accordance with

Procedure ADM 02-400, Revision 9, "Posttrip Reviews," and recommended that the

reactor be started once all mode restraints were satisfied.

2.3 Plant Startup

The inspectors monitored the plant startup that occurred on November 11, 1992.

The shift supervisor briefed the crew, describing the overall sequence of

activities to take the reactor critical and the subsequent power increase.

The precautior.s and limitations of Procedure GEN 00-003, Revision 26, "llot

Standby to Minimum Load," were reviewed. During the approach to criticality

at a position of 45 steps on Control Bank 0, the digital rod position

indicator (DRPI) indicated that Control Rod D-12 had dropped. The reactor

operator immediately stopped the control rod withdrawal. The supervising

operator entered Offnormal Procedure 0FN 00-011, Revision 3, " Dropped or

Misaligned Rod, and Realignment," and TS 3.1.3.1 that specified, for an urgent

failure alarm in the rod control system, restore the inoperable rod to

operable.

The op9rators contacted I&C personnel so that an investigation could be

- conducted. The shift supervisor directed the operators to reinsert the

control rods and reenter Mode 3, HOT STANDBY, until the technicians resolved

the rod control system problems. As the operator began inserting control

rods, Control Rod D-12 indicated 30 steps on the DRPI with Control Rod Bank D

at 39 steps on the demand counter; consequently, operators stopped the control

rod insertion. After the operators consulted with 1&C personnel and

determined no further problems would occur by further rod insertions, the

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operators continued the shutdown. As operators inserted the control rods,

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Control Rod D-12 traveled into the reactor core with the other Control Bank D

rods. When all Control Bank D rods were at 0' steps and Control' Bank C rods

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were at 115 steps, the supervising operator exited TS 3.1.3.1 because he was

confident that all rods were aligned. After all control rods were inserted,

the licensee entered Mode 3 and exited Procedure OFN 00-011.

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The !&C technicians determined the problem was within the DRPI= system. A

review of vendor documents revealed that the probable cause of _the indication

error was a signal cable, a magnetic indicating coll, or: a circuit-card. The

I&C technicians determined that above 30 steps the data encoder card for

Control Rod 0-12 in Data Cabinet B failed to translate the-voltage signal into

a digital signal. Subsequently, the technicians used a card tester verifying _ '

that the data encoder card was defective. After replacing the data encoder

card for Control Rod D-12, the technicians verified that the data encoder card

developed the appropriate digital signal over the entire range of control rod

movement.

After replacement of the DRPI data encoder card, the licensee recalculated a

new estimated critical boron concentration in preparation for a plant startup.

The reactor became critical at 110 steps on Control Bank D and a boron

concentration of 856 parts per mi_llion (ppm). The operators increased reactor

power to 30 percent then maintained a constant power level for 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> until

the secondary chemistry met specifications. The operators had adjusted the 1

power range nuclear instruments periodically during the power increase. On

November 13, 1992, at 99 percent reactor power by the nuclear instruments, the

operators stabilized the power increase and performed a calorimetric, primary

heat balance. By performing the calorimetric, the operators determined the

actual power level was 96 percent. After adjusting the nuclear instruments,

the operators increased power to 100 percent.

2.4 Assessment

The inspectors responded immediately to the control room. The inspectors

observed the licensed operators respond to the trip. Command and control was

excellent and communications among the reactor operators and supervising

operator were generally good; however, the inspectors noted that the operators

did not use the repeat-back technique while responding to the reactor-trip.

The shif t supervisor remained in the _ background, carefully observing the plant

-and the crew and maintaining an overview of the event response. The shift

crew appropriately responded to the event'in accordance with procedures. -The- -

inspectors noted that the call superintendent and other operations perronnel

had arrived in the control room-to provide support to the onduty crew. 'I&C

personnel had been contacted within the first 5 minutes and were examining the

exciter relays.

Management provided good oversight at the status' meeting that-was held

following the reactor trip. Personnel came prepared with: time estimates'for

equipment that required repair. The forced outage list was reviewed and the-

mandatory items, rod control system power supply and the manual reactor trip

shunt trip surveilltnce, were directed to be completed.

Personnel involved in the posttrip review represented a multidisciplined task

group as specified in Procedure ADM 02-400. The discussions regarding the-

sequence of events were thorough. The posttrip review group properly

classified- the trip as a Condition I because the cause was positively known

and all safety systems functioned properly. The licensee promptly reported

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the reactor trip to the NRC operations center and provided updates as new

information about the trip became available. The licensee will submit

Licensee Event Report 92-016 for this event.

The inspectors determined from discussions with 1&C personnel that the seismic

alarm was a momentary spike and was not representative of a seismic event.

The recorded magnitude of the event barely exceeded the alarm threshold and

was much lower than the previous seismic data associated with the noise events

in February and March 1992. The inspectors also reviewed the basis for the

momentary DEI spike. The licensee had a similar occurrence at the start of

Refuel 2 when they nanually scrammed the reactor while shutting down with some

failed fuel elements. The reviews of the anomalies were thorough. The

inspectors determined that the investigation of the DRPI system problems was

well planned and implemented.

The inspectors noted that the operators were surprised that the computer alarm

for the letdown system radiation monitor had saturated and alarmed. The

inspectors interviewed personnel and reviewed Procedure CHM 03-131,

Revision 0, " Failed fuel Monitor SJ RE01 Setpoint Adjustment." The procedure

was issued in September 1992 and provided a method to assure that the letdown

radiation monitor was more sensitive to reactor coolant activity. The

procedure allowed the monitor alarm setpoints to be varied rather than being

set at the previous, relatively high, constant values of 13.6 uCi/ml for the

alert setpoint and 136 uCi/ml for the alarm setpoiht. The procedure required

a 30-day average coolant activity to be determined. The alert setpoint for

the radiation monitor was set at 0.5 uti/ml above the 30-day average value,

and the alarm setpoint was set at 5.0 uCi/ml above the 30-day average. The

inspectors determined that the operators had not received training on the

changes to the alarm setpoint. During the screening prccess of design

changes, the licensee determined that this change was not significant enough

to warrant training. As a result, the operators did not expect the alarm.

The inspectors considered the lack of training because of the setpoint change

to be a weakness.

During the containment walkdown, quality control personnel identified a

1/16-inch d): meter boric acid crystal at spare Canopy Seal Penetration 25;

however, no active leakage was observed. Because there was no active leakage

and a previous vendor evaluation determined that a small amount of leakage was

acceptable, the licensee evaluated the discrepancy and determined that the

plant could be operated in this condition until Refuel VI. The spare canopy

seal weld had similar leakage identified following the previous forced

shutdown in February 1992. At that time, the licensee determined that the

leakage was not pressure boundary leakage because the connection was threaded

and seal welded to prevent backing off.

During the reactor startup, the inspectors noted that the licensed operators

performed the startup activities and required surveillances in accordance with

procedures. Excellent communications existed among the reactor operators and

the supervising operator. The supervising operator ensured his directions

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were understood. The shift supervisor quickly decided to shut down the

reactor and stop the approach to criticality when the DRPI problem occurred.

2.5 Conclusions

Operations personnel demonstrated excellent performance during both the plant

trip recovery and the startup evolutions. Plant management maintained

effective oversight during the forced outage. The inspectors determined that

control room personnel did not use repeat backs during communications;

however, no miscommunications were observed. The lack of operator training

for a setpoint change associated with the letdown system radiation monitor was

considered a weakness. The plant startup activities were conservative. The

licensee conducted thorough investigations into deficiencies identified during

the forced shutdown.

3 OPERATIONAL SAFETY VERIFICATION (71707)

The objectives of this inspection were-to ensure that the facility was being

operated safely and in conformance with license and regulatory requirements

and that the licensee's management control systems were effectively

discharging the licensee's responsibilities for continued safe operation. The

inspectors monitored licensee activities related to: performance enhancement

program (PEP) employee survey results meeting, low boron concentration in the

refueling water storage tank (RWST), boron injection tank outlet isolation

valve - valve actuator maintenance, control room annunciators, fuel

reliability indicator (FRI), RWST suction valve - valve actuator maintenance,

and an emergency preparedness drill.

The methods used to perform this inspection included direct observation of

activities and equipment, control room operations, tours of the facility,

interviews and discussions with licensee personnel, independent verification

of safety-system status and TS limiting conditions for operation, corrective

actions, and review of facility records.

3.1 PEP Employee Survey Results Meetinq

On October 21, 1992, licensee management conducted meetings with all employees

to summarize the results of the PEP employee survey and present management's

response to tha survey. The survey was designed to identify issues and

concerns needing improvement. A third-party consultant and the PEP team

initiated the survey in July 1992.

The survey questionnaire was presented to all employees in August 1992. The

questionnaire included 106 questions designed to explore employee perceptions

about organizational groups and categories af functional areas, such

as: (1) management, (2) personnel policies, (3) communications, and

(4) procedures. Over 94 percent of the employees responded to the

questionnaire. The results were statistically analyzed for perceptions in and

among organizutional groups and in functional areas. Management incorporated

the employees survay results into the development of the PEP action plans.

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The inspectors attended one of the meetings. Licensee management explained

the PEP and communicated that changes would result as action plans were

developed and implemented.

3.2 Low Boron Concentration in RWST

On October 15,1992, at 12:14 p.m. the licensee entered f he action statements

for TS 3.1.2.6 and TS 3.5.5 after the RWST boron concentration was measured at

2151 ppm. TS 3.1.2.6 and TS 3.5.5 require that the boron concentration be

maintained between 2400 and 2500 ppm while in Modes 1, 2, 3, and 4. The

action statements require that with the RWST inoperable, restore the boron

concentration to within specifications in I hour or begin a controlled

shutdown. The licensee initiated preparations for a plant shutdown, initiated

preparations for requesting a Temporary Waiver of Compliance f-om NRC, and

requested chemistry to resample and analyze the boron concentr.. ion. After

chemistry personnel had increased the sample flush volume, they determined the

boron concentration to be 2403 ppm. Sebsequently, the licensee exited the TS

action statements.

The inspectors determined that the RWST high-level alarm annunciated in the

control room at 10:35 a.m. on October 15, 1992. The licensee-nominally

maintains the RWST level at 98 percent with the high-level alarm at

99 percent. The reactor operator responded to the alarm in accordance with

the procedure by requesting chemistry to sample the RWST and initiating steps

to lower the RWST level. The reactor operator dispatched a nonlicensed

operator to open Valve BN V017, RWST drain valve (refer to Attachment 1), to

lower the level and clear the alarm. The nonlicensed operator reported that

upon opening the valve no flow was observed, and the control room observed no

change in level. Concurrently, a chemistry technician sampled fre. the drain

line located upstream of Valve BN V017. The operators initiated letdown of

the RWST through the spent fuel pool cleanup system, an alternate draiu path,

to recover level. The high level alarm cleared at 12:38 p.m. The licensee

determined that there were no activities ongoing that could have caused water

to flow into the tank, thereby resulting in an RWST level increase.

Consequently, the licensee concluded that the high level alarm was spurious

and wcs generated because the true level was being maintained too close to the

setpoint.

Chemistry resampled the RWST at both the tank drain line and the 24-inch

header to the emergency core coeling system pumps. These results were 21s.

and 2443 ppm, respectively. Chemistry, after determining the piping

configuration of the RWST drain line, increased the flush volume at the sample

point from 2.5 to 20 gallons and obtained a sample with a concentration of

2403 ppm at 2:22 p.m. Anothcr samole obtained at 2:35 p.m. indicated that the

boron concentration was 2440 ppm. Chemistry personnel took additional samples

from the normal sample location and from the spent fuel pool clean-up

recirculation sample point. In addition, the results of previous weekly

analysis were reviewed. All results were approximately 2440 ppm which was

within the error of analysis. These data indicated that the RWST baron

concentration had bcen within sne ification the entire time.

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The normal sample point for determ_ining the RWST boron concentration is a

3/4-inch sample line attached to the 6-inch drain pipe. Downstream of the

sample point-is Valve BN V017. Next, the tank overflow pipe joins the drain

pipe between Valve BN V017 and Check Valve LF V034, RWST overflow to drain

system. After Check Valve LF V034, the drain pipe is routed to the waste

holdup tanks in the radwaste building. The licensee suspected that Check

Valve LF V034 was stuck closed so that when the nonlicensed operator opened

Valve BN V017, water in the overflow pipe backflowed into the sample-point

pipe volume.

On October 16, 1992, the licensee organized a task force of individuals from

nuclear safety engineering, systems engineering, operations, anel chemistry to-

investigate the circumstances leading to the event.

As a result of the initial investigation, the task force found:

a No water flowed into the RWST.

  • Since the drain line originated from a 3-foot deep sump inside the RWST,

11 feet from the tank side, the sample flush volume was inadequate. The

task force initiated Reportability Evaluation Request 92-075 to ensure

the issue would be evaluated for reportability and initiated Performance

improvement _ Request CP 92-0704 to ensure all the corrective actions were

completed,

a Water with a boron concentration of 1700 ppm existed 'in the overflow-

line as determined by samnling the top of the full overflow pipe. The-

standing water supported the conclusion that Check Valve LF V034 was

stuck closed. The licensee determined that the borated water in the

overflow pipe was diluted by condensation.

  • No source of water into the tank would cause overflow out the tank vent,

and the tank vent was adequately sized to-handle the inflow.

Consequently, the tank would not overpressurize.-

The task force initiated a work request (WR) to examine the operability of

Check Valve LF V034 and the insulating flange downstream of the check valve.

Also, the task force reviewed _ previous WRs that- indicated Check Valve LF V034

was sticking. In 1985 maintenance personnel determined that the check valve.

operated correctly but that an insulating flange may not have had the correct

configuration and did not permit flow. In 1988 the licensee administratively.

closed the WR without actually examining the downstream piping and the. .

insulating flange. The-inspectors considered ~the_ failure to' comp!ete the

previously scheduled work activity a significant_ weakness that contributed to

this event. The inspectors considered this to he'an additicaal example of-

past corrective action weaknesses (for which enforcemen'. action. has been

taken) that are now being resolved.

i As documented on the performance improvement request, chemistry changed

L Procedure CHM 01-080, Revision 4, " Sampling of the Refueling Water Storage

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Tank," to require a 20-gallon flush when sampling from the RWST drain line

sample point. The licensee determined this flush amount was necessary becaus'e

'the volume preceding the sample point was 8 volumes greater than originally

calculated. In addition, chemistry evaluated sampling flush methods for all

other tanks and found no discrepancies.

The licensee determined the the check valve operated properly and that the

drain line downstream of the check valve was full of water. The insulating

flange probably had a blank in the flange that _ existed since the original-

hydrostatic test of the line. When replacement gaskets for the flanged

connection are received, the pipe will be drained to confirm the blank in the '

insulating flange. ,

The inspectors concluded that the task force formed to investigate this everd

identified appropriate corrective actions. However, the inspectors noted that

the licensee had missed previous opportunities to correct the RWST drain line

configuration deficiencies.

The inspectors determined t'at the task force did not fully consider other

important aspects of the investigation. The need for operator training was

not investigated. The inspectors determined, through interviews, that

licensed operators lacked the knowledge that the RWST had no bladder. The

generic' issues were not explored. An in-depth review of other tanka to assure

that overflow drain lines were in the correct configuration was not conducted.

An information tag was piaced on the chemical and volume control system panel

near the boric acid tank controller used to fill the RWST. Operators

responding in accordance with the_ alarm procedure would be directed'to utilize

the overflow drain valve. However, until the drain lire blockage was

corrected, the RWST drain valve would not function, as designed, since =the

blockage was downstream of the valve. The licensee failed to initiate a

temporary change to the alarm procedure.

After the inspectors pointed out the deficiencies in the investigation, the

licensee reviewea training aspects of the event-and initiated =a review of

generic issues. Also, the licensee initiated and completed a- temporary change

to the_ alarm nrocedure. When the inspectors questioned the licensee

concerning other information tag weaknesses, the licensee stated that they

presently perform quarterly information tag audits. The licensee performs the

audits to verify that the information tag is needed and that-_the information

tag still provides the required information. Additionally, the -licensee

stated they will complete an audit of_ all outstanding information tags to

determine whether similar deficiencies _ exist. Alarm Procedure ALR 00-047E,

Revision 4, "RWST LEV HILO,"' Step 4.4.3 directs personnel to drain the RWST :

upon receipt of a high -level alarm by opening Valve BN V017. As described

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above, the pipe downstream was blocked and the drain path unavailable. The ,

failure to initiate.a temporary change to Procedure ALR 00-047E is' a violation

of TS 6.8.1.a (482/9231-01).

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3.3 Boron injection Tank Outlet Isolation Valve - Valve Actuator Maintenance

On October 28, 1992, while performing maintenance on Motor-0perated

Valve (MOV) EM HV8801B, boron injection tank outlet isolation, in accordance

with WR 50396-92 instructions, electricians identified a potentially

nonqualified torque switch and limit switch gear case. The torque switch was

manufactured from melamine (white) plastic material instead of the fibrite

(brown) plastic material, and the limit switch gear case was aluminum instead

of brass.

The licensee had recently issued Procedure MGE LT-008, Revision 0, " Routine

Electrical Limitorque Operator Maintenance," to provide upgraded instructions-

for routine preventive maintenance of MOVs. Procedure MGE LT-008, Step 4.10

specified that the torque switch should be fibrite and that the limit switch

gear case should be brass for environmentally qualified valves outside of

containment. Consequently, the electricians questioned the adequacy of the

internal components of the actuator.

The licensee entered Procedure KGP-1215, Revision 0, " Evaluation of

Nonconforming Condition of Installed Plant Equipment," that provided guidance

for evaluating indeterminate conditions. The licensee entered the procedure

to determine whether the valve was operable with the existing apparent

deficiencies. MOV EM HV8801B is a limit-closed valve and does not rely upon

the torque switch for motor control. The licensee determined from review of

their Motor Operated Valve Application Guide and Electric Power Research

Institute information that the use of an aluminum limit switch gear casing was

a concern, inside the containment only, because of the chemical reactions

between sodium hydroxide and aluminum. The licensee concluded that the

deficiencies would not have affected the ability of the valve to perform its

required safety functions.

As corrective action to eliminate future confusion, the licensee initiated a

procedure change service request that clarified the required environmental

conditions for aluminum versus brass limit switch gear boxes outside of

containment. The licensee's long-term plans included replacing the aluminum

limit switch gear boxes with brass as each valve is overhauled for the valves

located outside of containment. From review of the work package, the

inspectors determined that no other problems occurred during conduct of the

maintenance. The Valve Operations and Test Evaluation System test was

satisfactorily accomplished. The inspectors determined from discussions with

the licensee that the melamine torque switch was not a concern for this valve

because of shrinkage induced by radiation; however, this valve was susceptible

to roll-pin failures.

Upon receipt of a 10 CFR 21 report dated December 11, 1990, concerning SMB00

torque switch roll pin failures, the licensee initiated several Industry

Technical Information Program (ITIP) Items:

' Item 1513 required that engineering to evaluate the torque switches used

in conjunction with heavy spring packs.

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o Item 1514 required maintenance personnel to develop ~ a replacement

schedule.

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a Item 1515 required operations to develop guidance to minimize j

declutching of the actuator for the affected valves and required

verifying valve operability after declutching- the valve actuator.

The inspectors verified that operations had developed an information tag that

described actions to be taken when declutching the affected valves.

Maintenance personnel had developed a schedule to replace the melamine torque

switches susceptible to roll-pin failures by_the end of Refuel VI. Forty-six

out of 88 safety-related valves had their torque switches. replaced during

Refuel V. Similarly, 4 out of 16 nonsafety-related valves had their torque

switches replaced in Refuel V.

Plant Modification Request 3749 provided a disposition -for torque switches

with the affected roll pins located in the warehouse and in the field. The

affected torque switches located in the warehouse had been returned to the

vendor and refurbished. Some of the affected torque switches located in the

field were to be replaced during Refuel V or sat the first available-

opportunity. The disposition recommended that all remaining affected valves

have the torque switch replaced during Refuel VI.

3.4 Control Room Annunciators

On.0ctober 16, 1992, the Callaway Plant experienced a loss- of control-board

annunciators. On October 17, 1992, while' removing jumpers from field

multiplexor power supplies, the fuses on all four field multiplexors and other

-

logic power supplies failed, The failed power-supplies resulted in a

significant number of the control panel antunciators- being illuminated. The

licensee thought only the illuminated annurciators were inoperable.

Subsequently,. the licensee determined that all annunciators were inoperable.

This condition existed for 56_ minutes until the fuses were replaced.

The _ inspectors questioned licensee personnel about whether the events at

Callaway could occur at Wolf Creek and what actions were being implemented.

The licensee informed the inspectors that thay were awaiting a root cause-to

be identified by the Callaway plant but that-they were. maintaining

communication with their counterparts. The licensee contacted the Callaway

plant and determined that fuses in the power supplies-located in the ~ control

room should be checked weekly. The weekly checks were _necessary to-ensure

that the power supply fuses had not failed since an inoperable power supply

would -prevent annunciators from alarming. Subsequently, the licensee

implemented a. requirement to periodically monitor the fuses in the power

supply panel to verify that the annunciators were operable.

The licensee developed a temporary-modification that provided indicating

lights behind the. control panel-that remained illuminated whenever the power

supplies were energized. The licensee added requirements to the control room

logs for monitoring the power supply status lights once every 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />. While

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implementing the temporary modification, the licensee removed the fuses one at

a time and photographed the main control board annunciators.- The-licensee

used the photographs to identify the annunciators illuminated upon a loss of

each power supply. The licensee highlighted the annunciator drawings- i

'

identifying all annunciators associated with each individual power supply that

would be inoperable upon loss of the power supply. The annunciator _ drawings-

were placed in the' control room to provide guidance to the operators upon a

loss of annunciators.

The inspectors determined that emergency preparedness personnel were

communicating with operations ;ersonnel and had initiated changes to-their

emergency action levels. The licensee's emergency action levels specified

that an alert should be declared upon a loss of all direct current (DC) power.

The inspectors determined that the affected emergency action level previously

specified "most or all annunciators or a loss of DC power;" however, the-

licensee changed the emergency action levels to eliminate the ambiguity of-

that phrase to prevent misinterpretation. At that time, the licensee believed

that their annunciator system could only be lost by a loss of all DC power.

Because of recent industry events, particularly the event at Callaway, the

licensee conducted a more detailed investigation into the annunciator system.

The licensee determined that a loss of a single breaker on-the PK 51 DC bus

could eliminate the ability of all annunciators to function. The oversight

could have resulted in licensed personnel failing to make an appropriate

emergency classification. 1

The licensee informed the inspectors that they had been reviewing their  ;

annunciator design in response to ITIP Item 2069, Significant Event ,

Report 16-92: " Loss of Control Room Annunciators and Plant Monitoring

Computer System," which was assigned to their design engineering group and the

training department. Specific-licensee actions that were in process included

a review of the system design by system engineering and a review of Offnormal-

Procedure 0FN 00-029, " Loss of Nonvital 125 volt DC Bus PK01, PK02, PK03,-and

PK04," by operations personnel for adequacy. The licensee initiated Simulator

Modification Package 92-143 to accomplish the simulator modifications with a

required completion date of April 1, 1994. The inspectors determined from

interviews with the involved licensee personnel that changes were being made

to Procedure 0FN 00-029 to specifically address a loss of annunciation.

Although the licensee had-established a completion date of April-1994 for-

modeling the. simulator for a complete. loss of annunciators, the__ inspectors

determined from discussions with training personnel that the'_ simulator

modeling -should be completed by February 1993 because of the increased

sensitivity following the Callaway event. The Training Department will

discuss this event in Requalification Cycle 92-3 that will begin in

February 1993.

3.5 Failed Fuel Elements

The inspectors monitored the increase in the FRI parameter. Procedure

ADM 01-221, Revision 3, " Failed Fuel Action Plan," defined FRI and defined

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four action levels. The FRI is the steady state reactor coolant system

Iodine 131 activity corrected for the tramp uranium contribution and

normalized to a common purification rate. Tramp uranium is uranium particles

that remain on the outside of fuel elements following the manufacturing

process.

The licensee estimated, from review of chemistry parameters, that

approximately three to four fuel elements had pinhole cladding failures. The

first indication was an increase in the reactor coolant system gaseous

activity obtained from the ratio of Xenon 133 to Xenon 135. The licensee

entered FR1 Action level One on September 18, 1992, because of the increased

primary coolant gaseous activity, Upon entering action _ level one, the

licensee began evaluating data to determine the number and type of fuel

failures. The licensee initiated actions to review fabrication and design

records and initiated plans to perform fuel inspections during the refueling

outage.

3.6 RWST Suction Valve - Valve Actuator Maintenance

' On November 7,1992, as operators placed Residual Heat Removal (RHR) Pump B in

pull to lock while performing Procedure STS BN-201,- Revision 3 " Borated

Refueling Water Storage System Inservice Valve Test," the operators noted that

the engineered safety features status panel light for MOV BN HV88128, RWST to

RHR B suction, illuminated white and no alarm was received when they closed

the valve. The light extinguished upon the opening the valve.

Procedure STS BN-201 provided guidance for stroke time testing of valves that

are located in the flow path from the RWST to safety-related pumps. These

light indications occurred in a different order than expected; consequently,

the operator initiated WR 05598-92 so that technicians would investigate the

annunciator problem. The operators believed that the problem was with the

status panel light circuit; consequently, the operator did not consider that

the valve may be inoperable. The licensed operator demonstrated a good.

awareness of all control panel indications available.

'

On November 9, 1992, at 4:10 p.m., the shift supervisor declared RHR Pump B

inoperable because of the uncertainty of.the operability of MOV BN HV8812B

resulting from Limit Switch Rotor 3 being set 180 degrees from the required

position. The licensee entered TS 3,5.2 that allowed 72 nours to repair the-

valve or begin a controlled plant shutdown. The licensee initiated an

operability review for the valve operability in accordance with

Procedure KGP-1215. The licensee's operability evaluation docume'nted that the

Rotor 3 contacts included a' spare, the engineered safety features status panel

indicating light, the 'RWST 10-10 level test interlock circuitry, and the

interlock permissive for Valve BB PCV8702B, RHR Pump B. suction-from Reactor -

Coolant- System Loop 4 hot leg.

Valve BB PCV8702B is used when RHR Train B is placed in service for cooling

the reactor coolant system after the reactor is shutdown. With Limit Switch

Rotor 3 set incorrectly, Valve ~ BB PCV87028 would not receive a permissive

signal to open, as designed, when_ MOV BN HV8812B was closed. The failure of

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Valve BB PCV87028 to open resulted in the inability of the licensee to use RHR

Train B to remove decay heat whenever the reactor was shutdown. The licensee

determined that no automatic functions for MOV BN HV88128 were disabled;

therefore, the valve remained operable. The licensee had reviewed the

maintenance history for MOV BN HV8812A, RWST to RHR A suction, and the

licensee determined that no adjustments were made to MOV BN HV8812A.

Consequently, a common mode failure did not exist.

The licensee determined that the limit switch rotor position for Rotor 3 was

incorrectly specified as 6 percent FROM FULL OPEN. Further review determined

that upon transfer of data from the licensee's previous MOV Setpoint

Document WCHA-04 to the new MOV design configuration sheets located in

Document E-025-00007, a data transfer error occurred for MOV BN HV88128, Limit

Switch Rotor 3. The WCMA-04, Limit Switch Rotor 3 setting was specified as

6 percent FROM FULL CLOSED. The licensee's review determined the root cause j

was personnel oversight. The licensee identified several contributng causes.

'

The first cause identified was the similarity in appearance of the "0" and the  ;

"C" on the data sheets. Another contributing factor was most transfers were  :

one-to-one; however, 9 of 153 valves did not follow the convention, including

this valve. A total of- 2300 pieces of data were transfered and verified.

Consequently, the licensee also attributed personnel error and inattention to

detail to the independent reviewer. Electricians referred to the E-025-0007

design configuration document for rotor settings as part of maintenance

activities that.specify setting limit-switch rotors. The licensee documented

this discrepancy on Performance Improvement Request NP 92-0741.

The inspectors determined that the inadequate E-025-00007 specification data

sheet resulted in maintenance work instructions that were inappropriate to the

circumstances. The licensee corrected the-af fected valve data specification -

sheet and identified other valve data sheets that were affected. Four of the

data sheets had data transposition errors related to rotor settings.- The

licensee reviewed maintenance activities related to each of the four valves

determining that the only valve worked was MOV BN HV88128. The failure to

have adequate instructions for the adjustment violated 10 CFR 50, Appendix-B,

Criterion III, because the licensee failed to ensure that design requirements'

were properly translated into work instructions. However, the violation will

not be cited because the criteria specified in paragraph VII.B.2 of the NRC

Enforcement Policy were satisfied.-- The licensee identified this deficiency

and evaluated the occurrence for reportability. The licensee promptly

reviewed other potentially affected valves for similar data transportation

errors. - The licensee reviewed their process, determining'that the appropriate

programmatic reviews had been conducted.

The licensee determined that M0V BN HV88128 rotors were reset during-

~

corrective maintenance conducted in September 1992 to repair the soft clutch

mechanism and replace the motor pinion gear in accordance with WR 04681-92

(refer to NRC Inspection Report 50-482/92-28, Section 3.2). While reviewing-

the work-activities accomplished under WR 04681-92 and licensee activities-

related to followup of the abnormal status panel indication, the inspectors

determined that corrective WR 04681-92 had required performance of

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Procedure STS BN-201, as a postmaintenance test. This inadequate

postmaintenance test was different from the issues raised in NRC Inspection-

Report 50-482/92-30 because the previous inadequate postmaintenance test was

related to planned preventive maintenance activities. The licensee's

corrective actiors described at the Enforcement Conference addressed review of

preventive maintenance work instructions. The inspectors reviewed .

Procedure STS BN-201 determining that the test did not require operators to

monitor the status panel indicating lights. Consequently, the operators did

not identify the offnormal status light indication during the postmaintenance

test activities.

The failure to notice the improper light status following the maintenance

activities resulted in Train B shutdown cooling being inoperable for

approximately 55 days, from September 17 through November 9, 1992. Throughout

this period, the plant was in Modes 1 through 3. Consequently, the ability to

remove decay heat was not required to be operable. The licensee's maintenance

program requirements were specified, in part, by Procedure ADM 01-057,

Revision 25, " Work Request," Attachment 8. The attachment provided guidance

'

and expectations for the performance of postmaintenance testing. In

particular, Attachment 8, Step-2.A, specified that postmaintenance testing is

used to verify that the maintenance w:e performed correctly, the equipment

performs its intended function, and that a new deficiency has not been

created. The inspectors-determined that the postmaintenance test instructions

were not appropriate to the circumstances as required by Procedures

ADM 01-057. This is a violation (482/9231-02) because the-postmaintenance

test failed to assure that the limit switch rotors were properly adjusted.

3.7 Emergency Preparedness Drill

On November 20, 1992, the licensee conducted a medical emergency with

contamination emergency preparedness drill. The drill was well designed and

exercised all groups involved. The scenario placed-a' worker in a contaminated

area (in protective clothing) in the auxiliary building who responded to the-

emergency evacuation alarm by clearing the area. The individual panicked and:

exited through a turbine building stairwell (a clean area) and, subsequently,

fell down the stairs which resulted in a simulated serious injury. The

inspectors observed portions of the drill and attended the critique following '

the drill.

'

The critique was well performed and included free and open discussions of the

lessons learned in command and control, communications, health physics

boundary problems in an unexpected circumstance, and medical treatment.

Lessons learned will be incorporated into training and further exercises are

planned to assure resolution of observed problems.

3.8 Conclusions

Licensee PEP activities continued, and the licensee reported the results of-

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the employee survey to the employees.

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The use of a task group to perform a root cause investigation into the

apparent RWST level increase and the inadequate sampling methodology was a -

positive licensee resporise to an event. The root cause and immediate

corrective action determinations were good;- however, the overall result of the-

investigation was diminished because personnel did not consider the generic

implications by reviewing the other tank configurations.for similar

deficiencies and since the operators were not properly notified of the drain

line configuration. The task group did not evaluate other tontributing

causes. The inspectors also concluded that the licensee.had previous-

opportunities to correct a problem with the RWST drain line and considered

this an additional example resulting from corrective action program

weaknesses.

Licensee maintenance personnel identified potential MOV operability issues.

Personnel promptly completed the operability evaluations.

The licensee's review of how the loss of annunciator event at Callaway

affected Wolf Creek Generating Station was good.

The licensee's evaluation of the fuel clad failures was thorough.

A noncited violation was identified because a weakness in design controls

resulted in inadequate maintenance instructions. The inspectors identified a

violation' because the licensee 'had conicted an inadequate postmaintenance

test. The postmaintenance test failed to identify that an error was

introduced during performance of an MOV maintenance activity.

The licensee conducted an excellent medical emergency drill and critique.

4 MAINTENANCE OBSERVATIONS (62703)

The purpose of inspections in this area was to ascertain that maintenance

activities on safety-related systems and components were conducted .in

accordance with approved procedures and TS. Methods used in this inspecticn

included direct observations of maintenance' activities _ and review of records.

4.1 Safetv-Related Batter _v and Battery Charger Maintenance

In response to several failures during the past year associated with the-NK 23-

safety-related battuy charger, the inspectors reviewed the maintenance

history of the battery chargers and the batteries, discussed the history with'

the electrical maintenance engineer responsible for the DC bus components,-and ,

observed battery maintenance activities.

There have been two failures of the NK 23 charger amplifier and firing boards,,

in November 1991 and, again, in June 1992 (refer to NRC Inspection-

Report 50-482/92-08). The failure of the amplifier and firing. boards caused

voltage fluctuations on the DC bus. Historically, there_was one other failure

of amplifier and firing boards, which affected the NK 24 charger, since the

battery chargers were installed.

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The licensee returned the amplifier and firing boards to the vendor for

evaluation of the failure mechanism. The vendor determined both boards

operated satisfactorily after initial troubleshooting and after being-

subjected to a_100-hour operational test. However, the vendor communicated

that the float potentiometer, a varianle resistor in the circuit but not on

the firing board, could have caused the appearance of a failure. The float

potentiometer can change resistance characteristics because of heat

degradation. The licensee discussed this problem with other utilities and

determined that industry experiences were mixed. The licensee incorporated

into their charger maintenance activities inspecting, adjusting, and, if

necessary, replacing the float potentiometer if further altage fluctuations

occur.

Intermittent bettery monitoring alarms on the NK 13 battery monitor has been a

long-standing problem that the licensee has pursued for resolution.- The

battery monitor compares the total battery voltage of 135 volt DC to the

voltage created by each half of the battery cells. The setpoint has a very

low tolerance range of i 0.01 volt DC. Four battery cells located on the same

side of the NK 13 battery were determined to have low voltage but were within

specifications. The low voltage condition of the cells has maintained the

voltage very close to the low voltage setpoint of the battery monitor but

above the TS limits. The vendor suggested that the electrolyte levels could

be adjusted by transferring electrolyte from high to low specific gravity

celle to equalize the voltage on both halves of the battery. The licensee

implemented this procedure four times without success.

To resolve this issue, the licensee decided that charging the cells

individually, or up to four cells in series, could increase the cell voltage.

A procedure was developed, reviewed, and approved by the Plant Safety Review

Committee for the activity. The inspectors observed portions of WR 02164-92.

The WR included the use of Procedure MPE BA-013, Revision 0, " Charging

Individual Battery Cells," and special work instructions. The inspectors

found that the WR provided good instructions for_-the performance of the

i activity, with precautions for proper isolation of the battery charger from

the safety-related battery. The inspectors determined from discussions with-

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licensee personnel that the cell charging was not fully successful.- The craft

personnel were knowledgeable of the task and followed the WR,

Another long-standing problem, since 1985, has been the corrosion of the cell

terminal posts. The individual battery cells utilize a soft seal, an_0-ring,

between flat washers and seal nuts at the battery posts. Electrolyte vapor

has leaked from the seals, which corrodes the terminal post and terminals.

When initially identified, the licensee and vendor could not determine an

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effective solution, consequently, the licensee aggre sively developed a

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program to-inspect the batteries for corrosion. The licensee perforr:s visual

inspections weekly and quarterly. If the visual inspection reveals-corrosion,

the terminal resistance is checked prior to and following cleaning activities.

The battery post and terminal is cleaned and covered with_a protective grease.

During the last refueling outage, the licensee completely disassembled and

cleaned the batteries. There was no indication of corrosion in the seal area

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that could cause the cell cover to crack and break. The licensee determined

the soft post seal design prevented cracking of the battery cover. The vendor

suggested using an epoxy seal in the 0-ring area. However, the licensee ruled '

out that recommendation because a buildup of corrosion could cause battery

cover cracking if a hard seal was present. The licensee is considering

replacement of the batteries before the end of life because of the corrosion

problem. The licensee maintains a historical and trending program to monitor

bo~.h the charger and battery problems. The inspectors, in addition to

co nducting the above evaluation, reviewed and observed portions of the battery

inspections.

The inspectors concluded the licensee addressed the problems with battery

chargers very well and in sufficient depth. The activities associated with

the battery corrosion and the low voltage condition of some battery calls by

the licensee is commendable. Tho history and trending program of the Class IE

DC bus and associated equipment was excellent.

4.2 RHR Train B Maintenance

During the RHR Train B maintenance outage, the inspectors observed the

implementation of:

o WR 52303-92, RHR B Pump Motor Oil Sampling, on November 4, 1992, and

o WR 52306-92, RHR B Room Cooler Maintenance and Inspection, on

November 4, 1992.

During the performance of WRs 52303-92 and 52304 32 by electricians in the

RHR B pump room, the inspectors noticed a flexible connector disconnected

between the fixed conduit and flexible conduit for the bearia oil temperature

that was routed to the top of the RHR pump motor. The maintenance workers did

not notice nor document the dis. nnected conduit. The inspectors informed the

electrician's supervisor of the loose connector after review of the completed

WRs. The electrical supervisor agreed that the workman's porceptions of their

responsibility was narrow since only equipment required u be repaired was

considered. The supervisor agreed th.t the workman should take a broader view

of the utilization of environmental discrepancy sheet while in a work area and

stated that th h expectation would be communicated in shift meetings. The

licensee prompt b initiated a WR to have the connector repaired. The

inspectors con:idered the electricians' failure to identify this discrepancy

to be a weakneu

4.3 Gate Seal Inspection and Replacement in the Spent Fuel Pool

On November 5, 1992, the licensee began inspection activities on the gate seal

for the cask lording pool and the fuel transfer canal gates. In order to

inspect the gates, the gates were lifted off the storage location and moved to

a locatior, where the divcrs could safely examine the seals. While relocating

the fuel transfer canal gate, a quality assurance auditor raised a concern

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that the gate may have been over spent fuel elements. 1he licensee stopped

the work activities after placing the gate in a safe condition. The licensee

initiated a reportability evaluation request to determine reportability and an

investigation to determine the circumstances surrounding this issue. This

issue was significant because it may have been a violation of TS 3.9.7, which

states that loads in excess of 2250 pounds shall be prohibited from travel

over fuel assemblies in the spent fuel pool. The licensee replanned and

successfully completed the work after resolving the method of movement of the

gate so that it would not travel over fuel assemblies. The inspectors

observed the movement of the cask loading pool gate but not the movement of

the fuel transfer canal gate. Radiological controls in place for the diver's

work were exec 11ent. The licensee did not complete the reportability

evaluation nor their investigation before the- report period ended. The

inspectors noted that work planning and control related to this issue may be

inadequate. This item will remain unresolved (482/9231-03) pending further

NRC inspection.

4.4 Safety-injection Accumulator level Indication

4

The inspectors reviewed WRs associated with the Safety injection Accumulator

Tank B level indication. On October 12, 1992, the level indication failed

high, and the licensee initiated WR 05300-92 to troubleshoot EP L10952, Safety

injection Accumulator Tank B level transmitter. The transmitter failed when

moisture penetrated the flexible conduit and entered into the transmitter from -

a Containment Cooler B drain pan water leak. During troubleshooting, the I&C

technicians examined the other accumulator level and pressure transmitter

conduits for similar conditions, with no problems being identified. The-

itcensee initiated WR 05335-92 to install a moisture seal at the flexible

conduit connector to prevent moisture intrusion after replacing the

transmitter. The transmitter wiring connections-are not environmentally

qualified. The licensee is considering installing moisture seals on the other

accumulator flexibic connectors during the next outage. The inspectors

determined that the licensee immediately examined the failure for generic

issues.

4.5 Steam Generator Blowdown Tank Drain Line Weld Repairs

On November 18, 1992, a pinhole steam leak occurred in the 8-inch steam

generator blowdown tank drain line to the heater drain tank. The leak--

occurred on the drain pipe directly opposite of a 3-inch penetration from the

- startup feedwater pump recirculation line. The startup feedwater pump *

recirculation line has an orifice installed upstream of the recirculation

penetration. The itcensee concluded that the impingement of the flow from the

orifice eroded the drain pipe opposite of the orifice. Ultrasonic examination

revealed that the indication was 1/2 inch in diameter with a pinhole _  :

penetrating t he pipe. Since the leak was not._able to be isolated, the

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-licensee encapsulated the line surrounding the pinhole leak. The inspectors

reviewed the WR, observed portions of the work activities, discussed the

results of the ultrasonic examination with the test engineers, and discussed -

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the issue with the engineer responsible for the erosion / corrosion program. ,

The inspectors concluded the licensee had adequately assessed and offcctively i

resolved the leak. l

4.6 Miscellaneous Maintenance Activities

The inspectors observed the following work activities:

a WR 50403-92, Safety Injection Train 8 Discharge Accumulator injection

Valve - Motor Operated Valve EH HV88218, on October 14, 1992, I

o WR 52202-92, Safety injection Pump B 011 Change, on October 14, 1992,

a WR 52395-92, Safety injection Pump B Breaker, Preventive Haintenance

inspection, on October 14, 1992, and

a WR 00243-92, Safety injection Pump B Breaker, Replace Prop Spring, on

October 14, 1992.

The craft personnel performed the maintenance activities in accordance with

detailed work instructions that were appropriate to the work conducted. The

craft were experienced and knowledgeable. The inspectors determined that work

was stopped when an instruction was not clear. Maintenance equipment and test

instr uments were within calibration. Personnel adhered to the radiation work

permit-instructions, where applicable, for protective clothes and other

radiation worker practices.

4.7 Conclusions-

The licenseo maintenance practices relative to the safety-related batteries

was commendable. Craft personnel performing specific maintenance in the RHR B-

room did not identify and document a loose connector; the inspectors 1

considered the failure to identify the component deficiency to be a weakness.

The inspectors identified an unresolved item because licensee work controls

for loads over spent fuel may have resulted in a TS violation. The licensee

effectively repaired a failed level transmitter and a' pinhole leak created by

erosion.

5 SURVEILLANCE OBSERVATIONS (61726)

The purpose of this inspection was to ascertain whether surveillance of

safety-significant systems and components was being conducted in accordance

with TS and approved procedures.

5.1 Operator Daily Loos

In October 1992 the inspectors accompanied a nonlicensed operator on his

rounds in the auxiliary building. The nonlicensed operator utilized

Procedure CKL ZL-001, Revision 16, " Auxiliary Building Log and Daily Reading-

Sheets." The inspectors determined that the nonlicensed operator was:-

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(1) knowledgeable and aware of the plant conditions, (2) cautious and

deliberate during the rounds, took appropriate readings, checked equipment for

levels, touched pump bearings for excessive heat buildup, and observed each

area for leaks or spills, and (3) key carded into each door, as required.

5.2 Shutdown Margin Determination

On November ll, 1992, the inspectors observed reactor engineers perform

Procedure STS RE-004, Revision 11. " Shutdown Margin Determination," as

required during the reactor startup. The inspectors determined that the

reactor engineers performing the surveillance were knowledgeable about the

procedure requirements. The licensee had a software program on a personal

computer that required specific inputs such as the time since the shutdown,

power level prior to shutdown, and the current baron concentration. After

inputing the parameters, the program provided an estimate of the shutdown

margin. The procedure was performed at various intervals while the plant was

in Mode 3, with all data meeting specifications.

5.3 Conclusions

lhe knowledge level and deliberations of a nonlicensed operator during

operator rounds indicated that nonlicensed personnel were sensitized to the

importance of proper logtaking.

6 COLD WEATHER PREPARATION (71714)

The inspectors conducted this inspection to evaluate the effectiveness of

licensee actions to protect plant equipment during extremely cold weather.

6.1 Licensee Preparations

The inspectors verified that Procedure S1N Gp-001, Revision 9, " Plant

Winterization," provided detailed guidance for implementing cold weather

protection. The procedure provided cautions for ensuring area space heaters

and heat tracing for the tanks operated properly. The procedure specified

that upon unavailability of the auxiliary steam system, the outside tanks were

required to be placed on recirculation. Procedure ADM 02-030, Revision 12,

" Reading Sheets and Shif t Rounds Instructions," provided general guidance for

operators conducting rounds to monitor heat trace circuits.

The inspectors independently verified that the plant heating steam system

supplies to various safety-related air supply units were operable. The

inspectors verified that the power supplied to selected heat trace circuits

was properly lined up. The inspectors compared a listing of required

winterization preventive maintenance' activities to completed preventive

maintenance activities to ensure work was being implemented,

The inspectors verified that: the licensee's cold weather checklists were

properly completed; maintenance activities were implemented to assure that

heat tracing, space heaters, and thermostats operated properly; required cold

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weather inspections were completed; alarm response procedures provided

adequate guidance for responding to freeze ')rotection alarms; and fire

protection systems were monitored.  !

6.2 Auxiliary Steam System Activities

The licensee began implementing cold weather protection preparations in

August 1992 when they conducted an auxiliary steam boiler train outage to

ensure the auxiliary steam boiler and the various auxiliary steam system pumps

operated properly. - Detween August 3 and October 24, 1992, the licensee

replaced ) ump shafts for the auxiliary steam feedwater aumps on four occasions

because tie pump shafts had seized during operation. T1e licensee believed a

stress riser occurred because the interior threads in the pump shaft that held

the pump impeller bolt were bored too far into the hole. Following the second

shaft failuro, vendor personnel observed the disassembly and reassembly of the

auxiliary steam feedwater pump, verifying that all critical measurements met

specifications and that the > ump was properly reassembled. The licensee

modified the shaft after a tiird failure. The new pump shaft was threaded.

with the impeller attached by a nut. The auxiliary steam feedwater pump with

the redesigned shaft o)erated for 4 days prior to failing when the pump shaft

seized. The licensee .1ad investigated several potential causes for the shaft

cracking; however, the licensee could not determine the cause of the numerous

recent failures.

Following the initial failure on September 4, 1992, the licensee researched

the possibility of obtaining new parts. The licensee. determined that their

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model of auxiliary steam feedwater pump was not manufactured as a unit but

spare parts could be manufactured. Ilowever, the parts were fabricated as

customized parts with at least a 6-week lead time._ The licensee began

reviewing other pump designs so that they could lower the part procurement

lead time and reduce the expense. The system engineers determined that the

piping would require modification for a different pump and began developing a

plant modification. After the new shaft design failed on October 20, 1992,

the licensee expedited procuring new pumps and prepared Plant Modification

Request 4465, " Auxiliary Steam feedwater Pump Replacement," to modify the pipe

configuration.

The licensee changed the pumps and modified the piping configuration in

accordance with Plant Modification Request 04465. The licensee installed the

Train A auxiliary steam feedwater pump on October 24, 1992, and placed the

auxiliary steam system in service on October 25, 1992. The Train B auxiliary

steam feedwater pump was installed on October 29, 1992. Throughout the period

that the pumps were out of service, the licensee placed the water storage

unks on recirculation to prevent any chance of freezing.

-6.3 Conclusions

The licensee expended considerable effort to protect the )lant against the

effects of cold weather. The licensee's sensitivity to tie problems

associated with cold weather was demonstrated by their efforts to make

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operable an auxiliary steam feedwater pump. The licensee had a very good

program to protect against cold weather.

7 MANAGEMENT MEETING (30702)

On October ll3,1992, a public meeting between NRC-and the Wolf Creek Nuclear

Operating Corporation was conducted in the Region IV NRC office to discuss the

licensee's Management Action Plan and the development and implementation of

the PEP. The meeting provided a brief summary of the number of Management

Action Plan items that will be incorporated into the PEP and the number of

action items that will undergo closure as defined by the Management Action

_

Plan. The meeting provided beneficial uformation about both programs.

The presentation on the PEP program provided a history of the program

development to date and an overview of upcoming program milestones. The

program resulted from third party reviews conducted at the request of the

owner companies. The. consultant aided the PEP team in developing the program

from interviews with plant management and a review of assessments conducted by

NRC and other reviewing organizations. After initial development of the

program action plan areas of emphasis, an employee survey was conducted.- The

PEP action plans should be completely developed by the end of the first

ouarter of 1993.

8 FOLLOWUP (92700)

8.1 (Closed) Unresolved item 482/9228-01: Loss of Charaina and letdown Flows

On October 1,1992, while an operator transferred from Centrifugal Charging

Pump (CCP) A.to the positive displacement pump (PDP), charging flow stopped

and letdos;n flow decreased on two occasions for approximately 20.and

27 seconds, respectively. The initial loss 'of flow occurred when a licensed

operator failed to close the PDP recirculation valve in accordance with the

procedure. The second . loss of flow was postulated to be caused by hydrogen '

gas leaving solution on' the suction side of the ?DP and collecting in the

pulsation damper. At the en' of toe last inspection period, the inspectors

questioned the licensee as to whetter the gas bubble could have gas-bound the

CCPs.

Procedure SYS BG-201, Revision 15. " Shifting Between Positive Displacement and

Centrifugal Charging Pumps," provided instructions in step 4.2.6 to close the

PDP recirculation valve, M0V BG HV8109. While transferring from CCP A to the

'

PDP on October 1, 1992, a licensed operator failed to close MOV BG HV8109 as

i specified, which resulted in decreased letdown flow and a loss of charging

, flow. The failure to follow the procedure is a violation of TS 6.8.1.a

l (482/9231-04). This procedural violation was caused by I1 censed operator

j inattention to detail.

i

During this inspection period, the inspectors reviewed the licensee's '

calculations for head loss in the suction piping from the volume control tank

to the PDP and the CCPs. The licensee's calculations demonstrated that the

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- gas could not leave solution on the suction side of the pumps. Since the gas

could not leave solution,'there was no possibility of binding the CCPs. At  :

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the end of the inspection period, the licensee stated they would provide an

engineering evaluation by December 14, 1992, that described the most probable-

cause of the second PDP loss of flow. The licensee believed that the hydrogen l'

might have been formed in the PDP pump cylinders, since the licensee had

previously experienced cylinder spring failures created by hydrogen

embrittlement.

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ATTACHMENT 2

1 PERSONS CONTACTED

P. D. Adam, Supervisor, Reactor Engineering

R. S. Benedict, Manager, Quality Control

A. B. Clason, Supervisor, Maintenance Engineering

R. D. Flannigan, Manager, Nuclear Safety Engineering

D. E. Gerroits, Manager, Instrumentation and Control ,

N. W. Gioadley, Manager, Equipment Engineering

R. W. Holloway, Manager, Maintenance and Modifications

L. W. Holloway, Supervisor, System Engineering

D. Jacobs, Supervisor, Mechanical Maintenance

R. K. Lewis, Supervisor, Results Engineering

W. M. Lindsay, Manager, Quality Assurance

R. L. Logsdon, Manager, Chemistry

J. D. Lutz, Regulatory Compliance Engineer

0. L. Haynard, Vice President, Plant Operations

K. J. Moles, Manager, Regulatory Services

T. S. Morrill, Manager, Radiation Protection

D. G. Moseby, Supervisor, Operations

F. T. Rhodes, Vice President, Engineering

T. L. Riley, Supervisor, Regulatory Compliance

D. B. Smith, Marager, Modifications

C. M. Sprout, Manager, System Engineering

J. D. Stamm, Manager, Plant Design Engineering

H. L. Stubby, Supervisor, Technical Training

5. G. Wideman, Supervisor Licensing

M. G. Williams, Manager, Plant Support

B. D. Withers, President and Chief Executive Officer

The above licensee personnel attended the exit meeting, in addition to the

personnel listed above, the inspectors contacted other personnel during this

inspection period.

2 EXIT MEETING

An exit meeting was conducted on November 25, 1992. During this meeting, the

inspectors reviewed the scope and findings of the report. The licensee did

not identify as proprietary any information provided to, or reviewed by, the

inspectors.

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ATTACHMENT 3

LIST OF ACRONYMS

CCP centrifugal charging pump

DC direct current

DEI dose equivalent iodine

DRPI digital rod position indication

FRI fuel reliability indicator

I&C instrumentation and controls

ITIP Industry Technical Information Program

MOV motor operated valve

PDP positive displacement pump

PEP Performance Enhancement Program

ppm parts per million -

RHR residual heat removal

RWST refueling water storage tank

IS Technical Specifications

uti/ml microcurie per milliliter

WR work request

_