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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20148T6101997-07-0303 July 1997 Follow-up to Special Rept SR-96-003-01:on 970411,damage to Cables for Sensors 1A & 1B Discovered.Sensor Cable for 7B Also Found Damaged.Cables for Channels 1A,1B & 7B Found Saturated W/Oil.Sensors Replaced for Channels 1A,1B & 7B ML20148N7281997-06-26026 June 1997 Special Rept SR-97-002-00:on 970513,personnel Identified Design Discrepancy for 'B' CCW Train Radiation Monitor. Design Flaw Existed Since Plant Built.Design Change DC-3537 Approved to Reroute Cooling Water Line from Connection ML20135E9641996-12-10010 December 1996 Special Rept SR-96-003-00:on 961027,valve & Loose Parts Monitoring Sys Declared Inoperable.Caused by Failure of Sensor on Channel 1.Sensor Will Be Replaced During Refueling Outage 8 ML20113E4501996-07-0303 July 1996 Special Rept SR-96-001-00:on 960603,output Breaker for EDG B Failed to Close.Caused by Intermittent Malfunction of Contacts on Synchronizing Switch.Performed Troubleshooting & Replaced EDG B Synchronizing Switch ML20094P5911995-11-27027 November 1995 Special Rept SR-95-004-00:on 951030,EDG Tripped on Turbocharger Low Lube Oil Pressure.Generated Condition Rept 95-1102 ML20094G2031995-11-0808 November 1995 Special Rept SR-95-003-00:on 951010,EDG Experienced Crankcase Overpressurization.Caused by Poor Lubricating Conditions During Startup & Rapid Loading Led to Tin Transfer from Piston to Cylinder Liner ML20093L8421995-10-23023 October 1995 Special Rept SR-95-002-00 on 951011,ABB C-E Identified Leaking Plug Due to build-up of Boric Acided Crystals Around OD of Plug.Leaking Plug Removed by Tig Relaxation & Replaced/Another Rolled Mechanical Plug ML20086E0181995-07-0707 July 1995 Special Rept SR-94-001-01:on 940228 & 0302,EDG a Experienced Nonvalid Failures Due to Worn Mechanical Governor Parts. Mechanical Governor & Faulty Relay Replaced & Procedure OP-009-02, EDG Revised ML20070N6601994-05-0404 May 1994 Special Rept SR-94-003:on 940404,EDG a Experienced Nonvalid Failure While Performing Valid Test.Probably Caused by Emergency Mode Master Run Relay 4EX1 de-energized During Run.Troubleshooting in Progress ML20065A3761994-03-29029 March 1994 Special Rept SR-94-001,on 940228,EDG a Tripped on Overspeed. Caused by Faulty Contacts in Relay of Electronic Grovernor Droop.Faulty Relay & Mechanical Governor Replaced ML20059B9521993-10-26026 October 1993 Special Rept SR-93-001-01,final Rept:On 930811,declared Condenser Vacuum Pump Wide Range Gas Monitor PRM-IRE-002 Inoperable.Monitor Returned to Svc on 930901.Inoperability of Subj Monitor Did Not Pose Safety Concern ML20056H1011993-09-0101 September 1993 Special Rept SR-93-001-00:on 930811,condenser Vacuum Pump WRGM PRM-IRE-002 Declared Inoperable & Not Returned to Svc within Seven Days.Monitor Will Be Returned to Svc After Low Range Sample Flow Cv Repaired & Functionally Checked ML20126M5881993-01-0606 January 1993 Special Rept SR-92-003:on 921207,EDG a Failed to Reach Rated Speed & Voltage in Less than or Equal to 10 S.Caused by Failure to Properly Secure Turning Gear Brackets.Control Brackets for Turning Gear Interlock Valves Adjusted ML20127M4981992-11-24024 November 1992 Special Rept SR-92-002-00:on 921023,component Cooling Water (CCW) A/B Radiation Monitor Was Inoperable for More than 30 Days.Ts Change Request NPF-38-127,dtd 921021 Submitted,Which Changes Operability Requirement ML20116B2121992-10-23023 October 1992 Special Rept SR-92-001-00:on 921010,inservice Eddy Current Exam of SG Tubing Completed,Per 10CFR50.36(c)(2).Total Number of Tubes Have Been Plugged in SG Shown as Listed ML20086K8731991-12-11011 December 1991 Special Rept SR-91-007-00:on 911111,diesel Generator a Loaded to 4.3 MW & Tripped.Caused by Inadequate Positioning of Turbocharger Inlet Air Butterfly Valve Limit Switch Mounting Bracket.Limit Switch Repositioned ML20086G0201991-11-27027 November 1991 Special Rept SR-91-002-02:on 910318,emergency Diesel Generator a Experienced Crankcase Overpressurization.Caused by Stuck Piston Rings.Piston & Piston Liner Replaced & Improper Temp Differential Will Be Corrected ML20083D4431991-09-23023 September 1991 Special Rept SR-91-002-01:on 910318,emergency Diesel Generator a Experienced Crankcase Overpressurization.Caused by Stuck Piston Rings & Improper Temp Differential.Cylinder Liner,Piston Assemblies & Rod Bearings Replaced ML20082U6231991-09-16016 September 1991 Special Rept SR-91-003-01:on 910406,inservice Eddy Current Exam of Facility SG Tubing Completed by Westinghouse.Rept Submitted Per Tech Specs 4.4.4.5 & 6.9.2.Rotating Pancake Coil Exam Results Verified No Detectable Degradation ML20082T2121991-09-13013 September 1991 Special Rept:On 910820,EDG Secured During Surveillance Test Due to Power Dropping Resistor Failure.Power Dropping Resistor Assembly Replaced.Health & Safety of Public & Plant Personnel Not Affected by This Event ML20082C4021991-07-15015 July 1991 Special Rept 91-005-00:on 910619,EDG a Tripped on Turbocharger Lube Oil Low Pressure During Performance of Operating Procedure 903-068.Procedure Changed to Require Lubrication of Turbocharger ML20073Q8001991-05-29029 May 1991 Special Rept SR-91-04-00:on 910429,EDG a Failed Invalidly Due to Spurious Turbocharger Lube Oil Pressure Trip.Edg Restarted.Oil Pressure Remained within Normal Operating Limits & OP-903-068 Completed ML20073B3231991-04-19019 April 1991 Special Rept SR-91-003-00,re 910406 Completion of Inservice Eddy Current Exam of Steam Generator tubing.Follow-up Rept Will Be Submitted by 920406,per Tech Spec 4.4.4.5.b.Total Number of Tubes Plugged in Each Steam Generator Listed ML20084U8591991-04-17017 April 1991 Special Rept SR-91-002-00:on 910318,emergency Diesel Generator a Experienced Crankcase Overpressurization. Possibly Caused by Improper Temp Differential Between Jacket Cooling Water & Lube Oil Temp.Liner Replaced ML20072Q8931991-03-18018 March 1991 Special Rept SR-91-001-00:on 910207,channel 2 of SPDS Failed & Could Not Be Restored within 7 Days.On 910214, Channel 2 of Qualified SPDS Sensor 8 Out of Svc for More than 7 Days.Channel 2 Probe Will Be Replaced ML20065R6021990-12-12012 December 1990 Special Rept SR-90-003-00:on 901112,invalid Failure of Emergency Diesel Generator a Occurred.Caused by Mechanical Failure of 30 Psig Reducer in Control Air Sys & Crack on Spring Cap of Reducer.All Reducers Inspected ML20246C9091989-05-0303 May 1989 Special Rept SR-89-001-01:on 890206 & 0403,emergency Diesel Generator a Declared Inoperable.Caused by Fuse Not Being Secured in Fuse Holder & Oxidation of Speed Control Circuit Relay Contacts.Contacts Cleaned & Fuses & Holders Checked ML20245A3951989-04-10010 April 1989 Special Rept SR-88-004-01:on 880420,inservice Eddy Current Exam of Steam Generator Tubing Completed by Westinghouse.Two Tubes Exceeded Plugging Limit in Steam Generator A.All Discrepancies Resolved ML20236B0941989-03-0808 March 1989 Special Rept:On 890206,emergency Diesel Generator Secured Due to Failure of Speed Control Circuit While Generator in Manual Operation.Caused by Oxidation of Relay Contacts in Governor Control Circuitry.Contacts Replaced ML20206H4901988-11-18018 November 1988 Special Rept SR-88-009-00:on 880909,emergency Diesel Generator Tripped Due to Incorrect Valve Lineup.Caused by Personnel Error.Valves Opened ML20151U8841988-08-16016 August 1988 Special Rept SR-88-008-00:on 880726,plant Stack Effluent Accident wide-range Gas Monitor Declared Inoperable.Caused by Pump Failing Step 8.4.2.18 Which Checks high-range Sample Flow within Specified Tolerance.Transmitter Replaced ML20151C1121988-07-15015 July 1988 Special Rept SR-88-007-00:on 880628,primary Meteorological Tower Instruments out-of-svc Greater than Seven Days.Caused by Instruments Being Out of Calibr.Temp Elements Replaced & Corrective Maint on Delta Temp Instruments Completed ML20151C0781988-07-15015 July 1988 Special Rept SR-88-006-00:on 880616,emergency Diesel Generator B Tripped Due to Personnel Error.Caused by Failure to Raise Load within 5 S.Operating Procedure OP-9-002 Reviewed & Considered to Adequately Address Operation ML20195H7171988-06-20020 June 1988 Special Rept SR-88-005-00:on 880511,unit Was in Refueling Mode When Operations Personnel Declared Seismic Monitor SM-IYR-6021 Inoperable.Plastic Lexan Mounting Board Appeared to Be Deformed Due to Heat.Monitor Will Be Relocated ML20153F3831988-05-0404 May 1988 Special Rept SR-88-003-01:on 850801-880404 Several Failures of Emergency Diesel Generators to Start Occurred.Caused by Actuation of Trips Which Bypassed in Emergency Mode.Trip Sensor Replaced ML20153F2541988-05-0404 May 1988 Special Rept SR-88-004-00:on 880420,inservice Eddy Current Exam of Steam Generator Tubing Completed.Rept Submitted in Accordance W/Tech Specs 4.4.4.5.a.Number of Tubes Plugged in Each Steam Generator Listed ML20148F1021988-03-21021 March 1988 Special Rept SR-85-002-01:on 851230,discovered Emergency Diesel Generator a Failed to Complete Surveillance Run as Defined in Procedure OP-903-068 & Tech Spec 4.8.1.1.2a.5. Cause Not Determined.Minor Adjustments Made to Governor ML20148F0971988-03-18018 March 1988 Special Rept SR-88-003-00:from 850801-880308,several Emergency Diesel Generators Failed to Start.Caused by Malfunctioning Trip Mechanisms.Diesels Will Not Be Taken Out of Svc Until Plant Scheduled to Be out-of-svc for Maint ML20149J3411988-02-18018 February 1988 Special Rept SR-88-001-00:on 880128,during Plant Startup Operations,Personnel Declared Fuel Handling Exhaust Wide Range Gas Monitor out-of-svc for Calibr.Caused by Extensive Teardown.Procedure Revised ML20236Q1121987-11-16016 November 1987 Special Rept SR-87-006-00:on 871028,primary Meteorological Tower Upper Wind Speed & Wind Direction Instrument out-of- Svc in Excess of 7 Days.Caused by Failed Signal Converter. Parts Replaced & Instrument Returned to Svc on 871104 ML20236Q2621987-11-13013 November 1987 Special Rept SR-87-005-00:on 871103,Tech Specs 3.3.3.1 & 6.9.2 Violated.Caused by Inoperability of Effluent Accident wide-range Gas Monitor for More than 7 Days Due to Damaged Connectors.New Monitor Should Be Installed by 871125 ML20235J8531987-09-24024 September 1987 Special Rept SR-87-004-00 Re Results of Inservice Eddy Current Exam of Steam Generator Tubing Completed on 861214. No Indication of Degradation Greater than or Equal to 20% Through Wall Detected in Steam Generator a ML20237G9341987-08-21021 August 1987 Special Rept SR-87-003-00:on 870731 & 0809,condenser Vacuum Vacuum Pump Discharge Wide Range Gas Monitor (WRGM) Inoperable.Caused by Water Blockage of Sample Lines.Wrgm Restarted & Being Tested for Operation ML20234B2111987-06-29029 June 1987 Special Rept SR-87-002-00:on 870606,high Range Gas Monitor Inoperable Greater than 7 Days.Caused by Faulty Display Module & Lack of Spares & Quality Documentation.Module Replaced & Monitor Returned to Svc After Functional Test ML20215H0841987-06-17017 June 1987 Special Rept SR-87-001-00:on 870527,during Full Reactor Power,Condenser Vacuum Pump Discharge Wide Range Gas Monitor Declared Inoperable.Caused by Failed Input/Output Circuit Board & Low Range Detector.Faulty Components Replaced ML20205G1731987-03-18018 March 1987 Ro:On 870222,steam Line Break on Scavenging Steam Vent Line from Moisture Separator Reheater Experienced.Caused by Classic Fatigue Failure in Heat Affected Zone of Weld Joining Alloy 800 Matl.Temporary Restraints Added W3P87-0237, Suppl 1 to Special Rept SR-85-001:on 850916,seismic Monitor Mounted on Pressurizer Found Damaged & Inoperable.Relocation of Seismic Monitor Completed,But Tech Spec Not Yet Approved1987-01-19019 January 1987 Suppl 1 to Special Rept SR-85-001:on 850916,seismic Monitor Mounted on Pressurizer Found Damaged & Inoperable.Relocation of Seismic Monitor Completed,But Tech Spec Not Yet Approved ML20214V2821986-09-26026 September 1986 Special Rept SR-86-005-00:on 860909 & 17,secondary & Primary Towers Removed from Svc,Respectively,But Not Returned to Svc within 7 Days.Caused by Need to Replace Hoist Cables. Secondary Tower Returned to Svc on 860916 ML20206J6331986-06-20020 June 1986 Special Rept SR-86-004-00:on 860523,emergency Diesel Generator a Malfunctioned.Caused by Failure of Power Parallel Voltage Dropping Resistor in Electrical Governor Control Circuit.Power Resistors & Amplifier Replaced ML20211H3531986-06-13013 June 1986 Special Rept SR-86-003-00:on 860523,wide-range Gas Monitor PRM-JR-0110 Declared Inoperable.Caused by Performance of Functional Test Per Procedure MI-3-382.Check Valve Removed & Seat Reworked.Monitor Returned to Svc on 860604 1997-07-03
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217F2891999-10-13013 October 1999 Drill 99-08 Emergency Preparedness Exercise on 991013 ML20217G7211999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Waterford 3 Ses. with ML20211Q2141999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Waterord 3 Ses.With ML20210Q6361999-07-31031 July 1999 Corrected Monthly Operating Rept for July 1999 for Waterford 3 ML20210S0581999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Waterford 3.With ML20210D8951999-07-23023 July 1999 Safety Evaluation Accepting First 10-yr Interval Inservice Insp Plan Requests for Relief ISI-018 - ISI-020 ML20209H3781999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Waterford 3 Ses. with ML20195J8951999-06-17017 June 1999 Safety Evaluation Granting Relief for Listed ISI Parts for Current Interval,Per 10CFR50.55a(g)(5)(iii) ML20207E8631999-06-0303 June 1999 Safety Evaluation Accepting Licensee 990114 Submittal of one-time Request for Relief from ASME B&PV Code IST Requirements for Pressure Safety Valves at Plant,Unit 3 ML20195K3391999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Waterford 3 Ses.With ML20195C3041999-05-28028 May 1999 Annual Rept on Abb CE ECCS Performance Evaluation Models ML20206S7401999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Waterford 3.With ML20205T2621999-04-22022 April 1999 LER 99-S02-00:on 990216,contract Employee Inappropriately Granted Unescorted Access to Plant Protected Area.Caused by Personnel Error.Security Personnel Performed Review of Work & Work Area That Individual Was Involved with ML20205N9671999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Waterford 3 Ses.With ML20205E8531999-03-30030 March 1999 Corrected Pages COLR 3/4 1-4 & COLR 3/4 2-6 to Rev 1, Cycle 10, Colr ML20205A6331999-03-25025 March 1999 SER Accepting Request to Use Mechanical Nozzle Seal Assemblies as an Alternative Repair Method,Per 10CFR50.55a(a)(3)(i) for Reactor Coolant Sys Applications at Plant,Unit 3 ML20204H1401999-03-23023 March 1999 Rev 1 to Engineering Rept C-NOME-ER-0120, Design Evaluation of Various Applications at Waterford Unit 3 ML20204H1231999-03-22022 March 1999 Rev 1 to Design Rept C-PENG-DR-006, Addendum to Cenc Rept 1444 Analytical Rept for Waterford Unit 3 Piping ML20204H2451999-03-22022 March 1999 Rev 2 to C-NOME-SP-0067, Design Specification for Mechanical Nozzle Seal Assembly (Mnsa) Waterford Unit 3 ML20204F0791999-03-17017 March 1999 Rev 1 to Waterford 3 COLR for Cycle 10 ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207F3491999-03-0505 March 1999 LER 99-S01-00:on 990203,contraband Was Discovered in Plant Protected Area.Bottle Was Determined to Have Been There Since Original Plant Construction.Bottle Was Removed & Security Personnel Performed Search of Area.With ML20204B5141999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Waterford 3.With ML20203H8591999-02-17017 February 1999 Safety Evaluation Accepting Licensee Second Ten Year ISI Program & Associated Relief Requests for Plant,Unit 3 ML20199H6261999-01-21021 January 1999 Safety Evaluation Accepting Classification of Instrument Air Tubing & Components for Safety Related Valve Top Works.Staff Recommends That EOI Revise Licensing Basis to Permit Incorporation of Change ML20199C9101998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Waterford 3.With ML20196F4911998-12-0101 December 1998 SER Accepting Request for Relief ISI2-09 for Waterford Steam Electric Station,Unit 3 & Arkansas Nuclear One,Unit 2 ML20206N4131998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Waterford 3.With ML20195C4841998-11-0606 November 1998 SER Accepting QA Program Change to Consolidate Four Existing QA Programs for Arkansas Nuclear One,Grand Gulf Nuclear Station,River Bend Station & Waterford 3 Steam Electric Station Into Single QA Program ML20195E5161998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Waterford 3.With ML20155C1351998-10-26026 October 1998 Rev B to Entergy QA Program Manual ML20154K0801998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Waterford 3 Ses. with ML20151W8331998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Waterford,Unit 3. with ML20237B6831998-08-17017 August 1998 LER 98-S01-00:on 980723,discovered That Waterford 3 Physical Security Plan,Safeguards Document Was Not Under Positive Control of Authorized Person at All Times.Caused by Human Error/Inappropriate Action.Counseled Employee Involved ML20237C5661998-08-17017 August 1998 Safety Evaluation Accepting Licensee Request for Exemption from Section Iii.O of Appendix R to 10CFR50 ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML20237B5261998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Waterford 3 ML20236S9031998-07-22022 July 1998 SER Accepting Rev 19 to Quality Assurance Program for Waterford Steam Electric Station,Unit 3 ML20198H3911998-07-14014 July 1998 Non-proprietary Rev 5 to HI-961586, Thermal-Hydraulic Analysis of Waterford-3 Spent Fuel Pool ML20236N4181998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Waterford,Unit 3 ML20248E7781998-06-0101 June 1998 Annual Rept on Abb CE ECCS Performance Evaluation Models ML20249A4711998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Waterford 3 Ses ML20196A4051998-05-31031 May 1998 Rept of Facility Changes,Tests & Experiments,Per 10CFR50.59 for 970601-980531. with ML20198H4681998-05-20020 May 1998 Non-proprietary Rev 1 to HI-981942, Independent Review of Waterford Unit 3 Spent Fuel Pool Cfd Model ML20247A3891998-05-0101 May 1998 SG Eddy Current Examination (8th Refueling Outage) ML20247F6761998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Waterford,Unit 3.W/ ML20217M8951998-04-30030 April 1998 QA Program Manual ML20217P8281998-04-0707 April 1998 Safety Evaluation Accepting Relief Authorization for Alternative to Requirements of ASME Section Xi,Subarticle IWA-5250 Bolting Exam for Plants,Per 10CFR50.55a(a)(3)(i) ML20216B1751998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Waterford 3 Ses ML20217M1411998-03-0303 March 1998 Rev 2 of Waterford 3 Cycle 9 Colr 1999-09-30
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- April- 17,1991-1U.S. Nuclear Regulatory Commission ATTENTION: Document Control Desk-
-h Washir,gton, D.C. 20555-Waterford 3 SES
SUBJECT:
Docket No. 50-382 License No. NPF-38 Reporting of Special Report i
Gent'lemen:
Attached isiSpecial Report Number SR-91-002-00 for-Waterford Steam Electric Station-Unit 3. This Special Report is submitted per 10CFR50.36(c)(2) :and i Yechnicalf Specifications 4.8.1.1.3 and 6.9.2.
Very trulyfyours, pe- j - a J.R. McGaha .
. General-Manager Plant-Operations
- JRM/DDW:jrr -
' Attachment
- cc: Messrs. R.0, Martin G.L. Florreich J.T. Wheelock - INP0 Records Center
'E.L. Blake )
0.L. Wigginton-
-N.S. Reynolds NRC Resident Inspectors Office
- r. 9104230110 91o417 ggM DR :ADOCK 050003a2 POR
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7 Special Report 91 002 00 Valid failure of Emergency Diesel Generator ' A' due to overpressurization of the crankcase.
INTRODUCTION On March 18, 1991, Waterford Steam Electric Station Unit 3 was in cold shutdown when Emergency Diesel Generator (EDG) 'A' experienced a crankcase overpressurization. The EDG was being run in accordance with the prerequisites of the 18 month Emergency Diesel Engine Inspection procedure, HM 003 015, when the overpressurization occurred. The operator observing the EDG run, depressed the emergency stop button and pulled the overspeed trip.
This event has been classified as a valid diesel failure and is being reported in accordance with Technical Specification 4.8.1.1.3, The root cause of this event is still under investigation. A possible root cause, based on vendor bulletin information, is an improper temperature differential between jacket cooling water and lube oil temperatures, A related possible contributing cause is an omission of relevant information in that the vendor did not provide a service news bulletin which specifically identified the possible adverse consequences of the previously-mentioned temperature diff erential. The piston and piston liner have been replaced and the improper temperature differential will be corrected. A revision to this special report will be submitted if a more positive root cause determination is made,
s
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NARRATIVE i
At 0457 hours0.00529 days <br />0.127 hours <br />7.556217e-4 weeks <br />1.738885e-4 months <br /> on March 18, 1991, Waterford Steam Electric Station Unit 3 was in cold shutdown when Emergency Diesel Generator (EDG) (EIIS Identifier EK ENG) 'A' experienced a crankcase (EIIS Identifier BLK) overpressurization.
Personnel operating the EDG depressed the emergency stop push button and pulled the overspeed trip after the overpressure condition occurred. This event has been classified as a valid diesel failure and is reported in accordance with Technical Specification 4.8.1.1.3.
EDG 'A' was started at 0221 to commence the prerequisite 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> continuous run of the 18 Month Emergency Diesel Engine Inspection procedure, MM 003-015, The purpose of the run was a pre maintenance heatup and engine analysis prior to placing the unit out of service for the EDG ' A' refueling outage inspection. EDG 'A' was loaded to 4400 kilowatts when the crankcase overpressurization occurred, All 10 cylinder _ relief assemblies lifted, filling the room with oil vapor. The room was exited and there were no personnel injuries.- After the vapor cleared, the room was entered and a crankcase oil sample was drawn, This oil sample was found to be within specifications. An on site fuel dilution test also yielded satisfactory
'results.
An inspection of the EDG cylinders, pistons, rods (EIIS Identifier ROD),
and bearings was commenced as required by MM 003-015. The inspection revealed that the 5 left (SL) cylinder liner (EIIS Identifier LNR) exhibited intermittent 1 1/2 by 3 inch longitudinal rough spots or scuff marks perpendicular to the piston pin. Vertical scratch marks were noted throughout
- the length of the cylinder. Additionally, the metal-on the underside of the p
I piston had been discolored by heat. A borescope inspection of the other pistons indicated satisfactory results. Disassembly and inspection of four-H l
l 2
j other pistons,-SR, IL, 1R and 8L, revealed normal wear.
Of parcicular interest was a missing piece of chrome from the SL piston cylinder liner. The missing chrome flake is approximately 1/4 inch.in diameter. The SL cylinder liner was analyzed at the vendor's metallurgical lab to determine the cause and consequence of the missing chrome. The chrome flaking was determined to be a result of pre crankcase overpressurization scuffing rather than a cause of the crankcase overpressurization.
Cooper Bessemer Service News Bulletin number 688, dated June 26, 1985, addressed the possibility of " cylinder scuffing, piston seizure and... crankcase explosion" if jacket cooling water temperature was not maintained 5 degrees Fahrenheit higher than piston lube oil temperature.
Waterford 3 had not received this bulletin from the vendor, but a consultant who was familiar with bulletin 688 noted that Waterford 3 EDG logs showed that jacket cooling water temperature was being maintained 4 degrees lower than piston lube. oil temperature. Maintaining the recommended temperature differential would reportedly prevent a crankcase explosion caused by frictional heat resulting from scuffing of the cylinder in the piston skirt crea. The piston is cast steel with a thin outer coating of tin. The piston cy'inder wall is coated with chrome. Although the reasons are not known, there is empirical industry evidence that indicates that an improper temperature differential causes the cast steel in the piston skirt area to become exposed. This cast steel surface then scuffs the chrome cylinder wall, eventually generating enough frictional heat to cause a crankcase explosion.
The fact that this temperature differential condition had existed at Waterford 3 on both EDGs for several years with no deleterious effects and the , fact that none of the other EDG 'A' cylinders had scuff marks casts doubt that the improper temperatore differential is the root cause. Consequently, this l
3
temperature differential is being evaluated as only a possible root cause. A related possible contributing cause is an omission of relevant information in that Cooper-Bessemer Service News Bulletin Number 688 was not received at Waterford 3 from the vendor.
This failure is the second failure during a valid test of EDG 'A' at Waterford 3 since the operating license was issued. There has also been one failure during a valid test of EDG 'B'. The jacket water and lube oil thermostatic valve thermo elements have been replaced and the resulting temperature differential is zero. Establishing a lube oil temperature which is lower than jacket water temperature will require utilizing a different lube oil thermo element. A lower temperature lube oil thermo-element has been requested from the vendor and the vendor will provide these thermo elements pending completion of their evaluation and procurement process. To address the second possible root cause, Waterford 3 will verify that Cooper Bessemer Service News Bulletins are received in order by checking that the bulletin number is sequential. Additionally, the vendor now has a designated point of contact for all nuclear users who will be used to closely track the bulletins.
Reducing the lube oil temperature below the vendor's recommendation is being considered. A consultant will evaluate this failure and make a recommendation regarding the optimum jacket water to lube oil temperature differential. EDG 'B' cylinders will also be inspected for evidence of scuffing.
A review of industry experience revealed that crankcase over-pressurizations at other plants have been attributed to metal cuttings in piston pin oil grooves, improper piston pin fit up, piston bushing failure, lube oil pump bearing failure, a loose piston pin bolt, and water leaks.
Additionally, four crankcase overpressurizations attributed to piston to liner 4
l .
seizures have indeterminate root causes. All of these root causes have been l
systematically eliminated during the root cause investigation, Specifically, no metal cuttings were found in EDG 'A'. The vendor determined that although two piston bushings needed to be reconditioned, the piston bushings could have been used in their previcus condition. An improper piston pin fit up would have caused a piston seizure soon after the initial EDG start. The EDG lube oil pump functioned satisfactorily. No loose piston pin bolts were noted and the crankcase oil sample was within specification.
EDG 'A' was declared operable at 1930 on April 12, 1991. The following items were replaced during the refueling outage: SL cylinder liner and piston assembly, 5R piston assembly, IL piston assembly, and 5 and 1 rod bearings.
The it and SR pistons and bushings were reconditioned.
The current surveillance test interval is at least once per 31 days, which is in conformance with the schedule of Regulatory Position C.2.d. The crankcase relief assemblies functioned as designed and EDG 'B' remained operable throughout the time that EDG 'A' was out of service therefore, this event did not present a hazard to the health and safety of the general public.
Plant Contact W.R. Brian, Plant Engineering Superintendent, 504/464-3127 I
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