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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO
MONTHYEARML20046D3721993-08-10010 August 1993 Special Rept SR-91-002-03:on 910318,EDG a Experienced Overpressurization.Caused by Gross Cylinder to Cylinder Load Imbalance.Event Classified as Failure Per Reg Guide 1.108.Pulled & Replaced Cylinders ML20028H8441991-01-25025 January 1991 Special Rept SR-90-004-00:on 901226,emergency Diesel Generator Tripped on Loss of Field While Operating at 100% Power.Caused by Faulty Motor Operated Potentiometer.Faulty Component Replaced ML20011F3501990-02-23023 February 1990 Special Rept SR-90-002-00:on 900128,emergency Diesel Generator a Declared Inoperable to Perform Automatic Synchronization Test.Caused by Thick Oil Forming in Low Turbocharge Lube Oil Pressure Sensing Device.Device Cleaned ML20005G7681990-01-12012 January 1990 Special Rept SR-90-001-00:on 891229,condenser Vacuum Pump Wide Range Gas Monitor Inoperable Due to Spurious Alarms. Functional Test Per Maint Instruction (MI)-003-386 Satisfactorily Performed ML19351A4061989-10-16016 October 1989 Special Rept SR-89-002-00:on 890930,video Scan of Steam Generator 1 Tubesheet Indicated Presence of Foreign Object Lodged in Tube.Object Identified as Calibr Tube Pressure Cap.Caused by Inadequate Corrective Action 1993-08-10
[Table view] Category:LER)
MONTHYEARML20046D3721993-08-10010 August 1993 Special Rept SR-91-002-03:on 910318,EDG a Experienced Overpressurization.Caused by Gross Cylinder to Cylinder Load Imbalance.Event Classified as Failure Per Reg Guide 1.108.Pulled & Replaced Cylinders ML20028H8441991-01-25025 January 1991 Special Rept SR-90-004-00:on 901226,emergency Diesel Generator Tripped on Loss of Field While Operating at 100% Power.Caused by Faulty Motor Operated Potentiometer.Faulty Component Replaced ML20011F3501990-02-23023 February 1990 Special Rept SR-90-002-00:on 900128,emergency Diesel Generator a Declared Inoperable to Perform Automatic Synchronization Test.Caused by Thick Oil Forming in Low Turbocharge Lube Oil Pressure Sensing Device.Device Cleaned ML20005G7681990-01-12012 January 1990 Special Rept SR-90-001-00:on 891229,condenser Vacuum Pump Wide Range Gas Monitor Inoperable Due to Spurious Alarms. Functional Test Per Maint Instruction (MI)-003-386 Satisfactorily Performed ML19351A4061989-10-16016 October 1989 Special Rept SR-89-002-00:on 890930,video Scan of Steam Generator 1 Tubesheet Indicated Presence of Foreign Object Lodged in Tube.Object Identified as Calibr Tube Pressure Cap.Caused by Inadequate Corrective Action 1993-08-10
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217F2891999-10-13013 October 1999 Drill 99-08 Emergency Preparedness Exercise on 991013 ML20217G7211999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Waterford 3 Ses. with ML20211Q2141999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Waterord 3 Ses.With ML20210Q6361999-07-31031 July 1999 Corrected Monthly Operating Rept for July 1999 for Waterford 3 ML20210S0581999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Waterford 3.With ML20210D8951999-07-23023 July 1999 Safety Evaluation Accepting First 10-yr Interval Inservice Insp Plan Requests for Relief ISI-018 - ISI-020 ML20209H3781999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Waterford 3 Ses. with ML20195J8951999-06-17017 June 1999 Safety Evaluation Granting Relief for Listed ISI Parts for Current Interval,Per 10CFR50.55a(g)(5)(iii) ML20207E8631999-06-0303 June 1999 Safety Evaluation Accepting Licensee 990114 Submittal of one-time Request for Relief from ASME B&PV Code IST Requirements for Pressure Safety Valves at Plant,Unit 3 ML20195K3391999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Waterford 3 Ses.With ML20195C3041999-05-28028 May 1999 Annual Rept on Abb CE ECCS Performance Evaluation Models ML20206S7401999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Waterford 3.With ML20205T2621999-04-22022 April 1999 LER 99-S02-00:on 990216,contract Employee Inappropriately Granted Unescorted Access to Plant Protected Area.Caused by Personnel Error.Security Personnel Performed Review of Work & Work Area That Individual Was Involved with ML20205N9671999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Waterford 3 Ses.With ML20205E8531999-03-30030 March 1999 Corrected Pages COLR 3/4 1-4 & COLR 3/4 2-6 to Rev 1, Cycle 10, Colr ML20205A6331999-03-25025 March 1999 SER Accepting Request to Use Mechanical Nozzle Seal Assemblies as an Alternative Repair Method,Per 10CFR50.55a(a)(3)(i) for Reactor Coolant Sys Applications at Plant,Unit 3 ML20204H1401999-03-23023 March 1999 Rev 1 to Engineering Rept C-NOME-ER-0120, Design Evaluation of Various Applications at Waterford Unit 3 ML20204H1231999-03-22022 March 1999 Rev 1 to Design Rept C-PENG-DR-006, Addendum to Cenc Rept 1444 Analytical Rept for Waterford Unit 3 Piping ML20204H2451999-03-22022 March 1999 Rev 2 to C-NOME-SP-0067, Design Specification for Mechanical Nozzle Seal Assembly (Mnsa) Waterford Unit 3 ML20204F0791999-03-17017 March 1999 Rev 1 to Waterford 3 COLR for Cycle 10 ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207F3491999-03-0505 March 1999 LER 99-S01-00:on 990203,contraband Was Discovered in Plant Protected Area.Bottle Was Determined to Have Been There Since Original Plant Construction.Bottle Was Removed & Security Personnel Performed Search of Area.With ML20204B5141999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Waterford 3.With ML20203H8591999-02-17017 February 1999 Safety Evaluation Accepting Licensee Second Ten Year ISI Program & Associated Relief Requests for Plant,Unit 3 ML20199H6261999-01-21021 January 1999 Safety Evaluation Accepting Classification of Instrument Air Tubing & Components for Safety Related Valve Top Works.Staff Recommends That EOI Revise Licensing Basis to Permit Incorporation of Change ML20199C9101998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Waterford 3.With ML20196F4911998-12-0101 December 1998 SER Accepting Request for Relief ISI2-09 for Waterford Steam Electric Station,Unit 3 & Arkansas Nuclear One,Unit 2 ML20206N4131998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Waterford 3.With ML20195C4841998-11-0606 November 1998 SER Accepting QA Program Change to Consolidate Four Existing QA Programs for Arkansas Nuclear One,Grand Gulf Nuclear Station,River Bend Station & Waterford 3 Steam Electric Station Into Single QA Program ML20195E5161998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Waterford 3.With ML20155C1351998-10-26026 October 1998 Rev B to Entergy QA Program Manual ML20154K0801998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Waterford 3 Ses. with ML20151W8331998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Waterford,Unit 3. with ML20237B6831998-08-17017 August 1998 LER 98-S01-00:on 980723,discovered That Waterford 3 Physical Security Plan,Safeguards Document Was Not Under Positive Control of Authorized Person at All Times.Caused by Human Error/Inappropriate Action.Counseled Employee Involved ML20237C5661998-08-17017 August 1998 Safety Evaluation Accepting Licensee Request for Exemption from Section Iii.O of Appendix R to 10CFR50 ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML20237B5261998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Waterford 3 ML20236S9031998-07-22022 July 1998 SER Accepting Rev 19 to Quality Assurance Program for Waterford Steam Electric Station,Unit 3 ML20198H3911998-07-14014 July 1998 Non-proprietary Rev 5 to HI-961586, Thermal-Hydraulic Analysis of Waterford-3 Spent Fuel Pool ML20236N4181998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Waterford,Unit 3 ML20248E7781998-06-0101 June 1998 Annual Rept on Abb CE ECCS Performance Evaluation Models ML20249A4711998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Waterford 3 Ses ML20196A4051998-05-31031 May 1998 Rept of Facility Changes,Tests & Experiments,Per 10CFR50.59 for 970601-980531. with ML20198H4681998-05-20020 May 1998 Non-proprietary Rev 1 to HI-981942, Independent Review of Waterford Unit 3 Spent Fuel Pool Cfd Model ML20247A3891998-05-0101 May 1998 SG Eddy Current Examination (8th Refueling Outage) ML20247F6761998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Waterford,Unit 3.W/ ML20217M8951998-04-30030 April 1998 QA Program Manual ML20217P8281998-04-0707 April 1998 Safety Evaluation Accepting Relief Authorization for Alternative to Requirements of ASME Section Xi,Subarticle IWA-5250 Bolting Exam for Plants,Per 10CFR50.55a(a)(3)(i) ML20216B1751998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Waterford 3 Ses ML20217M1411998-03-0303 March 1998 Rev 2 of Waterford 3 Cycle 9 Colr 1999-09-30
[Table view] |
Text
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POWER & LIGHT WATERFORD 3 SES
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W3A90-0114 l A4.05.
QA' 1
February 23,.1990 ;
U.S. Nuclear Regulatory Commission- 1 ATTENTION: Document Control Desk Washington, D.C. 20555 ;
SUBJECT:
'Waterford 3 SES Docket No. 50-382 .
License No.~NPF-38 I Reporting of Special Report Attached is Special Report Number SR-90-002-00 for Waterford~ Steam
' Electric Station Unit 3. This Special Report.is submitted per~ ,
- 10CFR50.36(c)(2) and Technical Specifications 4.8.1.1.3 and 6.9.2.
s Very truly yours, 0.R. McGaha
' Plant Manager - Nuclear i JRM/JEF/rk .
~ Attachment
- cc Messrs. R.D. Martin J.T. Whcolock - INPO Records Center E.L. Blake W.M'. Stevenson
- D.L. Wigginton NRC Resident Inspectors r
9003050183 900223 D PDR S
ADOCK 050003G2 PDC P
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"AN EQUAL OPPORTUNITY NMPLOYER"
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p S SPECIAL REPORT
[- SR-90-002-00 g,_ invalid Failure of Emergency Diese1' Generator A ,
'Due to. Spurious Operation of A Trip That is Bypassed in the Emergency Mode INTRODUCTION At 1430 hours0.0166 days <br />0.397 hours <br />0.00236 weeks <br />5.44115e-4 months <br /> on January 28, 1990, Waterford Steam Electric Station Unit 3 was shutdown, in Mode S, when Emergency Diesel Generator (EDG) A was declared inoperable to perform an automatic synchronization test. EDG A tripped on low turbocharger lube oil pressure when it was started for the test. This-event has been classified as an invalid failure.
The root cause of the event is thick oil forming in the low turbocharger lube oil pressure shutdown sensing device. During engine startup, the low turbocharger lube oil pressure shutdown is blocked to allow time for oil pressure to buildup and reset the oil pressure sensing device. The viscous oil prevented resetting the trip before the starting sequence timed out. The sensing device was removed, cicaned, and recalibrated. EDG A engine low lube oil shutdown sensing device and EDG B low turbocharger lube oil shutdown sensing device were inspected to verify a similar condition did not exist.. The .
low turbocharger lube oil pressure trip is bypassed in the emergency mode and would not have affected the ability of the EDG to perform its designed safety function. Therefore, there was no hazard to plant equipment or the health and safety of the general public, h
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J At 1430 hours0.0166 days <br />0.397 hours <br />0.00236 weeks <br />5.44115e-4 months <br /> on January 28, 1990, Waterford Steam Electric Station UnitD3 was 'l
[ ! shutdown in: Mode 5. when Emergency Diesel Generator'.(EDC) A was declared l Linoperableito perform Special Test Procedure (STP) '251569 "EDG Automatic ,
' Synchronization Test." EDG A tripped on low turbocharger-lube oil pressure approximately_ ten-seconds after it was started'for this STP.- Operations l
. personnel noted_that.the local turbocharger lube oil pressure gauge' indicated-
, .the~normally expected operating value when the trip. occurred.- The event has
- been classified as ~an invalid diesel generator f ailure by the criteria of l
.y l Regulatory Guide 1.108 C.2.e(2) due to a malfunction of equipment that_is non-operative in the emergency operating mode. This report is submitted pursuant--
" to Technical-Specification (TS) 4.8.1.1.3 and 6.9.2.
Troubleshooting of the EDG was performed. The turbocharger low pressure shutdown sensing device was found to be in calibration tolerances but responded I slower than expected. Thick oil was found inside the sensing device. The device was cleaned out and recalibrated. EDG A engine low lube oil shutdown -
sensing device and EDG' B. low turbocharger ~1ube oil shutdown sensing device vere inspected to verify a similar condition did not exist. After starting and 1 loading EDG A in accordance with operating procedure (0P) 009-002 " Emergency -I Diesel Generator" at 1507 hours0.0174 days <br />0.419 hours <br />0.00249 weeks <br />5.734135e-4 months <br /> on January 30, 1990, EDG A was declared operabic.
The. root cause of the event was thick' oil forming in the low turbocharger lube :
oil pressure shutdown sensing device. During engine startup, the low turbocharger l lube oil pressure shutdown is locked out to allow time-for the oil pressure to-
-buildup and reset the low pressure sensing device. The viscous oil prevented resetting the trip before the starting sequence timed out. After the oil was cleaned out, the sensing device responded as expected. Because a similar
_ problem was not found in the other low lube oil pressure shutdown sensing devices inspected, this is believed to be an isolated case. The calibration
. preventive maintenance task of the lube oil pressure trips is being modified to
.-include clean and inspect the lube oil pressure sensing devices every eighteen
. months to prevent-viscous oil from forming in the lube oil pressure sensing
' devices.
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- .'There has only[beenione failure during a valid
- test of EDG A_at Waterford 3# <
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, 4 Laince'theLoperatingl license was issued. The' surveillance test interval required 1
- by TS Table 4.8-1 has alway's been '.'at least- i once; per 31- days" since ' issuance ' of1
(; the9 operating license.1The low turbocharger lube oil pressure ' trip 'is bypaaeed j
[@ in thefemergency' mode _and would-not affect.the ability-lofJthe:EDG!to perform l ,
fh
? 4 its !safetiyf f' unction; Therefore, this event did not present 'aLhazardt to plant -
~
1 Jequipment'or:the: health and safety of the. general'public.
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r; 1 T.H.-Smith . Plant Engineering Superintendent, 504/464-3127.- [i
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