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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20148T6101997-07-0303 July 1997 Follow-up to Special Rept SR-96-003-01:on 970411,damage to Cables for Sensors 1A & 1B Discovered.Sensor Cable for 7B Also Found Damaged.Cables for Channels 1A,1B & 7B Found Saturated W/Oil.Sensors Replaced for Channels 1A,1B & 7B ML20148N7281997-06-26026 June 1997 Special Rept SR-97-002-00:on 970513,personnel Identified Design Discrepancy for B CCW Train Radiation Monitor. Design Flaw Existed Since Plant Built.Design Change DC-3537 Approved to Reroute Cooling Water Line from Connection ML20135E9641996-12-10010 December 1996 Special Rept SR-96-003-00:on 961027,valve & Loose Parts Monitoring Sys Declared Inoperable.Caused by Failure of Sensor on Channel 1.Sensor Will Be Replaced During Refueling Outage 8 ML20113E4501996-07-0303 July 1996 Special Rept SR-96-001-00:on 960603,output Breaker for EDG B Failed to Close.Caused by Intermittent Malfunction of Contacts on Synchronizing Switch.Performed Troubleshooting & Replaced EDG B Synchronizing Switch ML20094P5911995-11-27027 November 1995 Special Rept SR-95-004-00:on 951030,EDG Tripped on Turbocharger Low Lube Oil Pressure.Generated Condition Rept 95-1102 ML20094G2031995-11-0808 November 1995 Special Rept SR-95-003-00:on 951010,EDG Experienced Crankcase Overpressurization.Caused by Poor Lubricating Conditions During Startup & Rapid Loading Led to Tin Transfer from Piston to Cylinder Liner ML20093L8421995-10-23023 October 1995 Special Rept SR-95-002-00 on 951011,ABB C-E Identified Leaking Plug Due to build-up of Boric Acided Crystals Around OD of Plug.Leaking Plug Removed by Tig Relaxation & Replaced/Another Rolled Mechanical Plug ML20086E0181995-07-0707 July 1995 Special Rept SR-94-001-01:on 940228 & 0302,EDG a Experienced Nonvalid Failures Due to Worn Mechanical Governor Parts. Mechanical Governor & Faulty Relay Replaced & Procedure OP-009-02, EDG Revised ML20070N6601994-05-0404 May 1994 Special Rept SR-94-003:on 940404,EDG a Experienced Nonvalid Failure While Performing Valid Test.Probably Caused by Emergency Mode Master Run Relay 4EX1 de-energized During Run.Troubleshooting in Progress ML20065A3761994-03-29029 March 1994 Special Rept SR-94-001,on 940228,EDG a Tripped on Overspeed. Caused by Faulty Contacts in Relay of Electronic Grovernor Droop.Faulty Relay & Mechanical Governor Replaced ML20059B9521993-10-26026 October 1993 Special Rept SR-93-001-01,final Rept:On 930811,declared Condenser Vacuum Pump Wide Range Gas Monitor PRM-IRE-002 Inoperable.Monitor Returned to Svc on 930901.Inoperability of Subj Monitor Did Not Pose Safety Concern ML20056H1011993-09-0101 September 1993 Special Rept SR-93-001-00:on 930811,condenser Vacuum Pump WRGM PRM-IRE-002 Declared Inoperable & Not Returned to Svc within Seven Days.Monitor Will Be Returned to Svc After Low Range Sample Flow Cv Repaired & Functionally Checked ML20046D3721993-08-10010 August 1993 Special Rept SR-91-002-03:on 910318,EDG a Experienced Overpressurization.Caused by Gross Cylinder to Cylinder Load Imbalance.Event Classified as Failure Per Reg Guide 1.108.Pulled & Replaced Cylinders ML20126M5881993-01-0606 January 1993 Special Rept SR-92-003:on 921207,EDG a Failed to Reach Rated Speed & Voltage in Less than or Equal to 10 S.Caused by Failure to Properly Secure Turning Gear Brackets.Control Brackets for Turning Gear Interlock Valves Adjusted ML20127M4981992-11-24024 November 1992 Special Rept SR-92-002-00:on 921023,component Cooling Water (CCW) A/B Radiation Monitor Was Inoperable for More than 30 Days.Ts Change Request NPF-38-127,dtd 921021 Submitted,Which Changes Operability Requirement ML20116B2121992-10-23023 October 1992 Special Rept SR-92-001-00:on 921010,inservice Eddy Current Exam of SG Tubing Completed,Per 10CFR50.36(c)(2).Total Number of Tubes Have Been Plugged in SG Shown as Listed ML20086K8731991-12-11011 December 1991 Special Rept SR-91-007-00:on 911111,diesel Generator a Loaded to 4.3 MW & Tripped.Caused by Inadequate Positioning of Turbocharger Inlet Air Butterfly Valve Limit Switch Mounting Bracket.Limit Switch Repositioned ML20086G0201991-11-27027 November 1991 Special Rept SR-91-002-02:on 910318,emergency Diesel Generator a Experienced Crankcase Overpressurization.Caused by Stuck Piston Rings.Piston & Piston Liner Replaced & Improper Temp Differential Will Be Corrected ML20083D4431991-09-23023 September 1991 Special Rept SR-91-002-01:on 910318,emergency Diesel Generator a Experienced Crankcase Overpressurization.Caused by Stuck Piston Rings & Improper Temp Differential.Cylinder Liner,Piston Assemblies & Rod Bearings Replaced ML20082U6231991-09-16016 September 1991 Special Rept SR-91-003-01:on 910406,inservice Eddy Current Exam of Facility SG Tubing Completed by Westinghouse.Rept Submitted Per Tech Specs 4.4.4.5 & 6.9.2.Rotating Pancake Coil Exam Results Verified No Detectable Degradation ML20082T2121991-09-13013 September 1991 Special Rept:On 910820,EDG Secured During Surveillance Test Due to Power Dropping Resistor Failure.Power Dropping Resistor Assembly Replaced.Health & Safety of Public & Plant Personnel Not Affected by This Event ML20082C4021991-07-15015 July 1991 Special Rept 91-005-00:on 910619,EDG a Tripped on Turbocharger Lube Oil Low Pressure During Performance of Operating Procedure 903-068.Procedure Changed to Require Lubrication of Turbocharger ML20073Q8001991-05-29029 May 1991 Special Rept SR-91-04-00:on 910429,EDG a Failed Invalidly Due to Spurious Turbocharger Lube Oil Pressure Trip.Edg Restarted.Oil Pressure Remained within Normal Operating Limits & OP-903-068 Completed ML20073B3231991-04-19019 April 1991 Special Rept SR-91-003-00,re 910406 Completion of Inservice Eddy Current Exam of Steam Generator tubing.Follow-up Rept Will Be Submitted by 920406,per Tech Spec 4.4.4.5.b.Total Number of Tubes Plugged in Each Steam Generator Listed ML20084U8591991-04-17017 April 1991 Special Rept SR-91-002-00:on 910318,emergency Diesel Generator a Experienced Crankcase Overpressurization. Possibly Caused by Improper Temp Differential Between Jacket Cooling Water & Lube Oil Temp.Liner Replaced ML20072Q8931991-03-18018 March 1991 Special Rept SR-91-001-00:on 910207,channel 2 of SPDS Failed & Could Not Be Restored within 7 Days.On 910214, Channel 2 of Qualified SPDS Sensor 8 Out of Svc for More than 7 Days.Channel 2 Probe Will Be Replaced ML20028H8441991-01-25025 January 1991 Special Rept SR-90-004-00:on 901226,emergency Diesel Generator Tripped on Loss of Field While Operating at 100% Power.Caused by Faulty Motor Operated Potentiometer.Faulty Component Replaced ML20065R6021990-12-12012 December 1990 Special Rept SR-90-003-00:on 901112,invalid Failure of Emergency Diesel Generator a Occurred.Caused by Mechanical Failure of 30 Psig Reducer in Control Air Sys & Crack on Spring Cap of Reducer.All Reducers Inspected ML20011F3501990-02-23023 February 1990 Special Rept SR-90-002-00:on 900128,emergency Diesel Generator a Declared Inoperable to Perform Automatic Synchronization Test.Caused by Thick Oil Forming in Low Turbocharge Lube Oil Pressure Sensing Device.Device Cleaned ML20005G7681990-01-12012 January 1990 Special Rept SR-90-001-00:on 891229,condenser Vacuum Pump Wide Range Gas Monitor Inoperable Due to Spurious Alarms. Functional Test Per Maint Instruction (MI)-003-386 Satisfactorily Performed ML20246C9091989-05-0303 May 1989 Special Rept SR-89-001-01:on 890206 & 0403,emergency Diesel Generator a Declared Inoperable.Caused by Fuse Not Being Secured in Fuse Holder & Oxidation of Speed Control Circuit Relay Contacts.Contacts Cleaned & Fuses & Holders Checked ML20245A3951989-04-10010 April 1989 Special Rept SR-88-004-01:on 880420,inservice Eddy Current Exam of Steam Generator Tubing Completed by Westinghouse.Two Tubes Exceeded Plugging Limit in Steam Generator A.All Discrepancies Resolved ML20236B0941989-03-0808 March 1989 Special Rept:On 890206,emergency Diesel Generator Secured Due to Failure of Speed Control Circuit While Generator in Manual Operation.Caused by Oxidation of Relay Contacts in Governor Control Circuitry.Contacts Replaced ML20206H4901988-11-18018 November 1988 Special Rept SR-88-009-00:on 880909,emergency Diesel Generator Tripped Due to Incorrect Valve Lineup.Caused by Personnel Error.Valves Opened ML20151U8841988-08-16016 August 1988 Special Rept SR-88-008-00:on 880726,plant Stack Effluent Accident wide-range Gas Monitor Declared Inoperable.Caused by Pump Failing Step 8.4.2.18 Which Checks high-range Sample Flow within Specified Tolerance.Transmitter Replaced ML20151C1121988-07-15015 July 1988 Special Rept SR-88-007-00:on 880628,primary Meteorological Tower Instruments out-of-svc Greater than Seven Days.Caused by Instruments Being Out of Calibr.Temp Elements Replaced & Corrective Maint on Delta Temp Instruments Completed ML20151C0781988-07-15015 July 1988 Special Rept SR-88-006-00:on 880616,emergency Diesel Generator B Tripped Due to Personnel Error.Caused by Failure to Raise Load within 5 S.Operating Procedure OP-9-002 Reviewed & Considered to Adequately Address Operation ML20195H7171988-06-20020 June 1988 Special Rept SR-88-005-00:on 880511,unit Was in Refueling Mode When Operations Personnel Declared Seismic Monitor SM-IYR-6021 Inoperable.Plastic Lexan Mounting Board Appeared to Be Deformed Due to Heat.Monitor Will Be Relocated ML20153F3831988-05-0404 May 1988 Special Rept SR-88-003-01:on 850801-880404 Several Failures of Emergency Diesel Generators to Start Occurred.Caused by Actuation of Trips Which Bypassed in Emergency Mode.Trip Sensor Replaced ML20153F2541988-05-0404 May 1988 Special Rept SR-88-004-00:on 880420,inservice Eddy Current Exam of Steam Generator Tubing Completed.Rept Submitted in Accordance W/Tech Specs 4.4.4.5.a.Number of Tubes Plugged in Each Steam Generator Listed ML20148F1021988-03-21021 March 1988 Special Rept SR-85-002-01:on 851230,discovered Emergency Diesel Generator a Failed to Complete Surveillance Run as Defined in Procedure OP-903-068 & Tech Spec 4.8.1.1.2a.5. Cause Not Determined.Minor Adjustments Made to Governor ML20148F0971988-03-18018 March 1988 Special Rept SR-88-003-00:from 850801-880308,several Emergency Diesel Generators Failed to Start.Caused by Malfunctioning Trip Mechanisms.Diesels Will Not Be Taken Out of Svc Until Plant Scheduled to Be out-of-svc for Maint ML20149J3411988-02-18018 February 1988 Special Rept SR-88-001-00:on 880128,during Plant Startup Operations,Personnel Declared Fuel Handling Exhaust Wide Range Gas Monitor out-of-svc for Calibr.Caused by Extensive Teardown.Procedure Revised ML20236Q1121987-11-16016 November 1987 Special Rept SR-87-006-00:on 871028,primary Meteorological Tower Upper Wind Speed & Wind Direction Instrument out-of- Svc in Excess of 7 Days.Caused by Failed Signal Converter. Parts Replaced & Instrument Returned to Svc on 871104 ML20236Q2621987-11-13013 November 1987 Special Rept SR-87-005-00:on 871103,Tech Specs 3.3.3.1 & 6.9.2 Violated.Caused by Inoperability of Effluent Accident wide-range Gas Monitor for More than 7 Days Due to Damaged Connectors.New Monitor Should Be Installed by 871125 ML20235J8531987-09-24024 September 1987 Special Rept SR-87-004-00 Re Results of Inservice Eddy Current Exam of Steam Generator Tubing Completed on 861214. No Indication of Degradation Greater than or Equal to 20% Through Wall Detected in Steam Generator a ML20237G9341987-08-21021 August 1987 Special Rept SR-87-003-00:on 870731 & 0809,condenser Vacuum Vacuum Pump Discharge Wide Range Gas Monitor (WRGM) Inoperable.Caused by Water Blockage of Sample Lines.Wrgm Restarted & Being Tested for Operation ML20234B2111987-06-29029 June 1987 Special Rept SR-87-002-00:on 870606,high Range Gas Monitor Inoperable Greater than 7 Days.Caused by Faulty Display Module & Lack of Spares & Quality Documentation.Module Replaced & Monitor Returned to Svc After Functional Test ML20215H0841987-06-17017 June 1987 Special Rept SR-87-001-00:on 870527,during Full Reactor Power,Condenser Vacuum Pump Discharge Wide Range Gas Monitor Declared Inoperable.Caused by Failed Input/Output Circuit Board & Low Range Detector.Faulty Components Replaced ML20205G1731987-03-18018 March 1987 Ro:On 870222,steam Line Break on Scavenging Steam Vent Line from Moisture Separator Reheater Experienced.Caused by Classic Fatigue Failure in Heat Affected Zone of Weld Joining Alloy 800 Matl.Temporary Restraints Added 1997-07-03
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217F2891999-10-13013 October 1999 Drill 99-08 Emergency Preparedness Exercise on 991013 05000382/LER-1999-014, :on 990910,reactor Shutdown Due to Loss of Controlled bleed-off Flow,Occurred.Caused by Rotating Baffle failure.Two-piece Rotating Baffle of Original Design Was Located & Installed,In Order to Repair RCP 2B1999-10-12012 October 1999
- on 990910,reactor Shutdown Due to Loss of Controlled bleed-off Flow,Occurred.Caused by Rotating Baffle failure.Two-piece Rotating Baffle of Original Design Was Located & Installed,In Order to Repair RCP 2B
ML20217G7211999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Waterford 3 Ses. with 05000382/LER-1999-013, :on 990825,exceeding TS Limits for RCS Cooldown Rate Was Discovered.Caused by Inadequate Content & Inadequate Implementation of TS Requirements.Page 2 of 2 in Attachment 2 of Incoming Submittal Not Included1999-09-23023 September 1999
- on 990825,exceeding TS Limits for RCS Cooldown Rate Was Discovered.Caused by Inadequate Content & Inadequate Implementation of TS Requirements.Page 2 of 2 in Attachment 2 of Incoming Submittal Not Included
05000382/LER-1999-012-01, :on 990812,potential Operation with Both Control Room Normal Outside Air Intakes Valves Inoperable Occurred.Cause for Event Was Indeterminate.Seat Leakage Requirements Calculated.With1999-09-13013 September 1999
- on 990812,potential Operation with Both Control Room Normal Outside Air Intakes Valves Inoperable Occurred.Cause for Event Was Indeterminate.Seat Leakage Requirements Calculated.With
ML20211Q2141999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Waterord 3 Ses.With 05000382/LER-1999-011-01, :on 990801,with Plant Operating 100% Power, Lowering RCP Seal Pressures,Along with Dropping Controlled bleed-off (Cbo) & Increasing Cbo Temp Discovered.Caused by fatigue-induced Failure of Rotating Baffle of RCP 2B1999-08-31031 August 1999
- on 990801,with Plant Operating 100% Power, Lowering RCP Seal Pressures,Along with Dropping Controlled bleed-off (Cbo) & Increasing Cbo Temp Discovered.Caused by fatigue-induced Failure of Rotating Baffle of RCP 2B
05000382/LER-1999-010-01, :on 990726,discovered Inadequate Pumping Capacity in Dry Cooling Tower Area.Caused by Inadequate Design Control.Portable Pumps Were Installed in Each Dry Cooling Tower Areas to Ensure Sufficient Pumping Capacity1999-08-26026 August 1999
- on 990726,discovered Inadequate Pumping Capacity in Dry Cooling Tower Area.Caused by Inadequate Design Control.Portable Pumps Were Installed in Each Dry Cooling Tower Areas to Ensure Sufficient Pumping Capacity
05000382/LER-1999-009-01, :on 990727,discovered App R Noncompliance Condition Involving Inadequate Separation of Safe Shutdown Cables.Caused Design Analysis Deficiency.Compensatory Measures Were Established1999-08-26026 August 1999
- on 990727,discovered App R Noncompliance Condition Involving Inadequate Separation of Safe Shutdown Cables.Caused Design Analysis Deficiency.Compensatory Measures Were Established
ML20210Q6361999-07-31031 July 1999 Corrected Monthly Operating Rept for July 1999 for Waterford 3 ML20210S0581999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Waterford 3.With 05000382/LER-1999-008-01, :on 990629,failure to Perform Testing of ESF Filtration Units Per TS Was Noted.Cause for Testing Charcoal Samples Contrary to TS Could Not Be Determined.All Future Analysis Will Be Performed IAW ASTM D3803-1989,per GL 99-021999-07-29029 July 1999
- on 990629,failure to Perform Testing of ESF Filtration Units Per TS Was Noted.Cause for Testing Charcoal Samples Contrary to TS Could Not Be Determined.All Future Analysis Will Be Performed IAW ASTM D3803-1989,per GL 99-02
05000382/LER-1999-007-01, :on 990625,operation Outside Tornado Missile Protection Licensing Basis for turbine-driven EFW Pump & Steam Supply Piping,Was Discovered.Caused Indeterminent. Entergy Will Submit 10CFR50.90 to NRC Staff1999-07-23023 July 1999
- on 990625,operation Outside Tornado Missile Protection Licensing Basis for turbine-driven EFW Pump & Steam Supply Piping,Was Discovered.Caused Indeterminent. Entergy Will Submit 10CFR50.90 to NRC Staff
ML20210D8951999-07-23023 July 1999 Safety Evaluation Accepting First 10-yr Interval Inservice Insp Plan Requests for Relief ISI-018 - ISI-020 05000382/LER-1999-006-01, :on 990614,plant Experienced Automatic Reactor Trip Following Loss of 7kV Bus.Caused by Spurious Actuation of Relay on Either RCP 1A or 2A.Personnel Performed Final Switchgear Walkdown with Indications Normal.With1999-07-14014 July 1999
- on 990614,plant Experienced Automatic Reactor Trip Following Loss of 7kV Bus.Caused by Spurious Actuation of Relay on Either RCP 1A or 2A.Personnel Performed Final Switchgear Walkdown with Indications Normal.With
ML20209H3781999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Waterford 3 Ses. with 05000382/LER-1999-005-01, :on 980702,determined That Four Contacts in Control Circuits of EFW Control Valves Were Untested.Caused by Personnel Error.Untested Contacts Have Been Tested1999-06-24024 June 1999
- on 980702,determined That Four Contacts in Control Circuits of EFW Control Valves Were Untested.Caused by Personnel Error.Untested Contacts Have Been Tested
ML20195J8951999-06-17017 June 1999 Safety Evaluation Granting Relief for Listed ISI Parts for Current Interval,Per 10CFR50.55a(g)(5)(iii) ML20195J9741999-06-16016 June 1999 Safety Evaluation Supporting Amend 152 to License NPF-38 ML20207E8631999-06-0303 June 1999 Safety Evaluation Accepting Licensee 990114 Submittal of one-time Request for Relief from ASME B&PV Code IST Requirements for Pressure Safety Valves at Plant,Unit 3 ML20195D5491999-06-0303 June 1999 Safety Evaluation Supporting Amend 151 to License NPF-38 ML20195K3391999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Waterford 3 Ses.With ML20195C3041999-05-28028 May 1999 Annual Rept on ABB CE ECCS Performance Evaluation Models 05000382/LER-1999-004-02, :on 990415,discovered That Complete Response Time for ESFAS Containment Cooling Function Had Not Been Performed.Caused by Response Time Testing Deficiency. Procedures Will Be Revised to Include Subject Testing1999-05-14014 May 1999
- on 990415,discovered That Complete Response Time for ESFAS Containment Cooling Function Had Not Been Performed.Caused by Response Time Testing Deficiency. Procedures Will Be Revised to Include Subject Testing
ML20206S7401999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Waterford 3.With ML20205T2621999-04-22022 April 1999 LER 99-S02-00:on 990216,contract Employee Inappropriately Granted Unescorted Access to Plant Protected Area.Caused by Personnel Error.Security Personnel Performed Review of Work & Work Area That Individual Was Involved with ML20206A9641999-04-21021 April 1999 Safety Evaluation Supporting Amend 150 to License NPF-38 05000382/LER-1999-003-02, :on 990311,determined That Four Containment Vacuum Relief valves,CVR-101,CVR-201,CVR-102 & CVR-202,were Not Tested.Caused by Contractor Supply of Misinformation. Details of Event Discussed with Contractor.With1999-04-0909 April 1999
- on 990311,determined That Four Containment Vacuum Relief valves,CVR-101,CVR-201,CVR-102 & CVR-202,were Not Tested.Caused by Contractor Supply of Misinformation. Details of Event Discussed with Contractor.With
ML20205N9671999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Waterford 3 Ses.With ML20205E8531999-03-30030 March 1999 Corrected Pages COLR 3/4 1-4 & COLR 3/4 2-6 to Rev 1, Cycle 10, Colr ML20205A6331999-03-25025 March 1999 SER Accepting Request to Use Mechanical Nozzle Seal Assemblies as an Alternative Repair Method,Per 10CFR50.55a(a)(3)(i) for Reactor Coolant Sys Applications at Plant,Unit 3 05000382/LER-1999-002-03, :on 990225,discovered RCS Pressure Boundary Leakage on Two Inconel 600 Instrument Nozzles.Caused by Axial Cracks Near HAZ of Nozzle Partial Penetration Welds Resulting from Pwscc.Leaking Nozzles Have Been Repaired1999-03-25025 March 1999
- on 990225,discovered RCS Pressure Boundary Leakage on Two Inconel 600 Instrument Nozzles.Caused by Axial Cracks Near HAZ of Nozzle Partial Penetration Welds Resulting from Pwscc.Leaking Nozzles Have Been Repaired
ML20204H1401999-03-23023 March 1999 Rev 1 to Engineering Rept C-NOME-ER-0120, Design Evaluation of Various Applications at Waterford Unit 3 ML20204H1231999-03-22022 March 1999 Rev 1 to Design Rept C-PENG-DR-006, Addendum to Cenc Rept 1444 Analytical Rept for Waterford Unit 3 Piping ML20204H2451999-03-22022 March 1999 Rev 2 to C-NOME-SP-0067, Design Specification for Mechanical Nozzle Seal Assembly (Mnsa) Waterford Unit 3 ML20204F0791999-03-17017 March 1999 Rev 1 to Waterford 3 COLR for Cycle 10 ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207F3491999-03-0505 March 1999 LER 99-S01-00:on 990203,contraband Was Discovered in Plant Protected Area.Bottle Was Determined to Have Been There Since Original Plant Construction.Bottle Was Removed & Security Personnel Performed Search of Area.With ML20204B5141999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Waterford 3.With ML20203H8151999-02-17017 February 1999 Safety Evaluation Supporting Amend 149 to License NPF-38 ML20203H8591999-02-17017 February 1999 Safety Evaluation Accepting Licensee Second Ten Year ISI Program & Associated Relief Requests for Plant,Unit 3 05000382/LER-1999-001, :on 990105,TS 3.0.3 Was Entered.Caused by Less than Adequate Chiller Thermostat Control.Placed Tamper Seal on Chiller Thermostat.With1999-02-0404 February 1999
- on 990105,TS 3.0.3 Was Entered.Caused by Less than Adequate Chiller Thermostat Control.Placed Tamper Seal on Chiller Thermostat.With
ML20202H9161999-02-0202 February 1999 Safety Evaluation Supporting Amend 148 to License NPF-38 ML20199H6261999-01-21021 January 1999 Safety Evaluation Accepting Classification of Instrument Air Tubing & Components for Safety Related Valve Top Works.Staff Recommends That EOI Revise Licensing Basis to Permit Incorporation of Change 05000382/LER-1998-020, :on 981204,determined That Certain Core Power Distribution SRs Had Been Incorrectly Scheduled.Caused by TS Change Implementation Error.Will Perform Final Review of TS SRs with 4.0.4 Exemption.With1998-12-31031 December 1998
- on 981204,determined That Certain Core Power Distribution SRs Had Been Incorrectly Scheduled.Caused by TS Change Implementation Error.Will Perform Final Review of TS SRs with 4.0.4 Exemption.With
ML20199C9101998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Waterford 3.With ML20198F4691998-12-21021 December 1998 Safety Evaluation Supporting Amend 147 to License NPF-38 ML20196F4911998-12-0101 December 1998 SER Accepting Request for Relief ISI2-09 for Waterford Steam Electric Station,Unit 3 & Arkansas Nuclear One,Unit 2 ML20206N4131998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Waterford 3.With ML20195C4841998-11-0606 November 1998 SER Accepting QA Program Change to Consolidate Four Existing QA Programs for Arkansas Nuclear One,Grand Gulf Nuclear Station,River Bend Station & Waterford 3 Steam Electric Station Into Single QA Program 1999-09-30
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.g T Entergy 5 "' m on " a " '"<-
Operations W3BS 91-0268 A4.05 QA September 23, 1991 U.S. 14uclear Regulatory Commission ATTEll110N: Document Control Desk Washington, D.C.
20555 SUBJEC'i : Waterford 3 SES Docket No. 50-382 License No. NPF-38 Reporting of Special Report Gentlemen:
Attached is Special Report Number SR-91002-01 for Waterford Steam Electric Station Unit 3.
This Special Report is submitted per 10CFR50.36(c)(2) and Technical Specifications 4.8.1.1.3 and 6.9.2.
Very truly yours,
(~~
- )
OMAG P D.F. Packer General Manager Plant Operations DfP/DDW/rk Attachment cc:
Messrs. R.D. Martin G.L. Florreich J.T. Wheelock - INPO Records Center E.L. Blake N.S. Reynolds NRC Resident inspectors Office
--)
0110010005 910 C ADOCK0500((.
J FDR t
Special iteport 91 002-01 Valid inilure of Emergency Diesel Generat or ' A' due to overptessurization of the crankcase.
4 1H11ME11W On 14 arch 18, 1991, Wat eriot d Stenin I: lect ric Stationi Unit 3 was in cold shutdown when 1:roergency Diesel Generator (LDG)
'A' expericined a crankense ove :T r e t.s u r i z a t i c.n. The CDG was being run in accordance with the pret equisit es of the 18 suonth Emergency Diesel Engine Inspection proceduse, M 003 015, when the overpressurization occursed.
The operat or obset ving the I:DG run depressed the emet ge-ncy stop but ton and pulled the overspeed t rip.
This, event has been classifled as a valid diesel failure and is being reported in accordance with Technical Specification 4.b...).3.
The root cause of this. event in stuck piston rings. A possible root cause, based on vendor bulletin informatlon, vos an in: proper temperature dif ferential between jacket cooling vator and lube oli teitperatures.
The lube oil t o jacket water temperatut e differential han been eliminated as a root cause.
A related possible contributing cause was an omission of relevant.
information in that the vendor did not. provide a service news bulletin which specifically identified the posulble adverse consequences of the previously-mentioned temperature differential.
This possibic contributing cause is now considered a noncausal factor. -The piston and piston liner have been replaced and t he titproper temperature dif ferential will be corrected.
4
NARRATIVE At 0457 hours0.00529 days <br />0.127 hours <br />7.556217e-4 weeks <br />1.738885e-4 months <br /> on March 18, 1991. Vaterford Steam Electric Station Unit 3 was in cold shutdown when Emergency Diesel Generator (EDC) (Ells Identifier EK ENG)
'A' experienced a crankcase (EIIS Identiller BLK) overpressurization.
Personnel operating the EDG depressed the emergency stop push button and pulled the overspeed trip after the overpressure condition occurred. This event has been classified as a valid diesel failure and is reported in accordance with technical Specification 4.8.1.1.3.
EDG
'A' was started at 0221 to connence the prerequisite 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> continuous run of the 18 Month Emergency Diesel Engine Inspection procedure, XM 003-015. The purpose of the run was a pre maintenance heatup and engine analysis prior to placing the unit out of service for the EDG ' A' refueling outage inspection.
EDG 'A' was loaded to 4400 kilowatts when the crankcase i
overpressuriration occurred. All 10 cylinder relief assemblics lifted, filling the room with oil vapor.
The room was exited and there were no personnel injuries.
After the vapor cleared, the room was entered and a crankcase oil sample was drawn. This oil sample was found to be within specifications. An on site fuel dilution test also yielded satisfactory results.
An inspection of the EDG cylinders, pistons, rods (Ells identifier ROD),
and bearings was commenced as required by MM 003-015. The inspection revealed that the 5 left (SL) cylinder liner (Ells Identifier LNR) exhibited e
intermittent 1 1/2 by 3 inch longitudinal rough spots or scuff marks perpendicular to the piston pin. Vertical scratch marks were noted throughout the length of the cylinder. Additionally, the metal on the underside of the piston had been discolored by heat. A borescope inspection of the other pistons indicated satisfactory results.
Disassembly and inspection of four
I other pistons, SR, IL, IR and 8L, revealed normal wear.
Of particular interest was a missing piece of chromo irom the $L piston cylinder liner.
'the missing chrome flake is approximately 1/4 inch in diameter.
The 5L cylinder liner was analyzed at the vendor's n.etallurgical lab to determine the cause and consequence of the missing chrome.
Cooper Bessemer Service News Bulletin ntunber 688, dated June 76, 1985, addressed the possibility of " cylinder scuffing, piston seizure and... crankcase explosion" if jacket cooling water temperature was not maintained 5 degrees Fahrenheit higher than piston luhe oil tempetature.
Waterford 3 had not received this bulletin f rom the vendor, but a consultant who was familiar with bulletin 688 noted that Watertord 3 EDG logs showed that jacket cooling water temperature was being maintained 4 degrees lower than piston lube oil temperature. Maintaining the reconnended temperature dif ferential would reportedly prevent a crankcase explosion caused by frictional heat resulting from scuffing of the cylinder in the piston skirt area. The piston is cast steel with a thin outer coating of tin.
The piston cylinder wall is coated with chrome.
Although the reasons are not known, there is empirical industry evidence that indicates that an improper ten:perature differential causes the cast steel in the piston skirt area to become exposed. This cast steel surface then scuffs the chrome cylinder wall, eventually generating enough frictional heat to cause a crankcase explosion.
The fact that this temperature differential condition had existed at Waterford 3 on both EDGs for several years with no deleterious cffects and the fact that none of the other EDG
'A' cylinders or EDG 'li' cylinders had scuf f marks cast s doubt that the improper temperature differential is the root cause.
Based on determinations made by the vendor and an outside consultant, the improper temperature differential has been eliminated as a root cause.
A noncausal
4 factor is an omissien of relevant information in that Cooper Bessemer Service News Bulletin Number 688 was not received at Waterford 3 from the vendor.
This failure is the second failure during a valid test of EDG
'A' at Waterford 3 since the operating license was issued. There has also been one failure during a valid test of EDG
'B'.
The jacket water and lube oil thermostatic valve thermo elements have been replaced and the teru1 ting temperature differential is zero.
Establishing a lube oil temperature which is lower than jackat water temperature will require utilizing a different lube oli thermo element. A lower temperature lube oil thermo element has been requested from the vendor and the vendor will provide these thermo elements pending completion of their evaluation and procurement process. To address the noncausal factor, initial corrective a, tion consisted of coordinating with the Cooper Bessemer Nuclear Users Group to ensure that Waterford 3 now has all applicable Cooper Bessemer Service News Bulletins.
To ensure all applicable Cooper-Bessemer Service News Bulletins are received in the future, the system engineer will receive Cooper Bessemer Service News Bulletins from the Cooper-Bessemer Nuclear Users Group. Additionally, the vendor has a designated point of contact for all nuclear users who will be used to closely track the bulletins.
A review of industry experience revealed that crankcase over.
+
pressurizations at other plants have been attributed to metal cuttings in piston. pin oil grooves,-improper pisten pin fit up, piston bushing failure, lube oil pump bearing failure, a loose piston pin bolt, and water leaks.
Additionally, four crankcase overpressurizations attributed to piston to-liner seizures have indeterminate root causes.
All of these root causes have been systematically eliminated during the root cause investigation.
Specifically, no metal cuttings were found in EDGA'.
The vendor determined that although
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- two piston bushings needed to be reconditioned, the piston bushings could have been used in their previous condition.
An improper piston pin fit.up would have caused a piston seizure soon after the initial EDG start.
The EDG lube oil pump functioned satisfactorily.
No loose piston pin bolts were noted and the crankcase oil sample was within specification.
EDG
'A' was declared operable at 1930 on April 12, 1991.
The followind items were replaced during the refueling outage:
5L cylinder liner and piston assembly, SR piston assembly, IL piston assembly, and 5 and 1 rod bearings.
The IL and SR pistons and bushings were reconditioned.
Af ter further analysis of the cylinder SL components associated with the overpressurization incident, the vendor concluded that the overpressurization was caused by stuck piston rings.
Deposits built up behind the rings until the rings were no longer free to move.
Additional deposits forced the compression rings against the liner and significantly reduced lubrication.
The lack of lubrication resulted in ring chatter and increased surf ace temperatures on the piston and liner. As temperatures increased, the chrome plating on the liner cracked and began spalling off.
A piece of chrome plate debris lodged between th niston and liner. The resilting friction caused the piston area around tr icbris to become incandescent, the incandescent area Ignited the crankcase oil vapor causing the crankcase overpressurization (REF:
Cooper Energy Services Materials Laboratory Report ID#1345).
Based on the inspection results of the other cylinders, the stuck ring condition on cylinder SL is considered to be an isolated incident. To ensure that no incipient failure mechanisms are active, however, EDC
'A' will be inspected during the next refueling outage.
During this inspection, at least six pistons will be pulled from a sampling of cylinders.
Liner chrome thickness and piston tin thi.kness will be measured to determine if abnormal l
1
wear is occurring.
Piston rings will be checkad for residue buildup and debris. All cylinders from which the pistons are not removed will be inspected by borescope. Additional pistons will be pulled as necessary based on inspection results. Vaterford 3 intends to have vendor experts assist with the inspections of both EDO
'A' and EDG 'B' to help ensure a most thorough evaluation.
The current surveillance test interval for EDG 'B' is at least once per 31 days.
The current surveillence test interval for EDG ' A' is once every seven days.
These surveillance test interv.ds are in conformance with the schedule of Regulatory Position C.2.d.
The reankcase relief assemblies functioned as designed and EDG 'B" remained operable theoughout the time (nat EDG
'A' was out of service therefore, this event did not present a hazard to the health and safety of the public.
Plant
Contact:
W.R. Brian, Plant Engineering Superintendent, 504/464 3127 l
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