Letter Sequence Response to RAI |
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EPID:L-2020-LLR-0038, Alternative Request IR-4-03 for Use of an Alternative Non-Code Methodology to Demonstrate Structural Integrity of Class 3 Moderate-Energy Piping (Approved, Closed) |
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MONTHYEARML20076A5492020-03-14014 March 2020 Alternative Request IR-4-03 for Use of an Alternative Non-Code Methodology to Demonstrate Structural Integrity of Class 3 Moderate-Energy Piping Project stage: Request ML20075A0322020-03-15015 March 2020 Request for Additional Information (E-mail Dated 3/15/2020) Alternative Request IR-4-03 for Use of an Alternative Non-Code Methodology to Demonstrate Structural Integrity Project stage: RAI ML20076J3722020-03-16016 March 2020 Summary of NRC Verbal Authorization (E-mail Dated 3/16/2020) Alternative Request IR-4-03 for Use of Alternative Non-Code Methodology: Project stage: Other ML20076C8332020-03-16016 March 2020 Response to Request for Additional Information (E-mail Dated 3/16/2020) Alternative Request IR-4-03 for Use of Alternative Non-Code Methodology Project stage: Response to RAI ML20076F3002020-03-16016 March 2020 Follow-on Response to Request for Additional Information (E-mail Dated 3/16/2020) Alternative Request IR-4-03 for Use of Alternative Non-Code Methodology Project stage: Response to RAI ML20189A2062020-07-16016 July 2020 Relief Request IR-4-03 Concerning Non-Code Methodology to Demonstrate Structural Integrity of Class 3 Moderate-Energy Piping Project stage: Approval 2020-03-15
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Category:E-Mail
MONTHYEARML24032A4702024-02-0101 February 2024 Change in Estimated Review Schedule Revision to TS Design Features Section to Remove the Nine Mile Point Unit 3 Nuclear Project, LLC ML24024A0202024-01-24024 January 2024 Correction to Safety Evaluation Associated Wit Amendment No. 288 - Revision to Applicability Term for RCS Heat-Up and Cooldown Pressure-Temperature Limitations Figures ML24024A2452024-01-24024 January 2024 1/24/2024 E-mail from R.Guzman to S.Sinha - Acknowledgement of Error in SE for Amendment No. 288 - Revision to Applicability Term for RCS Heatup and Cooldown Pressure-Temperature Limitations Figures ML23326A0132023-11-22022 November 2023 Acceptance Review Determination LAR to Support Implementation of Framatome Gaia Fuel ML23318A0952023-11-14014 November 2023 Request for Additional Information (E-mail Dated 11/14/2023) LAR to Revise TSs Related to Framatome Gaia Fuel ML23317A0732023-11-13013 November 2023 Acceptance Review Determination - License Amendment Request Modification of TS SR 4.3.6.a ML23297A2312023-10-24024 October 2023 E-mail to File - Summary of September 13, 2023, Meeting with Dominion to Discuss Proposed LAR to Support Cycle Reloads Using Framatome Gaia Fuel ML23265A2302023-09-22022 September 2023 Acceptance Review Determination - License Amendment Request Revision to TS Design Features Section to Remove the Nine Mile Point Unit 3 Nuclear Project, LLC ML23258A0552023-08-31031 August 2023 Setup of Online Reference Portal and Audit Plan for the NRC Staff'S Review of LAR to Use Framatome Small Break and Realistic Large Break LOCA Methodologies (08/31/2023 e-mail) ML23199A2832023-07-18018 July 2023 Request for Additional Information (E-mail Dated 7/18/2023) LAR to Revise the Pressure-Temperature Limits ML23172A0752023-06-21021 June 2023 Acceptance Review Determination LAR to Revise TSs for Reactor Core Safety Limits, Fuel Assemblies, and COLR Related to Framatome Gaia Fuel ML23171B0522023-06-20020 June 2023 NRR E-mail Capture - RAI for Review of Appendix F to DOM-NAF-2-P (Redacted) ML23145A0052023-05-25025 May 2023 Acceptance Review Determination Exemption to Use Framatome Gaia Fuel Assemblies Containing Fuel Rods Fabricated with M5 Fuel Rod Cladding ML23145A0042023-05-25025 May 2023 Acceptance Review Determination LAR to Use Framatome Small Break and Realistic Large Break LOCA Methodologies ML23115A3022023-04-24024 April 2023 4/24/2023 E-mail from R.Guzman to S.Sinha - Acknowledgement of Error in Issuance of Amendments Adoption of TSTF-359, Increase Flexibility in Mode Restraints ML23089A1882023-03-29029 March 2023 Request for Additional Information (E-mail Dated 3/29/2023) Spring 2022 Steam Generator Tube Inspection Report ML23067A2162023-03-0707 March 2023 NRR E-mail Capture - RAI for North Anna, 1 & 2, Surry 1 & 2, Millstone, 2 & 3, Request for Approval of App. F Fleet Report DOM-NAF-2-P, Qual of the Framatome ORFEO-GAIA and ORFEO-NMGRID CHF Correlations in the Dominion VIPRE-D Computer Code ML23038A0152023-02-0707 February 2023 Acceptance Review Determination LAR to Revise the Applicability Term for RCS Heatup and Cooldown Pressure-Temperature Limitations Figures ML23024A1522023-01-24024 January 2023 Acceptance Review Determination LAR to Supplement Burnup Credit of Criticality Safety Analysis ML23018A0352023-01-17017 January 2023 NRR E-mail Capture - Acceptance Review for Fleet Report Re Appendix F of DOM-NAF-2-P (L-2022-LLT-0003) ML22320A5752022-11-16016 November 2022 E-mail to File - Summary of October 18, 2022, Meeting with Dominion to Discuss Requested Actions for Implementing Framatome Gaia Fuel ML22298A2052022-10-25025 October 2022 Acceptance Review Determination for Alternative Request for Extension of Examination Interval for Reactor Pressure Vessel Head Penetration Nozzles ML22292A3212022-10-19019 October 2022 Acceptance Review Determination for Alternative Request for Containment RSS Pump Periodic Verification Testing Program ML22297A1802022-10-0707 October 2022 Email Acknowledgement to Dominion Energy Nuclear Decommissioning Trust Fund Disbursement 30 Day Notification for Millstone Power Station Unit 1: Docket No 50-245 ML22278A0932022-10-0505 October 2022 E-mail to File - Summary of September 7, 2022, Meeting with Dominion to Discuss Proposed Supplement to the Spent Fuel Pool Criticality Safety Analysis (EPID L-2022-LRM-0059 ML22272A0332022-09-29029 September 2022 Memo E-mail to File - Summary of August 29, 2022, Meeting with Dominion to Discuss Proposed Alternative Request Post-peening follow-up Volumetric Exam of RPV Head Penetration Nozzle ML22252A1772022-09-0909 September 2022 Memo E-mail to File - Summary of August 9, 2022, Meeting with Dominion to Discuss Proposed Alternative Reqeust Recirculation Spray Pump Flow Testing (EPID L:2022-LRM-0057) ML22242A0452022-08-23023 August 2022 NRR E-mail Capture - Dominion GL 04-02 Response Draft RAIs (L-2017-LRC-0000) ML22174A3552022-06-23023 June 2022 NRR E-mail Capture - Acceptance Review for Dominion Fleet LAR to Implement TSTF-554 (L-2022-LLA-0078) ML22123A0812022-05-0303 May 2022 Acceptance Review Determination for Proposed LAR for TS Change Applicable to TSTF-359, Increase Flexibility in Mode Restraints ML22069A7192022-03-10010 March 2022 E-mail from R. Guzman to S. Sinha - Millstone Unit 3 Steam Generator Outage Conference Call ML22020A4122022-01-11011 January 2022 1/11/2022 State Consultation E-mail, R. Guzman to J. Semancik Millstone Power Station, Unit 3 Planned Issuance of Amendment to Clarify Shutdown Bank TS and Add Alternate Control Rod Position Monitoring Requirements ML21348A7392021-12-14014 December 2021 E-mail - Acceptance Review Determination Alternative Request IR-4-09 for Use Alternative Brazed Joint Assessment Methodology for Class 3 Moderate Energy Piping ML21347A9412021-12-13013 December 2021 E-mail from R.Guzman to S.Sinha - Acknowledgement of Error in Safety Evaluation for Amendment No. 280 Measurement Uncertainy Recapture Power Uprate ML21334A1922021-11-30030 November 2021 NRR E-mail Capture - Audit Plan for Reactor Core Thermal-Hydraulics Using the VIPRE-D Appendix E Review ML21326A1502021-11-22022 November 2021 NRR E-mail Capture - Acceptance Review for Relocation of Unit Staff Requirements to the QAPD LAR (L-2021-LLA-0195) ML21306A3302021-11-0202 November 2021 NRR E-mail Capture - Acceptance Review for TSTF-569 LAR ML21297A0072021-10-19019 October 2021 E-mail from R. Guzman to S. Sinha - Acknowledgemnt of Error in SE for Millstone Power Station, Unit 3, Amendment No. 279 Addition of Analytical Methodology to the COLR for LBLOCA ML21286A7372021-10-13013 October 2021 Additional Element Included in the Implementation Plan for the Surry Fuel Melt Safety Limit (SL) LAR ML21223A3042021-08-11011 August 2021 Request for Withholding Information from Public Disclosure Proposed LAR to Add an Analytical Methodology to the COLR for a Large Break LOCA ML21200A2562021-07-19019 July 2021 7/19/2021 E-mail Pressurizer Steam Space Line Classification ML21195A2442021-07-13013 July 2021 NRR E-mail Capture - Draft RAI Appendix E to Topical Report DOM-NAF-2 Qualification of the Framatome BWU-I CHF Correlation in the Dominion Energy VIPRE-D Computer Code ML21182A2902021-07-0101 July 2021 7/1/2021 E-mail - Request for Additional Information Alternative Frequency to Supplemental Valve Position Verification Testing Requirements ML21147A2982021-05-27027 May 2021 Correction to Projected Review Completion Date, ASME Section XI Inservice Inspection Program Relief Requests, Limited Coverage Examinations, Third Period, 3rd 10-year Inservice Inspection Interval (EPID L-2020-LLR-0081 to LLR-0088) ML21141A0482021-05-18018 May 2021 5/18/2021 E-mail Proposed License Amendment Request Measurement Uncertainty Recapture Power Uprate ML21112A3082021-04-22022 April 2021 Request for Additional Information (E-mail Dated 4/22/2021) License Amendment Request for Measurement Uncertainty Recapture Power Uprate ML21105A1152021-04-15015 April 2021 Request for Additional Information (e-mail Dated 4/15/2021) Proposed LAR for Addition of Analytical Methodology to the Core Operating Limits Report for a LBLOCA ML21103A0532021-04-13013 April 2021 NRR E-mail Capture - Millstone Unit No. 3 - Acceptance Review Determination: Request for Alternative Frequency to Supplemental Valve Position Indication Verification Testing Requirement ML21084A0042021-03-25025 March 2021 3/25/2021 E-mail, Acceptance Review Determination, Proposed License Amendment Request to Revise Shutdown Bank TS Requirements and Add Alternate Control Rod Position Monitoring Requirements 2024-02-01
[Table view] Category:Response to Request for Additional Information (RAI)
MONTHYEARML23361A0942023-12-21021 December 2023 Response to Request for Additional Information Regarding Proposed License Amendment Request to Revise Technical Specifications for Reactor Core Safety Limits, Fuel Assemblies and Core Operating Limits Report . ML23248A2132023-08-30030 August 2023 Response to Request for Additional Information Regarding Proposed License Amendment Request to Revise the Applicability Term for Reactor Coolant System Heatup and Cooldown Pressure-Temperature. ML23208A0922023-07-26026 July 2023 Request for Approval of Appendix F of Fleet Report DOM-NAF-2-P Qualification of Framatome ORFEO-GAIA and OORFE-NMGRID CHF Correlations in the Dominion Energy Vipre-D Computer Code Response L-04-002, Stations - NRC Generic Letter 2004-02, Potential Impact of Debris Blockage on Emergency Recirculation During Design Basis Accidents at Pressurized-Water Reactors Fleet Response to Request for Additional Information2023-05-0808 May 2023 Stations - NRC Generic Letter 2004-02, Potential Impact of Debris Blockage on Emergency Recirculation During Design Basis Accidents at Pressurized-Water Reactors Fleet Response to Request for Additional Information ML23124A3642023-04-20020 April 2023 Response to Request for Additional Information for Spring 2022 Steam Generator Tube Inspection Report ML23096A2982023-04-0606 April 2023 Units 1 and 2 and Millstone Power Station, Units 2 and 3 - Request for Approval of Appendix F of Fleet Report DOM-NAF-2-P Qualification of the Framatome ORFEO-GAIA and ORFEO-NMGRID CHF Correlations in the Dominion ML22312A4432022-11-0707 November 2022 NRC Generic Letter 2004-02, Potential Impact of Debris Blockage on Emergency Recirculation During Design Basis Accidents at Pressurized-Water Reactors Fleet Response to RAI ML21259A0852021-09-15015 September 2021 North Ann, and Surry, Units 1 and 2, Millstone, Units 2 and 3, Request for Approval of Appendix E of Fleet Report DOM-NAF-2-A Qualification of the Framatome BWU-I CHF Correlation in the Vipre-D Computer Code Response to Request for Addition ML21209A7622021-07-26026 July 2021 Response to Request for Additional Information for Alternative Request V-01 - Proposed Request for Alternative Frequency to Supplemental Valve Positionn Verification Testing Requirements ML21153A4132021-06-0202 June 2021 Response to Request for Additional Information Regarding License Amendment Request for Measurement Uncertainty Recapture Power Uprate ML21147A4772021-05-27027 May 2021 NRC Generic Letter 2004-02, Potential Impact of Debris Blockage on Emergency Recirculation During Design Basis Accidents at Pressurized-Water Reactors - Final Supplemental Response ML21140A2992021-05-20020 May 2021 Response to Request for Additional Information for Proposed License Amendment Request to Add an Analytical Methodology to the Core Operating Limits Report for a Large Break Loss of Coolant Accident ML21133A2852021-05-13013 May 2021 Stations, Units 1 & 2 and Millstone Power Station, Units 2 and 3 - Request for Approval of Appendix E Fleet Report DOM-NAF-2-A Qualification of the Framatome Bwui CHF Correlation in the Dominion Energy VIPRE-D Computer Code ML21105A4332021-04-15015 April 2021 Final Supplemental Response to NRC Genetic Letter 2004-02 on Potential Impact of Debris Blockage on Emergency Recirculation During Design Basis Accident at Pressurized-Water Reactors ML21105A4822021-04-15015 April 2021 Response to Request for Additional Information for Proposed License Amendment Request to Revise the Millstone, Unit 2 Technical Specification for Steam Generator Inspection Frequency ML21081A1362021-03-19019 March 2021 Response to Request for Additional Information for Alternative Request RR-05-06 - Inspection Interval Extension for Steam Generator Pressure-Retaining Welds and Full-Penetration Welded Nozzles ML20274A3462020-09-30030 September 2020 Response to Request for Additional Information for License Amendment Request to Revise Battery Survillance Requirements ML20261H5982020-09-17017 September 2020 Response to Request for Additional Information for License Amendment Request to Revise Technical Specification Table 3.3-11, Accident Monitoring Instrumentation ML20252A1912020-09-0404 September 2020 Response to Request for Additional Information Regarding License Amendment Request for a One-Time Deferral of the Millstone Unit 3 Steam Generator Inspections ML20209A5362020-07-27027 July 2020 Response to Request for Additional Information Regarding Relief Request IR-3-33 for Limited Coverage Examinations Performed in the Second Period of the Third 10-Year Inspection Interval ML20079K4242020-03-19019 March 2020 Response to Request for Additional Information for License and Request to Revise TS 3.8.1.1, A.C Sources - Operating, to Support Maintenance and Replacement of the Millstone Unit 3 'A' Reserve Station Service Transformer and 345 Kv South Bu ML20076C8332020-03-16016 March 2020 Response to Request for Additional Information (E-mail Dated 3/16/2020) Alternative Request IR-4-03 for Use of Alternative Non-Code Methodology ML20048A0192020-02-11011 February 2020 Response to Request for Additional Information for License Amendment Request to Revise TS 3.8.1.1, A.C. Sources - Operating, to Support Maintenance and Replacement of a Reserve Station Service Transformer and 345 Kv South Bus. ML20042D9962020-02-10010 February 2020 Response to March 12, Request for Information Enclosure 2, Recommendation 2.1, Flooding Focused Evaluation/Integrated Assessment Submittal ML19284A3972019-10-0303 October 2019 Response to NRC Request for Additional Information on License Amendment Request to Adopt 10 CFR 50.69 ML19249B7672019-08-29029 August 2019 Enclosure 1 - Millstone, Units 2 and 3 and ISFSI; North Anna, Units 1 and 2 and ISFSI; and Surry, Units 1 and 2 and ISFSI - Response to EAL Scheme Change RAIs ML19092A3322019-03-27027 March 2019 Response to Request for Additional Information for Proposed Technical Specification Changes for Spent Fuel Pool Storage and New Fuel Storage ML19011A1112018-12-18018 December 2018 Supplement to the Flooding Hazard Reevaluation Report in Response to 50.54(F) Information Request Regarding Near-Term Task Force Recommendation 2.1: Flooding ML18340A0282018-11-29029 November 2018 Response to Request for Additional Information for Proposed Technical Specifications Changes for Spent Fuel Pool Storage and New Fuel Storage ML18302A1202018-10-22022 October 2018 Response to Request for Additional Information for License Amendment Request to Revise the Technical Specification for Control Building Ventilation Inlet Instrumentation ML18235A3212018-08-17017 August 2018 Response to Request for Additional Information for Proposed Alternative Request P-06 for 'C' Charging Pump ML18225A0662018-08-0606 August 2018 Response to Request for Additional Information for Alternative Requests Associated with the In-Service Testing Program for Pumps, Valves, and Snubbers Fifth and Fourth 10-Year Interval Updates ML18205A1762018-07-19019 July 2018 Response to Request for Additional Information for Alternative Requests Associated with the In-Service Testing Program for Pumps, Valves, and Snubbers Fifth and Fourth 10-Year Interval Updates for Units 2 and 3 ML18170A0932018-06-14014 June 2018 Response to Request for Additional Information Regarding License Amendment Request to Revise Integrated Leak Rate Test (Type a) and Type C Test Intervals ML18151A4672018-05-24024 May 2018 Response to Request for Additional Information Regarding License Amendment Request to Revise Integrated Leak Rate Test (Typed a) and Type C Test Intervals ML17338A0572017-11-22022 November 2017 Response to Request for Supplemental Information Regarding Generic Letter 2016-01, Monitoring of Neutron-Absorbing Materials in Spent Fuel Pools ML17300A2202017-10-24024 October 2017 Response to Information Need Request Regarding Mitigating Strategies Assessment (MSA) Report for Flooding ML17053A1062017-02-16016 February 2017 Response to Request for Additional Information Regarding Proposed Alternative Requests RR-04-24 and IR-3-30 for Elimination of the Reactor Pressure Vessel Threads in Flange Examination ML17038A0052017-01-31031 January 2017 Response to RAI Regarding End of Cycle 23 and End of Cycle 17 Steam Generator Tube Inspection Reports, CAC MF8507 & MF8506 ML16365A0362016-12-22022 December 2016 Response to March 12, 2012 Information Request High Frequency Sensitive Equipment Functional Confirmation for Recommendation 2.1 ML16365A0322016-12-21021 December 2016 Response to March 12, 2012 Information Request, Spent Fuel Pool Seismic Evaluation for Recommendation 2.1 ML16321A4542016-11-10010 November 2016 Connecticut and Virginia Electric & Power Company Response to Request for Additional Information Revision 22 of Quality Assurance Program Description Topical Report ML16312A0642016-11-0101 November 2016 Units 1 & 2, Surry, Units 1 & 2, Response to Generic Letter 2016-01, Monitoring of Neutron-Absorbing Materials in Spent Fuel Pools ML16294A2702016-10-18018 October 2016 Response to Request for Additional Information for License Amendment Request Regarding Realistic Large Break Loss of Coolant Accident Analysis - RAI Questions 1 Through 3 ML16291A5082016-10-12012 October 2016 Response to Follow Up Request to Revise ECCS TS 3/4.5.2 and FSAR Chapter 14 to Remove Charging ML16202A0402016-07-14014 July 2016 Response to Request for Additional Information Regarding Spent Fuel Pool Heat Load Analysis License Amendment Request ML16188A1962016-06-30030 June 2016 NRC Regulatory Issue Summary 2016-09 Preparation and Scheduling of Operator Licensing Examinations ML16182A0372016-06-27027 June 2016 Response to Request for Additional Information for License Amendment Request to Revise ECCS TS 3/4.5.2 and FSAR Chapter 14 to Remove Charging ML16159A2382016-06-0101 June 2016 Isfsis, Response to NRC Request for Information Security Plan, Training and Qualification Plan, Safeguards Contingency Plan and ISFSIs Security Program, Rev. 21 ML16148A7012016-05-20020 May 2016 Response to Request for Additional Information Regarding ASME Section XI Inservice Inspection Program Relief Requests for Limited Coverage Examinations Performed in the Fourth 10-Year Inspection Interval 2023-08-30
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From: Shayan.Sinha@dominionenergy.com To: Guzman, Richard
Subject:
[External_Sender] RE: Millstone Unit 3 - REQUEST FOR ADDITIONAL INFORMATION: Alternative Request IR 03 For Use of an Alternative Non-Code Methodology to Demonstrate Structural Integrity [EPID: L-2020-LLR-0038]
Date: Monday, March 16, 2020 1:02:51 PM Attachments: Attachment to RAI for RR IR-4-03 (SN 20-110) MPS3 Service Water Piping-weld Sketch.pdf
- Rich, Please find DENCs response below:
DENC Serial Number 20-110 Request for Additional Information for RR IR-4-03 NRC RAI question In the licensees relief request under Compensatory Actions, it states that ultrasonic testing (UT) will be used to verify that the degradation of the piping base metal adjacent to and under the reinforcement pad fillet weld and the reinforcing pad base metal is within the bounds of the structural integrity determination provided in Attachment 2. Please define the acceptance criteria which will be used for the UT examinations as described in your compensatory actions. Please clarify that if the structural integrity determination does not meet the bounds of the analysis, the licensee will repair the location in accordance with the ASME Code immediately.
DENC Response An acceptance criterion of 0.215 inches is being applied to the UT thickness measurements for each of the following components: the reinforcing pad, branch pipe, and main pipe. The acceptance criterion was determined by recalculation of the Code stress equations for an increased unreinforced tee stress intensity factory (SIF), per ASME Code Section III figure NC 3672.9(a)-1. The acceptance criterion of 0.215 inches is based on the weld thickness which is most limiting. Should UT measurements determine any thickness less than that analyzed in Attachment 2, the A train of Service Water will be declared inoperable.
NRC RAI question Please provide a sketch which provides the location of the portion of joint that will be monitored by UT for structural integrity. Identify the potential leak paths, system water flow, and areas to be examined by UT as part of your compensatory actions.
DENC Response Attached is a sketch of typical reinforced Branch to Pipe connections including the potential leak paths, system water flow and areas to be examined by UT.
The circumference of the main pipe and branch pipe have been and will continue to be scanned using a zero-degree transducer from the toe of the fillet weld outward over a two-inch wide band.
The integrity of the base metal under the main pipe and branch pipe to reinforcing pad fillet welds has been and will continue to be evaluated using a 70-degree angle beam transducer scanning perpendicular to the fillet weld. For the main pipe, this examination covers approximately 2 inches of piping base metal that extends under the reinforcing pad.
For the branch pipe, the angle beam exam covers the base metal under the fillet weld to the butt weld joining the branch run to the main run. These angle beam exams are informational and intended to assist in locating degradation. Angle beam cannot be used to quantify material thickness. The determination of acceptability is based on the zero-degree UT reading for degradation extending beyond the toe of the reinforcement pad to fillet welds.
The zero degree and 70-degree examinations performed on the main piping cover all but approximately 16 inches of the circumference of the pipe. This limitation occurs where the main run flange proximity to the branch run piping limits access.
The reinforcing pad integrity is evaluated using a zero-degree transducer at selected locations across the reinforcing pad.
From: Guzman, Richard <Richard.Guzman@nrc.gov>
Sent: Sunday, March 15, 2020 7:15 PM To: Shayan Sinha (Services - 6) <Shayan.Sinha@dominionenergy.com>
Subject:
[EXTERNAL] Millstone Unit 3 - REQUEST FOR ADDITIONAL INFORMATION: Alternative Request IR-4-03 For Use of an Alternative Non-Code Methodology to Demonstrate Structural Integrity [EPID: L-2020-LLR-0038]
- Shayan, The NRC staff is reviewing the information provided in the subject alternative request dated March 14, 2020, and has determined that additional information is needed to complete its review. Shown below is the NRC staffs request for additional information (RAI) question.
Please provide your response as soon as possible, in support of DENCs requested approval date as specified in the submittal. Please contact me if you have any questions.
~~~~~~~~~~~~
Rich Guzman Sr. PM, Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation U.S. Nuclear Regulatory Commission Office: O-9C7 l Phone: (301) 415-1030 Richard.Guzman@nrc.gov REQUEST FOR ADDITIONAL INFORMATION (RAI)
DOMINION ENERGY NUCLEAR CONNECTICUT, INC.
MILLSTONE POWER STATION, UNIT 3 ALTERNATIVE REQUEST IR-4-03 FOR USE OF AN ALTERNATIVE NON-CODE METHODOLOGY TO DEMONSTRATE STRUCTURAL INTEGRITY OF CLASS 3 MODERATE-ENERGY PIPING DOCKET NO. 50-423 By letter dated March 14, 2020, Dominion Energy Nuclear Connecticut, Inc. (Dominion, the licensee) submitted relief request (RR) IR-4-03, to use a non-code methodology in lieu of repair allowed by the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code,Section XI, IWA-4000, in order to address a through-wall leak in a reinforced branch connection of the service water system at Millstone Power Station, Unit 3 (Millstone 3). Specifically, the licensee requested NRC verbal authorization of the alternate method for evaluating structural integrity of the through-wall leak condition identified on the Millstone 3 A train service water header. The NRC staff is reviewing the submittal and has determined that additional information as requested below is needed to support completion of its review.
Request for Additional Information for RR IR-4-03 In the licensees relief request under Compensatory Actions, it states that ultrasonic testing (UT) will be used to verify that the degradation of the piping base metal adjacent to and under the reinforcement pad fillet weld and the reinforcing pad base metal is within the bounds of the structural integrity determination provided in Attachment 2. Please define the acceptance criteria which will be used for the UT examinations as described in your compensatory actions. Please clarify that if the structural integrity determination does not meet the bounds of the analysis, the licensee will repair the location in accordance with the ASME Code immediately.
Please provide a sketch which provides the location of the portion of joint that will be monitored by UT for structural integrity. Identify the potential leak paths, system water flow, and areas to be examined by UT as part of your compensatory actions.