ML20065T721
| ML20065T721 | |
| Person / Time | |
|---|---|
| Site: | Kewaunee |
| Issue date: | 02/29/1980 |
| From: | Ruiter G WISCONSIN PUBLIC SERVICE CORP. |
| To: | |
| Shared Package | |
| ML20065T713 | List: |
| References | |
| NUDOCS 8211020663 | |
| Download: ML20065T721 (4) | |
Text
.
Docket 50-305 p
KEWAUNEE NUCLEAR POWER PLANT
SUMMARY
OF OPERATING EXPERIENCE FEBRUARY, 1980 On February 3, a solenoid valve failure on IB main feedwater OPERATIONS:
control valve air system caused the valve to shut resulting The in a low steam generator water level reactor trip.
unit was returned to service the same day.
Repaired and recalibrated some boric acid heat tracing MAINTENANCE:
temperature controllers.
Adjusted steam driven auxiliary feedwater pump governor linkage to provide proper speed control.
4 Repaired CC system and a CVC system pipe leak.
Modified some seismic hangers on service water piping.
Modified some hangers on RHR piping.
Repaired leaking main steam controlled relief valve.
Rebuilt a charging pump.
Repaired a knife switch in a diesel generator supply circuit breaker.
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8211020663 800310 PDR ADOCK 05000305 R
4 AYERAGE DAILY UNIT P0W ER LEYEL D3 C EET NO-50-305 UNIT-KEWAUNEE COMPLETED DY-G. H. RUITER TELEPHONE-414-388-2560 I207 l
REPORT MONTH FEBRUARf, 1900 AVERAGE DAILY DAY POWEB LEVEL
526
{
3 224 4
513 5
526 6
527 7
527 8
526 i
9 530 i
10 527 11 526 12 526 13 525 14 526 15 526 16 526 17 526 4
18 525 l
19 526 20 530 i
21 527 22-52G 23 530 24 525 25 526 t
26 526 27 531 28 527 o
0 29 526 l
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D3CKET NO-50-305 C03PLETED BY-G.
H.
RUITER OPZR ATI NG STATUS TYLEPHONE-414-388-2560 %207 j
1 UNIT N A ME KEWAUNEE
- h***********************************
2 REPORTING PERIOD FE390 ART, 1900
- NOTES Unrestricted unit operations with the exception of one unscheduled v
3 LICENSED THERM AL POWER (MWT) 1650
- outage as noted.
4 NA9EPLATE RATING (GROSS NUE) 560 v
5 DESIGN ELECTRICAL RATING (NT.T 4WE) 535 e
6 3AXIM93 D9PENDABLE CAPACITY (GROSS MW E) 545 7 MAXIMU M DS PEND ADLE CAP ACIT'T (NET MWE) 576 4
S IT CHANGES CCCUB IN CAPACITT RATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT, GIVE REASONS None b
s 9 POW ER L EVEL TO THICH R ESTPICTED, IF ANY (NET MWE) None 10 REASONS FOR RESTRICTIONS, IF ANT N/A b
THIS MONTH TR-TO-DITE CUMULATIVE b
11 HOURS IN DEPORTING PERIOD 69G 1440 50041 12 NU3BER OF HOURS REACTOR WAS CRITICAL 693.0 1173.0 42175.5 l
13 REACTOR RESERVE SHUTDOV9 HOURS 0.0 152.7 2330.5 la HOUPS GENER ATOP ON-LINF.
691.9 1155.8 41151.6 b
15 UNIT RESERVE SUTDOEN HOURS 0.0 0.0 10.0 4i 16 GROSS THER 3 AL ENERGY GENER ATED (M F't) 1124015 1837940 62989071
]
17 GROSS ELECTRICAL ENERGY GENESATPD (MW H) 375G00 612500 20796300 l
18 NET ELECTRICAL ENERGI GEMBR ATED (MW R) 359111 504991 19784069
/
19 UNIT SERVICE FACTOR 99.4 00.3 82.3
-} %,
20 UNIT AV AIL ABILITY FACTOR 99.4 00.3 82.2 i
21 UNIT CAPACITY F ACTOR (USING MDC NET) 90.1 77.2 75.4 j
'A 22 UNIT CAPACITY FACTOR (USING DER MET) 96.4 75.9 73.9
! s, l
23 UNIT FDECED OUT AGE R ATE 0.6 19.7
- 5. 8
~
V 24 SHUTDOW NS SCHEDULED OVER NEXT 6 MONTHS (TIPE, DATE, AND DURATION OF EACH) l Petueling; May 10, 1980; six weeks
%w 25 IF SHUT DOWN AT END OF RPPORT PERIOD, ESTIPATED D4TE OF STARTOP - N/A 1
-m.
=
..E UNIT S HUTD00N5 A5D POV ER REDDCTIONS e'
DOCKET NO: 50-305 DNIT NAME: Kevaunee DATE: March 1, 1980 I
COMPLETED BY:
G.
H.
Ruiter TELEPHONE: 414-388-2560 x207 REPORT MONTH - FEBRUARY, 1?80 l
(JANUARY DATA REPEATED THIS MONTH TO INDICATE LER NU5BER 80-002)
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NO. l DATE iTYPE l DURATION lBEASONl METHOD l LER NUBBER lSYS l COMPONENT l COMMENTS l
4 il i
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. 1 I
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't 1 1 1/ 4/801 F i 15.4 i A 1 3 i
N/A I EB 1 ELECON l
1.
Bus fault from Main A uxiliary transformer [
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resulted in a turbine / reactor trip..
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4
- l 21 1 1/17/801 F i 158.7 l A I 3 1
80-002 1 EB 1 TRANSF I 2a. Bushing failure in Reserve Auxiliary I il I
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transformer caused loss of power to ' all but 1 I
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i safeguards busses.
Unit trip followed i I
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I 2h I I F i 106.0 l A I 4 i
N/A l CB i B ECFU M i 2b. Apparent failure of No.
2 seal on 1B RCP I
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I extended this outage.
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N/A I HH I YALTOP l 3.
Solenoid valve failure on 18 main feedwater I I
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l control valve air system caused the valve to l I
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I shut resulting in a low steam generator water I i 1.
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1 level, reactor trip.
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TYPE-REASON M ETHO D SYSTER & COMPONENT CODES fl F3 Forced A-Equlpaent Failure (Explain) 1-Manual From NUREG-0161 2-Manual Scras St Scheduled B-Maintenance or Test C-Re fue ling J-Automatic Scram 4
D-Regulatory Bestriction 4-Continuations E-operator Training C License Examination 5-load Reductions F-Administrative 9-Other i
1 G-operational Error (Explais)
.I 0-@thes REnfpBaBnD.