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NRC r d 3ee u.$. NUCLEAR LEIULATORY COMMISSION APPROVEO OMe NO. 31So4to4 Ecl2ES. S/3086 LICENSEE EVENT REPORT (LER)
FACILITV NAME (1) e DOCKET NUMBER (2)
PAuf G Waterford Steam Electric Station Unit'3 015 l 010 l o l 31812 1 lOFl013 TITLE to)
Reactor Trip on Dropped Control Element Assemb1v EVENT DATE (8)
LER NUMSER 48)
REPORT DATE (7)
OTHER FACILITIES INVOLVED (8)
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MONTH DAY YEAR FActLITV N AMEs DOCKET NUM8ER($l MONTH DAY YEAR YEAR N/A 0l5l0l0l0l l l 0l1 0l7 8
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NAME TELEPHONE NUMBER AREA CODE T. Smith, Maintenance Superintendent 51 014 41614I-1 3111318 COMPL ETE ONE LINE FOR EACH COMPONENT PAILURE DESCRISED IN THl3 REPC817 H3)
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I I I I I I SUPPLEMENTAL REPORT EXPECTED (14)
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w osi ABSTRACT At 1452 hours0.0168 days <br />0.403 hours <br />0.0024 weeks <br />5.52486e-4 months <br /> on January 7, 1986 Waterford Steam Electric Station Unit 3 was operating at 100% reactor power for the previous 14 days when a reactor trip occurred on low Departure from Nucleate Boilire Ratio (DNBR). Upon stabilizing plant conditions in mode 3 (hot standby), operations personnel attributed the reactor trip to the inadvertent dropping of Control Element Assembly 31.
Due to the penalty factors associated with this Control Element Assembly, the Core Protection Calculators (EIIS System Code AA) initiated a low DNBR trip.
The event has been attributed to a faulty Automatic Control Element Assembly Calculator Timing Module (EIIS Component Code TMR). Troubleshooting failed to detect any anomallies within the card; however, the card has been sent to Combustion Engineering for evaluation.
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r U S. NUCLEA3 OtiULJ. TORY COMMISSION aC Form 304A LICENSEE EVENT REPORT (LER) TEXT C2NTINUAT13N APr ovEo OMS No am-cio.
E MPIRES 8/31/86 FACILITY NAmt (H DOCKET feUMSER (28 LtR NUMGER 86)
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vtAR W:terford Steam Electric Station Unit 3 0 l5 l0 [o l0 l3 l8 l 2 8l6 0 l 0] 1 0l0 Ol2 0F 0 l3 TEXT (# more space e segured, ese aesponst N#C Form Jssrs)im
NARRATIVE
At 1452 hours0.0168 days <br />0.403 hours <br />0.0024 weeks <br />5.52486e-4 months <br /> on January 7, 1986 Waterford Steam Electric Station Unit 3 was operating at 100% reactor power for the previous 14 days when a reactor trip occurred on low Departure from Nucleate Boiling Ratio (DNBR) (The signal emanates from the' Core Protection Calculators, EIIS System Code JC.).
Upon receiving the reactor trip, operations personnel entered procedures OP-902-000,
" Emergency Entry Procedure" and OP-902-001, " Uncomplicated Reactor Trip Recovery Procedure". Plant conditions were subsequently stabilized in mode 3 (hot standby).
An investigation immediately following the trip indicated that Control Element Assembly 31 (part length rod) (EIIS System Code AA) may have inadvertently fallen into the core. Due to the design of the Core Protection Calculators, a sufficiently large penalty factor was generated to trip the unit.
SAFETY CONSEQUENCES AND IMPLICATIONS
l The above event resulted in an actuation of the Reactor Protettive System in which no primary system parameters were exceeded. Since the Con *.rol Element Assemblies and the Reactor Protective System (EIIS System Code JC) functioned as designed, the event in no way placed Waterford 3 in a degraded safety condition.
CORRECTIVE ACTION
~
An investigation indicated the reactor trip was due to the inadvertent dropping of Control Element Assembly 31.
It is suspected that the dropped rod was due to a faulty Automatic Control Element Assembly Calculator Timing Module (The ACTM card monitors and analyzes electrical currents within the Control Rod Drive NTC FOIM 364A C $3D
u s. =uctfi.a (Etut*ToRv coMMissiou ge ma LICENSEE EVENT REPORT (LER) TEXT CONTINUATION 4eeaovf o oue so. mo-om E XPiR Es. 8'31185 FaCILITV NAME (1)
DOCKET NUMEER (2)
LER NUMSER (6)
PaGE (3)
YEAR v ea u ea Utterford Steam Electric Station Unit 3 0 l5 l 0 l 010 l 318 l 2 816 0 l 0l 1 Ol0 0l3 0F 0l3 TEXT ## more space a reeumt, use a#prM NAC Forrn J66A sJ (17)
Mechanism) (EIIS Component Code TMR); however, an inspection of the card did not reveal any signs of damage.
In addition, maintenance personnel monitored coil currents within the system. The results of this test proved satisfactory.
The subject card was replaced on January 23, 1986 and sent to Combustion Engineering for evaluation.
SIMILAR EVENTS
None PLANT CONTACT T. Smith, Maintenance Superintendent, 504/464-3138.
NEC FOCM 366a
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- NEW ORLEANS, LOUISIANA 70174. (SO4) 366-2345 U $ N iYSSE February 6, 1986 W3P86-0024 A4.05 QA Director, Office of Nuclear Reactor Regulation ATTENTION: Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555 Subject: Waterford 3 SES Docket No. 50-382 License No. NPF-38 Reporting of Licensee Event Report
Dear Sirs:
Attached is Licensee Event Report Number LER-86-001-00 for Waterford 3.
This Licensee Event Report is submitted per 10CFR50.73(a)(2)(iv).
Very truly yours, m
c/
K.W. Cook Nuclear Support & Licensing Manager KWC:GEW:sms Attachment i
cc:
R.D. Martin, G.W. Knighton, J.H. Wilson, NRC Resident Inspectors Office, INPO Records Center (J.T. Wheelock), B.W. Churchill, W.M. Stevenson Sr 9
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| 05000382/LER-1986-001, :on 860107,reactor Trip Occurred on Dropped Control Element Assembly (Cea).Caused by Faulty Automatic CEA Calculator Timing Module.Card Replaced on 860123 & Sent to C-E for Evaluation |
- on 860107,reactor Trip Occurred on Dropped Control Element Assembly (Cea).Caused by Faulty Automatic CEA Calculator Timing Module.Card Replaced on 860123 & Sent to C-E for Evaluation
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000382/LER-1986-002, :on 860122,control Element Assembly 88 Dropped Into Core,Precipitating Reactor Trip.Caused by Not Turning on Fan Blower Toggle Switch & Isolation Valves Failing to Open.Procedure Changed Re Gag Removal |
- on 860122,control Element Assembly 88 Dropped Into Core,Precipitating Reactor Trip.Caused by Not Turning on Fan Blower Toggle Switch & Isolation Valves Failing to Open.Procedure Changed Re Gag Removal
| 10 CFR 50.73(a)(2)(1) | | 05000382/LER-1986-003, :on 860124,0204 & 09,inadvertent Actuations of ESF Portion of Control Room Ventilation Sys Occurred.Caused by Technician Bumping Monitor,Electrical Spike & Chlorine Detector Alarm.Caution Signs Posted |
- on 860124,0204 & 09,inadvertent Actuations of ESF Portion of Control Room Ventilation Sys Occurred.Caused by Technician Bumping Monitor,Electrical Spike & Chlorine Detector Alarm.Caution Signs Posted
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000382/LER-1986-004, :on 860314,LPSI Pump B Discharge Valve Found Closed W/Danger Tag Affixed.Caused by Personnel Error.Valve Opened.Procedure UNT-5-003 Revised to Stress Function of Clearance Sheets |
- on 860314,LPSI Pump B Discharge Valve Found Closed W/Danger Tag Affixed.Caused by Personnel Error.Valve Opened.Procedure UNT-5-003 Revised to Stress Function of Clearance Sheets
| | | 05000382/LER-1986-005, :on 860318,during Mode 5,Surveillance Procedure OP-903-013 Error Resulted in Hot Leg Temp Accident.Caused by Suspect Monitoring Instrument Operability.Procedure Changed |
- on 860318,during Mode 5,Surveillance Procedure OP-903-013 Error Resulted in Hot Leg Temp Accident.Caused by Suspect Monitoring Instrument Operability.Procedure Changed
| 10 CFR 50.73(a)(2)(i) | | 05000382/LER-1986-006, :on 860322,discovered Weekly Surveillance for Inservice Boric Acid Makeup Tank a (Cb) Not Performed Since 860310.Caused by Lack of Sufficient Means to Track Numerous Surveillances |
- on 860322,discovered Weekly Surveillance for Inservice Boric Acid Makeup Tank a (Cb) Not Performed Since 860310.Caused by Lack of Sufficient Means to Track Numerous Surveillances
| 10 CFR 50.73(a)(2)(1) | | 05000382/LER-1986-007, :on 860406,fire Watch Tour for Fire Impairment 85-232 Not Satisfactorily Performed.Caused by Misnumbered Pages in Fire Watch Log.Responsibilities for Handling Logs Posted |
- on 860406,fire Watch Tour for Fire Impairment 85-232 Not Satisfactorily Performed.Caused by Misnumbered Pages in Fire Watch Log.Responsibilities for Handling Logs Posted
| 10 CFR 50.73(a)(2)(i) | | 05000382/LER-1986-008, :on 860504 & 10,emergency Feedwater Actuation Signals Occurred.Caused by Failure of Reactor Operator to Remove Bypass on Hi Steam Generator 2 Delta P Bistable for Channel A.Surveillance Procedure Revised |
- on 860504 & 10,emergency Feedwater Actuation Signals Occurred.Caused by Failure of Reactor Operator to Remove Bypass on Hi Steam Generator 2 Delta P Bistable for Channel A.Surveillance Procedure Revised
| | | 05000382/LER-1986-009, :on 860509,while Operating at 100% Power, Uncomplicated Reactor Trip Occurred.Caused by Failure of Reed Switch on Control Element Assembly 35.Faulty Switch Replaced & Assembly Calculator Returned to Svc |
- on 860509,while Operating at 100% Power, Uncomplicated Reactor Trip Occurred.Caused by Failure of Reed Switch on Control Element Assembly 35.Faulty Switch Replaced & Assembly Calculator Returned to Svc
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000382/LER-1986-010, :on 860602,secondary Coolant Sys Not Sampled for Specific Activity as Required by Tech Specs.Caused by Personnel Error.Surveillance Rescheduled to Specific Day of Wk |
- on 860602,secondary Coolant Sys Not Sampled for Specific Activity as Required by Tech Specs.Caused by Personnel Error.Surveillance Rescheduled to Specific Day of Wk
| | | 05000382/LER-1986-011-01, Forwards LER 86-011-01,revised Per Determination That Deviations to App R Requirements for Fire Barriers w/228 Seals Identified to Have Sleeve Type Configuration as Described in LER Not Required | Forwards LER 86-011-01,revised Per Determination That Deviations to App R Requirements for Fire Barriers w/228 Seals Identified to Have Sleeve Type Configuration as Described in LER Not Required | | | 05000382/LER-1986-012, :on 860625,discovered That Surveillance for Fire Doors D221 & D222 Not Performed on Daily Basis.Caused by Lack of Interdepartmental Communication.Procedure OP-903-001 Revised |
- on 860625,discovered That Surveillance for Fire Doors D221 & D222 Not Performed on Daily Basis.Caused by Lack of Interdepartmental Communication.Procedure OP-903-001 Revised
| 10 CFR 50.73(a)(2)(i) | | 05000382/LER-1986-013, :on 860630,reactor Trip & Low DNBR Ratio & Emergency Feedwater Activation Occurred.Caused by Unlocked Cable Connector for Control Element Assembly 35.Maint Personnel Revised Procedure MI-13-523 |
- on 860630,reactor Trip & Low DNBR Ratio & Emergency Feedwater Activation Occurred.Caused by Unlocked Cable Connector for Control Element Assembly 35.Maint Personnel Revised Procedure MI-13-523
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000382/LER-1986-014, :on 860710,maint Personnel Inadvertently Opened Safety Injection Tank 1B & 2B Isolation Valves.Caused by Inadequate Work Instructions.Personnel Will Be Prevented from Disconnecting Leads While Performing Work |
- on 860710,maint Personnel Inadvertently Opened Safety Injection Tank 1B & 2B Isolation Valves.Caused by Inadequate Work Instructions.Personnel Will Be Prevented from Disconnecting Leads While Performing Work
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000382/LER-1986-015, :on 860714,loss of Shutdown Cooling Occurred. Caused by Simultaneous Use of Methods of Draining RCS & Inaccurate Level Indication.Procedures OP-1-003 & OP-901-046 Revised |
- on 860714,loss of Shutdown Cooling Occurred. Caused by Simultaneous Use of Methods of Draining RCS & Inaccurate Level Indication.Procedures OP-1-003 & OP-901-046 Revised
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000382/LER-1986-016, :on 860804 & 21,boron Concentration for Safety Injection Tanks Fell Below Tech Spec Limit.Caused by Insufficient Procedural Requirements.Procedure Change Will Be Made to Prevent Recurrence |
- on 860804 & 21,boron Concentration for Safety Injection Tanks Fell Below Tech Spec Limit.Caused by Insufficient Procedural Requirements.Procedure Change Will Be Made to Prevent Recurrence
| 10 CFR 50.73(a)(2)(1) | | 05000382/LER-1986-017, :on 860811,chemistry Technicians Failed to Sample Proper Gas Decay Tank.Caused by Operations Personnel Realigning Inservice Tanks W/O Informing Chemistry Technicians.Procedure Revised |
- on 860811,chemistry Technicians Failed to Sample Proper Gas Decay Tank.Caused by Operations Personnel Realigning Inservice Tanks W/O Informing Chemistry Technicians.Procedure Revised
| 10 CFR 50.73(a)(2)(1) | | 05000382/LER-1986-018, :on 860903,seismically Unqualified Power Supply Panel for Hydrogen Recombiner Discovered.Caused by Absence of Structural Weld.Outside Foundation Weld Installed.W/ |
- on 860903,seismically Unqualified Power Supply Panel for Hydrogen Recombiner Discovered.Caused by Absence of Structural Weld.Outside Foundation Weld Installed.W/
| 10 CFR 50.73(a)(2)(i) | | 05000382/LER-1986-019, :on 860909,during Full Power,Reactor Tripped Due to Turbine Trip.Caused by Alternate Drain Valve Failure Resulting in hi-hi Level in Moisture Separator Reheater Shell Drain Tank 2.Valve Reworked |
- on 860909,during Full Power,Reactor Tripped Due to Turbine Trip.Caused by Alternate Drain Valve Failure Resulting in hi-hi Level in Moisture Separator Reheater Shell Drain Tank 2.Valve Reworked
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000382/LER-1986-020, :on 860915,18 & 1002,ESF Portion of Control Room Ventilation Sys Actuated Inadvertently.Caused by Electrical Spikes in Control Room Outside Air Intake Radiation Monitors.Evaluation Continuing |
- on 860915,18 & 1002,ESF Portion of Control Room Ventilation Sys Actuated Inadvertently.Caused by Electrical Spikes in Control Room Outside Air Intake Radiation Monitors.Evaluation Continuing
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000382/LER-1986-021, :on 860924,hourly Firewatch Tour Not Performed in Shutdown Cooling HX Room B.Caused by Personnel Error.Post Order for Firewatch Patrol Revised |
- on 860924,hourly Firewatch Tour Not Performed in Shutdown Cooling HX Room B.Caused by Personnel Error.Post Order for Firewatch Patrol Revised
| 10 CFR 50.73(a)(2)(4) | | 05000382/LER-1986-022, :on 861020,control Room Isolation Occurred. Caused by Degraded Electrical Connection in Barton Model 765 Flow Transmitter.Transmitter Replaced |
- on 861020,control Room Isolation Occurred. Caused by Degraded Electrical Connection in Barton Model 765 Flow Transmitter.Transmitter Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000382/LER-1986-023, :on 861020,reactor Tripped Coincident W/ Emergency Feedwater Actuation.Caused by Dropped Control Element Assembly Due to Failed Lower Gripper Hall Effect Sensor on Assembly 21.Sensor Replaced |
- on 861020,reactor Tripped Coincident W/ Emergency Feedwater Actuation.Caused by Dropped Control Element Assembly Due to Failed Lower Gripper Hall Effect Sensor on Assembly 21.Sensor Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000382/LER-1986-024, :on 861021,boric Acid Condensate Tank D Inadvertently Discharged to Circulating Water Sys.Caused by Procedural Noncompliance.Operating Procedure Revised & Operations Personnel Counseled |
- on 861021,boric Acid Condensate Tank D Inadvertently Discharged to Circulating Water Sys.Caused by Procedural Noncompliance.Operating Procedure Revised & Operations Personnel Counseled
| 10 CFR 50.73(a)(2)(i) | | 05000382/LER-1986-025, :on 861022,reactor Trip Occurred.Caused by Trying to Maintain Steam Generator Levels at Low Reactor Power for Prolonged Period,Following Reactor Trip on 861021. Valve Positioner Replaced |
- on 861022,reactor Trip Occurred.Caused by Trying to Maintain Steam Generator Levels at Low Reactor Power for Prolonged Period,Following Reactor Trip on 861021. Valve Positioner Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000382/LER-1986-026, :on 861120,inadvertent Actuation of Ventilation Emergency Filtration Sys in Fuel Handling Bldg Occurred. Caused by Personnel Error.Rev to Procedure MI-3-362 Initiated & Meeting Held W/Personnel |
- on 861120,inadvertent Actuation of Ventilation Emergency Filtration Sys in Fuel Handling Bldg Occurred. Caused by Personnel Error.Rev to Procedure MI-3-362 Initiated & Meeting Held W/Personnel
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000382/LER-1986-027, :on 861120,personnel Discovered That Fire Protection Valves Not Verified in Correct Position within 31 Days as Required by Tech Spec Due to Inadequate Procedures. Valves Verified in Open Position & Documented |
- on 861120,personnel Discovered That Fire Protection Valves Not Verified in Correct Position within 31 Days as Required by Tech Spec Due to Inadequate Procedures. Valves Verified in Open Position & Documented
| | | 05000382/LER-1986-029, :on 861228,hi-hi Alarm Occurred on Radiation Monitor ARM-IRE-0200.1S.Caused by Monitors Sensitivity to Electrical Spikes,Vibration & Light.Efforts Continuing to Reduce Sensitivity of Monitors |
- on 861228,hi-hi Alarm Occurred on Radiation Monitor ARM-IRE-0200.1S.Caused by Monitors Sensitivity to Electrical Spikes,Vibration & Light.Efforts Continuing to Reduce Sensitivity of Monitors
| 10 CFR 50.73(a)(2)(iv), System Actuation |
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