ML20009A938

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LER 81-020/03L-0:on 810606,condensate Water Storage Tank Level Went Below Tech Spec Limit.Caused by Normal Tank Water Usage During Startup & Turbine Testing Coincident W/ Demineralizer Regeneration
ML20009A938
Person / Time
Site: Kewaunee Dominion icon.png
Issue date: 07/06/1981
From: Lindberg P, Molzahn D
WISCONSIN PUBLIC SERVICE CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20009A933 List:
References
LER-81-020-03L, LER-81-20-3L, NUDOCS 8107140519
Download: ML20009A938 (1)


Text

LICENSEE EVENT REPORT L iTi10L BLOCX: l l l l ,U6 h (PLE ASE PRINT OR TYPE ALL REQUf RED INFORMATION) l0 l1l 7 0 9 l Wl LICENSEE Tl Kl Nl CODE Pl 114 l@l0 15 l 0 l - l 0LICENSE l 0 l NUMBEH 0 l 0 l 0 l- l 0 l250 l@l4 26 l1 l1 l1 l1 lhlb7 CAT LICENSL TYPE .50 l

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CON'T 101il  %",n"' I 1.l@l 01 s I 010101310 l s l@l 0 l 6 l 0 le l 811 l@ln 75 17 In 16 lalil@ 80 7 8 60 61 DOCKET NUMBER 68 6'J EVENT DATE 74 REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l o l 2 l [ During startup operations following the refueling shutdown, the level in the conden- l lo Ial l sate water storage tank (CST) went below the T.S. limit. This placed'the facility l j o 1.: l l under LCO T. S. 3.4b. Service water, the safety grade backup supply to the Aux. I o 3 l Feedwater Pumps, was availabic. There was no effect on public safety. I 10161I l 10171 1 I 101811 I 7 8 9 80 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUSCODE COMPONENT CODE SUSCODE SUSCODE l0l9l 7 8 l Wl Fl@ Wh lz lh lA l Cl Cl Ul Ml Ulh Wh W h 9 to 11 12 13 IS 19 20

_ SEQUENTIAL OCCUR R E NCE REFORT REVISION L E R/RO EVENT YE MI REPOHT No. CODE TYPE NO.

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_ l218 22l1 l 23 ". 4 2G 27 28 23 30 31 32 AKEi AC PL NT ETH HOURS SB I D FORL b S. SUPPLIE MA FA TURER I33x l@l34 z l@ lzl@ Lz_J@ 10 l* 10 10 i LN_l@

41 LN_J@ LAJ@ lo10 Isis 18 3b 36 31 40 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 2.

l i l o l l Normal CST water usage during plant startup and turbine testine. coincident with do- l li j i l lmineralizer regeneration, caused the CST level to no below the T.S. limit. I lij7l l The S/C blowdown rate was reduced until the demineralizer was back in service and the I gg l CST level was returned to normal. A T.S. proposed revision has been submitted l 3 . l (2-20-81) to permit the CST level to drop below 75,000 gallons during plant startup. I 7 8 9 80 S  % POWE R OTHER STATUS D4S Y DISCOVERY DESCRIPTION li l5 l Wh l0 l 0l 0lhlNA l W h ! Ooerator observation l A TlVITY CO TENT RELEASED OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE 1 G W h [_zj @ lNA l l NA 45 l

80 7 8 9 10 11 44 FERSONNEL EXPOSURES NUV8ER TYPE DESCRIPTION l

i 7 l 0 l 0 l 0 lhWhl NA PERSONNE L INJU IES NUYBER DESCRIPTION 7

i a 8 9 l0l0l0l@l 11 12 NA l 80 LOSS OF OR DAMAGE To FACILITY h TYPE DESCRIPTION v i 9

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PUBU$TY 8107140519 810706 NRC USE ONLY .

PDR ADOCK 05000305 7

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ISSUE 10 g PDR l 68 69 lllllllllllll7 80 5 NAME OF PREPARER

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PHONE:

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