05000305/LER-1982-035-03, /03L-1:on 821216,during Full Power Operation, Pinhole Leak Discovered in Suction Line from Vol Control Tank to Charging Pumps.Caused by Vibrations & Pulsations in Associated Piping.Leak Plugged

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/03L-1:on 821216,during Full Power Operation, Pinhole Leak Discovered in Suction Line from Vol Control Tank to Charging Pumps.Caused by Vibrations & Pulsations in Associated Piping.Leak Plugged
ML20028F436
Person / Time
Site: Kewaunee 
Issue date: 01/14/1983
From:
WISCONSIN PUBLIC SERVICE CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20028F425 List:
References
LER-82-035-03L, LER-82-35-3L, NUDOCS 8302010350
Download: ML20028F436 (1)


LER-1982-035, /03L-1:on 821216,during Full Power Operation, Pinhole Leak Discovered in Suction Line from Vol Control Tank to Charging Pumps.Caused by Vibrations & Pulsations in Associated Piping.Leak Plugged
Event date:
Report date:
3051982035R03 - NRC Website

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