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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J2471994-10-0606 October 1994 LER 94-009-00:on 940909,EDG G-02 Inadvertently Started & Station Battery Charger D-08 Tripped Off Due to Blown Fuse. Caused by Inadequate Procedure.Blown Fuse Replaced & Electrical Distribution Sys Restored to normal.W/941006 Ltr ML20029C8511994-04-22022 April 1994 LER 94-001-00:on 940323,identified That Feedwater Flow May Have Been Underestimated Since Beginning of Operating Cycle. Caused by Degradation of Signals from Transducers.Transducer replaced.W/940422 Ltr ML20044E5571993-05-17017 May 1993 LER 92-009-01:on 921012,identified That Ccws Surge Tank Vent Valves Outside Design Basis Due to Oversight During Original Design of CCW Sys.Proposes to Replace Radiation Detector & Associated Circuitry W/Dedicated safety-related Sys ML20044E6221993-05-17017 May 1993 LER 93-006-00:on 930416,discovered That Outside CIV Not Leak Tested,Per TS 15.4.4.III.D Requirements Due to Review on 840202,recommending That Valve Be Tested During RHR Hydrostatic Testing.Subj Valve replaced.W/930517 Ltr ML20044D8811993-05-14014 May 1993 LER 93-005-00:on 930415,containment Accident Fan Time Delay Relay 1-TDR-26 (Turbine Bldg Cooler Svc Water Inlet Valve 1SW-2880) Unexpectedly Closed.Caused by Failure to Recognize Presence of Relay in Contact.Function Changed ML20044D2061993-05-10010 May 1993 LER 93-003-00:on 930328,Point Beach Unit 2 Tripped Due to Surveillance Testing Problems.Test Procedures Can Trip Unit Due to Equipment or Human Failure.Failure Tests Delayed Until Unit 1 & Knpp Restored to power.W/930510 Ltr ML20024H2151991-05-21021 May 1991 LER 91-003-00:on 910429,charging Sys Check Valve 1-370 Discovered W/Leakage in Excess of Limits Due to Worn Disc Arm Bushing Steps.Worn Disc Arm Bushing Steps Cladded W/ E308 Weld Matl & Hand Filed to Design contour.W/910521 Ltr ML20029C2101991-03-20020 March 1991 LER 91-002-01:on 901009,inadvertent Start of Auxiliary Feedwater Pump Occurred.Caused by Inadequate Test Procedures.Auxiliary Feedwater Pump Secured & Maint Work Request Mwr 904517 initiated.W/910320 Ltr ML20029C1141991-03-12012 March 1991 LER 91-010-01:on 900816,axial Flux Differential Outside Tech Specs Limits Due to Malfunction of Turbine Electrohydraulic Governor Control.Operator Training Revised. W/910319 Ltr ML20028H0321990-09-27027 September 1990 LER 90-011-00:on 900829,low Net Positive Suction Head to Containment Spray Pumps W/Eccs in Recirculation Mode Occurred.Caused by Procedural Deficiency.Temporary Procedure Changes initiated.W/900927 Ltr ML20043G2011990-06-0808 June 1990 LER 90-005-00:on 900510,steam Generator lo-lo Level Reactor Trip Occurred During Cold Shutdown.Caused by Inadequate Warning Sign Posting.Nonconformance Rept Written to Document Event & Recommend evaluation.W/900608 Ltr ML20042G7761990-05-0909 May 1990 LER 90-003-00:on 900409,determined That Piping & Supports in Fuel Oil Pumphouse Could Not Be Demonstrated to Perform Support Functions.Caused by Design Base Not Sufficiently Documented.Mod Performed to Support Fuel Oil Piping ML20042G7791990-05-0808 May 1990 LER 90-004-00:on 900404,single Failure Potential in Safeguards Switchgear B03/B04 Tie Breaker Discovered & Could Have Resulted in Failure of Diesel Generator.Control Power Fuses for Tie Breakers Removed ML20042F5361990-05-0404 May 1990 LER 90-001-00:on 900405,auxiliary Feed Pump Inadvertently Started.Caused by Inadequate Design.Schematic Push to Test Lamp Circuitry Will Be Added to Elementary Wiring Diagrams & Personnel Briefed on Potential circuitry.W/900504 Ltr ML20042F1971990-05-0202 May 1990 LER 90-002-00:on 900402,main Steam Safety Valve 1-MS-2013 Failed to Relieve Setpoint During Tech Spec Testing.Caused by Personnel Error During Setpoint Adjustment.Safety Valves 1-MS-2011,1-MS-2006 & 1-MS-2008 restored.W/900502 Ltr ML20011D5131989-12-19019 December 1989 LER 89-010-00:on 891120,auxiliary Feedwater Flow Transmitters Inadvertently Isolated.Caused by Error in Approved Procedure & Personnel Cognitive Error.Unit 1 Transmitters Valved Back Into Svc immediately.W/891219 Ltr ML19351A6721989-12-15015 December 1989 LER 89-009-00:on 891115,unexpected Steam Generator a lo-lo Level & Steam Generator B lo-lo Level Reactor Trip Signals Experienced.Caused by Installation of Analog Signal Generator.Procedures revised.W/891215 Ltr ML19332F7011989-12-11011 December 1989 LER 89-008-01:on 890910,ATWS Mitigating Actuation Circuitry Automatically Bypassed at About 42% Reactor Power.Caused by Less than Adequate Tech Spec Change.Power Descension to 38% initiated.W/891211 Ltr ML19332E7221989-12-0707 December 1989 LER 89-009-00:on 891107,D05 & D06 Station Batteries Declared Inoperable.Caused by Original Design Deficiency.Mod Completed to Restore Battery D05 to Operable Status by Replacing Eight nonsafety-related breakers.W/891207 Ltr ML19332E8921989-12-0404 December 1989 LER 89-008-00:on 891103,during Refueling,Contractor Personnel Generated False Trip Signal While Investigating Wiring Discrepancy in Reactor Protection Sys Instrument Racks.Caused by Labeling Error.Supply changed.W/891204 Ltr ML19332F0901989-11-28028 November 1989 LER 89-003-01:on 890712,tank B Level Channel 2LE-934 Began to Indicate Spuriously.Caused by Moisture Intrusion Between Halar Insulator & Sensing Rod.Level Detector Replaced & Channel Reestablished for Accumulator Tank B.W/891128 Ltr ML19332C8411989-11-22022 November 1989 LER 89-007-00:on 891027,Train a Safety Injection Signal Generated During Installation of Mod in Containment High Pressure Circuit.Caused by Inadequate Installation Procedure.Procedure changed.W/891122 Ltr ML19327C2001989-11-14014 November 1989 LER 89-006-01:on 891015,steam Generator Tubes Found Degraded,W/Undefined Signal & W/Axial Indications in Tubesheet Area.Degradation Caused by Time.Affected Tubes Plugged or Preventively sleeved.W/891114 Ltr ML19327C0651989-11-0606 November 1989 LER 89-005-00:on 891006,intermediate Range High Level Trip Signal Unexpectedly Generated During Course of Routine Source Range Channel Calibr.Caused by Loose Connection of Input/Output Cable.Connection tightened.W/891106 Ltr ML19327B3061989-10-19019 October 1989 LER 89-008-00:on 890910,ATWS Mitigating Actuation Circuitry Automatically Bypassed at About 42% Reactor Power, Disenabling Sys.Caused by High Tech Spec Setpoint.Enable/ Disable Setpoint Reset to 30%.W/891019 Ltr ML18041A1611987-11-16016 November 1987 LER 87-004-01:on 870515,voltage Lost on Red Instrument Bus Resulting in Reactor Protection Sys Actuation.Caused by Excessive Current Demand by ferro-resonant Circuit.Plant Mods to Load Bank Proposed ML18041A1341986-07-0303 July 1986 LER 86-003-00:on 860603,reactor Trip Occurred Due to Loss of Power on White Instrument Bus.Caused by Trip of White Inverter Output Breaker.Procedures for Placing Inverter on Line Will Be revised.W/860703 Ltr ML20028E3551983-01-13013 January 1983 LER 82-029/03L-0:on 821216,automatic Monitoring & Alarm Program Constant Found Incorrect.Caused by Unknown Personnel W/Access to on-line Computer.Value of Constant Restored & Control Rods Alignment Verified ML20028E2381983-01-13013 January 1983 LER 82-028/03L-0:on 821215,routine Test on Fire Detection Sys Found Panel D407 Which Monitors Unit 1 Rod Drive Room Inoperable.Caused by Blown Fuse.Fuse & Indication Lights Replaced on 821215.Detection Sys Undergoing Design Review ML20028E1791983-01-13013 January 1983 Updated LER 82-020/01X-1:on 821102,while Performing Type B & C Leakage Tests of Containment Penetrations & Isolation Valves,One Valve Had Leakage Exceeding Limit.Cause Not Stated.Valve Clapper & Seat Lapped ML20028E3031983-01-11011 January 1983 LER 82-027/03L-0:on 821211,operator Noted That Steam Generator Pressure Transmitter 1PT-469 Indicated Higher than Other Channels.Caused by Frozen Sensing Line Due to Inadequate Interim Piping Insulation ML20028E3211983-01-10010 January 1983 Updated LER 82-017/01X-2:on 821030,w/unit Shut Down for Refueling,Eddy Current Exam of Steam Generator Tubes Indicated Four Tubes in Steam Generator a & Three Tubes in Steam Generator B Exceeded Plugging Limit.Caused by Caustic ML20028C2431982-12-27027 December 1982 LER 82-020/01T-0:on 821103,following Type B & C Leak Rate Tests,Total as-measured Leakage Exceeded Tech Spec Limit, Causing Reactor Coolant Pump Component Cooling Water to Have Excessive Leakage.Cause Not Stated.Clapper & Seat Lapped ML20023B3251982-12-10010 December 1982 Updated LER 82-017/01T-1:on 821030,verified That Indications for Four Steam Generator a Tubes & Three Steam Generator B Tubes Exceeded 40% Plugging Limit During Eddy Current Exam on 821026-30.Cause Not Stated.Tubes Mechanically Plugged ML20028B4151982-11-15015 November 1982 LER 82-017/01T-0:on 821030,four Tubes in Steam Generator a & Three Tubes in Steam Generator B Indicated Degradation Greater than 40% Plugging Limit.Caused by Intergranular Attack.Tubes Mechanically Plugged ML20028A0371982-11-0505 November 1982 LER 82-008/03L-0:on 821006,low Steam Line Pressure Setting for Pressure Instrument 2PT-478 Found Lower than Allowed by Tech Specs.Caused by Bumping of Setpoint Adjustment Knob.Instrument Tested & Realigned ML20027D6821982-11-0303 November 1982 LER 82-018/01T-0:on 821015,incorrect Instrument Bus Supply Shifted to Alternate Supply Following Rept of Fire in Supply Breaker for 1GYO4 Motor Generator Set,Causing Loss of Redundancy on Containment Pressure Indicator 1PT-950 ML20052G4501982-05-12012 May 1982 LER 82-002/01T-0:on 820428,during Eddy Current Exam, Discovered Abnormal Degradation in Fuel Cladding,Rcpb & Primary Containment.Seludge Lancing Will Be Performed ML20052G3701982-05-0707 May 1982 LER 82-009/03L-0:on 820408,4.16-kV Safeguards Undervoltage Relays Did Not Meet 0-volt Time Delay Spec.Caused by Manufacturer Characteristic Curves.Relays Not Capable of Less than 0.38-s.Tech Spec Change Requested on 820427 ML20052G3831982-05-0707 May 1982 LER 82-011/03L-0:on 820415,during Biweekly Calibr Check ICP 2.1 of Reactor Protective Sys Functions,Overpower Delta T Setpoint 2 for Channel 2 Found Less Conservative than Tech Spec Limit.Caused by Setpoint Drift in Impulse Summer Unit ML20052G6331982-05-0707 May 1982 LER 82-010/03L-0:on 820414,ICP 2.9 Found Not to Provide for Proper Unblocking of Source Range High Flux Reactor Trip Over Small Range of Instrument Readings.Caused by Failure to Identify Subtle Procedural Flow.Procedure to Be Revised ML20052B4521982-04-23023 April 1982 LER 82-008/03L-0:on 820323,minor Installation Defects Noted on Four of Six Containment Pressure Transmitters Installed as TMI Response Mod.Caused by Backfit Contractor QC Program Breakdown ML20050B2661982-03-25025 March 1982 LER 82-006/01T-0:on 820311,type B & C Valve Leakage Tests Exceeded Tech Spec Limits.Caused by Corrosion.Svc Air Check Valves Disc Replaced & Valve Cover Remachined ML20041F4861982-03-0808 March 1982 LER 82-005/01T-01:on 820222,poison Test Samples & Two Fuel Assemblies W/Less than 1-yr Cooling Period Found Placed Next to Divider Wall in Spent Fuel Pool.Caused by Tech Spec Misinterpretation ML20041E4911982-03-0404 March 1982 LER 82-004/03L-0:on 820206,during Inservice Testing, Differential Pressure Instrument 4007 for Auxiliary Feed Pump P38A Found Isolated.Probably Caused by Failure to Return Instrument to Svc Following Calibr ML20041E6131982-03-0202 March 1982 LER 82-003/01T-0:on 820217,during Surveillance Testing, Emergency Diesel Generator 3D Failed to Operate.Caused by Sticking Shutdown Solenoid Plunger on Woodward Type UG8 Governor.Solenoid Cleaned,Checked & Generator Tested ML20049H6981982-02-23023 February 1982 LER 82-001/03L-0:on 820203,boric Acid Heat Tracing Circuit P-42 Found Inoperable.Caused by Failed Thermon Type 4 Circuit Controller.Circuit Controller Replaced ML20040G6811982-02-0505 February 1982 LER 82-001/03L-0:on 820107,steam Generator Pressure Sensing Lines Discovered Frozen on a Steam Generator.Caused by Inadequate Freeze Protection & Extremely Cold Weather.Addl Heat Lamps Installed ML20040G5801982-02-0505 February 1982 LER 82-002/03L-0:on 820112,during Hot shutdown,1PT-469 Steam Generator Pressure Transmitter Isolated by Maint Personnel Due to Leaking Coupling.Pressure Sensing Tubing Showed Signs of Steam Leak Due to Freezing ML20040D3791982-01-18018 January 1982 LER 81-020/03L-0:on 811219,frozen Sensing Line Caused High Indication of Steam Generator Pressure Instrument 1PT-482. Caused by Incomplete Insulation of Line & by Cold Weather. Instrument Placed in Tripped Position & Tubing Thawed 1994-04-22
[Table view] Category:RO)
MONTHYEARML20024J2471994-10-0606 October 1994 LER 94-009-00:on 940909,EDG G-02 Inadvertently Started & Station Battery Charger D-08 Tripped Off Due to Blown Fuse. Caused by Inadequate Procedure.Blown Fuse Replaced & Electrical Distribution Sys Restored to normal.W/941006 Ltr ML20029C8511994-04-22022 April 1994 LER 94-001-00:on 940323,identified That Feedwater Flow May Have Been Underestimated Since Beginning of Operating Cycle. Caused by Degradation of Signals from Transducers.Transducer replaced.W/940422 Ltr ML20044E5571993-05-17017 May 1993 LER 92-009-01:on 921012,identified That Ccws Surge Tank Vent Valves Outside Design Basis Due to Oversight During Original Design of CCW Sys.Proposes to Replace Radiation Detector & Associated Circuitry W/Dedicated safety-related Sys ML20044E6221993-05-17017 May 1993 LER 93-006-00:on 930416,discovered That Outside CIV Not Leak Tested,Per TS 15.4.4.III.D Requirements Due to Review on 840202,recommending That Valve Be Tested During RHR Hydrostatic Testing.Subj Valve replaced.W/930517 Ltr ML20044D8811993-05-14014 May 1993 LER 93-005-00:on 930415,containment Accident Fan Time Delay Relay 1-TDR-26 (Turbine Bldg Cooler Svc Water Inlet Valve 1SW-2880) Unexpectedly Closed.Caused by Failure to Recognize Presence of Relay in Contact.Function Changed ML20044D2061993-05-10010 May 1993 LER 93-003-00:on 930328,Point Beach Unit 2 Tripped Due to Surveillance Testing Problems.Test Procedures Can Trip Unit Due to Equipment or Human Failure.Failure Tests Delayed Until Unit 1 & Knpp Restored to power.W/930510 Ltr ML20024H2151991-05-21021 May 1991 LER 91-003-00:on 910429,charging Sys Check Valve 1-370 Discovered W/Leakage in Excess of Limits Due to Worn Disc Arm Bushing Steps.Worn Disc Arm Bushing Steps Cladded W/ E308 Weld Matl & Hand Filed to Design contour.W/910521 Ltr ML20029C2101991-03-20020 March 1991 LER 91-002-01:on 901009,inadvertent Start of Auxiliary Feedwater Pump Occurred.Caused by Inadequate Test Procedures.Auxiliary Feedwater Pump Secured & Maint Work Request Mwr 904517 initiated.W/910320 Ltr ML20029C1141991-03-12012 March 1991 LER 91-010-01:on 900816,axial Flux Differential Outside Tech Specs Limits Due to Malfunction of Turbine Electrohydraulic Governor Control.Operator Training Revised. W/910319 Ltr ML20028H0321990-09-27027 September 1990 LER 90-011-00:on 900829,low Net Positive Suction Head to Containment Spray Pumps W/Eccs in Recirculation Mode Occurred.Caused by Procedural Deficiency.Temporary Procedure Changes initiated.W/900927 Ltr ML20043G2011990-06-0808 June 1990 LER 90-005-00:on 900510,steam Generator lo-lo Level Reactor Trip Occurred During Cold Shutdown.Caused by Inadequate Warning Sign Posting.Nonconformance Rept Written to Document Event & Recommend evaluation.W/900608 Ltr ML20042G7761990-05-0909 May 1990 LER 90-003-00:on 900409,determined That Piping & Supports in Fuel Oil Pumphouse Could Not Be Demonstrated to Perform Support Functions.Caused by Design Base Not Sufficiently Documented.Mod Performed to Support Fuel Oil Piping ML20042G7791990-05-0808 May 1990 LER 90-004-00:on 900404,single Failure Potential in Safeguards Switchgear B03/B04 Tie Breaker Discovered & Could Have Resulted in Failure of Diesel Generator.Control Power Fuses for Tie Breakers Removed ML20042F5361990-05-0404 May 1990 LER 90-001-00:on 900405,auxiliary Feed Pump Inadvertently Started.Caused by Inadequate Design.Schematic Push to Test Lamp Circuitry Will Be Added to Elementary Wiring Diagrams & Personnel Briefed on Potential circuitry.W/900504 Ltr ML20042F1971990-05-0202 May 1990 LER 90-002-00:on 900402,main Steam Safety Valve 1-MS-2013 Failed to Relieve Setpoint During Tech Spec Testing.Caused by Personnel Error During Setpoint Adjustment.Safety Valves 1-MS-2011,1-MS-2006 & 1-MS-2008 restored.W/900502 Ltr ML20011D5131989-12-19019 December 1989 LER 89-010-00:on 891120,auxiliary Feedwater Flow Transmitters Inadvertently Isolated.Caused by Error in Approved Procedure & Personnel Cognitive Error.Unit 1 Transmitters Valved Back Into Svc immediately.W/891219 Ltr ML19351A6721989-12-15015 December 1989 LER 89-009-00:on 891115,unexpected Steam Generator a lo-lo Level & Steam Generator B lo-lo Level Reactor Trip Signals Experienced.Caused by Installation of Analog Signal Generator.Procedures revised.W/891215 Ltr ML19332F7011989-12-11011 December 1989 LER 89-008-01:on 890910,ATWS Mitigating Actuation Circuitry Automatically Bypassed at About 42% Reactor Power.Caused by Less than Adequate Tech Spec Change.Power Descension to 38% initiated.W/891211 Ltr ML19332E7221989-12-0707 December 1989 LER 89-009-00:on 891107,D05 & D06 Station Batteries Declared Inoperable.Caused by Original Design Deficiency.Mod Completed to Restore Battery D05 to Operable Status by Replacing Eight nonsafety-related breakers.W/891207 Ltr ML19332E8921989-12-0404 December 1989 LER 89-008-00:on 891103,during Refueling,Contractor Personnel Generated False Trip Signal While Investigating Wiring Discrepancy in Reactor Protection Sys Instrument Racks.Caused by Labeling Error.Supply changed.W/891204 Ltr ML19332F0901989-11-28028 November 1989 LER 89-003-01:on 890712,tank B Level Channel 2LE-934 Began to Indicate Spuriously.Caused by Moisture Intrusion Between Halar Insulator & Sensing Rod.Level Detector Replaced & Channel Reestablished for Accumulator Tank B.W/891128 Ltr ML19332C8411989-11-22022 November 1989 LER 89-007-00:on 891027,Train a Safety Injection Signal Generated During Installation of Mod in Containment High Pressure Circuit.Caused by Inadequate Installation Procedure.Procedure changed.W/891122 Ltr ML19327C2001989-11-14014 November 1989 LER 89-006-01:on 891015,steam Generator Tubes Found Degraded,W/Undefined Signal & W/Axial Indications in Tubesheet Area.Degradation Caused by Time.Affected Tubes Plugged or Preventively sleeved.W/891114 Ltr ML19327C0651989-11-0606 November 1989 LER 89-005-00:on 891006,intermediate Range High Level Trip Signal Unexpectedly Generated During Course of Routine Source Range Channel Calibr.Caused by Loose Connection of Input/Output Cable.Connection tightened.W/891106 Ltr ML19327B3061989-10-19019 October 1989 LER 89-008-00:on 890910,ATWS Mitigating Actuation Circuitry Automatically Bypassed at About 42% Reactor Power, Disenabling Sys.Caused by High Tech Spec Setpoint.Enable/ Disable Setpoint Reset to 30%.W/891019 Ltr ML18041A1611987-11-16016 November 1987 LER 87-004-01:on 870515,voltage Lost on Red Instrument Bus Resulting in Reactor Protection Sys Actuation.Caused by Excessive Current Demand by ferro-resonant Circuit.Plant Mods to Load Bank Proposed ML18041A1341986-07-0303 July 1986 LER 86-003-00:on 860603,reactor Trip Occurred Due to Loss of Power on White Instrument Bus.Caused by Trip of White Inverter Output Breaker.Procedures for Placing Inverter on Line Will Be revised.W/860703 Ltr ML20028E3551983-01-13013 January 1983 LER 82-029/03L-0:on 821216,automatic Monitoring & Alarm Program Constant Found Incorrect.Caused by Unknown Personnel W/Access to on-line Computer.Value of Constant Restored & Control Rods Alignment Verified ML20028E2381983-01-13013 January 1983 LER 82-028/03L-0:on 821215,routine Test on Fire Detection Sys Found Panel D407 Which Monitors Unit 1 Rod Drive Room Inoperable.Caused by Blown Fuse.Fuse & Indication Lights Replaced on 821215.Detection Sys Undergoing Design Review ML20028E1791983-01-13013 January 1983 Updated LER 82-020/01X-1:on 821102,while Performing Type B & C Leakage Tests of Containment Penetrations & Isolation Valves,One Valve Had Leakage Exceeding Limit.Cause Not Stated.Valve Clapper & Seat Lapped ML20028E3031983-01-11011 January 1983 LER 82-027/03L-0:on 821211,operator Noted That Steam Generator Pressure Transmitter 1PT-469 Indicated Higher than Other Channels.Caused by Frozen Sensing Line Due to Inadequate Interim Piping Insulation ML20028E3211983-01-10010 January 1983 Updated LER 82-017/01X-2:on 821030,w/unit Shut Down for Refueling,Eddy Current Exam of Steam Generator Tubes Indicated Four Tubes in Steam Generator a & Three Tubes in Steam Generator B Exceeded Plugging Limit.Caused by Caustic ML20028C2431982-12-27027 December 1982 LER 82-020/01T-0:on 821103,following Type B & C Leak Rate Tests,Total as-measured Leakage Exceeded Tech Spec Limit, Causing Reactor Coolant Pump Component Cooling Water to Have Excessive Leakage.Cause Not Stated.Clapper & Seat Lapped ML20023B3251982-12-10010 December 1982 Updated LER 82-017/01T-1:on 821030,verified That Indications for Four Steam Generator a Tubes & Three Steam Generator B Tubes Exceeded 40% Plugging Limit During Eddy Current Exam on 821026-30.Cause Not Stated.Tubes Mechanically Plugged ML20028B4151982-11-15015 November 1982 LER 82-017/01T-0:on 821030,four Tubes in Steam Generator a & Three Tubes in Steam Generator B Indicated Degradation Greater than 40% Plugging Limit.Caused by Intergranular Attack.Tubes Mechanically Plugged ML20028A0371982-11-0505 November 1982 LER 82-008/03L-0:on 821006,low Steam Line Pressure Setting for Pressure Instrument 2PT-478 Found Lower than Allowed by Tech Specs.Caused by Bumping of Setpoint Adjustment Knob.Instrument Tested & Realigned ML20027D6821982-11-0303 November 1982 LER 82-018/01T-0:on 821015,incorrect Instrument Bus Supply Shifted to Alternate Supply Following Rept of Fire in Supply Breaker for 1GYO4 Motor Generator Set,Causing Loss of Redundancy on Containment Pressure Indicator 1PT-950 ML20052G4501982-05-12012 May 1982 LER 82-002/01T-0:on 820428,during Eddy Current Exam, Discovered Abnormal Degradation in Fuel Cladding,Rcpb & Primary Containment.Seludge Lancing Will Be Performed ML20052G3701982-05-0707 May 1982 LER 82-009/03L-0:on 820408,4.16-kV Safeguards Undervoltage Relays Did Not Meet 0-volt Time Delay Spec.Caused by Manufacturer Characteristic Curves.Relays Not Capable of Less than 0.38-s.Tech Spec Change Requested on 820427 ML20052G3831982-05-0707 May 1982 LER 82-011/03L-0:on 820415,during Biweekly Calibr Check ICP 2.1 of Reactor Protective Sys Functions,Overpower Delta T Setpoint 2 for Channel 2 Found Less Conservative than Tech Spec Limit.Caused by Setpoint Drift in Impulse Summer Unit ML20052G6331982-05-0707 May 1982 LER 82-010/03L-0:on 820414,ICP 2.9 Found Not to Provide for Proper Unblocking of Source Range High Flux Reactor Trip Over Small Range of Instrument Readings.Caused by Failure to Identify Subtle Procedural Flow.Procedure to Be Revised ML20052B4521982-04-23023 April 1982 LER 82-008/03L-0:on 820323,minor Installation Defects Noted on Four of Six Containment Pressure Transmitters Installed as TMI Response Mod.Caused by Backfit Contractor QC Program Breakdown ML20050B2661982-03-25025 March 1982 LER 82-006/01T-0:on 820311,type B & C Valve Leakage Tests Exceeded Tech Spec Limits.Caused by Corrosion.Svc Air Check Valves Disc Replaced & Valve Cover Remachined ML20041F4861982-03-0808 March 1982 LER 82-005/01T-01:on 820222,poison Test Samples & Two Fuel Assemblies W/Less than 1-yr Cooling Period Found Placed Next to Divider Wall in Spent Fuel Pool.Caused by Tech Spec Misinterpretation ML20041E4911982-03-0404 March 1982 LER 82-004/03L-0:on 820206,during Inservice Testing, Differential Pressure Instrument 4007 for Auxiliary Feed Pump P38A Found Isolated.Probably Caused by Failure to Return Instrument to Svc Following Calibr ML20041E6131982-03-0202 March 1982 LER 82-003/01T-0:on 820217,during Surveillance Testing, Emergency Diesel Generator 3D Failed to Operate.Caused by Sticking Shutdown Solenoid Plunger on Woodward Type UG8 Governor.Solenoid Cleaned,Checked & Generator Tested ML20049H6981982-02-23023 February 1982 LER 82-001/03L-0:on 820203,boric Acid Heat Tracing Circuit P-42 Found Inoperable.Caused by Failed Thermon Type 4 Circuit Controller.Circuit Controller Replaced ML20040G6811982-02-0505 February 1982 LER 82-001/03L-0:on 820107,steam Generator Pressure Sensing Lines Discovered Frozen on a Steam Generator.Caused by Inadequate Freeze Protection & Extremely Cold Weather.Addl Heat Lamps Installed ML20040G5801982-02-0505 February 1982 LER 82-002/03L-0:on 820112,during Hot shutdown,1PT-469 Steam Generator Pressure Transmitter Isolated by Maint Personnel Due to Leaking Coupling.Pressure Sensing Tubing Showed Signs of Steam Leak Due to Freezing ML20040D3791982-01-18018 January 1982 LER 81-020/03L-0:on 811219,frozen Sensing Line Caused High Indication of Steam Generator Pressure Instrument 1PT-482. Caused by Incomplete Insulation of Line & by Cold Weather. Instrument Placed in Tripped Position & Tubing Thawed 1994-04-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARNPL-99-0569, Monthly Operating Repts for Sept 1999 for Pbnp,Units 1 & 2. with1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pbnp,Units 1 & 2. with ML20212D5961999-09-15015 September 1999 Safety Evaluation Supporting Licensee IPEEE Process.Plant Has Met Intent of Suppl 4 to GL 88-20 NPL-99-0051, Monthly Operating Repts for Aug 1999 for Pbnp,Units 1 & 2. with1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Pbnp,Units 1 & 2. with NPL-99-0449, Monthly Operating Repts for July 1999 for Pbnp,Units 1 & 2. with1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Pbnp,Units 1 & 2. with ML20196J4251999-06-30030 June 1999 Safety Evaluation Authorizing Proposed Alternatives Described in Relief Requests VRR-01,ROJ-16,PRR-01 & VRR-02 ML20209D2691999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Pbnps,Units 1 & 2 ML20196F3341999-06-22022 June 1999 Safety Evaluation for Implementation of 422V+ Fuel Assemblies at Pbnp Units 1 & 2 ML20195F9781999-06-10010 June 1999 Unit 2 Refueling 23 Inservice Insp Summary Rept for Form NIS-1 ML20209D2751999-05-31031 May 1999 Revised MORs for May 1999 for Pbnps,Units 1 & 2 NPL-99-0328, Monthly Operating Repts for May 1999 for Pbnp,Units 1 & 2. with1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Pbnp,Units 1 & 2. with NPL-99-0273, Monthly Operating Repts for Apr 1999 for Point Beach Nuclear Plant,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Point Beach Nuclear Plant,Units 1 & 2.With ML20196F3521999-04-30030 April 1999 Non-proprietary WCAP-14788, W Revised Thermal Design Procedure Instrument Uncertainty Methodology for Wepc Point Beach Units 1 & 2 (Fuel Upgrade & Uprate to 1656 Mwt - NSSS Power) NPL-99-0193, Monthly Operating Repts for Mar 1999 for Pbnp,Units 1 & 2. with1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Pbnp,Units 1 & 2. with NPL-99-0134, Monthly Operating Repts for Feb 1999 for Pbnp,Units 1 & 2. with1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Pbnp,Units 1 & 2. with ML20207D6751999-02-22022 February 1999 Assessment of Design Info on Piping Restraints for Point Beach Nuclear Plant,Units 1 & 2.Staff Concludes That Licensee Unable to Retrieve Original Analyses That May Have Been Performed to Justify Removal of Shim Collars ML20206R9001999-01-13013 January 1999 SER Accepting Nuclear Quality Assurance Program Changes for Point Beach Nuclear Plant,Units 1 & 2 NPL-99-0008, Monthly Operating Repts for Dec 1998 for Pbnp,Units 1 & 2. with1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Pbnp,Units 1 & 2. with NPL-99-0091, 1998 Annual Results & Data Rept for Pbnps,Units 1 & 2. with1998-12-31031 December 1998 1998 Annual Results & Data Rept for Pbnps,Units 1 & 2. with ML20198C7671998-12-10010 December 1998 Safety Evaluation Accepting Licensee Proposed Alternative to ASME BPV Code,1986 Edition,Section XI Requirement IWA-2232, to Use Performance Demonstration Initiative Program During RPV Third 10-yr ISI for Plant,Unit 2 NPL-98-1006, Monthly Operating Repts for Nov 1998 for Point Beach Nuclear Plant,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Point Beach Nuclear Plant,Units 1 & 2.With ML20195J5101998-11-16016 November 1998 Proposed Revs to Section 1.3 of FSAR for Pbnp QA Program ML20198J5941998-11-0303 November 1998 1998 Graded Exercise,Conducted on 981103 NPL-98-0948, Monthly Operating Repts for Oct 1998 for Point Beach Nuclear Plant,Units 1 & 2.With1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Point Beach Nuclear Plant,Units 1 & 2.With NPL-98-0880, Special Rept:On 980913,fire Alarm Control Panels Inoperable for More That Fourteen Days.Troubleshooting of D-401 Panel Following Installation of Replacement Batteries Revealed No Apparent Cause for Spurious Alarms.Panel D-401 Restored1998-10-21021 October 1998 Special Rept:On 980913,fire Alarm Control Panels Inoperable for More That Fourteen Days.Troubleshooting of D-401 Panel Following Installation of Replacement Batteries Revealed No Apparent Cause for Spurious Alarms.Panel D-401 Restored ML20154M9121998-10-14014 October 1998 Unit 1 Refueling 24 Repair/Replacement Summary Rept for Form NIS-2 ML20154L6751998-10-14014 October 1998 Unit 1 Refueling 24 ISI Summary Rept for Form NIS-1 NPL-98-0826, Monthly Operating Repts for Sept 1998 for Point Beach Nuclear Plant,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Point Beach Nuclear Plant,Units 1 & 2.With ML20151W3851998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Pbnp Units 1 & 2 NPL-98-0653, Monthly Operating Repts for July 1998 for Point Beach Nuclear Plant,Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20151W4471998-07-31031 July 1998 Corrected Page to MOR for July 1998 for Pbnp Unit 2 ML20151W4541998-07-31031 July 1998 Corrected Page to MOR for July 1998 for Pbnp Unit 1 ML20236Q3161998-07-10010 July 1998 Safety Evaluation Accepting Licensee Proposed Alternative to ASME Code Requirements PTP-3-01 & PTP-3-02 ML20236L6771998-07-0707 July 1998 Safety Evaluation Approving Wepco Implementation Program to Resolve USI A-46 at Point Beach NPP Units 1 & 2 NPL-98-0558, Monthly Operating Repts for June 1998 for Pbnp,Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Pbnp,Units 1 & 2 ML20151W4261998-06-30030 June 1998 Corrected Page to MOR for June 1998 for Pbnp Unit 2 ML20151W4221998-05-31031 May 1998 Corrected Page to MOR for May 1998 for Pbnp Unit 2 NPL-98-0481, Monthly Operating Repts for May 1998 for Point Beach Nuclear Plant,Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20151W4011998-04-30030 April 1998 Corrected Page to MOR for April 1998 for Pbnp Unit 2 NPL-98-0356, Monthly Operating Repts for April 1998 for Point Beach Nuclear Plant,Units 1 & 21998-04-30030 April 1998 Monthly Operating Repts for April 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20217F3131998-04-17017 April 1998 Safety Evaluation Accepting Proposed Alternative to ASME Code for Surface Exam of Nonstructural Seal Welds,For Plant, Unit 1 ML20216D7071998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20151W3981998-03-31031 March 1998 Corrected Page to MOR for March for Pbnp Unit 2 NPL-98-0209, Special Rept Re Fire Barrier Inoperable for Greater than Seven Days.Compensatory Measures Implemented in Accordance W/Fire Protection Program Requirements During Time That Barriers Were Inoperable1998-03-30030 March 1998 Special Rept Re Fire Barrier Inoperable for Greater than Seven Days.Compensatory Measures Implemented in Accordance W/Fire Protection Program Requirements During Time That Barriers Were Inoperable ML20217A8501998-03-19019 March 1998 SER Accepting Proposed Changes Submitted on 980226 by Wiep to Pbnp Final SAR Section 1.8 Which Will Impact Commitments Made in Pbnp QA Program Description.Changes Concern Approval Authority for Procedures & Interviewing Authority ML20216J0101998-03-17017 March 1998 Safety Evaluation Accepting Third 10-yr Inservice Insp Interval Relief Request RR-1-18 for Plant NPL-98-0159, Monthly Operating Repts for Feb 1998 for Point Beach Nuclear Plant,Units 1 & 21998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20151W3891998-02-28028 February 1998 Corrected Page to MOR for Feb 1998 for Pbnp Unit 2 ML20216D7121998-02-28028 February 1998 Revised Corrected MOR for Feb 1998 for Point Beach Nuclear Plant,Unit 2 NPL-98-0084, Monthly Operating Repts for Jan 1998 for Point Beach Nuclear Plant,Units 1 & 21998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20198L1151998-01-0808 January 1998 SER Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Point Beach Nuclear Plant,Units 1 & 2 1999-09-30
[Table view] |
Text
NRC FORM 366
- U. S. NUCLE AR REGULATORY COMMISSION (7 7M
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7 8 NLM86 R 63 EVENT OATE T OArE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h f5T 1IWith the unit in cold shutdown for a required 60 effective full power l PT31 I day steam generator testing program, an 800 psi' secondary-to-primary
,o,,,; hydrostatic leak test of the steam generators was performed on 3-11-80. ,
No leaks were identified in the "A" steam generator. Inspection of the "B" steam generator revealed one tube (R23C44) leaking approximately 3 drops / min., one tube (R8C37) that appeared wet .nd one wec plug end (R23C50). This event is reportable per T. S. 15.6.9.2.A.3 and similar 7 8 Sto otners. So
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4J lWl1l2l0lg 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h g lA previously scheduled eddy current inspection program was performed. ;
24 tubes in the "A" steam generator and 32 tubes in the "B" steam generator were explosively plugged except for the hot leg side of three tubes in the "B" steam t,Tenerator which have been pulled for laboratory examination. The three tube holes will be weld plugaed and two leakina ITTTI 1 oreviously T)1ucced tubes wi11 be recair welded. A h9drostatic test willi 7 e abe m
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l ATTACHMENT TO LICENSEE EVENT REPORT 80-002/OlT-0 :
Wisconsin Electric Power Company Point Beach Nuclear Plant Unit 1 Docket No. 50-266 Unit 1 was placed in cold shutdown at 0215 hours0.00249 days <br />0.0597 hours <br />3.554894e-4 weeks <br />8.18075e-5 months <br /> on 1 March 6, 1980, for the 60 effective full power day steam generator )
testing program required by the Confirmatory Order of November 30, '
1979. When taken off line the unit had primary-to-secondary I l
leakage of approximately 30 gallons per day, which is well below the Technical Specification and Confirmatory Order limits. The ;
leak rate haJ been stable at this valta since the unit returned to service on December 23, 1979 following steam generator repair work.
Prior to performing the 800 psi secondary-to-primary ;
leak test, a 2000 psi primary-to-secondary differential pressure leak test was conducted.
At 0400 hours0.00463 days <br />0.111 hours <br />6.613757e-4 weeks <br />1.522e-4 months <br /> on March 11, 1980 the 800 psi secondary-to-primary hydrostatic leak test of the Unit 1 "B" steam generator
. was completed. The "A" steam generator leak test was completed at 2020 hours0.0234 days <br />0.561 hours <br />0.00334 weeks <br />7.6861e-4 months <br /> the same day. No leaks were identified in the "A" steam generator. In the "B" steam generator, one tube (R2C44) was observed to be leaking approximately three drops per minute. Another tube (R8C37) appeared to be wet, but no water was dripping from
- the tube; a defect was later identified in this tube. The end of an existing explosive plug (R23C50) was wet, but no water was dripping from the plug.
After performing the leak test, an eddy current inspection was performed in compliance with the Confirmatory Order of November 30, 1979. The eddy current program performed was nutually agreed upon with the NRC and was similar to the inspection program conducted in December 1979. The program consisted of approximately 1,000 tubes in each steam generator concentrated mainly in the region where deep crevice tube defects have been found in the past.
However, over 100 of the tubes inspected in each generator were
. randomly located throughout the generator including the wedge area and the full length of these tubes was inspected. All the other tubes were inspected through the first support only.
Of the tubes inspected in the "A" steam generator, 24 were identified as having indications in the hot leg deep crevice region. Included in the 24 tubes a're six tubes with undefinable indications which were plugged as a conservative measure. No eddy current indications were found at or above the top of the tubesheet. No degraded tube indications were found in the cold leg side of those tubes which were inspected for the full length.
_1_
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All tubes in the "A" steam generator with indications were explosively plugged on March 17, 1980.
Of the tubes inspected in the "B" steam generator, 26 were idencified as having indications in the hot leg deep crevice region; one tube had a defect one-half inch above the tubesheet, and no defect was identified in the leaking tube.
Included in the 26 tubes are three tubes with undefinable indica-tions which were plugged as a conservative measure. No degraded tube indications were found in the cold leg side of those tubes which were inspected for the full length.
All tubes with indications, including the leaking tube, were explosively plugged on March 17, 1980 (see Table 2 for details), except for the hot leg side of three tubes which are being pulled for laboratory examination. The three tubes being pulled are:
' R19C37 with a 58% defect located one-half inch above the tubesheet.
R30C41 with a 47% deep crevice defect.
R26C53 with a 86% deep crevice defect that is similar to other undefinable indications.
The hot leg ends of these tubes have been weld plugged following tube pulling. Two previously plugged tubes (R23C50 and R29C41) have also been weld repaired. Four tubes which may have been damaged during tube pulling were also plugged as a precautionary measure.,
All defects detected in both steam generators were extremely small volume. The experience accumulated during recent outages with multi-frequency eddy current equipment and familiarity with Point Beach tubesheet signals has made definition of these small defects possible.
The unit is expected to return on line on approximately March 29 after tube pulling, weld plugging, hydrostatic testing, and crevice flush operation.
This event is reportable in accordance with Technical Specification 15.6.9.2.A.3.
TABLE 1 .
"A" STEAM GENERATOR TUBES PLUGGED Tube Defect Location R12C19 80% 19-21" above tube end R07C22 29/96% 12/17" above tube end R18C22 - 66% 20" above tube end R10C23 41% 20" above tube end R07C24 83% 17-20" above tube end R08C24 79% 17-21" above tube end R25C45 69% 12-20" above tube end R20C48 85% 21" above tube end R09C49 90% 21" above tube end R17C50 85% 19" above tube end R19C50 97% 11" above tube end R20C50 97% 11" above tube end R12C59 87% 21" above tube end R12C61 83% 17" above tube end R14C63 80% 19" above tube end R15C66 60% 18" above tube end R20C41 91% 19" above tube end R25C43 73% 17" above tube end R15C28 Undefinable Indication 21" above tube end R28C34 Undefinable Indication 18-20" above tube end R28C35 Undefinable Indication 17" above tube end RllC46 Undefinable Indication 12-21" above tube end R29C52 Undefinable Indication 14" above tube end R08C27 Undefinable Indication 15-20" above tube end e
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TABLE 2 "B" STEAM GENERATOR TUBES PLUGGED Tube Defect Location s
R18C25 75% 18" above tube end R13C2d 73% 21" above tube end R13C33 71% 20" above tube end R06C34 91% 11" above tube end R20C35 68% 21" above tube end R08C37 89% 5" above tube end R19C37 58% 1/2" above tubesheet R10C41 70% 21" above tube end R30C41 47% 21" above tube end R30C42 48% 21" above tube end R22C46 76% 15" above tube end R24C48 84% 12" above tube end R30C48 85% 21" above tube end R25C49 84% 5" above tube end R20C51 99% 16" above tube end R23C54 86% 4"-21" above tube end R23C57 56% 17" above tubo end R21C58 83% 21" above tube end R02C72 92% 3" above tube end R14C59 75% 21" above tube end R21C63 62% 21" above tube end R12C67 66% 21" above tube end R25C55 74% 15" above tube end R26C53 86% 18" above tube end R30C43 Undefinable Indication 21" above tube end R22C63 Undefinable Indication 21" above tube end R22C64 Undefinable Indication 20" above tube end R23C44 Leaking tube; no defect identified R21C42 Plugged as a precautionary measure; possibly damaged during tube pulling R31C42 Plugged as a precautionary measure; possibly damaged during tube pulling R28C40 Plugged as a precautionary measure; possibly damaged ,
during tube pulling R30C40 Plugged as a precautionary measure; possibly damaged during tube pulling S 8 semedp en =<e .-
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