ML19319C914

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LER 78-020/01T-0:on 780425,low Flow Condition Found on Decay Heat Removal Pump 1-A.Cause Being Evaluated & Corrective Action Formulated.Revision to LER Will Be Submitted Upon Evaluation Completion
ML19319C914
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 05/03/1978
From: Cooper J
FLORIDA POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19319C911 List:
References
LER-78-020-01T, LER-78-20-1T, NUDOCS 8003040862
Download: ML19319C914 (2)


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SUPPLEMENTARY INFORMATION 15 v

japort No.:' 50-302/78-020/01T-0

2. Facility: Crystal River Unic #3 -
3. Report Date: 3 May 1978

'4.- Occurrence Date: 25 April 1978

5. Identification of Occurrence:

7ecay Heat Removal Pump 1-A inoperable creating a condition contrary to Technical Specification 6.9.1.8.1.

6. Conditions Prior to Occurrence:

l Mode 6 refueling.

7. Description of Occurrence:

At 2200 on 25 April 1978 it. was observed that low flow condition existed on Decay Heat Removal Pump 1-A (DHP l-A). Upon disassembly of DEP l-A it was discovered that the pump shaft had sheared at the impeller end.

The pump manufacturer and supplier representatives have been oc site and pump shaft breakage evaluations are now in progress.

C' ' esignation of Apparent Cause: l k' ( . .

The cause-of this event is presently being evaluated. Upon determina-

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tion of cause a revision to th*is report will be submitted.

9. Analysis of Occurrence:

No hazard to the health and safety of the plant or general public as plant was defueled.

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10. Corrective Action:

Corrective actions are presently being formulated by the pump manufact-urer and supplier.

11. Failure Data:

This is the second occurrence of an event of this type.

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