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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With 990827 Ltr ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML18152B7261999-01-21021 January 1999 LER 99-001-00:on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable ML18152B5811998-12-16016 December 1998 LER 98-013-00:on 981122,turbine/reactor Trip on High SG Level Occurred.Caused by Instrument Failure.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B5781998-12-16016 December 1998 LER 98-014-00:on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened ML18152B7041998-12-0101 December 1998 LER 98-012-00:on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With 981201 Ltr ML18152B6161998-11-0606 November 1998 LER 98-011-00:on 981008,diesel Driven Fire Pump Failed to Start During Performance of Monthly Operability Test.Caused by Faulty Overspeed Trip Device Failure.Diesel Driven Fire Pump Declared Inoperable ML18152B6081998-10-23023 October 1998 LER 98-010-01:on 980715,intake Canal Level Probes Were Inoperable Due to Marine Growth.Caused by Design of Canal Level Instrumentation.Canal Level Probes Will Continue to Be Monitored More Closely ML18152B7811998-07-31031 July 1998 LER 98-010-00:on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status ML18153A2581998-06-0303 June 1998 LER 98-009-00:on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed ML18152B8241998-05-22022 May 1998 LER 98-008-00:on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed ML18152B7951998-04-29029 April 1998 LER 98-007-00:on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6 ML18153A2521998-04-22022 April 1998 LER 98-005-01:on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame ML18153A2511998-04-22022 April 1998 LER 98-006-00:on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced ML18153A2391998-03-13013 March 1998 LER 98-005-00:on 980212,fire Watch Insp Frequency Exceeded One H Occurred.Category 2 Root Cause Evaluation Being Conducted to Determine Cause of Event.Station Deviation Issued ML18153A2341998-03-0909 March 1998 LER 98-003-00:on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A2251998-03-0404 March 1998 LER 98-002-00:on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket ML18153A2201998-02-0606 February 1998 LER 98-001-00:on 980108,deficient Test Due to Faulty Test Equipment Resulted in TS Violation.Caused by Faulty Vibration Analyzer Cable or Loose Connection.Station Deviation Rept Was submitted.W/980206 Ltr ML18153A2071998-01-13013 January 1998 LER 97-012-01:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Two Breakers in Security Distribution Panel.Reset Affected Breakers Which Restored Power to Security Systems & Affected Doors ML18153A2101998-01-13013 January 1998 LER 97-009-01:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Caused by Inadequate Maint of Intake Canal Level Probes.Subject Probes Were Cleaned, Tested Satisfactorily & Returned to Operable Status ML18153A1911997-11-26026 November 1997 LER 97-011-00:on 971030,determined That Periodic Test Procedures for Testing Reactor Trip Bypass Breakers Did Not Test Manual Undervoltage Trip.Caused by mis-interpretation of Term in-service. Procedures Revised ML18153A1971997-11-26026 November 1997 LER 97-012-00:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Breaker in Security Distribution Panel in Central Alarm Station (CAS) Panel.Breakers in Affected CAS Panel Reset ML18153A1921997-11-25025 November 1997 LER 97-010-00:on 971028,discovered Missed Fire Protection Surveillance Pt.Caused by Personnel Error.Satisfactorily Completed PT Procedure 0-OPT-FP-009 & Diesel Driven Fire Pump 1-FP-P-2 Declared operable.W/971125 Ltr ML18153A1831997-11-12012 November 1997 LER 97-009-00:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Cause Indeterminate.Divers Inspected,Cleaned & Returned Probes to Operable Status & Initiated Interdepartmental Team to Investigate Cause ML18153A1791997-11-0707 November 1997 LER 97-008-00:on 971011,invalid Actuation of ESF Occurred. Caused by Personnel Errors.Main CR Bottled Air Sys Isolated & Containment Hydrogen Analyzer Heat Tracing Actuation Signal Reset ML18153A1721997-10-30030 October 1997 LER 97-007-00:on 970930,determined That Plant Was Outside App R Design Basis Due to Vital Bus Isolation Issue.Caused by Personnel Error.Installed Circuit Protective Device During Oct 1997 Refueling Outage ML18153A1421997-06-10010 June 1997 LER 97-001-01:on 970123,shutdown Occurred Due to Drain Line Weld Leak.Inspected & Tested Turbine Trip Actuation circuitry.W/970610 Ltr ML18153A1391997-05-28028 May 1997 LER 97-005-00:on 970502,Unit 1 Power Range Nuclear Instrumentation Was Inoperable Due to Personnel Error.Sro & STA That Were Involved in Event Were Counseled ML18153A1291997-04-18018 April 1997 LER 97-006-00:on 970320,loss of Refueling Integrity Due to Inadequate Containment Closure Process & Verification.Fuel Movement Stopped IAW Action Statement Requirements of TS 3.10.B.W/970418 Ltr ML18153A1281997-04-15015 April 1997 LER 97-004-00:on 970317,main Steam Safety Valve Was Outside as Found Setpoint Tolerance.Specific Cause Unknown,However, Minor Setpoint Drift Can Be Expected.No Immediate Corrective Actions performed.W/970415 Ltr ML18153A1241997-04-0808 April 1997 LER 97-002-01:on 970116,one Train of Auxiliary Ventilation Sys Was Inoperable Outside of Ts.Caused by Personnel Error. Submitted Deviation Rept Re Reverse Rotation of Fan & Work Request to Adjust linkage.W/970408 Ltr ML18153A1191997-03-19019 March 1997 LER 97-001-00:on 970218,manual Reactor Trip & ESF Actuation Occurred Due to Loss of EHC Control Power.Caused by Momentary Short.Relay Card Was replaced.W/970319 Ltr ML18153A1201997-03-19019 March 1997 LER 97-003-00:on 970219,loss of Pressurizer Heaters Resulted in Manual U1 Trip & U2 ESF Actuation.Caused by Loss of Group C Pressurizer Proportional Heaters.Reactor Trip Breakers Were Verified open.W/970319 Ltr ML18153A1131997-02-20020 February 1997 LER 97-001-00:on 970123,shutdown Occurred Due to Steam Drain Line Weld Leak.Management Was Notified & Shift Supervisor Invoked Requirements of TS 4.15.C.1.W/undtd Ltr ML18153A1101997-02-13013 February 1997 LER 97-002-00:on 970116,one Train of Auxiliary Ventilation Sys Declared Inoperable.Caused by Personnel Error.Properly Adjusted Damper 1-VS-MOD-58B & Exited Seven Day LCO on 970116.W/970214 Ltr ML18153A0951997-01-0202 January 1997 LER 97-002-00:on 961213,automatic Reactor Trip Occurred During Planned Shutdown.Caused by Steam Flow/Feedwater Flow Mismatch.Rps Functioned as Designed & Plant Placed in Hot Shutdown ML18153A0931996-12-12012 December 1996 LER 96-008-00:on 961112,water Gas Decay Tank Oxygen Analyzer Pressure Sensors Inoperable Due to Vendor Supplied Equipment Not Meeting Procurement specifications.Post-implementation Procedures Revised & Transducers replaced.W/961212 Ltr ML18153A0691996-09-19019 September 1996 LER 96-007-00:on 960821,failed to Complete Fire Detection Zone Inspections within Required Time Period.Caused by Personnel Error.Counseled Personnel Re Fire Detection Zone Inspections & Revised Fire Watch training.W/960920 Ltr ML18153A0481996-08-26026 August 1996 LER 96-005-00:on 960803,manual Reactor Trip.Caused by Loss of Electro Hydraulic Control Pressure.Repaired Two Compression Fitting Union Connections on Leaking Fitting & Performed Evaluations on Other tubing.W/960826 Ltr ML18153A0521996-08-20020 August 1996 LER 96-004-01:on 960510,discovered Hydrogen Analyzers Inoperable.Caused by Procedural Deficiencies.Implemented Permanent Changes to Hydrogen Analyzer Instrument Calibr Procedures.W/960820 Ltr ML18153A0321996-07-30030 July 1996 LER 96-006-01:on 960618,anti-corrosion Coating Had Not Been Reapplied to Station Battery 2B.Caused by Procedural Error in That Verbatim TS Compliance Not Reflected in Procedures. Coating Was Applied to batteries.W/960730 Ltr ML18153A0281996-07-17017 July 1996 LER 96-006-00:on 960618,failed to Apply anti-corrosion Coating to Station Battery 2B.Caused by Procedural Error. Applied anti-corrosion Coating to Batteries & Revised TS 4.6.C.1.f Re Battery Coating requirements.W/960717 Ltr ML18153A0141996-07-0202 July 1996 LER 96-004-00:on 960606,turbine/reactor Trip Occurred.Caused by High Level in Steam Generator B.Placed Plant in Hot Shutdown Condition,Calculated Shutdown Margin & Monitored Critical Safety Function Status trees.W/960702 Ltr 1999-08-27
[Table view] Category:RO)
MONTHYEARML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With 990827 Ltr ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML18152B7261999-01-21021 January 1999 LER 99-001-00:on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable ML18152B5811998-12-16016 December 1998 LER 98-013-00:on 981122,turbine/reactor Trip on High SG Level Occurred.Caused by Instrument Failure.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B5781998-12-16016 December 1998 LER 98-014-00:on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened ML18152B7041998-12-0101 December 1998 LER 98-012-00:on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With 981201 Ltr ML18152B6161998-11-0606 November 1998 LER 98-011-00:on 981008,diesel Driven Fire Pump Failed to Start During Performance of Monthly Operability Test.Caused by Faulty Overspeed Trip Device Failure.Diesel Driven Fire Pump Declared Inoperable ML18152B6081998-10-23023 October 1998 LER 98-010-01:on 980715,intake Canal Level Probes Were Inoperable Due to Marine Growth.Caused by Design of Canal Level Instrumentation.Canal Level Probes Will Continue to Be Monitored More Closely ML18152B7811998-07-31031 July 1998 LER 98-010-00:on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status ML18153A2581998-06-0303 June 1998 LER 98-009-00:on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed ML18152B8241998-05-22022 May 1998 LER 98-008-00:on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed ML18152B7951998-04-29029 April 1998 LER 98-007-00:on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6 ML18153A2521998-04-22022 April 1998 LER 98-005-01:on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame ML18153A2511998-04-22022 April 1998 LER 98-006-00:on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced ML18153A2391998-03-13013 March 1998 LER 98-005-00:on 980212,fire Watch Insp Frequency Exceeded One H Occurred.Category 2 Root Cause Evaluation Being Conducted to Determine Cause of Event.Station Deviation Issued ML18153A2341998-03-0909 March 1998 LER 98-003-00:on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A2251998-03-0404 March 1998 LER 98-002-00:on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket ML18153A2201998-02-0606 February 1998 LER 98-001-00:on 980108,deficient Test Due to Faulty Test Equipment Resulted in TS Violation.Caused by Faulty Vibration Analyzer Cable or Loose Connection.Station Deviation Rept Was submitted.W/980206 Ltr ML18153A2071998-01-13013 January 1998 LER 97-012-01:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Two Breakers in Security Distribution Panel.Reset Affected Breakers Which Restored Power to Security Systems & Affected Doors ML18153A2101998-01-13013 January 1998 LER 97-009-01:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Caused by Inadequate Maint of Intake Canal Level Probes.Subject Probes Were Cleaned, Tested Satisfactorily & Returned to Operable Status ML18153A1911997-11-26026 November 1997 LER 97-011-00:on 971030,determined That Periodic Test Procedures for Testing Reactor Trip Bypass Breakers Did Not Test Manual Undervoltage Trip.Caused by mis-interpretation of Term in-service. Procedures Revised ML18153A1971997-11-26026 November 1997 LER 97-012-00:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Breaker in Security Distribution Panel in Central Alarm Station (CAS) Panel.Breakers in Affected CAS Panel Reset ML18153A1921997-11-25025 November 1997 LER 97-010-00:on 971028,discovered Missed Fire Protection Surveillance Pt.Caused by Personnel Error.Satisfactorily Completed PT Procedure 0-OPT-FP-009 & Diesel Driven Fire Pump 1-FP-P-2 Declared operable.W/971125 Ltr ML18153A1831997-11-12012 November 1997 LER 97-009-00:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Cause Indeterminate.Divers Inspected,Cleaned & Returned Probes to Operable Status & Initiated Interdepartmental Team to Investigate Cause ML18153A1791997-11-0707 November 1997 LER 97-008-00:on 971011,invalid Actuation of ESF Occurred. Caused by Personnel Errors.Main CR Bottled Air Sys Isolated & Containment Hydrogen Analyzer Heat Tracing Actuation Signal Reset ML18153A1721997-10-30030 October 1997 LER 97-007-00:on 970930,determined That Plant Was Outside App R Design Basis Due to Vital Bus Isolation Issue.Caused by Personnel Error.Installed Circuit Protective Device During Oct 1997 Refueling Outage ML18153A1421997-06-10010 June 1997 LER 97-001-01:on 970123,shutdown Occurred Due to Drain Line Weld Leak.Inspected & Tested Turbine Trip Actuation circuitry.W/970610 Ltr ML18153A1391997-05-28028 May 1997 LER 97-005-00:on 970502,Unit 1 Power Range Nuclear Instrumentation Was Inoperable Due to Personnel Error.Sro & STA That Were Involved in Event Were Counseled ML18153A1291997-04-18018 April 1997 LER 97-006-00:on 970320,loss of Refueling Integrity Due to Inadequate Containment Closure Process & Verification.Fuel Movement Stopped IAW Action Statement Requirements of TS 3.10.B.W/970418 Ltr ML18153A1281997-04-15015 April 1997 LER 97-004-00:on 970317,main Steam Safety Valve Was Outside as Found Setpoint Tolerance.Specific Cause Unknown,However, Minor Setpoint Drift Can Be Expected.No Immediate Corrective Actions performed.W/970415 Ltr ML18153A1241997-04-0808 April 1997 LER 97-002-01:on 970116,one Train of Auxiliary Ventilation Sys Was Inoperable Outside of Ts.Caused by Personnel Error. Submitted Deviation Rept Re Reverse Rotation of Fan & Work Request to Adjust linkage.W/970408 Ltr ML18153A1191997-03-19019 March 1997 LER 97-001-00:on 970218,manual Reactor Trip & ESF Actuation Occurred Due to Loss of EHC Control Power.Caused by Momentary Short.Relay Card Was replaced.W/970319 Ltr ML18153A1201997-03-19019 March 1997 LER 97-003-00:on 970219,loss of Pressurizer Heaters Resulted in Manual U1 Trip & U2 ESF Actuation.Caused by Loss of Group C Pressurizer Proportional Heaters.Reactor Trip Breakers Were Verified open.W/970319 Ltr ML18153A1131997-02-20020 February 1997 LER 97-001-00:on 970123,shutdown Occurred Due to Steam Drain Line Weld Leak.Management Was Notified & Shift Supervisor Invoked Requirements of TS 4.15.C.1.W/undtd Ltr ML18153A1101997-02-13013 February 1997 LER 97-002-00:on 970116,one Train of Auxiliary Ventilation Sys Declared Inoperable.Caused by Personnel Error.Properly Adjusted Damper 1-VS-MOD-58B & Exited Seven Day LCO on 970116.W/970214 Ltr ML18153A0951997-01-0202 January 1997 LER 97-002-00:on 961213,automatic Reactor Trip Occurred During Planned Shutdown.Caused by Steam Flow/Feedwater Flow Mismatch.Rps Functioned as Designed & Plant Placed in Hot Shutdown ML18153A0931996-12-12012 December 1996 LER 96-008-00:on 961112,water Gas Decay Tank Oxygen Analyzer Pressure Sensors Inoperable Due to Vendor Supplied Equipment Not Meeting Procurement specifications.Post-implementation Procedures Revised & Transducers replaced.W/961212 Ltr ML18153A0691996-09-19019 September 1996 LER 96-007-00:on 960821,failed to Complete Fire Detection Zone Inspections within Required Time Period.Caused by Personnel Error.Counseled Personnel Re Fire Detection Zone Inspections & Revised Fire Watch training.W/960920 Ltr ML18153A0481996-08-26026 August 1996 LER 96-005-00:on 960803,manual Reactor Trip.Caused by Loss of Electro Hydraulic Control Pressure.Repaired Two Compression Fitting Union Connections on Leaking Fitting & Performed Evaluations on Other tubing.W/960826 Ltr ML18153A0521996-08-20020 August 1996 LER 96-004-01:on 960510,discovered Hydrogen Analyzers Inoperable.Caused by Procedural Deficiencies.Implemented Permanent Changes to Hydrogen Analyzer Instrument Calibr Procedures.W/960820 Ltr ML18153A0321996-07-30030 July 1996 LER 96-006-01:on 960618,anti-corrosion Coating Had Not Been Reapplied to Station Battery 2B.Caused by Procedural Error in That Verbatim TS Compliance Not Reflected in Procedures. Coating Was Applied to batteries.W/960730 Ltr ML18153A0281996-07-17017 July 1996 LER 96-006-00:on 960618,failed to Apply anti-corrosion Coating to Station Battery 2B.Caused by Procedural Error. Applied anti-corrosion Coating to Batteries & Revised TS 4.6.C.1.f Re Battery Coating requirements.W/960717 Ltr ML18153A0141996-07-0202 July 1996 LER 96-004-00:on 960606,turbine/reactor Trip Occurred.Caused by High Level in Steam Generator B.Placed Plant in Hot Shutdown Condition,Calculated Shutdown Margin & Monitored Critical Safety Function Status trees.W/960702 Ltr 1999-08-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18152A2811999-10-12012 October 1999 Technical Basis for Elimination of Nozzle Inner Radius Insps (for Nozzles Other than Reactor Vessel),Technical Basis for ASME Section XI Code Case N-619. ML18152B3531999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Surry Power Station,Units 1 & 2.With 991012 Ltr ML18152B6651999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Surry Power Station Units 1 & 2.With 990915 Ltr ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With 990827 Ltr ML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18151A3981999-08-13013 August 1999 SPS Unit 2 ISI Summary Rept for 1999 Refueling Outage. ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18152B3791999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Surry Power Station,Units 1 & 2.With 990811 Ltr ML18152B3911999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Surry Power Station,Units 1 & 2.With 990713 Ltr ML18152B4341999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Surry Power Station,Units 1 & 2.With 990614 Ltr ML20195E2401999-05-31031 May 1999 Rev 2 to COLR for SPS Unit 2 Cycle 16 Pattern Ag ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML18152B4161999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Surry Power Station Units 1 & 2.With 990512 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML18152B6511999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Surry Power Station Units 1 & 2 ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML18152B7331999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Surry Power Station,Units 1 & 2.With 990310 Ltr ML18152B5421999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Surry Power Station,Units 1 & 2.With 990210 Ltr ML18151A3031999-01-29029 January 1999 ISI Summary Rept for 1998 Refueling Outage,Including Form NIS-1, Owners Rept for ISIs & Form NIS-2, Owners Rept for Repairs & Replacements. ML18152B7261999-01-21021 January 1999 LER 99-001-00:on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable ML18152B6011998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Surry Power Station,Units 1 & 2.With 990115 Ltr ML18152B5781998-12-16016 December 1998 LER 98-014-00:on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B5811998-12-16016 December 1998 LER 98-013-00:on 981122,turbine/reactor Trip on High SG Level Occurred.Caused by Instrument Failure.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened ML18152B7041998-12-0101 December 1998 LER 98-012-00:on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With 981201 Ltr ML18152B7081998-11-30030 November 1998 Rev 0 to COLR for Surry 1 Cycle 16,Pattern Un. ML18152B5721998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Surry Power Station,Units 1 & 2.With 981214 Ltr ML18152B6161998-11-0606 November 1998 LER 98-011-00:on 981008,diesel Driven Fire Pump Failed to Start During Performance of Monthly Operability Test.Caused by Faulty Overspeed Trip Device Failure.Diesel Driven Fire Pump Declared Inoperable ML18152B6241998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Surry Power Station Units 1 & 2.With 981111 Ltr ML18152B6081998-10-23023 October 1998 LER 98-010-01:on 980715,intake Canal Level Probes Were Inoperable Due to Marine Growth.Caused by Design of Canal Level Instrumentation.Canal Level Probes Will Continue to Be Monitored More Closely ML18152B6881998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Surry Power Station Units 1 & 2.With 981012 Ltr ML18153A3271998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Surry Power Station,Units 1 & 2 ML18152B7811998-07-31031 July 1998 LER 98-010-00:on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status ML18153A3161998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Surry Power Station Units 1 & 2.W/980807 Ltr ML18152B7621998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Surry Power Station,Units 1 & 2.W/980707 Ltr ML18153A2581998-06-0303 June 1998 LER 98-009-00:on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML18153A3141998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Surry Power Station,Units 1 & 2.W/980610 ML18152B8241998-05-22022 May 1998 LER 98-008-00:on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed ML18152B8161998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Surry Power Station Units 1 & 2.W/980508 Ltr ML18152B7951998-04-29029 April 1998 LER 98-007-00:on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6 ML18153A2511998-04-22022 April 1998 LER 98-006-00:on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced ML18153A2521998-04-22022 April 1998 LER 98-005-01:on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame ML20217P9941998-04-0707 April 1998 Safety Evaluation Granting Licensee Third 10-yr Inservice Insp Program Relief Requests SR-018 - Sr-024 ML18153A2951998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Sps,Units 1 & 2.W/ 980408 Ltr ML18153A2391998-03-13013 March 1998 LER 98-005-00:on 980212,fire Watch Insp Frequency Exceeded One H Occurred.Category 2 Root Cause Evaluation Being Conducted to Determine Cause of Event.Station Deviation Issued ML18153A2341998-03-0909 March 1998 LER 98-003-00:on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A2251998-03-0404 March 1998 LER 98-002-00:on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket 1999-09-30
[Table view] |
Text
ACCELERATE:D DISjRIBUTION DEMONST~TION SYSTElv1 REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:90013310127 DOC.DATE: 90/08/24 NOTARIZED: NO DOCKET#
FACIL:50-281 Surry Power Station, Unit 2, Virginia Electric & Powe 05000281 AUTH.NAME AUTHOR AFFILIATION KANSLER,M.R. Virginia Power (Virginia Electric & Power Co.)
RECIP.NAME RECIPIENT AFFILIATION R
SUBJECT:
LER 89-019-01:on 891122,svc water MOVs to RSHXs inoperable due to personnel error in removing flood protection.
W/9 ltr. D DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR } ENCL TITLE: 50.73/50.9 Licensee Event Report (LER),-Yncident7Rpt, etc.
/ SIZE: s s I
I NOTES:lcy NMSS/IMSB/PM. 05000281 A
RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL D PD2-2 IJ1. 1 1 PD2-2 PD 1 1 BUCKLEY 1. B 1 1 D INTERNAL: ACNW 2 2 ACRS 2 2 s AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 NRR/DET/ECMB 9H 1 1 NRR/DET/EMEB9H3 1 1 NRR/DLPQ/LHFBll 1 1 NRR/DLPQ/LPEBlO 1 1 NRR/DOEA/OEABll 1 1 NRR/DREP/PRPBll 2 2 NRR/DST/SELB 8D .1 1 NRR/DST/SICB.7E NRR/DST/SRXB 8E 1
1 1
1 d~LB8g~ 1 1
1 1
RES/DSIR/EIB 1 1 RGN2 FILE 01 1 1 EXTERNAL: EG&G BRYCE,J.H 3 3 L ST LOBBY WARD 1 1 NRC PDR 1 1 NSIC MAYS,G 1 1 NSIC MURPHY,G.A 1 1 NUDOCS FULL TXT 1 1 R
NOTES: 1 1 I
D S I I
Al D
D NOTE TO ALL "RIDS" RECIPIENTS:
s PLEASE HELP US TO REDUCE WASTE! CONT ACT THE DOCUMENT CONTROL DESK, ROO!'vl Pl-37 (EXT. 20079) TO ELHvllNATE YOUR NAME FROl\1 DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 34 ENCL 34
Virginia Electric and Power Company Surry Power Station P. 0. Box 315 Surry, Virginia 23883 August 24, 1990.
U. S. Nuclear Regulatory Commission Serial No.: 90-528 Document Control Desk Docket No.: 50-281 Washington, D. C. 20555 License *No.: DPR-37 Gentlemen:
Pursuant to* Surry Power Station Technical Specifications, Virginia Electric and Power Company hereby submits the following updated Licensee Event Report for Unit 2.
REPORTNUMBER 89-019-01 This report has been reviewed by the Station. Nuclear
- Safety and Operating Committee andl will be reviewed by Corporate Nuclear Safety.
Very truly Enclosure cc: Regional[ Administrator Suite 2900 101 Marietta Street, NW 0 1 ",,t,.,**
~ \
Atlanta, Georgia 30323 I.;
.,1
I"" ___
19-83, unDATED t < REPORT POW 28-06-01 U.S. NUCLlAR REGULATORY COMMISSION AP,.ROVED OMII NO. Jllill-OIIM LICENSEE EVENT REPORT (LERI EXPIRES: l/31/E FACILITY NAME 111 Surry Power Station, Unit 2 IDOCKET NUMIER 121 I
, IOF PAGE 131 01s10101012,s I 1 017 TITLE ,,
Service Water. HOVs to the RSIIXs Inoperable Due to Personnel Error in Removing Flood Protection EVENT DATE IS, LE R NUMBER 16, REPORT DATE 171 OTHER FACILITIES INVOLVED Ill MONTH DAY YEAR YEAR )\ SEQUENTIAL NUMBE" :/ "EVl!IIO"< MONTH NUMBE" DAY" YEAR FACILITY NAMES DOCKET NUMIIERISI 01s1010101 I I 1 I1 21 2 8 9 sl 9 - o J1 I 9-- oJ 1 ois 2 I4 9 Jo 0 1s10 IO I OI I I THIS REFORT IS SUBMITTED PURSUA';T TO THE REOUIREMEI\ITS OF 10 CFR i: IC"'I~* :,r,1 o* ';0'1 C' '"~ *o**OrN*f'lg/ f11l OPERATII\IG MOOE 19, N 20.1102101 20.-lcl
50.73111121h*I
-- 73.71101 POWER zo.*10&1,1111m IIO.:Nlcl111 I0.731all21M 73.711cl
-- LEVEL CIDI I 01 o,o zo.1106l1ICIIIWI II0.311cll2l II0~7311112Hriil
- OTHEII (SJ>><ify in A/IIWCI belot111 *nd in T*xt. NRC Form 20.*IOll11f1 Hilll
..x II0.73111121111
- I0.731111211*Hll1Al .JISliA/
illil\l:l\:\\ll\\\l\l\ll\ll\l\l:llll\lll\\\\\\\\l\:\lllllllll\\lll:i\
- =:::::::::::::::::::::::::::::::::::::::::::::::::::::::::::::::::
- ZO.*IOIII 111llt.l 20.00111,11111,1 II0.7311112HMI I0.731all2111111 IID.731111211.iiillll II0.731tll2Hxl LICENSEE CONTACT FOR THIS LEA 1121 NAME TELEPHONE NUMBER AREA CODE M. R. Kansler, Station Manager 81014 3j 5 I 71 -13 I 11814 COMPLETE ONE LINE FC>R EACH ~NENT FAILUIIE DESCRIIED IN THIS IIEl'ORT 1131 CAUSE SYSTEM COMPONENT MANUFAC-TURER REPORTABLE TO I\IPRDS
- <>:::::ir:::i: }(}? CAUSE SYSTEM COMPONENT MANUFAC-
.TURER
~EPORTABLE TO NPROS i::;=:1;=1::=ttt:::::!::'.:::rm: r 1{}??'}{\\\\(({*,:;:_..... . . ::::::::!\:\\\ti:\\\:(l(\j\\\:(f\:\\ii I I I I I I I :---*-:-:-:-*-:-:-:-:,:-:-:-:-:-:-:-:-:-: I I I I I I I I I I I I I I :l:i::lili:iiiil:!:!:ililllifi~i::llf\/liii:!i!!!l'. I I I I I I I liiilliiii!iililil!!!l!lil!jjlj/lllllllliilllllllli aw,LEMENTAL IIDOIIT IJOIICTID 11'1 MONTH DAY YEAII EXPECTED
~
IUIMISSION l Yl!I /If..-.~,. EXf'ECTED .SUIIMIS$10N DATE/ NO DATE 1151 I I I AISTflACT /Limit ro r400 u,ac~. ,.,., ,,>Pro*m1*r,1,- fiftHn tin11**11>>C1 n,,i,9-,,;ran l,naJ-1111 On November 22, 1989 at 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br />, Unit 2 was at *hot shutdown. During routine walkdowns in the Unit 2 turbine building, in preparation for a unit startup, it was noted that the flood protection oikes had* been removed from one side of the valve pits for the service water (SW) supply motor operated valves (MOVs) to the recirculation spray heat exchangers (RSHXs). Work was in progress near the valve pit area for replacement of the SW piping. The affected valves, MOV-SW-
- 203A/B/C/D, were declared inoperable and a 30 hour3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> action statement to cold shutdown was entered. ..
A four hour non-emergency report was made to the Nuclear Regulatory Commission (NRC) pursuant to 10CFR50.72, paragraph (b)(2)(i) on the November 22, 1989 event. The dikes were replaced on November 22, 1989 at 2053. On December 13, 1989 with Units 1 and 2 at 100% power, it was discovered that backflow preventers were not in place m the two emergency* switchgear room floor drains. A flood watch was already in place at the time of discovery of the missing devices because of other concerns identified during engin,eering review. The backflow preventers were reinstalled on January 31, 1990.
NIIC,_ . .19-131
U.S. NUCLEAR REGULATORY COMMISSION NRC FORM 366A APPROVEO 0MB NO. 3150-0104 16-891 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICEINSEE EVENT REPORT (LER) *INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH IP-530). U.S. NUCLEAR REGULATORY COMMISSION. WASHINGTON. DC 20555. AND TO 1*HE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER 121 LER NUMBER (6)
- PAGE 131 Surry Power Station, Unit 2 0 j 5 IO IO IO I2 J 8 I 1 819 - 0 I 11 9 - 0Jl O 12 OF O17 TEXT (If more space;, n,quired, uu additional NRC Form 3ti&4 '*11171
- 1. 0 DESCRIPTION OF THE EVENT On November 22, 1989 at 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br />, Unit 2 was at hot shutdown * (HSD).
- During routine walkdowns in the Unit 2 turbine building, in preparation for a unit startup, it was noted that the.* flood protection dikes *(EiIS:-BAF) were removed from one side of the valve pits for the service water. (SW) (EIIS-BI) supply motor operated valves (MOVs) (EIIS-ISV) to the
. recirculation spr.ay heat exchangers (RSHXs) (MOV-SW-203A/B/C/D). At the time of- the discovery, work was in progress near the valve pit area for' replacement of the SW p1pmg to the mam control room (MCR)/emergency switchgear room (ESGR) chillers and charging pump SW pumps. The work was being performed 1n accordance with design change procedure DC-87-34. The flood dikes were removed on October 25, 1989 Ill accordance with a field change to the procedure to facilitate insta11ation of missile protection plates for the new SW piping.
WhHe the dikes were removed, the Unit 2 reactor coolant
- syte.m exceeded a temperature and pressure of 350 degrees Fah:renheit/450 psig
- during two time periods: from November 6 at 0555 hours0.00642 days <br />0.154 hours <br />9.176587e-4 weeks <br />2.111775e-4 months <br /> to Novembver 7 at 1000 hours0.0116 days <br />0.278 hours <br />0.00165 weeks <br />3.805e-4 months <br /> and from November 20 at 2256 hours0.0261 days <br />0.627 hours <br />0.00373 weeks <br />8.58408e-4 months <br /> until the dikes were reinstalled on November 22 at 2053 hours0.0238 days <br />0.57 hours <br />0.00339 weeks <br />7.811665e-4 months <br />. The RSHXs are required to be operable whenever unit conditions exceed 350 degrees Fahrenheit/450 psig.
The four (4) SW supply MOVs
- to the RSHXs were declared ino1,>erable at 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br />, and a 30 hour3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> action statement to ach:leve cold shutdown was entered. A four hour non-emergency report was made to the NRC pursuant to 10CFR50.72, paragraph (b)(2)(i).
~
NRi; FORM 366A (6-89)
U.S. NUCLEAR REGULATORY COMMISSION APPROVEO oM*B NO. 3150-0104 EXPIRES: 4/30/92 ESTIMATED BU~DEN PER. RESPONSE :ro COMPLY *wTH THIS LICEI\ISEE EVENT REPORT (LEB) INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD
.. . TEXT CONTINUATION COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P-5301. U.S. NUCLEAR REGULATORY COMMISSION. WASHINGTON. DC 20555. AND TO 1HE PAPERWORK REDUCTION PROJECT (3150-0104). OFFICE OF MANAGEMENT AND BUDGET. WASHINGTON. DC 20503.
DOCKET NUMBER (21 LER NUMBER (6) . PAGE (3)
FACILITY NAME Ill.
YEAR
. Surry* Power Station, Unit 2 0 5 0 0 0 2 8 1 8. 9 - 0 1 9 - 0 1 0 *3 OF O 7 TEXT /ff mar-. :,pace is raquir-.d, use *ddition*I NRC Form 366A'*I 117)
On December 13, with Unit 1 and 2 at 100% power, during walkdowns - performed to identify potential deficiencies. that may exist in flood protection devices
- for safety related equipment, it was determined that the backflow preventers (EIIS-BFP) were not in place in the two ESGR floor drains (EIIS-PRN). These backflow devices were designed to prevent backflow of *water *from the turbine building, through the floor drains, into the ESGR in the event of a turbine. building flood.
- 2. 0 SAF:ETY CONSEQUENCES AND IMPLICATIONS -
The reci~culation spray system consists of four independent traillls, each containing a pump, heat _exchanger
- and discharge spra,y ring.
- The system is* required to be operable whenever the reactor coolant system temperature *and. pressure is greater than 35_0 degrees Fahrenheit/450 psig. The recirculation . spray (RS) system is used in conjunction with the containment spray
- system (EHS-BE) following a design basis accident (DBA) to depressurize the
- containment* below atmospheric *pressure and maintain it depressurized for an extended period. The RS systiem also provides for long-term heat removal capability folh>wing a DBA. Each of the four trains is 50% capacity.
Service water is used as *the cooling medium for the heat exchangers and is provided through
- the subject MO Vs. The MOVs are
- 1ocated in two adjacent valve pits at the 9' 6" elevation of the turbine building. The valves are physically located below the floor elevation. Analyses conducted
- during 1972.:74 determined that the safety related MOVs io the RSHXs could be adversely affected by flooding caused* by circulating water (CW) or fire protection water piping rupture. The dikes were _installed to ensure the MOV s would remain operable in the event of flooding.
U.S. NUCLEAR REGULATORY COMMISSION NRG.FORM 366A APPROVED 0MB NO. 3150-0104 16-891 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICEMSEE EVENT REPORT (LER) INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION *AND REPORTS MANAGEMENT BRANCH IP-5301. U.S. NUCLEAR REGULATORY COMMISSION. WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT 13150-01041, OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
DOCKET NUMBER 121 LER NUMBER 161 PAGE 131 FACILITY NAME 111 REVISION YEAR NUMBER Surry Power Station, Unit 2 0 5 0 0 0 2 8 1 8 9 - 0 1. 9 - 0 1 0 4 OF O 7 TEXT /ff more Sf!"ctJ is n,quimd, u.., oddition*I NRC Form 366A '*I 1171 The consequences of the dikes being removed is minimized by the following:
Water level . sensors are provided m pits located near the CW Hne expansion . joints (a potential source of *flooding).* These expa.nsion joints were replaced with safety* related components in both units during the . most recent outages making the probability of their failure remote.
- Alarms are provided in the control room to quickly alert the operators . of an abnormal condition. Operators would* take the necessary actions to e*nsure the plant was maintained in* a safe* condition following recei.ipt of an alarm.
Floor drains in the turbine building, Unit* 1 ESGR, and cable tunnel are connected to a common piping system . that drains into the turbine building sumps. Flood dikes are provided .at entrances to*. the ESGRs to prevent water from entering the rooms in the event of* flooding in adjoining areas. With the backflow devices removed from the floor drains, the potential existed for water to enter the ESGR from the adjoining turbine building in the event of a turbine building flood.
The consequences of the backflow devices being removed are minimized by the following:
Ther. e are two drains, each 3" in diameter, in the ESGR. The wate:r level in the turbine building is not expected to exceed one foot during the postulated turbine
Consequently, the flow through the drains irito the ESGR would be a.t a low rate due to the low hydraulic head. This low rate, coupled with the early warning of a turbine building flood provided by the level sensors discussed above, would allow operators . sufficient time to take the necessary corrective actions prior to the water level in the ESGR obtaining a height that could *affect safety related equipment.
NRC FORM 366A U.S. NUCLEAR REGULATORY_ COMMISSION APPROVED 0MB NO. 3150-0104 16-891 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICEI\ISEE EVENT REPORT (LER) INFORMATION COLLECTION REQUEST: 50.0 HRS. FORW/IRD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS Tl:.XT CONTINUATION AND REPORTS MANAGEMENT BR_ANCH (P-5301. U.S. NUCLEAR REGULATORY COMMISSION. WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3150-01041, OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME 111 DOCKET NUMBER (21 PAGE 131 LER NUMBER 161 .
YEAR ':::::::*::. SEQUENTIAL ::'.::::? REVISION
- . NUMBER
- :::::::: NUMBER Surry Power Station, Unit 2 01s101010121s11 819 -01119- 011 01s oFol7 TEXT (If more -co is required, use addroonol 1VRC Form 366A'si 1171 In addition, turbine building flooding coincident with a design basis accident is not postulated to occur. Consequently, the health and safety of the £Ublic were not affected.
3.0 CA.!!.S.E.
The event was caused by personnel error. The removal of the dikes was authorized via a field change to Design Change 87-
- 34. The engineers preparing the field change failed to address the controls that would be _required for the re_moval of the dikes. In addition, the documents used to provide the instructions for the removal of the dikes were inadequate and reduced the effectiveness of subsequent
- reviews required for final approval of the field change. The field change controlling document stated that -the revision was necessary to provide
- additional details -and instructions for installation of the new SW line missile protection covers. Removal of the dikes was not specified in the field change controlling document. The instruction to remove the dikes was placed on a revised drawing in the form of a note on a construction detail for the installation of the covers. The note stated *that the dikes were to be removed and reinstalled as required with no stipulation of required unit conditions or required contingency actions.
The backflow devices were originally installed in 1977 as part of a flood protection design change. It could not be determined when or why these devices were -removed.
- 4. 0 IM.ru[EDIATE CORRECTIVE ACTION{S)
The four SW supply MOVs to the RSHXs were declared inopf:rable, and a 30 hour3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> action statement to CSD was entered.
Construction personnel were directed to reinstall the flood dikes.
. U.S. NUCLEAR REGULATORY COMMISSION NRC FORM 366A APPROVED 0MB NO. 3150-0104 (6-891 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT (LERI INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P,530). U.S. NUCLEAR _
REGULATORY COMMISSION; WASHINGTON. DC 20555. AND TO 1'HE PAPERWORK REDUCTION PROJECT (3150-0104). OFFICE OF MANAGEMENT AND BUDGET. WASHINGTON. DC 20503 .
DOCKET NUMBER (21 LER NUMBER (61 . PAGE (3)
FACILITY NAME (11 YEAR Surry Power Station, Unit 2 05000 281 89 0 6 OF O 7 TEXT (If mon, space is n,quired, use eddftion*I NRC Form 366A'sl (171 No immediate actions were required after the. discovery of the miss.ing
- backflow devices since a flood watch had been established earlier as a precaution due to deficiencies in flood protc!ction equipment previously identified. during engineering review.
- 5. 0 ADDITIONAL CORRECTIVE ACTION(S)
The flood dikes were reinstalled at 2053 hours0.0238 days <br />0.57 hours <br />0.00339 weeks <br />7.811665e-4 months <br /> on November 22, 1989, the 30 hour3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> Technical Specification action statement
. was exited.
An ,engineering evaluation was performed
- to allow installation of plugs in the drains as an interim measure until the appropriate backflow devices could be obtained and installed.
The backflow devices were reins.talled on January 31, 1990.
- 6. 0 ACTIONS TO PREVENT RECURRENCE A memorandum describing the removal of the flood dikes was sent to design engineering personnel in,* order to heighten their awareness. The memorandum also reemphasized that instructions for specific work
- for design control documents must be included in the controlling procedure )and not mer~ly added to sketches and drawings.
An engineering review has been initiated to review the commitments and design bases relating to flood protection of safety related equipment. As part of this review, walkdowns of plant areas requiring flood protection .were conducted to identify and document any additional deficiencies. In addition to rninstalling the backflow preventers, cover plates over the component cooling and bearing cooling heat exchanger service water supply valves were replaced with dikes to enhance flood
I I
- U.S. NUCLEAR REGULATORY COMMISSION NRC FORM 366A (6-89) - APPROVED 0MB NO. 3150-0104 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT (LERI INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P-530), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO
'THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME 111 DOCKET NUMBER 121 LER NUMBER (6) PAGE 131 Surry Power Station, Unit 2 0 15 IO ID ID 121 8J l 8J 9 - Oil 19 -0 J l O 17 OF O 17 TEXT /If more .,,.co is required, use additional N8C Form 366A's/ 1171 protection. Draft procedures have been generated to identify the necessary attributes* to be monitored as part of routine verification of the mechanical integrity of existing flood protection -dikes and ESGR backflow devices. These measures -
are to be incorporated into station preventive maintenance schedules.
Flood protection dikes throughout_ the plant . have been stenciled* with a cautionary legend. Cautionary plaques have also been installed near the backflow preventers.
- 7. 0 SIMILAR EVENTS None.
- 8. 0 MANUFACTURER/MODEL NUMBER NIA.