ML18086A504

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Forwards LER 81-007/03L-0.Detailed Event Analysis Encl
ML18086A504
Person / Time
Site: Salem PSEG icon.png
Issue date: 05/11/1981
From: Uderitz R
Public Service Enterprise Group
To: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML18086A505 List:
References
NUDOCS 8105190159
Download: ML18086A504 (3)


Text

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.. PS~G Public Service Electric and Gas Company 80 Park Plaza Newark, N.J. 07101 Phone 201/430-7000 May* 11, 1981 Mr. Boyce H. Grier Director of USNRC Off ice of Inspection and Enforcement Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406

Dear Mr. Grier:

LICENSE NO. DPR-75 DOCKET NO. 50-311 REPORTABLE OCCURRENCE 81-07/03L Pursuant to the requirements of Salem Generating Station Unit No. 2 Technical Specifications, Section 6.9.1, we are submitting Licensee Event Report for Reportable Occurrence 81-07/03L. This report is required within thirty (30) days of the occurrence.

Sincerely yours,

  1. 4'!~~-/j ~

R. A. Uderitz General Manager -

Nuclear Production CC: Director, Office of Inspection and Enforcement (30 copies)

Director, Office of Management Information and Program Control (3 copies) s i

The Ener9y People:*

8105190 /5"~ 95-2001 i3501~1 4 BO

() PS~G

  • Public Service Electric and Gas Company BO Park Plaza Newark, N.J. 07101 Phone 201/430-7000 May 11, 1981 Mr. Boyce H. Grier Director of USNRC Off ice of Inspection and Enforcement Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406

Dear Mr. Grier:

LICENSE NO. DPR-75 DOCKET NO. 50-311 REPORTABLE OCCURRENCE 81-07/03L Pursuant to the requirements of Salem Generating Station Unit No. 2 Technical Specifications, Section 6.9.1, we are submitting Licensee Event Report for Reportable Occurrence 81-07/03L. This report is required within thirty (30) days of the occurrence.

Sincerely yours,

/44~1' ~

R. A. Uderitz General Manager -

Nuclear Production

~fJDirector, Office of Inspection and Enforcement (30 copies)

Director, Office of Management Information and Program Control (3 copies)

The Energy People 95-2001 1350M) 4-c

-816~t§i9

Report Number: 81--03L Report Date: May 11, 1981

~ Occurrence Date: 4/23/81 Facility: Salem Generating Station, Unit 2 Public Service Electric & Gas Company Hancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:

Failure of No. 22 Auxiliary Feedwater Pump to Start CONDITIONS PRIOR TO OCCURRENCE:

Mode 3 - Rx Power 0% - Unit Load 0 MW DESCRIPTION OF OCCURRENCE:

While attempting to start the No. 22 Auxiliary Feedwater Pump, it was discovered that the relay flags for phases A and C on Breaker 2BlD (the pump's feeder breaker) had dropped. Action Statement 3.7.1.2 was entered at 0200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br />. Investigation revealed that the breaker would not latch closed.

This occurrence constituted operation in a degraded mode IAW Technical Specification 6.9.1.9.b.

DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:

Equipment Failure - The wipe of the breaker's trip latch had drifted out of adjustment.

ANALYSIS OF OCCURRENCE:

Technical Specification 3.7.1.2 requires that with one Auxiliary Feedwater Pump inoperable, restore at least three Auxiliary Feed-water Pumps (two capable of being powered from separate vital busses and one capable of being powered by an operable steam supply system) to operable status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or be in hot shutdown within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

CORRECTIVE ACTION:

In accordance with Maintenance Procedure M3D, the wipe of the trip latch was reset to the correct travel. Megger checks of all input phases wer~ made and found to be satisfactory. The breaker was tested satisfactory and the Action Statement terminated at 1100 hours0.0127 days <br />0.306 hours <br />0.00182 weeks <br />4.1855e-4 months <br /> on April 23, 1981.

FAILURE DATA:

General Electric 4 kV Magne-Blast Circuit Breaker Serial #0224A6269-012 Prepared By W. J. Steele SORC Meeting No. Manager - Salem Geerating Station 81-34