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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:RO)
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17265A7621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Re Ginna Npp.With 991008 Ltr ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7471999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Re Ginna Npp.With 990909 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Re Ginna Npp.With 990806 Ltr ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7131999-07-22022 July 1999 Special Rept:On 990407,radiation Monitor RM-14A Was Declared Inoperable.Caused by Failed Communication Link from TSC to Plant Process Computer Sys.Communication Link Was re-established & RM-14A Was Declaed Operable on 990521 ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7211999-07-19019 July 1999 ISI Rept for Third Interval (1990-1999) Third Period, Second Outage (1999) at Re Ginna Npp. ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A7661999-06-30030 June 1999 1999 Rept of Facility Changes,Tests & Experiments Conducted Without Prior NRC Approval for Jan 1998 Through June 1999, Per 10CFR50.59.With 991020 Ltr ML17265A7011999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Re Ginna Npp.With 990712 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17265A6681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Re Ginna Nuclear Power Plant.With 990608 Ltr ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG ML17265A6391999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Re Ginna Nuclear Power Plant.With 990510 Ltr ML17265A6361999-04-23023 April 1999 Part 21 Rept Re Power Supply That Did Not Work Properly When Drawn from Stock & Installed in -25 Vdc Slot.Power Supply Will Be Sent to Vendor to Perform Failure Mode Assessment.Evaluation Will Be Completed by 991001 ML17265A6301999-04-18018 April 1999 Rev 1 to Cycle 28 COLR for Re Ginna Npp. ML17265A6251999-04-15015 April 1999 Special Rept:On 990309,halon Systems Were Removed from Svc & Fire Door F502 Was Blocked Open.Caused by Mods Being Made to CR Emergency Air Treatment Sys.Continuous Fire Watch Was Established with Backup Fire Suppression Equipment ML17265A6551999-04-0909 April 1999 Initial Part 21 Rept Re Mfg Deficiency in Replacement Turbocharger for B EDG Supplied by Coltec Industries. Deficiency Consisted of Missing Drain Port in Intermediate Casing.Required Oil Drain Port Machined Open ML17265A6291999-03-31031 March 1999 Rev 0 to Cycle 28 COLR for Re Ginna Npp. ML17265A6241999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ginna Station.With 990409 Ltr ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A5661999-03-0101 March 1999 Rev 26 to QA Program for Station Operation. ML17265A5961999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Ginna Nuclear Power Plant.With 990310 Ltr ML17265A5371999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Re Ginna Nuclear Power Plant.With 990205 Ltr ML17265A5951998-12-31031 December 1998 Rg&E 1998 Annual Rept. ML17265A5001998-12-21021 December 1998 Rev 26 to QA Program for Station Operation. ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4761998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Re Ginna Nuclear Power Plant.With 981210 Ltr ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4531998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Re Ginna Nuclear Power Plant.With 981110 Ltr ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A4291998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Re Ginna Nuclear Power Plant.With 981009 Ltr 1999-09-30
[Table view] |
Text
~ CATEGORY 1 REGULATORY INFORMATION DISTRIBUTION SYSTEM
~ (RIDS)
ACCESSION NBR:9604150112 DOC.DATE: 96/04/08 NOTARIZED: NO DOCKET FACZL:50-244, Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH. NAME AUTHOR AFFILIATION ST.MARTIN,J.T. Rochester Gas & Electric Corp.
MECREDY,R.C. Rochester Gas & Electric Corp.
RECIP.NAME RECIPIENT AFFILIATION JOHNSON,A.R.
SUBJECT:
LER 96-002-00:on 960307,secondary transient occurred. Caused by oss of B condenser circulating water pump.C/As:
thermography performed.W/960408 ltr.
DISTRIBUTION CODE: ZE22T COPIES RECEIVED:ZTR ENCL SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72). 05000244 Q 0
RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD1-1 PD 1 1 JOHNSON,A 1 1 INTERNAL: ~PD B 2 2 AEOD/SPD/RRAB 1 1 LE 1' NRR/DE/ECGB 1 1 NRR/DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HZCB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRCH/HQMB 1 1 NRR/DRPM/PECB 1 1 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 RES/DSZR/EZB 1 1 RGN1 FILE 01 1 1 0
EXTERNAL: L ST LOBBY WARD 1 1 LITCO BRYCE,J H 2 2 NOAC MURPHYgG ~ A 1 1 NOAC POOREIW. 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 NOTE TO AI L "RIDS" REC?PIENTSI PLEASE HELP US TO REDUCE WASTEl CONTACT THE DOCUMENT CONTROL DESK)
ROOM OWFN 5D 5(EXT. 415.2063) TO ELIMINATE YOUR NAME FROM DTSTRXDUTXON LXSTS FOR DOCUMENTS YOU DON'T NEEDI FUL L TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 25 ENCL 25
Q AND ROCHESTER GAS AIVDFlFCTRIC CORPORATE ~ 89 FAST AVENUE, ROCHESTERhl, Y. 14@'49-OGOl ARFA CODE r 16 546.2700 April 8, 1996 U.S. Nuclear Regulatory Commission Document Control Desk Attn: Allen R. Johnson PWR Project Directorate I-1
. Washington, D.C. 20555
Subject:
LER 96-002, Secondary Transient, Caused by Loss of "B" Condenser Circulating Water Pump, Results in Manual Reactor Trip R.E. Ginna Nuclear Power Plant Docket No. 50-244 In accordance with 10 CFR 50.73, Licensee Event Report System, item (a) (2) (iv), which requires a report of, "Any event or condition that resulted in a manual or automatic actuation of any engineered safety feature (ESF), including the reactor protection system (RPS)", the attached Licensee Event Report LER 96-002 is hereby submitted.
This event has in no way affected the public's health and safety.
Very truly yours, Robert C. Mecredy xc: U.S. Nuclear Regulatory Commission Mr. Allen R. Johnson (Mail Stop 14B2)
PWR Project Directorate I-1 Washington, D.C. 20555 U.S. Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 U.S. NRC Ginna Senior Resident Inspector I~gflAg ) pyP I
/
9604i50ii2 960408 PDR ADOCK 05000244 S PDR
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPIROVED BY OMB NO. 3150-0104 (4-95) ExpIREs 04/30/96 ESTIMATED BURDEN PER RESPONSE To COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUEST: 50.0 HRS.
LICENSEE EVENT REPORT (LER) REPORTED LESSONS LEARNED AAE INCORPORATED INTO THE UCENSING PROCESS ANO FED BACK To INDUSTRY. FORWARD COMMENTS REGARDING BURDEN ESTIMATE To THE (Soe reverse for required number of INFOAMATION ANO RECORDS MANAGEMENT BRANCH IT.6 F33),
digits/characters for each b(ockl U.S. NUCLEAR REGUlATORY COMMISSION, WASHINGTON. DC 20555-0001, AND To THE PAPERWOAK REDUCTION PROJECT FACILITY NAME Il) OOCKET IrUMetR (3) PAGE 13)
R.E. Ginna Nuclear Power Plant 05000244 1OF9 rrLE 14)
Secondary Transient, Caused by Loss of "8" Condenser Circulating Water Pump, Results in Manual Reactor Trip EVENT DATE I5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (6)
FACILITYNAME OCKET NUMBER SEQUEN)1AL REVISION MONTH OAY YEAR NUMBER NUMBER MONTH DAY YEAR ACILITYNAME OOCKET NUMBER 03 07 96 96 002 00 04 08 96 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR E) (Chock one or more) I11)
MODE (9) 20. 2201 (b) 20.2203(a) (2)(v) 50.73(a) (2)(i) 50.73(a)(2)(viii) 20.2203(a) (1) 2o.2203(a)(3) (il 50.73(a)(2)(II) 50.73(a)(2)(x)
POWER LEVEL (10) 97 20.2203(a)(2)(i) 20.2203(al(3) (ii) 50.73(al(2) (iiil 73.71 20.2203(a) (2) (ii) 20.2203(a)(4) X 5O.73(a)(2)(iv) OTHER 20.2203(a)(2) (iii) 50.36(c)(l) 50.73(a)(2)(v) Specrfy m Abstrect be)o W or In NRC Form 366A 20.2203(a) (2)(iv) 50.36(c) (2) 50.73(a)(2)(vii)
LICENSEE CONTACT FOR THIS LER (12)
ELEPHONB NVMBLR )Include Ares Code)
John T. St. Martin - Technical Assistant l716) 771-3641 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESC RIBED IN THIS REPORT (13)
REPORTABLE REPORTABLE CAUSE SYSTEM COMPONENT MANUFACTURER CAUSE SYSTEM COMPONENT MANUFACTURER TO NPRDS To NPRDS SUPPLEMENTAL REPORT EXPECTED (14) MONTH DAY YEAR EXPECTED YES SUBMISSION (If yos, complete EXPECTED SUBMISSION DATEl. X NO DATE (15)
ABSTRACT (Limit to 1400 spaces, I.o., approximately 15 single-spaced typowritton lines) (16)
On March 7, 1996, at approximately 1814 EST, with the plant at approximately 97% steady state reactor power (Mode 1), the "8" condenser circulating water pump tripped. This resulted in a reduction of main condenser heat removal capability. Immediate action was to decrease turbine load to less than 50%, as per procedure AP-CW.1.
However, due to condenser backpressure increasing above the limit for the satisfactory operating region for the main turbine, at approximately 1822 EST, the Shift Supervisor conservatively ordered a manual reactor trip. The Control Room operators performed the actions of procedures E-0 and ES-0.1. Following the reactor trip, all systems operated as designed, and the reactor was stabilized at hot shutdown conditions (Mode 3).
The underlying cause of the tripping of the "8" condenser circulating water pump was due to actuation of the power factor protection relay, which tripped the circuit breaker for the pump. The cause of the reactor trip was manual operator action.
This event is NUREG-1022 Cause Code (E).
Corrective action to prevent recurrence is outlined in Section V.B.
NRC FOAM 366 (4-95)
NRC FORM B66A U.S. NUCLEAR REGULATORY COMMISSION I4.95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITYNAME I1) DOCKET LER NUMBER I6) PAGE I3)
YEAR SEQUENTIAL REVISION NUMBER NUMBER 2 OF 9 R.E. Ginna Nuclear Power Plant 05000244 96 002 00 TEXT llfmore spece is required, use eddi tionel copies of NRC Form 366A/ I17)
PRE-EVENT PLANT CONDITIONS:
The main circulating water system supplies cooling water to the main condensers to condense steam exhausted from the two low pressure turbines. The system consists of two headers, each of which is supplied by a circulating water (CW) pump. Each header supplies a main condenser. The headers are cross-connected upstream of the main condensers to allow for reduced power operations with a single operating CW pump. After passing through the main condensers, CW is returned to the lake via a common discharge canal.
The plant was at approximately 97% steady state reactor power (Mode 1) with no significant activities in progress. On March 7, 1996, at approximately 1814 EST, the Control Room operators received Main Control Board Annunciator J-16 (Motor Off CW-EH Emerg Oil Seal Oil BU), caused by the trip of the "B" CW pump.
The trip of the "B" CW pump was followed by closure of the discharge valve for the "B" CW pump. This resulted in a decrease in total CW flow and an imbalance in CW flow to the two main condensers. This caused a vacuum imbalance between the main condenser hotwells. (There was a loss of approximately 40% of the main condenser heat removal capability due to the CW pump trip.) Since the condensers are connected, the difference in backpressure resulted in condensate water being "pushed" from the "B" hotwell to the "A" hotwell. Voiding of the "B" hotwell resulted in reduction of Net Positive Suction Head (NPSH) to the condensate pumps, thus also reducing main feedwater (MFW) pump suction pressures.
These abnormal conditions developed because the "8" CW pump had tripped rather than having been secured as part of an orderly transition to single CW pump operation. Although the plant can operate at up to 50% power on a single CW pump, the system must first be reconfigured; specifically, the discharge isolation valve for the pump to be secured must be closed before the CW pump is stopped. In this case, the discharge isolation valve was initially open when the "8" CW pump tripped. As a result, cross-connected flow from the "A" CW pump discharged back to the idle "B" CW pump rather than being forced through the "B main condenser, until the discharge isolation valve for the "B" CW pump closed.
The Control Room operators observed that the "B" CW pump had tripped, entered Abnormal Operating Procedure AP-CW.1 (Loss of a CW Pump), and performed the appropriate actions. A turbine load reduction was initiated. Within three minutes turbine load had been reduced to less than 50%. At this point, the load reduction was stopped. Reactor power was at 69%, when the load reduction was stopped, and continued to decrease. Due to reduced CW flow and loss of hotwell level in the "B" hotwell, "B" condenser backpressure increased above the limit for the satisfactory operating region for the main turbine.
NRC FORM 366A I4.95)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION
<4-95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITYNAME <1) DOCKET LER NUMBER <6) PAGE <3)
YEAR SEQUENTIAL REVISION NUMBER NUMBER R.E. Ginna Nuclear Power Plant 05000244 3 OF 9 96 002 00 TEXT (Ifmore spaceis required, use additional copies of NRC Form 366A/ <17)
DESCRIPTION OF EVENT:
A. DATES AND APPROXIMATE TIMES OF MAJOR OCCURRENCES:
March 7, 1996, 1814 EST: "8" condenser circulating water (CW) pump trips.
0 March 7, 1996, 1822 EST: Event date and time.
0 March 7, 1996, 1822 EST: Discovery date and time.
0 March 7, 1996, 1822 EST: Control Room operators manually trip the reactor, verify both reactor trip breakers open, and verify all control and shutdown rods inserted.
0 March 7, 1996, 1834 EST: Control Room operators manually close both main steam isolation valves to limit a reactor coolant system cooldown.
0 March 7, 1996, 1848 EST: Plant is stabilized at hot shutdown condition (Mode 3).
B. EVENT:
On March 7, 1996, at approximately 1818 EST, reactor power was at approximately 69% and still decreasing. Due to the loss of the "B" condenser circulating water (CW) pump there was reduced cooling water flow in the "B" main condenser for a period of time. This resulted in an imbalance in condenser cooling in the hotwells as backpressure increased in the "B" condenser, leading to a vacuum imbalance between the "A" and "B" condensers. "B" hotwell level indication showed no level, and "A" hotwell level indication showed high hotwell level. In addition, as per design, condenser steam dump was in operation after the rapid turbine load reduction to decrease reactor coolant system (RCS) temperature to match the turbine load.
The combination of reduced cooling water to the "B" condenser, decreased hotwell level, and steam dump into the hotwell caused the temperature in the "8" hotwell to increase. Part of the condensate pump suction was from the hotter water in the "B" hotwell causing a decrease in condensate pump flow and discharge pressure. Low condensate pressure resulted in a'n automatic start of the standby condensate pump and automatic opening of the condensate bypass valve.
Main feedwater (MFW) pump net positive suction head (NPSH) and suction pressure decreased due to this transient. The Control Room operators received Main Control Board Annunciators H-1 (Feed Water Pump Lo Suet Press 185 PSI) and H-17 (Feed Pump Net Positive Suction Head) and responded appropriately to these alarms.
NRC FORM 366A <4.95)
NRC FORM 566A U.S. NUCLEAR REGULATORY COMMISSION (4-95l LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1) DOCKET LER NUMBER (6) PAGE (3)
YEAR SEQUENTIAL REVI I N NUMBER NUMBER 4 OF 9 R.E. Ginna Nuclear Power Plant 05000244 96 002 00 TEXT (lfmore spaceis required, use edditionel copies o/ iVRC Form 366A) (17)
The secondary system transient affected the control signal from the Advanced Digital Feedwater Control System (ADFCS) to the main feedwater regulating valves (MFRV), calling for valve opening due to shrinking steam generator (SG) levels. During the time of the valve open demand, MFW pump suction pressure recovered, resulting in a large increase in feedwater flow. This large flow continued until levels in the "A" and "B" SGs reached the MFW Isolation setpoint of 67%, at which time the "A" and "B" MFRVs closed per design. Beginning at approximately 1819 EST on March 7, MFW Isolation occurred four (4) times for the "A" SG and three (3) times for the "B" SG.
Within two minutes, the valve open demand signal from ADFCS moderated, MFW flow stabilized, and SG levels started to stabilize.
Procedure AP-CW.1 provides guidance for operation with elevated condenser backpressure. (The backpressure limit provides protection for the low pressure turbine last stage blading.) When backpressure increased above the limit for the satisfactory operating region and remained there for five (5) minutes, the shift supervisor ordered a manual reactor trip. The Control Room operators performed the immediate actions of Emergency Operating Procedure E-0 (Reactor Trip or Safety Injection).
They transitioned to Emergency Operating Procedure ES-0.1 (Reactor Trip Response) when it was verified that both reactor trip breakers were open, all control and shutdown rods were inserted, and safety injection was not actuated or required. During the performance of ES-0.1, the Control Room operators noted that a reactor coolant system (RCS) cooldown was occurring and manually closed both main steam isolation valves (MSIV) at approximately 1834 EST. This action mitigated the RCS coo!down.
Pressurizer (PRZR) level decreased to a low level of approximately 8% during the RCS coo!down, automatically closing the letdown isolation valves when level decreased below 13%. PRZR level was increased above 13% within five (5) minutes, and letdown was subsequently reinstated by the Control Room operators.
The plant was stabilized in Mode 3 (hot shutdown) (at approximately 1848 EST) using Plant Operating Procedures 0-2.1 (Normal Shutdown to Hot Shutdown) and 0-3 (Hot Shutdown with Xenon Present). The "B" CW pump was restored to service at approximately 2038 EST on March 8, 1996, after completion of an inspection of the associated protective relays, circuit breaker, and electrical circuitry from the circuit breaker to the motor.
C. INOPERABLE STRUCTURES, COMPONENTS, OR SYSTEMS THAT CONTRIBUTED TO THE EVENT:
None D. OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:
None NRC FORM 366A (4 95)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (4.95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME I1) OOCKET LER NUMBER I6) PAGE I3)
YEAR SEQUENTIAL REVISION NUMBER NUMBER 5 OF 9 R.E. Ginna Nuclear Power Plant 05000244 96 002 00 TEXT iifmore spece is required, use eddi donel copies of NRC Form 366A/ I17)
E. METHOD OF DISCOVERY:
The trip of the "B" CW pump was immediately apparent to the Control Room operators due to Main Control Board (MCB) Annunciator J-16 and MCB indicating lights for the "B" CW pump. The reactor trip was manually initiated and was confirmed by plant response, alarms, and indications in the Control Room.
OPERATOR ACTION The Control Room operators promptly identified the loss of the "8" CW pump and performed the appropriate actions of AP-CW.1. The shift supervisor conservatively ordered a reactor trip when condenser backpressure increased above the limit for the satisfactory operating region.
After the reactor trip, the Control Room operators performed the appropriate actions of procedures E-0 and ES-0.1. The MSIVs were manually closed approximately twelve (12) minutes after the trip to limit further RCS cooldown. Appropriate actions were taken to restore levels in the "A" and "B" SGs and to increase PRZR level. When PRZR level was increased, letdown was manually restored to service. The plant was stabilized in Mode 3 (hot shutdown).
Subsequently, the Control Room operators notified higher supervision and the NRC per 10CFR50.72 (b) (2) (ii), non-emergency four hour notification, at approximately 2150 EST on March 7, 1996.
G. SAFETY SYSTEM RESPONSES:
All safeguards equipment functioned properly. All three auxiliary feedwater (AFW) pumps started when SG levels decreased below 17% after the reactor trip.
III. CAUSE OF EVENT:
A. IMMEDIATECAUSE:
The immediate cause of the reactor trip was manual trip initiation, ordered by the Shift Supervisor due to elevated condenser backpressure.
B. INTERMEDIATE CAUSE:
The intermediate cause of the elevated condenser backpressure was a trip of the "B" CW pump.
NRC FORM 366A I4-95)
NRC Fo M 366A U.S. NUCLEAR REGULATORY COMMISSION
<4-95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITYNAME <1) DOCKET LER NUMBER <6) PAGE <3)
YEAR SEQUENTIAL REVISION NUMBER NUMBER 6 OF 9 R.E. Ginna Nuclear Power Plant 05000244 96 002 00 TEXT Iifmore speceis required, use addi tionel copies of NRC Form 366A/ <17)
ROOT CAUSE:
The underlying cause of the trip of the "B" CW pump was the tripping of the power factor protective relay for the "B" CW pump motor. This relay was activated due to a decrease in the power factor for this motor.
o The "B" CW pump motor was initially operating at a reduced lagging power factor.
o Long term oxidation of the variable auto transformer contact surfaces was noted, which reduced DC current to the motor field, thus reducing the power factor.
The combination of these factors caused the power factor protective relay to activate at its design setpoint.
This event is NUREG-1022 Cause Code (E), "Management I Quality Assurance Deficiency".
The tripping of the "B" CW pump meets the NUMARC 93-01, "Industry Guideline for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants", definition of a "Maintenance Preventable Functional Failure".
IV. ANALYSIS OF EVENT'his event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a) (2) (iv),
which requires a report of, "Any event or condition that resulted in a manual or automatic actuation of any engineered safety feature (ESF), including the reactor protection system (RPS)". The manual reactor trip is an actuation of the RPS, and MFW Isolation and AFW pump starts are actuations of an ESF.
An assessment was performed considering both the safety consequences and implications of this event with the following results and conclusions:
There were no operational or safety consequences or implications attributed to the trip of the "B" CW pump and subsequent manual reactor trip because:
o The two reactor trip breakers opened as required.
o All control and shutdown rods inserted as designed.
o The plant was stabilized at Mode 3 (hot shutdown).
NRC FORM 366A <4.95)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION I4-95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITYNAME I1) DOCKET LER NUMBER I6) PAGE I3)
YEAR SEQUENTIAL REVISION NUMBER NUMBER R.E. Ginna Nuclear Power Plant 05000244 7 OF 9 96 002 00 TEXT llfmore space is required, use addi donal copies of NRC Form 366A/ I17)
The Ginna Updated Final Safety Analysis Report (UFSAR) transient, "Loss of Condenser Vacuum", can occur from failure of the circulating water system, as stated in Section 15.2.4 of the UFSAR. In the event of loss of condenser vacuum, the turbine will be tripped, and, therefore, the event is bounded by the turbine trip event (UFSAR Section 15.2.2). This UFSAR transient was examined and compared to the plant response for the actual event. The plant behavior was found to be consistent with the assumptions detailed in the accident analysis. As described in Section 15.2.2.4, a loss of load with or without a direct or immediate reactor trip presents no hazard to the integrity of the RCS or the main
'steam system. The integrity of the core is maintained by operation of the reactor protection system prior to exceeding any thermal design limits.
o The total time of operation of the turbine with elevated condenser backpressure did not exceed the recommendations of the turbine manufacturer.
The Ginna Improved Technical Specifications (ITS) Limiting Conditions for Operation (LCOs) and Surveillance Requirements (SRs) were reviewed with respect to the post trip review data. The following are the results of that review:
PRZR pressure decreased below 2205 PSIG during the transient prior to the reactor trip.
During this time a thermal power ramp load reduction was in progress within the limits of LCO 3.4.1. Therefore, compliance with ITS was maintained. The RCS temperature DNB limit (577.5 degrees F) was not approached.
0 After the reactor trip, the RCS cooled down to approximately 535 degrees F and was subsequently stabilized at 547 degrees F. The cooldown was within the limits of LCO 3.4.3. In addition, the required shutdown margin was maintained at all times during the RCS cooldown.
o Both SG levels decreased following the reactor trip to below 16% indicated narrow range level. This is an expected transient. SR 3.4.5.2 states that in order to demonstrate that a reactor coolant'loop is operable, the SG water level shall be >/= 16%. Thus, both coolant loops were inoperable, even though both loops were still in operation and performing their intended function of decay heat removal.
Both SGs were available as a heat sink, and sufficient AFW flow was maintained for adequate steam release from both SGs. Both loops were restored to operable status when SG levels were restored to >/= 16% ("A" SG level in less than five (5) minutes, and "B" SG level in less than four (4) minutes). As required by LCO 3.4.5 Required Actions C.1, C.2, and C.3, the reactor trip breakers were open, the CRDMs were deenergized, no operation involving a reduction in RCS boron concentration occurred, and actions to restore both loops to operable status were immediately taken during the time SG levels were (16%. Therefore, compliance with LCO 3A.5 was maintained.
NRc FORM 366A I4-95)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION
~ (4.95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITYNAME (1) DOCKET LER NUMBER (6) PAGE (3)
YEAR SEQUENTIAL REVISION NUMBER NUMBER 8 OF 9 R.E. Ginna Nuclear Power Plant 05000244 g6 .. pp2 pp TEXT Iifmore spaceis required, use edditionel copies of NRC Form 366A/ (17)
Based on the above and the review of post trip data and past plant transients, it can be concluded that the plant operated as designed, that there were no unreviewed safety questions, and that the public's health and safety was assured at all times.
V. CORRECTIVE ACTION:
A. ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS:
0 The SGs were restored to operable status when SG level increased above 16% levels, by addition of auxiliary feedwater. Subsequently, levels were returned to their normal operating levels.
PRZR level was increased to its normal operating level, and letdown flow was restored.
0 The power factor protective relay for the "B" CW pump motor was inspected and tested satisfactorily.
Thermography was performed on the "B" CW pump motor circuit breaker and internal components. This thermography indicated there was high resistance on the variable auto transformer wiper contact. The transformer was cleaned, and resistance was restored to acceptable values.
0 CW motor test data was reviewed and found satisfactory.
ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
K 0 Procedure AP-CW.1 has been quarantined due to content that does not adequately control plant response. In the interim, Operations management has directed that upon loss of a CW pump, the reactor will be tripped, and further actions will be as per Procedure E-p.
0 The loss of CW pump transient will be evaluated, and changes will be made to procedure AP-CW.1 prior to removing AP-CW.1 from quarantine.
0 A maintenance procedure has been revised to have the electrical parameters of the motors for both CW pumps monitored by electricians, and adjustments to power factor will be made under rules in the Work Control System.
0 A preventive maintenance repetitive task (REPTASK) has been initiated to ensure periodic cleaning of the variable auto transformer wiper contacts (during CW pump breaker maintenance).
NRC FORM 366A (4-95)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (4.95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITYNAME (1) DOCKET LER NUMBER (6) PAGE (3)
YEAR SEQUENTIAL REVISION NUMBER NUMBER Ginna Nuclear Power Plant 05000244 9 OF 9 '.E.
96 002 00 TEXT llfmore spoce is required, use eddi rl'encl copies of fVRC Form 366Al (17)
VI. ADDITIONAL INFORMATION'.
FAILED COMPONENTS:
The "B" CW pump motor is a Westinghouse "Life Line" series motor, Model ¹ 110P662H01, frame size HR-111-SPL, rated for 4000 volts and 1750 horsepower.
PREVIOUS LERs ON SIMILAR EVENTS:
A similar LER event historical search was conducted with the following results:
\
LER 85-019 was a similar event (loss of CW pump caused a plant transient, resulting in an automatic reactor trip) with a different root cause for the loss of the CW pump. The corrective action to prevent recurrence would not have prevented LER 96-002.
LER 95-008 was a similar event floss of CW pump caused a plant transient, resulting in a manual reactor trip) with a different root cause for the loss of the CW pump. The corrective action to prevent recurrence would not have prevented LER 96-002.
C. SPECIAL COMMENTS:
None NRC FORM 366A (4.95)