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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000244/LER-1999-011, :on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With1999-09-22022 September 1999
- on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With
05000244/LER-1999-004, :on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed1999-08-24024 August 1999
- on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed
05000244/LER-1999-007, :on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians1999-07-23023 July 1999
- on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians
05000244/LER-1998-003, :on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored1999-07-22022 July 1999
- on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored
05000244/LER-1999-010, :on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With1999-07-15015 July 1999
- on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With
05000244/LER-1999-001, :on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With1999-06-21021 June 1999
- on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With
05000244/LER-1999-009, :on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With1999-06-0202 June 1999
- on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With
05000244/LER-1999-008, :on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With1999-05-27027 May 1999
- on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With
05000244/LER-1999-006, :on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With1999-05-21021 May 1999
- on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With
05000244/LER-1999-005, :on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With1999-05-13013 May 1999
- on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With
05000244/LER-1999-003, :on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With1999-03-31031 March 1999
- on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With
05000244/LER-1999-002, :on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With1999-03-29029 March 1999
- on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With
05000244/LER-1998-005, :on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With1998-12-21021 December 1998
- on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With
05000244/LER-1998-004, :on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery1998-12-17017 December 1998
- on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery
05000244/LER-1998-002, :on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R371998-07-14014 July 1998
- on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37
05000244/LER-1998-001, :on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells1998-03-11011 March 1998
- on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells
05000244/LER-1997-007, :on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified1998-02-0606 February 1998
- on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified
05000244/LER-1997-006, :on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status1998-02-0606 February 1998
- on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status
05000244/LER-1997-005, :on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset1997-12-0101 December 1997
- on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset
05000244/LER-1997-004, :on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage1997-11-24024 November 1997
- on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage
05000244/LER-1997-003, :on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped Configuration1997-09-29029 September 1997
- on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped Configuration
05000244/LER-1997-002, :on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 171997-08-19019 August 1997
- on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17
05000244/LER-1996-009, :on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe1997-08-11011 August 1997
- on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe
05000244/LER-1997-001, :on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F1997-03-0303 March 1997
- on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F
05000244/LER-1996-015, :on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected Line1997-01-22022 January 1997
- on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected Line
05000244/LER-1996-013, :on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened1996-11-27027 November 1996
- on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened
05000244/LER-1996-012, :on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was Replaced1996-09-19019 September 1996
- on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was Replaced
05000244/LER-1996-011, :on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were Secured1996-09-0505 September 1996
- on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were Secured
05000244/LER-1996-010, :on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure Revised1996-09-0505 September 1996
- on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure Revised
05000244/LER-1996-008, :on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G Level1996-08-0606 August 1996
- on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G Level
05000244/LER-1996-007, :on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet Replaced1996-07-12012 July 1996
- on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet Replaced
05000244/LER-1996-006, :on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 21996-06-20020 June 1996
- on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2
05000244/LER-1996-005, :on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs Revised1996-06-17017 June 1996
- on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs Revised
05000244/LER-1996-004, :on 960309,decrease in Steam Generator Level Occurred.Caused by Failed Open Atmospheric Relief Valves. Booster Relay Replaced1996-04-0808 April 1996
- on 960309,decrease in Steam Generator Level Occurred.Caused by Failed Open Atmospheric Relief Valves. Booster Relay Replaced
05000244/LER-1996-002, :on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography Performed1996-04-0808 April 1996
- on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography Performed
05000244/LER-1996-001, :on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled1996-03-18018 March 1996
- on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled
05000244/LER-1995-009, :on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/1995-12-14014 December 1995
- on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/
05000244/LER-1995-008, :on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating Levels1995-09-25025 September 1995
- on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating Levels
05000244/LER-1995-007, :on 950803,lost Power from 34.5 Kv Offsite Power Circuit 751 Due to Offsite Electrical Storm,Resulting in Automatic Start of EDG B.Offsite Power Restored,Edg B Stopped & Realigned & Circuit 751 Cleared1995-09-0101 September 1995
- on 950803,lost Power from 34.5 Kv Offsite Power Circuit 751 Due to Offsite Electrical Storm,Resulting in Automatic Start of EDG B.Offsite Power Restored,Edg B Stopped & Realigned & Circuit 751 Cleared
05000244/LER-1995-006, :on 950630,34.5 Kv Offsite Power Circuit 751 Was Lost Due to Offsite Lightning Strike & Resulted in Automatic Start of a Edg.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1 to Stabilize Plant1995-07-31031 July 1995
- on 950630,34.5 Kv Offsite Power Circuit 751 Was Lost Due to Offsite Lightning Strike & Resulted in Automatic Start of a Edg.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1 to Stabilize Plant
05000244/LER-1995-005, :on 950607,FW Isolation on High SG Level Occurred.Caused by Decrease in Instrument Air Pressure Due to an Air Leak in Containment.Fw Flow Switched to Manual Control1995-07-0707 July 1995
- on 950607,FW Isolation on High SG Level Occurred.Caused by Decrease in Instrument Air Pressure Due to an Air Leak in Containment.Fw Flow Switched to Manual Control
05000244/LER-1995-003, :on 950407,inadvertent Automatic SI Actuation Occurred When Technician Unblocked SIAS Due to Misleading Procedural Direction.Pressurizer Pressure Channel P-431 Bistable Proving Switch Reinstated1995-05-0808 May 1995
- on 950407,inadvertent Automatic SI Actuation Occurred When Technician Unblocked SIAS Due to Misleading Procedural Direction.Pressurizer Pressure Channel P-431 Bistable Proving Switch Reinstated
05000244/LER-1995-004, :on 950407,SG Tube Degradation Occurred Due to Iga/Scc That Caused QA Manual Reportable Limits to Be Reached.Sleeved or Plugged Affected Tubes W/Accepted Industry Repair Methods1995-05-0808 May 1995
- on 950407,SG Tube Degradation Occurred Due to Iga/Scc That Caused QA Manual Reportable Limits to Be Reached.Sleeved or Plugged Affected Tubes W/Accepted Industry Repair Methods
05000244/LER-1995-002, :on 950212,concurrent Indication of Individual CR Position Briefly Unavailable.Caused by Short Circuit. Repair of Short Circuit Completed1995-03-14014 March 1995
- on 950212,concurrent Indication of Individual CR Position Briefly Unavailable.Caused by Short Circuit. Repair of Short Circuit Completed
05000244/LER-1995-001, :on 950203,pressurizer Safety Valves Lift Settings Found Above TS Tolerance During post-svc Test,Due to Setpoint Shifts That Resulted in Independent Trains Being Considered Inoperable1995-03-0606 March 1995
- on 950203,pressurizer Safety Valves Lift Settings Found Above TS Tolerance During post-svc Test,Due to Setpoint Shifts That Resulted in Independent Trains Being Considered Inoperable
05000244/LER-1994-012, :on 940921,approx 1032 Edst W/Reactor at Approx 98% Steady State Power,Power from Circuit 751 Was Lost. Caused by Automatic Actuation of B Emergency D/G Was Due to Undervoltage.Safeguards Buses Were Restored1994-10-21021 October 1994
- on 940921,approx 1032 Edst W/Reactor at Approx 98% Steady State Power,Power from Circuit 751 Was Lost. Caused by Automatic Actuation of B Emergency D/G Was Due to Undervoltage.Safeguards Buses Were Restored
05000244/LER-1994-011, :on 940917,indicating Lamp on B Train Safeguards Initiation Cabinet Failed.Caused by Loss of 125 Vdc Control Power.Burned Out Indicating Lamp & Blown Fuse Replaced1994-10-17017 October 1994
- on 940917,indicating Lamp on B Train Safeguards Initiation Cabinet Failed.Caused by Loss of 125 Vdc Control Power.Burned Out Indicating Lamp & Blown Fuse Replaced
05000244/LER-1994-010, :on 940916,volt Bus 12B Inadvertenly Tripped. Caused by Defective Procedure.Normal Power Supplies Restored & B Emergency Diesel Generator Stopped & Aligned for Auto Standby1994-10-17017 October 1994
- on 940916,volt Bus 12B Inadvertenly Tripped. Caused by Defective Procedure.Normal Power Supplies Restored & B Emergency Diesel Generator Stopped & Aligned for Auto Standby
05000244/LER-1994-009, :on 940809,SI Pumps Declared Inoperable Due to Leak at Socket Weld in Common Recirculation Line for SI Pumps.Affected Weld Inspected & Removed & Maint Procedure for Overhaul of SI Pumps Will Be Upgraded1994-09-0808 September 1994
- on 940809,SI Pumps Declared Inoperable Due to Leak at Socket Weld in Common Recirculation Line for SI Pumps.Affected Weld Inspected & Removed & Maint Procedure for Overhaul of SI Pumps Will Be Upgraded
05000244/LER-1994-008, :on 940613,B Safety Injection Pump Was Declared Inoperable During Monthly Surveillance Test.Caused by Broken Motor Rotor Bar.B SI Pump Motor Rotor Bars Were Replaced & B SI Pump Motor Was Reassembled1994-07-13013 July 1994
- on 940613,B Safety Injection Pump Was Declared Inoperable During Monthly Surveillance Test.Caused by Broken Motor Rotor Bar.B SI Pump Motor Rotor Bars Were Replaced & B SI Pump Motor Was Reassembled
1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17265A7621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Re Ginna Npp.With 991008 Ltr ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr 05000244/LER-1999-011, :on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With1999-09-22022 September 1999
- on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With
ML17265A7471999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Re Ginna Npp.With 990909 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed 05000244/LER-1999-004, :on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed1999-08-24024 August 1999
- on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed
ML17265A7341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Re Ginna Npp.With 990806 Ltr ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent 05000244/LER-1999-007, :on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians1999-07-23023 July 1999
- on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians
ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7131999-07-22022 July 1999 Special Rept:On 990407,radiation Monitor RM-14A Was Declared Inoperable.Caused by Failed Communication Link from TSC to Plant Process Computer Sys.Communication Link Was re-established & RM-14A Was Declaed Operable on 990521 05000244/LER-1998-003, :on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored1999-07-22022 July 1999
- on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored
ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7211999-07-19019 July 1999 ISI Rept for Third Interval (1990-1999) Third Period, Second Outage (1999) at Re Ginna Npp. 05000244/LER-1999-010, :on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With1999-07-15015 July 1999
- on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With
ML17265A7011999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Re Ginna Npp.With ML17265A7661999-06-30030 June 1999 1999 Rept of Facility Changes,Tests & Experiments Conducted Without Prior NRC Approval for Jan 1998 Through June 1999, Per 10CFR50.59.With 05000244/LER-1999-001, :on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With1999-06-21021 June 1999
- on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With
ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis 05000244/LER-1999-009, :on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With1999-06-0202 June 1999
- on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With
ML17265A6681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Re Ginna Nuclear Power Plant.With ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 05000244/LER-1999-008, :on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With1999-05-27027 May 1999
- on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With
ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr 05000244/LER-1999-006, :on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With1999-05-21021 May 1999
- on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With
ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr 05000244/LER-1999-005, :on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With1999-05-13013 May 1999
- on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With
ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG ML17265A6391999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Re Ginna Nuclear Power Plant.With ML17265A6341999-04-23023 April 1999 Safety Evaluation Supporting Amend 74 to License DPR-18 ML17265A6361999-04-23023 April 1999 Part 21 Rept Re Power Supply That Did Not Work Properly When Drawn from Stock & Installed in -25 Vdc Slot.Power Supply Will Be Sent to Vendor to Perform Failure Mode Assessment.Evaluation Will Be Completed by 991001 ML17265A7251999-04-23023 April 1999 Rev 1 to Rept of Development of Rg&E Seismic Safe SD Equipment & Relay Review Lists for USI A-46 ML17265A6301999-04-18018 April 1999 Rev 1 to Cycle 28 COLR for Re Ginna Npp ML17265A6251999-04-15015 April 1999 Special Rept:On 990309,halon Systems Were Removed from Svc & Fire Door F502 Was Blocked Open.Caused by Mods Being Made to CR Emergency Air Treatment Sys.Continuous Fire Watch Was Established with Backup Fire Suppression Equipment ML17265A6551999-04-0909 April 1999 Initial Part 21 Rept Re Mfg Deficiency in Replacement Turbocharger for B EDG Supplied by Coltec Industries. Deficiency Consisted of Missing Drain Port in Intermediate Casing.Required Oil Drain Port Machined Open ML17265A6181999-04-0606 April 1999 Safety Evaluation Concluding Proposed Rev 26 to Rg&E QAP for Station Operation Incorporating Reductions in Stated Commitments Will Continue to Comply with QA Criteria of App B to 10CFR50 & Therefore,Acceptable ML17265A6291999-03-31031 March 1999 Rev 0 to Cycle 28 COLR for Re Ginna Npp ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr 05000244/LER-1999-003, :on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With1999-03-31031 March 1999
- on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With
ML17265A6241999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ginna Station.With 990409 Ltr 05000244/LER-1999-002, :on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With1999-03-29029 March 1999
- on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With
ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A5581999-03-0101 March 1999 Rev 1 to Gnpp Internal Flooding Probabilistic Safety Assessment Final Rept ML17265A5661999-03-0101 March 1999 Rev 26 to QA Program for Station Operation. 1999-09-30
[Table view] |
text
('A'19'(90RY j REGULA RY INFORMATION DISTRIBUTI SYSTEM (RIDS) 1 ACCESSION NBR:9609130028 DOC.DATE: 96/09/05 NOTARIZED:
NO DOCKET FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G
05000244 AUTH.NAME AUTHOR AFFILIATION MARTIN,J.T.
Rochester Gas
& Electric Corp.
MERCREDY,R.C.
Rochester Gas a Electric Corp.
RECIP.NAME RECIPIENT AFFILIATION VISSINGiG.S.
SUBJECT:
LER 96-011-00:on 960807,improper configuration of circuit breaker occurred.Due to undetected internal interference, resulting in automatic start of both auxiliary feedwater pumps. Running AFW pumps were secured.W/960905 ltr.
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TITLE: 50.73/50.9 Licensee Event Report (LER), incident Rpt, etc.
NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72).
05000244 E
RECIPIENT ID CODE/NAME PD1-1 PD INTERNAL:
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4ND ROCHESTERGASANDELECTRICCORPORATION
~ 89EASTAVfNUE,ROCHESTER,N.Y Id6d9000I 7
AREA CODE7165d62700 ROScRT C. MECREDY Vce President Nvctear Ooerrst'or s September 5, 1996 U.S. Nuclear Regulatory Commission Document Control Desk Attn:
Guy S. Vissing Project Directorate I-1 Washington, D.C. 20555
Subject:
LER 96-011, Improper Configuration of Circuit Breaker, Due to Undetected Internal Interference, Results in Automatic Start of Both Auxiliary Feedwater Pumps R.E. Ginna Nuclear Power Plant Docket No. 50-244
Dear Mr. Vissing:
In accordance with 10 CFR 50.73, Licensee Event Report System, item (a) (2) (iv), which requires a report of, "Any event or condition that resulted in a manual or automatic actuation of any engineered safety feature (ESF), including the reactor protection system (RPS)", the attached Licensee Event Report LER 96-011 is hereby submitted.
Th!s event has in no way affected the public's health and safety.
Very truly yours, Robert C. Mecredy xc:
Mr. Guy S. Vissing (Mail Stop 14C7)
PWR Project Directorate I-1 Washington, D.C.
20555 U.S. Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna Senior Resident Inspector c7609i30028 960905 PDR aOOCK 05000 44 S
PDR
NRC FORM 366 (4-95)
U.S. NUCLEAR REGULATORY COMMISSIO LICENSEE EVENT REPORT (LER)
(See reverse for required number of digits/characters fcr each block)
APPROVED BY OMB NO. 3160%104 EXPIRES 04/30/98 ESTIMATED BURDEN PER
RESPONSE
To COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUEST: 50.0 HRS.
REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSING PROCESS AND FED BACK To INDUSTRY.
FORWARD COMMENTS REGARDING BURDEN ESTIMATE To THE INFORMATION AND RECORDS MANAGEMENT BRANCH (T-6 F33),
U.S. NUCI.EAR REGULATORY COMMISSION, WASHINGTON, DC 20555 cool, AND TO THE PAPERWORK REDUCTION PROJECT FACIUTYNAMEIII R.E. Ginna Nuclear Power Plant DOCKET NUMBERI2) 05000244 PAOE I3) 1OF5 TITLE(4I Improper Configuration of Circuit Breaker, Due to Undetected Internal Interference, Results in Automatic Start of Both Auxiliary Feedwater Pumps EVENT DATE (6)
LER NUMBER (6)
REPORT DATE (7)
OTHER FACILITIES INVOLVED(8)
MONTH 08 DAY 07 YEAR 96 SEQUENTIAL REVISION NUMBER NUMBER 96 011 00 MONTH OAY 09 05 96 FACIUTYNAME FACIUTYNAME DOCKET NUMBER DOCKET NUMBER OPERATING MODE (9)
POWER LEVEL (10) 000 20.2201(b) 20.2203(a) (1) 20.2203(a)(2)(i) 20.2203(a)(2)(ii) 20.2203(a)(2) (iii) 20.2203(a) (2) (iv) 20.2203(a) (2) (v) 20.2203(a) (3) (i) 20.2203(a)(3) (ii) 20.2203(a) (4) 50.36(c)(1) 50.36(c)(2) 50.73(a) (2)(i) 50.73(a)(2) (ii) 50.73(a) (2) (iii)
X 50.73(a)(2)(iv) 50.73(a)(2)(v) 50.73(a)(2)(vii)
THIS REPORT IS SUBMITTED PUR SUANT TO THE REQUIREMENTS OF 10 CFR %: (Check one or more)
(11) 50.73(a) (2)(viii) 50.73(a)(2) (x) 73.71 OTHER Specify in Abstract below or m NRC Form 366A NAME LICENSEE CONTACT FOR THIS LER (12)
ELEFHONE NUMBER ilncrvde Area Codel John T. St. Martin - Technical Assistant COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESC (716) 771-3641 RIBED IN THIS REPORT (13)
CAUSE
SYSTEM COMPONENT MANUFACTURER To NPRDS
CAUSE
SYSTEM COMPONENT MANUFACTURER REPORTABLE To NPROS SUPPLEMENTAL REPORT EXPECTED (14)
YES (If yes, complete EXPECTED SUBMISSION DATE).
X NO EXPECTED SUBMISSION DATE (16)
MONTH DAY YEAR ABSTRACT (Limitto 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16)
On August 7, 1996, at approximately 2009 EDST, the plant was in IVlode 3 with the reactor coolant system being maintained at a temperature of 545 degrees F and a pressurizer pressure of 2235 PSIG.
With no auxiliary feedwater pumps running and one main feedwater pump circuit breaker racked out in the "test" position,'n "AFW Bypass Switch" was moved from "Defeat" to "Normal". An undetected improper configuration of the circuit breaker created the logic that both main feedwater pump breakers were already open.
This created the logic for autostart of both the "A" and "B" motor-driven auxiliary feedwater pumps.
Immediate action was to stabilize auxiliary feedwater flow to both steam generators.
The underlying cause of the autostart was that the logic for autostart divas present due to an undetected internal interference within the circuit breaker between the racking arm and the actuating rod for the 52S auxiliary switch, which prevented this switch from opening to provide the circuit logic that the breaker was in the closed position.
This event is NUREG-1022 Cause Code (A).
Corrective action to prevent recurrence is outlined in Section V.B.
NRC FORM 366 (4-95)(4-95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION U.S. NUCLEAR REGULATORY COMMISSION FACILITYNAME (1)
R.E. Ginna Nuclear Power Plant DOCKET 05000244 LER NUMBER (6)
YEAR SEQUENTIAL REVISION NUMBER NUMBER 96
011
00 PAGE (3) 2 OF 5
TEXT iifmore speceis required, use edditionef copies of NRC Form 366Aj (17)
PRE-EVENT PLANT CONDITIONS:
On August 7, 1996, at approximately 2009 EDST, the plant was in Mode 3 as a result of a voluntary plant shutdown to upgrade motor-operated valves in the residual heat removal IRHR) system.
Valve upgrades were completed and plant heatup and startup was in progress.
The reactor coolant system IRCS) was being maintained at a temperature of approximately 545 degrees F and a pressurizer (PRZR) pressure of approximately 2235 PSIG.
The circuit breaker for the "A" main feedwater IMFW) pump had jumpers installed and was closed in the "test" position, to comply with temporary administrative requirements.
Auxiliary feedwater IAFW) pumps had just been secured as directed by these temporary administrative requirements, so there were no AFW pumps running.
II.
DESCRIPTION OF EVENT
A.
DATES AND APPROXIMATE TIMES OF MAJOR OCCURRENCES
o August 7, 1996, 2009 EDST: Event date and time.
o August 7, 1996, 2009 EDST: Discovery date and time.
o August 7, 1996, 2024 EDST: One running AFW pump is secured.
o August 7, 1996, 2135 EDST: All running AFW pumps are secured.
EVENT:
On August 7, 1996, at approximately 2009 EDST, the plant was in Mode 3. The RCS was being maintained at a temperature of approximately 545 degrees F
and a
PRZR pressure of approximately 2235 PSIG. As directed by Normal Operating Procedure 0-1.2, "Plant Startup From Hot Shutdown to Full Load", the Control Room operators moved an "AFW Bypass Switch" from the "Defeat" to the "Normal" position. Due to an undetected improper configuration of the circuit breaker for the "A"MFW pump, the 2 of 2 logic for both MFW pump breakers open was present, which caused an autostart of both the "A" and "B" AFW pumps.
The Control Room operators observed the autostart of both the "A" and "B" AFW pumps, and controlled AFW flow to the desired flow rate for Mode 3 conditions.
One of the running AFW pumps was secured at approximately 2024 EDST.
The Control Room operators requested that plant electricians investigate the problem.
Electricians determined, when racking out the circuit breaker into the "test" position, the breaker positioning arm had travelled beyond its mechanical stop.
This caused an undetected interference between the racking arm and the 52S auxiliary switch actuating rod, which prevented the 52S switch from opening to provide circuit logic that the breaker was in the closed position.
The breaker was properly racked out, and electricians verified there was no interference and that the 52S switch had opened.
NIIC FOAM 366A (4-95)
tl(4-95)
LICENSEE EXTENT REPORT (LER)
TEXT CONTINUATION U.S. NUCLEAR REGULATORY COMMISSION FACILITYNAME (1)
R.E. Ginna Nuclear Power Plant DOCKET 05000244 LER NUMBER (6)
YEAR SEQUENTIAL REVISION NUMBER NUMBER 96
011
00 PAGE (3) 3 OF 5
TEXT (Ifmore spece is required, use eddi donel copies ofNRC Form 366AJ (17)
C.
INOPERABLE STRUCTURES, COMPONENTS, OR SYSTEMS THATCONTRIBUTEDTO THE EVENT:
None D.
OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED
None E.
METHOD OF DISCOVERY
This event was immediately apparent when both the "A" and "B" AFW pumps autostarted after the AFW Bypass Switch was placed in the "Normal".position.
OPERATOR ACTION
After both the "A" and "B" AFW pumps autostarted, the Control Room operators took prompt actions to control AFW flow. They requested that the plant electricians determine the cause of the problem.
The Control Room operators subsequently notified higher supervision and notified the NRC per 10CFR50.72 (b) (2) (ii), non-emergency four hour notification, at approximately 2226 EDST on August 7, 1996.
G.
SAFETY SYSTEM RESPONSES:
Both the "A" and "B" AFW pumps autostarted as per design.
CAUSE OF EVENT
A.
IMMEDIATECAUSE:
The immediate cause of the autostart of both the "A" and "B" AFW pumps was the autostart logic, which was satisfied by 52S contacts providing circuit logic that both MFW pump breakers were open and an AFW Bypass Switch in "Normal".
B.
INTERMEDIATECAUSE:
The intermediate cause of autostart logic being satisfied was an undetected improper configuration of the "A"'MFWpump circuit breaker.
NRC FORM 36:6 I's)(4-95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION U.S. NUCLEAR REGULATORYCOMMISSION FACILITYNAME (1)
DOCKET LER NUMBER (6)
PAGE (3)
R.E. Ginna Nuclear Power Plant 05000244 YEAR SEQUENTIAL REVISION NUMBER NUMBER 4
OF 5
96
011
00 TEXT Iifmore space is required, use additional copies ofNRC Form 36@A/ (17)
C.
ROOT CAUSE:
The underlying cause of the improper configuration was an undetected internal interference within the "A" MFW pump circuit breaker.
When the breaker was racked out to the test position, the breaker positioning arm travelled beyond its mechanical stop.
This caused interference between the racking arm and the actuating rod for the 52S auxiliary contact switch. Therefore, while the breaker was physically closed in the "test" position, the auxiliary switch did not provide circuit logic that the breaker was in the closed position.
This situation was created to be in compliance with the Ginna Station Improved Technical Specifications (ITS) Table 3.3.2-1 Function 6.f. To prevent an unnecessary actuation of both AFW pumps during Mode 2 conditions, a MFW pump breaker may be administratively closed in the test position, provided it is capable of being tripped on undervoltage and overcurrent conditions.
The administrative requirements were established to comply with ITS Table 3.3.2-1, which requires the autostart function of the motor-driven AFW pump upon opening of both MFW pump breakers during Modes 1 and 2. Prior to Amendment No. 61 to the ITS, this function was only required in Mode 1 when the MFW pumps were actually in service.
The addition of Mode 2 (when the MFW pumps may not be in service) was inadvertently added to the ITS by Amendment No. 61.
This event is NUREG-1022 Cause Code (A), "Personnel Error". This error was a cognitive error on the part of a plant electrician, who did not detect the interference between the racking arm and the actuating rod.
This error was associated with activities that were covered by an approved procedure, and was not contrary to that procedure.
The procedural guidance was correct, but enhancements to the procedure have been identified. There were no unusual characteristics of the location of this breaker that contributed to this event.
Note that this interference can only be created when racking the breaker out to the test position.
The autostart of the AFW pump does not meet the NUMARC 93-01, "Industry Guideline for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants",
definition of a
"Maintenance Preventable Functional Failure".
IV.
ANALYSIS OF EVENT
This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a) (2) (iv),
which requires a report of, "Anyevent or condition that resulted in a manual or automatic actuation of any engineered safety feature (ESF), including the reactor protection system (RPS)".
The start of an AFW pump is an actuation nf an ESF.
An assessment was performed considering both the safety consequences and implications of this event with the following results and conclusions:
There were no operational or safety consequences or implications attributed to the autostart of both the "A" and "B" AFW pumps because:
o The autostart occurred with acceptable levels in both S/Gs.
AFW flow was controlled to maintain these levels.
NRC FOR)A 366A (4.95)(4-96)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION U.S. NUCLEAR REGULATORY COMMISSION FACILITYNAME(1)
R.E. Ginna Nuclear Power Plant DOCKET 05000244 LER NUMBER (6)
YEAR SEQUENTIAL REVISION NUMBER NUMBER 96
011
00 PAGE (3) 5 OF 5
TEXTllfmore spaceis required, use additional copies ofNRC Form 366A/ (17) o The limiting case for the supply of AFW is the Loss of Feedwater accident at 100'/o power.
The plant condition at the time of this event was less than 5% power.
Based on the above, it can be concluded that the public's health and safety was assured at all times.
V.
CORRECTIVE ACTION
A.
ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMALSTATUS:
AFW flow was controlled as desired to maintain S/G level.
o The running AFW pumps were secured.
B.
ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
The ITS willbe revised to eliminate the need for having a MFW pump breaker closed in the test position during Mode 2 conditions.
Procedure 0-2.1 will be enhanced to include specifically addressing that the 52S switch actuating rod is in the correct position when the breaker is racked out in the test position.
Vi.
ADDITIONALINFORMATION:
A.
FAILED COMPONENTS:
None B.
PREVIOUS LERs ON SIMILAREVENTS:
A similar LER event historical search was conducted with the following results: No documentation of similar LER events with the same root cause could be identified. However, LERs96-004, 96-008, and 96-010 are similar events with different root causes.
C.
SPECIAL COMfvlENTS:
None NRC FORM 9 "~A (4-95)
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| | Reporting criterion |
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05000244/LER-1996-001, :on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled |
- on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(e)(2)(v) | 05000244/LER-1996-002, :on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography Performed |
- on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography Performed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | 05000244/LER-1996-003, Forwards LER 96-003,Rev 1.HPES Completed,Root Cause Analysis Completed & Corrective Actions Identified | Forwards LER 96-003,Rev 1.HPES Completed,Root Cause Analysis Completed & Corrective Actions Identified | | 05000244/LER-1996-004, :on 960309,decrease in Steam Generator Level Occurred.Caused by Failed Open Atmospheric Relief Valves. Booster Relay Replaced |
- on 960309,decrease in Steam Generator Level Occurred.Caused by Failed Open Atmospheric Relief Valves. Booster Relay Replaced
| | 05000244/LER-1996-005, :on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs Revised |
- on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | 05000244/LER-1996-006, :on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2 |
- on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | 05000244/LER-1996-007, :on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet Replaced |
- on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet Replaced
| | 05000244/LER-1996-008, :on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G Level |
- on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G Level
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | 05000244/LER-1996-009-02, Forwards LER 96-009-02 Re Leak Outside Containment Due to Weld Defect.Further Assessment Determined That Leak Rate Is within Design Basis & Entry Into TS LCO 3.0.3 Was Not Required | Forwards LER 96-009-02 Re Leak Outside Containment Due to Weld Defect.Further Assessment Determined That Leak Rate Is within Design Basis & Entry Into TS LCO 3.0.3 Was Not Required | | 05000244/LER-1996-009, :on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe |
- on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | 05000244/LER-1996-010, :on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure Revised |
- on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | 05000244/LER-1996-011, :on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were Secured |
- on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were Secured
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | 05000244/LER-1996-012, :on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was Replaced |
- on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | 05000244/LER-1996-013, :on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened |
- on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(e)(2)(i) | 05000244/LER-1996-015, :on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected Line |
- on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected Line
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) |
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