ML051190494

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IR 05000298-05-002; on 01/01/05 - 03/24/05; for Cooper Nuclear Station, Maintenance Rule Implementation, Personnel Performance During Nonroutine Evolutions, Operability Evaluations, Control to Radiological Significant Areas, Event Followup.
ML051190494
Person / Time
Site: Cooper Entergy icon.png
Issue date: 04/29/2005
From: Hay M
NRC/RGN-IV/DRP/RPB-C
To: Edington R
Nebraska Public Power District (NPPD)
References
IR-05-002
Download: ML051190494 (46)


See also: IR 05000298/2005002

Text

April 29, 2005

Randall K. Edington, Vice

President-Nuclear and CNO

Nebraska Public Power District

P.O. Box 98

Brownville, NE 68321

SUBJECT: COOPER NUCLEAR STATION - NRC INTEGRATED INSPECTION

REPORT 05000298/2005002

Dear Mr. Edington:

On March 24, 2005, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection

at your Cooper Nuclear Station. The enclosed integrated inspection report documents the

inspection findings which were discussed on April 14, 2005, with Mr. S. Minahan, General

Manager of Plant Operations, and other members of your staff.

This inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, the NRC identified seven findings which were evaluated

under the risk significance determination process as having very low safety significance

(Green). The NRC also determined that there were six violations associated with these

findings. However, because these violations were of very low safety significance and the issues

were entered into the licensees corrective action program, the NRC is treating these findings as

noncited violations, consistent with Section VI.A.1 of the NRCs Enforcement Policy. These

noncited violations are described in the subject inspection report. If you contest the violations or

significance of the NCVs, you should provide a response within 30 days of the date of this

inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,

ATTN: Document Control Desk, Washington, DC 20555-0001, with copies to the Regional

Administrator, U.S. Nuclear Regulatory Commission, Region IV, 611 Ryan Plaza Drive,

Suite 400, Arlington, Texas 76011-4005; the Director, Office of Enforcement, U.S. Nuclear

Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the

Cooper Nuclear Station facility.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response will be made available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records component of NRCs

document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Nebraska Public Power District -2-

Should you have any questions concerning this inspection, we will be pleased to discuss them

with you.

Sincerely,

/RA/

Michael C. Hay, Chief

Project Branch C

Division of Reactor Projects

Docket: 50-298

License: DPR-46

Enclosure:

NRC Inspection Report 05000298/2005002

w/attachment: Supplemental Information

cc w/enclosure:

Michael T. Boyce, Nuclear Asset Manager

Nebraska Public Power District

1414 15th Street

Columbus, NE 68601

John C. McClure, Vice President

and General Counsel

Nebraska Public Power District

P.O. Box 499

Columbus, NE 68602-0499

P. V. Fleming, Licensing Manager

Nebraska Public Power District

P.O. Box 98

Brownville, NE 68321

Michael J. Linder, Director

Nebraska Department of

Environmental Quality

P.O. Box 98922

Lincoln, NE 68509-8922

Chairman

Nemaha County Board of Commissioners

Nemaha County Courthouse

1824 N Street

Auburn, NE 68305

Sue Semerena, Section Administrator

Nebraska Public Power District -3-

Nebraska Health and Human Services System

Division of Public Health Assurance

Consumer Services Section

301 Centennial Mall, South

P.O. Box 95007

Lincoln, NE 68509-5007

Ronald A. Kucera, Deputy Director

for Public Policy

Department of Natural Resources

P.O. Box 176

Jefferson City, MO 65101

Director

State Emergency Management Agency

P.O. Box 116

Jefferson City, MO 65102-0116

Chief, Radiation and Asbestos

Control Section

Kansas Department of Health

and Environment

Bureau of Air and Radiation

1000 SW Jackson, Suite 310

Topeka, KS 66612-1366

Daniel K. McGhee

Bureau of Radiological Health

Iowa Department of Public Health

401 SW 7th Street, Suite D

Des Moines, IA 50309

William J. Fehrman, President

and Chief Executive Officer

Nebraska Public Power District

1414 15th Street

Columbus, NE 68601

Jerry C. Roberts, Director of

Nuclear Safety Assurance

Nebraska Public Power District

P.O. Box 98

Brownville, NE 68321

Nebraska Public Power District -4-

Chief Technological Services Branch

National Preparedness Division

Department of Homeland Security

Emergency Preparedness & Response Directorate

FEMA Region VII

2323 Grand Boulevard, Suite 900

Kansas City, MO 64108-2670

Nebraska Public Power District -5-

Electronic distribution by RIV:

Regional Administrator (BSM1)

DRP Director (ATH)

DRS Director (DDC)

DRS Deputy Director (KSW)

Senior Resident Inspector (SCS)

Branch Chief, DRP/C (MCH2)

Senior Project Engineer, DRP/C (WCW)

Team Leader, DRP/TSS (RLN1)

RITS Coordinator (KEG)

RidsNrrDipmIipb

DRS STA (DAP)

J. Dixon-Herrity, OEDO RIV Coordinator (JLD)

RidsNrrDipmIipb

CNS Site Secretary (SLN)

W. A. Maier, RSLO (WAM)

SISP Review Completed: __mch__ ADAMS: : Yes G No Initials: __mch____

Publicly Available G Non-Publicly Available G Sensitive  : Non-Sensitive

R:\_CNS\2005\CN2005-02RP-SCS.wpd

RIV:RI:DRP/C SRI:DRP/C C:DRS/EB C:DRS/OB C:DRS/PEB C:DRS/PSB C:DRP/C

SDCochrum SCSchwind JAClark ATGody LJSmith MPShannon MCHay

T - WCWalker T - WCW /RA/ /RA/ /RA/ DAHolman /RA/

4/29/05 4/29/05 4/28/05 4/28/05 4/28/05 4/28/05 4/28/05

OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket.: 50-298

License: DPR-46

Report: 05000298/2005002

Licensee: Nebraska Public Power District

Facility: Cooper Nuclear Station

Location: P.O. Box 98

Brownville, Nebraska

Dates: January 1 through March 24, 2005

Inspectors: S. Schwind, Senior Resident Inspector

S. Cochrum, Resident Inspector

L. Carson II, Senior Health Physicist

W. Sifre, Reactor Inspector

Approved By: M. Hay, Chief, Branch C, Division of Reactor Projects

Enclosure

Contents

SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1. REACTOR SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1R04 Equipment Alignment . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1R05 Fire Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2

1R06 Flood Protection Measures . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

1R07 Heat Sink Performance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

1R08 Inservice Inspection Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

1R11 Licensed Operator Requalification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

1R12 Maintenance Rule Implementation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

1R13 Maintenance Risk Assessments and Emergent Work Evaluation . . . . . . . . . . . 8

1R14 Personnel Performance During Nonroutine Evolutions . . . . . . . . . . . . . . . . . . . 8

1R15 Operability Evaluations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 11

1R16 Operator Workarounds . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 13

1R17 Permanent Plant Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 14

1R19 Postmaintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 14

1R20 Refueling and Outage Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15

1R22 Surveillance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15

1R23 Temporary Plant Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16

1EP6 Drill Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16

2. RADIATION SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

2OS1 Access Control To Radiological Significant Areas . . . . . . . . . . . . . . . . . . . . . . 17

4. OTHER ACTIVITIES . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 22

4OA1 Performance Indicator Verification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 22

4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23

4OA3 Event Followup . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 24

4OA4 Crosscutting Aspects of Findings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28

4OA5 Other Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28

4OA6 Meetings, Including Exit . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 29

40A7 Licensee-Identified Violations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 29

ATTACHMENT: SUPPLEMENTAL INFORMATION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 29

KEY POINTS OF CONTACT . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

LIST OF DOCUMENTS REVIEWED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-2

LIST OF ACRONYMS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-5

Enclosure

SUMMARY OF FINDINGS

IR05000298/2005002; 01/01/05 - 03/24/05; Cooper Nuclear Station, Maintenance Rule

Implementation, Personnel Performance During Nonroutine Evolutions, Operability Evaluations,

Access Control to Radiological Significant Areas, Event Followup, and Other Activities.

The report covered a 3-month period of inspection by resident inspectors and region-based

inspectors. Six Green noncited violations, one Green finding, and three unresolved items were

identified. The significance of the issues is indicated by their color (Green, White, Yellow, or

Red) and was determined by the significance determination process in Inspection Manual

Chapter 0609. Findings for which the significance determination process does not apply are

indicated by the severity level of the applicable violation. The NRC's program for overseeing

the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor

Oversight Process, Revision 3, dated July 2000.

A. NRC-Identified and Self-Revealing Findings

Cornerstone: Initiating Events

  • Green. A self-revealing finding was identified regarding the failure to perform

adequate maintenance on the reactor protection system motor generator.

Inadequate maintenance on reactor protection system Motor Generator B resulted

in a winding failure and internal fault on the motor. The licensee failed to

incorporate vendor recommendations to periodically disassemble, clean, and

inspect the motor into maintenance activities.

This finding was considered more than minor since it affected the initiating events

cornerstone attribute of availability, reliability, and maintenance of equipment. This

finding was determined to have very low safety significance since it did not

contribute to the likelihood of a primary or secondary system loss of coolant

accident, did not contribute to a loss of mitigation equipment, and did not increase

the likelihood of a fire or internal/external flood (Section 1R12).

Cornerstone: Mitigating Systems

regarding the failure to implement the operability determination procedure. The

licensee failed to meet timeliness goals and documentation requirements for

evaluating the operability of the service water discharge strainers following high

differential pressure conditions.

This finding was more than minor since it was associated with the operability of

mitigating equipment and could become a more significant safety concern if left

uncorrected. This finding was determined to have very low safety significance

since the licensee was ultimately able to demonstrate operability of the affected

equipment. This finding had cross-cutting aspects associated with human

performance (Section1R15).

Enclosure

-2-

Criterion V, was identified for the failure to provide adequate instructions for

restoring the service water system to an operable configuration following the

completion of maintenance activities. This condition existed from January 21

through February 11, 2004, and resulted in Division 2 of the service water system

as well as Emergency Diesel Generator 2 being inoperable for 21 days.

The finding was greater than minor because it affected the reliability of the service

water system, which is relied upon to mitigate the effects of an accident. The

finding was determined to have a very low safety significance based on the results

of a Phase 3 Significance Determination Process evaluation (Section 4OA5).

Cornerstone: Emergency Preparedness

  • Green. The inspectors identified a noncited violation of 10 CFR 50.54(q) for the

failure to implement the emergency plan during an actual plant event. On

March 14, 2005, at approximately 2:51 a.m., station operators reported to the

control room that there was a fire in a trash bin in the multipurpose facility inside

the protected area. At approximately 3:08 a.m., heavy smoke and flames were

seen inside a container near the trash bin and the fire brigade leader reported to

the control room that the fire was not out. The fire was declared out at 3:13 a.m.

Emergency classification requirements state that a fire within the protected area

which takes longer than 10 minutes to extinguish meets the criteria for a

Notification of Unusual Event. No such declaration was made by the control room.

This finding affected the Emergency Preparedness cornerstone and was more than

minor because it affected the cornerstone attribute of emergency response

organization performance during an actual event response. This finding was

determined to be of very low safety significance since it only involved the failure to

declare a Notification of Unusual Event during an actual plant event. This finding

also had crosscutting aspects associated with human performance (1R14).

Cornerstone: Occupational Radiation Safety

  • Green. Two examples of a self-revealing noncited violation of Technical

Specification 5.7.2 were reviewed in which individuals entered locations in the

drywell that were not barricaded and posted as locked high radiation areas. On

January 18, 2005, at approximately 2:25 a.m., a worker who entered the drywell

unexpectedly received an electronic dosimeter dose rate alarm. Additionally, at

approximately 4:23 a.m., a second worker also received a dose rate alarm.

Radiation protection technicians measured 1,500 millirem per hour at

30 centimeters on the 943-foot elevation and 1,200 millirem per hour at

30 centimeters on the 901-foot elevation. This occurrence was entered into the

licensees corrective action program. However, immediate corrective actions taken

from the first event were not adequate to prevent the second event.

Enclosure

-3-

The issues are greater than minor because they were associated with a

cornerstone attribute (exposure control) and affected the associated cornerstone

objective because failure to control locked high radiation areas has the potential to

cause unplanned and unintended personnel dose. Using the Occupational

Radiation Safety Significance Determination Process, the inspector determined

that the finding was of very low safety significance because it did not involve:

(1) ALARA planning and controls, (2) an overexposure, (3) a substantial potential

for overexposure, or (4) an impaired ability to assess dose. Additionally, this

finding had crosscutting aspects associated with human performance and problem,

identification, and resolution (Section 2OS1.1).

when the radiation protection staff failed to perform an adequate survey of the

radiological hazards associated with the movement of the reactor transfer canal.

On January 19, 2005, electronic dosimeters of two workers unexpectedly alarmed

after they entered the dryer/separator pool and began moving the reactor fuel

transfer canal. The licensees investigation revealed that radiation protection staff

allowed the lifting and movement of the transfer canal before surveys were

performed on the bottom of the transfer canal. Radiation levels were as high as

700 millirem per hour at 30 centimeters and 1,200 millirem per hour on contact with

the bottom of the transfer canal. This occurrence was entered into the licensees

corrective action program.

The issue is greater than minor because it was associated with a cornerstone

attribute of program and process and affected the associated cornerstone objective

because inadequate radiation surveys have the potential to cause unplanned and

unintended personnel dose. Using the Occupational Radiation Safety Significance

Determination Process, the inspector determined that the finding was of very low

safety significance because it did not involve: (1) ALARA planning and controls,

(2) an overexposure, (3) a substantial potential for overexposure, or (4) an

impaired ability to assess dose. This finding also had crosscutting aspects

associated with human performance (Section 2OS1.2).

reviewed. Specifically, on January 5, 2005, an individual entered a properly posted

and controlled high radiation area in the condenser bay without authorization and

without observing the access controls that were in place. Licensee staff

determined that the individual entered the high radiation area without being logged

on the proper special work permit and without being made knowledgeable of the

radiological conditions in the area as required by the Technical Specifications. The

general radiation levels were found to be as high as of 300 millirem per hour. This

occurrence was entered into the licensees corrective action program.

The failure to notify radiation protection staff and to be briefed on the radiological

conditions before entering a high radiation area is greater than minor because it

was associated with a cornerstone attribute of program and process and affected

Enclosure

-4-

the cornerstone objective to ensure the adequate protection of the workers health

and safety from exposure to radiation because unauthorized entry into a high

radiation area could increase personnel dose. Using the Occupational Radiation

Safety Significance Determination Process, the inspector determined that the

finding was of very low safety significance because it did not involve: (1) ALARA

planning and controls, (2) an overexposure, (3) a substantial potential for

overexposure, or (4) an impaired ability to assess dose. This finding also had

crosscutting aspects associated with human performance (Section 2OS1.3).

B. Licensee-Identified Violations

Violations of very low safety significance, which were identified by the licensee, have

been reviewed by the inspectors. Corrective actions taken or planned by the licensee

have been entered into the licensees corrective action program. These violations and

corrective actions are listed in Section 4OA7 of this report.

Enclosure

REPORT DETAILS

The plant was operating at full power at the beginning of this inspection period. On January 15,

2005, the reactor was shut down for Refueling Outage 22. A normal reactor startup was

performed on February 17, the main turbine was synchronized to the grid on February 18, and

full power was achieved on February 20. Reactor power was reduced to approximately

70 percent on February 25 for a control rod pattern adjustment. Full power operation was

resumed on February 27.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R04 Equipment Alignment

Partial Equipment Alignment Inspections

a. Inspection Scope

The inspectors performed four partial equipment alignment inspections (four inspection

samples). The walkdowns verified that the critical portions of the selected systems were

correctly aligned per the system operating procedures. The following systems were

included in the scope of this inspection:

walkdown included accessible portions of the drywell on February 9, 2005, and the

suppression chamber on February 16. The walkdowns concentrated on

environmental qualification of equipment, seismic qualification of equipment, and

cleanliness.

  • Service Water (SW) System Loop B while Loop A was out of service for planned

maintenance on January 12, 2005. The walkdown included portions of the system

in the SW pump room and the control room.

maintenance on January 20, 2005. The walkdown included portions of the system

in the diesel generator room and control room.

  • EDG 2 while EDG 1 was out of service for planned maintenance on February 8,

2005. The walkdown included portions of the system in the diesel generator room

and control room.

b. Findings

No findings of significance were identified.

Enclosure

-2-

1R05 Fire Protection

.1 Quarterly Walkdowns

a. Inspection Scope

The inspectors performed six fire zone walkdowns to determine if the licensee was

maintaining those areas in accordance with its fire hazards analysis report (six

inspection samples). The walkdowns verified that fire suppression and detection

equipment were operable, that transient combustibles and ignition sources were

appropriately controlled, and that passive fire protection features were in place and

operable as required by the fire hazards analysis report. The following areas were

included in the scope of this inspection:

  • Fire Zone 2E, Steam Tunnel
  • Fire Zone 13A, Turbine Operating Floor
  • Fire Zone 3C, Reactor Building 932 elevation
  • Fire Zone 2A, Reactor Building 903 elevation

b. Findings

No findings of significance were identified.

.2 Annual Fire Drill

a. Inspection Scope

The inspectors observed the plant fire brigade during an unannounced fire drill on

January 26 (one inspection sample) to assess the licensees ability to fight fires.

Observations focused on the following aspects of the drill:

  • Protective clothing/turnout gear was properly donned.
  • Self-contained breathing apparatus equipment was properly worn and used.
  • Fire hose lines were capable of reaching all necessary fire hazard locations, the

lines were laid out without flow constrictions, and the hose was simulated as being

charged with water.

  • The fire area of concern was entered in a controlled manner (e.g., fire brigade

members stayed low to the floor and felt the door for heat prior to entry into the fire

area of concern).

Enclosure

-3-

  • Sufficient firefighting equipment was brought to the scene by the fire brigade to

properly perform their firefighting duties.

  • The fire brigade leader's firefighting directions were thorough, clear, and effective.
  • Radio communications with the plant operators and between fire brigade members

were efficient and effective.

  • Members of the fire brigade checked for fire victims and propagation into other

plant areas.

  • Effective smoke removal operations were simulated.
  • The firefighting preplan strategies were utilized.
  • The licensee planned drill scenario was followed and the drill objectives

acceptance criteria were met.

b. Findings

No findings of significance were identified.

1R06 Flood Protection Measures

a. Inspection Scope

The inspectors performed an inspection of the internal flood protection features for the

SW pump room (one sample). The inspection included a walkdown of flood protection

features, a review of procedures, the Updated Final Safety Analysis Report, selected

design criteria documents, and design calculations, including:

Revision 2

  • Calculation NEDC 91-069, Moderate Energy Line Break Flooding, dated June 12,

1991

The walkdown verified that flood protection features were in place and operable as

required by the flooding analysis for the service water pump room.

b. Findings

No findings of significance were identified.

Enclosure

-4-

1R07 Heat Sink Performance

a. Inspection Scope

The inspectors performed one heat sink performance review (one inspection sample) by

observing the inspection activities on Reactor Equipment Cooling Heat Exchanger A

performed on January 10, 2005, and reviewed the last set of test data for the heat

exchanger taken on November 15, 2004. A review of the heat exchanger performance

evaluation was conducted to identify potential deficiencies that could mask degraded

performance. The inspectors reviewed the type, location, and calibration of

instrumentation used to acquire the data to verify its acceptability for the evaluation. The

evaluation review was conducted and documented in accordance with Performance

Evaluation Procedure 13.15.1, Reactor Equipment Cooling Heat Exchanger

Performance Analysis, Revision 22.

b. Findings

No findings of significance were identified.

1R08 Inservice Inspection Activities

.1 Performance of Nondestructive Examination (NDE) Activities

a. Inspection Scope

Procedure 71111.08 requires the review of a minimum sample of five NDE activities of at

least two or three different types. The inspector witnessed the performance of five

volumetric and two surface examinations. This sample of NDE activities is listed in the

attachment.

For each of the NDE activities reviewed, the inspector verified that the examinations

were performed in accordance with American Society of Mechanical Engineers (ASME)

Code requirements.

During the review of each examination, the inspector verified that appropriate

nondestructive examination procedures were used, that examinations and conditions

were as specified in the procedure, and that test instrumentation or equipment was

properly calibrated and within the allowable calibration period. The inspector also

reviewed documentation to verify that indications revealed by the examinations were

dispositioned in accordance with the ASME Code specified acceptance standards.

The inspector verified the certifications of four Level II NDE personnel observed

performing examinations or identified during review of completed examination packages.

The inspection procedure requires review of one or two examinations from the previous

outage with recordable indications that were accepted for continued service to ensure

Enclosure

-5-

that the disposition was done in accordance with the ASME Code. There were no

recordable indications that required evaluation during the last outage.

If the licensee completes welding on the pressure boundary for Class 1 or 2 systems

since the beginning of the previous outage, the procedure requires verification that

acceptance and preservice examinations were done in accordance with the ASME Code

for one to three welds. There were no welds available for review; however, the inspector

did review the licensees procedures governing weld repairs and found that they were in

accordance with ASME Code requirements.

The procedure also requires verification that one or two ASME Code Section XI repairs

or replacements meet Code requirements. There were no code repairs or replacements

available at the time of this inspection.

Findings

No findings of significance were identified.

.2 Identification and Resolution of Problems

a. Inspection Scope

The inspector reviewed selected inservice inspection related condition reports issued

during the current and past refueling outages. The review served to verify that the

licensees corrective action process was being correctly utilized to identify conditions

adverse to quality and that those conditions were being adequately evaluated, corrected,

and trended.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification

a. Inspection Scope

On January 13, 2005, the inspectors observed one session of licensed operator

requalification training (one inspection sample) in the plant simulator. The training

evaluated operator ability to perform the major plant evolutions for a normal reactor

shutdown in preparation for the upcoming refueling outage. Observations were focused

on the following key attributes of operator performance:

  • Crew performance in terms of clarity and formality of communications
  • Ability to take timely and appropriate actions

Enclosure

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  • Prioritizing, interpreting, and verifying alarms
  • Correct implementation of procedures, including the alarm response procedures
  • Timely control board operation and manipulation, including high-risk operator

actions

  • Oversight and direction provided by the shift supervisor, including the ability to

identify and implement appropriate Technical Specification requirements, reporting,

emergency plan actions, and notifications

  • Group dynamics involved in crew performance

The inspectors also verified that the simulator response during the training scenario

closely modeled expected plant response during an actual event.

b. Findings

No findings of significance were identified.

1R12 Maintenance Rule Implementation

a. Inspection Scope

The inspectors reviewed two equipment performance issues (two inspection samples) to

assess the licensees implementation of their maintenance rule program. The inspectors

verified that components which experienced performance problems were properly

included in the scope of the licensees maintenance rule program and that the

appropriate performance criteria were established. Maintenance rule implementation

was determined to be adequate if it met the requirements outlined in 10 CFR 50.65 and

Administrative Procedure 0.27, Maintenance Rule Program, Revision 15. The

inspectors reviewed the following equipment performance problems:

CNS-2005-00980)

b. Findings

Introduction. A self-revealing, Green finding was identified regarding the failure to

perform adequate maintenance on the RPS motor generator system.

Details. On January 30, the RPS MG B failed due to an internal fault on the motor for

the MG. The apparent cause, which was later confirmed by vendor analysis, was the

fact that the motor had aged to the point where a turn-to-turn short circuit within the

Enclosure

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stator winding had occurred due to insulation breakdown. Both RPS MGs were original

plant equipment and had been in operation for over 30 years on nearly a continuous

basis. Because the RPS MG A had a similar history to the failed MG, both motors were

removed and sent to an offsite facility for inspection and repair. Although the MG motor

failed during Refueling Outage 22 while the RPS bus was being powered from an

alternate source, the age-related failure mechanism was present during normal

operation. A loss of both RPS MGs would have resulted in a reactor scram and a loss

of one MG would have affected reactor equipment cooling, reactor recirculation MG

ventilation, and standby gas treatment systems.

The licensee conducted an apparent cause determination which discovered that a

preventive maintenance program did not exist for the MGs and recommended a

preventive maintenance program be established for RPS MGs. This was based on

vendor guidance that recommended periodic disassembly, cleaning, and inspection.

The apparent cause determination also noted that the licensees preventive

maintenance optimization project had considered the vendors recommendations but

rejected them based on performance history of the equipment and predictive

maintenance activities. Predictive maintenance work orders to detect failures similar to

the one experienced were generated to conduct off-line testing during Refueling

Outage 22 but were rejected from the outage schedule due to timing of the request and

the perceived low risk of failure. Immediate corrective actions for this condition included

issuing a preventive maintenance request implementing the maintenance

recommendation contained in the vendor manual.

Analysis. The lack of an adequate preventive maintenance program for RPS MGs was

considered a performance deficiency which affected the Initiating Events cornerstone.

This finding was considered more than minor since it affected the cornerstone attribute

of equipment availability, reliability, and maintenance. Based on the results of a

Significance Determination Process, Phase 1 evaluation, the finding was determined to

have very low safety significance (Green) since it did not contribute to the likelihood of a

primary or secondary system loss of coolant accident, did not contribute to a loss of

mitigation equipment, and did not increase the likelihood of a fire or internal/external

flood.

Enforcement. The components affected by this finding were not considered

safety-related; therefore, no violation of NRC requirements was identified. The licensee

entered this finding into their corrective action program as CR-CNS-2005-00980. This

finding is identified as FIN 05000298/2005002-01, Inadequate Maintenance Resulted in

Failure of Reactor Protection System Power Supply.

Enclosure

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1R13 Maintenance Risk Assessments and Emergent Work Evaluation

a. Inspection Scope

The inspectors reviewed five risk assessments (five inspection samples) for planned or

emergent maintenance activities to determine if the licensee met the requirements of

10 CFR 50.65(a)(4) for assessing and managing any increase in risk from these

activities. Evaluations for the following maintenance activities were included in the

scope of this inspection:

  • Refueling Outage 22 overall risk assessment dated January 15, 2005
  • Risk associated with repairs to EDG 1 on February 11, 2005
  • Risk associated with controlled burns in the vicinity of offsite power lines on

March 15, 2005

  • Risk associated with main turbine trip block testing on March 17, 2005
  • Risk associated with repairs to EDG 1 on March 23, 2005

b. Findings

No findings of significance were identified.

1R14 Personnel Performance During Nonroutine Evolutions

a. Inspection Scope

For the five nonroutine events described below (five inspection samples), the inspectors

reviewed operator logs, plant computer data, and strip charts to determine what

occurred, how the operators responded, and whether the response was in accordance

with plant procedures.

  • On November 20, 2004, the inspectors responded to the control room following an

unexpected SW system pressure drop after starting an idle SW pump. The

inspectors verified that systems responded as designed and that operators took

appropriate actions to stabilize plant conditions. The inspectors also observed the

licensees troubleshooting activities, which determined that the SW discharge

strainer in each loop had clogged with silt during the pump start which caused the

low pressure condition in the SW system.

  • On February 2, the inspectors responded to the control room to assess operators

response to a possible reactor draindown event after receiving reactor building

high sump level alarms. Followup investigation determined that no drain path from

Enclosure

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the reactor vessel existed. The cause of the sump level alarm was a valve

misalignment in the control rod drive hydraulic system which allowed water from

the condensate storage tank to drain into the sump.

  • On February 7, the inspectors responded to the control room following a complete

loss of shutdown cooling. Shutdown cooling was lost following a failure of EDG 1

during a sequential load test which resulted in a loss of an operating fuel pool

cooling pump and both operating residual heat removal (RHR) pumps and partial

draindown of both RHR loops. The inspectors observed recovery actions and

reviewed the licensees implementation of Technical Specifications (TS) and their

emergency plan.

  • On February 12, 2005. the inspectors responded to the control room during the

reactor pressure vessel hydrostatic test to evaluate compliance with TS 3.4.9.

During hydrostatic testing, using Surveillance Procedure 6.MISC.504, ASME

Class 1 Hydrostatic Test, Revision 2, the control room operators suspended the

test until it could be determined if reactor coolant system pressure and temperature

were being controlled in accordance with TS 3.4.9. The licensee determined the

requirements of TS 3.4.9 were satisfied and continued the test. The inspectors

observed the plant pressurization and verified that the licensee satisfied TS 3.4.9

during the test.

  • On March 14, 2005, inspectors responded to the site following a fire in the

multipurpose facility (MPF). The fire had been extinguished before the inspectors

arrived. The inspectors verified that there was no impact to safety-related

equipment and that no radioactive material was involved. The inspectors also

reviewed the licensee implementation of their emergency plan during the event.

b. Findings

Introduction. A Green, noncited violation (NCV) of 10 CFR 50.54(q) was identified for

the failure to implement the emergency plan during an actual plant event.

Description. On March 14, at approximately 2:47 a.m., control room operators received

a smoke alarm from the MPF and both fire pumps started. An auxiliary operator was

dispatched to the MPF to investigate the alarm and, at 2:51 a.m., reported to the control

room that there was a fire in a trash bin. The control room entered Emergency

Procedure 5.4FIRE and dispatched the fire brigade. The operator immediately

extinguished the fire in the trash bin using a fire hose from a hose station in the vicinity.

The operator and a radiation protection technician, who had also responded to the

scene, began to overhaul the trash bin. During overhaul activities, the auxiliary operator

noted that a shipping container adjacent to the burning trash bin had been scorched by

the flames and the container felt hotter than he expected. The operator also stated that,

at the time, he was unsure if the fire had originated inside the container. The operator

reported to the control room that the fire in the trash bin had been extinguished and the

Enclosure

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control room sounded the all-clear alarm. The fire brigade arrived at the scene a

2:58 a.m. The operator reported his concerns regarding the shipping container to the

fire brigade leader before leaving the area.

The fire brigade made the decision to open the shipping container which required cutting

a lock on the door. The container was opened at approximately 3:08 a.m., at which time

heavy smoke and flames were seen inside the container and the fire brigade leader

reported to the control room that the fire was not out. The fire brigade extinguished the

flames with a fire hose and the fire was declared out at 3:13 a.m.

The cause of the fire was determined to be a failed high pressure mercury vapor lamp

located directly above the trash bin. The lamp burst and the hot filament fell into the

trash bin, igniting the contents. It was noted that this lamp was flickering several days

before the fire, indicative of immanent failure. The vendor for this particular style of lamp

recommended routine replacement of these lamps prior to failure since failure can result

in the lamp bursting which has been known to start fires. The licensee had no program

to routinely replace these lamps prior to failure.

The MPF is located inside the protected area, adjacent to the power block. Emergency

Plan Implementing Procedure (EPIP) 5.7.1, Emergency Classification, Revision 31,

states that a fire within the protected area which takes longer than 10 minutes to

extinguish meets the criteria for a Notification of Unusual Event. No such declaration

was made by the control room despite a report that the fire was not out 17 minutes after

the initial report of the fire. The licensee stated that they believed the fire in the trash bin

and the fire in the shipping container were two separate events and each fire was

extinguished within 10 minutes.

Analysis. Failure to implement the emergency plan during an actual event was

considered to be a performance deficiency. This finding affected the Emergency

Preparedness cornerstone and was more than minor because it affected the cornerstone

attribute of emergency response organization performance during actual event

response. Using MC 0609, Significance Determination Process, Appendix B, this

finding was determined to be of very low safety significance since it only involved the

failure to declare a Notification of Unusual Event during an actual plant event.

This finding also had crosscutting aspects associated with human performance. This

assessment was based on the fact that sufficient information was available during the

event for the control room crew to have made the decision to enter the emergency plan.

Enforcement. 10 CFR 50.54(q) requires that the licensee shall maintain and follow an

emergency plan. Cooper Nuclear Stations emergency plan, as implemented by

EPIP 5.7.1, required the declaration of a Notification of Unusual Event based on a fire

that took longer the 10 minutes to extinguish. The licensee did not make this declaration

even though the fire in the MPF on March 14, 2005, took a total of 22 minutes to

extinguish. Because this violation is of very low safety significance and because the

licensee entered it into their corrective action program as Condition Report CR-2005-

Enclosure

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02295, this violation is being treated as noncited in accordance with Section VI.A of the

Enforcement Policy: NCV 05000298/2005002-02, Failure to Implement Emergency Plan

During a Fire.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors reviewed five operability determinations (five inspection samples)

associated with mitigating system capabilities to ensure that the licensee properly

justified operability and that the component or system remained available so that no

unrecognized increase in risk occurred. These reviews considered the technical

adequacy of the licensees evaluation and verified that the licensee considered other

degraded conditions and their impact on compensatory measures for the condition being

evaluated. The inspectors referenced the Updated Safety Analysis Report, Technical

Specifications, and the associated system design criteria documents to determine if

operability was justified. The inspectors reviewed the following equipment conditions

and associated operability evaluations:

  • Nonconforming conditions (excessive calcium) in the Division 1, 250 Vdc batteries

cells (CR-CNS-2003-00720)

postaccident radiological conditions (CR-CNS-2004-04153)

B discharge strainer blow down valves (CR-CNS-2005-02115 and CR-CNS-2005-

02293)

  • Source Range Monitor A erratic behavior (spiking) (CR-CNS- 2005-00638)
  • SW discharge strainers clogged with silt during the SW pump start (CR-CNS-2004-

07409)

b. Findings

Introduction. A Green NCV of TS 5.4.1 was identified regarding the failure to follow

Procedure 0.5 OPS, Operations Review of Notification/Operability Determinations,

Revision 23.

Description. On November 20, 2004, at approximately 8:25 a.m., with two SW pumps in

service, operators started an additional pump for planned maintenance. Control room

operators immediately observed an unexpected pressure drop in both loops of SW, high

differential pressure alarms on both SW discharge strainers, and isolation of the

nonessential SW loads. Operators subsequently started the fourth SW pump to attempt

to restore system pressure. This resulted in both SW discharge strainers becoming

Enclosure

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clogged with silt and automatically starting their backwash cycle. Operators in the SW

pump room noted at 8:26 a.m. that both SW discharge strainer differential pressure

instruments indicated greater than the operability limit. System pressure stabilized in

SW Loop A after the strainer had backwashed for approximately 3 minutes; however,

pressure was not restored in SW Loop B until operators bypassed the strainer

approximately 16 minutes later. The licensee concluded that the strainers became

clogged with silt during the start of idle SW pumps. Both strainers were cleaned and

returned to service approximately 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> later

System Operating Procedure 2.2.71, Service Water System, Revision 74, states that

SW zurn [discharge] strainers have an operability limit of 15 psid based on structural

integrity of the strainer basket. Operators declared SW Loop B inoperable when the

discharge strainer was bypassed, but failed to declare either SW loop inoperable based

on exceeding this differential pressure limit. In addition, the licensee did not document a

reasonable assurance of operability for the SW system until 6:23 p.m. on November 20,

2004, 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> after discovery of the condition. TS 3.7.2 (B) requires the plant to be

placed in Mode 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and Mode 4 within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br /> if both SW loops are

inoperable. Administrative Procedure 0.5OPS required that a reasonable assurance of

operability be documented as soon as practical and commensurate with the safety

importance of the components affected; otherwise declare equipment inoperable if a

reasonable assurance of operability did not exist. No such assurance was documented,

nor was SW Loop A immediately declared inoperable. During subsequent interviews,

the licensee stated that, despite the lack of documentation, and despite the indicated

differential pressure across SW Discharge Strainer A, operators believed that a

reasonable assurance of operability existed at the time of discovery since the differential

pressure returned to normal approximately 3 minutes after the start of the event. Based

on the guidance in Generic Letter 91-18, the inspectors concluded that the 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br />

used document a reasonable assurance of operability not commensurate with safety

given that no actions were taken to shut down the reactor and the TS-required action

was to be in Mode 3 in 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

Immediate corrective actions for this event included cleaning and inspection of both SW

discharge strainers. The strainers were found to be 80 to 90 percent clogged with sand.

No mechanical damage was found during the inspections.

Analysis. The failure to follow station procedures was considered a performance

deficiency which affected the Mitigating Systems Cornerstone since it was associated

with the operability of mitigating equipment. This finding was considered more than

minor since failure to follow station procedures, specifically those which would require

short-term TS actions to be implemented, could become a more significant safety

concern if left uncorrected. Based on the results of a significance determination

process, Phase 1 evaluation, this finding was determined to have very low safety

significance (Green) since it did not represent an actual loss of the safety function of the

system and the licensee was ultimately able to demonstrate operability of the affected

equipment.

Enclosure

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This finding had crosscutting aspects associated with human performance. This

assessment was based on the fact that Procedure 0.5OPS reflected current guidance

regarding operability determinations and that a significant amount of training had been

conducted, yet personnel still failed to follow the procedure. Furthermore, operators

failed to declare the affected components inoperable, despite the fact that an

indeterminate state of operability existed on the SW system for approximately 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br />.

Enforcement. TS 5.4.1 (a) requires written procedures to be implemented as

recommended by Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.

Appendix A recommends procedures for equipment control. Administrative

Procedure 0.5OPS, Operations Review of Notification/Operability Determinations,

Revision 23, required operators to document a basis for reasonable assurance of

operability commensurate with safety importance of the system affected or to declare the

equipment inoperable. Contrary to this requirement, the operators failed to document a

reasonable assurance of operability in a time frame commensurate with safety and failed

to declare affected equipment inoperable in the absence of a reasonable assurance of

operability. Because this violation was of very low safety significance and was entered

in the corrective action program as CR-CNS-2004-07409, this violation is being treated

as an NCV consistent with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000298/2005002-03, Failure to Follow Operability Determination Procedure.

1R16 Operator Workarounds

a. Inspection Scope

The inspectors reviewed one potential operator work around item (one inspection

sample) to evaluate its affect on mitigating systems and the operators ability to

implement abnormal or emergency procedures. In addition, open operability

determinations and selected condition reports were reviewed and operators were

interviewed to determine if there were additional degraded or nonconforming conditions

that could complicate the operation of plant equipment. The following potential operator

workaround was reviewed:

  • Operation of Temperature Control Valve SW-TCV-451A in manual versus

automatic.

b. Findings

No findings of significance were identified.

1R17 Permanent Plant Modifications

a. Inspection Scope

The inspectors reviewed a modification to replace all four reactor feed check valves

during Refueling Outage 22 (one inspection sample). The inspection included a review

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of the modification package and observations of field work to install the new check

valves. The inspectors also observed and reviewed the results from the

postmaintenance testing.

b. Findings

No findings of significance were identified.

1R19 Postmaintenance Testing

a. Inspection Scope

The inspectors reviewed or observed six selected postmaintenance tests (six inspection

samples) to verify that the procedures adequately tested the safety function(s) that were

affected by maintenance activities on the associated systems. The inspectors also

verified that the acceptance criteria were consistent with information in the applicable

licensing basis and design basis documents and that the procedures were properly

reviewed and approved. Postmaintenance tests for the following maintenance activities

were included in the scope of this inspection:

  • Corrective maintenance to clean the valve plug and valve seat on Main Steam

Isolation Valve MS-AOV-AO80B (Work Order 4403744)

  • Preventive maintenance on SW-MO-2128 to clean and inspect the valve operator

(Work Order 4345839)

  • Corrective Maintenance on EDG 1 to replace a failed diode and Relay 4EMX1

(Work Order 4426786)

  • Installation of Containment Isolation Logic Change modification to implement GE

Service Information Letter 131 (Change Evaluation Document 6014280)

  • Corrective maintenance on the reactor building crane to upgrade equalizer plates

and welds in response to a 10 CFR Part 21 notification (CR-CNS-2005-00094)

  • Corrective maintenance to replace a leaking fuel injector on EDG 1 (CR-CNS-

2005-02449)

b. Findings

No findings of significance were identified.

1R20 Refueling and Outage Activities

a. Inspection Scope

Enclosure

-15-

The inspectors evaluated the licensees outage activities associated with Refueling

Outage 22 to ensure that: risk was considered in developing the outage schedule;

administrative risk reduction methodologies were implemented to control plant

configuration; mitigation strategies were developed for losses of key safety functions;

and the operating license and Technical Specification requirements were satisfied to

ensure defense-in-depth. Specifically, the following activities were included in the scope

of this inspection:

  • A review of the Refueling Outage 22 schedule, Revision 1, including the outage

risk assessment

  • Control room observations of the reactor shutdown and initial cooldown, including

primary containment walkdown immediately after shutdown.

  • Daily review of critical parameter associated with reactor vessel level, shutdown

cooling operations, and offsite power availability.

  • Daily review of scheduled work, prioritization, control, and the outage risk

assessment for that work

  • Control room observations of the reactor startup and heatup.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors observed or reviewed the following six surveillance tests (six inspection

samples) to ensure that the systems were capable of performing their safety function

and to assess their operational readiness. Specifically, the inspectors verified that the

following surveillance tests met TS requirements, the Updated Safety Analysis Report,

and licensee procedural requirements:

  • 6.PC.503, Drywell-to-Suppression Chamber Leakage Test, Revision 14,

performed on January 18, 2005

and HEPA [High Efficiency Particulate Air] Filter In-Place Leak Test, and

Component Leak Test (Div 2), Revision 9, performed on January 19

  • 6.PC.513, Main Steam Local Leak Rate Tests, Revision 11, performed on

January 20, 2005

Enclosure

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Revision 7, performed on January 21, 2005

  • 6.PC.519, Reactor Core Isolation Coolant (RCIC) Local Leak Rate Tests,

Revision 10, performed on February 8, 2005

  • 6.1DG.302, Undervoltage Logic Functional, Load Shedding, and Sequential

Loading Test (Div I), Revision 29, performed on February 14, 2005

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications

a. Inspection Scope

The inspectors reviewed one temporary plant modification (one inspection sample),

Work Order 4420251, implemented on January 13, which raised the condensate storage

tank heater setpoint from 40 degrees to 70 degrees. This was in support of Refueling

Outage 22 vessel floodup due to the reactor vessel minimum temperature of 68 degrees.

The inspectors verified that the change did not require NRC approval prior to

implementation and adequate controls on the installation existed.

b. Findings

No findings of significance were identified

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

a. Inspection Scope

The inspectors observed the licensee perform one emergency preparedness drill on

March 9 (one inspection sample). Observations were conducted in the control room,

technical support center, and emergency operations facility. During the drill, the

inspectors assessed the licensees performance related to classification, notification,

and protective action recommendations. Following the drill, the inspectors reviewed the

licensees critique to determine if issues were appropriately identified and documented.

The following documents were reviewed during this inspection:

Enclosure

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b. Findings

No findings of significance were identified.

2. RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiological Significant Areas

a. Inspection Scope

This area was inspected to assess the licensees performance in implementing physical

and administrative controls for airborne radioactivity areas, radiation areas, high

radiation areas, and worker adherence to these controls. The inspector used the

requirements in 10 CFR Part 20, the Technical Specifications, and the licensees

procedures required by Technical Specifications as criteria for determining compliance.

During the inspection, the inspector interviewed the radiation protection manager,

radiation protection supervisors, and radiation workers. The inspector performed

independent radiation dose rate measurements. and reviewed the following items:

  • Performance indicator events and associated documentation packages reported by

the licensee in the Occupational Radiation Safety Cornerstone

  • Controls (surveys, posting, and barricades) of the Reactor Building, Drywell,

Refueling Floor, Turbine Building, and Radwaste Building radiation, high radiation

areas, and airborne radioactivity areas

  • Radiation work permits, procedures, engineering controls, and air sampler

locations

  • Conformity of electronic personal dosimeter alarm setpoints with survey indications

and plant policy; workers knowledge of required actions when their electronic

personnel dosimeter noticeably malfunctions or alarms

radioactivity work areas

  • Physical and programmatic controls for highly activated or contaminated materials

(nonfuel) stored within the spent fuel storage pool

  • Self-assessments related to the access control program since the last inspection
  • Corrective action documents related to access controls

Enclosure

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  • Licensee actions in cases of repetitive deficiencies or significant individual

deficiencies

  • Special work permit briefings and worker instructions
  • Adequacy of radiological controls such as required surveys, radiation protection job

coverage, and contamination controls during job performance

  • Dosimetry placement in high radiation work areas with significant dose rate

gradients

and very high radiation areas

  • Controls for special areas that have the potential to become very high radiation

areas during certain plant operations

  • Posting and locking of entrances to all accessible high dose rate - high radiation

areas and very high radiation areas

  • Radiation worker and radiation protection technician performance with respect to

radiation protection work requirements

Either because the conditions did not exist or an event had not occurred, no

opportunities were available to review the following items:

  • Licensee event reports (LERs), audits, and special reports related to the access

control program since the last inspection

  • Adequacy of the licensees internal dose assessment for any actual internal

exposure greater than 50 millirem CEDE (committed effective dose equivalent)

The inspector completed 21 of the required 21 samples.

b. Findings

.1 Introduction. The inspector reviewed a Green, self-revealing NCV of TS 5.7.2, resulting

from the licensees failure to barricade and post two areas as locked high radiation

areas.

Description. On January 18, 2005, two workers who entered the drywell unexpectedly

received electronic dosimeter alarms because they entered individual areas with

radiation levels in excess of 1,000 millirem per hour. Radiation protection staff members

measured 1,500 millirem per hour at 30 centimeters on the 943-foot elevation near Fan

Enclosure

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Cooler C and a 24-inch RHR B pipe and 1,200 millirem per hour at 30 centimeters on

the 901-foot elevation near an 18-inch core spray pipe.

A review of the circumstances revealed the following:

  • radiation protection personnel were unaware of the change to radiological

conditions;

  • the two areas were not barricaded or conspicuously posted;
  • the licensee did not install area radiation monitors set to alarm if radiation levels

increased in order to provide a visual and an audible signal to alert personnel in

the area of the increase.

Analysis. The failure to control a locked high radiation area in accordance with TS 5.7.2

is a performance deficiency. This finding is greater than minor because it is associated

with the Occupational Radiation Safety Program and Process Attribute and affected the

cornerstone objective, which is to ensure adequate protection of worker health and

safety from exposure to radiation. This occurrence involved workers unplanned,

unintended dose or potential for such a dose that could have been significantly greater

as a result of a single, minor, reasonable alteration of circumstances. Using the

Occupational Radiation Safety Significance Determination Process, the inspector

determined that the finding was of very low safety significance because it did not involve:

(1) ALARA planning and controls, (2) an overexposure, (3) a substantial potential for

overexposure, or (4) an impaired ability to assess dose.

This finding had associated aspects in human performance and problem identification

and resolution. The licensees immediate corrective actions from the first event

(2:25 a.m.) were not effective in precluding the second event (4:23 a.m.). Additionally,

the licensee did not control the drywell as a locked high radiation area, pursuant to

TS 5.7.2, until 6 a.m.

Enforcement. TS 5.7.2, requires, in part, that areas accessible to personnel with dose

rates such that a major portion of the body could receive in one hour a deep dose

equivalent in excess of 1000 millirem per hour at 30 centimeters from the source of

radiation be provided with locked doors to prevent unauthorized entry. For individual

high radiations areas accessible to personnel that are located within large areas, such

as containment, or areas where no enclosure exists for purposes of locking and no

enclosure can be reasonably constructed around the individual area, that area shall be

barricaded and conspicuously posted. Additionally, area radiation monitors that have

been set to alarm if radiation levels increase need to be in place to provide a visual and

an audible signal to alert personnel in the area of the increase.

The failure to barricade, post, and control these locked high radiation areas in the

drywell were two examples of a violation of TS 5.7.2. Since these failures to control

locked high radiation areas resulted in an occurrence of very low safety significance

Enclosure

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were entered into the licensees corrective action program Condition Report CR-CNS-

2005-00380, this violation is being treated as an NCV consistent with Section VI.A of the

NRC Enforcement Policy: NCV 5000298/2005002-04, Failure to Control a Locked High

Radiation Area in Accordance with TS 5.7.2.

.2 Introduction. The inspector reviewed a Green, self-revealing NCV involving the radiation

protection staffs failure to perform an adequate survey in the dryer/separator pool before

moving the reactor fuel transfer canal pursuant to 10 CFR 20.1501(a).

Description. On January 19, 2005, the radiation protection staff allowed the lifting and

movement of the transfer canal before surveys were completed on the bottom of the

transfer canal. Electronic dosimeters of two workers unexpectedly alarmed after they

entered the dryer/separator pool and began moving the reactor fuel transfer canal. After

the workers electronic dosimeter alarmed, a radiation protection technician surveyed the

bottom of the transfer canal, and the radiation levels detected were 1,200 millirem per

hour on contact and 700 millirem per hour at 30 centimeters. Consequently, the

workers had the potential to receive unintended and unexpected radiation exposure

because the magnitude and extent of radiation levels and potential radiological hazards

were not fully evaluated.

Analysis. The failure to conduct adequate radiation surveys is a performance deficiency.

This finding is greater than minor because it is associated with the Occupational

Radiation Safety Program and Process attribute and affected the cornerstone objective,

which is to ensure adequate protection of worker health and safety from exposure to

radiation. This occurrence involved workers unplanned, unintended dose or potential

for such a dose that could have been significantly greater as a result of a single, minor,

reasonable alteration of circumstances. Using the Occupational Radiation Safety

Significance Determination Process, the inspector determined that the finding was of

very low safety significance because it did not involve: (1) ALARA planning and

controls, (2) an overexposure, (3) a substantial potential for overexposure, or (4) an

impaired ability to assess dose.

Enforcement. Pursuant to 10 CFR 20.1003, survey means an evaluation of the

radiological conditions and potential hazards incident to the production, use, transfer,

release, disposal, or presence of radioactive material or other sources of radiation.

10 CFR 20.1501(a) requires, in part, that each licensee make or cause to be made

surveys that may be necessary for the licensee to comply with the regulations in

10 CFR Part 20 and that are reasonable under the circumstances to evaluate the extent

of radiation levels and the potential radiological hazards that could be present.

10 CFR 20.1201 requires, in part, that the licensee control the occupational dose to

individual adults to the dose limits in 10 CFR Part 20. The inspector determined that the

licensees failure to survey the bottom of the transfer canal prevented them from

controlling individuals occupational dose.

Because this failure to perform complete radiation surveys resulted in an occurrence of

very low safety significance, and it has been entered into the licensees corrective action

Enclosure

-21-

program (Condition Report CR-CNS-2005-00427), this violation is being treated as an

NCV consistent with Section VIA of the NRC Enforcement Policy:

NCV 5000298/2005002-05, Failure to Perform an Adequate Survey to Evaluate

Radiological Hazards per 10 CFR 20.1501.

.3 Introduction. The inspector reviewed a Green, self-revealing NCV of TS 5.7.1, resulting

from an individual entering a high radiation area without authorization and without noting

the access controls that were in place.

Description. On January 5, 2005, a worker entered a high radiation area in the

condenser bay without being logged on the proper special work permit and without

having the radiation protection staff brief him on the radiological conditions.

Consequently, the individual was exposed to unplanned and unintended radiation

exposure. During the investigation of the occurrence, the licensee staff determined that

an individual entered the condenser bay high radiation area and his electronic dosimeter

alarmed because the alarm dose rate setpoint was exceeded. Radiation protection staff

further determined that the individual entered a TS high radiation area without: (1) being

logged on the proper special work permit and (2) being briefed on the radiological

conditions in the area. The radiation levels in the general area where found to be in

excess of 300 millirem per hour.

Analysis. The failure to notify radiation protection and get briefed on the radiological

conditions before entering a high radiation area is a performance deficiency. This

finding is greater than minor because it was associated with the Occupational Radiation

Safety Program and Process attribute and affected the cornerstone objective to ensure

the adequate protection of worker health and safety. This occurrence involved a

workers unplanned, unintended dose, or potential for such a dose, that could have been

significantly greater as a result of a single, minor, reasonable alteration of

circumstances. Using the Occupational Radiation Safety Significance Determination

Process, the inspector determined that the finding was of very low safety significance

because it did not involve: (1) ALARA planning and controls, (2) an overexposure,

(3) a substantial potential for overexposure, or (4) an impaired ability to assess dose.

Enforcement. TS 5.7.1 requires, in part, that entry into high radiation areas shall be

controlled by the issuance of a special work permit that requires a radiation monitoring

device that continuously integrates the radiation dose rate in the area and alarms when

preset integrated dose is received. Entry into such areas with this monitoring device

may be made only after dose rate levels have been established and personnel have

been made aware of them.

Because this failure to control access to a high radiation area resulted in an occurrence

of very low safety significance, and it has been entered into the licensees corrective

action program (Condition Report CR-CNS-2005-00062), this violation is being treated

as an NCV consistent with Section VI.A of the NRC Enforcement Policy: NCV

5000298/200502-06, Failure to Gain Authorized Access to a High Radiation Area in

Accordance with TS 5.7.1.

Enclosure

-22-

4. OTHER ACTIVITIES

4OA1 Performance Indicator Verification

a. Inspection Scope

The inspector sampled licensee submittals for the performance indicators listed below

from June 2004 to January 2005. To verify the accuracy of the performance indicator

data reported during that period, performance indicator definitions and guidance

contained in Nuclear Energy Institute 99-02, "Regulatory Assessment Indicator

Guideline," Revision 2, were used to verify the basis in reporting for each data element.

Occupational Radiation Safety Cornerstone

  • Occupational Exposure Control Effectiveness Performance Indicator

Licensee records reviewed included corrective action documentation that identified

occurrences of locked high radiation areas (as defined in the licensees TS), very high

radiation areas (as defined in 10 CFR 20.1003), and unplanned personnel exposures (as

defined in Nuclear Energy Institute 99-02). Additional records reviewed included ALARA

records and whole body counts of selected individual exposures. The inspector

interviewed licensee personnel that were accountable for collecting and evaluating the

performance indicator data. In addition, the inspector toured plant areas to verify that

high radiation, locked high radiation, and very high radiation areas were properly

controlled. No significant regulatory problems or concerns were identified during this

procedure.

Public Radiation Safety Cornerstone

  • Radiological Effluent Technical Specification/Offsite Dose Calculation Manual

Radiological Effluent Occurrences

The inspector reviewed radiological effluent release program corrective action records

and annual effluent release reports documented from June 2004 to January 2005 to

determine if any liquid or gaseous effluent releases resulted in events that exceeded the

performance indicator thresholds. The inspector interviewed licensee personnel that

were accountable for collecting and evaluating the performance indicator data.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

.1 Routine Review of Identification and Resolution of Problems

Enclosure

-23-

a. Inspection Scope

The inspectors reviewed a selection of condition reports written during the inspection

period to verify the licensee was entering conditions adverse to quality into the corrective

action program at an appropriate threshold. Additionally, the inspectors verified that

condition reports were appropriately categorized and dispositioned in accordance with

the licensees procedures, and in the case of significant conditions adverse to quality, to

review the adequacy of licensee root cause determinations, extent of condition reviews,

and implemented corrective actions. The following condition report was reviewed in

depth during this period (one sample):

February 7

b. Findings

No findings of significance were identified.

.2 Occupational Radiation Safety Sample Review

a. Inspection Scope

The inspectors evaluated the effectiveness of the licensee's problem identification and

resolution processes regarding exposure tracking, higher than planned exposure levels,

and radiation worker practices. The inspector reviewed the corrective action documents

listed in the attachment against the licensees problem identification and resolution

program requirements.

b. Findings

No findings of significance were identified.

.3 Identification and Resolution of Problems Crosscutting Aspects of Findings

Section 2OS1.1 describes a finding with crosscutting aspects associated with problem

identification and resolution.

4OA3 Event Followup

.1 (Closed) LER 05000298/2004004-00. Loss of Safety Function Due to Past

Inoperabilities of HPCI System

This LER reported that, on two occasions the licensee failed to report the loss of a safety

function caused by operators disabling the HPCI system during scram recovery actions.

HPCI started automatically on a low reactor vessel level signal following reactor scrams

on May 26 and November 28, 2003. On both occasions, operators placed the HPCI

Enclosure

-24-

auxiliary oil pump in pull-to-lock to disable the system since HPCI injection was not

required or desired. This action was not covered by procedure and would have

prevented HPCI from automatically initiating if needed later in the scram recovery.

These two instances were not reported to the NRC in accordance with 10 CFR 50.72;

however, the inspectors reviewed each occurrence and concluded that violations had

occurred associated with inadequate procedures or failure to follow procedures. These

noncited violations were documented in NRC Integrated Inspection Reports

05000298/2003006 and 05000298/2004002. The licensee discovered their oversight in

reporting these occurrences while evaluating a third instance where operators disabled

HPCI due to a degraded condition in June 2004. The licensee reported the third

instance in LER 05000298/2004003-00. Although the failure to report the loss of a

safety function was a violation of 10 CFR 50.72, it constitutes a violation of minor

significance since the NRC would not have taken different action had the reports been

submitted. This minor violation is not subject to enforcement action in accordance with

Section IV of the Enforcement Policy. This LER is closed.

.2 Failure of a 4160 V General Electric Magne Blast Breaker

a. Inspection Scope

The inspectors conducted a followup inspection for the failure of a 4160 V General

Electric Magne Blast breaker to close on demand. The failure occurred on

December 29, 2004, when operators attempted to start SW Pump A remotely from the

control room. The followup inspection included a review of the licensees root cause

analysis and corrective actions as well as their extent of condition review.

b. Findings

Introduction. A self-revealing finding was identified regarding a safety-related 4160 V

breaker associated with SW Pump A that failed to close and latch on demand. This

finding is unresolved pending receipt of information necessary to assess the safety

significance of this issue.

Description. On December 29, 2004, control room operators attempted to start SW

Pump A from the control room. During the attempt, the circuit breaker closed and then

immediately tripped open. As a result, SW Pump A was declared inoperable in

accordance with TS 3.7.2.

The circuit breaker for SW Pump A is a 4160 V General Electric Magne Blast breaker.

Troubleshooting on the breaker by the licensee indicated that a critical clearance

between the prop pin and the breaker frame was inadequate. There was also evidence

that the prop pin had come in contact with the frame, which would have prevented the

breaker from latching in the closed position during operation. The breaker had been

overhauled in January 2000 and, during receipt inspection by the licensee, the prop pin

clearance was verified to be adequate. The licensee determined that, although the

clearance was adequate in 2000, insufficient spacers between the prop pin and frame

Enclosure

-25-

allowed the prop pin to travel along its shaft during breaker operation until it contacted

the frame.

In December 2000, Resolve Condition Report 2000-1165 documented a similar failure of

the breaker for SW Booster Pump B due to inadequate clearances between the prop pin

and frame. This breaker had recently been overhauled and the licensee was able to

verify that the prop pin clearance was adequate following overhaul, but the pin had

traveled along the shaft and become misaligned during successive breaker operations.

As a result, the licensees breaker engineer recommended the addition of washers

between the pin and frame to ensure that this critical clearance was maintained. In

addition, the population of safety-related breakers were inspected, including the breaker

for SW Pump A, to ensure that adequate clearance existed between the pin and frame;

however, the work request to perform this inspection did not require the verification or

addition of the spacers recommended by the breaker engineer. The breaker for SW

Pump A was verified to have adequate clearances during this inspection, but no spacers

were added to ensure the clearance was maintained.

Analysis. The inspectors concluded that this finding was more than minor because it

affected the Mitigating Systems cornerstone attribute of equipment reliability and

availability. Further inspection is required to determine the actual impact on the SW

systems capability to perform its safety function.

Enforcement. The finding remains unresolved pending receipt of additional information

needed to determine the actual impact on the SW systems capability to perform its

safety function: Unresolved Item (URI)05000298/2005002-07, SW Pump A 4160 V

Breaker Failure.

.3 Failure of EDG 1 due to Lube Oil Leak

a. Inspection Scope

The inspectors observed the licensees response to a lube oil instrument line failure on

EDG 1 during a monthly surveillance test which may have rendered the EDG inoperable.

In addition, the inspectors reviewed the licensees root cause and corrective actions for

this failure.

b. Findings

Introduction. A self-revealing finding was identified regarding a lube oil leak on EDG 1

which had the potential to render the EDG inoperable. This finding remains unresolved

pending further review to determine if the EDG would have been capable of performing

its safety function.

Description. On December 30, 2004, approximately 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> after starting EDG 1 for a

routine monthly surveillance test, control room operators received a diesel lube oil low

level alarm. An operator was dispatched to the diesel room where it was discovered that

Enclosure

-26-

a 1/4-inch instrument line for the engine-driven lube oil pump discharge pressure switch

had broken, resulting in an estimated 7 gallon-per-minute oil leak. It was also estimated

that 100 to 150 gallons of oil leaked from the lube oil system into the room. Operators

immediately secured EDG 1 and declared it inoperable. The instrument line was

repaired and the diesel was declared operable the following day.

The licensee determined that the instrument line failure was caused by high cycle fatigue

of the instrument line and its fittings. This line had been modified in 1989 to replace the

copper line with stainless steel. Vendor drawings for the EDG lube oil system specified

a 90° elbow at the engine-driven lube oil pump discharge pressure tap leading to the

pressure switch. The modification installed a straight fitting with an instrument root valve

which extended perpendicular to the discharge pipe for approximately 6 inches. This

configuration was susceptible to vibration induced, high-cycle fatigue. In their root cause

analysis, the licensee noted that this instrument line developed leaks on three other

occasions since the modification in 1989, but, during repairs, the system was never

returned to the vendors original design. The modified configuration eventually led to the

catastrophic failure of the instrument line fittings. The lube oil system for EDG 2 was

configured in accordance with the vendor drawings and was not susceptible to this

failure mechanism.

Analysis. The inspectors concluded that this finding was more than minor because it

affected the Mitigating Systems cornerstone attribute of equipment reliability and

availability. Further review of the EDG design and capabilities is required to determine

the actual impact on the EDGs capability to perform its safety function.

Enforcement. The finding remains unresolved pending receipt of additional information

needed to determine the actual impact on the EDGs capability to perform its safety

function: URI 05000298/2005002-08, EDG 1 Oil Leak.

.4 SW Discharge Strainer Clogging

a. Inspection Scope

The inspectors conducted a followup inspection for the SW discharge strainer clogging

event that occurred on November 20, 2004. This followup inspection included a review

of the licensees root cause analysis and corrective actions as well as their extent of

condition review.

b. Findings

Introduction. An unresolved item was identified regarding conditions adverse to quality

in the SW system intake, which resulted in both SW discharge strainers clogging.

Description. As discussed in Section 1R14, both SW discharge strainers became

clogged with silt after starting additional SW pumps on November 20, 2004. Both

strainers were cleaned and returned to service approximately 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> later.

Enclosure

-27-

Since initial plant operation in 1974, the licensee has experienced silt intrusion in the

intake structure. Based on a 1973 hydrology study of the Missouri River and the intake

structure, a guide wall was constructed in front of the intake structure in 1974 to reduce

sediment intrusion. The guide wall was designed to provide sediment reduction at a

nominal river level of 885 feet. However, river flows and levels over the past several

years have been significantly below normal, with the average river level having

decreased approximately 5 feet over the past 4 years. The hydrology study also

demonstrated that a relatively large increase in the suspended sediment entering the

SW bay occurs when river level decreases below 877 feet. River level averaged

between 875 and 876 feet during the 2 weeks prior to the event.

The licensee also noted that the SW strainers were the subject of numerous condition

reports over the past 3 years; however most were classified as trend only even though

they documented increased debris loading due lower than normal river levels.

Immediately prior to the strainer clogging event, a trend of several SW strainer high

differential pressure alarms was noted in the corrective action program and operators

logs, including a condition report identifying sand carrying over the SW bay traveling

screens. The licensees root cause team concluded that these were precursor events

that were not sufficiently addressed to prevent the SW strainer clogging event.

Immediate corrective actions for this condition included the installation of a differential

pressure monitoring system on the SW discharge strainers, increased frequency of

strainer cleaning from 3 months to 6 weeks, increased sparger rotation, and increased

SW pump rotation from weekly to daily. The licensee also accelerated their plans to

modify the guide wall and repair the SW sparging system to reduce the buildup of silt in

the SW intake bay.

Corrective actions for this condition were previously implemented or scheduled for

implementation with varying degrees of success. In 1988, the frequency of starting idle

SW pumps was increased due to silt buildup in the SW intake. In 2003, the river bottom

adjacent to the intake structure was dredged; however, this dredging removed the rip-

rap lining the river bottom, which resulted in an increased silting problem by allowing

river bottom silt to flow into the intake. The rip-rap was replaced in April 2004. Long-

term corrective actions included modification of the guide wall to restore its function at

lower river, an upgrade of the traveling screens with an improved design, and installation

of turning vanes along the river bed to divert the flow of silt away from the intake

structure. The remainder of these corrective actions were scheduled for completion in

October 2006.

Analysis: The inspectors concluded that the silt intrusion into the intake structure, which

resulted in both SW discharge strainers becoming clogged, was a significant condition

adverse to quality and was more than minor since it affected the Mitigating Systems

cornerstone attribute of equipment reliability and availability. Corrective actions were

implemented with varying degrees of success and longer-term corrective actions were

scheduled to be implemented, which would have reduced the likelihood of this event.

This item remains unresolved pending further review of the scope of the remaining

corrective actions to determine if the implementation schedule was reasonable and to

Enclosure

-28-

further evaluate the corrective action already implemented to determine if the licensee

took reasonable actions to prevent this event.

Enforcement: This finding is unresolved pending further review of the licensees

corrective actions: URI 05000298/2005002-09, Both SW Discharge Strainers Clogged

Due to Silt Intrusion.

4OA4 Crosscutting Aspects of Findings

Sections 1R14 and 1R15 describe findings with human performance aspects.

4OA5 Other Activities

(Closed) AV 05000298/2004014-01: Inadequate Instructions for Restoration of the SW

System Following Maintenance

NRC Inspection Report 05000298/2004014 documented an apparent violation

associated with inadequate instructions for restoration of the gland water supply to SW

Pumps B and D following maintenance. This finding had the potential to render the

pumps incapable of performing their safety function during a postulated accident and

was determined to have a preliminary safety significance of greater than very low safety

significance. In a letter to Nebraska Public Power District dated March 31, 2005, the

NRC transmitted its final conclusion regarding the safety significance of this event. The

letter stated that the finding is of very low safety significance (Green) and that this

apparent violation is being treated as a noncited violation, consistent with Section VI.A of

the Enforcement Policy (NCV 05000298/2005002-07: Inadequate Instructions for

Restoration of the Service Water System Following Maintenance). This apparent

violation is closed.

4OA6 Meetings, Including Exit

On January 28, 2005, the inspectors presented the inspection results regarding access

to radiologic significant areas and inservice inspection to R. Edington, Vice President,

and other members of his staff who acknowledged the findings.

On April 14, 2005, the inspectors presented the results of the resident inspector

activities to Mr. S. Minahan and other members of his staff who acknowledged the

findings.

The inspectors confirmed that proprietary information was not provided or examined

during the inspection.

40A7 Licensee-Identified Violations

Enclosure

-29-

The following violation of very low significance (Green) was identified by the licensee

and is a violation of NRC requirements which meet the criteria of Section VI of the

NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.

valves in the heating and ventilation system did not have position limit switches

and associated equipment that could support environmental qualification under

10 CFR 50.49 requirements. Based upon a new radiation analysis, it was

determined that these limit switches could be exposed to a more harsh

environment than previously considered. The licensee determined the switches

would need to be replaced to comply with 10 CFR 50.49 requirements. This NCV

was considered to have very low safety significance because the position limit

switches do not adversely affect the safety function of the valves.

sign or signs bearing the radiation symbol and the words "CAUTION, RADIATION

AREA. However, on December 11, 2004, a radiation protection technician found

an unposted area outside the RHR B heat exchanger room with general area dose

rates of 7 millirem per hour. This same dose rate had been previously identified on

November 29, 2004, but the radiation protection staff did not post the area as

required. Consequently, the radiation area outside the RHR B heat exchanger

room remained unposted for 11 days. Using the Occupational Radiation Safety

Significance Determination Process, the inspector determined that the finding was

of very low safety significance because it was not an ALARA finding, there was no

overexposure or substantial potential for an overexposure, and the ability to assess

dose was not compromised. The licensee documented this event in Condition

Report CR-CNS-2004-7624.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

J. Bednar, Emergency Preparedness Manager

C. Blair, Engineer, Licensing

D. Cook, Technical Assistant to General Manager

S. Minahan, General Manager of Plant Operations

T. Chard, Radiological Manager

K. Chambliss, Operations Manager

J. Christensen, General Manager of Support

J. Edom, Risk Management

R. Estrada, Corrective Actions Manager

J. Flaherty, Site Regulatory Liaison

P. Fleming, Licensing Manager

D. Knox, Maintenance Manager

W. Macecevic, Work Control Manager

J. Roberts, Director, Nuclear Safety Assurance

R. Shaw, Shift Manager

J. Sumpter, Senior Staff Engineer, Licensing

K. Tanner, Shift Supervisor, Radiation Protection

R. Hayden, Emergency Preparedness Staff

T. Chard, Manager, Radiation Protection

R. Edington, Vice President

S. Blake, Manager, Quality Assurance

K. Fili, Manager, Nuclear Projects

D. Kimbell, Outage Manager

G. Kline, Director, Engineering

NRC Personnel

L. Ricketson, Senior Health Physicist

S. Cochrum, Senior Resident Inspector

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000298/2005002-07 URI SW Pump A 4160 V Breaker Failure (4OA3..2)05000298/2005002-08 URI EDG 1 Oil Leak (4OA3.3)05000298/2005002-09 URI Both SW Discharge Strainers Clogged Due to Silt

Intrusion (4OA3.4)

A-1 Attachment

Opened and Closed

05000298/2005002-01 FIN Inadequate Maintenance Resulted in Failure of Reactor

Protection System Power Supply (1R12)05000298/2005002-02 NCV Failure to Implement Emergency Plan During a Fire (1R14)05000298/2005002-03 NCV Failure to Follow Operability Determination

Procedure (1R15)05000298/2005002-04 NCV Failure to Conspicuously Post and Barricade Two Areas in

the Drywell as Locked High Radiation Area in Accordance

with TS 5.7.2 (2OS1.1)05000298/2005002-05 NCV Failure to Perform an Adequate Survey to Evaluate

Radiological Hazards per 10 CFR 20.1501 (2OS1.2)05000298/2005002-06 NCV Failure to Gain Authorized Access to a High Radiation Area

in Accordance with TS 5.7.1 (2OS1.3)05000298/2005002-07 NCV Inadequate Instructions for Restoration of the SW System

Following Maintenance (4OA5)

Closed

05000298/2004004-00 LER Loss of Safety Function Due to Past Inoperabilities of HPCI

system (4OA3.1)05000298/2004014-01 AV Inadequate Instructions for Restoration of the SW System

Following Maintenance (4OA5)

LIST OF DOCUMENTS REVIEWED

Section 1R08: Inservice Inspection Activities

Procedures

3.28, Inservice Inspection and Testing Programs, Revision 20

3.28.1, Inservice Inspection Program Implementation, Revision 9

54-ISI-124-02, Ultrasonic Examination of Ferritic Piping Welds and Vessel Welds Two Inches

or Less in Thickness, Revision 2

54-ISI-130-41, Procedure for the Remote Ultrasonic Examination of BWR Core Shroud

Assembly Seam Welds, Revision 37

54-ISI-135-05, Linearity and Beam Spread Measurements, Revision 5

A-2 Attachment

54-ISI-173-03, ASME Section XI Examination Coverage, Revision 3

54-ISI-240-41, Visible, Solvent Removable Liquid Penetrant Examination, Revision 41

54-ISI-270-42, Wet or Dry Magnetic Particle Examination Procedure, Revision 42

54-ISI-805-06, Ultrasonic Examination of Reactor Vessel Welds, Revision 6

54-ISI-806-02, Manual Ultrasonic Through Wall and Length Sizing of Ultrasonic Indications in

Reactor Pressure Vessel Welds, Revision 2

54-ISI-829-02, Manual Ultrasonic Examination of Dissimilar Metal Piping Welds, Revision 2

54-ISI-833-02, Ultrasonic Examination of Reactor Equipment Cooling System Piping Welds at

Cooper Nuclear Station, Revision 2

54-ISI-835-08, Ultrasonic Examination of Ferritic Piping Welds, Revision 8

54-ISI-836-08, Ultrasonic Examination of Austenitic Piping Welds, Revision 8

54-ISI-837-06, Ultrasonic Through Wall Sizing of Piping Welds, Revision 6

54-ISI-850-04, Manual Ultrasonic Examination of BWR Reactor Vessel Nozzle Inner Radius

Regions and Nozzle to Shell Welds (Inner 15%), Revision 4

54-ISI-858-00, Automated Ultrasonic Examination of Core Shroud Assembly Welds,

Revision 0

QAP 9.1, Welding Procedure and Performance Qualification, Revision 10

QAP 9.2, Post Weld Heat Treat Procedure (Electric Resistance Heaters Only), Revision 2

QAP 9.3, Workmanship and Visual Inspection Criteria for ASME Welding, Revision 16

QAP 9.4, Pre-Heat Procedure (Electric Resistance Heaters Only), Revision 3

QAP 9.6, Liquid Penetrant Inspection Procedure, Revision 10

QAP 9.7, Magnetic Particle Inspection Procedure, Revision 7

20.A.100-1986, Radiographic Examination of Welds, General Requirements

20.A.131-1986, Radiographic Examination of Welds

Ultrasonic Examinations

CNSDP073-RF022 CNSDP065-RF022 CNSDP104-RF022

CNSDP061-RF022 CNSDP106-RF022 CNSDP097-RF022

A-3 Attachment

Condition Reports

CR-CNS-2004-00099 CR-CNS-2004-04375 CR-CNS-2004-06481

CR-CNS-2004-00276 CR-CNS-2004-05024 CR-CNS-2004-06529

CR-CNS-2004-01360 CR-CNS-2004-05116 CR-CNS-2004-06628

CR-CNS-2004-01457 CR-CNS-2004-06304 CR-CNS-2004-07100

CR-CNS-2004-03441 CR-CNS-2004-06431 CR-CNS-2005-01191

CR-CNS-2004-03643 CR-CNS-2004-06432

Section 2OS1: Access Control To Radiologically Significant Areas (IP71121.01)

Procedures

9.ALARA.4 Radiation Work Permits, Revision5

9.RADOP.1 Radiation Protection at CNS, Revision 4

9.RADOP.2 Radiation Safety Standards and Limits, Revision 6

9.RADOP.3 Area Posting and Access Control, Revision 15

Radiation and Special Work Permits

2005-0001

2005-0008

2005-0009

2005-1039

2005-1056

2005-1099

Condition Reports

2004-06792 2004-07416 2004-07624 2004-07783 2005-00042 2005-00062 2005-00077

2005-00194 2005-00380 2005-00398 2005-00418 2005-00427 2005-00600 2005-00624

2005-00786

Self-Assessments/Audits

Radiological Protection Depart On-Going Self-Assessment Report 3Q2004

Miscellaneous

2003 Annual Radioactive Effluent Report

A-4 Attachment

LIST OF ACRONYMS

ALARA as low as is reasonably achievable

ASME American Society of Mechanical Engineers

CFR Code of Federal Regulations

EDG emergency diesel generator

FIN finding

HPCI high pressure coolant injection

LER licensee event report

MG motor generator

MPF multipurpose facility

NCV noncited violation

NDE nondestructive examination

NRC U.S. Nuclear Regulatory Commission

RCIC reactor core isolation cooling

RHR residual heat removal

RPS reactor protection system

SW service water

TB to be determined

TS Technical Specification

URI unresolved item

A-5 Attachment