ML032110555
ML032110555 | |
Person / Time | |
---|---|
Site: | Indian Point ![]() |
Issue date: | 07/30/2003 |
From: | Eselgroth P, Brian Holian Division Reactor Projects I |
To: | Dacimo F Entergy Nuclear Northeast |
References | |
FOIA/PA-2003-0379, FOIA/PA-2003-0388 IR-03-007 | |
Download: ML032110555 (35) | |
See also: IR 05000247/2003007
Text
July 30, 2003
Mr. Fred Dacimo
Site Vice President
Entergy Nuclear Northeast
Indian Point Nuclear Generating Station
295 Broadway, Suite 1
Post Office Box 249
Buchanan, NY 10511-0249
SUBJECT: INDIAN POINT 2 - NRC INTEGRATED INSPECTION REPORT
050000247/2003007
Dear Mr. Dacimo:
On June 28, 2003, the US Nuclear Regulatory Commission (NRC) completed an inspection at
the Indian Point 2 Nuclear Power Plant. The enclosed integrated inspection report documents
the inspection findings, which were discussed on July 9, 2003, with yourself and other members
of your staff.
The inspection examined activities conducted under your license as they relate to safety and
compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed
personnel.
Based on the results of this inspection, the inspectors identified two findings of very low safety
significance (Green) which did not present an immediate safety concern. One of the findings
was determined to be a violation of NRC requirements. However, because it was of very low
safety significance and because the issue has been addressed and entered into your corrective
action program, the NRC is treating this issue as a non-cited violation, in accordance with
Section VI.A.1 of the NRCs Enforcement Policy. If you deny this non-cited violation, you should
provide a response with the basis for your denial, within 30 days of the receipt of this letter, to
the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555-
001; with copies to the Regional Administrator, Region 1; the Director, Office of Enforcement;
and the NRC Resident Inspector at the Indian Point 2 facility.
Since the terrorist attacks on September 11, 2001, NRC has issued five Orders and several
threat advisories to licensees of commercial power reactors to strengthen licensee capabilities,
improve security force readiness, and enhance controls over access authorization. In addition to
applicable baseline inspections, the NRC issued Temporary Instruction 2515/148, "Inspection of
Nuclear Reactor Safeguards Interim Compensatory Measures," and its subsequent revision, to
audit and inspect licensee implementation of the interim compensatory measures required by
order. Phase 1 of TI 2515/148 was completed at all commercial power nuclear power plants
during calender year '02 and the remaining inspection activities for Indian Point 2 were
completed in January 2003. The NRC will continue to monitor overall safeguards and security
controls at Indian Point 2.
Mr. Fred Dacimo 2
In accordance with 10 CFR 2.790 of the NRCs "Rules of Practice," a copy of this letter and its
enclosure will be available electronically for public inspection in the NRC Public Document Room
or from the Publicly Available Records (PARS) component of the NRCs document system
(ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-
rm/adams.html (the Public Electronic Reading Room). Should you have any questions
regarding this report, please contact Mr. Peter Eselgroth at 610-337-5234.
Sincerely,
/RA/ by
Peter W. Eselgroth
Acting For/
Brian E. Holian, Deputy Director
Division of Reactor Projects
Docket No.50-247
License No. DPR-26
Enclosure: Inspection Report 05000247/2003007
w/Attachment: Supplemental Information
cc w/encl: G. J. Taylor, Chief Executive Officer, Entergy Operations
M. R. Kansler, President - Entergy Nuclear Operations, Inc.
J. Herron, Senior Vice President and Chief Operating Officer
C. Schwarz, General Manager - Plant Operations
D. Pace, Vice President, Engineering
R. Edington, Vice President, Operations Support
J. McCann, Manager, Nuclear Safety and Licensing
J. Kelly, Director, Nuclear Safety Assurance
J. Comiotes, Director, Nuclear Safety Assurance
C. Faison, Manager, Licensing
H. Salmon, Jr., Director of Oversight
J. Fulton, Assistant General Counsel, Entergy Nuclear Operations, Inc.
P. Smith, Acting President, New York State Energy, Research
and Development Authority
J. Spath, Program Director, New York State Energy Research
and Development Authority
P. Eddy, Electric Division, New York State Department of Public Service
C. Donaldson, Esquire, Assistant Attorney General, New York Department
of Law
T. Walsh, Secretary, NFSC, Entergy Nuclear Operations, Inc.
D. ONeill, Mayor, Village of Buchanan
J. G. Testa, Mayor, City of Peekskill
R. Albanese, Executive Chair, Four County Nuclear Safety Committee
S. Lousteau, Treasury Department, Entergy Services, Inc.
Chairman, Standing Committee on Energy, NYS Assembly
Chairman, Standing Committee on Environmental Conservation, NYS Assembly
Mr. Fred Dacimo 3
Chairman, Committee on Corporations, Authorities, and Commissions
M. Slobodien, Director, Emergency Planning
B. Brandenburg, Assistant General Counsel
P. Rubin, Operations Manager
Assemblywoman Sandra Galef, NYS Assembly
C. Terry, Niagara Mohawk Power Corporation
County Clerk, Westchester County Legislature
A. Spano, Westchester County Executive
R. Bondi, Putnam County Executive
C. Vanderhoef, Rockland County Executive
E. A. Diana, Orange County Executive
T. Judson, Central NY Citizens Awareness Network
M. Elie, Citizens Awareness Network
D. Lochbaum, Nuclear Safety Engineer, Union of Concerned Scientists
Public Citizens Critical Mass Energy Project
M. Mariotte, Nuclear Information & Resources Service
F. Zalcman, Pace Law School, Energy Project
L. Puglisi, Supervisor, Town of Cortlandt
Congresswoman Sue W. Kelly
Congresswoman Nita Lowey
Senator Hillary Rodham Clinton
Senator Charles Schumer
J. Riccio, Greenpeace
A. Matthiessen, Executive Director, Riverkeepers, Inc.
M. Kapolwitz, Chairman of County Environment & Health Committee
A. Reynolds, Environmental Advocates
M. Jacobs, Director, Longview School
D. Katz, Executive Director, Citizens Awareness Network
P. Gunter, Nuclear Information & Resource Service
P. Leventhal, The Nuclear Control Institute
K. Copeland, Pace Environmental Litigation Clinic
R. Witherspoon, The Journal News
W. DiProfio, PWR SRC Consultant
W. Russell, PWR SRC Consultant
W. Little, Associate Attorney, NYSDEC
Mr. Fred Dacimo 4
Distribution w/encl: H. Miller, RA/J. Wiggins, DRA (1)
H. Nieh, RI EDO Coordinator
P. Habighorst, SRI - Indian Point 2
P. Eselgroth, DRP
R. Laufer, NRR
W. Cook, DRP
R. Martin, DRP
Region I Docket Room (w/concurrences)
DOCUMENT NAME: C:\ORPCheckout\FileNET\ML032110555.wpd
After declaring this document An Official Agency Record it will be released to the Public. To
receive a copy of this document, indicate in the box: "C" = Copy without
attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy
OFFICE RI/DRP RI/DRP E RI/DRP E
NAME Phabighorst/wac for PEselgroth/wac BHolian/pwe for
for
DATE 07/09/03 07/30 /03 07/30/03
OFFICIAL RECORD COPY
U.S. NUCLEAR REGULATORY COMMISSION
REGION I
Docket No. 50-247
License No. DPR-26
Report No. 05000247/2003007
Licensee: Entergy Nuclear Operations, Inc.
Facility: Indian Point 2 Nuclear Power Plant
Location: Buchanan, New York 10511
Dates: March 30, 2003 - June 28, 2003
Inspectors: Peter Habighorst, Senior Resident Inspector
Lois James, Resident Inspector
Mark Cox, Resident Inspector, IP3
Monica Salter-Williams, Reactor Engineer
Peter Wen, NRR/DRIP/RGEB Inspector
William Cook, Senior Project Engineer
John McFadden, Health Physicist
Greg Smith, Senior Physical Security Inspector
David Silk, Senior Emergency Preparedness Inspector
Approved by: Peter W. Eselgroth, Chief
Projects Branch 2
Division of Reactor Projects
i Enclosure
TABLE OF CONTENTS
TABLE OF CONTENTS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ii
SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . iii
Report Details . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
Summary of Plant Status . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
1. REACTOR SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
1R01 Adverse Weather Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
1R02 Evaluation of Changes, Tests, or Experiments . . . . . . . . . . . . . . . . . . . . . . . . . 2
1R04 Equipment Alignment . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2
1R05 Fire Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3
1R07 Heat Sink Performance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5
1R11 Operator Requalification Inspection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5
1R12 Maintenance Effectiveness . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6
1R13 Maintenance Risk Assessment and Emergent Work Activities . . . . . . . . . . . . . . 7
1R14 Personnel Performance During Non-Routine Plant Evolutions and Events . . . . 8
1R15 Operability Evaluations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9
1R16 Operator Workarounds . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 11
1R19 Post Maintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 11
1R22 Surveillance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12
1EP4 Emergency Action Level and Emergency Plan Changes . . . . . . . . . . . . . . . . . 13
2. RADIATION SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 13
2OS1 Access Control to Radiologically Significant Areas . . . . . . . . . . . . . . . . . . . . . 13
2OS2 ALARA Planning and Controls . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 14
2OS3 Radiation Monitoring Instrumentation and Protective Equipment . . . . . . . . . . . 15
3. SAFEGUARDS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16
3PP4 Security Plan Changes . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16
4. OTHER ACTIVITIES (OA) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17
4OA1 Performance Indicator Verification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17
4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . 18
4OA6 Meetings, Including Exit . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20
ATTACHMENT: SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED . . . . . . . . . . . . . . . . . . . . . . . . . . . A-2
LIST OF CONDITION REPORTS GENERATED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-3
LIST OF DOCUMENTS REVIEWED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-4
LIST OF BASELINE INSPECTIONS PERFORMED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-7
LIST OF ACRONYMS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-7
ii Enclosure
SUMMARY OF FINDINGS
IR 05000247-03-07, on March 30, 2003 - June 28, 2003, Entergy Nuclear Operations, Inc.;
Indian Point 2 Nuclear Power Plant; Operability Evaluations; and Problem Identification and
Resolution Samples.
The report covered a twelve-week period of inspection by resident and announced region-based
and headquarters-based inspectors. Two Green findings, of which one was a non-cited violation
(NCV), were identified. The significance of the findings are indicated by their color (Green,
White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination
Process (SDP). The NRCs program for overseeing the safe operation of commercial nuclear
power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated
July 2000.
A. NRC- Identified and Self-Revealing Findings
Cornerstone: Mitigating Systems
Green. The inspector identified that the licensees operability evaluation during a 13.8 KV
system reduced voltage test was not complete. The operability evaluation did not
evaluate accident load carrying capability and it did not address communication protocols
between the distribution company (Con Edison) and Entergy to restore from the test in a
timely manner.
The finding is more than minor because it impacts the attribute of the mitigating system
cornerstone objective. Specifically, the cornerstone objective is to ensure that the 13.8
KV system is capable of performing its safety function during a postulated loss of normal
power event without undesirable consequences. This finding was determined to be of
low safety significance because there was no actual loss of either the 138 KV or 13.8 KV
offsite power supplies during the short duration of the degraded voltage condition on the
13.8 KV feed. (Section 1R15)
Green. The inspector identified a violation of 10 CFR 50, Appendix B, Criterion XVI.
Entergy did not evaluate and take effective corrective actions associated with a material
substitution for the No. 22 component cooling water (CCW) pump inboard bearing oil
level indication system. The substitute bearing oil level indication system contributed to
the failure of the No. 22 CCW pump on December 5, 2002.
This finding is greater than minor since it is associated with the design control attribute of
the mitigating systems cornerstone and affected the cornerstone objective. The
inspectors conducted a Phase 1 SDP screening and determined that the failure to take
effective corrective action on No. 22 CCW pump was of a very low safety significance
since the redundant train components were operable and unaffected by this inadequate
modification. Accordingly, this issue was treated as a Non-cited Violation. (4OA2)
B. License-Identified Violations
None
iii Enclosure
Report Details
Summary of Plant Status
Indian Point Unit 2 began the period at full Rated Thermal Power (RTP) and operated at full
power until April 28, 2003. On April 28, the unit experienced a main turbine trip on over-
frequency and a reactor trip due to a generator load reject as a result of electrical faults on the
off site 345 KV and 138 KV distribution systems (reference report detail 1R14). On May 1, 2003,
the unit was restored back to RTP. On May 24, 2003, following issuance of the Technical
Specification amendment, RTP was increased from 3,071.4 to 3114.4 thermal megawatts. The
unit operated at RTP throughout the remainder of the inspection period.
1. REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity and Emergency
Planning
1R01 Adverse Weather Protection
a. Inspection Scope (71111.01)
The inspector reviewed hot weather preparations by the licensee. The inspector selected
licensee controls in the following plant areas: central control room, auxiliary boiler
feedwater pump, intake structure, and the 480 volt switchgear room. Documents
reviewed by the inspector are listed below:
- SOP 11.1, Ventilation System Operation
- ARP SCF Window 4-4, 22 ABFP Inlet Valves 1310A/1310B Not Fully Open
- ARP SJF, Window 4-1, 480 Volt Switchgear Temperature Hi
- OASL 15.90, Inclement Weather Conditions
- AOI 11.1, Failure of CCR Air Conditioners/Fan Systems
- OAD 22, Seasonal Weather Preparation
- OAD 44, Summer Reliability
- Reactor Protection System and Auxiliary feedwater System Design Basis
Documents
- List of Unit 2 control room deficiencies
- Updated Final Safety Analysis Report Sections 7.2.4.2 and 9.3.3
- Individual Plant Examination of External Events (IPEEE) Table 6.5-1
The inspector walked down selected plant areas to verify availability of ventilation and air
conditioning units, availability of back-up mitigation equipment as defined in AOI 11.1,
and material condition of various temperature sensors and recorders.
b. Findings
No findings of significance were identified.
1R02 Evaluation of Changes, Tests, or Experiments
Enclosure
2
a. Inspection Scope (71111.02)
The inspector reviewed the 10 CFR 50.59 evaluation associated with the increase in TAVG
from 559 0F to 562 0F to verify that this change to the facility and associated procedures,
as described in the Updated Final Safety Analysis Report (UFSAR), was reviewed and
documented in accordance with 10 CFR 50.59 and that the safety issues pertinent to the
change were properly resolved or adequately addressed. This evaluation was selected
based on the safety significance of the changes and the risk to structures, systems, and
components.
The inspector reviewed the licensees evaluation package, 02-0344-PR-02-RE, and
interviewed engineering personnel cognizant of the associated 10 CFR 50.59 evaluation.
The evaluation concluded that the increase to the operating TAVG from 559 0F to 562 0F at
Indian Point Unit 2 does not adversely affect the safe operation of the plant and did not
require a change to the plant Technical Specifications. The inspector observed the
control room activities associated with raising TAVG on April 25, 2002. The inspector
noted that the licensee conducted this evolution in a thorough and deliberate manner.
During the review of associated operating procedures impacted by the TAVG increase, the
inspector questioned two conversion factors (one for the pressurizer level change and
the other for the reactor coolant system mass change) used in the licensees reactor
coolant system leakage surveillance procedure (SOP 1.7, Revision 35). As a result, the
licensee generated a condition report IP2-2003-02567) to provide values that more
accurately reflect the current plant conditions for the reactor water inventory calculation.
b. Findings
No findings of significance were identified.
1R04 Equipment Alignment
a. Inspection Scope (71111.04)
On April 18, 2003, the inspector performed a partial system walkdown of the 21 boric
acid transfer pump (BATP) while the 22 BATP was out of service for preventive
maintenance. The purpose of this walkdown was to verify equipment alignment and
identify any discrepancies that could impact the function of emergency boration, thereby
potentially increasing risk. The inspector observed the physical condition of the system
pump and valves and reviewed the operations logs. The inspector used check-off list
(COL) 3.1, Chemical and Volume Control System, for this walkdown and reviewed the
design basis document for the boric acid transfer system to verify the valve positions, as
defined in the COL, were appropriate.
On May 12, 2003, the inspector performed a partial system walkdown of the 21 and 22
safety injection trains while the 23 safety injection pump was being surveillance tested
pursuant to PT-Q29C, 23 Safety Injection Pump. The purpose of this walkdown was to
verify equipment alignment and identify any discrepancies that could adversely impact
the reactor coolant system injection and heat removal functions and thereby potentially
Enclosure
3
increase risk. The inspector observed the physical condition of the subsystems and
reviewed the operations logs. The inspector used COL 10.1.1, Safety Injection System,
and COL 10.1.1.1, Backseated Safety Injection Recirculation Valves, for this walkdown
and reviewed the plant drawings 9321-F-2738, 9321-F-2735-131, and A235296-59 to
verify valve positions, as defined in the COLs, were appropriate. The inspector identified
minor housekeeping and valve and pump seal leakages that were documented in
Condition Report (CR) Nos. IP2-2003-2876, -2877, and -2878 by the licensee.
The inspector performed a partial system walkdown of the 21 emergency diesel
generator (EDG) to evaluate the operability of the starting air system while the 23 EDG
was removed from service for preplanned maintenance. The inspector checked for
correct valve and power alignments by comparing positions of valves, switches, and
electrical power breakers to COL 27.3.1, Diesel Generators, as well as applicable
chapters of the Final Safety Analysis Report (FSAR) to verify proper system alignment.
The inspector also verified starting air system pressure, component labeling, and the
condition of hangers and support installations.
Air compressor operation during the walkdown was observed to ensure that system
vibration and pump leakage was not excessive, and that system operating pressure met
operational and design specifications.
b. Findings
No findings of significance were identified. During the safety injection sub-system
walkdown, the inspector identified an operator work-around involving the 21 safety
injection motor-operated valve (856A) not previously entered into the licensees work-
around system. This minor observation is also discussed in report section 1R16.
1R05 Fire Protection
.1 Fire Protection Tours
a. Inspection Scope (71111.05)
The inspector toured the areas important to plant safety and risk based upon a review of
Section 4.0, Internal Fires Analysis, and Table 4.6-2, Summary of Core Damage
Frequency Contributions from Fire Zones, in the Indian Point 2 Individual Plant
Examination for External Events (IPEEE). The objective of this inspection was to
determine if the licensee had adequately controlled combustibles and ignition sources
within the plant, effectively maintained fire detection and suppression capability, and had
adequately established compensatory measures for degraded fire protection equipment.
The inspector evaluated conditions related to: 1) licensee control of transient
combustibles and ignition sources; 2) the material condition, operational status, and
operational lineup of fire protection systems, equipment and features; and 3) the fire
barriers used to prevent fire damage or fire propagation. The areas reviewed were:
- Fire Zone 1, Component Cooling Water Pump Room
- Fire Zone 90A/91A, Spent Fuel Pool Building
Enclosure
4
- Fire Zone 25, 23 Station Battery
- Fire Zone 11, Cable Spreading Room
- Fire Zone 650, Gas Turbine 1 Room
- Fire Zone 17, Turbine Oil Reservoir Area
- Fire Zone 47A, 12' and 15' Turbine Building
- Fire Zone 48A, 3.3' and 15' Turbine Building
Reference material consulted by the inspector included the Fire Protection
Implementation Plan, Pre-Fire Plan, and Station Administrative Orders (SAOs)-700, Fire
Protection and Prevention Policy, SAO-701, Control of Combustibles and Transient Fire
Load, SAO-703, Fire Protection Impairment Criteria and Surveillance, and Calculation
PGI-00433, Combustible Loading Calculation. The inspector identified a number of
minor items related to drawing errors in the pre-fire plan sketch and penetration drawings
and a few minor housekeeping items. The associated condition reports for these minor
issues are identified in the Attachment to this inspection report.
b. Findings
No findings of significance were identified.
.2 Fire Brigade Observation
a. Inspection Scope (71111.05)
On June 13, 2003, the inspectors observed an announced fire brigade drill. The drill was
in accordance with the pre-planned drill scenario for a 21 auxiliary boiler feedwater pump
motor fire. This was a routine training drill for current fire brigade members. The purpose
of this observation was to evaluate the readiness of the licensee's personnel to prevent
and fight fires. The inspector evaluated the following aspects:
- Protective clothing/turnout gear is properly donned.
- Self-contained breathing apparatus (SCBA) equipment is properly worn and used.
- Fire hose lines are capable of reaching all necessary fire hazard locations, are
laid out without flow constrictions, and are simulated being charged with water.
- Fire area is entered in a controlled manner.
- Sufficient fire fighting equipment is brought to the scene by the fire brigade.
- Effective smoke removal operations are simulated.
- The fire fighting pre-plan strategies are utilized.
- The licensees pre-planned drill scenario is followed.
- The drill objectives and acceptance criteria are met.
The inspector reviewed Station Administrative Order (SAO) -706, Fire Brigade
Organization, Operation, and Training, and procedure OASL 15.22, Fire Brigade
Requirements, to confirm the minimum fire brigade manning during the drill was
achieved.
Some minor deficiencies, not impacting the ability of the fire brigade to fight a fire, were
addressed during the drill critique and were entered into the Condition Reporting System
Enclosure
5
(CR-IP2-2003-03778, CR-IP2-2003-03780, CR-IP2-2003-03786, and CR-IP2-2003-
03791).
b. Findings
No findings of significance were identified.
1R07 Heat Sink Performance
a. Inspection Scope (71111.07)
The inspector verified that the licensees program was adequate to ensure proper heat
exchanger performance for the Nos. 21 and 22 component cooling water (CCW) heat
exchangers. The inspection consisted of a review of the most recently completed
performance tests, (PT-2Y10A, 21 CCW HX Test, and PT-2Y10B, CCW HX Test,
conducted on October 7, 2002 and October 11, 2002, respectively), examination of the
preliminary engineering calculation No. PGI-00462-01, Component Cooling Water Heat
Exchanger Performance Evaluation, and discussions with the responsible performance
engineer. The inspector noted that these performance tests were conducted just prior to
the Cycle 15 refueling outage in the Fall of 2002, during which both heat exchangers
were opened for a planned clearing and inspection. The inspector also reviewed
completed performance test results for both CCW heat exchangers dating back to July
1991.
b. Findings
No findings of significance were identified.
1R11 Operator Requalification Inspection
a. Inspection Scope (71111.11)
On May 4, 2003, the inspector observed the performance of an operating crew (2C)
during licensed operator re-qualification training. Specifically, the inspector observed a
simulator exam associated with lesson plan ESR-024-007. The inspection was
conducted to assess the adequacy of the training, licensed operator performance,
emergency plan implementation, and the adequacy of the licensees critique.
b. Findings
No findings of significance were identified.
1R12 Maintenance Effectiveness
.1 22 EDG Load Test
a. Inspection Scope (71111.12Q)
Enclosure
6
The inspector evaluated Entergys corrective actions for the emergency diesel generator
(EDG) system equipment issues identified during the EDG 22 load test (PT-M21B)
performed on April 23, 2003, to assess the effectiveness of the licensees maintenance
rule implementation. The inspector reviewed the EDG system performance history and
assessed the licensees maintenance rule determination for the equipment issue
involving the two loose fuel line capscrews found during the test (CR IP2-2003-02392).
The inspector reviewed Entergys problem identification and resolution actions for this
issue and evaluated Entergys monitoring, analysis, and disposition of the issues in
accordance with station procedures and 10 CFR 50.65, "Requirements for Monitoring the
Effectiveness of Maintenance." The inspector noted that after correcting the EDG 22
problem, the licensee also checked the same parts in EDG 21 and EDG 23; the problem
observed in EDG 22 was not found in the other two EDGs.
b. Findings
No findings of significance were identified.
.2 Auxiliary Feedwater System
a. Inspection Scope (71111.12Q)
The inspectors evaluated Entergys work practices and preventive maintenance activities
for the auxiliary feedwater system to assess the effectiveness of maintenance activities.
The inspectors reviewed the performance history of the auxiliary feedwater pumps to
assess the adequacy of the licensee's corrective actions and to evaluate Entergys
monitoring, evaluations, and dispositions of issues completed in accordance with station
procedures and the requirements of 10 CFR 50.65, "Requirements for Monitoring the
Effectiveness of Maintenance." The inspectors reviewed the following documents
associated with the system design and licensing basis:
Enclosure
7
Procedures and Documents
- Maintenance Rule Basis Document for the Auxiliary Feedwater System
- Design Bases Document for the Auxiliary Feedwater System
- UFSAR Chapter 10, Steam and Power Conversion System
- System Health Report, Auxiliary Feedwater System, 4th Quarter 2002 and 1st
Quarter 2003
- Condition Reports CR-IP2-2003-03244; CR-IP2-2002-09642; CR-IP2-2002-
10943; and CR-IP2-2003-00165
- Work Order Nos. IP2-00-15677; IP2-97-96621; IP2-02-02856; and IP2-02-03503
b. Findings
No findings of significance were identified.
1R13 Maintenance Risk Assessment and Emergent Work Activities
a. Inspection Scope (71111.13)
The inspector observed selected portions of emergent maintenance work activities to
assess the licensees risk management in accordance with 10 CFR 50.65 (a)(4). The
inspector verified that the licensee took the necessary steps to plan and control emergent
work activities, to minimize the probability of initiating events, and to maintain the
functional capability of mitigating systems. The inspector observed and/or discussed risk
management with maintenance and operations personnel for the following activities:
- Work Order (WO) IP2-03-14398, perform bearing clearance check on EDG 22
- WO IP2-02-38919, EDG 22 Starting Air System
- WO IP2-03-05130, troubleshooting power range upper channel high flux deviation
- WO IP2-03-13972, replace and rescale main turbine steam dump controller
circuits in anticipation of NRC approval of a reactor thermal power uprate
amendment request
- WO IP2-03-06817, repairs to 22 component cooling water pump discharge check
valve (761B)
- WO IP2-03-18744, Loop 22 setpoint change for reactor coolant system low flow
reactor protection system bistable setpoints
b. Findings
No findings of significance were identified.
Enclosure
8
1R14 Personnel Performance During Non-Routine Plant Evolutions and Events
.1 Partial Loss of Power Reactor Trip/Turbine Trip
Introduction. On April 28, 2003, offsite electrical disturbances caused a reactor trip and
partial loss of normal power. At 4:41 p.m. a phase A ground fault on 345 KV
transmission line No. Y94 occurred. During the automatic isolation of the Y94 fault, a
138 KV breaker (No. F7) in the Buchanan substation faulted to ground. These two faults
and the response of protective relaying at the Millwood substation, resulted in a loss of
the credited 138 KV power supplies to both Units 2 and 3 for approximately five minutes.
During this period of time, the IP2 main generator was supplying portions of the 345 KV
system through one of its two output breakers. After repeated unsuccessful attempts to
restore the No. Y94 line by the transmission network operator, the remaining 345 KV
output transmission lines for the IP2 generator were lost. This resulted in a full load
reject and trip of the main turbine on over-frequency.
The resultant turbine/reactor trip placed the plant in natural circulation with all three
emergency diesel generators started and two of the four 480 volt safeguards buses
energized by the No. 22 EDG. The event was documented in the licensees corrective
action program via condition report IP2-CR-2003-2511.
This event was similar, with respect to the in-plant consequences, to events on
December 26, 2001 (inspection report 50-247/2001-011) and July 28, 1997 (inspection
report 50-247/97-010).
a. Inspection Scope (71111.14)
The inspector observed operator response to the event, including their use of emergency
operating procedures. The inspector compared the plant response to Updated Final
Safety Analysis Report (UFSAR) section 14.1.13, Turbine Overspeed, UFSAR Section
14.1.8, Loss of Load, and UFSAR Section 14.1.12, Loss of Station Auxiliaries. The
inspector also reviewed licensee corrective actions to prevent recurrence of this event.
The inspector reviewed the transient and compared it to NRC safety evaluation report
dated 1982. The safety evaluation report concluded that no event or condition could
result in the simultaneous or consequential loss of both required circuits from the offsite
power network to the onsite distribution system. The inspector observed the post-trip
review presented to the on-site review committee on April 29, 2003. The inspector
reviewed the post-trip review report as defined in operations administrative directive
(OAD) 23, Post Trip Review and Evaluation Procedure. The inspector also evaluated
equipment issues not associated with the offsite power perturbation.
b. Findings
No findings of significance were identified.
Enclosure
9
.2 Unavailability of Emergency Planning Zone Sirens
a. Inspection Scope
The inspectors evaluated the licensees problem identification and evaluations associated
with a number of emergency planning siren failures, as reported per 10 CFR 50.72
between February 2003, and June 17, 2003. The inspector observed the on-line
monitoring of siren performance at the emergency operations facility, reviewed the
licensees assessment of overall system availability, and discussed proposed corrective
actions with cognizant licensee personnel.
The inspector consulted NRC Manual Chapter 0609, Appendix B for examples of a loss
and/or degraded risk significant planning standard 10 CFR 50.47(b)(5), associated with
the public alert and notification system (ANS). The NRC staff had previously
documented a review of ANS siren failures in report 50-247/2003-003, detail 4OA2.
b. Findings
No findings of significance were identified.
1R15 Operability Evaluations
a. Inspection Scope (71111.15)
The inspectors reviewed the below listed condition reports and associated operability
evaluations to ensure that operability was properly justified and that the component or
system remained available, without a significant degradation in performance or
unrecognized operability issue. The inspectors used Technical Specifications, Updated
Final Safety Analysis Report, and design basis documents, as appropriate.
- CR-IP2-2003-03548, GT-1 Main Battery Reduced Voltage
- CR-IP2-2003-01718 - Failure of Valve 883, RHR Pump Return Line to RWST
Stop.
- CR-IP2-2003-02805 - EDG Building Intake Louvers As-Found Settings
- CR-IP2-2003-03470 - 13.8 KV System Degraded Voltage Testing by System
Operator
- CR-IP2-2003-4051 - Water in the 21 and 22 Emergency Diesel Generator Fuel
Oil Storage Tanks
- CR-IP2-2003-2342, 18-inch snubber (BFD-6-3) on Main Feedwater Line Leaking
Oil
Enclosure
10
b. Findings
Introduction. The inspector identified an incomplete operability evaluation. The
operability evaluation involved the 13.8 KV electrical system during a planned voltage
reduction test.
Description. At 12:55 a.m. on May 28, 2003, the Unit 2 control room was notified by the
Con Edison system operator that a voltage reduction test of 8% would be performed on
the 13.8 KV feeders in the Buchanan Substation. The Con Edison system operator
subsequently notified the control room that the test was completed at 2:24 a.m. The
inspector determined that Entergy received no prior notification of the test and that there
was no evaluation performed by Entergy to determine the impact of the test on 13.8 KV
offsite power operability. Further, Operations Department personnel did not question the
impact of the voltage test on operability of the 13.8 KV system. Based upon the
inspectors expressed concern that an operability evaluation had not been performed in
response to the planned reduced voltage test of the 13.8 KV system, Entergy initiated CR
IP2-2003-3470 to address operability of the system and to evaluate the needed protocols
between Con Edison and Entergy for the coordination of offsite electrical power system
testing.
The licensees operability evaluation determined that if a safety injection and a loss of
offsite power (138 KV system) occurred, the emergency diesel generators would
automatically start and operators would manually place the generators on the safeguards
buses. The operability evaluation also documented that operators would manually tie the
13.8 KV source to safeguard buses. The inspector identified that the operability
evaluation did not evaluate if the reduced voltage condition could support in-plant
accident loads, as defined in the Technical Specification bases. Further, the operability
evaluation did not address communication protocols between the distribution company
and Entergy in the event there is a need to restore the 13.8 KV system during a
postulated loss of normal power (138 KV). Abnormal operating instruction AOI-27.1.1,
Loss of Normal Power, does not tie the 13.8 KV system to the safeguards buses unless
it is predicted that the preferred 138 KV system will not be available for greater than 30
minutes. Notwithstanding, the licensee concluded that there was reasonable assurance
of system operability during the short duration degraded voltage test.
Analysis. The inspectors concluded that the licensees operability evaluation was
incomplete based on the absence of an evaluation of in-plant accident electrical loads
that would be supplied by the 13.8 kV power feed and the absence of established
communication protocols between Entergy and Con Edison for the control of degraded
system voltage testing. The inspectors referenced NRC Generic Letter (GL) 91-18,
Information to Licensees Regarding Two NRC Manual Sections on Resolution of
Degraded and Non-Conforming Conditions and on Operability, in support of their
conclusion. GL 91-18 states, in part, that when a systems capability is degraded to a
point where it cannot perform with reasonable assurance of reliability, the system should
be judged inoperable. Entergy did not document sufficient basis for their operability
evaluation or provide appropriate guidance to plant operators and the distribution
operator in the event of a condition which warranted use of the 13.8 KV electrical power
feed.
Enclosure
11
The inspectors used NRC Manual Chapter 0612, Appendix B, to disposition this issue.
The finding was more than minor because it impacted the attribute of the mitigating
system cornerstone objective. Specifically, the cornerstone objective is to ensure that
the 13.8 KV system is capable of performing its safety function during a postulated loss
of normal power event without undesirable consequences. This finding was determined
to be of low safety significance because the degraded conditions was of a short duration
and there was no actual loss of the normal offsite power supplies (138 KV or 13.8 KV)
during the test. (FIN 50-247/2003-007-01)
Enforcement. The incomplete operability evaluation does not represent a violation of
regulatory requirements.
1R16 Operator Workarounds
a. Inspection Scope (71111.16)
The inspector reviewed the licensees list of active operator burdens to assess the
cumulative effects on system reliability, availability, and potential for mis-operation of a
system. The inspector also toured various areas of the plant to evaluate deficient
conditions and potential impact to operators during EOP or AOP usage. At the time of
the inspection, no operator work-arounds were identified by Entergy. The inspector used
OASL 15.43, Operator Burden Program as a reference for this review.
b. Findings
No findings of significance were identified.
The inspector noted that one deficiency in the primary auxiliary building that impacted
operators during emergency operating procedure usage (ES 1.4, Transfer to Hot Leg
Recirculation) was a failed breaker handle for valve 856A, 21 safety injection cold leg
isolation valve. Entergy added this deficiency as an operator workaround and repaired
the breaker handle on the motor control center during the inspection period.
1R19 Post Maintenance Testing
a. Inspection Scope (71111.19)
The inspector reviewed post-work test (PWT) procedures and associated testing
activities to assess whether: 1) the effect of testing in the plant had been adequately
addressed by control room personnel; 2) testing was adequate for the maintenance work
order (WO) performed; 3) acceptance criteria were clear and adequately demonstrated
operational readiness consistent with design and licensing documents; 4) test
instrumentation had current calibrations, range, and accuracy for the application; and 5)
test equipment was removed following testing.
The selected testing activities involved components that were risk significant as identified
in the IP2 Individual Plant Examination. The regulatory references for the inspection
Enclosure
12
included Technical Specification 6.8.1.a. and 10 CFR 50, Appendix B, Criteria XIV,
Inspection, Test, and Operating Status. The following testing activities were evaluated:
- WO IP2-03-05119, Re-work on 22 Containment Spray Pump Discharge Stop
Valve 866D
- WO IP2-03-13966, PWT to Perform PT-Q27A, 21 Auxiliary Feedwater Pump
- WO IP2-02-39537, EDG 22 Two SOP Tests on PCV-5005 and PCV-5006
- WO IP2-03-16404, PWT to Perform PT-Q43 to Stroke FCV-1207
b. Findings
No findings of significance were identified.
1R22 Surveillance Testing
a. Inspection Scope (71111.22)
The inspector reviewed surveillance test procedures and observed testing activities to
assess whether: 1) the test preconditioned the component tested; 2) the effect of the
testing was adequately addressed in the control room; 3) the acceptance criteria
demonstrated operational readiness consistent with design calculations and licensing
documents; 4) the test equipment range and accuracy was adequate and the equipment
was properly calibrated; 5) the test was performed per the procedure; 6) the test
equipment was removed following testing; and 7) test discrepancies were appropriately
evaluated. The surveillance tests observed were based upon risk significant components
as identified in the IP2 Individual Plant Examination. The regulatory requirements that
provided the acceptance criteria for this review were 10 CFR 50, Appendix B, Criterion V,
Instructions, Procedures, and Drawings, Criterion XIV, Inspection, Test, and Operating
Status, Criterion XI, Test Control, and Technical Specifications 6.8.1.a. The following
test activities were reviewed:
- PT-Q33A, 21 Charging Pump
- PI-M2, Containment Building Inspection
- PT-M21B, Emergency Diesel Generator 22 Load Test
- TOI 213 Tavg Increase to 562 degrees F
- PT-Q27A, 21 Residual Heat Removal Pump Test
- PT-Q31A, 21 Auxiliary Component Cooling Pump
b. Findings
No findings of significance were identified.
During the monthly containment inspection, the inspectors noted that the non-licensed
operator was not familiar with the location of the seven conoseals on top of the reactor
vessel head. The inspection was re-performed on April 18 and confirmed there was no
leakage from the flanged instrument tubes on top of the vessel head. The visual
inspection of the conoseal flanges was a commitment to NRC Generic Letter 88-05,
Enclosure
13
Boric Acid Corrosion of Carbon Steel Reactor Pressure Boundary Components in PWR
Plants.
1EP4 Emergency Action Level and Emergency Plan Changes
a. Inspection Scope (71114-04)
During an in-office inspection conducted May 19 - 20, 2003, the inspectors reviewed
recent changes to Emergency Plan documents as stated in the attachment to this report.
A thorough review was conducted of aspects of the plan relating to the risk significant
planning standards (RSPS), such as classifications, notifications, and protective action
recommendations. A general review was conducted for non-RSPS portions. These
changes were reviewed against 10 CFR 50.54(q) to ensure that the changes do not
decrease the effectiveness of the plan, and that the changes to meet the standards of 10
CFR 50.47(b) and the requirements of Appendix E. All of the changes made to the
Emergency Plan or implementing procedures are subject to future inspections to ensure
that the results of the changes continue to meet NRC regulations.
b. Findings
No findings of significance were identified.
2. RADIATION SAFETY
Cornerstone: Occupational Radiation Safety (OS)
2OS1 Access Control to Radiologically Significant Areas
a. Inspection Scope (71121.01)
The inspector reviewed radiological work activities and practices and procedural
implementation during tours and observations of the facilities. Additionally, the inspector
reviewed procedures, records, and other program documents to evaluate the
effectiveness of access controls to radiologically significant areas.
On April 9, 2003, the inspector toured and observed work activities in selected portions of
the fuel handling building and the chemical systems building in Unit 1, including the area
in the sphere annulus area where the pipe from the north curtain drain was located. On
April 10, the inspector, accompanied by the Technical Support Manager, toured and
observed work activities on various elevations in the primary auxiliary and fuel handling
buildings in Unit 2. At the routine radiologically controlled area (RCA) access control
point, the inspector observed radiation workers logging into the RCA on radiological work
permits (RWPs) using electronic dosimeters and observed radiation workers exiting the
RCA and then logging out of their RWPs. The inspector examined the use of personnel
dosimetry and the radiological briefings for radiation workers.
On May 21, 2003, the inspector toured and observed work activities in selected portions
of the fuel handling building and of the chemical systems building in Unit 1, including the
Enclosure
14
area in the sphere annulus area where the pipe from the north curtain drain was located.
On May 21 and 23, the inspector toured and observed work activities on various
elevations in the primary auxiliary, fuel handling, and maintenance and outage buildings
in Unit 2. On May 22, inspectors examined the outside and inside of the old steam
generator storage building. Also, during these walkdowns, the inspector observed and
verified the appropriateness of the posting, labeling, and barricading of radioactive
material, radiation, contamination, high radiation, and locked high radiation areas. The
inspector reviewed work activities by both radiation workers and radiation protection
technicians for compliance with the RWP requirements and radiological protection
procedures. Specifically, the radiological controls for replacing packing on the No. 22
charging pump, covered by radiological work permit No. 032023, were reviewed and
observed.
The inspector reviewed radiological work activities and practices and procedural
implementation during tours and observations of the facilities and inspected procedures,
records, and other program documents to evaluate the effectiveness of Entergys access
controls to radiologically significant areas.
The inspector performed a selective examination of program documents (reference the
List of Documents Reviewed) to evaluate the adequacy of radiological controls. The
review was against criteria contained in 10 CFR 19.12, 10 CFR 20 (Subparts D, F, G, H,
I, and J), Technical Specifications, and site procedures.
b. Findings
No findings of significance were identified.
2OS2 ALARA Planning and Controls
a. Inspection Scope (71121.02)
The inspector reviewed the effectiveness of Entergys program to maintain occupational
radiation exposure as low as is reasonably achievable (ALARA).
During the inspection week, the inspector discussed the Unit 2 cumulative dose result for
2002 (248 person-rem) and the three-year-average (2000 through 2002) cumulative dose
result for Unit 2 (279.2 person-rem) with the Indian Point Energy Center (IPEC) Technical
Support Manager and the Radiation Protection Manager. The inspector also discussed
the actual versus projected cumulative year-to-date dose results for 2003 for Units 1 and
2 with the Radiation Protection Manager.
During the inspectors tour of Unit 2 on April 10, 2003, accompanied by the Technical
Support Manager, the inspector examined the decontamination efforts accomplished
during the first quarter of the year and reviewed the planned source term and exposure
reduction efforts anticipated over the next five years.
The inspector performed a selective examination of documents (reference the List of
Documents Reviewed) for regulatory compliance and for adequacy of control of radiation
Enclosure
15
exposure. The review was against criteria contained in 10 CFR 20.1101 (Radiation
protection programs), 10 CFR 20.1701 (Use of process or other engineering controls),
and site procedures.
The inspector performed a selective examination of procedures and program documents
(List of Documents Reviewed Attachment) for regulatory compliance and for adequacy of
control of radiation exposure. The review was against criteria contained in 10 CFR
20.1101 (Radiation protection programs), 10 CFR 20.1701 (Use of process or other
engineering controls), and site procedures.
b. Findings
No findings of significance were identified.
2OS3 Radiation Monitoring Instrumentation and Protective Equipment
a. Inspection Scope (71121.03)
The inspector reviewed the program for health physics instrumentation to determine the
accuracy and operability of the instrumentation.
During the plant tours described in Section 2OS1 of this report, the inspector reviewed
field instrumentation utilized by health physics technicians and plant workers to measure
radioactivity and radiation levels, including portable field survey instruments, hand-held
contamination frisking instruments, and continuous air monitors. The inspector also
reviewed installed radiation monitors including whole body friskers, portal monitors, area
monitors, and process monitors. The inspector verified current calibration, source
checking, and proper instrument function. The inspector also identified and noted the
condition, operability, and calibration status of selected installed area and process
radiation monitors and any accessible local indication information for those monitors.
The inspector performed a selective examination of documents (reference the List of
Documents Reviewed) for regulatory compliance and adequacy. The review was against
criteria contained in 10 CFR 20.1501, 10 CFR 20 Subpart H, site Technical
Specifications, and site procedures.
On May 21, the inspector met with the cognizant radiological engineer to discuss the
corrective actions for the issue identified in CR-IP2-2002-04583. The issue involved the
need to periodically evaluate and document the impact that difficult-to-detect
radionuclides have on the detection capabilities and limits of the contamination
monitoring instrumentation in use. The inspector also reviewed selected use/calibration
procedures (reference the List of Documents Reviewed) for this instrumentation.
b. Findings
No findings of significance were identified.
3. SAFEGUARDS
Enclosure
16
3PP4 Security Plan Changes
a. Inspection Scope (71130.04)
An in-office review was conducted of changes to the Security Plan, identified as
Revision 21A, submitted to the NRC on August 16, 2002, in accordance with the
provisions of 10 CFR 50.54(p). The review was conducted to confirm that the changes
were made in accordance with 10 CFR 50.54(p), and did not decrease the effectiveness
of the plan.
The NRC recognizes that some requirements contained in this program plan may have
been superceded by the February 25, 2001 interim compensatory measures order.
An in-office review was conducted of changes to the licensees Training and Qualification
Plan identified as Revision 0. This document was submitted to the NRC on December 9,
2002, in accordance with the provisions of 10 CFR 50.54(p). The review was conducted
to confirm that the changes were made in accordance with 10 CFR 50.54(p), and did not
decrease the effectiveness of the Training and Qualification Plan. The NRC recognizes
that some requirements contained in the Training and Qualification Plan may have been
superceded by the February 2002 Interim Compensatory Measures Order.
b. Findings
No findings of significance were identified.
Enclosure
17
4. OTHER ACTIVITIES (OA)
4OA1 Performance Indicator Verification
The inspector reviewed the licensees performance indicator (PI) data collecting and
reporting process as described in procedure SAO-114, Preparation of NRC and WANO
Performance Indicators. The purpose of the review was to determine whether the
methods for reporting PI data are consistent with the guidance contained in Nuclear
Energy Institute (NEI) 99-02, Regulatory Assessment Performance Indicator
Guidelines, Revisions 1 and 2. The inspection included a review of the indicator
definitions, data reporting elements, calculation methods, definition of terms, and
clarifying notes for the performance indicators. Plant records and data were sampled
and compared to the reported data. The inspector reviewed the licensees actions to
address and satisfactorily resolve discrepancies in the performance indicator data.
.1 Unplanned Power Changes Greater than 20% over 7000 Critical Hours
a. Inspection Scope (711151)
The inspector performed a periodic review of the 3rd and 4th quarters of 2002 and the 1st
quarter of 2003 performance indicator (PI) data submitted by the licensee for the
unplanned power changes greater than 20% over 7000 critical hours to determine
accuracy and completeness. The inspectors researched the control room operating logs
and the condition reporting system to identify power reductions greater than 20% during
these quarters. The inspectors compared the PI data against the guidance contained in
b. Findings
No findings of significance were identified.
.2 Safety System Unavailability - Auxiliary Feedwater
a. Inspection Scope (71151)
The inspector reviewed Entergys PI data for Auxiliary Boiler Feedwater (ABFW) Safety
System Unavailability to verify that the PI data was accurate and complete. The
inspectors compared the PI data reported by the licensee to information gathered from
the control room logs, condition reports, and work orders for the 2nd, 3rd, and 4th quarters
of 2002. In addition, the inspectors interviewed the system engineers. The inspectors
compared the PI data against the guidance contained in NEI 99-02
b. Findings
No findings of significance were identified.
.3 Reactor Coolant System Specific Activity
Enclosure
18
a. Inspection Scope
The inspector reviewed the PI for reactor coolant system (RCS) specific activity for the
period from January 2002 - March 2003. The RCS specific activity PI is reported as a
percentage of the maximum Technical Specification limit for dose equivalent iodine-131
in micro-Curies per cubic centimeter. For the period reviewed, this PI remained in the
Green band. The inspector reviewed monthly average RCS sample results based upon
daily samples obtained per IPC-S-009-S, Primary Sampling System Sentry. The
inspector also observed a daily sample on May 14, 2003. The inspector compared the PI
data against the guidance contained in NEI 99-02.
b. Findings
No findings of significance were identified.
.4 Scrams With Loss of Normal Heat Removal
a. Inspection Scope
The inspector reviewed the PI for scrams with loss of normal heat removal (LNHR) for
the period from January 2002 - March 2003 (the inspector notes that Entergys PI data
for Unplanned Scrams Per 7,000 Critical Hours was reviewed during the previous
quarterly inspection, reference report No. 50-247/2003-003). The scrams with LNHR PI
monitors the number of unplanned scrams while critical, during the previous 12 quarters,
that involved a loss of the normal heat removal path through the main condenser. The
inspector reviewed operator logs, licensee event reports, and monthly operating reports
to compare PI data reported by the licensee. The inspector compared the PI data
against the guidance contained in NEI 99-02.
b. Findings
No findings of significance were identified.
4OA2 Identification and Resolution of Problems
.1 Annual Sample Associated with the Failure of No. 22 Component Cooling Water (CCW)
Pump
a. Inspection Scope (71152
The inspector reviewed the corrective actions associated with the failure of No. 22 CCW
pump which occurred on December 5, 2002. This failure was documented in condition
report No. IP2-2002-11242. The pump failure involved inadequate lubrication of the
inboard bearing. This condition was caused by the oiler, which maintains the bearing
housing oil level, being bent in the downward direction thus lowering the oil level at the
bearing. The corrective actions were completed and the condition report closed out on
May 9, 2003. The inspector reviewed the condition report, and its associated apparent
cause evaluation and corrective actions, to verify that the cause(s) of the pump failure
Enclosure
19
was properly identified and evaluated, the corrective actions were appropriate to resolve
the problem, and that actions were properly implemented in a timely manner,
commensurate with the safety significance. The inspector discussed this event with the
system engineer and the Corrective Actions Department staff. The inspector also
reviewed the vendor technical manual and the design change package (MSAP-91-
00014-PGI).
b. Findings
Introduction. A Green non-cited violation was identified by the inspectors. This finding is
based on the failure of Entergy to properly evaluate and take effective corrective actions
associated with the failure of the No. 22 CCW pump on December 5, 2002, resulting
from an improper material substitution on the inboard bearing oil level indication system
performed in March 2000. This finding was determined to be a violation of 10 CFR 50,
Appendix B, Criterion XVI.
Description. On March 15, 2000, the licensee performed corrective maintenance to
resolve excessive oil leaks on the No. 22 CCW pump piping between the bearing
housing and oiler. This work was performed under work order No. NP-99-1111. The
original equipment piping was 1/4-inch schedule 80 carbon steel and consisted of two
lengths of threaded pipe connected by a 90 degree elbow. Due to recurrent oil leaks
from the threaded connections, the original piping was replaced with 3/8-inch stainless
steel tubing. The need for an elbow was negated by placing a 90-degree bend in the
tubing. This change in configuration effectively resolved the problem with oil leaks. No
engineering analysis was performed for this change since it was determined to be a
below the level of detail change in system configuration.
On December 5, 2002, No. 22 CCW pump failed due to inadequate lubrication of the
inboard bearing. Upon licensee investigation it was determined that the oiler was at a
lower position than required due to the tubing being bent in a downward direction at the
90-degree bend. The licensee noted that the tubing was not as rigid as the original
configuration and returned the system back to its original carbon steel piping design.
Analysis. The inspector-identified performance deficiency is an ineffective evaluation
and corrective actions for safety-related equipment, as documented in the December
2002 condition report No. IP2-2002-11242. While the unapproved 2000 modification did
not directly cause the pump to fail, it did introduce a new failure mode because the
stainless steel tubing was less rigid and could be more easily bent (a causal factor of the
pump failure). While the licensee stated that the bearing lubrication piping configuration
was thought to have been outside the scope of a modification, inspector review of the
vendor technical manual drawings identified a clearly depicted threaded pipe
configuration. In addition, design change MSAP-91-00014-PGI credited the 1/4-inch
schedule 80 carbon steel pipe in its seismic analysis assumptions. The inspectors
review of condition report (CR) No. IP2-2002-11242 identified that no evaluation was
conducted to determine how the replacement of the piping occurred without an
engineering evaluation or how the configuration change bypassed the modification
process. The CR evaluation also overlooked the fact that the seismic analysis had been
invalidated by the substitution of stainless steel tubing for threaded carbon steel pipe. No
Enclosure
20
action was taken by Entergy to confirm that the modified configuration could have
performed its safety function in a design basis event between March 2000 and December
2002.
This finding is more than minor since it is associated with the design control attribute of
the mitigating systems cornerstone and affected the cornerstone objective. The
inspectors conducted a Phase 1 SDP screening and determined that the failure to
adequately maintain design control on No. 22 CCW pump was of a very low safety
significance since the redundant train components were operable and unaffected by this
unauthorized tubing modification.
Enforcement. 10 CFR 50, Appendix B, Criterion XVI, states that measures shall be
established to assure that nonconformances are promptly identified and corrected.
Contrary to the above, Entergys evaluation and corrective actions associated with CR
IP2-2002-11242 did not address appropriate corrective actions associated with how an
unapproved modification to the No. 22 CCW pump bearing housing and oiler piping
configuration was made in March 2000. Because this failure to implement adequate
corrective actions is of very low safety significance and has been entered into the
licensees corrective actions program (CR-IP2-2003-03652), this violation is being treated
as a non-cited violation, consistent with Section VI.A of the NRC Enforcement Policy.
(NCV 50-247/2003-007-02). Entergy has proposed corrective actions to reinforce with
maintenance and engineering personnel that configuration control changes require
proper review and approval.
4OA6 Meetings, Including Exit
The inspectors met with Indian Point 2 representatives at the conclusion of the inspection
on July 9, 2003. At that time, the purpose and scope of the inspection were reviewed,
and the preliminary findings were presented. The licensee acknowledged the preliminary
inspection findings.
The inspector asked the licensee whether any materials examined during the inspection
should be considered proprietary. No proprietary information was reviewed during this
inspection.
Enclosure
A-1
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Entergy:
W. Axelson Support Supervisor
S. Baer HP Supervisor
J. Barry Radiological Engineer
R. Cranker Radiation Protection Technician
M. Dampf Health Physics Manager
R. Deschamps Radiological Protection Superintendent
R. Decensi Technical Support Manager
J. Dirset Radiation Protection Technician
R. Fucheck HP Supervisor
D. Gately Radiation Protection Coordinator
B. Kyler HP Supervisor
R. LaVera Radiological Engineer
R. Majes Radiological Engineer
R. Richards HP Supervisor
R. Rodino Radiological Engineer
E. Salisbury Radiological Engineer
W. Scholtens Waste Management Contractor
R. Solanto HP Supervisor
J. Stewart HP Supervisor
R. Tagliomonte Waste Management Supervisor
G. Tiberi Dosimetry Technician
N. Azevedo ISI Supervisor
W. Axelson Support Supervisor
T. Burns Environmental Supervisor
J. Comiotes Director, Nuclear Safety Assessment
L. Cortopassi IP3 Training Manager
F. Dacimo Vice-President
S. Davis IP2 Licence Operator Requalification Training Supervisor
J. DeRoy General Manager Plant Operations, IP3
K. Finucan Emergency Planning Staff
K. Finvean Reactor Vessel Head Inspection, Assistant Project Manager
M. Gillman IP3 Operations Manager
L. Glander Dosimetry Supervisor
J. Goebel Reactor Vessel Head Inspection, Project Manager
F. Inzirillo Manager Emergency Planning
T. Jones Nuclear Safety and Licensing
J. McCann Nuclear Safety and Licensing Manager
F. Mitchell HP Supervisor
D. Pace VP - Engineering - ENN
J. Perrotta Quality Assurance Manager
R. Penny Manager, Engineering Programs
K. Richett HP Technician
Attachment
A-2
R. Sachatello Radiological Consultant
C. Schwarz General Manager, IP2 Plant Operations
G. Schwartz Chief Engineer
H. Salmon Quality Assurance Director
M. Smith Director of IP3 Engineering
R. Solanto HP Supervisor
S. Stevens HP Technician
J. Stewart HP Supervisor
D. Sullivan-Weaver Emergency Planning Staff
J. Tuohy Design Engineering Manager
J. Wheeler Site Training Manager
F. Wilson Superintendent, Operations Training
M. Wilson Emergency Planning Staff
J. Bonner Entergy Northeast Offsite power coordinator
R. Burroni Supr. I&C Maintenance
P. Gropp Manager, DBI Program
T. Jones Licensing
T. Klein Senior Design Engineer
R. Milici Supr. Electrical Design Engineer
T. McCaffrey Supr. Electrical System Engineer
S. Petrosi Manager, Design Engineering
J. Quirk DBD Coordinator
J. Raffaele Sr. Lead Electrical Engineer, DBI Project
J. Tuohy Manager, Engineering Support
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Open/Closed
50-247/03-07-01 FIN Inadequate operability evaluation for the 13.8 KV system
50-247/03-07-02 NCV Ineffective corrective actions associated with an unauthorized
modification to the 22 component cooling water pump
Attachment
A-3
LIST OF CONDITION REPORTS GENERATED
IP2-200303443 Small hole in the mortar joint between concrete blocks in the south wall of
the 23 battery room
IP2-2003-3464 Safety evaluation 95-058-EV reclassification of Fire Zone 25 barriers as
unclassified from Type 1" was not approved by on-site review committee
IP2-2003-2877 Valve 1843B, 22 Safety Injection Pump thrust balance line as a slight
IP2-2003-2876 Scaffolding exists in the area of the Refueling Water Storage Tank without
scaffolding tags in place
IP2-2003-2878 22 Safety Injection Pump has evidence of seal leakage at the pump
inboard seal. Dried boron, not active.
IP2-2003-2959 PI-M2 Vapor containment monthly inspection was performed and
information on the conoseal location and schematic drawings were not
incorporated into the procedure.
IP2-2003-03940 Problems with valve labeling and abnormal operating instruction (AOI)
11.1
IP2-2003-2597 NRC observed during plant startup that both PORV block valves were
open contrary to check off list COL 01-01 during plant startup
IP2-2003-04245 Programmatic failure on closure of condition reports to PCNs
IP2-2003-3652 Failure of the 22 Component Cooling Water Bearing
IP2-2003-2595 Seal Injection Flow Momentarily to zero flow during charging pump speed
adjustments
Attachment
A-4
LIST OF DOCUMENTS REVIEWED
Indian Point Energy Center Emergency Plan, Rev 03-01
IP-EP-115, Emergency Plan Forms, Rev 1, 2
IP-EP-130, Emergency Notifications and Mobilization, Rev 0
IP-EP-250, Emergency Operations Facility, Rev 0
IP-EP-251, Alternate Emergency Operations Facility, Rev 1
IP-EP-255, Emergency Operations Facility Management and Liaisons, Void
IP-EP-260, Joint News Center, Rev 0
IP-EP-310, Dose Assessment, Rev 1
IP-EP-410, Protective Action Recommendations, Rev 1
IP-EP-510, Meteorological, Radiological & Plant Data Acquisition System, Rev 1
IP-EP-520, Modular Emergency Assessment & Notification System (MEANS), Rev 1
IP-EP-610, Emergency Termination and Recovery, Rev 1
IP-EP-620, Estimation of Total Population Exposure, Rev 1
IP-1002, Emergency Notification and Communication, Rev 29, Void (IP2)
IP-1010, Central Control Room, Rev 9, 10 (IP2)
IP-1011, Joint News, Void (IP2)
IP-1015, Radiological Monitoring Outside the Protected Area, Rev 11 (IP2)
IP-1019, Coordination of Corporate Response, Void (IP2)
IP-1030, Emergency Operations Facility, Void (IP2)
IP-1038, Offsite Emergency Notifications, Void (IP3)
IP-2001, ED, POM, Shift Managers Procedure, Rev 18 (IP3)
IP-2005, CR Offsite Communicator, Void (IP3)
IP-2300, Emergency Activation of the Emergency Operations Facility, Void (IP3)
IP-2302, EOF Technical Advisor & Information Liaison, Void (IP3)
IP-2303, EOF Radiological Assessment Team Leader, Void (IP3)
IP-2304, EOF Dose Assessment Health Physicist, Void (IP3)
IP-2305, EOF Midas Operator, Void, (IP3)
IP-2306, EOF Security Officer, Void (IP3)
IP-2307, EOF Clerk, Void (IP3)
IP-2308, EOF Direct Line Communicator, Void (IP3)
IP-2309, EOF Offsite Communicator, Void (IP3)
IP-2310, EOF Onsite Radiological Communicator, Void (IP3)
IP-2311, EOF Offsite Radiological Communicator, Void (IP3)
Section 2OS1, Access Control to Radiologically Significant Areas
- Self-assessment, HP access control system, April 6, 2003
- Self-assessment, Remote HP monitoring/3-year period, January 16, 2003
Section 2OS2, ALARA Planning and Controls
- IP1 daily ALARA information for April 6, 2003
- IP2 daily ALARA information for April 6, 2003
- ALARA suggestion program inputs (March/April 2003)
- IPEC ALARA committee meeting presentation handout for March 27, 2003
- Indian Point Energy Center/Radiation protection/Strategic plan for exposure
Attachment
A-5
reduction, 2003 - 2008
Section 2OS3, Radiation Monitoring Instrumentation and Protective Equipment
- Self-assessment, Review of dosimetry records, May 9, 2002 to February 14,
2003
Sections 1EP4, Emergency Action Level and Emergency Plan Changes
Emergency Plan for Indian Point Unit Nos 1 and 2, Rev 01-02a
Indian Point 3 Emergency Plan, Rev 46
Indian Point Energy Center Emergency Plan, Rev 02-01
IP-EP-251, Alternate Emergency Operations Facility, Rev 0
IP-EP-255, Emergency Operations Facility Management and Liaisons, Rev 1, 2
IP-EP-310, Dose Assessment, Rev 0
IP-EP-410, Protective Action Recommendations, Rev 0
IP-EP-510, Meteorological, Radiological & Plant Data Acquisition System, Rev 0
IP-EP-520, Modular Emergency Assessment & Notification System (MEANS), Rev 0
IP-EP-610, Emergency Termination and Recovery, Rev 0
IP-EP-620, Estimation of Total Population Exposure, Rev 0
IC/EALs, Initiating Conditions & Emergency Action Levels, Rev 9 (IP3)
IP-1001, Determining the Magnitude of Release, Rev 17, Void (IP3)
IP-1002, Emergency Notification and Communication, Rev 27, 28 (IP2)
IP-1003, Obtaining Meteorological Data, Rev 18, Void (IP3)
IP-1004, MIDAS Computer System, Rev 16, Void (IP3)
IP-1010, Central Control Room, Rev 6, 7, 8 (IP2)
IP-1013, Protective Action Recommendations, Rev 8, (IP2)
IP-1015, Radiological Monitoring Outside the Protected Area, Rev 10 (IP2)
Section 2OS1, Access Control to Radiologically Significant Areas
- SAO-302, Rev. 19, Radiation work permit (RWP) program
- HP-SQ-3.005, Rev. 24, HP work scheduling
- HP-SQ-3.013, Rev. 12, Routine surveys outside normal RCA
- HP-SQ-3.109, Rev. 28, Control of high radiation, locked high radiation, special
locked high radiation, and very high radiation areas
- RWP 032023, Rev. 0, Charging pump maintenance, repair, and test; Task 22-
Work in 22 charging pump cubicle
- Self-assessment of Technical Support Integration
Attachment
A-6
Section 2OS2, ALARA Planning and Controls
- RS-S-8.005, Rev. 5, ALARA cost-benefit analysis tracking log
- RS-SQ-8.006, Rev. 6, Radiological support ALARA design review
- RS-SQ-8.101, Rev. 5, Temporary shielding program
- IP1 daily ALARA information for May 18, 2003
- IP2 daily ALARA information for May 18, 2003
Condition Reports
199807874
199906643
200000978
200009088
200009884
200009892
200100559
200100750
200205411
200205377
200205379
200205384
200206578
200207521
200207918
200208627
200303284
Design Basis Documents
480 Volt AC System
Procedures
ENN-LI-102, Rev. 2, Corrective Action Process
SAO-112, Rev. 6, Condition Reporting Process (superceded by ENN-LI-102)
Section 2OS3, Radiation Monitoring Instrumentation and Protective Equipment
- HP-9.012, Rev. 4, Operation of Eberline RM-14 and RM-20
- HP-9.067, Rev. 8, Calibration of the Eberline PCM-1A/1B
- HP-9.082, Rev. 1, Efficiency check of G-M pancake type detectors
- HP-9.512, Rev. 5, Calibration of the Eberline RM-14/RM-20 radiation monitors
- HP-9.590, Rev. 1, Calibration of Eberline tool contamination monitor
- HP-9.591, Rev. 4, Calibration procedure for National Nuclear Model Gamma-
40/60 portal monitor
- HP-9.593, Rev. 2, Calibration and operation of Eberline gamma tool monitor
Attachment
A-7
(GTM)
- HP-SQ-3.002, Rev. 17, Equipment and materials release requirements
- HP-SQ-3.011, Rev. 17, Radiation and contamination survey techniques
- Health physics continuing training lesson plan, LP No. HCT0301.01,
Instrumentation sensitivity and contamination control, Rev. 0
- Assessment of the sensitivity to internal contamination for the PCM-1B and
Gamma 60 personnel contamination monitors at IP2, March 2002, by
Cabrera Services
LIST OF BASELINE INSPECTIONS PERFORMED
71111.01 Adverse Weather 1R01
71111.04 Equipment Alignment 1R04
71111.05 Fire Protection 1R05
71111.07 Heat Sink Performance 1R07
71111.11 Operator Requalification 1R11
71111.12 Maintenance Effectiveness 1R12
71111.13 Maintenance Risk Assessment and Emergent Work Activities 1R13
71111.14 Personnel Performance During Non-Routine Plant Evolutions 1R14
71111.15 Operability Evaluations 1R15
71111.16 Operator Workarounds 1R16
71111.19 Post Maintenance Testing 1R19
71111.22 Surveillance Testing 1R22
71111.23 Temporary Plant Modifications 1R23
71114-04 Emergency Action Level and Emergency Plan Changes 1EP4
71121.01 Access Control to Radiologically Significant Areas 2OS1
71121.02 ALARA Planning and Controls 2OS2
71121.03 Radiation Monitoring Instrumentation and Protective Equipment 2OS3
71151 Performance Indicator Verification 4OA1
71152 Problem Identification and Resolution Sample 4OA2
71153 Event Followup 4OA3
LIST OF ACRONYMS
ABFW auxiliary boiler feedwater
AFWP auxiliary feedwater pump
ALARA as low as reasonably achievable
AOI abnormal operating instruction
BATP boric acid transfer pump
CAP corrective action program
CCR central control room
CCW component cooling water
CFR Code of Federal Regulations
COL check off list
CR condition report
EDG emergency diesel generator
EFPY effective full power years
Attachment
A-8
OAD operations administrative directive
EOF emergency operations facility
IP Indian Point
IP2 Indian Point Unit 2
IPEC Indian Point Energy Center
IPEEE individual plant examination for external events
kV kilo-volt
LNHR loss of normal heat removal
NCV non-cited violation
NEI Nuclear Energy Institute
NRC Nuclear Regulatory Commission
NRR Nuclear Reactor Regulation
OS occupational safety
PI performance indicator
PM post maintenance
PT penetrant testing
PWT post-work test
RCA radiologically controlled area
RMS radiation monitoring system
RPM radiation protection manager
RSPS risk significant planning standard
RTP rated thermal power
RV reactor vessel
RWP radiation work permit
SAO station administrative order
SDP significance determination process
SI safety injection
SOP system operating procedure
TA temporary alteration
TS technical specifications
UFSAR Updated Final Safety Analysis Report
V volt
WO work order
Attachment