IR 05000388/2013007

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IR 05000388-13-007, 01/14/203 - 02/07/2013, Susquehanna Steam Electric Station, Unit 2
ML13080A158
Person / Time
Site: Susquehanna Talen Energy icon.png
Issue date: 03/21/2013
From: Chris Miller
Division of Reactor Safety I
To: Rausch T
Susquehanna
References
IR-13-007
Download: ML13080A158 (43)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION rch 21, 2013

SUBJECT:

SUSQUEHANNA STEAM ELECTRIC STATION UNIT 2 - NRC SPECIAL INSPECTION REPORT 05000388/2013007

Dear Mr. Rausch:

On February 7, 2013, the U.S. Nuclear Regulatory Commission (NRC) completed a Special Inspection at your Susquehanna Steam Electric Station. The inspection was conducted in response to the repetitive nature of operational problems related to reactor vessel level control, which contributed to five valid Reactor Protection System actuations between November 9 and December 19, 2012, at Susquehanna Unit 2, repetitive issues with the operation of the Integrated Control System (ICS), and specific questions related to operational decision-making that led to the December 19, 2012 unplanned reactor shutdown. The NRCs initial evaluation of this event satisfied the criteria in NRC Inspection Manual Chapter (IMC) 0309, Reactive Inspection Decision Basis for Reactors, for conducting a Special Inspection. The Special Inspection Team (SIT) Charter (Attachment 2 of the enclosed report) provides the basis and additional details concerning the scope of the inspection. The enclosed inspection report documents the inspection results, which were discussed at the exit meeting on February 7, 2013, with you and other members of your staff.

The inspection team examined activities conducted under your license as they relate to safety and compliance with Commission rules and regulations and with the conditions of your license.

The inspection team interviewed various plant personnel including operations personnel involved in the December 19, 2012, automatic plant shutdown. The inspectors reviewed plant logs, selected procedures and records, event evaluations, causal investigations, relevant performance history, and corrective actions planned and completed to assess the significance and potential consequences of issues related to the December 19, 2012, event.

The inspection team concluded that Susquehanna Unit 2 operated within acceptable limits, and no equipment malfunctioned during the automatic reactor shutdown. Nonetheless, the inspection team identified several issues related to human performance and compliance with procedures that contributed to the event. The enclosed chronology (Attachment 3 of the enclosed report) provides additional details regarding the timeline and sequence of events. This report documents two non-cited violations (NCVs) and one finding (FIN) of very low safety significance (Green). However, because of the very low safety significance of the violations and because they were entered into your correction action program, the NRC is treating them as non-cited violations (NCV) consistent with Section 2.32 of the NRC Enforcement Policy. If you contest any violations documented in the enclosed report, you should provide a response within 30 days of the date of the inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Senior Resident Inspector at Susquehanna Steam Electric Station. In addition, if you disagree with the cross cutting aspect assigned to any finding in this report, you should provide a response within 30 days of the date of the inspection report, with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC Senior Resident Inspector at Susquehanna Steam Electric Station.

In accordance with Title 10 of the Code of Federal Regulation (10 CFR) Part 2.390 of the NRC's

"Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room and from the Publicly Available Records (PARS) component of NRCs document system, Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Christopher G. Miller, Director Division of Reactor Safety Docket No. 50-388 License No. NPF-22

Enclosure:

Inspection Report 05000388/2013007 w/Attachments: Supplemental Information (Attachment 1)

Special Inspection Team Charter (Attachment 2)

Detailed Sequence of Events (Attachment 3)

Simplified System Drawings (Attachment 4)

REGION I==

Docket No.: 50-388 License No.: NPF-22 Report No.: 05000388/2013007 Licensee: PPL Susquehanna, LLC (PPL)

Facility: Susquehanna Steam Electric Station, Unit 2 Location: Berwick, Pennsylvania Dates: January 14 through February 7, 2013 Team Manager: Donald E. Jackson, Chief Operations Branch Division of Reactor Safety Team Leader: John Caruso, Senior Operations Engineer Division of Reactor Safety Team: John Richmond, Senior Reactor Inspector Engineering Support Branch 3 Division of Reactor Safety Justin Hawkins, Resident Inspector (Limerick)

Division of Reactor Projects Approved By: Christopher G. Miller, Director Division of Reactor Safety Enclosure

SUMMARY OF FINDINGS

IR 05000388/2013007; 01/14/2013 - 02/7/2013; Susquehanna Steam Electric Station, Unit 2;

Inspection Procedure 93812, Special Inspection.

A three-person NRC team, comprised of two regional inspectors and one resident inspector, conducted this Special Inspection. Inspectors identified two non-cited violations (NCVs) and one finding (FIN) of very low safety significance (Green). The significance of most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual Chapter (IMC)0609, "Significance Determination Process" (SDP), dated June 2, 2011. Cross-cutting aspects are determined using IMC 0310, Components Within Cross-Cutting Areas, dated October 28, 2011. All violations of NRC requirements are dispositioned in accordance with the NRCs Enforcement Policy, dated June 7, 2012. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4.

Cornerstone: Initiating Events

Green.

Inspectors identified a Green NCV of Technical Specification (TS) 5.4.1,

Procedures, related to the requirement to operate the feedwater system in accordance with procedures and implement the procedure change process. The PPL procedures implementing these requirements state that if an approved document that addresses the circumstances does not exist, then create a procedure or perform the task using another approved method (i.e., troubleshooting plan or work order). Contrary to this requirement, on December 19, 2012, Pennsylvania Power and Light (PPLs) operators opened the breaker to the A Reactor Feed Pump (RFP) discharge isolation valve (3A)valve motor operator (i.e., when the 3A valve failed to open as expected) without establishing or implementing procedural guidance or implementing another process such as a troubleshooting plan or work order. This action resulted in the feedwater control system logic causing closure of other feedwater valves, isolating all normal feedwater flow to the Reactor Pressure Vessel (RPV), and a subsequent automatic reactor shutdown (scram) on low water level. The PPL staff entered this issue into their corrective action program (CAP) as Condition Report (CR) 1668242, and conducted site-wide training on procedural use and adherence standards.

The inspectors identified a performance deficiency because on December 19, 2012, PPL did not implement an approved procedure to open the breaker to the 3A valve motor operator, which resulted in a subsequent unplanned reactor scram. This finding is more than minor because it is associated with the human performance attribute of the Initiating Events Cornerstone and adversely impacted the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Additionally, this finding was similar to example 4.b of IMC 0612, Appendix E, Examples of Minor Issues. The finding was evaluated using NRC IMC 0609 Appendix A, User Guidance for Significance Determination for At-Power Situations, and the Station Standardized Plant Analysis Risk (SPAR) Model for a detailed risk assessment. Based upon the detailed risk assessment, the change in core damage frequency associated with this performance deficiency was in the low E-7 range, or of very low safety significance (Green). The inspectors determined that this finding had a cross-cutting aspect in the area of Human Performance, Work Control, i

because PPL operators did not appropriately plan work activities associated with opening the 3A valve manually by incorporating the need for planned contingencies, compensatory actions and abort criteria consistent with nuclear safety. H.3(a) (Section 3)

Cornerstone: Mitigating Systems

Green.

A self-revealing Green NCV of TS 5.4.1, Procedures, was identified involving the failure to incorporate the results of a Failure Modes and Effects Analysis (FMEA)completed in January 2010 into applicable operating procedures. The FMEA identified a vulnerability involving operator response to a loss of power to the RFP discharge isolation valves 3A (B, C) during the transfer from Discharge Pressure Mode (DPM) to Flow Control Mode (FCM). Specifically, PPLs FW operating procedures were not maintained to ensure operators could adequately recover RPV water level control when challenged with a system failure such as the condition that resulted in the Unit 2 scram on December 19, 2012. The PPL staff entered this issue into the CAP as AR-OPG-1654037, CR 1666244, and CR 1666253.

The finding was more than minor because it was associated with the procedure quality attribute of the Mitigating Systems Cornerstone and adversely impacted the objective to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). The finding was evaluated using NRC IMC 0609, Attachment 0609.04, Initial Characterization of Findings, and Appendix A, User Guidance for Significance Determination for At-Power Situations, and screened as very low safety significance (Green) per Exhibit 2. The inspectors determined that this finding had a cross-cutting aspect in the area of Human Performance, Resources, because PPL staff did not ensure that procedures were complete, accurate and up-to-date to assure nuclear safety. Specifically, PPLs engineering modification procedures and checklists did not ensure that known single point design vulnerabilities were adequately addressed in FW procedures to ensure operators could adequately recover reactor water level prior to the Unit 2 reactor scram on December 19, 2012. H.2(c) (Section 3)

Green.

A self-revealing finding (FIN) of very low safety significance (Green) was identified for PPL staffs failure to follow their CAP procedure, NDAP-QA-0702, Action Request and Condition Report Process, in response to an identified issue with the FW system. Specifically, on August, 23, 2011, PPLs staff did not initiate an action request (AR) or condition report (CR) after determining that ICS digital FW valve control needed to be placed in Manual Valve Control mode prior to de-energizing the 3A motor operated valve (MOV) in order to prevent a loss of all FW flow. This issue went unaddressed and subsequently on December 19, 2012, Unit 2 scrammed on low RPV water level when operators, while attempting to open the stuck 3A valve, opened the 3A valve power supply breaker with the A RFP FW valve controls in automatic causing a loss of all normal FW. The PPL staff entered this issue into the CAP as CR 1653480.

The finding was more than minor because it was associated with the human performance attribute of the Mitigating Systems Cornerstone and adversely impacted the objective to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). The finding ii

was evaluated using NRC IMC 0609, Attachment 0609.04, Initial Characterization of Findings, and Appendix A, User Guidance for Significance Determination for At-Power Situations, and screened as very low safety significance (Green) per Exhibit 2. The inspectors determined that this finding had a cross-cutting aspect in the area of Problem Identification and Resolution, CAP, because PPLs staff did not implement the CAP with a low threshold for identifying issues completely, accurately, and in a timely manner commensurate with their safety significance. Specifically, PPLs staff did not identify non-conforming issues for FW valve control, design and operation that eventually led to a loss of normal FW and scram of Unit 2 on December 19, 2012. P.1(a) (Section 5)iii

REPORT DETAILS

1. Background and Description of Event

In accordance with the Special Inspection Team (SIT) Charter (Attachment 2), the inspection team conducted a detailed review of the December 19, 2012, unplanned reactor shutdown event at Susquehanna Steam Electric Station, Unit 2 including: a review of prior related Feedwater (FW) Integrated Control System (ICS) equipment problems on November 9 and December 16, 2012; operator training and Just-In-Time Training (JITT); pre-job briefs, operator procedures; use of human performance error prevention techniques; licensee management oversight; and the effectiveness of the CAP and operator work around (OWA) program with respect to ICS equipment problems after the ICS modification was installed in 2010 (Unit 1) and 2011 (Unit 2).

The inspection team gathered information from the NRC resident inspectors, the plant process computer (PPC) alarm printouts and parameter trends, interviewed station personnel, observed simulator training and fidelity for ICS, reviewed procedures, logs, and various technical documents to develop a detailed sequence of events (Attachment 3).

On December 19, 2012, at 1731, Unit 2 reactor shut down (scrammed) from 18 percent power with the main generator on the grid. Operators were swapping the A RFP from Discharge Pressure Mode (DPM) (i.e., single element digital FW control) to Flow Control Mode (FCM) (i.e., three element digital FW control) with the B RFP in standby. At 1709, Operators placed the A RFP in FCM. During this transition, at 1711, operators observed that ICS did not reposition the 3A valve to open as expected.

At 1715, the Shift Manager (SM) and the operators discussed opening the 3A valve motor operator power supply breaker and manually opening the valve off its closed seat.

The SM then called the Outage Control Center (OCC) at 1720, and the OCC confirmed the 3A valve not opening was a repeat issue from the operator challenge list. At 1730, the SM contacted the OCC to inform them of the decision to manually open 3A valve.

Operators were sent to the 3A valve and its motor operator power supply breaker with the intent of removing power from the motor operator and then manually opening the 3A valve off its closed seat using the clutch and local hand wheel. This decision was based, in part, on previous history of the 3A valve failing to open on August 23, 2011.

When the operator opened the 3A power supply breaker at 1730, the 3A valve position indicating lights were deenergized, and the ICS system logic sensed the 3A valve in its open position (i.e., when power was lost to the valves green indicating light, the ICS logic input was zero volts, which the logic used as input for a full open valve position).

As a result the Startup Level Control Valve

(41) and the Startup Isolation Valve (51A),automatically closed as designed, resulting in loss of all normal FW to the Unit 2 RPV.

Operators attempted to take manual control of the B RFP discharge isolation valve (51B) and place the B RFP in service in DPM. The 51B valve indicated manual control but did not respond to operator demands due to FW system constraints concerning the first RFP being selected to FCM. During this short time period (less than 2 minutes),

RPV water level rapidly lowered; and before operators could take the mode switch to shutdown, an automatic scram occurred at 1731 due to low RPV water level of 13 inches.

The 3A valve power supply breaker was reclosed, and operators were able to place the A RFP back in DPM to restore RPV level control during post scram actions.

2. Integrated Control System (ICS) Design and Modification

a. Inspection Scope

The team determined that ICS is a non-safety related balance-of-plant process control system, which PPL staff had designated as important to safety. The Unit 2 ICS was installed in 2011. The team reviewed ICS as-built design drawings, and procedures, including normal and abnormal operating procedures to determine whether the original (i.e., pre-ICS modification) design basis, licensing basis, or performance capability of the FW flow and RPV water level control system capabilities had been degraded by the ICS modification. The team assessed PPL staff's technical evaluations and design details, and interviewed licensed operators, licensed operator simulator instructors, and engineering personnel to determine whether the ICS would function in accordance with the modification's assumptions, and with design and licensing requirements. Drawings and procedures were reviewed to verify whether they were properly updated to reflect the post-modification design and operation. Selected post modification test (PMT)results were reviewed to verify whether the acceptance criteria had been met.

Findings/Observations No findings of significance were identified.

The inspection team identified an ICS design weakness in that the ICS design did not incorporate good engineering practice. Specifically, the ICS did not validate the 3A valve position input as either valid or invalid data for automatic control functions but did validate the position input for indication on the Human-Machine Interface (HMI) display screen (e.g., yellow/red for valid, or gray with cyan boarder for invalid). As a result, when an operator opened the 3A power supply breaker, the 3A valve position circuit was deenergized and the ICS system logic sensed the 3A valve in its open position. As a result the 41 and 51A valves automatically closed as designed. At the same time the 3A valve position indication changed to gray with a cyan border on the HMI display screen.

This design allowed ICS to perform automatic control functions using an invalid valve position, which directly led to a significant operator challenge and subsequent plant scram due to a loss of normal FW flow to the reactor. The inspectors determined this issue of concern was not a performance deficiency because there was no standard identified that had not been met.

After the December 19, 2012 event, PPLs staff identified that the ICS modification had changed the control logic for FW MOVs controlled by ICS from momentary contacts (original hand switch) to maintained contacts (ICS software switch). The effect of the maintained contact was to bypass the MOV contactor seal-in circuit and allow the contactor to re-energize if the torque switch were to relax and re-close. The inspection team determined that this design change was not evaluated during the modification process, as required by PPL's design verification process, and was contrary to PPL's design requirements and specifications for Limitorque MOVs. The PPL staff determined this issue did not directly contribute to the event because the likely cause for the 3A valve failing to open (e.g., stuck on its closed seat) was not related to potential MOV motor hammering. The inspection team determined that this was a minor design deficiency because PPLs staff subsequently determined that the effect of potential motor hammering did not exceed the design capability of the Limitorque operator. The PPL staff entered this issue into their CAP as CR 1654543.

The inspection team also identified ICS HMI display human factors issues of concern as follows:

When the operator selects an ICS controller pop-up screen, the controller screen covers up a significant portion of the system screen and the associated process variables that the operator might need in order to adjust the controller settings. The PPL staff entered this issue into their CAP program as CR 1661485.

Invalid MOV position indication may not be sufficiently prominent to alert an operator during periods of high stress, such as during transient response. Specifically, an invalid indication changes the color of a valve icon bow-tie from yellow/red to gray with a small cyan border, instead of a bright backlit color that could stand out at a distance. As an example, when 3A valve power supply breaker was opened on December 19, 2012, the HMI indication changed from yellow (valve closed) to gray with cyan border (invalid/unknown position). In addition, the invalid indication of a gray bow-tie was backlit in a gray box. The PPL staff entered this issue into their CAP program as CR 1661485.

The inspectors determined these issues of concern involved insufficient consideration of human factors. There were no performance deficiencies identified because the inspectors did not identify a standard that had not been met.

3. Procedures

a. Inspection Scope

As part of the SIT Charter, dated January 7, 2012, the inspectors were tasked with evaluating the effect of operating procedures and previous procedure changes associated with ICS on the December 19, 2012 event. The inspection team interviewed the control room operators, as well as engineering and management personnel that were directly involved with the recent unplanned shutdowns and reactor scrams involving ICS on Unit 2. The inspectors reviewed PPLs procedures (i.e., standard operating, off-normal, transient and scram procedures that involved FW and ICS control), operating logs, licensee event reports, root cause evaluations, and recent AR/CRs generated for ICS issues.

b. Findings

/Observations

(1) Failure to Maintain Adequate Feedwater Procedures
Introduction.

A self-revealing Green NCV of TS 5.4.1, Procedures, was identified involving the failure to incorporate the results of a Failure Modes and Effects Analysis (FMEA) completed in January 2010 into station operating procedures. The FMEA identified a vulnerability involving operator response to a loss of power to the 3A (B, C)valve during the transfer from DPM to FCM.

Description.

On January 22, 2010, the FMEA of the ICS modification package identified a single point vulnerability regarding the 3A valve closed status. During the transition from DPM (i.e., single element startup level control) to FCM (i.e., three element FW level control), if power is interrupted to the 3A valve motor operator, the ICS system senses the 3A valve is in the open position and the FW control valves (i.e., 41 and 51A), will automatically close resulting in loss of all normal FW flow to the Unit 2 RPV. The ICS digital feedwater control system was designed to use the voltage applied to a valve position indicating light circuit (i.e., red light, green light) as the logic input for valve position. The ICS was designed to use "zero volts" on the valve's green light as the valve full open position indication for ICS logic operation (i.e., the green light is lit when the valve is closed or intermediate, and not lit when full open). This ICS design vulnerability allowed a zero voltage input, due to the loss of control voltage to the MOV (when the breaker was opened) to be interpreted as a valve full open signal, which in turn allowed the ICS logic to automatically close the 41 and 51 valves, as designed after the 3A valve "indicated that it had gone full open.

This system vulnerability allowed ICS to perform automatic control functions using an invalid valve position, and had the potential for a significant operator challenge to control RPV water level and possibly cause a reactor scram on loss of normal FW flow. The FMEA stated that the mitigation action for this design vulnerability was to have the operators maintain the system in manual control during certain modes of operation. The inspectors determined that this known system vulnerability was reviewed by PPLs staff during the modification installation process, but not specifically addressed in FW procedures.

On December 19, 2012, Unit 2 scrammed at 18 percent power with the main generator connected to the grid. At the time of the scram, operators were swapping the A RFP from DPM to FCM with the B RFP in standby. The Unit 2 A RFP 3A valve failed to open during this transition. Operators were sent to the 3A valve and opened the power supply breaker with the intent of manually opening the valve off its closed seat locally and then closing the breaker. This decision making was based, in part, on the August 23, 2011 event (discussed in Section 5). When the operator opened the 3A power supply breaker, the 3A valve position circuit was deenergized and the ICS system sensed the 3A valve in its default position (open), as a result the 41 and 51A valves, automatically closed as designed, resulting in a loss of all normal FW. Operators attempted to take manual control of the B RFP and place it in service in DPM per OP-245-001, RFP and RFP Lube Oil System, but RPV water level rapidly lowered and a scram occurred on low RPV water level.

The inspectors noted that at the time of the December 19, 2012 event, procedure OP-245-001 did not contain guidance to the operators regarding a loss of power to the 3A valve during the DPM to FCM transfer. The PPL staff revised the procedure after the event to add a caution and procedural steps to address this issue. The inspectors determined that the revised procedure did not contain guidance on how to respond to a closure of the 51A valve if closure of the 41 valve is not recognized by the operator within the initial 10 seconds. In response to the inspectors observation, PPLs staff wrote CR 1663285 to address this procedural issue.

Analysis.

The performance deficiency associated with this issue is that PPLs staff did not maintain adequate FW operating procedures that ensured operators could recover RPV water level control when challenged with the single point vulnerability prior to the Unit 2 reactor scram on December 19, 2012. The performance deficiency was evaluated in accordance with IMC 0612, Appendix B, Issue Screening, and determined to be more than minor because it was associated with the procedure quality attribute of the Mitigating Systems Cornerstone and adversely impacted the objective to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). The finding was evaluated using Section A of Exhibit 2 of NRC IMC 0609, Attachment 0609.04, Initial Characterization of Findings, and Appendix A, User Guidance for Significance Determination for At-Power Situations, and screened as very low safety significance (Green), because the performance deficiency did not result in a loss of safety function or represent an actual loss of function of one or more non-Technical Specification trains of equipment designated as high safety-significant in accordance with PPLs maintenance rule program for greater than 24 hrs.

The inspectors determined that this finding had a cross-cutting aspect in the area of Human Performance, Resources, because PPLs staff did not ensure that procedures were complete, accurate and up-to-date to assure nuclear safety. Specifically, PPLs engineering modification procedures and checklists did not ensure that known single point design vulnerabilities were adequately addressed in FW procedures to ensure operators could adequately recover reactor water level prior to the Unit 2 reactor scram on December 19, 2012. H.2(c)

Enforcement.

TS 5.4.1.a, Procedures, requires, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Regulatory Guide (RG) 1.33, Revision 2, Appendix A. RG 1.33, Appendix A lists activities that should be covered by written procedures. Section 4 identifies procedures for startup, operation, and shutdown which indicate 4.o FW system (FW pumps to reactor vessel). Contrary to the above, in January 2010, PPLs staff failed to maintain adequate FW operating procedures that ensured operators could adequately recover RPV water level control when challenged with the single point vulnerability described in the FMEA. This resulted in the Unit 2 scram on December 19, 2012. Because this finding is of very low safety significance and was entered into PPLs CAP as AR-OPG-1654037, CRA 1666244, and CRA 1666253, it is being treated as an NCV in accordance with the NRCs Enforcement Policy. (NCV 05000388/2013007-01, Failure to Maintain Adequate Feedwater Procedures)

During the inspectors review of the December 19 scram and previous ICS events, the inspectors noted additional examples of PPL procedural issues. Specifically:

Inspector interviews conducted after the December 19 event indicated the operator incorrectly used the wrong side of the Hard Card (operator aid) for loss of a feed pump when in either DPM or FCM. The operator placed the standby B RFP in-service in DPM after he had previously entered ICS FCM for the A RFP rather than placing the B RFP in-service in FCM using the back side of the Hard Card. The inspectors determined the Hard Card provided weak procedural guidance and should be revised to clarify when each side of the card should be utilized. (CR 166244)

On August 23, 2011, the 3A valve would not move from its closed position during a reactor startup. The PPL staff classified the issue as an Operator Challenge in the Operator Burdens list. The inspectors determined that no workaround instructions or compensatory actions were developed and given to the operators as required by the Operator Burden procedure. The Operator Burdens process had been previously identified by the resident inspectors (March 2011) and Operations Nuclear Oversight (December 2011) as being ineffective in informing operator decision making and inadequate in identifying, tracking, evaluating and resolving Operator Burdens. On January 11, 2013, PPL staff issued 13-02 Hot Box (Operations Read and Sign),

Operator Aggregate Index, after determining the Operator Aggregate Index and Operator Burdens procedure were ineffective. Prior to the December 19, 2012, Unit 2 reactor scram, PPL's operator aggregate index had identified 5 Operator Work Arounds (OWAs), 4 operator challenges, and 8 control room deficiencies for both Units. The Hot Box investigation on January 11, 2013, yielded a significant increase of 11 OWAs, 21 operator challenges, and 19 control room deficiencies. The inspectors determined while this performance deficiency contributed to valve 3A not being addressed, the most significant cause of this loss of FW event was inadequate CAP implementation, which is addressed in the finding documented in section 5.b.(1).

For the November 9, 2012, Unit 2 scram, the inspectors determined that procedures ON-200-101 and OP-AD-001, provided insufficiently clear procedural guidance for post scram RPV water level band operation and level control when ICS is unavailable. The inspectors determined that these procedures should be revised to enhance the guidance provided to the operators. (CR 1652942)

For the December 16, 2012, Unit 2 scram, the inspectors determined that ON-200-101 provided insufficiently clear procedural guidance for post scram RPV level band control to the operators. The PPL staff revised this procedure to include guidance within the procedural steps on ensuring operators prioritize raising RPV water level post scram to ensure a second scram signal is not received. The inspectors determined that this procedure should be revised to enhance the guidance provided to the operators. (CR 1652942)

(2) Failure to Establish and Implement Written Procedures Prior to Operating Plant Equipment
Introduction.

The inspectors identified a Green NCV of TS 5.4.1, Procedures, for PPL staffs failure to establish and implement a written procedure on December 19, 2012, while operators took actions not described in procedures associated with a previously identified equipment issue with the 3A valve during a Unit 2 reactor startup and power ascension.

Description.

On December 19, 2012, operators were in the process of swapping the A RFP from DPM to FCM with the B RFP in standby. The 2 A RFP 3A valve failed to open as expected during this transition. When the 3A valve failed to open, Shift Supervision directed operators to the 3A valve and its power supply breaker with the intent of de-energizing the breaker locally and then manually opening the 3A valve off its closed seat. This decision making was based, in part, on the August 23, 2011 event (discussed in Section 5). However, the operating crew overlooked the fact that on August 23, 2011 the ICS was in manual operation, vice automatic.

When the operators opened the 3A valve power supply breaker, the ICS system sensed the 3A valve was in the open position and the FW control valves, 41 and 51A, automatically closed as designed, resulting in loss of all normal FW flow to Unit 2.

Operators attempted to take manual control of the B RFP FW 51B valve and to place the B RFP in service in DPM. The 51B valve indicated manual control, but did not respond to operator demands due to unrecognized FW system constraints when the first RFP was selected to FCM. During this time period, RPV water level rapidly lowered, and before operators could take the mode switch to shutdown, an automatic scram occurred on low RPV water level. After the scram, the 3A valve power supply breaker was reclosed, and operators were able to place the A RFP back in DPM to restore RPV level control.

The inspectors determined through operator interviews that PPLs staff had a history of not adequately addressing non-safety related MOV issues, such as suspected valve binding or failure of the valve to open, by de-energizing the valve power supply breaker and then manually opening the valve off its closed seat. Operators stated that PPLs staff routinely conducted these actions on stuck closed MOVs, without an approved or written procedure. During the review of PPL procedures, the inspectors noted the following PPL procedural requirements:

NDAP-QA-0029, Procedure and Work Instruction Use and Adherence, Section 5.1.3, states in part, if an approved document that addresses the circumstances does not exist, then create a procedure per the Procedure Change Process, NDAP-QA-0004, or perform the task using another approved method (i.e. troubleshooting plan, work order). NDAP-QA-0510, Troubleshooting Plant Equipment, Section 5.11, states in part, Troubleshooting Activities - Troubleshooting activities include but are not limited to the following evolutions5.11.13 Repositioning valves or breakers and manual operation of Motor Operated Valves OP-AD-002, Standards for Shift Operations, Section 2.4, states in part, when conducting tasks during all plant operational modes and during transients, operating crews are expected to precisely control plant evolutions in accordance with approved procedures and control plant evolutions effectively by using procedures.

NDAP-QA-1902, Integrated Risk Management, Att. B, Reactivity Manipulations, indicates that work on the FW system and ICS presents a potential reactivity risk because it could possibly affect reactivity. Att. C states to conduct the risk activity according to applicable procedure or instruction.

The inspectors determined that the PPLs staff did not follow these procedural requirements related to the 3A valve manipulations in accordance with approved procedures.

Analysis.

The performance deficiency associated with this issue is that PPLs staff did not follow TS required procedures on December 19, 2012, while attempting to resolve a problem with the operation of the 3A FW valve during Unit 2 reactor startup and power ascension. The issue was evaluated in accordance with IMC 0612 and determined to be more than minor because it was associated with the human performance attribute of the Initiating Events cornerstone and adversely impacted the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Additionally, this finding was similar to example 4.b of IMC 0612, Appendix E, Examples of Minor Issues.

The finding was evaluated using Section B of Exhibit 1 of NRC IMC 0609 Appendix A, User Guidance for Significance Determination for At-Power Situations. Since the performance deficiency caused a reactor shutdown (scram) and the loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition (e.g. loss of condenser, loss of feedwater) a detailed risk evaluation was required. This evaluation used the Susquehanna Station Unit 2 SPAR Model, Revision 8.21. Based upon initial review of the performance deficiency using 0609.04, Initial Characterization for Findings, the Senior Reactor Analyst (SRA) implemented the SPAR Model to conduct a detailed risk assessment. The SRA modeled the performance deficiency using the event assessment methodology and set the Loss of Feed Water Initiating Event to 1.0 and the remaining initiating events to zero. Based upon discussions with the site PRA staff, control room operators do not inhibit the automatic depressurization system on a plant transient, except for anticipated transients without scram (ATWS) events. Accordingly, the basic event for operator manual depressurization (ADS-XHE-XM-MDEPR) was set to FALSE (never fails).

Consequently, the risk associated with this finding was determined to be in the low E-7 range or of very low safety significance (Green). The dominant core damage sequences involve a loss of feedwater with subsequent failure of suppression pool cooling and containment venting, followed by loss of feedwater events with failures to scram (ATWS)related core damage sequences. External event contributions were not significant for this performance deficiency and the overall estimated change in core damage frequency was conservatively high due to the plant transient being initiated at a low reactor power level (18% vice 100% power) following a plant shutdown.

The inspectors determined that this finding had a cross-cutting aspect in the area of Human Performance, Work Control, because PPLs staff did not appropriately plan work activities associated with opening the 3A valve manually by incorporating the need for planned contingencies, compensatory actions and abort criteria consistent with nuclear safety. H.3(a)

Enforcement.

TS 5.4.1.a, Procedures, requires, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in RG 1.33, Revision 2, Appendix A. RG 1.33, Appendix A lists activities that should be covered by written procedures. Section 1 identifies Administrative procedures, among which is 1.d Procedure Adherence and Temporary Change Method. Specifically, PPL procedure NDAP-QA-0029, Procedure and Work Instruction Use and Adherence, Section 5.1.3, states in part, if an approved document that addresses the circumstances does not exist, then create a procedure per the Procedure Change Process, NDAP-QA-0004, or perform the task using another approved method (i.e. troubleshooting plan, work order). Contrary to this, PPLs staff did not establish and implement an approved document or the procedure change process when operators opened the 3A valve power supply breaker. Consequently, when this breaker was opened, the FW control valves automatically closed, resulting in loss of all normal FW and an automatic reactor scram on low RPV water level. Because this finding is of very low safety significance and was entered into PPLs CAP as CR 1668242, it is being treated as an NCV in accordance with the NRCs Enforcement Policy. (NCV 05000388/2013007-02, Failure to Establish and Implement Written Procedures for Operating Plant Equipment)

4. Training and Operator Knowledge

a. Inspection Scope

The inspection team interviewed personnel, reviewed simulator modeling and operator performance, reviewed crew training material and Just-In-Time Training (JITT) material for the initial and subsequent reactor startups, remedial training for the operators involved with the event, and training plans developed after the event on December 19, 2012. The inspection team also reviewed previous ICS related events from November 9, 2012, and December 16, 2012.

b. Findings

/Observations No findings were identified.

The inspection team identified weaknesses in PPLs operator training program, including:

Training lesson plans did not address the logic inputs from the RFP discharge isolation valves to the ICS. PPLs ICS classroom and simulator training for licensed operators and technical plant staff was limited in scope regarding ICS malfunctions and transients (e.g., RFP trip, loss of a single reactor level indicator, loss of a steam instrument). The training did not provide ICS FW startup level control training opportunities with malfunctions such as loss of power to an MOV (e.g., single point vulnerability identified in the ICS design which credited operator manual actions).

Therefore, the operators were not aware through training that a loss of control power to these valves during the transition from DPM to FCM would result in a loss of normal FW (CR 1665479)

Licensed Operator Requalification (LOR) Exam Bank contained limited ICS and FW Malfunctions. For example, the inspectors reviewed the six Job Performance Measures (JPMs) in the LOR Exam bank and noted that the tasks examined included mostly routine FW operations with only one alternate path JPM that tested operator response to an ICS/FW malfunction. The LOR exam simulator scenarios were also reviewed and found to contain limited ICS malfunctions (i.e., a total of three FW/ICS malfunctions). (CR1661759)

JITT conducted for the reactor startup prior to the December 19, 2012 event was not administered to all operators on shift at the time of the event. The inspectors found that only three of the eight control room operators attended the training [the Reactor Operator (RO), the Unit Supervisor (US), the Reactivity Senior Reactor Operator (SRO)]. The inspection team also found that the optional operator training prior to the event did not include any simulator exercises on RFP startup, placing FW in 3 element control and transitioning from DPM to FCM, and FW ICS transients. (CR 1661470 and 1661762)

The inspection team identified potential operator knowledge weaknesses, including:

Operators controlling FW during the December 19, 2012 event did not use the Hard Card (operator aid) properly (see Section 3); and did not attempt to take RFP valve control in manual to reopen both the 41 and 51A valves. (CR 1666244)

During the November 9, 2012 event, the operators did not fully understand: 1) what narrow range level indications were available; and 2) that the narrow/wide range level divergence would increase with time as reactor pressure decreased during plant cool down. (CR1659749)

During the December 16, 2012 event, the operators failed to prioritize the number one method of preventing RPV stratification ahead of the other 5 methods listed in ON-200-101. Also, the operator did not recognize that the Reset Setpoint Setdown button needed to be pressed prior to raising level set-point per OP-245-001.

(CR1659749)

The inspectors concluded that these potential ICS licensed operator training and knowledge weaknesses point to the need for PPLs staff to conduct more in-depth ICS training and testing for both licensed operators and technical plant staff. (CR 1665479)

5. Corrective Action Program (CAP) and Operator Workaround Process Effectiveness

a. Inspection Scope

As part of the SIT Charter, dated January 7, 2012, inspectors were tasked with determining the effectiveness of the CAP with respect to ICS equipment problems since installation of the ICS modification in 2010 on Unit 1 and 2011 on Unit 2. The inspection team interviewed personnel, reviewed various CAP and Operator Burdens procedures, and PPLs staff generated CRs/ARs related to ICS and FW.

b. Findings

/Observations Failure to Implement the CAP

Introduction.

A self-revealing finding (FIN) of very low safety significance (Green) was identified for PPL staffs failure to implement CAP procedure, NDAP-QA-0702, Action Request and Condition Report Process, in response to an identified issue with the FW system.

Description.

On August 23, 2011, PPL operators were in the process of starting up Unit 2. After reaching approximately 18 percent power, operators attempted to place the A RFP in FCM from DPM per procedure OP-245-001, RFP and RFP Lube Oil System.

During this transition to FCM, the 3A valve did not open as expected. After resetting the 3A valve thermal overload relay that was found tripped, operators placed the ICS FW control system in the Manual Valve Control mode. A second attempt to open the 3A valve was also unsuccessful. The Operations staff consulted with the ICS FW Subject Matter Expert (SME) and opened the 3A valve power supply breaker, then manually manipulated the 3A valve off its closed seat. At this point, the 3A valve thermal overload relay was again reset, the breaker was closed and the valve was opened. After operators placed the ICS FW valve controls in the automatic mode, the SME recognized that because of the system design, the FW valve controls needed to be in the Manual Valve Control mode prior to opening the 3A valve power supply breaker in order to prevent ICS from falsely recognizing the 3A valve as being fully opened which would in turn result in a loss of normal FW flow (i.e., automatically closing of the 41 and 51A valves). Although the SME recognized this issue and communicated it to other operators via internal PPL emails, no action request (AR) or condition report (CR) was generated to capture the issue into the CAP. As a result no corrective actions were developed or implemented to ensure the vulnerability was addressed in written procedures.

The inspectors determined that PPLs Action Request and Condition Report Process procedure, NDAP-QA-0702, Section 6.1 states, in part, all PPL personnel have the obligation to initiate an AR for identified or perceived problems, issues, concerns and non-conformances. Based on this procedural requirement, the inspectors determined that contrary to PPL procedure, the system design vulnerability identified on August 23, 2011, concerning the FW valve controls should have been documented in the CAP when it was identified by the SME and operations personnel. This issue went unaddressed until subsequently on December 19, 2012, Unit 2 scrammed on low RPV water level when operators opened the 3A valve power supply breaker with the A RFP FW valve controls in automatic, causing a loss of all normal FW.

Analysis.

The performance deficiency associated is that PPLs staff did not implement their CAP process by initiating a CR in response to identified FW system issues. The issue was evaluated in accordance with IMC 0612 Appendix B, Issue Screening, and determined to be more than minor because it was associated with the human performance attribute of the Mitigating Systems Cornerstone and adversely impacted the objective to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). The finding was evaluated using Section B of Exhibit 1 of NRC IMC 0609, Attachment 0609.04, Initial Characterization of Findings, and Appendix A, User Guidance for Significance Determination for At-Power Situations, and screened as very low safety significance (Green) because the performance deficiency did not result in a loss of safety function or represent an actual loss of function of one or more non-Technical Specification trains of equipment designated as high safety-significant in accordance with the licensees maintenance rule program for greater than 24 hrs.

The inspectors determined that this finding had a cross-cutting aspect in the area of Problem Identification and Resolution, CAP, because PPLs staff did not implement the CAP with a low threshold for identifying issues completely, accurately, and in a timely manner commensurate with their safety significance. Specifically, PPLs staff did not identify non-conforming issues for FW valve control, design and operation that eventually led to a loss of FW and scram of Unit 2 on December 19, 2012. P.1(a)

Enforcement.

This finding does not involve enforcement action since no violation of regulatory requirements was identified. This was because PPLs procedure, NDAP-QA-0702, Action Request and Condition Report Process, is not required to be implemented as part of Susquehannas 10 CFR 50, Appendix B, Quality Assurance Program for systems such as Feedwater, which are not safety-related. The PPL staff has entered the issue into the CAP as CR 1653480. Because this finding does not involve a violation, it is identified as an FIN. (FIN 05000388/2013007-03, Failure to Implement the Corrective Action Process)

The inspectors noted two similar, but minor examples of PPLs staff failing to implement the CAP. Specifically:

On August 25, 2011, two days after the 3A valve did not open upon demand for the first time, Operations generated CR 1455447 and PCWO 1456387 to address the 3A valve issue during the next scheduled or forced outage. The inspectors reviewed the Unit 2 operating history and identified that PPLs staff had multiple opportunities to address the 3A valve issue during outages in June and November of 2012, but did not. On October 18, 2012, operations staff generated CR 1632449 to add the 3A valve work order to the November turbine outage. The PPL staff closed this CR and disapproved the work for the outage because the 3A valve had not exhibited any issues during plant startups earlier in 2012. The inspectors concluded that the PPL staff did not have a sufficient technical basis for concluding the valve was reliable without taking any corrective actions. (CR 1653480)

Following the December 19, 2012 event when Unit 2 scrammed on low RPV reactor water level when operators opened the 3A valve power supply breaker with the A RFP FW valve controls in automatic causing a loss of all FW, PPLs staff conducted troubleshooting activities to determine the cause for an issue with the FW 51B valve failing to open. The PPL staff observed locally that the 51B MOV motor hammering was occurring for 1 to 2 minutes following valve closure. An engineering evaluation of this issue identified that the differential pressure across the closed 51B valve was significantly greater than the design capability of the Limitorque operator for the valve. The evaluation also determined that the Limitorque operator had a self-locking worm gear design that should not have been susceptible to torque switch relaxation and subsequent motor hammering.

Inspectors determined that PPLs staff failed to identify that the 51B MOV motor hammering was a non-conforming condition with the valve's design. The inspectors reviewed PPL staffs actions and found that no MOV diagnostics were performed or scheduled, no grease samples were taken or evaluated, and no specific follow-up actions for the 51B valve were planned. The PPL staff initiated a CR to evaluate the MOV logic change, but did not enter the 51B valve motor hammering issue into the CAP for further evaluation or correction. Because of this, the inspectors determined that this was contrary to NDAP-QA-0702, Section 6.1 states, in part, that all PPLs personnel have the obligation to initiate a CR for identified or perceived problems, issues, concerns and non-conformances, and Section 8.1.1 that states, in part, that if during the course of an evaluation, or within the course of answering a corrective action a new potential issue is identified, a new CR should be implemented. The inspectors determined the failure to initiate a CR for a 51B non-conforming condition was a minor performance deficiency because the valve functions as an isolation valve to the Start-up Level Control Valve and is normally positioned fully open or fully closed. The failure of this valve to open would have been self revealing, and only one train of FW (e.g., only one of the three 51 valves) is required to open to support start-up level control. (CR 1654543)

6. Organizational Response

6.1 Crew Roles and Responsibilities

a. Inspection Scope

The inspection team interviewed personnel, reviewed various procedures and records to assess PPLs personnel crew roles and responsibilities before, during and after the December 19, 2012 event.

b. Findings

/Observations No findings were identified.

During operator interviews, the inspection team identified that:

It was not clear which SRO had given the order to take manual actions to open the 3A valve. The inspectors found that the action to open the 3A valve was discussed between the SROs (i.e., Shift Manager, Unit Supervisor, Reactivity SRO, and General Operating SRO) and ROs assigned to the shift and a consensus was reached that was endorsed by the SM.

The General Operating (GO) SRO position is not currently defined in a PPL procedure. Roles and responsibilities for licensed operators are defined in Conduct of Operations Procedures. The PPL staff has entered this issue into the CAP as CR 1661456.

6.2 Immediate Response and Restart Readiness Assessment

a. Inspection Scope

The inspection team interviewed personnel, reviewed various procedures and records to assess PPL staffs immediate response and restart readiness after the December 19, 2012 event.

b. Findings

/Observations No findings were identified.

The inspection team determined:

PPL staffs evaluation of potential motor hammering during trouble shooting activities to determine the cause for the 51B valve failing to open and the extent of condition for other ICS controlled FW MOVs was inadequate (See Section 5 for the 51B valve inadequate evaluation). Following PPL staffs observation of motor hammering on 51B, PPL staff investigated whether the 3A and HV-20616A1-C1 valves were also subject to motor hammering. With the MOVs in a static condition (e.g., valves had not been recently stroked), local visual observations and motor thermography were performed to determine whether motor hammering was occurring. EWR 1654453 was presented at the Startup Plant Operation Review Committee (PORC) meeting and documented that these valves were found to be "satisfactory with no cycling at the time of investigation."

However, the inspectors determined that based on the short term nature of the hammering condition immediately following valve closure, as observed with the 51B, the field investigation results were inconclusive as to whether the other MOVs were also subject to on-going motor hammering issues. (CR 1654543)

During PPL staffs trouble shooting of the 3A valve, the 3A MOV was re-lubricated prior to performing the valve diagnostic testing. The inspectors determined that such pre-conditioning could mask degraded as-found high friction issues which could have contributed to the failure of the 3A valve to open on December 19, 2012. The PPL staff has entered the issue into the CAP as CR 1654543.

7. Post-Event Root Cause Evaluation and Actions

a. Inspection Scope

The inspection team reviewed PPL staffs Root Cause Analysis (RCA) report for the event to determine whether the causes and associated human performance issues were properly identified. Additionally, the inspection team assessed whether interim and planned long-term corrective actions were appropriate to address the cause(s).

b. Findings

/Observations No findings were identified. The PPL staff identified two root causes and one causal factor in their RCA:

Root Cause-1 (RC1): The decision to open the HV20603A valve breaker was made without a formal evaluation of impacts (knowledge based decision) that reflected a conditioned operator response and inadequate risk evaluation of activities.

Root Cause 2 (RC2): Opportunities were missed to identify and provide compensation for the design of the ICS logic interface when opening the valve breaker.

Causal Factor 1 (CF1): The Operations Burden program (OI-AD-096) did not provide evaluated compensatory actions or drive the correction of the identified issue with the HV20603A valve prior to Dec 2012 event.

The inspectors determined that the RCA was generally thorough and considered RC2, and CF1 reasonable. In addition, the inspectors determined that the associated proposed corrective actions appeared to adequately address the underlying causal factors with the exception of Procedure Use and Adherence (PU&A).

The inspectors concluded that the RC1 was too narrowly focused and did not identify PU&A as a root cause. The RCA concluded the operators were in process (i.e.

complying with procedures). The RCA focused on OP-AD-001, Operations Standards for System and Equipment Operation, which states in step 10.2, Operators shall take manual actions to operate equipment when the auto functions fail. This is mentioned in a number of places in the RCA. There are two other salient points that were not mentioned in the RCA discussion of PU&A: 1) OP-AD-001, step 10.2 is preceded by a caution which states, Personnel injury or further degradation to plant equipment may result from operating equipment in manual that is normally operated in automatic; and 2) OP-AD-001, also states in Section 7.4, Overriding system/equipment controls or interlocks shall not be allowed unless specifically authorized by, or in accordance with, approved procedures. It provides an example as opening circuit breakers. Since the plant had been in a stable condition for almost a half hour on December 19, 2012, prior to the crew opening the breaker for the 3A valve, the inspectors determined there was no urgency for the crew in proceeding in the face of uncertainty. In contrast during a plant transient (i.e., in a situation where it is necessary to implement Off-Normal or Emergency Operating Procedures), it is appropriate for the crew to take timely actions to stabilize the plant (e.g. taking manual control of a malfunctioning automatic system).

NDAP-QA-0029, step 5.14.2, states that if a document cannot be performed as written or there is an unexpected result to place the equipmentin a safe, stable condition and if actions required are outside of the procedure or work instruction, then use approved site processes to maintain configuration control. The inspectors determined that the plant was in a stable condition and therefore it was inappropriate to take manual action to open the breaker without written direction.

The RCA states that due to the significant number of stuck valve issues present at the plant, the operators were somewhat preconditioned to respond to stuck valves in this manner as the normal and accepted approach (i.e., culture at Susquehanna). NDAP-QA-0029 allows shift supervision to provide direction on how to resolve the issue and return to the procedure. However, it does not specify how and with what process this should be done (i.e. switching orders, procedure change, or troubleshooting activity, etc.). As discussed above in section 3.b(2), NRC finding Failure to Establish and Implement Written Procedures Prior to Operating Plant Equipment, there are a number of established station procedures and processes that should have stopped the crew from initiating troubleshooting activities without written guidance.

The inspectors concluded that the staff generating the RCA missed an opportunity to address and reinforce operation staffs PU&A standards. The inspectors noted that PPLs staff issued the Operations Intervention Plan (AR 1665479) on January 28, 2013, which is an effort aimed at strengthening procedure use and adherence standards and changing the cultural environment at the station. In response to the inspectors concern, PPLs staff initiated CR 1668242.

4OA6 Meetings, Including Exit

Exit Meeting Summary

On February 7, 2013, the inspection team discussed the inspection results with Mr.

Timothy S. Rausch, Senior Vice President and Chief Nuclear Officer, PPL Susquehanna and members of his staff. The inspection team confirmed that proprietary information reviewed during the inspection period was returned to PPL.

A-1-1

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

T. Rausch, Senior Vice President and Chief Nuclear Officer
P. Bone, Reactor Operator
L. Crawford, Assistant Operations Manager-Shift
R. Cover - Senior Assessor, Nuclear Oversight
M. Crowthers, Corporate Project Manager
J. Glaser, Senior I&C Engineer
M. Hanchuruck, Licensed Operator Requalification Program Supervisor
J. Hartzell, Supervisor Plant Analysis Program
T. Iliadis, General Manager of Operations
M. Jacopetti, Unit Supervisor, Operations
A. Jardine, Operations Manager
J. Jennings, Supervisor Nuclear Regulatory Affairs
M. Lichtner, Shift Manager, Operations
J. Petilla, Supervisor Nuclear Regulatory Affairs
A. Price, RCA Team Leader
D. Przjemski, Senior Design Engineer
P. Scanlon, Manager Engineering Programs
J. Schleicher, Supervisor Design Engineering
S. Skoras, Senior Risk Assessment Engineer
H. Strahley, Assistant Operations Manager-Training
R. Streeper, Operations Training Manager
J. Tripoli, Manager Nuclear Regulatory Affairs
J. Willis - Unit Supervisor, Operations
B. Yu, Senior Electrical Design Engineer

NRC Personnel

P. Wilson, Deputy Director, Division of Reactor Projects
D. Jackson, Chief Operations Branch, Division of Reactor Safety
M. Gray, Chief Branch 4, Division of Reactor Projects
P. Finney, Senior Resident Inspector - Susquehanna
J. Grieves, Resident Inspector - Susquehanna
A. Rosebrook, Senior Project Engineer, Division of Reactor Projects

A-1-2

SUPPLEMENTAL INFORMATION

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened/Closed:

05000388/2013007-01 NCV Failure to Maintain Adequate Feedwater Procedures (Section 3.b.(1))
05000388/2013007-02 NCV Failure to Establish and Implement Written Procedures for Operating Plant Equipment (Section 3.b.(2))
05000388/2013007-03 FIN Failure to Implement the Corrective Action Process (Section 5.b.(1))

Closed:

None

A-1-3 SUPPLEMENTAL INFORMATION

LIST OF DOCUMENTS REVIEWED