IR 05000354/2018002
| ML18200A301 | |
| Person / Time | |
|---|---|
| Site: | Hope Creek |
| Issue date: | 07/18/2018 |
| From: | Fred Bower NRC Region 1 |
| To: | Sena P PSEG Power |
| References | |
| IR 2018002 | |
| Download: ML18200A301 (21) | |
Text
July 18, 2018
SUBJECT:
HOPE CREEK GENERATING STATION UNIT 1 - INTEGRATED INSPECTION REPORT 05000354/2018002
Dear Mr. Sena:
On June 30, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Hope Creek Generating Station (HCGS). On July 10, 2018, the NRC inspectors discussed the results of this inspection with Mr. Eric Carr, Site Vice President, and other members of your staff.
The results of this inspection are documented in the enclosed report.
NRC inspectors documented one finding of very low safety significance (Green) in this report.
This finding involved a violation of NRC requirements. The NRC is treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.
If you contest the violation or significance of this NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S.
Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I, and the NRC Resident Inspector at HCGS.
In addition, if you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC, 20555-0001; with copies to the Regional Administrator, Region I, and the NRC Resident Inspector at HCGS. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations (10 CFR ) Part 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Fred L. Bower, III, Chief Reactor Projects Branch 3 Division of Reactor Projects
Docket No.:
50-354 License No.: NPF-57
Enclosure:
Inspection Report 05000354/2018002
Inspection Report
Docket Number:
50-354
License Number:
Report Number:
Enterprise Identifier: I-2018-002-0062
Licensee:
Facility:
Hope Creek Generating Station (HCGS)
Location:
Hancocks Bridge, NJ 08038
Inspection Dates:
April 1, 2018 to June 30, 2018
Inspectors:
J. Hawkins, Senior Resident Inspector
S. Haney, Resident Inspector
N. Floyd, Reactor Inspector
J. Furia, Senior Health Physicist
Approved By:
Fred L. Bower, III, Chief
Reactor Projects Branch 3
Division of Reactor Projects
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring PSEGs performance at
Hope Creek Generating Station (HCGS Unit 1 by conducting the baseline inspections described in this report in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
NRC identified and self-revealed findings, violations, and additional items are summarized in the table below.
List of Findings and Violations
Inadequate Instructions for Station Service Water Pump Maintenance Cornerstone Significance Cross-Cutting Aspect Inspection Results Section Reactor Safety -
Mitigating Systems Green NCV 05000354/2018002-01 Open/Closed H.1 - Human Performance -
Resources 71111.22 A self-revealing Green non-cited violation (NCV) of Title 10 of the Code of Federal Reguations (10 CFR) Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, was identified for PSEG providing inadequate written instructions for the performance of maintenance to ensure the station service water (SSW) system remains capable of performing its safety function. Specifically, the PSEG maintenance procedure for SSW pump and motor removal and replacement did not provide adequate instruction to prevent galvanic corrosion when connecting the B SSW pump to its seismic supports, which ultimately resulted in the pump failing its in-service test due to elevated vibration levels on February 18, 2018.
PLANT STATUS
Hope Creek Generating Station (HCGS) began the inspection period at 100 percent power and operated at full power until March 24, 2018, when the unit entered end-of-cycle coastdown operations. On April 12, 2018, operators commenced a shutdown, from 92 percent power, for a planned refueling and maintenance outage (H1R21). Following the completion of refueling and maintenance activities, operators commenced a reactor startup on May 9, 2018. On May 21, 2018, the A reactor feedwater pump tripped during measurement uncertainty recapture (MUR)power ascension testing. This resulted in intermediate runbacks of both reactor recirculation pumps (RRPs) and an unplanned downpower to 70 percent power. Following corrective maintenance and further testing, operators returned the unit to 100 percent power on May 24, 2018. There were no other operational power changes of regulatory significance for the remainder of the inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess PSEG performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Summer Readiness (1 Sample)
The inspectors evaluated summer readiness of offsite and alternate AC power systems.
71111.04 - Equipment Alignment
Partial Walkdown (3 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
- (1) D main steam line and H safety relief valve (SRV) discharge piping on April 25, 2018
- (2) B torus to drywell vacuum breaker on May 1, 2018
- (3) Control rod drive hydraulic control unit accumulators during a reactor manual control system lock up on May 25, 2018
71111.05AQ - Fire Protection Annual/Quarterly
Quarterly Inspection (5 Samples)
The inspectors evaluated fire protection program implementation in the following selected areas:
- (1) High pressure coolant injection (HPCI) battery and associated battery room on April 1, 2018
- (2) Feedwater sealing boundary valve (F032B) area on April 24, 2018
- (3) Drywall pad and torus area on May 2, 2018
- (4) Reactor core isolation cooling (RCIC) system on June 20, 2018
- (5) Refuel floor on June 28, 2018
71111.06 - Flood Protection Measures
Cables (1 Sample)
The inspectors evaluated cable submergence protection in:
- (1) SSW manhole 103 during the week of June 18, 2018
71111.07 - Heat Sink Performance
Heat Sink (2 Samples)
The inspectors evaluated PSEGs monitoring and maintenance of the B1 and B2 safety auxiliaries cooling system heat exchangers performance.
71111.08 - Inservice Inspection Activities
The inspectors evaluated PSEGs non-destructive examination and welding activities at Hope Creek by reviewing the following activities and programs from April 23 to April 27, 2018:
- (1) Volumetric Examinations a) Manual Ultrasonic Testing of residual heat removal (RHR) system pipe-to-elbow weld, 1-BC-20CCA-114-2.
- (2) Surface Examinations a) Magnetic Particle Testing of reactor water clean-up system weld buildup, 1-BG-008-S02-OVERLAY. This review involved welding activities associated with a pressure boundary risk significant system.
- (3) Visual Examinations a) In-vessel Visual Inspection of Jet Pump Components, Top Guide Hold Downs, Core Spray and Feedwater Piping Structural Attachments, and Core Shroud H9 Weld.
b) General Visual Examination of the Drywell and Torus Surfaces.
The inspectors reviewed the welding activities associated with the repair of a degraded elbow on Line 1-BG-008 in the reactor water clean-up system.
71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance
Operator Requalification (1 Sample)
The inspectors observed and evaluated a crew of licensed operators in the plants simulator during licensed operator requalification training that involved an open SRV, high vibration levels on a RRP, a RRP seal leak, and turbine trip on June 5, 2018.
Operator Performance (1 Sample)
The inspectors observed and evaluated a planned down power and shut down for the Hope Creek refueling outage (H1R21) on April 12. The inspectors observed and evaluated start up and power ascension activities from Hope Creek refueling outage (H1R21) on May 9, 2018.
71111.12 - Maintenance Effectiveness
Routine Maintenance Effectiveness (2 Samples)
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
- (1) Neutron monitoring system detector dry tubes found out of position on April 16, 2018
- (2) RHR shutdown cooling suction isolation valve relay failure on April 27, 2018
71111.13 - Maintenance Risk Assessments and Emergent Work Control
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
- (1) Yellow risk condition for shutdown cooling operation on April 13, 2018
- (2) Notification of an unsecured divider plate inside the remote shutdown panel on April 26, 2018
- (3) A fuel pool cooling pump trip on May 8, 2018
- (4) Notification of leading edge flow meter inaccuracy on May 18, 2018
- (5) A reactor feedwater pump trip during measurement uncertainty recapture power ascension testing on May 21, 2018
71111.15 - Operability Determinations and Functionality Assessments
The inspectors evaluated the following operability determinations and functionality assessments:
- (1) B RHR heat exchanger bypass valve excessive leakby on April 11, 2018
- (3) H SRV discharge piping vacuum breaker failure on April 25, 2018
- (4) B torus to drywell vacuum breaker failure to stroke open on May 1, 2018
71111.18 - Plant Modifications
The inspectors evaluated the following permanent modifications:
- (1) Design Change Package 80107709 - Power range neutron monitoring system upgrade
71111.19 - Post Maintenance Testing
The inspectors evaluated post maintenance testing for the following maintenance/repair activities:
- (2) A main steam line outboard main steam isolation valve repairs on April 30, 2018
- (3) RHR shutdown cooling suction isolation valve relay replacement on May 1, 2018
- (4) HPCI system warmup valve (F100) troubleshooting and repairs on May 2, 2018
- (5) Scram discharge volume vent and drain valve troubleshooting and repairs on May 4, 2018
- (6) Reactor core isolation cooling system governor valve repair on May 9, 2018
- (7) MUR troubleshooting and testing on May 16, 2018
71111.20 - Refueling and Other Outage Activities
The inspectors evaluated Hope Creek refueling outage (H1R21) activities from April 12, 2018 through May 11, 2018.
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance tests:
Routine
- (1) HC.OP-ST.BD-0004, RCIC quarterly test on May 10, 2018
- (2) HC.RE-ST.BF-0001, control rod 30-23 scram time testing on June 9, 2018
In-service (3 Samples)
- (1) HC.OP-IS.EA-0002, C SSW pump inservice test on February 18, 2018
- (2) HC.OP-IS.BJ-0001, HPCI system inservice test on June 5, 2018
- (3) HC.OP-IS.BD-0102, RCIC system valves cold shutdown inservice test on June 17, 2018
Containment Isolation Valve (2 Samples)
- (1) HC.OP-LR.AB-0001, A main steam line outboard main steam isolation valve local leak rate testing on April 16, 2018
- (2) HC.OP-LR.FD-0001, HPCI warmup valve leak rate testing on May 1,
RADIATION SAFETY
71124.01 - Radiological Hazard Assessment and Exposure Controls
Radiological Hazards Control and Work Coverage (1 sample)
The inspectors evaluated in-plant radiological conditions and performed independent radiation measurements during facility walkdowns and observation of radiological work activities. The inspectors examined the control of highly activated or contaminated materials stored within the spent fuel pools and the posting and physical controls for selected high radiation areas, locked high radiation areas, and very high radiation areas to verify conformance with the Occupational performance indicator.
Radiation Worker Performance and Radiation Protection Technician Proficiency
(1 sample)
The inspectors evaluated radiation worker performance with respect to radiation protection work requirements. The inspectors evaluated radiation protection technicians in performance of radiation surveys and in providing radiological job coverage.
71124.02 - Occupational As Low As Reasonably Achievable (ALARA) Planning and Controls
Implementation of ALARA and Radiological Work Control (1 sample)
The inspectors reviewed radiological work controls and ALARA practices during the observation of in-plant work activities. The inspectors verified use of shielding, contamination controls, airborne controls, radiation work permit controls, and other work controls were consistent with ALARA plans. The inspectors reviewed the results achieved against the intended ALARA estimates to confirm adequate implementation and oversight of radiological work controls.
OTHER ACTIVITIES - BASELINE
71151 - Performance Indicator Verification
The inspectors verified PSEGs performance indicator submittals listed below.
- (1) Unplanned Scrams per 7000 Critical Hours (April 1, 2017 through March 31, 2018)
- (2) Unplanned Power Changes per 7000 Critical Hours (April 1, 2017 through March 31, 2018)
- (3) Unplanned Scrams with Complications (April 1, 2017 through March 31, 2018)
- (4) Reactor Coolant System Specific Activity (April 1, 2017 through March 31, 2018)
- (5) Reactor Coolant System Leakage (April 1, 2017 through March 31, 2018)
71152 - Problem Identification and Resolution
Semiannual Trend Review (1 Sample)
The inspectors reviewed PSEGs corrective action program for trends that might be indicative of a more significant safety issue.
===71153 - Follow-up of Events and Notices of Enforcement Discretion
Events===
The inspectors evaluated PSEGs response to the following event:
- (1) Trip of the A reactor feed pump and subsequent RRP automatic runback to 70 percent of rated thermal power on May 21, 2018
Personnel Performance (1 Sample)
The inspectors evaluated response during the following non-routine evolutions or transients:
- (1) Conduct of power suppression testing on June 28,
INSPECTION RESULTS
Inadequate Instructions for Station Service Water Pump Maintenance Cornerstone Significance Cross-Cutting Aspect Report Section Reactor Safety - Mitigating Systems
Green NCV 05000354/2018002-01 Open/Closed H.1 - Human Performance - Resources 71111.22 A self-revealing Green NCV of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, was identified for PSEG providing inadequate written instructions for the performance of maintenance to ensure the SSW system remains capable of performing its safety function. Specifically, the PSEG maintenance procedure for SSW pump and motor removal and replacement did not provide adequate instruction to prevent galvanic corrosion when connecting the B SSW pump to its seismic supports, which ultimately resulted in the pump failing its in-service test due to elevated vibration levels on February 18, 2018.
Description:
Hope Creek utilizes a SSW system with four pumps to provide cooling to reactor and safety auxiliaries cooling systems heat exchangers during normal and emergency conditions. The SSW pumps are single stage, vertical pumps that connect to two seismic supports at an upper and lower location along the vertical column of the pump to restrict excessive vertical and lateral displacement during normal operation and any safe shutdown earthquake event.
Each seismic support is fabricated from a carbon steel plate and the pump casing is fabricated from aluminum bronze, which creates a dissimilar metal joint susceptible to galvanic corrosion between the pump and the seismic supports.
On February 18, 2018, while performing the B SSW pump in-service test, operators found vibrations at two motor points to be in the alert range and another in the required action range. Operators declared the pump inoperable and reviewed the pumps recent vibration data, which indicated that the pump vibration levels had been rising over the prior four weeks due to a potential pump misalignment. During the inspection of the pump, large areas of galvanic corrosion were found in the area of the bolting of both the upper and lower seismic supports. The rigid connection between the pump and seismic supports loosened and allowed movement that caused high vibration levels. Upon disassembly and replacement of the upper and lower seismic supports, PSEG identified the upper support flanges did not have the specified neoprene gaskets installed and neither flange had a flange isolation kit installed. This was contrary to drawing C-0106-0, Service Water Intake Structure Wall 102 & 103, that specifies using neoprene gasket material and a flange isolation kit to provide a dielectric barrier to prevent galvanic corrosion between the dissimilar metals of the pump casing and the seismic supports.
PSEG performed a causal evaluation (70198964) that determined that the B SSW pump was installed in October 2015 (30137509) with non-neoprene gasket material and no flange isolation kits. The improper installation resulted from less than adequate procedural guidance for connecting the pump to its seismic supports. Step 5.5.14 of maintenance procedure HC.MD-CM.EA-0001, Service Water Pump & Motor Removal & Replacement, did not provide instructions to install neoprene gaskets or flange isolation kits nor did it inform the technicians of the need to electrically isolate the pump from the seismic support as specified in drawing C-0106-0.
Corrective Actions: PSEGs corrective actions included replacement of the B SSW seismic supports and a revision to procedure HC.MD-CM.EA-0001 to ensure neoprene gaskets and flange isolation kits are installed and guidance to inform the technicians of the need to electrically isolate the pump from the seismic support. In addition, PSEG will perform extent of condition inspections of the seismic support connections for the other three SSW pumps.
Corrective Action Reference: Notification (NOTF) 20788227, 20799145, 20799146
Performance Assessment:
Performance Deficiency: PSEG providing inadequate written instructions for the performance of maintenance to ensure the SSW system remained capable of performing its safety function was a performance deficiency reasonably within PSEGs ability to foresee and correct, and which should have been prevented. Specifically, PSEG maintenance procedure HC.MD-CM.EA-0001 did not provide adequate instruction for installing neoprene gaskets and flange isolation kits in the SSW pump to seismic support connection, and resulted in the B SSW pump failing its in-service test due to elevated vibration levels on February 18, 2018.
Screening: This finding was more than minor in accordance with IMC 0612, Appendix B, Issue Screening, dated January 1, 2018, as it was associated with the Protection Against External Factors attribute (Seismic) of the Mitigating Systems cornerstone and adversely affected its objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage).
Specifically, inadequate maintenance on the SSW pump seismic supports resulted in excessive vertical and lateral displacement during normal operation, inoperability following the pump failing its in-service test, and could have resulted in not performing its safety function following an earthquake.
Significance: The inspectors assessed significance of this condition in accordance with IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated July 1, 2012. The finding screened to be of very low safety significance (Green), when the Exhibit 4, External Events Screening Questions were answered no because the finding would not cause a plant trip or an initiating event, would not degrade two or more trains of a multi-train system or function, would not degrade one or more trains of a system that supports a risk significant system or function, and did not involve the total loss of any safety function.
Cross Cutting Aspect: This finding, in accordance with IMC 0310, Aspects within the Cross-Cutting Areas, dated December 4, 2014, has a cross-cutting aspect in the Human Performance area associated with Resources, in that PSEG did not ensure that personnel, equipment, procedures, and other resources are available and adequate to support nuclear safety. Specifically, design details specified in drawing C-0106-0, Service Water Intake Structure Wall 102 & 103, were not included in maintenance procedure HC.MD-CM.EA-0001, Service Water Pump & Motor Removal & Replacement. (H.1)
Enforcement:
Violation: 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, states, in part, that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings of a type appropriate to the circumstance.
Contrary to the above, since October 2015, PSEGs SSW pump maintenance procedure, an activity affecting quality, was not appropriate to the circumstance. Specifically, procedure HC.MD-CM.EA-0001, Service Water Pump & Motor Removal & Replacement, did not provide instruction for connecting the B service water pump to its seismic support, consistent with the design details specified in drawing C-0106-0, Service Water Intake Structure Wall 102 & 103, which ultimately resulted in the pump failing its in-service test due to elevated vibration levels on February 18, 2018.
Disposition: This violation is being treated as a NCV, consistent with Section 2.3.2.a of the Enforcement Policy.
Observation 71152 Semi-Annual Trend Review The inspectors evaluated a sample of condition reports generated over the course of the past two quarters by departments that provide input to the quarterly trend reports. The inspectors determined that, in most cases, the issues were appropriately evaluated by PSEG staff for potential trends and resolved within the scope of the corrective action program. However, the inspectors noted instances where PSEG was not timely or did not recognize, until prompted by the inspectors that potential adverse trends existed. Examples of this are documented below:
FLEX Equipment Reliability and Preventive Maintenance NRC Inspection Report (IR) finding (FIN)05000354/2018001-01 documented multiple examples of PSEG not following procedures that implemented FLEX equipment preventive maintenance (PM), tracked FLEX equipment unavailability, screened FLEX equipment issues and appropriately addressed these issues in the corrective action program (CAP). During the second quarter of 2018, April 1, through June 30, 2018, the inspectors continued to note FLEX and beyond design basis-related NOTFs that were documented in the CAP, including a FLEX diesel generator failure to start (20796584), FLEX diesel pump excessive battery corrosion and terminal damage (20795300), B.5.b battery replacement PMs never created or performed (20794767), multiple spare FLEX diesel generator PMs not completed (20794005),disconnected FLEX diesel pump batteries (20797758) and identified gaps in maintaining FLEX equipment and unclear roles and responsibilities in FLEX equipment ownership and communication between operations, maintenance and engineering (20791974, 20791977, 20794358, 20798999). On June 3, 2018, the inspectors discussed these NOTFs in CAP concerning FLEX and what appeared to be an adverse trend with FLEX equipment and programs with PSEG. PSEG initiated a common cause evaluation (70201140) to address the inspectors concerns about the potential adverse trend.
Elevated Main Steam SRV Tailpipe Temperatures The inspectors noted that since Hope Creek restarted from the refueling outage on May 10, 2018, seven of the fourteen SRV tailpipe temperatures experienced 30 degree F step increases, which can indicate potential SRV pilot leakage. (H on May 10, K on May 13, D on May 15, E on May 24, P on May 29, B on June 8, F on June 19) After the P tailpipe temperature increased on May 29, the inspectors discussed the potential adverse trend with PSEG. The inspectors also noted that, over the last five operating cycles on average six SRV tailpipe temperatures experienced large temperature increases per cycle. PSEG initiated actions in NOTF 20796507 to address the potential adverse trend. The inspectors also noted that the H SRV tailpipe temperature was elevated prior to the most recent spring 2018 refueling outage and then again during reactor startup. In response, PSEG staff suspected that main seat leakage may be occurring. Based on a preliminary review of tailpipe temperatures changes during a planned down power in June 2018, PSEG concluded that the H and K SRV tailpipe temperatures likely exhibited signs of SRV main seat leakage. PSEG engineering continues to review the SRV tailpipe temperatures and pressure trends for all fourteen SRVs.
The inspectors considered that the increase in documented NOTFs concerning FLEX and elevated SRV tailpipe temperatures since January 1, 2018, represented inspector identified emerging trends. These examples also represented missed opportunities to effectively use all of the tools available in the CAP, including PSEGs trending procedure, LS-AA-125-1005, which discusses the generation of notifications and the routine conduct of cognitive trend analyses.
The inspectors evaluated all of the issues above in accordance with the guidance in IMC 0612, Appendix B, Issue Screening, and Appendix E, Examples of Minor Issues, and determined the issues were of minor significance because the inspectors did not identify any CAQ that were not appropriately corrected or scheduled for correction in a reasonable period of time as a result of the failure to implement the NOTF screening process appropriately.
Consequently, these issues were not subject to enforcement action in accordance with the NRCs enforcement policy.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On April 27, 2018, the inspectors presented the inservice inspection results to Mr. Eric Carr, Site Vice President, and other members of the PSEG staff.
- On May 4, 2018, the inspectors presented the radiation safety inspection results to Mr. Eric Carr, Site Vice President, and other members of the PSEG staff.
- On July 10, 2018, the inspector presented the quarterly resident inspector inspection results to Mr. Eric Carr, Site Vice President, and other members of the PSEG staff.
THIRD PARTY REVIEWS
Inspectors reviewed Institute on Nuclear Power Reactor reports that were issued during the inspection period.
DOCUMENTS REVIEWED
- Indicates NRC-identified
Section 1R01: Adverse Weather Protection
Procedures
HC.OP-AB.BOP-0004, Grid Disturances, Revision 25
HC.OP-GP.ZZ-0003, Station Preparations for Winter Conditions, Revision 31
OP-AA-108-107-1002, Salem and Hope Creek 500 kV Switchyard Operations Interface
Procedure, Revision 2
OP-AA-108-111-1001, Severe Weather and Natural Diaster Guidelines, Revision 15
WC-AA-107, Seasonal Readiness, Revision 25
Drawings
601701, 500, 13.8, 4 kV Elementary One Line, Revision 38
Notifications
20791678
20796541
Section 1R04: Equipment Alignment
Procedures
HC.MD-ST.AB-0003, SRV Discharge Piping Vacuum Breaker In-place Set-point Testing,
Revision 2
HC.OP-AB.IC-0001, Control Rod, Revision 16
HC.OP-AR.ZZ-0011, Overhead Annunciator Window Box C6, Revision 64
HC.OP-DL.ZZ-0026, Surveillance Log, Revision 160
HC.OP-ST.BF-0002, Control Rod Drive Accumulator Operability Check - Weekly, Revision 10
HC.OP-ST.GS-0004, Suppression Chamber / Drywell Vacuum Breaker Operability Test,
Revision 15
Notifications
20772157
20785190
20792630
20792837
20793061
20793259
20794633
20795520
Maintenance Orders/Work Orders
50150123
60138982
70198465
70199676
80122059
Miscellaneous
PM141Q-0113, VTD - Crosby Instruction Manual, Revision 15
Section 1R05: Fire Protection
Procedures
FRH-II-415, Hope Creek Pre-Fire Plan (HC PFP) - Drywell Pad and Torus Area, Revision 4
FRH-II-435, Hope Creek Pre-Fire Plan (HC PFP) - Steam Tunnel, RCIC, HPCI, Pipe Chases,
CRD Removal and Repair Areas, Revision 4
FRH-II-412, Hope Creek Pre-Fire Plan (HC PFP) - RCIC Pump and Turbine, RHR pump and
Heat Exchanger and Electrical Equipment Rooms, Revision 3
HC.OP-IS.BD-0101, RCIC Valves - In-service Test, Revision 64
HC.OP-IS.BD-0102, RCIC Valves - Cold Shutdown In-service Test, Revision 20
Notifications
20799450*
20791133
20791894
20798025
Maintenance Orders/Work Orders
202595
Section 1R06: Flood Protection Measures
Procedures
HC.CH-SO.LE-0002, Operation of the Station Service Water Cable Vault Dewatering System,
Revision 2
HC.MD-PM.ZZ-0022, SSW Electrical Manhole Water Inspection, Revision 3
Notifications
20777641
20782016
20790562
Maintenance Orders/Work Orders
212219
212716
269939
Section 1R07: Heat Sink Performance
Procedures
ER-AA-340-1002, Service Water Heat Exchanger and Component Inspection Guide, Revision 7
Notifications
20789918
20792010
20792186
20792210
20792551
Maintenance Orders/Work Orders
228940
228941
Section 1R08: In-service Inspection Activities
Procedures
54-ISI-363, Remote Underwater In-Vessel Visual Inspection of Reactor Pressure Vessel
Internals, Components, and Associated Repairs in Boiling Water Reactors, Revision 008
54-ISI-836, PDI Generic Procedure for the Ultrasonic Examination of Austenitic Piping Welds
PDI-UT-2, Revision 017
ER-AA-330, Conduct of Inservice Inspection Activities, Revision 11
NWP-13, Welding Procedure Specification for P1 to P1 Manual GTAW and SMAW Welds,
Revision 1
Notifications
20792495
20792926*
20793129*
Maintenance Orders/Work Orders
60138458
Miscellaneous
ISI-HC-LTP4-PLAN, Hope Creek Inservice Inspection Program Plan Fourth Ten-Year Inspection
Interval, Revision 0
Surface Examination Report for HC-1-BG-008-S02-OVERLAY, dated April 26, 2018
Ultrasonic Thickness Report for HC-1-BG-008-S02-OVERLAY, dated April 26, 2018
UT-18-011, UT Examination Report for 1-BC-20CCA-114-2 (Summary No. 1090005), dated
April 23, 2018
VEN-18-002 through -012, Visual Examination Reports for Drywell and Torus Accessible
Surfaces, dated April 27, 2018
WHR 80127, Weld History Record for HC-1-BG-008-S02-OVERLAY (WO# 60138458), dated
April 26, 2018
Section 1R11: Licensed Operator Requalification Program
Procedures
HC.RE-IO.ZZ-0001(Q), Core Operations Guidelines, Revision 53
HC.OP-IO.ZZ-0004, Shutdown From Rated Power to Cold Shutdown, Revision 104
HC.OP-IO.ZZ-0005, Cold Shutdown to Refueling, Revision 40
HC.OP-IO.ZZ-0006(Q), Power Changes During Operation, Revision 60
Miscellaneous
Reactivity Maneuver Plan 2018-0042, April 2018 - Shutdown to RF21, Revision 0
SG-780, Open SRV/ Recirc Vibes/ RRP Seal Leak/ Turbine Trip, dated May 17, 2018
Section 1R12: Maintenance Effectiveness
Procedures
ER-AA-310-1004, Maintenance Rule Performance Monitoring, Revision 14
HC.ER-PS.BB-0506, Lower Plenum Inspection Bases Document, Revision 1
HC.OP-GP.SM-0001, Defeating Isolation Signals During Refueling Operations, Revision 13
Notifications
20792044
20793971
20795835
Maintenance Orders/Work Orders
60135038
200179
200543
Miscellaneous
VTD 324351, Universal Dry Tube dated May 23, 2000
Section 1R13: Maintenance Risk Assessments and Emergent Work Control
Procedures
HC.OP-AB.COOL-0004, Fuel Pool Cooling, Revision 9
HC.OP-FT.ZZ-0006, Measurement Uncertainty Recapture Implementation & Power Ascension
Testing, Revision 0
HC.OP-IO.ZZ-0006, Power Changes During Operation, Revision 61
OP-AA-106-101, Significant Event Reporting, Revision 11
OP-AA-300, Reactivity Management, Revision 7
Notifications
20794031
20794304
20794685
20794713
20795468
20795469
20795822
Maintenance Orders/Work Orders
80116312
Miscellaneous
Section 1R15: Operability Determinations and Functionality Assessments
Procedures
HC.MD-ST.AB-0003, SRV Discharge Piping Vacuum Breaker In-place Set-point Testing,
Revision 2
HC.OP-ST.GS-0004, Suppression Chamber / Drywell Vacuum Breaker Operability Test,
Revision 15
SM.MD-GP.ZZ-0100, Lisega Snubber Rebuild Disassembly/Reassembly, Revision 1
SH.RA-ST.ZZ-0105, Snubber Examination and Testing, Revision 10
Notifications
20796237*
20751497
20772157
20785190
20791653
20792226
20792226
20792437
20792437
20792544
20792630
20792744
20792837
20793061
20793259
Maintenance Orders/Work Orders
50141732
50150123
50189841
203003
60138457
70191406
70198465
70199676
200251
200251
80113942
80122059
80122059
80122059
Miscellaneous
PM141Q-0113, VTD - Crosby Instruction Manual, Revision 15
Section 1R18: Plant Modifications
Procedures
VCC-AA-100, Standard Design Process, IP-ENG-001, Revision 0
Notifications
20790205
20792023
20793136
20793216
20793318
20793434
20793453
20794633
20794299
20794775
20795520
Maintenance Orders/Work Orders
60131640
80107709
Section 1R19: Post-Maintenance Testing
Procedures
HC.OP-FT.ZZ-0006, MUR Power Ascension Testing, Revision 0
HC.OP-LR.FD-0001, Containment Isolation Valve Type C Leak Rate Test 1FDHV-F002,
Revision 4
HC.OP-ST.BD-0004, RCIC System Response Time and Flow test - 18 Months, Revision 9
HC.OP-ST.BF-0006, SDV Vent and Drain Functional Test, Revision 5
HC.RE-CP.ZZ-0003, CRIDS Plant Process Computer Point Process, Revision 11
SM.MD-GP.ZZ-0100, Lisega Snubber Rebuild Disassembly/Reassembly, Revision 1
Notifications
20798788*
20751497
20777859
20787455
20790335
20791218
20791653
20791702
20791825
20791941
20792125
20792226
20792437
20792544
20792744
20793095
20793327
20793354
20793514
20793547
20793934
20794685
20794713
20794718
20797558
Maintenance Orders/Work Orders
30304771
50189841
50190280
203003
203292
60106987
60131857
60138457
60138464
60138464
60138572
60138628
70191406
200118
200144
200239
200251
201260
80113942
80122046
80122059
Miscellaneous
PN0-A61-4050-0026, Electrical Equipment Separation for Safeguards System, Revision 5
Section 1R20: Refueling and Other Outage Activities
Procedures
HC.OP-IO.ZZ-0009, Refueling Operations, Revision 39
OP-HC-300-2020, Review of Reactore Core Performance Information, Revision 2
Notifications
20789606
20790052
20790180
20790253
20790254
20790257
20791213
20791215
20791216
20791217
20791268
20791283
20791284
20791310
20791318
20791380
20791652
20791653
20791702
20791703
20791704
20791705
20791706
20791707
20791710
20791718
20791719
20791767
20791793
20791795
20791812
20791820
20791825
20791864
20791879
20791894
20791901
20791912
20791917
20791948
20791949
20791950
20791954
20791959
20791970
20791979
20791987
20791988
20791990
20791996
20792044
20792049
20792088
20792091
20792099
20792102
20792103
20792105
20792131
20792141
20792146
20792158
20792180
20792299
20792436
20792450
20792508
20792464
20792539
20792633
20792641
20792642
20792658
20792659
20792678
20792685
20792700
20792796
20792811
20792827
20792828
20792829
20792830
20792923
20792932
20792950
20793027
20793043
20793051
20793056
20793057
20793058
20793061
20793101
20793166
20793178
20793294
20793299
20793302
20793307
20793322
20793422
20793806
20793890
20793891
20794131
20794237
20794245
20794369
20794370
20794371
20794372
20794373
20794932
Miscellaneous
NFS18-025, Hope Creek Cycle 22 Core Loading Plan, Revision 0
Section 1R22: Surveillance Testing
Procedures
HC.MD-PM.FD-0001,
HC.OP-IS.BD-0102, RCIC System Valves - Cold Shutdown - In-service Test, Revision 20
HC.OP-IS.BJ-0001, HPCI Main and Booster Pump Set - 0P204 and 0P217 - In-service test,
Revision 65
HC.OP-LR.AB-0001, Containment Isolation Valve Type C Leak Rate Test 1ABHV-F022A and
1ABHV-F028A, Penetration PIA: A Main Steam Line, Revision 7
HC.OP-LR.FD-0001, Containment Isolation Valve Type C Leak Rate Test 1FDHV-F002,
Revision 4
HC.OP-ST.BD-0004, RCIC System Response Time and Flow test - 18 Months, Revision 9
HC.RE-ST.BF-0001, Control Rod Scram Time Surveillance, Revision 36
HC.RE-ST.BF-0001, Control Rod Scram Time Surveillance, Revision 37
Drawings
C-0106-0, Service Water Intake Structure Wall 102 & 103, Revision 12
Notifications
20745655
20790335
20791702
20791825
20791941
20791941
20792125
20792125
20793354
20793514
20793547
20794386
20794718
20798025
20798810
Maintenance Orders/Work Orders
30304771
30323025
50190280
50190280
202595
60106987
60131857
60138464
60138464
60138628
70189240
70198964
200128
200144
200239
80122046
80122346
Section 4OA2: Problem Identification and Resolution
Notifications
20783115
20787557
20792933
20794091
20794131
20794632
20795300
20795388
20795729
20796311
20796919
20797481
Maintenance Orders/Work Orders
70199841
200929
Miscellaneous
SC Standing Order 2018-22, Exiting FLEX/SAWA TSASs dated June 13, 2018
Section 4OA3: Follow-up of Events and Notices of Enforcement Discretion
Notifications
20793302*
20776639
20791894
20792700
20794411
20794413
20794522
20795822
Maintenance Orders/Work Orders
50190467
200128
200206
Procedures
NF-AB-431, Power Suppression Testing, Revision 6
HC.OP-FT.ZZ-0006
HC.OP-LR.AE-0003
HC.OP-SO.AE-0001
OP-HC-108-102, Management of Operations with the Potential to Drain the Reactor Vessel
(OPDRV), Revision 5
OP-HC-108-110-1001
Miscellaneous
Calculation BD-0020, RCIC Jockey Pump System Capabilities, Revision 0
Hope Creek Narrative Logs dated May 21, 2018