IR 05000346/2002017

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IR 05000346-02-017, Firstenergy Nuclear Operating Company, on 10/01-11/14/2002, Davis-Besse Nuclear Power Station, Identification and Resolution of Problems, Other Activities
ML023430380
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 12/09/2002
From: Grobe J
NRC/RGN-III
To: Myers L
FirstEnergy Nuclear Operating Co
References
IR-02-017
Download: ML023430380 (30)


Text

December 9, 2002

SUBJECT:

DAVIS-BESSE NUCLEAR POWER STATION NRC INTEGRATED INSPECTION REPORT 50-346/02-17

Dear Mr. Myers:

On November 14, 2002, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Davis-Besse Nuclear Power Station. The enclosed report documents the inspection findings which were discussed on November 14, 2002, with you and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. For the entire inspection period, the Davis-Besse Nuclear Power Station was under the Inspection Manual Chapter 0350 Process. The Davis-Besse Oversight Panel assessed inspection findings and other performance data to determine the required level and focus of followup inspection activities and any other appropriate regulatory actions. Even though the Reactor Oversight Process had been suspended at the Davis-Besse Nuclear Power Station, it was used as guidance for inspection activities and to assess findings.

Based on the results of this inspection, the NRC has determined that there were two findings of very low safety significance (green) identified in the report.

In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html(the Public Electronic Reading Room).

Sincerely,

/RA by C.Lipa Acting for/

John A. Grobe, Chairman Davis-Besse Oversight Panel Docket No. 50-346 License No. NPF-3

Enclosure:

Inspection Report 50-346/02-17

REGION III==

Docket No:

50-346 License No:

NPF-3 Report No:

50-346/02-17 Licensee:

FirstEnergy Nuclear Operating Company Facility:

Davis-Besse Nuclear Power Station Location:

5501 North State Route 2 Oak Harbor, OH 43449-9760 Dates:

October 1, 2002, through November 14, 2002 Inspectors:

S. Thomas, Senior Resident Inspector D. Simpkins, Resident Inspector R. Powell, Senior Resident Inspector (Perry Station)

J. Jacobson, Reactor Inspector, DRS M. Holmberg, Reactor Inspector, DRS Approved by:

Christine A. Lipa, Chief Branch 4 Division of Reactor Projects

SUMMARY OF FINDINGS

IR 05000346-02-17, FirstEnergy Nuclear Operating Company, on 10/01-11/14/2002,

Davis-Besse Nuclear Power Station. Identification and Resolution of Problems, Other Activities.

This report covers a seven week period of baseline resident inspection. The inspection was conducted by resident and Region III inspectors. Two findings of very low safety significance (Green) were identified during this inspection. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609 Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A.

Inspection Findings

Cornerstone: N/A

Green.

The inspectors observed a licensee employee warning two other licensee employees about the presence of NRC inspectors. This was a licensee performance deficiency in that 10 CFR 50.70(b)(4) requires, in part, that the arrival and presence of the NRC inspector is not announced or otherwise communicated by its employees or contractors to other persons at the facility unless specifically requested by the NRC inspector.

This was considered a finding of more than minor safety significance because if left uncorrected, it would become a more significant safety concern in that the NRC's ability to carry out its statutory mission would be impeded. The inspectors determined that this issue was not a violation of 10 CFR 50.70(b)(4) because the warning by the licensee employee was not widespread nor a significant intentional violation of the rule per the 10 CFR Part 50 Statement of Considerations. The inspectors concluded that this was a finding was of very low safety significance (Green) that was not suited for analysis by the significance determination process. (Section 4OA5.2)

Cornerstone: Mitigating Systems

Green.

The inspectors identified numerous examples of the improper implementation of the licensees corrective action program, in regards to evaluating and taking corrective actions for potentially reportable issues associated with the containment air coolers.

This was a performance deficiency.

This was considered a finding of more than minor safety significance because if left uncorrected it would become a more significant safety concern in that it could adversely impact the NRC in its effort to identify and resolve issues important to public safety.

The inspectors determined that the issue was not a violation of regulatory requirements because formal operability and reportability evaluations had not yet been completed.

(Section 4OA2.2)

B.

Licensee Identified Findings A violation of very low safety significance which was identified by the licensee has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. This violation and the corrective action tracking number are listed in Section 4OA7 of this report.

REPORT DETAILS

Summary of Plant Status

The plant was shutdown on February 16, 2002 for a refueling outage. During scheduled inspections of the control rod drive mechanism nozzles, significant degradation of the reactor vessel head was discovered. As a direct result of the need to resolve many issues surrounding the Davis-Besse reactor vessel head degradation, NRC management decided to implement Inspection Manual Chapter 0350, Oversight of Operating Reactor Facilities in a Shutdown Condition With Performance Problems. The fuel was removed from the reactor on June 26, 2002, and the plant remained shut down. For the entire inspection period, the Davis-Besse Nuclear Power Station was under the Inspection Manual Chapter 0350 Process. As part of this Process, several additional team inspections were conducted. The subjects of these inspections included; Reactor Head Replacement, Containment Health/Extent of Condition, System Health Assurance, Management and Human Performance, and Program Compliance.

The status of these inspections will not be included as part of this inspection report, but upon completion, each will be documented in a separate inspection report which will be made publically available on the NRC website.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity.

1RO1 Adverse Weather Protection (71111.01)

a. Inspection Scope

The inspectors reviewed relevant procedures and performed specific plant walkdowns to verify that safety-related plant equipment was protected from seasonal-related risks.

Additionally, where applicable, compensatory actions were also evaluated to be present and effective. The issues evaluated included:

  • Heat trace and freeze protection system degradation and aging; and

As well as focusing on specific safety related systems, the inspectors evaluated the broader potential impact of these issues on numerous safety related systems.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

a. Inspection Scope

The inspectors verified equipment alignment and identified any discrepancies that impacted the function of the system and potential increased risk. The inspectors also verified that the licensee had properly identified and resolved any equipment alignment problems that would cause initiating events or impact the availability and functional capability of this mitigating system. Specific aspects of this inspection included reviewing plant procedures, drawings, and the Updated Safety Analysis Report (USAR),to determine the correct system lineup and evaluating any outstanding maintenance work requests on the system or any deficiencies that would affect the ability of the system to perform its function. A majority of the inspectors time was spent performing a walkdown inspection of the system. Key aspects of the walkdown inspection included:

  • valves were correctly positioned and do not exhibit leakage that would impact their function;
  • electrical power was available as required;
  • major system components were correctly labeled, lubricated, cooled, ventilated, etc;
  • hangers and supports were correctly installed and functional;
  • essential support systems were operational;
  • ancillary equipment or debris does not interfere with system performance;
  • tagging clearances were appropriate; and
  • valves were locked as required by the licensees locked valve program.

During the walkdown, the inspectors also observed the material condition of the equipment to verify that there were no significant conditions not already in the licensees work control system. The inspectors performed a walkdown of the following system:

  • spent fuel pool cooling system.

b. Findings

No findings of significance were identified.

==1R05 Fire Protection

==

.1 Fire Protection Walkdowns of Risk Significant Plant Areas

a. Inspection Scope

The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of fire fighting equipment, the control of transient combustibles, and on the condition and operating status of installed fire barriers. The inspectors selected fire areas for inspection based on their overall contribution to internal fire risk, as documented in the Individual Plant Examination of External Events (IPEEE), their potential to impact equipment which could initiate a plant transient, or their impact on the plants ability to respond to a security event. Using the documents listed at the end of this report, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use, that fire detectors and sprinklers were unobstructed, that transient material loading was within the analyzed limits, and that fire doors, dampers, and penetration seals appeared to be in satisfactory condition.

The following areas or components were inspected:

  • battery room 1.

b. Findings

No findings of significance were identified.

.2 Plant Fire Drill Observation

a. Inspection Scope

The inspectors observed a fire brigade drill performed in an area important to plant safety. Specific fire brigade performance attributes verified by the inspectors included:

  • the fire brigade turnout gear was properly donned;
  • the fire area of concern was entered in a controlled manner;
  • sufficient fire fighting equipment was brought to the scene by the fire brigade;
  • the fire brigade leaders fire fighting directions were clear and effective;
  • radio communication between the fire brigade leader and the control room was efficient and effective;
  • fire fighting pre-plan strategies were utilized; and
  • the licensees pre-planned drill scenario was followed and the drill objective acceptance criteria were met.

b. Findings

No findings of significance were identified.

1R08 Inservice Inspection Activities

a. Inspection Scope

The inspectors evaluated the implementation of the licensees inservice inspection program for monitoring degradation of the reactor coolant system boundary and risk significant piping system boundaries, based on review of records and in-process observation of nondestructive examinations. From February 20, 2002 through March 6, 2002, and September 30, 2002 through October 3, 2002, the inspectors performed the following activities:



Observed acquisition and evaluation of eddy current data on the steam generators;



Observed steam generator tube plugging and plug removal;



Observed in-situ pressure test of tube 151-4 on steam generator A;



Observed dye penetrant and ultrasonic examination of 10 inch pipe to elbow weld DH-33B-CCB-6-7-SWB;



Reviewed repair and replacement records required by the American Society of Mechanical Engineers (ASME) Code for the following components:



Work Order 99-005601-00 Containment Spray Pump 1-1



Work Order 99-4337-008 Decay Heat Low Pressure Injection



Reviewed UT examination reports and evaluations for a linear indication identified in the main steam line atmospheric vent line weld MS 3A-EEB-1-30-FW-15a; and

  • Reviewed Steam Generator Condition Monitoring Results and Operational Assessments for Cycles 12 and 13.

The records reviewed and activities observed were evaluated for conformance with requirements in the ASME Code,Section III, Section V,Section IX, and Section XI.

The inspectors also reviewed a sample of inservice inspection related problems documented in the licensees corrective action program, to assess conformance with 10 CFR Part 50 Appendix B, Criterion XVI Corrective Action requirements.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed the licensee's implementation of the maintenance rule requirements to verify that component and equipment failures were identified and scoped within the maintenance rule and that select structures, systems and components were properly categorized and classified as (a)(1) or (a)(2) in accordance with 10 CFR 50.65. Specifically, the inspectors reviewed equipment issues and performance problems associated with the doors and hatches providing separation of essential trains for flooding, high energy line breaks, and negative and positive pressure conditions to verify the doors and hatches were properly scoped in accordance with the Maintenance Rule, whether failures were properly characterized, and whether performance criteria were appropriate.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessment and Emergent Work Evaluation

a. Inspection Scope

The inspectors reviewed the licensees management of plant risk during the implementation of the main generator relaying protection upgrade (Modification 90-0002). This activity was chosen based on its potential impact on increasing the probability of an initiating event or impacting the operation of safety significant equipment. The inspection was conducted to verify that evaluation, planning, control, and performance of the work were done in a manner to reduce the risk and minimize the duration where practical, and that contingency plans were in place where appropriate. The licensees daily configuration risk assessments, observations of shift turnover meetings, observations of daily plant status meetings, and the documents listed at the end of this report were used by the inspectors to verify that the equipment configurations had been properly listed, that protected equipment had been identified and was being controlled where appropriate, and that significant aspects of plant risk were being communicated to the necessary personnel.

b. Findings

No findings of significance were identified.

1R14 Personnel Performance During Nonroutine Plant Evolutions

a. Inspection Scope

On November 2, 2002, the inspectors completed their review of licensee personnel performance during a drain of the reactor coolant system. The inspectors compared operator performance to the applicable procedures, reviewed plant data and observed radiation and work control pre-job briefs.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors selected condition reports (CRs) which discussed potential operability issues for risk significant components or systems. These CRs were evaluated to determine whether the operability of the components or systems was justified. The inspectors compared the operability and design criteria in the appropriate sections of the Technical Specifications and USAR to the licensees evaluations presented on the issues listed below to verify that the components or systems were operable. Where compensatory measures were necessary to maintain operability, the inspectors verified by review of the documents listed at the end of the report that the measures were in place, would work as intended, and were properly controlled.

The issues evaluated were:

  • station blackout diesel generator cylinder exhaust temperatures low; and

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed post-maintenance testing activities associated with maintenance on important mitigating and support systems to ensure that the testing adequately verified system operability and functional capability with consideration of the actual maintenance performed. The inspectors used the appropriate sections of Technical Specifications and the USAR, as well as the documents listed at the end of this report, to evaluate the scope of the maintenance and verify that the post-maintenance testing performed adequately demonstrated that the maintenance was successful and that operability was restored. In addition, the inspectors reviewed CRs to verify that any minor deficiencies identified during these inspections were entered into the licensees corrective action system. The inspectors observed and evaluated test activities associated with the following:

  • decay heat valve 14A and 14B flow balancing;
  • station air compressor 2 motor repair; and
  • station blackout diesel generator, post outage.

b. Findings

No findings of significance were identified

1R22 Surveillance Testing

a. Inspection Scope

The inspectors witnessed the surveillance test and test data to verify that the equipment tested met Technical Specifications, USAR, and licensee procedural requirements, and also demonstrated that the equipment was capable of performing its intended safety functions. The activity was selected based on its importance in verifying mitigating system capability. The inspectors used the documents listed at the end of this report to verify that the test met the TS frequency requirements; that the test was conducted in accordance with the procedures, including establishing the proper plant conditions and prerequisites; that the test acceptance criteria were met; and that the results of the test were properly reviewed and recorded.

The following test was observed and evaluated:

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES (OA)

4OA1 Performance Indicator (PI) Verification

a. Inspection Scope

The inspectors reviewed the reported data for the following Performance Indicators:

  • Safety System Functional Failures (January 1 to September 30, 2002);

The inspectors used the definitions and guidance contained in Nuclear Energy Institute 99-02, Regulatory Assessment Indicator Guideline, Revision 2. The inspectors reviewed station logs, event notification reports, engineering logs, licensee event reports, condition reports, and chemistry data to verify the accuracy of the licensees data submission. Additionally, the inspectors reviewed revised reporting methodology developed in response to inspector identified concerns addressed by CR 02-7462, HPI System NRC Performance Indicator Desk Top Guide Inaccuracy in Unavailability.

a. Findings

No findings of significance were identified.

4OA2 Routine Review of Identification and Resolution of Problems

.1 Licensee Resolution of Condition Reports Containing Mode Restraints

a. Inspection Scope

The inspectors began to review the licensees process of resolving issues that had been placed into their corrective action program and had also been assigned a restraint for resolution prior to entering a specific operational Mode. The inspectors obtained a listing, dated November 5, 2002, of open condition reports with assigned mode restraints. This list contained approximately:

  • 15 Mode 1 restraints;
  • 42 Mode 2 restraints;
  • 168 Mode 3 restraints;
  • 541 Mode 4 restraints;
  • 111 Mode 5 restraints; and
  • 168 Mode 6 restraints.

Included as part of the corrective action to close out the condition reports that contained Mode restraints were attachments that specifically stated the corrective action taken to lift the Mode restraint. The inspectors evaluated a sampling of condition reports which contained completed corrective actions for restraints assigned to Mode 6.

b. Findings

No findings of significance were identified.

.2 Inadequate Implementation of the Corrective Action Process Which Led to Not

Identifying a Potentially Reportable Issue a.

Introduction The inspectors identified a Green finding when the licensee failed to properly implement the corrective action program for a potential operability issue involving all three of the containment air coolers.

b.

Description As part of their routine evaluation of condition reports, the inspectors engaged the licensee regulatory affairs staff regarding condition reports which documented evaluation of past operability issues and that had the potential to be reportable under the guidelines of 10 CFR 50.73. The inspectors inquired about how the issues documented in CR 02-2943, Containment Air Cooler Boric Acid Corrosion, had been resolved. This condition report, which identified potential seismic issues with all three containment air cooler support frames, rolled a large number of condition reports into one and included numerous corrective actions. This condition report was not identified as a potentially reportable issue and the regulatory affairs staff was unaware of this issue or that it was potentially a reportable issue under 50.73. Further evaluation revealed that, despite the fact that this condition report was classified as a significant condition adverse to quality and clearly states that the system has been declared inoperable, a number of additional issues were identified by the inspector during the review of condition report.

  • The operations staff did not check the block that would have required a formal operability evaluation be performed NOP-LP-2001, Condition Report Process, step 4.2.6.2, provided instruction that the SRO shall determine if an evaluation from a designated organization(s) is required to support your determination of operability or functionality. The originator of this condition report clearly stated that the system [containment air coolers] had been declared inoperable, but there was no information regarding why. Since each condition report must be treated as a stand alone document, there was insufficient basis documented in the condition report which justified the SROs decision to not request a formal operability evaluation.
  • The operations staff did not check the block that would have required a formal reportability evaluation be performed NOP-LP-2001, Condition Report Process, step 4.2.6.5, provided instruction that the SRO shall determine if the condition is reportable and if additional reportability review evaluation is required or needed. Additionally, the Programmatic Guideline for the Davis-Besse Condition Reporting Process, step 4.2.7.5, in part, stated for reportable events at Davis-Besse, the only events that are considered reportable by operations are those specified in DB-OP-00002 (Operations Section Event/Incident Notifications and Actions), and those reportable by Regulatory Affairs in accordance with 10 CFR 50.73. The originator of this condition report clearly stated that the system [containment air coolers] had been declared inoperable, but there was no information regarding why it was inoperable or how long it had been in that condition. Since the extent of the condition was unknown and the potential that this condition existed during operational modes when the containment air coolers were required, a formal reportability evaluation was required to be performed to address those questions.
  • The regulatory affairs staff review of the condition report missed the fact that this issue had the potential to be reportable The Programmatic Guideline for the Davis-Besse Condition Reporting Process, step 4.5.1, in part, stated designated Regulatory Affairs personnel shall review all condition reports to determine reportability. The potential reportability of this issue was not identified by the licensees Regulatory Affairs staff.
  • The regulatory affairs staff checked the reportable block no prior to completion of the operability checks for each the three containment air cooler.

Operability evaluations for the three containment air coolers were inappropriately assigned as corrective actions for Condition Report 02-2943. These operability evaluations were to be used to scope the extent of condition of the containment air coolers and whether they would have been operable when required, considering the fact that the degradation described in the condition report existed in the past. Prior to these operablilty evaluations being completed, the Regulatory Affairs staff inappropriately concluded that the issue was not reportable. Additionally, the due dates for corrective actions, which were initiated on July 3, 2002, a day after the condition report was issued, had been extended multiple times and were presently set at December 1, 2002. The time period for assessment was clearly in excess of the 60-day time clock for reportable issues as outlined in 10 CFR 73.

c.

Analysis The issue represented a licensee performance deficiency. The inspectors identified numerous examples of the improper implementation of the licensees corrective action program, in regards to evaluating and taking corrective actions for potentially reportable issues documented in Condition Report 02-2943. This was considered a finding of more than minor safety significance because if left uncorrected it would become a more significant safety concern in that it could adversely impact the NRC in its effort to identify and resolve issues important to public safety.

The inspectors determined that this issue was not a violation of regulatory requirements.

Although the inspectors identified examples of the improper implementation of the licensees corrective action program, formal operability and reportability evaluations had not yet been completed.

The inspectors concluded that this was a finding was of very low safety significance (Green) that was not suited for analysis by the significance determination process and was not a violation of regulatory requirements.

4OA3 Event Follow-UP

.1 (Closed) LER 50-346/2002-004-00: Containment Isolation Closure Requirements for

RCP Seal Injection Valves MU66A-D.

This LER documents a condition where the pressure regulating valve setpoint for the reactor coolant pump seal injection valves (MU66A-D) was inadequate to ensure closure of the valves upon receipt of a containment isolation signal. This condition represents a potential common-mode failure. As a result of this condition, during postulated accident conditions, a potential for uncontrolled radioactive leakage outside containment could be created. This condition has apparently existed since original plant construction, and is a violation of Technical Specification 3.6.3.1 for Modes 1-4. In addition, the valves were determined to be installed inconsistent with design assumptions. The causes of these conditions are less than adequate design interface communication and design control.

Design basis for category 1 and 2 air operated valves (AOVs) and their associated components will be established in accordance with the AOV reliability program manual.

MU66A-D and all other category 1 and 2 AOVs will be verified to conform to their design basis requirements.

The licensee identified that the pressure regulating valve setpoint for the reactor coolant pump (RCP) seal injection was inadequate to ensure closure of the valves upon receipt of a containment isolation signal. The condition apparently existed since original plant construction. Downstream of these isolation valves are check valves that are designed to prevent flow out of the reactor coolant system, thereby isolating the flow path regardless of whether the RCP seal injection valves are closed. The test history of the check valves was determined to be highly reliable and had no test failures in the past 10 years. The regional SRA performed a Phase 3 assessment and determined that the issue had very low safety significance (green) due to the low initiating event frequency of an interfacing system loss of coolant accident (ISLOCA), 1E-7, coupled with the check valves failure probability to prevent a potential ISLOCA if the RCP seal injection valve failed. The SRA also reviewed the licensees risk assessment and determined that the calculation was conservative given the assumptions used. The licensees analysis determined that the change in core damage frequency was in the 1E-8 range.

This LER was originally discussed in IR 50-346/02-10 and considered to be an Unresolved Item (URI) (URI 50-346/02-10-2), pending a formal evaluation of the risk imposed by this design issue. Based on the above evaluation of risk, URI 50-346/02-10-2 has been closed. A licensee-identified violation associated with this issue is discussed in Section 4OA7 of this report.

4OA5 Other Activities

One of the key building blocks in the licensees Return to Service Plan was the Management and Human Performance Excellence Plan. The purpose of this plan was to address the fact that management ineffectively implemented processes, and thus failed to detect and address plant problems as opportunities arose. The primary management contributors to this failure were grouped into the following areas:

  • Nuclear Safety Culture;
  • Management/Personnel Development;
  • Standards and Decision-Making;
  • Oversight and Assessments; and
  • Program/Corrective
  • Action/Procedure Compliance.

The resident inspectors had the opportunity to observe the day to day progress that the licensee made toward completing Return to Service Plan activities. Almost every inspection activity performed by the resident inspectors touched upon one of those five areas. Observations made by the resident inspectors were routinely discussed with the Davis-Besse Oversight Panel members and were used, in part, to gauge licensee efforts to improve their performance in these areas on a day-to-day basis.

.1 Resident Inspector Observations of Minor Issues Related to Restart Readiness

Examples of such observations included:

  • Large Backlog of Open Significant Root Cause Evaulations One issue that continued to challenge the inspectors' ability to assess the current overall status of licensee performance was the large number of root cause evaluations still in progress to support the resolution of several condition reports that were classified as Significant Conditions Adverse to Quality. At the time this report was submitted, the licensee had a backlog of 86 open root cause analysis in progress to address documented issues the licensee had deemed significant issues adverse to quality.
  • Failure to Install Equipment Hatch During Severe Weather On November 10, 2002, in response to a tornado warning, the Shift Manager directed the Duty Maintenance Supervisor to install the containment equipment hatch. On multiple occasions, maintenance personnel contacted operations personnel to inquire if the equipment hatch still needed to be installed. The net result was that the severe weather passed through the area, the tornado warning was lifted, and the equipment hatch never was installed. This example demonstrates that the organization has not fully internalized how an operations led organization functions.

This issue is of minor risk significance because no tornados were actually spotted in the owner controlled area and the action to install the containment equipment hatch was beyond the actions required by the licensees severe weather procedure for the existing plant configuration. This issue was captured in the licensee corrective action program as CR 02-9213.

These issues were selected because they occurred throughout the reporting period and illustrate examples of ongoing weaknesses in engineering, operations, and maintenance with respect to Standards and Decision-Making, Oversight and Assessments; and Program/Corrective Action/Procedure Compliance or challenged the ability of the inspectors to assess the current overall status of licensee performance.

.2 Inappropriate Licensee Notification of NRC Inspector Activity

a.

Introduction

The inspectors identified a Green finding when the inspectors observed licensee personnel forewarning other licensee personnel about the presence of NRC inspectors in containment. This was not considered a violation of regulatory requirements.

b.

Description

On November 8, 2002, while conducting a review of major work activities in containment, two inspectors overheard a conversation between three licensee employees. The conversation, in part, was as follows: I am surprised that RP [radiation protection personnel] let you into containment without any safety glasses,..... If you are going to work without glasses, be careful not to get anything in your eyes,..... and watch yourself because I heard that the NRC were on their way into containment. Since it was obvious that the licensee employee was not going to correct an infraction of the FENOC Industrial Safety Manual that states in part, that safety glasses with side shields shall be worn in all buildings in the protected area, except office areas, the inspector introduced himself and informed the individual without safety glasses that he needed to get some. Upon leaving containment, the inspectors informed senior licensee management of the conversation.

The inspector informed licensee management that employees who are aware of safety requirements should enforce those requirements when deficiencies are observed.

Additionally, licensee employees should not warn other licensee employees of the NRC inspectors presence as it could leave impression that behavior of licensee individuals was dependent on whether or not the NRC inspector was watching a given activity.

c.

Analysis

The inspectors determined that the issue represented a licensee performance deficiency. 10 CFR 50.70(b)(4) requires, in part, that the arrival and presence of the NRC inspector is not announced or otherwise communicated by its employees or contractors to other persons at the facility unless specifically requested by the NRC inspector. This was considered a finding of more than minor safety significance because if left uncorrected, it would become a more significant safety concern in that the NRC's ability to carry out its statutory mission would be impeded. The ability for the inspectors to evaluate as-found plant conditions and to observe work activities in progress, without forewarning of their presence, is essential for assessing the day-to-day performance of the licensee.

The inspectors determined that this issue was not a violation of regulatory requirements.

"[10 CFR] Part 50 Statement of Considerations," October 25, 1988, states that "The intent of this rule is to prevent site and contractor personnel from widespread dissemination... of the presence of an NRC inspector. It further states that "... the NRC expects to reserve enforcement action for significant intentional violations of the rule." The inspectors determined that there was no widespread dissemination of the presence of the NRC inspectors. A licensee mechanical maintenance person observed the NRC inspectors signing in at the auxiliary building radiation protection access point prior to entering containment. The same person warned the two other licensee employees of the NRC inspectors in containment. In addition, the inspectors determined that there was no significant intentional violation of the rule. The licensee reviewed General Employee Training and found no specific reference to 10 CFR 50.70(b)(4). Because the mechanical maintenance person was not trained on the regulation the inspectors determined that there was not a significant intentional violation of the rule. The licensee took action to include the regulation in General Employee Training.

The inspectors concluded that this was a finding was of very low safety significance (Green) that was not suited for analysis by the significance determination process and was not a violation of regulatory requirements.

4OA6 Exit Meetings

.1 The inspectors presented the inspection results to Mr. Fast, Plant Manager, and other

members of licensee management on November 14, 2002. The licensee acknowledged the findings presented. No proprietary information was identified.

.2 Intrim Exit Meeting

Biennial Inservice Inspection Activities (IP 71111.08) with Mr. A. Alford on October 3, 2002. Proprietary information was received and reviewed by the inspector and subsequently returned to the licensee. Licensee attendees at the interim exit acknowledged the findings presented and did not identify any potential report input as proprietary information.

4OA7 Licensee Identified Violations:

The following violations of very low safety significance (Green) were identified by the licensee and are violations of NRC requirements which meet the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600 for being dispositioned as Non-Cited Violations (NCVs):

NCV Tracking Number Requirements Licensee Failed to Meet 50-346/02-17-01 Technical Specification 3.6.3.1 requires that all containment isolation valves shall be operable with isolation times less than or equal to required isolation times for Modes 1, 2, 3, and 4.

Contrary to this requirement, a condition was identified where the pressure regulating valve setpoint for the reactor coolant pump seal injection valves (MU66A-D) was inadequate to ensure closure of the valves upon receipt of a containment isolation signal. This issue was determined to be of very low safety significance and will be treated as an NCV. This issue was documented in section 4OA3.1 of this report.

If the licensee contests these NCVs, the licensee should provide a response within 30 days of the date of this inspection report, the basis for the denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555-0001, with copies to the Regional Administrator, Region III; Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Davis-Besse facility.

KEY POINTS OF CONTACT Licensee A. Alford, Regulatory Affairs C. Daft, Staff Nuclear Engineer L. Meyers, Chief Operating Officer, FENOC R. Fast, Plant Manager G. Dunn, Outage Manager D. Gerren, Steam Generator Engineer J. Grabnar, Manager, Design Engineering G. Honma, Supervisor, Compliance D. Imlay, Superintendent, E&C Maintenance P. McCloskey, Manager, Regulatory Affairs G. Melssen, Maintenance Rule Coordinator W. Mugge, Manager, Nuclear Training R. Pell, Manager, Chemistry and Radiation Protection J. Powers, Director, Nuclear Engineering R. Rishel, PRA Specialist M. Roder, Manager, Plant Operations J. Rogers, Manager, Plant Engineering R. Schrauder, Director, Support Services A. Schumaker, Supervisor, Access Control (Acting)

G. Skeel, Manager, Nuclear Security M. Stevens, Director, Work Management G. Wolf, Senior Licensing Engineer LIST OF ITEMS OPENED CLOSED AND DISCUSSED Opened 50-346/02-17-01 NCV Containment Isolation Closure Requirements for RCP Seal Injection Valves MU66A-D.

Closed 50-346/2002-004 LER Containment Isolation Closure Requirements for RCP Seal Injection Valves MU66A-D 50-346/02-10-02 URI Containment Isolation Closure Requirements for RCP Seal Injection Valves MU66A-D 50-346/02-17-01 NCV Containment Isolation Closure Requirements for RCP Seal Injection Valves MU66A-D LIST OF ACRONYMS USED ADAMS Agency-wide Document Access and Management System AOV Air Operated Valve ASME American Society of Mechanical Engineers CARD Condition Assessment Resolution Document CFR Code of Federal Regulations CR Condition Report DHR Decay Heat Removal DRP Division of Reactor Projects DRS Division of Reactor Safety EDG Emergency Diesel Generator FENOC FirstEnergy Nuclear Operating Company HPI High Pressure Injection IMC Inspection Manual Chapter IR Inspection Report IPEEE Individual Plant Examination of External Events ISLOCA Inter-System Loss of Coolant Accident IST Inservice Test LER Licensee Event Report LOCA Loss of Coolant Accident NCV Non-Cited Violation NRC United States Nuclear Regulatory Commission OHS Office of Homeland Security PARS Publically Available Records PI Performance Indicator RCP Reactor Coolant Pump RCS Reactor Coolant System SSC System, Structure or Component SDP Significance Determination Process SFP Spent Fuel Pool SP Surveillance Procedure TS Technical Specifications URI Unresolved Item USAR Updated Safety Analysis Report LIST OF

DOCUMENTS REVIEWED

1R01

Adverse Weather

DB-OP-6913

Season Plant Preparation Checklist

Rev. 4

CR 02-06569

Heat Trace and Freeze Protection System Degradation and

Aging

CR 02-05764

SHHR - Freeze Protection for HPI Pump Minimum

Recirculation Line

CR 02-01187

BWST Vent Freeze Protection Circuit 12 Thermocouple Failed

CR 00-4107

Tech Spec Freeze Protection Point P97, BWST Overflow at

below 32 Degrees

CR 02-00921

Forebay Ice During Winter Refueling Outages

DB-OP-06331

Freeze Protection and Electrical Heat Trace

Rev. 4

1R04

Equipment Alignment

M-035

Piping and Instrumentation Diagram - Spent Fuel Pool Cooling

System

Rev. 48

OS-007

Operations Schematic - Spent Fuel Pool Cooling System

Rev. 19

1R05

Fire Protection

NRC Reg.

Guide 1.189

Fire Protection for Operating Nuclear Power Plants

FHAR

Davis Besse Fire Hazard Analysis Report

Rev. 42

DBNPS PFP

Davis Besse Pre-fire Plan

Rev. 2

CR 02-08525

Improperly Routed Fire Hose on Hose Reel

CR 02-08404

Fire Door Blocked Open

CR 02-0835

Fire Protection Piping Support Rusting in Service Building 5

CR 02-08157

Automatic Start of Electric Fire Pump

CR 02-07459

Fire Barriers and Penetrations

CR 02-07009

Shrr Switchyard/transformers - X01 Fire Water Piping Support

Split

CR 02-06845

Fire Watch Extinguishers

CR 02-06834

Smoldering Fire in Containment Building

CR 02-06769

Fire in Containment

CR 02-06533

Inadequate Fire Brigade Protective Equipment

CR 02-06525

Failed Appendix R Fire Wrap

CR 02-06452

Inadequate Number of Wraps of 3-m Firewrap Material

CR 02-06292

Accessibility to Fire Protection Equipment (Valve Fp269)

Hindered

CR 02-05378

Missing Nuts on Fire Protection Flange

CR 02-04332

Delay in Establishing Compensatory Actions for Known Fire

Impairment

CR 02-03961

Lack of Communication Regarding Fire Risks

1R08

Inservice Inspection Activities

CR 00-1187

Indication on Main Steam Line Outlet Nozzle

2/20/02

CR 02-00724

Loose Bolting on Snubber on Hanger DH-33C-GCB-10-H22

2/22/02

CR 02-00721

Cracked Welded OTGC Plugs

2/22/02

CR 02-01165

13RFO Eddy Current Examination of OTSGs Identified Tubing

Flaws

03/10/02

Modification

98-0045

Steam Generator Repairs 12th Refueling

Rev. 0

Radiographic Record FW-171; Boric Acid/HPCI Crossover

System

04/14/00

Radiographic Record FW-140; Boric Acid/HPCI Crossover

System

03/20/00

Radiographic Record FW-161; Boric Acid/HPCI Crossover

System

03/30/00

Ultrasonic Examination Record UT-002; 8 inch MS875 valve-

to-elbow weld

2/19/02

Ultrasonic Examination Record; 10 Core Flood Line Weld 10-

33B-CCB-6-7-SWB

2/22/02

Magnetic Particle Examination Record; 10 inch Core Flood

Line Weld 10-33B-CCB-6-7-SWB

2/21/02

Procedure 54-IS-367-03; Visual Examination for Leakage of

the Reactor Vessel Head

Rev. 3

Procedure 54-IS-100-06; Remote Ultrasonic Examination of

Control Rod Drive Mechanism (CRAM) Nozzles

Rev. 6

Procedure DB-PF-05058; Steam Generator Eddy Current Data

Analysis Guidelines

Rev. 3

Procedure 51-5001484-02; Qualified Eddy Current

Examination Techniques for Davis Besse

01/28/02

Procedure 54-IS-836-04; Ultrasonic Examination of Austenitic

Piping Welds

Rev. 4

Work Order 99-005771-00; IS VT-3 Bolting Examination

07/05/00

Work Order 91-005601-00; Containment Spray Pump 1-1

01/28/00

Bobbin Probe Fill Factor Equivalency; 51-5012000-00

04/06/01

Eddy Current Probe Extension Cable Comparison; 51-

5014354-00

09/10/01

Code Reconciliation Alloy 690; 51-1264415-03

10/01/97

Certified Material Test Report 29861; Inconel Filler Material

M.O. 82

10/25/94

Condition Monitoring Results for Davis Besse at Outage

2RFO and Operational Assessment for Cycle 13; MEECH-

0734-SR-3

Rev. 0

CMA Evaluation of Steam Generator Tubing at Davis Besse

13RFO; FA-DB-011-0

Rev. 0

Gas Tungsten Arc Welding of Stainless Steel P(8) Groove

With or Without Backing; WAS-A-8-2-1

Rev. 1

Procedure Qualification Record GAW; PER-003

03/09/77

Procedure Qualification Record GAW; PER-007

03/31/78

Eddy Current Examination Manual Davis Besse Unit 1 RAO 13

Rev. 0

1R12

Maintenance Effectiveness

NUMARC 93-01

Industry Guideline for Monitoring the Effectiveness of

Maintenance at Nuclear Power Plants

Rev. 2

CR 00-4139

Security/Fire Door

CR 01-0023

Inoperable Fire Door Without Compensatory Measures

CR 01-1886

Door 205 (Mech. Pen Room #2) Malfunction

CR 01-2632

Door 104A Found Open

CR 01-3472

Door 427 Problem

CR 02-0197

Functional Failure of Door 302

CR 02-0442

Door 201A (MPR#1) Was Found Open When Approached by

a Contract Employee

CR 02-1961

Door 509 Failed Inspection Criteria

CR 02-2791

Door 306 Found Unlatched

CR 02-4078

Door 406 Latch Failure

CR 02-5483

Door 308 Does Not Fully Close and Latch

1R13

Maintenance Risk Assessment and Emergent Work Evaluation

Contingency Plan for Main Generator Protection Upgrade Amod

90-0002, 13RFO-9

Rev 0

RFO Weekly Risk Summary (week of October 21, 2002)

1R14

Personnel Performance in Non-Routine Evolutions

DB-OP-06002

RCS Draining and Nitrogen Blanketing

Rev. 4

Standing

Order 2002-

0016

Radiation Protection Guidance for Monitoring

Rev. 1

1R15

Operability Evaluations

CR 02-08686

SBODG cylinder exhaust temperatures low

DB-SC-04271

SBODG Monthly Test

Rev. 3

Operability

Justification

2002-0034

EDG Lube Oil Monitoring

Rev. 0

CR 02-3732

EDG Lube Oil Monitoring

EDG Crankcase Lube Oil Sample Results (February - June,

2002)

EN-DP-01074

Predictive Maintenance

Rev. 3

M-180-00092

Instruction Manual 2600KW Emergency Dsl Generator Book 1

Rev. 0

Component/

Parameter

Scoping

Sheet CPS-

25

  1. 1 EDG Engine & Generator Lubrication Analysis

Rev. 7

1R19

Post-Maintenance Testing

Work Order

2-1796-000

Station Blackout Generator Relay Calibrations

Rev. 0

Work Order

2-3190-000

Station Blackout Generator Air-Start Compressor Train 2

Rev. 0

Work Order

2-982-000

Station Blackout Diesel Generator

Rev. 0

Work Order

2-6506-000

Station Blackout Radiator fan Motor 1

Rev. 0

Work Order

2-985-000

Station Blackout Battery Charger

Rev. 0

Work Order

2-983-000

Station Blackout Diesel Generator

Rev. 0

Work Order

2-5483-000

Station Blackout Batteries

Rev. 0

Work Order

2-984-000

Station Blackout Generator Relaying Cabinet

Rev. 0

DB-SS-4013

Station Air Compressor No. 2 Performance Check

Rev. 2

DB-OP-6251

Station and Instrument Air Operating Procedure

Rev. 2

CR 02-9050

Station Air Compressor 2 Oil Discoloration

DB-SC-4271

Station Blackout Diesel Generator Monthly Test

Rev. 3

CR 02-05911

Surveillance 4.5.2.H Not Met Following Modifications to

DH14A/B

DB-SP-10072

LPI System Injection Test

Rev. 0

DB-SP-10065

DH 13A/B and DH 14A/B Valve Test

Rev. 1

C-NSA-

049.02-010

Review of Test Data from DB-SP-10065 for Valve DH14A

1R22

Surveillance Testing

DB-SC-3071

Emergency Diesel Generator 2 Monthly Test

Rev. 3

4OA1 Performance Indicator (PI) Verification

NG-RA-

00810

Reactor Oversite NRC Performance Indicator Program

Rev. 0

CR 02-7462

HPI System NRC Performance Indicator Desk Top Guide

Inaccuracy in Unavailability

CR 02-3615

NRC Performance Indicator Input Data Sheets Missing

CR 01-2558

Reactor Coolant Iodine

CR 01-0132

Reactor Coolant Iodine 131 Increase

Performance

Indicator Data

Input Sheets,

Residual Heat Removal (January-September 2002)

DB-CH-

01815

Dose Equivalent I-131 Determination

Rev. 0

4OA2 Problem Identification and Resolution

CR 02-794

Containment Purge Valve CV5007 Failed Stroke Time Test

CR 02-3114

Decay Heat Valve 14A

CR 02-3339

Reactor Cavity Seal Plate Seal Clamp

CR 02-3662

CV5003A Did Not Fully Close During Testing

CR 02-3833

Ineffective Implementation of Corrective Action for CR 01-2820

Component Cooling Water to Emergency Diesel Generators

CR 02-3711

Latent Issue Review - Emergency Diesel Generator-Nuisance

Alarm at Local Emergency Diesel Generator Panel for Alternate

Shutdown

CR 02-4336

CRNVS Equipment Requirements During Fuel Handling in

Modes 5 and 6.

CR 02-4752

Latent Issue Review - Emergency Diesel Generator - Fire

Damper FD1036 Possible Obstruction

Nuclear Operating Administrative Procedure

NOP-LP-2001 - Condition Report Process

Rev. 1

Programmatic Guideline for Davis-Besse Condition Reporting

Process

Rev. 0

CR 02-9314

Untimely Determination of Condition Reportability

4OA3 Event Follow-up

LER 50-346/2002-004

Containment Isolation Closure Requirements for RCP Seal

Injection Valves MU66A-D

CR 02-9314

Untimely Determination of Condition Reportability

4OA5 Other Activities

CR 02-8860

Potential FME in #3 Containment Air Cooler Motor

CR 02-9213

Equipment Hatch Not Installed in a Timely Manner

CR 02-9278

Potential Violation of 10CFR50.70, Notification of Inspection

Independent Investigation Report of CR 02-9278