IR 05000341/2019003

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Integrated Inspection Report 05000341/2019003
ML19310E673
Person / Time
Site: Fermi 
Issue date: 11/06/2019
From: Eric Duncan
Reactor Projects Region 3 Branch 4
To: Peter Dietrich
DTE Energy
References
IR 2019003
Download: ML19310E673 (31)


Text

November 6, 2019

SUBJECT:

FERMI POWER PLANT, UNIT 2 - INTEGRATED INSPECTION REPORT 05000341/2019003

Dear Mr. Dietrich:

On September 30, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Fermi Power Plant, Unit 2. On October 16, 2019, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

Three findings of very low safety significance (Green) are documented in this report. Two of these findings involved violations of NRC requirements. We are treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violations or significance or severity of the violations documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector at Fermi.

If you disagree with a cross-cutting aspect assignment or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; and the NRC Resident Inspector at Fermi. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Eric R. Duncan, Chief Branch 4 Division of Reactor Projects

Docket No. 05000341 License No. NPF-43

Enclosure:

As stated

Inspection Report

Docket Number:

05000341

License Number:

NPF-43

Report Number:

05000341/2019003

Enterprise Identifier: I-2019-003-0058

Licensee:

DTE Electric Company

Facility:

Fermi Power Plant, Unit 2

Location:

Newport, MI

Inspection Dates:

July 01, 2019 to September 30, 2019

Inspectors:

T. Briley, Senior Resident Inspector

G. Edwards, Health Physicist

J. Harvey, Resident Inspector

L. Kozak, Senior Reactor Analyst

R. Ng, Project Engineer

T. Taylor, Resident Inspector

Approved By:

Eric R. Duncan, Chief

Branch 4

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Fermi Power Plant, Unit 2 in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Incorrect Datum Used to Assess Lake Levels Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000341/2019003-01 Open/Closed None (NPP)71111.01 The inspectors identified a finding of very low safety significance (i.e., Green) and an associated Non-Cited Violation (NCV) of 10 CFR 50, Appendix B, Criterion III, Design Control, when licensee personnel failed to have appropriate measures in place to assess the impact of projected Lake Erie water levels on the site. As a result, actual lake level, including any predicted maximum lake level during a flood watch or warning, was determined to be 1.3' [feet] higher during a flooding event than what was calculated.

Inadequate Response to an Out-of-Service Diesel Fire Pump Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000341/2019003-02 Open/Closed

[H.5] - Work Management 71111.18 A self-revealed finding of very low safety significance (i.e., Green) and an associated Non-Cited Violation (NCV) of Fermi License Condition 2.C.(9) was identified when licensee personnel failed to take appropriate actions in response to an out-of-service diesel fire pump.

Specifically, a temporary diesel fire pump (DFP) used to restore system functionality failed to function as designed and the risk plan that was developed could not be implemented as written.

Failure to Properly Pre-Plan Work in Accordance with the Work Control Conduct Manual Cornerstone Significance Cross-Cutting Aspect Report Section Barrier Integrity Green FIN 05000341/2019003-03 Open/Closed

[H.7] -

Documentation 71153 A self-revealed finding of very low safety significance (i.e., Green) was identified when the licensee failed to properly pre-plan maintenance activities on the Feedwater Distributed Control System in accordance with the Work Control Conduct Manual. This resulted in an unplanned loss of the gland seal exhauster trip safety function.

Additional Tracking Items

Type Issue Number Title Report Section Status LER 05000341/2019-001-00 LER 2019-001-00 for Fermi Unit 2, Unplanned Loss of Safety Function of Gland Seal Exhauster Trip During Planned Maintenance Due to Inadequate Procedure.

71153 Closed

PLANT STATUS

Unit 2 operated at or near rated thermal power during the entire inspection period with the exception of power changes to perform planned rod pattern adjustments.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

External Flooding Sample (IP Section 03.04) (1 Sample)

(1) The inspectors evaluated the licensee's readiness to cope with external flooding under the following conditions:

71111.04Q - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Emergency Diesel Generator (EDG) 12 while Combustion Turbine Generator (CTG)11-1 was out of service for planned maintenance during the week ending September 14, 2019
(2) Electric Fire Pump while the Diesel Fire Pump and a Temporary Alternate Diesel Fire Pump were out of service for corrective maintenance during the week ending September 7, 2019
(3) Division 1 Core Spray (CS) while Division 2 CS was out of service for planned maintenance during the week ending September 21, 2019
(4) Division 2 Non-Interruptible Air System (NIAS) after planned maintenance during the week ending September 28, 2019

71111.04S - Equipment Alignment

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated system configurations during a complete walkdown of the Emergency Equipment Cooling Water (EECW) system during the week ending September 28, 2019

71111.05Q - Fire Protection

Quarterly Inspection (IP Section 03.01) (4 Samples)

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) General Service Water Pump House during the week ending August 31, 2019
(2) Auxiliary Building Sub-Basement and NIAS Room during the week ending September 28, 2019
(3) Auxiliary Building Fifth Floor, Division 1 and Division 2 Standby Gas Treatment Rooms during the week ending September 28, 2019
(4) Reactor Building Basement and Sub-Basement, Northeast Corner Room during the week ending September 28, 2019

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 02.02a.) (1 Sample)

The inspectors evaluated internal flooding mitigation protections in the:

(1) Torus Room

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the Control Room during power ascension following a planned down power for Main Steam Isolation Valve (MSIV) testing and a rod pattern adjustment on September 8, 2019

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (2 Samples)

(1) The inspectors observed and evaluated an as-found simulator assessment during the week ending August 31, 2019
(2) The inspectors observed and evaluated an as-found simulator assessment during the week ending September 7, 2019

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Emergent maintenance on Mechanical Draft Cooling Tower Fan D during the week ending August 3, 2019
(2) Planned High Pressure Coolant Injection (HPCI) surveillance testing during the week ending August 24, 2019
(3) Planned CTG 11-1 maintenance, new CTG fuel oil storage tank installation, with an installed Alternate Diesel Fire Pump during the week ending September 14, 2019

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 02.02) (5 Samples)

The inspectors evaluated the following operability determinations and functionality assessments:

(1) Operability and functionality of the Standby Liquid Control (SLC) system following identification of a potential non-conservative Technical Specification associated with minimum SLC tank level, as documented in Condition Assessment Resolution Document (CARD) 19-21369
(2) Operability and functionality of the Suppression Chamber (Torus) structure following a missed Technical Requirements Manual (TRM) surveillance requirement to perform an exterior visual inspection, as documented in CARD 19-25694
(3) Functionality of the Diesel Fire Pump following identification of wear on the right angle drive anti-rotational clutch, as documented in CARD 19-26111
(4) Operability and functionality of the Reactor Core Isolation Cooling (RCIC) system following identification of an abnormal RCIC flow controller reading while the system was in a standby condition, as documented in CARDs 19-26174 and 19-26198
(5) Operability and functionality of the Division 2 Reactor Protection System (RPS),

Average Power Range Monitor (APRM), and Oscillation Power Range Monitor (OPRM) systems following abnormal light indications during a planned logic module functional test, as documented in CARD 19-26362

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (2 Samples)

The inspectors evaluated the following temporary or permanent modifications:

(1) Installation of an Alternate Diesel Fire Pump while the Diesel Fire Pump was out of service for an extended period (Temporary Modification)
(2) Installation of Gland Seal Exhauster trip function (Permanent Modification)

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated the following post maintenance tests:

(1) RPS Channel A2 Reactor Vessel Level 1 and 2 agastat relays following planned maintenance during the week ending July 13, 2019
(2) CTG 11-1 following planned maintenance during the week ending September 14, 2019
(3) Division 2 NIAS following planned maintenance during the week ending September 28, 2019

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Surveillance Tests (other) (IP Section 03.01)

(1) Low Pressure Coolant Injection (LPCI) Loop Select 480 Volt Swing Bus (72CF)automatic throwover scheme operability test during the week ending July 8, 2019
(2) Emergency Diesel Generator (EDG) 14 24-hour run followed by hot fast restart during the week ending August 3, 2019

Inservice Testing (IP Section 03.01) (2 Samples)

(1) High Pressure Coolant Injection (HPCI) pump and valve operability test at 1025 pounds per square inch (psi) during the week ending August 24, 2019
(2) Division 2 LPCI and Suppression Pool Cooling/Spray pump and valve operability test during the week ending August 31,

RADIATION SAFETY

71124.08 - Radioactive Solid Waste Processing and Radioactive Material Handling, Storage,

and Transportation

Radioactive Material Storage (IP Section 02.01)

The inspectors evaluated radioactive material storage.

(1) The inspectors toured the following areas:
  • Fermi 2 Radioactive Waste Building Basement
  • Fermi 2 Radioactive Waste Building Mezzanine
  • Fermi 2 Radioactive Waste Building Main Floor
  • Fermi 2 Radioactive Waste Onsite Storage Facility

The inspectors performed a container check (e.g., swelling, leakage and deformation)on the following containers:

  • 55 Gallon Drum 6512; Fermi 2 Radioactive Waste Onsite Storage Facility
  • 55 Gallon Drum 6572; Fermi 2 Radioactive Waste Onsite Storage Facility
  • 55 Gallon Drum 6577; Fermi 2 Radioactive Waste Onsite Storage Facility
  • 55 Gallon Drum 6578; Fermi 2 Radioactive Waste Onsite Storage Facility
  • 55 Gallon Drum 6225; Fermi 2 Radioactive Waste Onsite Storage Facility

Radioactive Waste System Walkdown (IP Section 02.02) (1 Sample)

The inspectors evaluated the following radioactive waste processing systems and processes during plant walkdowns:

(1) Liquid or Solid Radioactive Waste Processing Systems
  • Fermi 2 Spent Fuel Pool Cooling and Clean Up
  • Fermi 2 Asphalt Solidification System
  • Fermi 2 Floor Drain Collection System

Radioactive Waste Resin and/or Sludge Discharges Processes

  • Fermi 2 Spent Resin Tank
  • Fermi 2 Primary Resin System
  • Fermi 2 Resin Demineralizers

Waste Characterization and Classification (IP Section 02.03) (1 Sample)

The inspectors evaluated the radioactive waste characterization and classification for the following waste streams:

(1)

  • Fermi 2 Dry Active Waste
  • Fermi 2 Condensate Resin System

Shipment Preparation (IP Section 02.04) (1 Sample)

The inspectors evaluated and observed the following radioactive material shipment preparation processes:

(1)

  • EF2-19-051; UN (United Nations) 3321; Radioactive Material, LSA-II (Low Specific Activity-II), 7; 07/17/2019

Shipping Records (IP Section 02.05) (1 Sample)

The inspectors evaluated the following non-excepted package shipment records:

(1)

  • EF2-17-136; Dewatered Resin Liner, LH-16-017; 01/12/2018
  • EF2-18-007; Dewatered Resin Liner, LH-16-007; 01/19/2018
  • EF2-18-009; Dewatered Resin Liner, LH-17-005; 02/12/2018

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

MS08: Heat Removal Systems (IP Section 02.07)===

(1) Unit 2 (July 1, 2018 - June 30, 2019)

MS09: Residual Heat Removal Systems (IP Section 02.08) (1 Sample)

(1) Unit 2 (July 1, 2018 - June 30, 2019)

MS10: Cooling Water Support Systems (IP Section 02.09) (1 Sample)

(1) Unit 2 (July 1, 2018 - June 30, 2019)

BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10) (1 Sample)

(1) Unit 2 (July 1, 2018 - June 30, 2019)

OR01: Occupational Exposure Control Effectiveness Sample (IP Section 02.15) (1 Sample)

(1) Unit 2 (July 1, 2018 - June 30, 2019)

PR01: Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences Sample (IP Section 02.16) (1 Sample)

(1) Unit 2 (July 1, 2018 - June 30, 2019)

71152 - Problem Identification and Resolution

Semiannual Trend Review (IP Section 02.02) (1 Sample)

(1) The inspectors reviewed the licensees corrective action program for potential adverse trends in the issuance of parts and storage of quality material that could be indicative of a more significant safety issue

71153 - Followup of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02)

The inspectors evaluated the following Licensee Event Report (LER):

(1) LER 2019-001-00, Unplanned Loss of Safety Function of Gland Seal Exhauster Trip during Planned Maintenance Due to Inadequate Procedure (ADAMS Accession ML19060A290). The circumstances surrounding this LER are documented in the Results Section of this report.

INSPECTION RESULTS

Incorrect Datum Used to Assess Lake Levels Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems

Green NCV 05000341/2019003-01 Open/Closed

None (NPP)71111.01 The inspectors identified a finding of very low safety significance (i.e., Green) and an associated Non-Cited Violation (NCV) of 10 CFR 50, Appendix B, Criterion III, Design Control, when licensee personnel failed to have appropriate measures in place to assess the impact of projected Lake Erie water levels on the site. As a result, actual lake level, including any predicted maximum lake level during a flood watch or warning, was determined to be 1.3

[feet] higher during a flooding event than what was calculated.

Description:

As discussed in the Fermi Updated Final Safety Analysis Report (UFSAR), the determination of a mean Lake Erie water level reference point to ensure that safety-related structures, systems, and components (SSCs) are protected from flooding was based on 1935 New York Mean Tide (NYMT) lake level data. During this inspection period, the inspectors discovered that to calculate the maximum expected Lake Erie water level and assess site impact from potential flooding, the licensee utilized National Weather Service (NWS) data, which was based on 1985 International Great Lakes Datum (1985 IGLD) to determine the Lake Erie water level reference point. While inspecting the potential impacts of record high Lake Erie water levels, the inspectors discovered a non-conservative 1.3' difference between the two water level reference points.

The flooding design basis as described in the UFSAR ensured that safety-related SSCs would continue to be functional provided the Lake Erie water level was no higher than 575.3 using NYMT data. This accounted for a maximum postulated storm-induced wave surge and flooding to a level of 586.9 NYMT, or 3.9 above the site grade of 583.0. The inspectors reviewed NWS lake level data and discovered the current monthly mean level using 1985 IGLD data was 574.6, and was therefore less than the flooding design basis level of 575.3.

However, since the NYMT Lake Erie water level reference point was 1.3 lower than the NWS Lake Erie water level reference point, after adjusting for this difference, the actual maximum Lake Erie water level in the event of a storm-induced wave surging and flooding was 576.9 NYMT, which exceeded the maximum Lake Erie water level described in the UFSAR. The inspectors discussed the issue with licensee personnel, and the licensee subsequently performed evaluations to assess the actual impact on safety-related SSCs. In addition, the equipment and strategies assumed to be available for beyond-design-basis accidents (i.e.

FLEX equipment) were evaluated. Following these evaluations, and despite the high lake level and Lake Erie water level reference point difference, the licensee determined that safety-related SSCs would continue to be functional.

Regarding the licensees FLEX strategy, which relied upon adequate warning time from the NWS when certain flood levels were predicted, the licensee discovered that the NWS utilized a 1.5 uncertainty when performing lake level predictions. As a result, even with the difference in Lake Erie water level reference points, the plant would have received the prediction for extreme flood levels within a sufficient warning time to implement FLEX strategies.

As a result of the inspection, the licensee revised their Memorandum of Understanding (MOU) with the NWS to incorporate the difference between the datums. The licensee also implemented a monitoring program to ensure future Lake Erie water level increases were closely tracked.

Corrective Actions: The licensee entered this issue into their Corrective Action Program and established a formal monitoring plan to assess lake levels.

Corrective Action References: CARDs 19-25657, 19-25893, and 19-25820

Performance Assessment:

Performance Deficiency: The failure to develop appropriate measures to assess compliance with the flooding design and licensing basis, and to ensure an appropriate warning was received from the NWS to implement certain FLEX strategies was a performance deficiency.

Specifically, the difference in reference datum between site design documents and Lake Erie water level measurements was not accounted for.

Screening: The inspectors determined the performance deficiency was more than minor because if left uncorrected, it would have the potential to lead to a more significant safety concern. Specifically, a misunderstanding of current or predicted Lake Erie water level could result in the plant being in a condition outside its design and licensing basis, inoperable safety-related equipment, or an inability to perform response actions as planned for extreme flooding conditions. The inspectors consulted IMC 0612, Appendix E, Examples of Minor Issues, Examples 3j and 3k and the associated Note that followed these examples.

Specifically, when errors are discovered regarding design assumptions, if reasonable doubt exists as to the operability of safety-related SSCs (regardless if they are later determined operable), the issues can be considered more than minor. For this issue, reasonable doubt existed regarding safety-related SSCs because with the datum difference that existed in Lake Erie water level measurement the licensee was not within the design and licensing basis for flood protection.

Significance: The inspectors assessed the significance of the finding using Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors also consulted Appendix O, Significance Determination Process for Mitigating Strategies and Spent Fuel Pool Instrumentation. Based on actual Lake Erie levels, the finding screened as having very low safety significance (i.e., Green), because there was no loss of safety function for any of the safety-related SSCs. Further, no issues with implementation of the licensees FLEX strategy were identified.

Cross-Cutting Aspect: Not Present Performance. No cross cutting aspect was assigned to this finding because the inspectors determined the finding did not reflect present licensee performance.

Enforcement:

Violation: Title 10 CFR 50, Appendix B, Criterion III, Design Control, requires, in part, that measures shall be established to assure that the applicable regulatory requirements and the design basis, as defined in Part 50.2 and as specified in the license application, for those SSCs to which this Appendix applies, are correctly translated into specifications, drawings, procedures, and instructions.

Contrary to the above, since issuance of the Fermi 2 Operating License on July 15, 1985, until July 12, 2019, the licensee failed to establish measures to assure that regulatory requirements and the design basis were correctly translated into specifications, procedures, or instructions. The licensee utilized information from the National Weather Service to receive notifications of flood watches and warnings that were inconsistent with the methodology used in the UFSAR flooding design basis, without compensation for the existing difference in Lake Erie water level reference points being used. As a result, actual Lake Erie water levels were identified to be 1.3 higher at the site than reported, which could challenge safety-related SSCs.

Enforcement Action: This violation is being treated as an non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Inadequate Response to an Out-of-Service Diesel Fire Pump Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems

Green NCV 05000341/2019003-02 Open/Closed

[H.5] - Work Management 71111.18 A self-revealed finding of very low safety significance (i.e., Green) and an associated Non-Cited Violation (NCV) of Fermi License Condition 2.C.(9) was identified when licensee personnel failed to take appropriate actions in response to an out-of-service diesel fire pump.

Specifically, a temporary diesel fire pump (DFP) used to restore system functionality failed to function as designed and the risk plan that was developed could not be implemented as written.

Description:

On August 13, 2019, the licensee entered Technical Requirements Manual (TRM) Action 3.12.2 A.1 due to planned maintenance on the DFP. The TRM required either the pump to be restored or an alternate pump to be installed within 14 days. Upon discovery of extensive wear on components associated with the DFP right angle drive, the licensee concluded that the DFP would not likely be restored within 14 days. The licensee initiated actions to procure an alternate DFP to comply with the TRM requirements and restore full system capabilities. The licensee received and installed a temporary diesel-driven fire pump and exited the TRM action within the 14 day action requirement on August 27, 2019. On September 3, 2019, the licensee initiated a weekly test to operate the temporary DFP.

Approximately 10 minutes after the pump was started, pump coolant was observed to be leaking from the temporary fire pump. The pump was immediately shut down by the operators. Upon investigation, the licensee believed either the coolant had been overfilled and/or the engine had overheated. It was also noted that during the test the pump had been running with no system demand (i.e. dead-headed) during test preparations. After consulting with the vendor, the licensee determined that the pump should have had a minimum flow line installed to prevent damage from overheating under low-demand conditions. While the temporary pump did include a relief valve on the pump discharge, the system did not function in the same manner as the relief valve on the permanent pump, which provided both relief and minimum flow functions during pump operation.

In addition, the licensees risk plan to operate with a single electric pump available (pending re-design/re-work of the temporary DFP following this issue) relied upon power being available from the Combustion Turbine Generators (CTGs) in the event of a loss of offsite power. However, the licensee had removed all CTGs from service for planned maintenance.

As a result of these issues, the licensee coordinated with the temporary pump vendor to enable its relief valve to also function as a minimum flow line. Additionally, the licensee revised the risk plan to incorporate other strategies while the CTGs were out of service.

Corrective Actions: The licensee added a functional minimum flow line and revised the risk plan to ensure all elements of the plan could be performed.

Corrective Action References: CARDs 19-26837, 19-26615, and 19-26603

Performance Assessment:

Performance Deficiency: The failure to take necessary actions to minimize fire risk and perform repairs as soon as practical when fire equipment was taken out of service, as required by the fire protection program, was a performance deficiency. Specifically, fire risk was not minimized, and restoration of system capability was not timely when a temporary fire pump was installed with an inadequate design. Further, fire risk was not minimized when the risk plan that was developed could not be implemented as written due to credited backup power not being available.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Protection Against External Factors attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the availability, reliability, and capability of the fire protection system was adversely impacted by the installation of a temporary DFP that could not function as designed. Further, although normal power was available, the risk plan also relied upon a backup source of power that was not available had it been needed.

Significance: The inspectors assessed the significance of the finding using Appendix F, Fire Protection and Post - Fire Safe Shutdown SDP. The finding screened as having very low safety significance (i.e., Green) based on answering Yes to Question 1.4.3-A, which asked whether or not adequate fire water capacity still existed for equipment important for safe shutdown. In this case, the electric fire pump was still functional with normal power available.

Cross-Cutting Aspect: H.5 - Work Management: The organization implements a process of planning, controlling, and executing work activities such that nuclear safety is the overriding priority. The work process includes the identification and management of risk commensurate to the work and the need for coordination with different groups or job activities. Specifically, the licensee did not coordinate with the pump vendor to ensure all necessary plant technical requirements were incorporated into the design of the temporary fire pump. Further, site personnel with expertise in engineering modifications were not initially involved to ensure all technical requirements were incorporated into the design of the temporary fire pump.

Enforcement:

Violation: Fermi License Condition 2.C.(9) requires, in part, that the licensee shall maintain in effect all provisions of the approved fire protection program as described in the UFSAR. Section 9A.1.3.2.i of the Fermi UFSAR described the components of the fire protection program and required, in part, that assurance will exist that, actions are taken to minimize fire risk and repairs are made as soon as practical when fire equipment is taken out of service.

Contrary to the above, from August 27, 2019, until September 17, 2019, actions were not taken to minimize fire risk, nor were repairs made as soon as practical when the permanent diesel fire pump was out of service as required by Fermi License Condition 2.C.(9) as specified in UFSAR Section 9A.1.3.2.i. Specifically, a temporary diesel fire pump was installed that lacked a functional minimum flow line, which resulted in the pump failing its first weekly surveillance. This required extensive re-design, during which time the plant fire response capability was reduced to a single fire pump. Additionally, fire risk was not minimized because the fire risk plan that was developed for operating with only a single fire pump could not be implemented as written since backup power that was credited in the fire risk plan was not available.

Enforcement Action: This violation is being treated as an non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Observation: Trend in Incorrect Parts Issued or Ordered 71152 During a semi-annual trend review, the inspectors noted that a large number of CARDs initiated since January 2019 identified incorrect parts that had been ordered or issued for work. The inspectors shared this observation with licensee staff who agreed that it appeared a trend existed. The licensee initiated CARD 19-27102 as a result of the inspectors observations to document five recent issues. During further discussions with the licensee, the inspectors noted that 12 additional CARDs dating back to January 2019 also identified issues with incorrect parts. Within this group of CARDs, and upon further review, the licensee discovered a potential adverse trend within one particular department. In reviewing the CARDs, the inspectors also noted an inconsistent use of cause-codes within the CARDS to describe the various parts issues. In some cases, no cause-codes were assigned at all.

As such, the failure to utilize a consistent method of assigning cause codes to CARDs could result in plant personnel missing opportunities to identify trends before they become larger concerns. At the end of the inspection period, the licensee planned to further assess this issue.

Observation: Failure to Address a Trend in the Storage of Quality Material 71152 During a semi-annual trend review, the inspectors reviewed Elevation CARD 19-21685 from the sites Nuclear Quality Assurance (NQA) organization regarding the storage and staging of parts. The inspectors had also noted what appeared to be a number of CARDS written throughout the year that addressed the improper storage and handling of materials. The NQA Elevation CARD documented numerous recurring issues with the storage and handling of quality material that dated back to 2015, along with some more recent issues. The inspectors reviewed several of the actions that resulted from the Elevation CARD and from previous NQA audits. One of the primary issues was the discovery that quality and non-quality material were not being stored in accordance with plant procedures. In particular, parts had been issued, not used, and then not properly returned to the warehouse within the procedurally required timeframe, which increased the likelihood that material traceability could be lost and/or parts could be stored in an uncontrolled environment. From an NQA audit finding identified in CARD 15-22778, the licensee implemented a corrective action which established a recurring activity to periodically inspect areas of the plant where improperly stored material was being found (i.e., PST [Performance Scheduling and Tracking] events). The inspectors discovered that while the PSTs were being performed and generally found no issues, NQA continued to identify that parts were stored inappropriately, which eventually resulted in the Elevation CARD. While discussing the PST events with the inspectors, the licensee also identified that there was an allowance for the return of improperly stored material to the warehouse of up to 60 days, contrary to the site procedural requirements of 7 days (online work) or 30 days (outage work). Further, the licensee identified that the PST events did not require a check of non-quality material being stored improperly, which had also been identified as an issue. The licensee initiated a CARD to address the issues with how the PSTs were written.

The inspectors also reviewed an Interim Effectiveness Review (IER) that the licensee performed to support closure of the NQA Elevation CARD. This IER was completed on August 30, 2019, and concluded that actions associated with the Elevation CARD had been performed satisfactorily. However, on August 14, 2019, NQA denied a request to close the CARD based on the identification of continuing issues with the storage of material and the failure to correctly follow the appropriate process for closing NQA Elevations. As of October 3, 2019, the inspectors noted there had been no additional actions created to address the failure to close the NQA Elevation CARD, or develop a revised action plan to measure the effectiveness given the apparent discrepancy between the conclusion of the IER and NQAs assessment regarding the effectiveness of the corrective actions that had been performed.

Failure to Properly Pre-Plan Work in Accordance with the Work Control Conduct Manual Cornerstone Significance Cross-Cutting Aspect Report Section Barrier Integrity

Green FIN 05000341/2019003-03 Open/Closed

[H.7] -

Documentation 71153 A self-revealed finding of very low safety significance (i.e., Green) was identified when the licensee failed to properly pre-plan maintenance activities on the Feedwater Distributed Control System in accordance with the Work Control Conduct Manual. This resulted in an unplanned loss of the gland seal exhauster trip safety function.

Description:

On January 1, 2019, during reactor startup and at approximately 5 percent rated thermal power, the licensee began a planned maintenance activity to correct a failed main steam line flow indication associated with the digital Feedwater Distributed Control System (FW DCS).

This maintenance included performing a full system reboot of FW DCS. Before the maintenance was performed, the licensee attached an impact statement to the work order, as required by Work Control Conduct Manual (MWC) 10, Revision 39. Specifically, Step 4.40.1 of the MWC required, in part, In Maximo [the work order system software], under the safety/impact tab for Work Order, and under the impact statement section, provide the following: affected modes, Technical Specifications, technical requirements, expected alarms, precautions including system component status, any requirements prior to tagging, prohibited parallel work, trips/actions including trip(s) and action(s) to prevent, indications/actuations including indication(s) and actuation(s), system impact/PMT [post maintenance testing]

including plant system impact, system impact. However, the licensee failed to include information regarding the rod worth minimizer (RWM) and the turbine gland seal exhauster (GSE) trip in the impact statement that should have been included. When reviewing the work order prior to performing the maintenance activity, the Operations crew on shift noted the impact statement was missing a reference to the Technical Specifications for the RWM. As a result, the licensee was able to be prepared for the impact of the work on the RWM and enter the appropriate Technical Specification (TS) Limiting Condition for Operation (LCO).

However, the licensee failed to identify that the GSE trip function was also impacted, and therefore during the maintenance activity did not enter the associated TS LCO required action.

The GSE trip function is relied upon between 0 and 10 percent rated thermal power to ensure that dose limits do not exceed regulatory limits during a control rod drop accident. The impact to the GSE trip function when resetting the FW DCS resulted from a modification that was installed during the most recent refueling outage in October 2018. Therefore, resetting the FW DCS would not have previously impacted the GSE trip.

When FW DCS was reset, annunciator 4D32, MSL [Main Steam Line] Radn [Radiation] Mon

[Monitor] GS [Gland Seal] STM [Steam] EXHS [Exhaust] Trip Enabled, cleared and unexpectedly re-alarmed in the control room. Operators subsequently determined that the GSE trip function was disabled during the reset of FW DCS, which lasted approximately 1 minute and 19 seconds. As a result, the licensee submitted (EN) 53811 pursuant to 10 CFR 50.72(b)(3)(v)(C) and 10 CFR 50.72(b)(3)(v)(D) as any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to: 1) control the release of radioactive material, and 2) mitigate the consequences of an accident, respectively. On March 1, 2019, the licensee submitted Licensee Event Report (LER) 05000341/2019-001-00 for this event.

The licensee performed a causal evaluation and determined that the cause of the event was that the Failure Modes Effect and Analysis (FMEA) discussion in the engineering modification package did not specifically identify a loss of FW DCS as a failure mode for the GSE trip. In addition, the inspectors noted that Section 4.40, Work Order Safety/Impact Section Completion, of MWC 10 did not include suggested reference documentation for Operations personnel to review. As a result, the inspectors questioned the licensee as to what documentation was reviewed when generating the impact statement. The licensee stated a review of previous FW DCS work orders and impact statements, and the applicable FW DCS procedures was completed. Additionally, when reviewing corrective actions, the inspectors questioned whether all relevant documents were fully updated and if any additional failure modes were evaluated. Upon further review, the licensee determined additional documents were required to be updated to include information regarding the impact of the FW DCS on the GSE trip function. Also, the licensee determined there was a lack of alignment between the causal evaluation and correction actions, such that a review of additional failure modes was not performed to address the FMEA gap that was identified.

Corrective Actions: The licensee entered the issues into their Corrective Action Program.

Planned corrective actions included updating additional applicable procedures and design documents with the relevant GSE trip information and evaluating the lack of alignment between the causal statement and corrective actions.

Corrective Action References: CARDs 19-27084 and 19-26836

Performance Assessment:

Performance Deficiency: The licensees failure to properly pre-plan maintenance activities on the FW DCS in accordance with the Work Control Conduct Manual was a performance deficiency. Specifically, the licensee failed to evaluate the impact of FW DCS on the GSE trip instrumentation, which resulted in the unplanned loss of the GSE trip safety function.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the SSC and Barrier Performance attribute of the Barrier Integrity cornerstone and adversely affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events.

Specifically, the licensee disabled the GSE trip when the function was required. Without mitigating actions, the failure to trip the GSEs could have resulted in a dose above regulatory requirements if a control rod drop accident had occurred. Therefore, the required barrier was adversely impacted.

Significance: The inspectors assessed the significance of the finding using Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors determined that the performance deficiency affected the Barrier Integrity cornerstone. The finding was determined to be of very low safety significance (i.e., Green), because the inspectors answered Yes to the question, Does the finding only represent a degradation of the radiological barrier function provided for the control room, or auxiliary building, or spent fuel pool, or SBGT [Standby Gas Treatment ] system (BWR)? in Exhibit 3, Barrier Integrity Screening Questions.

Cross-Cutting Aspect: H.7 - Documentation: The organization creates and maintains complete, accurate and up-to-date documentation. The licensee failed to create and maintain complete, accurate and up-to-date documentation. Specifically, the licensees engineering design change document failed to completely identify all failure modes. Additionally, the licensee failed to update documentation associated with the FW DCS and GSE systems when implementing the plant modification in 2018, which could have aided in the licensees system impact evaluation.

Enforcement:

Because the Work Control Conduct Manual was not subject to the requirements of 10 CFR 50, Appendix B, Quality Assurance Criteria for Nuclear Power Plants and Fuel Processing Plant, the inspectors did not identify a violation of regulatory requirements associated with this finding.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On October 16, 2019, the inspectors presented the integrated inspection results to Mr. P. Dietrich, Senior VP and Chief Nuclear Officer, and other members of the licensee staff.
  • On July 18, 2019, the inspectors presented the Radiaton Protection inspection results to Mr. M. Caragher, Executive Director - Nuclear Production, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.01

Corrective Action

Documents

19-25280

NRC Identified: Local Lake Level Indication Reads Higher

than UFSAR Assumed Maximum Starting Level for Flood

07/12/2019

19-25458

Determine Impact of CARD 19-25280 and EFA-A30-19-007

on FLEX and Hardened Vent Required Equipment in MOP25

07/18/2019

19-25657

AOP 20.000.01 MOU for Flooding is Not Specific in Datum

Reference

07/29/2019

19-25893

Flood Analysis Past Functionality of FLEX Strategy in

Reverence to CARD 19-25657

08/05/2019

Miscellaneous

Adverse

Condition

Monitoring Plan

ACMP 19-016

Lake Erie Water Level Elevation

IGLD 1985

Brochure on the International Great Lakes Datum 1985

01/1992

NARP-18-0277

Letter of Agreement Between Fermi 2 and NOAA - National

Weather Service

11/19/2018

NARP-19-0140

Letter of Agreement Between Fermi 2 and NOAA - National

Weather Service

07/31/2019

National Ocean

Survey, Detroit,

Michigan

History and Theory of Datum Planes of the Great Lakes

TE-K11-19-039

Impact of Incorrect Datum Reference Used for Design

Maximum Flood Level on Past Functionality of FLEX/HCVS

(CARD 19-25657)

Procedures

20.000.01

Acts of Nature

0, 48, 49, 54

29.400.01

FLEX

ARP 7D22

General Service H2O Screen a H2O Level High/Low

MOP01-200

Severe Weather Guidelines

MOP25

Beyond-Design-Basis Event Coping Strategies Program

Document

Work Orders

38560633

Lube and Inspect Reactor/Auxiliary Building Water Tight

Doors

07/16/2014

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.04Q Corrective Action

Documents

05-24306

Add Electric Fire Pump to DC-6105, Dedicated Shutdown for

Appendix R Loads

07/20/2005

18-28658

Discharge Pressure Above Normal Parameters

10/23/2018

Drawings

6M721-2034

Diagram Core Spray System C.S.S. Reactor Building

AS

6M721-5707

Core Spray System Functional Operating Sketch

AG

6M721-5730-3

Non-Interruptible Control Air System Division I & II

Functional Operating Sketch

AL

6M721-5734

Emergency Diesel Generator System Functional Operating

Sketch

BH

6M721N-2046

P&ID Diesel Generator System Division I RHR Complex

AF

6M721N-2048

P&ID Diesel Fuel Oil System and Lube Oil System Division I

RHR Complex

AL

Miscellaneous

T13019

Temporary Change Notice - Fire Water Suppression System

Procedures

23.129

NIAS Divisions 1 and 2 Control Air Startup

117

23.203

Core Spray System

23.307

Emergency Diesel Generator System

27

28.504.03

Fire Suppression Water System Simulated Automatic

Activation Test

Work Orders

49771706

Perform 28.504.09 Electric Fire Pump Monthly Operability

Test

07/02/2019

50002740

Perform 28.504.09 Electric Fire Pump Monthly Operability

Test

07/30/2019

71111.04S

Drawings

6M721-5357

Emergency Equipment Cooling Water System Division II

BU

6M721-5444

Emergency Equipment Cooling Water System Division I

CC

Procedures

23.127

Reactor Building Closed Cooling Water/Emergency

Equipment Cooling Water System

145

71111.05Q Corrective Action

Documents

19-24505

2019 Fire Protection Self-Assessment Deficiency -

Investigate GSW Fire Rated Assemblies to be Included into

TRM 3.12.8

06/13/2019

19-26383

Diesel Fire Pump Room Fire Doors were Found Blocked

Open Without a Fire Impairment

08/23/2019

19-26426

Need DCR for Diesel Fire Pump Procedures to Address Log

Entry while Fire Doors to Diesel are Open

08/26/2019

Fire Plans

FB-AB-5-16b

Auxiliary Building, South Standby Gas Treatment System

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

(SGTS) Room, Zone 16, EL. 6776

FP-AB-5-16a

Auxiliary Building North Standby Gas Treatment (SGTS)

Room, Zone 16, Elevation 6776

FP-AB-5-16b

Auxiliary Building, South Standby Gas Treatment System

(SGTS) Room, Zone 16, Elevation 6776

Miscellaneous

9A.4-44

Fermi 2 UFSAR

TR 3.12.8

Fire Protection Fire Rated Assemblies

Procedures

28.502.02

CO2 System Valve Lineup Verification

35.000.242

Barrier Identification/Classification

FP-AB-BMT-4

Control Air Compressor Room, Zone 4 Elevation 5510

FP-GSW-1-31

General Service Water Pumphouse Zone 31

FP-RB-B-5b

Reactor Building Basement Northeast Corner Room Zone 5,

Elevation 5620

FP-RB-SB-5a

Reactor Building Sub-Basement Northeast Corner Room,

Zone 5, Elevation 5400

Work Orders

47714949

Perform 28.502.18 Division 1 SGTS CO2 Actuation Test

2/13/2018

48565671

Perform 28.502.18 Division 2 SGTS CO2 Actuation Test

01/31/2019

71111.06

Calculations

DC-5426

PBOC - High and Moderate Energy Line Break Evaluation

D

Corrective Action

Documents

19-23894

NRC Identified Concern: Housekeeping in Torus

05/21/2019

Drawings

29.100.01 SH 5

Secondary Containment and Radiation Release

6A721-2000-01

Reactor Building Sub-Basement Plan Elevation 5400 Scale

1/8=1-0

M

6A721-2000-02

Reactor Building Basement Plan Elevation 6520

N

6M721-2032

Sump Pump Diagram Radwaste System

BR

6M721-2224

Diagram Floor Drains All Floors Auxiliary and Reactor

Buildings

AA

7M721-2218

Floor and Equipment Drains Sub-Basement Plan Reactor

Building

Y

Procedures

ARP 2D82

Reactor Building Torus Sump Level Hi-Hi/Lo-Lo

ARP 2D83

Reactor Building Leakage to Torus Sump High

71111.11Q Miscellaneous

Reactivity

Maneuvering Plan

September 2019 RPA

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

SS-OP-904-1903

Evaluation Scenario

Procedures

MOP19

Operations Conduct Manual, Reactivity Management

26A

71111.13

Corrective Action

Documents

19-26718

Minimum Flow Line for Alternate Diesel Fire Pump Detached

from Pump Discharge Line

09/07/2019

19-26837

CTG Black Start Capability Removed When Relied Upon for

FPEE-19-0003

09/11/2019

Drawings

6M721-5444

Emergency Equipment Cooling Water Division 1

CC

Miscellaneous

EF2-PRA-005.11

High Pressure Coolant Injection (HPCI) System - System

Information Notebook

MMR12

Equipment Out of Service Risk Management

ODE-20

Protected Equipment

Procedures

20.300.120kV

Loss of 120kV

20.300.SBP

Loss of Offsite and Onsite Power

23.202

High Pressure Coolant Injection System

116

23.206

Reactor Core Isolation Cooling System

103

23.208

RHR Complex Service Water Systems

26

23.501.01

Fire Water Suppression System

MMR App H

On-Line Core Damage Risk Management Guidelines

MMR12

Equipment Out of Service Risk Management

MOP05-100

Protected Equipment

2C

ODE-20

Protected Equipment

71111.15

Calculations

DC-0623

Standby Liquid Control System Design Calculations

A

DC-4997

Standby Liquid Control Instrumentation Surveillance

Calibration

D

DC-4997

SLC Design Value Changes to Meet Power Uprate/Higher

Energy Cycles

DC-5961

WS01 Boron Injection Variables

DC-5962

WS01A Boron Weight Equivalents

Corrective Action

Documents

16-26260

Diesel Fire Pump Angle Drive Inspection Findings

08/09/2016

19-21369

Tech Spec 3.1.7 Figure 1 SLC Tank Level Limits Potentially

Non-Conservative

2/21/2019

19-24615

Diesel Fire Pump Engine SWI>Action Level B

06/18/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

19-25694

TRM Surveillance Requirement 3.6.1.1 Not Referenced in

Procedure or SST Event and Potentially Not Performed in

RF19

07/29/2019

19-26111

Condition of the DFP Right Angle Anti-Rotational Clutch

08/13/2019

19-26174

RCIC Flow Controller Issue Unable to be Resolved Under

WO 53945247

08/15/2019

19-26186

Lack of Follow-Through on a Known Component Degraded

Condition

08/16/2019

19-26198

RCIC Flow Issue

08/16/2019

19-26237

Missing Bolts in DFP Right Angle Drive

08/19/2019

19-26362

While Performing 44.010.143 Division 2 RPS Two Out of

Four Logic Module Functional Test on APRM 2 OPRM Trip

Light Did Not Come On Nor Did RPS Test Box Light Come

On (Both Acceptance Criteria)

08/22/2019

19-27084

Review and Address CARD Quality Issues with CARD 19-

20002

09/20/2019

Drawings

107E5901WH

C5100, C51R809A & B

107E5901WH

Two-Out-Of-Four Logic Module

29.100.01 SH 1A

RPV Control - ATWS

29.100.01 SH 3A

RPV Flooding & Emergency Depressurization - ATWS

6I721-2145-18

Schematic Diagram Power Range Neutron Monitoring

Reactor Protection System Outputs

H

6I721-2155-04

Schematic Diagram Reactor Protection System Relay

Tabulation

X

6I721-2155-07

Schematic Diagram Reactor Protection System Trip System

B System Relays

X

6I721-2155-08

Schematic Diagram Reactor Protection System Trip System

A Scram Trip Logic

M

6I721-2155-10

Schematic Diagram Reactor Protection System Scram

Solenoids

N

6I721-2235

RCIC System Instrumentation Loop

W

6I72102155009

Schematic Diagram Reactor Protection System Trip System

B Scram Trip Logic

M

6M721-2034

Core Spray System C.S.S. Reactor Building

AS

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

6M721-2044

Reactor Core Isolation Cooling System

BE

6M721-2045

Reactor Core Isolation Cooling (RCIC) System Barometric

Condenser

AS

Miscellaneous

MQA13-100

Quality Assurance Conduct Manual, Trend Condition

Evaluation Report

TE-P80-19-035

Condition of the Diesel Fire Pump Right Angle Drive

Procedures

44.110.004

Remote Shutdown RCIC Flow Indication Calibration

Work Orders

53945247

RCIC Pump Discharge Flow Transmitter Elec

71111.18

Corrective Action

Documents

19-27387

Alternate Diesel Fire Pump Trip during Weekly Surveillance

Run

09/30/2019

Drawings

6I721-2080-51

Visual Annunciator & Sequence Recorder Alarm Schematic

V

6I721-2125-06

Control System Feedwater (DCS-FW) External Connections

H

6I721-2331-07

Schematic Diagram Gland Sealing Steam Exhauster (E&W)

G

6M721-5733-1

Fire Protection Functional Operating Sketch

BX

Engineering

Changes

19-0014

Alternate Diesel Fire Pump (ADFP)

C

Engineering

Evaluations

FPEE-19-003

TR LCO 3.0.3 Evaluation for the Non-Functional Diesel Fire

Pump TRM Section TR3.12.2

Miscellaneous

EDP-37673

EDP Continuation Sheet - Scope of Work

Fermi 2 UFSAR

Other Auxiliary Systems

LRN-01-0410,

LCR H01-03

Letter to NRC from PSEG Nuclear LLC, Request for Change

to Technical Specifications Mechanical Vacuum Pump Trip

Instrumentation Hope Creek Generating Station Facility

Operating License NPF-57 Docket No. 50-354

01/04/2002

Work Request

Revision

55179348

PMT and TRSR Verification for TM 10-0014, Revision E

Procedures

28.504.03

Fire Suppression Water System Simulated Automatic

Actuation Test

Work Orders

54828250

TM 19-0014, Install Alternate Diesel Fire Pump at Pump

House

08/16/2019

54938127

Perform Temporary Diesel Fire Pump Weekly Operability

Test

09/12/2019

71111.19

Corrective Action

19-25181

Schedule Adherence A Work Not Completed as Scheduled

07/09/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Documents

19-26850

CTG 11-1 Lube Oil Leak

09/12/2019

19-26876

CTG 11-1 DC Power Supply Failure Alarm During SOP Run

09/12/2019

Drawings

6I721-2095-14

Schematic Diagram Nuclear Steam Supply Shut Off System

Trip System A

O

6I721-2095-18

Schematic Diagram NSSS System Main Steam Line

Outboard Isolation Valves B2103F028A, B, C, D

S

6I721-2155-22

Schematic Diagram Reactor Protection System Testability

Modification

L

Engineering

Changes

70056

CTG 11 Fuel Oil Tank Replacement

C

Miscellaneous

Fermi 2 Archived Operator Log

09/24/2019 -

09/26/2019

NRC-02-0036

Letter from Detroit Edison to NRC: Proposed Technical

Specification Change (License Amendment) - Response

Time Testing

05/23/2002

Procedures

23.324

Supervisory Control-120 KV Switchyard and CTG 11

Generators

23.601

Instrument Trip Sheets

35.318.017

Inspection and Testing of Multi-Contact Auxiliary Relays

44.020.011

Response Time Test of B21-N081A Reactor Vessel Low

Water Level 1 Transmitter

Work Orders

299261

Replace RPS Channel A2 Reactor Vessel Level 1 and 2

Agastat Relays

07/09/2019

46187487

Replace Desiccant in Division 2 NIAS Dryer

09/24/2019

244081

Change Crankcase Oil, Inspect Belts, Lube Motor Bearings,

and Clean Exterior

09/12/2019

50349443

Clean and Inspect CTG 11-1 Water Cooler and Inspect

Cooler Belts

04/02/2018

50349457

Calibrate 63HR Hydraulic Ratched Pressure Switch on CTG

11-1

04/02/2018

50349598

Semi-Annual Inspection of CTG 11-1

04/02/2018

50452150

Piping Tie In (FOST)

04/15/2018

54721898

CTG 11-1 Liquid Fuel Pump Bypass Servo Valve is Leaking

Fuel Oil While CTG is Operating

08/06/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

55165181

Repair CTG 11-1 Lube Oil Leak

09/12/2019

71111.22

Corrective Action

Documents

17-26455

Procedure Revision for LPCI Swing Bus Surveillance

24.321.07

08/01/2017

19-26353

HPCI Barometric Condenser Vacuum Pump Flashing Amps

08/22/2019

Drawings

6I721-2573-11

Schematic Diagram 480V Essential Bus 72C Position 3C &

MCC 72C-F Position 1C

Q

6M721-2035

High Pressure Coolant Injection System (HPCI) Reactor

Building

BN

6M721-2043

High Pressure Coolant Injection System Barometric

Condenser (HPCI) Reactor Building

AJ

6M721-2083

Residual Heat Removal (RHR) Division 2

CB

6SD721-2510-01

One Line Diagram 480V Essential Bus 72B, 72C, 72E, and

2F

BA

Miscellaneous

DC-0367

Pump Curves and Requirements, Volume 1

Q

Procedures

23.307

Emergency Diesel Generator System

26

24.202.01

HPCI Pump and Valve Operability Test at 1025 PSI

119

24.204.06

Division 2 LPCI and Suppression Pool Cooling/Spray Pump

and Valve Operability Test

24.307.33

Emergency Diesel Generator No. 14-24 Hour Run Followed

by Hot Fast Restart

Work Orders

48747466

Perform 24.404.06 Division 2 LPCI and Torus Cooling/Spray

Pump and Valve Operability Test

03/01/2019

49471252

Perform 24.204.06 Division 2 LPCI and Torus Cooling/Spray

Pump and Valve Operability Test

05/30/2019

49759149

Perform 24.321.07 480V Swing Bus 72 CF Automatic

Throw-Over Scheme Operability

07/08/2019

244112

Perform 24.202.01 HPCI Pump/Flow Test and Valve Stroke

at 1025 PSIG

08/20/2019

298122

Perform 24.204.06 Division 2 LPCI and Torus Cooling/Spray

Pump and Valve Operability Test

08/21/2019

71124.08

Corrective Action

Documents

CARD 18-21171

Dose Estimate Exceeded When Loading 8-120 Liner for

Transportation

2/12/2018

CARD 18-22666

Vendor Box Arrived on Site as a Non-Radioactive Shipment

With a RAM Tag

03/30/2018

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

CARD 18-23247

Telepole Failed Source Check Following RAM Shipment

Receipt

04/22/2018

Corrective Action

Documents

Resulting from

Inspection

CARD 19-25399

NRC Identified - Repairs to Spent Resin Tank Required

07/17/2019

Miscellaneous

NPRP-19-0016

Scaling Factors Report Dated February 4, 2019

2/14/2019

Procedures

65000.506

Shipping Low Specific Activity (LSA) Radioactive Material

65000.509

Shipping Greater Than A1, A2 Quantities of Radioactive

Material

65000.510

Shipping Limited Quantity of Radioactive Material

65000.610

Shipping Cask USA/9168/B(U)

Shipping Records EF2-17-136

Dewatered Resin Liner, LH-16-017

01/12/2018

EF2-18-003

Dewatered Resin Liner, LH-16-007

01/19/2018

EF2-18-009

Dewatered Resin Liner, LH-17-005

2/12/2018

71151

Corrective Action

Documents

Resulting from

Inspection

19-27175

NRC Identified Typographical Error in RCIC Monthly

Performance Indicator

09/24/2019

Miscellaneous

MSPI Derivation Report - Cooling Water System-

Unavailability Index

06/30/2019

Fermi 2 RHR Performance Indicators

08/01/2018 -

07/31/2019

MSPI Derivation Report - Residual Heat Removal System-

Unreliability Index

06/30/2019

MSPI Derivation Report - Residual Heat Removal System-

Unavailability Index

06/30/2019

Fermi 2 RCIC Performance Indicators

07/01/2018 -

06/30/2019

MSPI Derivation Report - Heat Removal Systems-

Unreliability Index

06/30/2019

N/A

Monthly Performance Indicator Submittal to the NRC for

Occupational Exposure Control Effectiveness

07/01/2018 -

06/01/2019

N/A

Monthly Performance Indicator Submittal to the NRC for

07/01/2018 -

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

RETS/ODCM Radiological Effluent Occurrences

06/01/2019

N/A

Monthly Performance Indicator Submittal to the NRC for

RCS Specific Activity

07/01/2018 -

06/01/2019

71152

Corrective Action

Documents

CARD Search Results, Keyword=Incorrect Part

01/01/2019 -

09/13/2019

19-21685

NQA Elevation - Leaders Actions Have Been Insufficient in

Correcting Fundamental Worker Behaviors for the Control

and Traceability of Safety-Related Material, Parts, and

Components

03/05/2019

19-21750

OSC Cognitive Trend in Supply Chain Performance Issues

03/06/2019

19-23431

Cognitive Trend: Non-Maintenance Related Rework Events

Due to Inadequate Engineering Parts Evaluations

05/03/2019

19-25682

Late Adds - Material Being Added to Work Orders Inside of

T10 (Adverse Trends per OSC)

07/29/2019

19-27524

NRC Identified Trend - Parts Issues

10/03/2019

Miscellaneous

NPMA-16-0040

Effectiveness Review for CARD 15-22778: NQA Audit

Finding - Safety Related (QA1) and Non-Safety (NQ) Spare

Parts Improperly Maintained

04/05/2016

Work Orders

44401214

PM: ME76; Perform MRTW of Unused Q Material from MEP

Buildings

05/20/2017

44477754

PM: ME77; Perform MRTW of Unused Q Material from MOV

Shop and Building 49

05/19/2017

71153

Corrective Action

Documents

18-30364

MSL B Flowrate Meter Downscale

2/25/2018

19-20002

4D32 MSL RADN MON GS STM EXHS Trip Enabled

Cleared with Power Less Than 10 Percent

01/01/2019

19-24865

19-20002-08 Performance Gap Analysis Tracking

06/28/2019

19-26836

NRC Identified 45.618.003 Reactor Feedwater System

Bailey DCS Maintenance Incomplete Information

09/11/2019

19-27084

Review and Address CARD Quality Issues with CARD 19-

20002

09/20/2019

Procedures

20.000.07

Fuel Cladding Failure

23.107

Reactor Feedwater and Condensate Systems

149

45.618.003

Reactor Feedwater System Bailey DCS Maintenance

ARP 3D82

Main Steam Line CH A/B/C/D Radiation Monitor Hi-Hi

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

MES90-119

Preparation and Control of Engineering Design Packages

MWC10

Work Control Conduct Manual-Chapter 10, Work Package

Preparation

Work Orders

2849877

Main Steam Line Flow Failed for Steam Lines on DCS Flat

Panel Display, Halt/Restart Both FW DCS Processors

01/1/2019