IR 05000341/2019010

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Biennial Problem Identification and Resolution Inspection Report 05000341/2019010
ML19273A900
Person / Time
Site: Fermi DTE Energy icon.png
Issue date: 09/30/2019
From: Eric Duncan
Reactor Projects Region 3 Branch 4
To: Fessler P
DTE Energy
References
IR 2019010
Download: ML19273A900 (24)


Text

September 30, 2019

SUBJECT:

FERMI POWER PLANT, UNIT 2BIENNIAL PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000341/2019010

Dear Mr. Fessler:

On August 16, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed a problem identification and resolution inspection at your Fermi Power Plant, Unit 2 and discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

The NRC inspection team reviewed the stations corrective action program and the stations implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for corrective action programs. Based on the sample reviewed, the team determined that the station had a low threshold for identifying issues and entering them into the Corrective Action Program. A risk-based approach was used to determine the significance of the issues and priority for issue evaluation and resolution. Corrective actions were usually implemented in a timely manner, commensurate with their safety significance.

However, the team identified examples of weaknesses in evaluating problems, and in the timeliness of corrective actions taken to resolve those problems.

The team also evaluated the stations processes for use of industry and NRC operating experience information and the effectiveness of the stations audits and self-assessments.

Based on the samples reviewed, operating experience was generally entered into the Corrective Action Program when appropriate and evaluated in accordance with Corrective Action Program implementing procedures. The use of operating experience was integrated into daily activities and found to be generally effective in preventing similar issues at the plant. In addition, self-assessments and audits were conducted at appropriate frequencies with sufficient depth for most departments based on the documents the team reviewed. Most of the self-assessments reviewed were found to be effective in identifying site performance deficiencies, programmatic concerns, and improvement opportunities. However, the team identified some weaknesses in your audits and self-assessments, and some inadequacies in your evaluation of industry and NRC operating experience.

Finally the team reviewed the stations programs to establish and maintain a safety conscious work environment, and interviewed station personnel to evaluate the effectiveness of these programs. Based on our review of your recent safety culture assessments and the results of the interviews we conducted, the team did not identify any impediment to the establishment of a safety conscious work environment. Your staff was aware of and generally familiar with the Corrective Action Program and other station processes, including the Employee Concerns Program, through which concerns could be raised.

The NRC inspectors did not identify any finding or violation of more than minor significance.

Based on the samples reviewed, and although a finding or violation was not identified during this inspection, the range and number of identified deficiencies and weaknesses in the Corrective Action Program and supporting processes led the team to conclude that your overall implementation of the Corrective Action Program at Fermi was marginally effective.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Eric R. Duncan, Chief Branch 4 Division of Reactor Projects

Docket No. 05000341 License No. NPF-43

Enclosure:

As stated

Inspection Report

Docket Number:

05000341

License Number:

NPF-43

Report Number:

05000341/2019010

Enterprise Identifier: I-2019-010-0047

Licensee:

DTE Electric Company

Facility:

Fermi Power Plant, Unit 2

Location:

Newport, MI

Inspection Dates:

July 29, 2019 to August 16, 2019

Inspectors:

V. Meghani, Reactor Inspector

R. Ng, Project Engineer

J. Rutkowski, Project Engineer

A. Shaikh, Senior Reactor Inspector

T. Taylor, Resident Inspector

Approved By:

Eric R. Duncan, Chief

Branch 4

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a biennial problem identification and resolution inspection at Fermi Power Plant, Unit 2 in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

OTHER ACTIVITIES - BASELINE

71152B - Problem Identification and Resolution Biennial Team Inspection (IP Section 02.04)

(1) The inspectors performed a biennial assessment of the licensees corrective action program, use of operating experience, self-assessments and audits, and safety conscious work environment.
  • Corrective Action Program Effectiveness: The inspectors assessed the corrective action programs effectiveness in identifying, prioritizing, evaluating, and correcting problems.
  • Operating Experience, Self-Assessments and Audits: The inspectors assessed the effectiveness of the stations processes for use of operating experience, audits, and self-assessments.
  • Safety Conscious Work Environment: The inspectors assessed the effectiveness of the stations programs to establish and maintain a safety conscious work environment.

INSPECTION RESULTS

Assessment 71152B Based on the samples reviewed, and the range and number of deficiencies and weaknesses in the licensee's Corrective Action Program and supporting processes that were identified through these samples, the team concluded that the licensee's implementation of the Corrective Action Program was marginally effective.

Effectiveness of Problem Identification:

Based on the samples reviewed, the team concluded that the licensee continued to identify issues at a low threshold and appropriately entered these issues into the Corrective Action Program. The team determined that problems were usually entered into the Corrective Action Program in a complete and accurate manner.

The team also noted that some deficiencies were identified by external organizations, including the NRC, that had not been previously identified by licensee staff and were subsequently entered into the Corrective Action Program. These externally-identified deficiencies represented missed opportunities by licensee staff to identify issues to be addressed through the Corrective Action Program.

The team found that the licensee utilized a number of Corrective Action Program support processes to identify problems, including the self-assessment and audit process and the Operating Experience Program. The licensee generally performed adequate department self-assessments and quality assurance audits to identify issues in station processes. Similarly, the licensee generally screened issues from both NRC and industry operating experience and entered them into the Corrective Action Program when they were applicable to the station.

However, the team identified several issues related to the self-assessment process and the Operating Experience Program. Details of these issues are discussed in the Observation section of this report.

The team determined that the licensee was generally effective at trending low level issues and taking appropriate corrective actions to prevent more significant issues from developing.

The licensee used the Corrective Action Program to document instances in which previous corrective actions were ineffective or were inappropriately closed.

The team performed a 5-year review of emergency diesel generator leakage. As part of this review, the team interviewed the emergency diesel generator system engineer, reviewed corrective action resolution documents (CARDs), plant health reports, and condition evaluations. In addition, the team performed a system walkdown to assess the material condition of the emergency diesel generator system and surrounding areas. The team concluded that emergency diesel generator leakage concerns were identified and entered into the Corrective Action Program at a low threshold, and concerns were resolved in a timely manner commensurate with their safety significance. For the areas walked down, the team did not identify any additional issues.

Effectiveness of Prioritization and Evaluation of Issues:

Based on the samples reviewed, the team determined that licensee performance was adequate with opportunities for improvement at prioritizing and evaluating issues commensurate with the safety significance of the identified problem. The Ownership Screening Committee and the Management Review Committee meetings were generally thorough and intrusive in reviewing issues and prioritizing actions. The team observed a productive dialogue between the members of these committees and the members challenged each other when dispositioning CARDs.

In general, once a degraded or non-conforming condition was identified, the Corrective Action Program directed that an equipment operability or functionality review be performed. The majority of the samples reviewed were evaluated in a timely manner. However, the team identified an issue with the technical rigor of some of these evaluations. Additional details of this issue are discussed in the Observation section of this report.

The team identified several issues related to the untimely screening and inadequate evaluation of operating experience. Additional details of these issues are described in Observation section of this report.

Effectiveness of Corrective Actions:

Based on the samples reviewed, the team determined that the licensee was adequate with opportunities for improvement in corrective action implementation. In general, corrective actions for deficiencies that were safety significant were implemented in an adequate and timely manner. Problems identified using a root cause or other cause methodologies were, in general, resolved in accordance with Corrective Action Program requirements. The corrective actions assignments that were sampled by the team for selected NRC documented violations and for licensee event reports (LERs) were generally effective and timely.

However, the team identified a relatively high number of systems that were categorized as Maintenance Rule (a)(1). The team reviewed selected Maintenance Rule (a)(1) systems and their corrective action plans and concluded there was a weakness in the licensee's equipment reliability program. Additional details of this weakness are discussed in the Observation section of this report.

The team also identified that corrective actions from Self-Assessments and Nuclear Quality Assurance (NQA) audits were not always implemented in a timely manner. Additional details of these issues are described in Observation section of this report.

Assessment 71152B Based on the samples reviewed, the team determined that licensee performance in the use of operating experience was adequate with some opportunities for improvement. The licensee screened industry and NRC operating experience information for station applicability. Based on these initial screenings, the licensee initiated actions in the Corrective Action Program to fully evaluate the impact, if any, to the station. When applicable, actions were developed and implemented to prevent similar issues from occurring. Operating experience lessons learned were communicated and incorporated into plant operations. The team observed the information being used in daily activities, such as pre-job briefs, as well as CARD reviews and investigations. However, the team identified a number of issues regarding the timeliness of the screening and technical rigor of Operating Experience evaluations. These issues are further discussed in the Observation section of this report.

Assessment 71152B Based on the samples reviewed, the team determined that the licensee's performance of self-assessments and audits was adequate with some opportunities for improvement. The licensee performed department self-assessments and quality assurance audits throughout the organization on a periodic basis. These self-assessments and audits were generally effective at identifying issues and enhancement opportunities at an appropriate threshold.

The self-assessments and audits reviewed by the team identified issues that were not previously known, including issues within the Corrective Action Program itself. Nuclear Quality Assurance (NQA) identified deficiencies with the licensee's processes and those issues were addressed by the station through the Corrective Action Program. However, the team identified several weaknesses between department self-assessments and NQA audits.

These weaknesses were related to the ability of the self-assessment and audit programs to cause timely, lasting change and prevent more significant issues from occurring. Additional details are discussed in the Observation section of this report.

Assessment 71152B Based on a review of documents and interviews with licensee staff, the team did not identify any impediment to the establishment of a safety conscious work environment.

The team reviewed the results from the 2018 Nuclear Safety Culture Assessment (NSCA)performed by the licensee, the subsequent root cause evaluation that was completed as prescribed by CARD 19-23612, Station Leaders Have Allowed a Culture of Rationalizing and Tolerating Unacceptable Performance, and Nuclear Safety Culture Monitoring Panel meeting minutes. The team also conducted focus group meetings and one-on-one interviews with more than 50 licensee staff concerning the effectiveness of the Corrective Action Program, the ability to raise issues, and the freedom from potential retaliation for raising issues.

In general, the licensee's staff was aware of and familiar with the Corrective Action Program and other processes, such as the Employee Concerns Program, to raise nuclear safety concerns. Licensee staff indicated they could raise safety concerns without a fear of retaliation. Through the interviews and document reviews, the team was not provided or identified any examples of retaliation for raising nuclear safety concerns. Although some work groups felt that the Corrective Action Program was not effective for addressing low level issues, the staff interviewed believed that operational issues and issues with high safety significance were being appropriately addressed in a timely manner.

Observation: Evaluation Technical Rigor Weaknesses 71152B During this inspection, the team identified a number of examples in which the licensees evaluations lacked technical rigor. In several cases, incorrect assumptions were used in decision-making processes such that the significance of the issue was marginalized, or the corrective actions were delayed.

For example, during the review of a Nuclear Quality Assurance (NQA) audit finding documented in CARD 19-20869, Inadequate Control of Safety-Related Fuses Maintained and Installed by Operators, the team identified that the shift manager relied on the successful operation of safety-related systems following fuse replacements and continued satisfactory performance of surveillances as an indicator of the safety-related pedigree of the newly installed fuses. The shift manager concluded that no nonsafety-related fuses had been installed in safety-related systems. Since satisfactory performance of post-maintenance testing and surveillances was not necessarily indicative of fuse performance at designed fault or over-current conditions, the team questioned the licensees operability conclusion. The licensee then provided an alternate basis for operability, which included operator interviews following the NQA audit finding and the procedure requirements to verify and document that correct fuses were being installed for use. However, the team noted that the NQA audit finding specifically stated that operators were not documenting the fuse replacement information and that safety-related and nonsafety-related fuses were stored in the same lockers. The licensee subsequently performed a cross-verification of safety-related and nonsafety-related fuses located in the same locker and determined that safety-related fuses did not have corresponding nonsafety-related fuses in the same locker boxes based on examining the procurement master material list. The licensee entered this issue into their Corrective Action Program as CARD 19-25794.

During the review of CARD 08-26828, Non-Qualified Support System to Ensure Adequate Post-LOCA [Loss-Of-Coolant-Accident] Emergency Depressurization, the team noted that this issue had been identified more than 10 years ago, but had not yet been resolved. This issue was associated with the qualification of equipment relied on to mitigate a design basis small break LOCA. The licensee classified this issue as a condition adverse to quality, but considered the emergency core cooling system fully operable. Following discussions with Engineering and Operations staff, the team determined that the staff in these departments did not have a common understanding of the issue. Operations staff stated they would follow the subject emergency operating procedure and restore the air system to containment when required to emergency depressurize the reactor pressure vessel. Engineering staff, however, understood that the air system may be available, but could not be relied upon for design basis accident mitigation because the equipment was not safety-related. This information was not shared between the two groups. It was unclear why Operations staff did not obtain that information from Engineering staff, even after the team posed the question. Therefore, the team concluded that a lack of technical rigor in the licensees operability determination for CARD 08-26828 led to an incorrect conclusion. The licensee entered this issue into their Corrective Action Program as CARD 19-26112 and 19-26154. At the end of the inspection, no additional compensatory actions were required since the licensee had recently verified that adequate trapped air inside the drywell piping had always been available to support emergency depressurization. As a result, the team did not identify a finding or violation of more than minor significance.

Both examples highlighted a lack of technical rigor in the licensees evaluation. As a result, incorrect assumptions were relied upon in the licensees decision-making process. At the end of the inspection, the licensee planned to evaluate this identified weakness through the CARDs identified above.

Observation: Equipment Reliability Program Weaknesses 71152B At the time of this inspection, 14 systems were in a Maintenance Rule (a)(1) status; which was unusually high, particularly for a single unit site. The team reviewed the Maintenance Rule (a)(1) system performance recovery plans for selected systems and interviewed the stations Maintenance Rule Program coordinator. As associated with these Maintenance Rule (a)(1) systems, the team also reviewed all Tier 1 system health reports and several Tier 2 and Tier 3 system Corrective Action Program documents. The licensee utilized system health reports as a trending tool for Tier 1 systems.

The team determined that the performance recovery plans were detailed and listed requirements and actions to return the systems to a Maintenance Rule (a)(2) status. The team concluded that the licensee had appropriately documented equipment issues that led to a Maintenance Rule (a)(1) status in the Corrective Action Program. Given that system health reports were generated only for Tier 1 systems and not considered in the Maintenance Rule review process, it was unclear if the licensees equipment trending practices could have identified an issue and taken actions prior to reaching a Maintenance Rule (a)(1) status. The team considered this a weakness in the licensees equipment reliability program.

The licensee completely revised procedure FBP-41, Equipment Reliability Program, in March 2019. This revised procedure described, a risk informed approach that extended beyond reliability initiatives to ensure emphasis of condition-based maintenance to minimize unavailability while maximizing reliability. It included activities that were essential for effective life cycle management, by ensuring proper prioritization, scheduling, and integration into site long range plans. This process supported a zero tolerance for unplanned failures on critical equipment. The procedure provided a uniform prioritization process for a proposed change or issue. The resultant ranking provided a means to determine the projects and/or initiatives that should be funded and implemented. As a result, the licensee developed a list of modifications and changes, along with schedules for the completion of required actions. The team concluded that, if properly implemented, this new process, over time, could potentially improve equipment reliability.

Observation: Operating Experience Review Inadequacies 71152B While the licensee generally addressed Operating Experience identified by external organizations appropriately, the team identified several instances where the licensee's reviews of NRC and industry operating experience were inadequate.

Information Notice (IN) 2017-04, High Energy Arcing Faults (HEAF) in Electrical Equipment Containing Aluminum Components, was issued by the NRC in August 2017. The issue was entered into the licensee's Corrective Action Program as CARD 18-21869 in March 2018.

However, the corrective action to investigate the use of aluminum components as documented in the CARD was still open at the time of this inspection. Upon questioning by the team, the licensee determined that the concern of aluminum increasing the effects of a HEAF were limited since the electrical design specifications and the plant's Support Engineering Practice Standards only allowed a limited use of aluminum in the electrical design of the plant. Given that the plant was designed with the separation of safety-related trains and fire areas, the licensee determined that there was reasonable assurance that the electrical systems would meet their design functions during any fault on a nonsafety-related system or a single failure of a safety-related system. The licensee entered the timeliness concern identified by the inspectors into their Corrective Action Program as CARD 19-26081.

Information Notice 2017-06, Battery and Battery Charger Short-Circuit Current Contributions to a Fault on the Direct Current Distribution System, was issued by the NRC in September 2017. Although the IN was subsequently entered into the licensees database to be screened, the issue was not entered into the Corrective Action Program until March 2018. It was also noted that the evaluation performed for the IN was later found to be inadequate by an NRC inspection team in early 2019. As a result, a new evaluation was performed through CARD 19-23651, which identified an operable-but-nonconforming condition that required plant modifications. The licensee entered the timeliness concern identified by the inspectors into their Corrective Action Program as CARD 19-26102.

Further, the inspectors identified two examples where industry operating experience did not result in an engineering evaluation, despite their potential applicability to the main steam isolation valves (MSIVs). In the first example, Licensee Event Report (LER) 2017-002 described MSIV pilot valve binding due to potential foreign material. A second example associated with LER 2018-002 described slow MSIV closure times due to foreign material introduced by the vendor during manufacturing. For the 2018 LER, the site screened the issue as not applicable to Fermi. In the case of the 2017 LER, the station had not considered the operating experience at all. After the inspectors reviewed the operating experience and questioned the site regarding their applicability, the licensee issued CARD 19-26074 to evaluate applicability since Fermi used the same vendor for the refurbishment of their equipment.

Although the team did not identify any violations of NRC requirements, these issues represented inadequacies in the licensee's screening and evaluation of operating experience in a timely manner such that potential issues with safety-related equipment might go unnoticed. Specifically, the licensee failed to ensure that all available avenues for Operating Experience were reviewed for applicability as LERs often described issues that could pertain to other sites, especially when associated with the same vendor or with parts issues.

Additionally, the licensee did not ensure that personnel with an appropriate level of expertise were reviewing issued Operating Experience, especially when specific sites were not specifically identified in the operating experience documents that were received.

Observation: Self-Assessment and Audit Weaknesses 71152B The team reviewed several department self-assessments regarding the storage and staging of material. These assessments were conducted in April 2017, October 2017, and April 2018. In April 2017, the results of a department self-assessment documented that all critical attributes concerning material storage areas and staged material were met. However, in May 2017, NQA performed an audit in the same area and identified a number of findings and, multiple barrier failures and programmatic breakdowns, regarding the storage and staging of material. Similarly, a department self-assessment performed in October 2017 and April 2018 documented that all critical attributes were met. However, in March 2019, NQA issued an elevation letter citing numerous issues in the storage and staging of material, and the fact that previous NQA findings had not been resolved. The team determined that this apparent disparity between the department self-assessment conclusions and the NQA findings throughout the period called into question the quality of the department reviews.

In another example, the team reviewed a common cause analysis performed in November 2017 regarding the control of measurement and test equipment (M&TE). While the common-cause analysis highlighted weaknesses in the program and instituted corrective actions that ultimately reduced the number of current issues, the team noted a history of similar M&TE control issues that dated back to at least early 2015. Specifically, in January 2015, NQA performed an audit that identified issues in the control of M&TE after use and in the trending of M&TE deficiencies. In May 2015, a department self-assessment identified that M&TE users did not understand their responsibilities for controlling M&TE. In January 2016, the site identified an emerging trend in M&TE that was assumed to have failed or had been lost. In June 2017, an NQA audit prompted an apparent cause analysis to address multiple gaps in the M&TE calibration program and the process for the control and issuance of M&TE. Finally, in October 2017, another adverse trend in the same area was identified, which led to the common cause analysis.

The examples above demonstrated that the licensee's self-assessments and audits did not always identify performance gaps. Further, when performance issues were identified by self-assessments and audits, they sometimes recurred before being effectively addressed.

The team also reviewed NRC finding 05000341/2018004-01 regarding a valve stem and disc that was dropped during a lifting and rigging evolution in 2018, and a subsequent formal self-assessment on lifting and rigging. This assessment identified that the previous self-assessment in lifting and rigging performed in February 2016 was not adequate. Specifically, in 2016, a lifting and rigging department self-assessment failed to identify gaps in Fermi procedures relative to industry standards. That self-assessment also failed to identify gaps in the first line supervisor's ability to monitor lifting and rigging evolutions.

In addition to the licensee-identified issues with the 2016 assessment, the team determined that the licensee had missed an opportunity to determine whether worker behavior contributed to the 2018 stem and disc drop event. For instance, the various analyses that were performed by the licensee in response to the 2018 stem and disc drop event referred to a culture of taking short cuts, having a can-do attitude that leads to poor decision-making and substandard performance, and a failure to conduct an adequate pre-job brief. While the 2016 self-assessment included a critical attribute associated with fundamental behaviors, the focus of this assessment did not include human performance, but rather on recommended qualifications, training, and the definition of roles among crew members.

In the three examples listed above, the team noted there were no corrective actions developed to explore why self-assessments and audits were either inadequate or not timely in addressing problems. The team concluded that while self-assessments and audits were performed in accordance with licensee procedures, performance gaps went unnoticed or uncorrected. The team concluded that this indicated a lack of intrusiveness in the licensee's assessment and a lack of vigilance in correcting performance issues.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On August 16, 2019, the inspectors presented the biennial problem identification and resolution inspection results to Mr. P. Fessler and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71152B

Corrective Action

Documents

05-24876

Blown Scram Pilot Fuse

08/22/2005

07-22140

Reactor Recirculation Pump Driver Mount Drain Lines

Potentially Direct Unidentified Leak Sources into the

Identified Leak Path

04/19/2007

07-23630

CDBI - UFSAR Anti-Vortex Methodology Non-Conservative

06/28/2007

08-26828

Non-Qualified Support System to Ensure Adequate Post-

LOCA Emergency Depressurization

10/15/2008

08-27506

DC-0501 Vol 1 HPCI Key Calculation Review Results

11/11/2008

09-26761

Key Calculation Review of DC-5490 Vol. I, Ventilation Air

Quality for EDG Switchgear Room

09/01/2009

10-28090

Reactor Building Superstructure Re-Analysis

09/14/2010

11-29120

DC-0919 Recommended Setting Changes

10/06/2011

11-29284

Legacy Circuit Design Associated with the RHR 4.16kV Load

Shed Scheme

10/12/2011

2-21134

Evaluate OE35219 (Preliminary - Automatic Reactor Trip

and Loss of Offsite Power Due to Failed Switchyard

Insulator) for Applicability to Fermi

2/10/2012

2-23735

Main Steam Line Radiation Monitor F Cage Broken Bolts

04/24/2012

2-24521

Review BWROG SC05-03 Analysis

05/16/2012

2-29077

Reactor Scram Due to H2 In-Leakage to Stator Water

11/07/2012

13-10103

Main Steam Piping Support Exceeds Design Load

06/07/2013

13-22663

EDP - Setpoint Change is Required for the TSC Upstream

HEPA Filter DP Switch

04/15/2013

13-24841

EDG Steady State Voltage and Frequency Technical

Specification Ranges

07/10/2013

14-21857

Configuration Control Discrepancy: Drawing M-3184-1

Doesn't Reflect the Plant Configuration of the Division 2

RHRSW Piping

03/01/2014

14-22610

Repetitive Failures of RPS Relay K17B

03/20/2014

14-22612

EDG 11 Manually Tripped During Surveillance Test Due to

Fire from Turbocharger Lagging

03/20/2014

14-22646

EDG 11 Jacket Coolant Leak at Standby Heater Control

03/21/2014

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Switch

14-23829

Lube Oil Leak from Body of R3000F111B During EDG 13

Governor Vent Run

05/02/2014

14-25670

EDG Lockwire Gauge is Inconsistent

07/11/2014

14-27839

Warehouse Cannot Properly Store Spare MSIV Actuators

10/06/2014

15-20167

NQA Recommendation - Benchmark and Develop

Performance Metrics for M&TE Program

01/08/2015

15-20168

NQA Recommendation - Formalize How M&TE is Turned

Over After Use

01/08/2015

15-21132

Calculation (DC-4931) Damper Minimum Air Pressure

Calculation Identified Margin Issue

2/12/2015

15-21952

Replacement CRD Pump Not Stored IAW Vendor Manual

03/17/2015

15-22182

Warehouse Documentation Did Not Match ASME Tube Plug

Heat Codes for Drywell Cooler #2

03/25/2015

15-22883

NRC Identified Issue: EDG-14 Oil Leak

04/22/2015

15-22949

Review and Revise SAM Program Section 3.2

04/24/2015

15-23047

Crankcase Vacuum Tubing Cracked at Fitting

04/28/2015

15-23171

Excessive Smoke from EDG 14 During SOP Run

05/02/2015

15-23277

RHRSW Return from RHR HX High Temperature Alarm

Setpoints Above Piping Design Temperature

05/07/2015

15-23290

Leaking Bypass Valve

05/07/2015

15-23679

M&TE Users Do Not Understand Responsibilities

05/27/2015

15-24444

Jet Pump Failure AOP May be Non-Conservative

06/26/2015

15-25177

Recommend Spare Parts for RHRSW Pump/Motor

07/27/2015

15-26907

29.ESP.03 EOP Support Tool Box Damaged

09/27/2015

15-27998

Discrepancy Identified in Replacement Coupling and

Installed Coupling For CRD Pump Replacement

10/19/2015

16-20417

Emerging Trend - CARDS on Assumed Failures of M&TE

01/15/2016

16-21485

NRC Resident Question Regarding AOV T4600F406

2/17/2016

16-21963

Switch Calibration Drift

03/02/2016

16-23673

Independent RHRSW Inspection - Piping Calculation is

Inconsistent with Drawing

05/04/2016

16-24088

Fuel Oil Leak on EDG 11 Fuel Oil Transfer Pump B

05/18/2016

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

16-24244

Starting Air Leak Inside EDG 14 Starting Air Compressor Air

Dryer

05/21/2016

16-25611

2016 EQ Program Self Assessment Deficiency

07/14/2016

16-25666

Lube Oil Leak on EDG 12 Flex Coupling

07/17/2016

16-26533

2016 CDBI Issue: Non-Conformance to Licensing Bases for

Evaluation of Degraded Voltage

08/17/2016

16-26814

Inclement Weather Results in Unplanned LCO Entry, EOP

Entry, and 8 Hour Report to NRC

08/27/2016

16-27087

Additional Support Not Evaluated in Pipe Stress Calculation

09/06/2016

16-28543

Single Rod Scram of CR 26-07

10/26/2016

16-29549

New Spider Bearing 0.010" Larger than Previous One

Installed on RHR Service Water Pump

11/29/2016

16-29936

Siren Performance - 200 Amp Fuses

2/14/2016

17-00469

EDG 13 Fuel Tank Room

2/23/2017

17-20141

SPF Failed Test of Shut Down Relay from Overspeed

Simulation Per WO 43631018 PM 1291

01/05/2017

17-20163

Use of RPS Test Box May Cause Loss of RPS Function

01/06/2017

17-21316

CCA: Steam Leaks on High Pressure Turbine 1st Stage

Pressure Instrument Lines

05/16/2017

17-21382

RERP Drill 02/14/17: Failure of Follow-Up Notifications

Objective

2/17/2017

17-21385

Common Cause Evaluation: Negative Trend Seen in Follow-

Up Notifications Performance

05/11/2017

17-22078

Evaluate the Impact on EAL Threshold Values EP-101

Based on OCDM Revision

03/15/2017

17-22236

CCA: Trend in Radiation Protection TPE Failures

05/10/2017

17-23685

Common Cause Evaluation: Emerging Trend -

Mispositionings in Operations

06/02/2017

17-23736

Adverse Trend - Foreign Material Exclusion

04/20/2017

17-24655

EACE: Failure of E1150F068B, Division 2 RHRSW HX

Outlet FCV to Open

17-24758

NQA Audit Finding - Repeat Finding on Improper Controls of

Safety-Related (QA1) and Non-Safety (NQ) Material

05/23/2017

17-24845

Several DevonWay Operating Experience Evaluations are

05/25/2017

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Overdue

17-25157

Division 2 RHRSW is Exceeding Maintenance Rule

Performance Criteria

06/08/2017

17-25383

NQA Audit 17-0107 Finding - Procedures for M&TE

Calibration Methods Not Properly Approved and Controlled in

Accordance with QA Program

06/16/2017

17-25480

NRC Information Notice 2017-03

06/21/2017

17-25545

CFR Part 21 for NUMAC PRNM 386SX Computer Module

and ASP Module

06/23/2017

17-26069

E1150F068B Monitoring and Inspection WOs Needed

07/19/2017

17-26338

NQA Audit 17-0110 Deficiency - Radioactive Material (RAM)

Control Gaps and Inconsistencies

07/27/2017

17-26340

NQA Audit 17-0110 Deficiency - Poor Housekeeping Inside

Contaminated Areas

07/27/2017

17-26351

Received 17D41 For Division 2 DW Temperature High

07/27/2017

17-26708

Division 1 CCHVAC Supply Fan Vibration Trend

08/09/2017

17-26894

NRC Identified Issue with Firearms Instructor Qualification

08/16/2017

17-27148

2017 NRC FP Triennial: Review FPEE-16-0001 to Determine

if the Addition of Steps to 20.000.18 Have an Impact on Time

Critical Operator Actions

08/25/2017

17-27225

Elevated Dose Rates Observed Coming From the FPCCU

Precoat Tank

08/29/2017

17-28757

Cognitive Trend in Maintenance - Assumed Failures of M&TE 10/26/2017

17-29262

NRC RIS 2017-05: Administration of 10 CFR Part 72

Certificate of Compliance

11/16/2017

18-00690

EDG 11 Engine Room

08/22/2018

18-00983

Standby Heating Discharge Control Temperature Switch is

Leaking for EDG 14

11/28/2018

18-20628

NRC Issues Regulatory Issue Summary 2018-01 on 10 CFR Part 37 Issues

01/24/2018

18-20786

NRC ENS Phone Not Communicating Correctly

01/29/2018

18-21062

Continuing Vibration Trend Division 1 CCHVAC Supply Fan

Motor

2/07/2018

18-21062-01

Complete MPFF Evaluation on Division 1 CCHVAC

2/27/2018

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

18-21869

(OE 2017-0395) NRC Information Notice 2017-04 - High

Energy Arcing Faults in Electrical Equipment Containing

Electrical Components

03/06/2018

18-22371

Leak Identified on R3001C006

03/21/2018

18-22931

Dry Cask Noble Fission Gas Release Response Strategy

04/11/2018

18-24354

Oil Leak from Flange Supplying EDG #11 LO Filter

06/01/2018

18-24437

EACE: EDG 11 Lube Oil Leak

08/23/2018

18-25713

Equipment Cause Evaluation: Recirc Pump Seal Purge

Relief Valve B3100F015B Repetitive Failures

08/24/2018

18-27810

Increased Dose Rates Experienced During RF19

10/04/2018

18-28008

Organizational Effectiveness Evaluation: Unexpected Dose

Rate Conditions After Opening the G3352F001

10/08/2018

18-29027

Root Cause Evaluation Report: E1150F068B Did Not Close

as Expected

01/16/2019

18-29102

2018 NSCA Results - Trait CO.2 Basis for Decisions

11/07/2018

18-29367

Part 21 for ITT Conoflow for GT25 Current to Pressure

Transducers

11/19/2018

18-29568

New Replacement Stem and Disc Dropped from Rigging with

Personnel Injury

11/29/2018

18-29620

2018 LIR Reactor Recirculation - Seal Purge Relief Valves

11/30/2018

18-29672

EDG 14 Air Coolant Hx Leaking Coolant

2/02/2018

18-29775

Clogged Drain Lines Resulting in Multiple Leaks

2/07/2017

18-29870

Reactor Building to Suppression Chamber Vacuum Breaker

UFSAR Nonconformance

2/08/2018

18-30322

EDG 13 JCS STBY Circulating Pump Seal Leaking

2/21/2018

18-30330

Adverse Trend in Lifting and Rigging Practices

2/21/2018

18-30400

NQA - Valve R3000F118B (Lube Oil Source Valve for

R30NA11B) Has Slight Weeping

2/27/2018

19-00209

130 DPM Leak from EDG 11 Coolant Standby Heating - Low

Temp SW Elec

04/08/2019

19-20549

EDG 13 Standby Lube Oil Pump Leak

01/24/2019

19-20652

Provide Additional Training/Information Regarding the

Purpose and Value of the Site Corrective Action Process

01/29/2019

19-20869

NQA Audit 19-0101 Finding: Inadequate Control of Safety-

2/06/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Related Fuses Maintained and Installed by Operations

19-21169

NRC Finding - Inadequate Lifting and Rigging Practices

Result in Damage to Division 2 Residual Heat Removal

Structures and Components

2/15/2019

19-21335

Operations Department Reset for Unacceptable Performance 02/20/2019

19-21397

  1. 1 and #9 Cylinder Liner Indicator Valve Adapter O-Rings

Found Leaking During Hydrostatic Test

2/22/2019

19-21433

NRC Violation - Inadequate Work Instructions for

Maintenance on EDG 14

2/25/2019

19-21685

NQA Elevation-Leaders Actions Have Been Insufficient in

Correcting Fundamental Worker Behaviors for the Control

and Traceability of Safety-Related Material, Parts, and

Components

03/05/2019

19-21969

Strategic Engineering Identified Part 21 Issue on Safety-

Related 4160V-480 Dry Transformers

03/13/2019

19-22077

EDG 13 Strategic Engineering Walkdown

03/18/2019

19-22412

SLC Ignition Continuity Loss Squib A

03/28/2019

19-22895

Evaluate Impact of Part 21 on SF-1154 Hydraulic Fluid Used

in Power Piping Snubbers

04/16/2019

19-23227

Recommend Review of Site Response to Open CARD 07-

23630

04/26/2019

19-23602

2019 AFI Station Leaders Have Not Corrected Worker

Behaviors Affecting Plant Status Control

05/09/2019

19-23612

Root Cause Evaluation of Culture that Allowed Rationalizing

and Tolerating Unacceptable Worker and Plant Performance

05/09/2019

19-23651

2019 DBAI: Information Notice IN 17-06 - Battery Chargers

(Ametek Chargers) May Contribute up to 10 Times their

Rating for a Short Period

05/10/2019

19-23897

No Tie-Down and/or Securing Devices Within the Off-Site

RET Team Van to Safely Secure Cargo

05/20/2019

19-24015

INPO Operating Experience Report for Exporting Radioactive

Material RIS 19-01 Clarification

05/24/2019

19-24107

Secondary Containment Doors Open at the Same Time

05/30/2019

19-24316

Tagouts/Protection Putting Operators at Risk

06/05/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

19-24655

DevonWay Errors Preventing Operating Experience

Evaluations from Being Properly Closed Out

06/20/2019

19-25978

2019 PI&R NRC Inspection Observation: CARD 19-24107 AI

  1. 4 Closure

08/07/2019

19-25988

2019 PI&R Inspection NRC Observations: Maintenance

Programs

08/07/2019

19-25989

2019 PI&R Inspection NRC Observations: Potential Missed

Opportunities to Address Maintenance Behavioral Gaps

08/07/2019

19-26074

2019 PIR - Evaluate Monticello MSIV OE

08/12/2019

19-26080

OE Review in DevonWay is Past Due

08/12/2019

Corrective Action

Documents

Resulting from

Inspection

19-25794

2019 PI&R Inspection - CARD 19-20869 Quality Less Than

Adequate to Support Conclusion of Reasonable Assurance

08/01/2019

19-25794

2019 PI&R Inspection - CARD 19-20869 Quality Less Than

Adequate to Support Conclusion of Reasonable Assurance

08/01/2019

19-25840

2019 NRC PI&R Inspection: NRC Identified Hanging Oil

Drops on EDG 11 Upper Air Start Distributor

08/02/2019

19-25840

NRC Identified Oil Drops on EDG 11 Upper Air Start

Distributor

08/02/2019

19-25933

Spec 3071-128-EJ Identified with a Deficiency

08/06/2019

19-25978

2019 PI&R NRC Inspection (Observation) - CARD 19-24107

AI #4 Closure

08/07/2019

19-25978

CARD 19-24107 AI #4 Closure

08/07/2019

19-25988

Maintenance Programs

08/07/2019

19-25988

2019 PI&R Inspection NRC Observations: Maintenance

Programs

08/07/2019

19-25989

2019 PI&R Inspection NRC Observations: Potential Missed

Opportunities to Address Maintenance Behavioral Gaps

08/07/2019

19-25989

Potential Missed Opportunities to Address Maintenance

Behavioral Gaps

08/07/2019

19-25993

2019 PI&R - Disposition of Paragon Labs Failure Analysis

Report TR1801449-01-0 Recommendations

08/08/2019

19-26074

2019 PI&R - Evaluate Monticello MSIV OE

08/12/2019

19-26074

Evaluate Monticello OE

08/12/2019

19-26081

2019 PI&R: Review of IN 2017-04 Has Not Been Completed

08/12/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

in a Timely Manner

19-26102

2019 PI&R: IN 2017-06 Not Reviewed in a Timely Manner

08/13/2019

19-26103

2019 PI&R

08/13/2019

19-26112

2019 PI&R - RFI-083: Discuss CARD 08-26828 Assurance of

Operability

08/13/2019

19-26139

2019 PI&R Inspection Insight on Part 21 Screening Practices

08/15/2019

19-26140

2019 PI&R Inspection - Insight on Evaluating Effectiveness

of Previous Self Assessments

08/15/2019

19-26141

2019 PI&R NRC Inspection (Observation) - Confidence in

CAP

08/15/2019

19-26143

2019 PI&R NRC Inspection (Observation) - Personnel

Associating SCWE with Industrial Safety Not Nuclear Safety

08/15/2019

19-26154

2019 PI&R Inspection - NRC Team Observation Related to

Older Open CARDs

08/15/2019

19-26179

2019 PI&R Inspection Concluded Fermi's Corrective Action

Program is Marginally Effective

08/16/2019

Drawings

6I721N-2578-06

Relaying & Metering Diagram Diesel Generator #11 Unit 2

X

6M721-5007

Diagram Primary Containment Pneumatic Supply System

Z

6M721-5988

Operator Time Critical Actions and Design Basis Sheet 1

E

Engineering

Changes

EDP-70032

Replacement of Bussmann MIN-3 Fuses with Bussmann

BBS-3 Fuses at C71P002B, D, F

TSR-36584

Re-Classify Auxiliary Building Superstructure as Seismic II/I

TSR-37859

Reconciled Design Loads

Engineering

Evaluations

17-22857

Apparent Cause Evaluation: Degraded Reactor Building

Pressure Due to OPDRVs

05/16/2017

18-23026

Root Cause Evaluation: Reactor Scram Due to Loss of 64

Transformer

04/16/2018

Miscellaneous

2019 CARD Backlog - July

Compensatory Monitoring Plan - 3D11 SLC Ignition

Continuity Loss/Circuit A Continuity Light is Off

03/29/2019

2017 CARD Backlog End of Year

D&Z Safety Conscious Work Environment Survey Results

05/29/2019

USA NSCA Survey Organization Level and Department

Statistics

08/10/2018

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Spring 2019 Fermi Employee Engagement Overview

05/06/2019

Listing of Systems in Maintenance Rule (a)(1) Status

07/15/2019

2018 CARD Backlog End of Year

16-0262

50.59 Screening - Revision to Programming of T41R800A/B

Recorder

ECP-19-001

(0801.26)

2019 First Quarter Report - Employee Concerns Program

04/30/2019

LER 17-22425

NRC 1 Hour-Reportable Physical Security (10 CFR 73.71)

03/23/2017

LER 17-24655

Division 2 RHR HX SW Outlet FCV Failed to Open

05/22/2017

LER 18-20257

Reactor Building Pressure > -0.125" During a Planned Swap

of Two Train to Single Train RBHVAC

01/11/2018

LER 18-28457

RHR Pump "C" Tripped After Auto Start During 24.307.02

10/18/2018

LER 19-21227

AB5-RB5 Interlock Switch Needs Adjustment

2/16/2019

Monticello

Nuclear

Generating Plant

LER 2017-002-00

Main Steam Isolation Valve Closure Time Outside of

Technical Specification Requirements

Monticello

Nuclear

Generating Plant

LER 2018-002-00

C Outboard Main Steam Line Isolation Valve Delayed

Closure Due to Foreign Material in the Air Valve

NAPI-18-0016

2018 Nuclear Safety Culture Assessment Report

11/01/2018

NQA 17-0114

Nuclear Quality Assurance Audit Report, Nuclear Quality

Assurance Audit of the Corrective Action and Operating

Experience Programs

11/06/2017 -

11/17/2017

NQA 18-0113

Nuclear Quality Assurance Audit Report, Quality Assurance

Audit of the Corrective Action and Operating Experience

Programs

11/05/2018 -

11/16/2018

OE 2018-0012

RIS17-08, Process for Scheduling and Allocating Resources

01/08/2018

SCR-37770

Revision to Programming of T41R800A/B Recorders

Procedures

24.307.14

Emergency Diesel Generator 11 - Start and Load Test

24.307.30

Emergency Diesel Generator No. 11 - 24 Hour Run Followed

by Hot Fast Restart

24.307.47

Emergency Diesel Generator 13 - Fast Start Followed by

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Load Reject

29.100.01 Sh 1

RPV Control

29.100.01 Sh 3

RPV Flooding, & Emergency Depressurization

29.100.01 Sh 4

RPV Alternative Level/Pressure Control

35.000.224

Alignment and Tension Adjustment of V-Belt Driven

Equipment

2.307.02

Logic System Functional Test of Division 2 EDG ECCS

Emergency Start Circuits and Automatic Trip/Bypass Circuits

ARP 1D30

RHR HX A Cooling H2O Discharge Temperature High

ARP 2D35

RHR HX B Cooling H2O Discharge Temperature High

FBP-41

Equipment Reliability Program

MMR Appendix D

Guidelines for Determining Functional Failures and

Maintenance Preventable Functional Failures

MMR Appendix F

Maintenance Rule Performance Criteria

MMR02

Maintenance Rule Program Description

6A

MMR06

Establishing Performance Criteria

MMR09

Establishment of Get Well Plans

17A

MQA11

Corrective Action Program

MQA11-200

Condition Initiation

1A

MQA11-300

Screening and Assignment

MQA11-400

Corrective Action Program Condition Disposition

MQA11-500

Non-Corrective Action Program Condition Dispositions

MQA11-500

Quality Assurance Conduct Manual Implementing Procedure

Non-Corrective Action Program Condition Disposition

MQA15

Quality Assurance Conduct Manual, Apparent Cause

Evaluations

Self-Assessments 17-0113

Quality Assurance Audit of the Equipment Reliability Program 10/31/2017

17-0114

Nuclear Quality Assurance Audit Report - Corrective Action

and Operating Experience Programs

2/18/2017

18-0110

Nuclear Quality Assurance Audit of the Radiological

Effluents, Radiological Material Transfer and Disposal, and

Radiation Protection Programs

08/27/2018

18-0113

Nuclear Quality Assurance Audit Report - Corrective Action & 12/14/2018

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Operating Experience Programs

2019Q1

Maintenance Continuous Learning Report

03/31/2019

NAPI-18-0014

Quick Hit Self-Assessment - CARD Closure Quality

09/28/2018

NAPI-19-0006

Focused Self-Assessment - Corrective Action Program

03/29/2019

NAQA-15-0001

NQA Special Oversight - M&TE

01/08/2015

NARP-17-0230

NRC Performance Indicator Comparative Analysis

05/03/2017

NARP-18-0155

Simulator Notifications Performance Assessment

05/15/2018

NPMA-16-0028

Focused Self-Assessment Report: Rigging, Lifting, and

Material Handling

2/22/2016

NPMA-19-0023

Focused Self-Assessment Report: Lifting and Rigging

Program

04/17/2019

NPOP-17-0066

Review of B.5.b Strategies

08/10/2017

NPOP-18-0466

Effectiveness Review for CARD 17-27545

05/22/2018

NPRP-18-0039

Quick Hit Self Assessment: Occupational ALARA Planning

and Controls

03/29/2018

NSSC-17-0006

Quick Hit Self-Assessment: Material Storage and Staging

04/27/2017

NSSC-17-0019

Quick Hit Self-Assessment: Material Storage and Staging

10/31/2017

NSSC-18-0002

Quick-Hit Self Assessment: Material Storage and Staging

04/16/2018

TMPE-18-0084

Quick Hit Self Assessment: Configuration Management and

Temporary Alterations

06/15/2018

Work Orders

25971306

Replace Scram Pilot Solenoid Fuses in C71P002F Per EDP-

70032

11/28/2018

25971310

Replace Scram Pilot Solenoid Fuses in C71P002B Per EDP-

70032

11/28/2018

26809154

Replace Scram Pilot Solenoid Fuses in C71P002D Per EDP-

70032

11/28/2018

37662340

Implement Mounting Configuration Change for EDG 14

Emergency Overspeed Switch

04/23/2015

46561773

Division 1 Reactor Building Differential Pressure Recorder

Response

2/23/2016

46671775

Implement a Software Change Request for T41R800B

2/23/2016