IR 05000341/2019002

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Integrated Inspection Report 05000341/2019002 and 07200071/2019001
ML19210D343
Person / Time
Site: Fermi, 07200071  DTE Energy icon.png
Issue date: 07/26/2019
From: Eric Duncan
Reactor Projects Region 3 Branch 4
To: Fessler P
DTE Energy
References
IR 2019001, IR 2019002
Download: ML19210D343 (27)


Text

July 26, 2019

SUBJECT:

FERMI POWER PLANT, UNIT 2INTEGRATED INSPECTION REPORT 05000341/2019002 AND 07200071/2019001

Dear Mr. Fessler:

On June 30, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Fermi Power Plant, Unit 2. On July 9, 2019, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.

If you contest the violation or significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector at Fermi. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Eric R. Duncan, Chief Branch 4 Division of Reactor Projects

Docket Nos.: 05000341 and 07200071 License No.: NPF-43

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000341 and 07200071

License Number:

NPF-43

Report Numbers:

05000341/2019002 and 07200071/2019001

Enterprise Identifiers: I-2019-002-0058 and I-2019-001-0111

Licensee:

DTE Electric Company

Facility:

Fermi Power Plant, Unit 2

Location:

Newport, MI

Inspection Dates:

April 1, 2019 to June 30, 2019

Inspectors:

S. Bell, Health Physicist

T. Briley, Senior Resident Inspector

N. Fields, Health Physicist

V. Myers, Senior Health Physicist

J. Nance, Resident Inspector

R. Ng, Project Engineer

J. Rutkowski, Project Engineer

T. Taylor, Resident Inspector

Approved By:

Eric R. Duncan, Chief

Branch 4

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Fermi Power Plant, Unit 2 in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Verify the Adequacy of the Design of the Reactor Building to Suppression Chamber Vacuum Breakers Cornerstone Significance Cross-Cutting Aspect Report Section Barrier Integrity Green NCV 05000341/2019002-01 Open/Closed None (NPP)71153 A finding of very low safety significance and an associated Non-Cited Violation (NCV) of 10 CFR 50, Appendix B, Criterion III, Design Control, was identified by the inspectors when the licensee failed to verify the adequacy of the design of the reactor building to suppression chamber vacuum breakers to ensure the associated butterfly isolation valves automatically closed upon increasing torus pressure and remain closed during all containment high pressure conditions. Specifically, during various loss of offsite power (LOP) and loss of coolant accident (LOCA) scenarios, the butterfly valves would not close automatically without manual operator action.

Additional Tracking Items

Type Issue Number Title Report Section Status LER 05000341/2018-007-00 LER 2018-007-00 for Fermi,

Unit 2, Reactor Building to Suppression Chamber Vacuum Breaker Condition Prohibited by Technical Specifications 71153 Closed LER 05000341/2019-002-00 LER 2019-002-00 for Fermi 2,

Secondary Containment Airlock Doors Opened at the Same Time Resulting in a Condition Prohibited by Technical Specifications 71153 Closed

PLANT STATUS

Unit 2 operated at or near rated thermal power during the entire inspection period with the exception of power changes to perform planned rod pattern adjustments.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Impending Severe Weather Sample (IP Section 03.03) (1 Sample)

(1) The inspectors evaluated the sites readiness for high winds potentially affecting lake level on April 11 and April 12, 2019

Summer Readiness Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated the summer readiness of offsite and alternate alternating current (AC) power systems

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (2 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Reactor Core Cooling Injection system while the High Pressure Coolant Injection (HPCI) system was out-of-service for planned surveillance testing during the week ending May 25, 2019
(2) Division 1 Non-Interruptible Air System (NIAS) during planned maintenance on Division 2 NIAS during the week ending May 25, 2019

71111.04S - Equipment Alignment

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated system configurations during a complete walkdown of the HPCI system during the week ending April 6, 2019

71111.05Q - Fire Protection

Quarterly Inspection (IP Section 03.01) (6 Samples)

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) Reactor Building First Floor, South Hydraulic Control Unit and Railroad Bay Area on April 10, 2019
(2) Reactor Building Fourth Floor, Standby Liquid Control Area on April 10, 2019
(3) General Service Water (GSW) Pump House during the week ending April 13, 2019
(4) Residual Heat Removal (RHR) Complex, Emergency Diesel Generator (EDG) 13 Room on April 24, 2019
(5) RHR Complex, EDG 11 Room on April 24, 2019
(6) Circulating Water (CW) Pump House during the week ending April 27, 2019

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 02.02a.) (1 Partial)

The inspectors evaluated internal flooding mitigation protections in the:

  • Torus Room during the week ending June 29, 2019

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the control room during a Recirculation System Digital Control System (DCS) module replacement during the week ending May 18, 2019

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness Inspection (IP Section 02.01) (3 Samples)

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1) Reactor Protection System (RPS) during the week ending April 13, 2019
(2) Reactor Recirculation System during the week ending April 27, 2019
(3) Primary Containment Isolation functions during the week ending May 18, 2019

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (2 Samples)

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Planned Recirculation System DCS module replacement during the week ending May 4, 2019
(2) Emergent Independent Spent Fuel Storage Installation (ISFSI) Cask 1 dye penetrant testing and gas monitoring within the time-to-boil period during the week ending June 8, 2019

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 02.02) (1 Sample)

The inspectors evaluated the following operability determinations or functionality assessments:

(1) Operability and functionality of the condensate storage tank, associated tank level instrumentation, and connected systems following the identification of the potential for vortex conditions at low tank levels, as documented in Corrective Action Resolution Document (CARD) 19-23227

71111.19 - Post-Maintenance Testing

Post Maintenance Test Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the following post maintenance tests:

(1) Reactor Water Cleanup (RWCU) isolation circuit timer following emergent maintenance during the week ending April 6, 2019
(2) Division 2 RHR Pump D Suppression Pool Suction Motor-Operated Valve (E1150-F004D) following planned maintenance during the week ending May 25, 2019 (3)24/48 Volt Battery Charger 2IB-1 following emergent maintenance during the week ending June 1, 2019
(4) Division 2 RHR Pump B discharge pressure trip unit following emergent maintenance during the week ending April 13, 2019

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Inservice Testing (IP Section 03.01)

(1) HPCI pump and valve operability test at 1025 pounds per square inch (psi) during the week ending May 26, 2019

Surveillance Tests (Other) (IP Section 03.01) (6 Samples)

(1) EDG 11 fast start and load test during the week ending April 12, 2019
(2) Division 1 Emergency Core Cooling System (ECCS) Reactor Vessel Water Level 2, Anticipated Transient Without Scram (ATWS)-Recirculation Pump Trip (RPT)functional test during the week ending April 12, 2019
(3) EDG 12 - Diesel Generator Service Water, Diesel Fuel Oil transfer, and Starting Air Compressor valve operability test on May 16, 2019
(4) Division 1 Standby Gas Treatment filter performance test during the week ending May 25, 2019
(5) Reactor Pressure Vessel Jet Pump 11 flow/pressure indication loop calibration on May 14, 2019
(6) Division 1 RHR Cooling Tower Fan Operability and RHR Service Water (RHRSW)valve line-up verification on May 15, 2019

71114.06 - Drill Evaluation

Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated an Emergency Preparedness Drill that was conducted on May 21,

RADIATION SAFETY

71124.06 - Radioactive Gaseous and Liquid Effluent Treatment

Calibration and Testing Program (Process & Effluent Monitors) (IP Section 02.02) (1 Sample)

(1) The inspectors reviewed the following gaseous and liquid effluent monitor instrument calibrations and tests:
  • Radwaste effluent radiation monitor
  • Onsite Storage Facility effluent radiation monitor

Dose Calculations (IP Section 02.05) (1 Sample)

The inspectors reviewed the following discharge permits to evaluate public dose calculations:

The inspectors also reviewed the following annual radiological effluent release reports:

  • 2017 Annual Report
  • 2018 Annual Report

Abnormal gaseous or liquid tank discharges

  • No abnormal gaseous or liquid tank discharges were available for review during this inspection

Instrumentation and Equipment (IP Section 02.04) (1 Sample)

The inspectors reviewed the following radioactive effluent discharge system surveillance test results:

(1) Standby Gas Treatment system

Sampling and Analysis (IP Section 02.03) (1 Sample)

The inspectors reviewed the following radioactive effluent sampling and analysis activities:

  • Standby Gas Treatment effluent sampling
  • Reactor Building effluent sampling
  • Onsite Storage Facility effluent sampling

Effluent discharges with inoperable monitors

  • Reactor Building

Walk Downs and Observations (IP Section 02.01) (1 Sample)

The inspectors walked down the following gaseous and liquid radioactive effluent monitoring and filtered ventilation systems to assess the material condition and verify proper alignment according to plant design:

  • Onsite Storage Facility Ventilation System

71124.07 - Radiological Environmental Monitoring Program

Groundwater Protection Initiative (GPI) Implementation (IP Section 02.02) (1 Sample)

(1) The inspectors assessed the implementation of the groundwater protection initiative

Site Inspection (IP Section 02.01) (1 Sample)

(1) The inspectors evaluated the radiological environmental monitoring program implementation

Walkdowns and calibration and maintenance record review

  • Air Sampling Station API-1, Estral Beach
  • Air Sampling Station API-2, Site Boundary North North West
  • Air Sampling Station API-3, Site Boundary North West
  • Air Sampling Station API-5, Site Boundary South
  • Air Sampling Station API-6, Site Boundary West North West
  • Dosimeter Monitoring Station T12, Pointe Mouille Game Area
  • Dosimeter Monitoring Station T22, North Side of Pointe Aux Peaux
  • Dosimeter Monitoring Station T23, South Side of Point Aux Peaux
  • Dosimeter Monitoring Station T25, Toll Road

The inspectors observed the following environmental sample collection and preparation:

  • Milk Sampling Location M-8, Calder Dairy

Licensee actions in response to missed sample, inoperable sampler, lost dosimeter, or anomalous measurement

  • 2017 first quarter dosimeter location T-7 found missing
  • 2017 third quarter dosimeter location T-37 found missing
  • 2017 fourth quarter dosimeter location T-37 found missing
  • 2018 first quarter dosimeter location T-47 found missing

Sampling program for the potential of licensed material entering groundwater

  • Condensate Storage Tank
  • Condensate Return Tank
  • U2100 Cable Vault

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified the licensee performance indicators submittals listed below:

BI02: RCS Leak Rate Sample (IP Section 02.11)===

(1) Unit 2 (April 1, 2018 - March 31, 2019)

MS06: Emergency AC Power Systems (IP Section 02.05) (1 Sample)

(1) Unit 2 (April 1, 2018 - March 31, 2019)

MS07: High Pressure Injection Systems (IP Section 02.06) (1 Sample)

(1) Unit 2 (April 1, 2018 - March 31, 2019)

71153 - Follow-Up of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02)

The inspectors evaluated the following licensee event reports (LERs):

(1) LER 05000341/2018-007-00, Reactor Building to Suppression Chamber Vacuum Breaker Condition Prohibited by Technical Specifications (ADAMS Accession ML19036A741). The circumstances surrounding this LER are documented in the Inspection Results Section of this report.
(2) LER 05000341/2019-002-00, Secondary Containment Airlock Doors Opened at the Same Time Resulting in a Condition Prohibited by Technical Specifications (ADAMS Accession ML19112A331). The circumstances surrounding this LER are documented in the Results Section of Integrated Inspection Report

===05000341/2019001 (ADAMS Accession ML19130A097)

OTHER ACTIVITIES

- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL

60855.1 - Operation of an Independent Spent Fuel Storage Installation at Operating Plants

Operation of an Independent Spent Fuel Storage Installation at Operating Plants===

(1) The inspector evaluated the licensees independent spent fuel storage installation (ISFSI) cask loading from June 17 through June 21, 2019. Specifically, the inspector observed the following activities:
  • Stack-Up and download of Multi-Purpose Canister (MPC)-596 from the transfer cask (HI-TRAC) to the storage cask (HI-STORM) at the Cask Transfer Facility (CTF)
  • Removal of the loaded HI-STORM and MPC-596 from the CTF for transport to the ISFSI pad
  • Heavy load movement of the HI-TRAC and empty MPC-587 up through the refuel floor hatch into the Dryer Separator Pit (DSP)
  • Loading spent fuel into MPC-587
  • Heavy load movement of the HI-TRAC and loaded MPC-587 out of the spent fuel pool into the DSP
  • Post-hydro dye penetrant weld evaluation for MPC-587
  • Blowdown, vacuum drying, and helium backfill evolutions for MPC-587
  • Radiological technical specification and general area surveys

The inspector performed a walkdown of the ISFSI pad, including independent radiation surveys, and a walkdown of the ISFSI haul path.

The inspector evaluated the following:

  • Spent fuel selection for the 11 casks in the loading campaign
  • Selected CARDs
  • The licensees change in Certificate of Compliance (CoC) loading amendment from Amendment 5 to Amendment 10, including a change in MPC type from MPC-68 to MPC-68M

INSPECTION RESULTS

Failure to Verify the Adequacy of the Design of the Reactor Building to Suppression Chamber Vacuum Breakers Cornerstone Significance Cross-Cutting Aspect Report Section Barrier Integrity

Green NCV 05000341/2019002-01 Open/Closed

None (NPP)71153 A finding of very low safety significance and an associated Non-Cited Violation (NCV) of 10 CFR 50, Appendix B, Criterion III, Design Control, was identified by the inspectors when the licensee failed to verify the adequacy of the design of the reactor building to suppression chamber vacuum breakers to ensure the associated butterfly isolation valves automatically closed upon increasing torus pressure and remain closed during all containment high pressure conditions. Specifically, during various loss of offsite power (LOP) and loss of coolant accident (LOCA) scenarios, the butterfly valves would not close automatically without manual operator action.

Description:

The reactor building to suppression chamber vacuum breakers consist of a power-to-close, spring-to-open butterfly isolation valve and a testable check valve in series. The function of the reactor building to suppression chamber vacuum breakers is to relieve vacuum when primary containment depressurizes below reactor building pressure. In addition, the two vacuum breakers in series (butterfly valve and check valve) must be closed to maintain a leak tight primary containment boundary. In accordance with Fermis Updated Final Safety Analysis Report (UFSAR), the butterfly valves are normally closed and open automatically to prevent formation of a negative pressure in the torus. The butterfly valves close automatically upon increasing torus pressure and remain closed during all containment high pressure conditions.

On December 8, 2018, while in Mode 4 (cold shutdown), the licensee identified a legacy design issue since initial power operation on January 23, 1988, in the control logic circuitry for the reactor building to suppression chamber vacuum breakers that prevented automatic closure of the butterfly isolation valves following power restoration from a LOP event. The reactor building to suppression chamber vacuum breaker check valves were not impacted by the design issue and therefore there was no loss of safety function. Procedural guidance was available to manually close the butterfly valves from the main control room following a LOP event.

On February 2, 2019, the licensee submitted LER 05000341/2018-007-00 (ADAMS Accession ML19036A741) to the NRC in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition which was prohibited by the plants Technical Specifications.

Technical Specification (TS) 3.6.1.7, Reactor Building-to-Suppression Chamber Vacuum Breakers, requires, in part, that each reactor building to suppression chamber vacuum breaker shall be operable in Mode 1, 2, and 3. As a consequence of this design control issue, the licensee declared that the reactor building to suppression chamber vacuum breaker butterfly valve in each line had been inoperable since initial power operation whenever the reactor was in Modes 1, 2, or 3. LCO 3.6.1.7 did not include any associated actions for the condition (failure to reclose following restoration of power), which placed the licensee in LCO 3.0.3, which required the licensee to place the reactor in Mode 2 within 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br />, Mode 3 within 13 hours1.50463e-4 days <br />0.00361 hours <br />2.149471e-5 weeks <br />4.9465e-6 months <br />, and Mode 4 within 37 hours4.282407e-4 days <br />0.0103 hours <br />6.117725e-5 weeks <br />1.40785e-5 months <br />. Since the licensee was not previously aware of the condition of the valve, the actions required by LCO 3.0.3 were not taken.

Although the design issue was identified by the licensee during an engineering evaluation of an unrelated issue associated with LOP/LOCA conditions, the inspectors identified inadequacies in the licensees characterization and evaluation of the issue of concern. Specifically, the licensee failed to document in their evaluation of the design issue why it was not identified during or in the years following original plant construction nor during periodic functional testing of the reactor building to suppression chamber vacuum breakers. In addition, the past operability evaluation was generic in nature stating that TS LCO 3.6.1.7 was not met (i.e. inoperable), but did not recognize that LCO 3.0.3 applied, and also was not met. When questioned by the inspectors, the licensees proposed TS actions did not involve TS LCO 3.0.3, which would have been required while the plant operated in Mode 1, 2, or 3 with the butterfly valves in their normally closed position. Therefore, the finding was considered NRC-Identified.

The licensees corrective action program ownership screening committee and management review committee both determined a formal causal evaluation was not necessary. Therefore, a qualitative description of the event stated the cause was a legacy design issue with a supporting technical justification. The design issue was corrected through a physical plant modification that included a post-maintenance functional test (open and close valve strokes)and a one-time post-maintenance test that consisted, in part, of removing and re-installing control power fuses to verify the butterfly isolation valves functioned as designed. The licensee did not document an evaluation of the effectiveness of past and present functional testing procedures until questioned by the inspectors. The inspectors determined current, post-modification reactor building to suppression chamber vacuum breaker functional test procedures (to open and close the butterfly valves) were adequate to verify automatic closure of the butterfly valves following power restoration from a LOP event.

Corrective Actions: A physical modification was implemented to re-wire the manual override portion of the vacuum breaker butterfly isolation valve control circuits so that the butterfly isolation valves would automatically re-close following the restoration of electrical power following a LOP event.

Corrective Action References: CARD 18-29870

Performance Assessment:

Performance Deficiency: The failure to verify the adequacy of the design of the reactor building to suppression chamber vacuum breakers to ensure the associated butterfly isolation valves close automatically upon increasing torus pressure and remain closed during all containment high pressure conditions (specifically following a restoration of electrical power)was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Design Control attribute of the Barrier Integrity cornerstone. Specifically, the reactor building to suppression chamber vacuum breaker butterfly isolation valves would not automatically close following a LOP event in order to perform their containment isolation function during all containment high pressure conditions.

Significance: The inspectors assessed the significance of the finding using Appendix A, Significance Determination of Reactor Inspection Findings for At - Power Situations. The inspectors concluded the issue was of very low safety significance (i.e., Green) based on answering No to Exhibit 3 Barrier Integrity Screening Questions B.1 and B.2.

Cross-Cutting Aspect: Not Present Performance. No cross cutting aspect was assigned to this finding because the inspectors determined the finding did not reflect present licensee performance.

Enforcement:

Violation: Title 10 CFR 50, Appendix B, Criterion III, Design Control, requires, in part, that the licensee provide for verifying or checking the adequacy of design, such as by the performance of design reviews, by the use of alternate or simplified calculation methods, or by performance of a suitable testing program. Fermi UFSAR Table 6.2-2, Note 24 states, in part, that each reactor building to suppression chamber butterfly valve is normally closed and opens automatically to prevent formation of a negative pressure in the torus and that the butterfly valve closes automatically upon increasing torus pressure and remains closed during all containment high pressure conditions.

Technical Specification LCO 3.6.1.7 requires that each reactor building to suppression chamber vacuum breaker be operable in Mode 1, 2, and 3. Technical Specification LCO 3.0.3 requires, in part, that when an LCO is not met and an associated action is not provided, the unit shall be placed in a Mode or other specified condition in which the LCO is not applicable and that this action shall be initiated within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> to place the unit, as applicable, in Mode 2 within 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br />; Mode 3 within 13 hours1.50463e-4 days <br />0.00361 hours <br />2.149471e-5 weeks <br />4.9465e-6 months <br />; and Mode 4 within 37 hours4.282407e-4 days <br />0.0103 hours <br />6.117725e-5 weeks <br />1.40785e-5 months <br />.

Contrary to the above, from initial power operation on January 23, 1988, until December 19, 2018, the licensee failed to verify the adequacy of the design of the reactor building to suppression chamber vacuum breakers to ensure the associated butterfly isolation valves close automatically upon increasing torus pressure and remain closed during all containment high pressure conditions. Specifically, during various LOP and LOCA scenarios, the butterfly valve would not close automatically without manual operator action. Additionally, because the licensee was not aware of the reactor building to suppression chamber vacuum breaker inoperability since initial power operation, the licensee failed to take the actions required by TS LCO 3.0.3 whenever the reactor had been in Modes 1, 2, or 3.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On May 23, 2019, the inspectors presented the Radiation Protection Program inspection results to Mr. M. Caragher, Plant Manager, and other members of the licensee staff.
  • On June 21, 2019, the inspectors presented the Independent Spent Fuel Storage Installation inspection results to Mr. J. Rivet, Mr. P. Crane, Mr. J. Haas, and other members of the licensee staff.
  • On July 9, 2019, the inspectors presented the integrated inspection results to Mr. P. Fessler and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

60855.1

ALARA Plans

RWP Number: 191061 Task Description: 2019 ISFSI

Campaign

2/19/2019

Calculations

HI-2125415

Thermal Evaluation of HI-STORM System in a Cask Transfer

Facility (CTF) at Fermi

03/25/2013

HI-2188547

Fermi MPC-68M Lifting Analysis

05/30/2019

RRTI-2995-05

Response to Request for Technical Information (RRTI)

Holtec International Helium Backfill - NRC Question

06/27/2019

Calibration

Records

1043-10181460

Traceable Certificate of Calibration for 3-Button Stopwatch

2/27/2019

6850-ACAL-

COMP-1-135032

Certificate of Calibration Accu-Flow Calibrated Leak Model #:

GPP-8-HE-QF25-110CC-SR15

03/22/2019

KELC-592390

Certificate of Calibration Extech Easyview 11A Type K

Thermometer

04/18/2019

Corrective Action

Documents

Selected ISFSI-Related CARDs Generated Since

July 21, 2016

16-0104

Quality Assurance Audit of the Independent Spent Fuel

Storage Installation (ISFSI) Program

05/02/2016

18-0102

Nuclear Quality Assurance Audit of the Independent Spent

Fuel Storage Installation Program

03/12/2018

CARD 19-24551

Trend on MPC Indications - Resolution Required

06/15/2019

CARD 19-24601

NQA - Receipt Inspection of ISFSI MPCs and Lids Not

Completed in Accordance with MMM12 Receipt and Source

Inspections

06/18/2019

Drawings

6A721Y-3000

ISFSI Delivery and Cask Haul Path

01/21/2016

Miscellaneous

Visual Examination Report, NDE VT Level II Personnel

Certificate, NDE PT Level II Personnel Certificate, and

Certification of Inspection, Examination and Testing

Personnel for NDE Personnel

04/25/2019

PCI Energy Services Welder Performance Qualifications and

Welder Maintenance Logs for Welding Personnel

04/25/2019

Visual Acuity Record and Non-Destructive Inspector

Certification Record for Mass Spectrometer Leak Testing

Personnel

04/30/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Quarterly TLD Data from TLD 68 for 2013, 2017, and 2018

Selected 72.48 Screenings and Evaluations Performed

Since July 21, 2016

DTE Electric Company Fermi 2 Nuclear Power Plant

Independent Spent Fuel Storage Installation 10 CFR 72.212

Evaluation Report ISFSI NRC Docket 72-71

04/22/2019

Fermi 2 UFSAR Section 17.2A Quality Assurance of the

Independent Spent Fuel Storage Installation

Composite Cask Load Reports for Campaign 3 Casks 1

Through 11

06/10/2019

Fermi Training Matrix

06/13/2019

Holtec International Qualification Records for Dry Cask

Personnel

05/29/2019

MC-GTAW

ASME Section IX Welding Procedure Specification and

Supporting Procedure Qualification Records

01/27/2017

MN-GTAW

ASME Section IX Welding Procedure Specification and

Supporting Procedure Qualification Records

01/27/2017

Certificate of

Conformance

91542-01

Detroit Electric Company (DTE) - Enrico Fermi Power Plant

Unit 2 DTE 4701334966 Change Order 1

05/23/2019

FER-DCS-001-R-

001

Fermi 2 Dry Cask Storage Fuel Characterization for Cycles 1

Through 12

2/30/2009

Holtec

International PO#

4700949383

HI-STORM 100 with MPC-68M Canister

2/26/2019

Procedures

2.RIG.17

Mobile Crane Operation

35.710.042

Multi-Purpose Canister (MPC) Loading

35.710.043

Blowdown, Drying, Sealing, and Backfill of the MPC

35.710.044

MPC Transport

35.710.045

Dry Cask Storage Equipment Preparation and Lay-Up

35.710.046

MPC Unloading

35.710.047

Responding to ISFSI Abnormal Conditions

35.710.048

MPC Preparation

35.710.049

HI-STORM Offloading and Preparation for Site Fabrication

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Completion

35.710.050

MPC Offloading and Handling

53.000.09

Dry Cask Storage Fuel Selection for Cask Loading

67.000.105

HI-TRAC Radiation Survey

67.000.106

HI-STORM Radiation Survey

67.000.107

MPC/HI-TRAC Contamination Survey

GQP-1.0

Project Organization and Documentation

GQP-1.1

QA Orientation and Project Training

GQP-12.0

Control of Measuring and Test Equipment

GQP-15.0

Non-Conforming Items

GQP-17.0

Quality Records

GQP-7.1

Procurement, Receipt, Storage, and Issue of ASME III

Subsection NCA-3800/NCA-4200 Weld Materials

GQP-8.1

Process Traveler

GQP-9.0

Training, Qualification, Examination, and Certification of NDE

Personnel in Accordance with SNT-TC-1A and CP-189

GQP-9.1

Training, Qualification, Examination, and Certification of

Inspection and Testing Personnel in Accordance with

ANSI/ASME N45.2.6-1978 and ASME NQA-1

GQP-9.2

High Temperature Liquid Penetrant Examination and

Acceptance Standards for Welds, Base Materials and

Cladding (50°-350°F)

GQP-9.6

Visual Examination of Welds

GWS-1

ASME Applications

07/24/2015

MMA07

Hoisting, Rigging, and Load Handling

26A

MMM12

Receipt and Source Inspections

WCP-3

Weld Material Control

07/09/2015

WCP-5

Weld and Base Metal Repair

09/23/2013

WCP-8

Preheating and Postweld Heat Treatment

09/23/2013

Radiation Work

Permits (RWPs)

191061

2019 ISFSI Campaign

03, 04

Self-Assessments Surveillance

Report 19-1003A

ISFSI Campaign #3 Preparation Assessment Report

05/30/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Work Orders

WO 45654006

Perform Licensing Renewal for HI-STORM Lifting Beam

Inspection

03/20/2019

WO 45654008

Perform Licenses Renewal Inspection/NDE of HI-TRAC Lift

Link

04/01/2019

WO 45654088

Perform Licenses Renewal Inspection/NDE of HI-STORM

Lifting Bracket

03/06/2019

WO 45662092

MPC Lifting Cleats Inspection

04/08/2019

WO 46777224

Low Profile Transporter Inspection

03/19/2019

WO 46777226

Perform License Renewal Inspection/NDE MPC Lift Lock

Assembly Inspection

03/19/2019

WO 46777470

Annual Vertical Cask Transporter Maintenance

2/05/2019

WO 48640668

NEIL Required-Perform F Frequent Inspection Per MIOSHA

R408.11872 Rule 1872(2)(A)

2/18/2019

WO 48689801

NEIL Required-RB Overhead Crane PM Inspections

04/17/2019

WO 48960565

SPF 2090

Perform 32.717.01 Monthly Rx Bldg Crane Manipulation-

NEIL Required

03/22/2019

71111.01

Corrective Action

Documents

10-20653

Engineering Evaluation of ITC Proposed Changes

01/26/2010

18-29819

Abnormal Noise on CB Disconnect Switch

2/06/2018

19-22736

Potential Degradation of Passive Vehicle Barrier System

04/11/2019

Miscellaneous

NOAA Webpage

NOAA Tides and Currents Webpage,

https://tidesandcurrents.noaa.gov, Position 9063090, Fermi

Power Plant

Procedures

20.000.01

Flooding

Work Orders

50014198

Perform Periodic Verification of Grid Adequacy

2/01/2019

218251

Perform Quarterly Walkdown of 120/345 kV Switchyards

06/20/2019

2583978

Abnormal Noise on CB Disconnect Switch

05/24/2019

71111.04

Drawings

6I721-2451-13

NIAS Division 1 Dryer P5002D012 Controls

N

6M721-2015

Station and Control Air

CQ

6M721-2044

Reactor Core Isolation Cooling System

BE

Procedures

23.129

Station and Control Air System

116

23.206

Reactor Core Isolation Cooling System

103

71111.04S

Corrective Action

Documents

19-22583

G3352F034 MOV Actuator Missing Stem Dust Cap

04/05/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Drawings

6M721-2035

High Pressure Coolant Injection (HPCI) System Reactor

Building

BN

6M721-2043

High Pressure Coolant Injection (HPCI) System Barometric

Condenser Reactor Building

AJ

Procedures

23.202

High Pressure Coolant Injection System

114

71111.05Q Fire Plans

FP-CWPH-1-32

Circulating Water Pumphouse Zone 32 Elevation 5836

Procedures

FP-GSW-1-31

General Service Water Pumphouse Zone 31

FP-RB-1-7b

Reactor Building South Control Rod Drive (CRD) and

Railroad Bay Area, Zone 7

FP-RB-4-17a

Reactor Building SLC System Zone 17 El. 6596

FP-RHR-1-11-

EDG

RHR Complex, EDG 11 Room, El. 5900

FP-RHR-1-13-

EDG

RHR Complex, EDG 13 Room, El. 590 0

71111.06

Corrective Action

Documents

19-23894

NRC Identified Concern: Housekeeping in Torus

05/21/2019

Drawings

29.100.01 SH 5

Continuous Use Procedure

6A721-2000-01

Reactor Building Sub-Basement Plan Elevation 5400 Scale

1/8 = 1-0

M

6A721-2000-02

Reactor Building Basement Plan Elevation 6520

N

6M721-2032

Sump Pump Diagram Radwaste System

BR

6M721-2224

Diagram Floor Drains All Floors Auxiliary and Reactor

Buildings

AA

7M721-2218

Floor and Equipment Drains Sub-Basement Plan Reactor

Building

Y

Procedures

ARP 2D82

Reactor Building Torus Sump Level Hi-Hi/Lo-Lo

ARP 2D83

Reactor Building Leakage to Torus Sump High

71111.11Q Miscellaneous

Operations

Conduct Manual

MOP01

Conduct of Operations

Operations

Conduct Manual

MOP19

Reactivity Management

26A

Operations

Operations Conduct

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Depaartment

Expectation ODE-

Procedures

23.138.01

Reactor Recirculation System

115

71111.12

Corrective Action

Documents

15-23626

C7100 Functional Failure Evaluation

05/25/2015

15-29250

Found Blown Fuse on Y Phase for RPS A Alternate

Transformer Feed

11/22/2015

16-28543

Single Rod Scram of CR 26-07

10/26/2016

17-20163

Use of RPS Test Box May Cause Loss of RPS Function

01/06/2017

17-21106

Review RPS for Maintenance Rule (a)(1) Classification

2/07/2017

17-23734

RPS-A EPA Breaker Found Tripped

04/19/2017

17-29439

Significant Arching in A RRMG Set Exciter Brushes - Root

Cause Evaluation

17-29735

B3105 Limiter 1 Being Enforced

2/05/2017

18-23130

Root Cause Evaluation Report - North RRMG Set Tripped

After Attempted Start

18-29870

Reactor Building to Suppression Chamber Vacuum Breaker

UFSAR Non-Conformance

2/08/2018

19-20117

Timer G33R616A Did Not Start Timing Immediately Upon

Actuation Signal during 44.020.151

01/04/2019

19-22916

Maintenance Rule Criteria for A7100 System has been

Exceeded

04/17/2019

Miscellaneous

(a)(1) Action Plan for Primary Containment Isolation

2/13/2016

Reactor Recirculation System System Health - Third Quarter

2018

Reactor Recirculation System System Health Report -

Second Quarter 2018

Maintenance Rule Monthly Evaluation Report for April 2019

05/02/2019

(a)(2) System Classification Review for Primary Containment

Isolation

09/16/2016

C7100 System Monitoring

2/20/2019

(a)(1) Action Plan

RPS (C71) Get Well Plan

(a)(1) Action Plan

B3100 Reactor Recirculation System Get Well Plan

MMR APP F

Maintenance Rule Conduct Manual, Appendix F -

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Maintenance Rule Conduct Manual

Procedures

23.628.02

Engineered Safety Features Actuation Instrumentation (RPS

and ECC)

71111.13

Corrective Action

Documents

19-24210

NQA - Holtec Field Condition Report to Evaluate Indication

Identified on Multi-Purpose Canister [MPC] S/N 0590 [PIS]

G1300A045 (CARD 19-24152) Was Not Reviewed and

Approved by Plant Support Engineering Per MES07

06/03/2019

19-24232

Foreign Material Identified in SFP

06/04/2019

19-24266

NQA - Expired Chemical Sherwin Dubl-Chek Developer D-

100 Found Staged for Use for Liquid Penetrant Testing on

Multi-Purpose Canister Welds

06/05/2019

Miscellaneous

Risk

Management

Plan

Multiple Alarms on C32K816, Replace INNIS21 and Cable

Assembly

05/14/2019

Work Orders

53570537

Multiple Alarms on C32-K816, RW and RR Flat Panel

Display. Troubleshoot and Repair

05/13/2019

71111.15

Corrective Action

Documents

07-23630

CDBI: UFSAR Anti-Vortex Methodology Non-Conservative

06/28/2007

07-23630-01

Prepare EDP to Increase CST Transfer Setpoint and

Refueling Level Requirements

07/27/2007

19-23227

Recommend Review of Site Response to Open CARD 07-

23630

04/26/2019

Miscellaneous

Crew Learning Opportunity (CLO) Worksheet

50.59 Screen 19-

20

Review of Compensatory Measures for CARD 07-23630

CST Vortex Issue

Bases 3.3.5.1

ECCS Instrumentation

MQA11-100

Operability Determination Process

2A

71111.19

Corrective Action

Documents

19-22486

Timer G33R616A Did Not Start Timing Immediately Upon

Actuation Signal during 44.020.152

04/02/2019

19-22650

RHR Pump Discharge Pressure at 0 PSIG

04/09/2019

19-23901

Mini on Valve E1150f004d

05/21/2019

19-24070

Human Performance Issue Battery Charger 2IB-1

05/29/2019

Drawings

5M721-6045

and 24 - 300# Powell O.S.Y. Gate Valve with Limitorque

Operator

A

6E721-2997-04

General Arrangement 24 Volt and 130 Volt Battery Chargers

E

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

6M721-2083

Residual Heat Removal (RHR) Division 2

CB

6SD721-2530-17

One Line Diagram 48/24V DC Instrumentation Batteries

Distribution

AM

6SD721-2531-14

Internal Wiring Diagram 24V ESF Battery Chargers

I

Procedures

35.306.020

Motor Operated Valve Mini Periodic Inspection

Work Orders

48565660

Perform Mini Periodic MOV Inspection (E1150-F004D)

05/21/2019

244172

Inspect/Test Division 2 24 VDC Battery Charger 2IB-1

05/29/2019

53586525

Timer G33R616A Did Not Start Timing Immediately Upon

Actuation Signal during 44.020.152

04/02/2019

53654676

RHR Pump Discharge Pressure at 0 PSIG

04/10/2019

54076383

Inspect/Test Division 2 24 VDC Battery Charger 2IB-1

05/29/2019

71111.22

Corrective Action

Documents

19-23952

Small Packing Leak Coming from E4100F068 HPCI Control

Valve

05/22/2019

Drawings

6M721-2035

High Pressure Coolant Injection (HPCI) System Reactor

Building

BN

6M721-2043

High Pressure Coolant Injection System (HPCI) Barometric

Condenser Reactor Building

AJ

Miscellaneous

Plan of the Day - Tuesday May 21, 2019

05/21/2019

Procedures

24.202.01

HPCI Pump and Valve Operability Test at 1025 PSI

118

24.202.08

HPCI Time Response and Pump Operability Test at 1025

PSI

24.307.14

Emergency Diesel Generator 11 - Start and Load Test

44.030.249

ECCS - Reactor Vessel Water Level (L2), ATWS-RPT

Division, Functional Test

Work Orders

46360904

Perform 43.404.001 Section 5.8 Division 1 Standby Gas

Treatment System Heater Operability

08/15/2018

46533988

Perform 43.404.001 Division 1 Standby Gas Treatment Filter

Performance Test

08/15/2018

46534020

Perform 43.404.001 Division 1 Standby Gas Treatment

System Charcoal Sample Withdrawal

08/16/2018

48698659

Perform 24.202.08 Sec-5.1 (Water Level) HPCI RTT and

Pump Operability at 1025 PSIG

05/22/2019

49189307

DGSW, DFOT and Starting Air Operability Test for EDG 12

05/15/2019

49336665

Division 1 RHR Cooling Tower Fan Operability and Valve

05/16/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Line-Up Verification Test

53629338

Calibration RPV Jet Pump 11 Flow/Pressure Indicating Loop

05/14/2019

71114.06

Corrective Action

Documents

19-23913

Untimely EAL Classification during ERO Drill

05/21/2019

19-23923

May 21, 2019 RERP Drill: Green Team OSC Staff Missing

Maintenance Team Members

05/22/2019

71124.06

18-29288

Potential Knowledge Issue Identified With General

Troubleshooting and Repair Of Radiation Monitors

11/14/2018

18-30351

Onsite Storage Facility Channel 5 Alarm Setpoint Increase

2/23/2018

19-23435

2018 Annual Effluent Report Submitted to the NRC

Contained Inaccuracies

05/03/2019

19-23711

Reactor Building System Particulate, Iodine, and Noble Gas

Sample Pump Failure

05/14/2019

Miscellaneous

2017 Annual Radioactive Effluent Release Report

04/30/2018

2018 Annual Radioactive Effluent Release Report

04/30/2019

NARP-14-0195

Acceptance of Emergency Action Level Basis Calculations

10/20/2014

NPRP-18-0112

On Site Storage Facility System Particulate, Iodine, and

Noble Gas Channel 5 Low Alarm Setpoint Needs to be

Adjusted

06/20/2018

NPRP-18-0215

Alarm Setpoint Adjustments on the Onsite Storage Facility

System Particulate, Iodine, and Noble Gas Monitor

Channel 5

2/21/2018

Work Orders

46675683

Perform 64.080.110 Circulating Water System Decant Line

Radiation Monitor Calibration

05/09/2018

46782282

Perform 64.080.102 Radioactive Waste Effluent Radiation

Monitor Calibration

05/30/2018

46926507

Perform 64.713.019 Attachment 17, Gaseous Effluent

Cumulative And Projected Dose (Monthly)

07/09/2018

47166492

Perform 64.713.019 Attachment 17, Gaseous Effluent

Cumulative and Projected Dose (Monthly)

08/15/2018

51089423

Process Radiation Monitor Onsite Storage Facility Ventilation

Exhaust Radiation Monitor Penthouse Instrument Rack

09/12/2018

51433193

Perform 64.080.102 Radioactive Waste Effluent Radiation

Monitor Calibration

08/03/2018

51822541

Onsite Storage Building Ventilation Exhaust Process

09/11/2018

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Radiation Monitoring System Calibration

2436065

Planned Vent/Purge of Primary Containment Atmosphere

11/16/2018

71124.07

Calibration

Records

44.100.001

Meteorological Monitoring - Wind Speed Channel Calibration

05/11/2018

Serial Number

6387

Radeco Model AVS-28A Calibration

04/08/2019

Serial Number

22

Radeco Model AVS-28A Calibration

04/08/2019

Serial Number

7572

Radeco Model AVS-28A Calibration

04/05/2019

Corrective Action

Documents

19-20363

Degraded Mechanical Equipment and Support Items Found

in CST/CRT Valve Vaults

01/16/2019

19-21419

Met Tower TRLCO 3.3.13 Condition B

2/24/2019

19-22281

Met Tower TRLCO 3.3.13 Condition B

03/25/2019

Miscellaneous

2017 Annual Radiological Environmental Operating Report

04/30/2018

Responses to D4000 Meteorological Questions

05/21/2019

2018 Annual Radiological Environmental Operating Report

04/30/2019

Procedures

Offsite Dose Calculation Manual (ODCM)

2.000.200

Land Use Census

2.000.201

Airborne Particulate and Iodine Sampling Using RADeCo

Model AVS-28A Air Sampler

2.000.203

REMP Results Analysis - Review and Action

2.000.207

Shipping Environmental Samples

67.000.104

Maintenance of Decommissioning Records

MRP30

Integrated Ground-Water Protection Program

Self-Assessments

Quick Hit Self-Assessment for the NEI 07-07 5-Year

Groundwater Protection Structures Review

01/16/2019

71151

Drawings

6M721-2223

Diagram All Floors Auxiliary and Reactor Buildings

Y

6M721-2224

Floor Drains All Floors Auxiliary and Reactor Buildings

AA

Engineering

Changes

Design Change

Package 80010

Separation of Drywell Identified and Unidentified Leakage

A

Miscellaneous

EDG MSPI and WANO Performance Indicators (April 2018 -

March 2019)

HPCI Performance Indicators (April 2018 - March 2019)

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

50.59 Screen 17-

280

Separation of Drywell Identified and Unidentifed Leakage

and Update UFSAR Figures 5.5.2 and 9.3-5 to Reflect

Changes per EDP 80010

A

MSPI

Mitigating Systems Performance Index (MSPI) Basis

Document

NEI 99-02

Regulatory Assessment Performance Indicator Guideline

Procedures

43.401.200

Local Leakage Rate Test Type B - General

43.401.511

Local Leakage Rate Test, Bypass Leakage Valves

41B

71153

Corrective Action

Documents

18-29870

Reactor Building to Suppression Chamber Vacuum Breaker

UFSAR Non-Conformance

2/08/2018

18-56668

2018 DBAI SA: 50.59 Screen 13-0098 Did Not Identify

UFSAR Impacts (Deficiency)

09/05/2018

19-23093

LER 2019-002 Submitted to the NRC with Clerical Errors

04/23/2019

19-23095

Incorrect/Confusing Title of Licensee Event Report in NRC

Submittal (NRC-19-0020)

04/23/2019

Drawings

6I721-2678-03

Torus to Rx Building Vacuum Breaker Valves T2300F450A

Through T2300F410

U

I-2678-03

U

Engineering

Changes

Design Change

Package 80071

Automatic Closure of Torus to RB Vacuum Breakers

Isolation Valves T2300F409 and T2300F410 After Loss of

AC Power

2/19/2018

Miscellaneous

LER 2019-002-00

Secondary Containment Airlock Doors Opened at the Same

Time Resulting in a Condition Prohibited by Technical

Specifications

Procedures

24.402.01

Drywell and Suppression Chamber Vacuum Breaker

Operability Test

& 40