IR 05000331/1996011

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Insp Rept 50-331/96-11 on 961025-1220.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support
ML20134C892
Person / Time
Site: Duane Arnold NextEra Energy icon.png
Issue date: 01/29/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20134C882 List:
References
50-331-96-11, NUDOCS 9702040119
Download: ML20134C892 (18)


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U. S. NUCLEAR REGULATORY COMMISSION REGION lli Docket No: 50-331 l

License No: DPR-49 l l

Report N /96011 l l

l Licensee: lES Utilities In First Street P. O. Box 351 Cedar Rapids, IA 52400-0351 l

Facility: Duane Arnold Energy Center Dates: October 25 - December 20,1996 Inspectors: K. Rieraer, Senior Resident inspector C. Lipa, Resident inspector M. Kurth, Reactor Engineer Approved by: M. Jordan, Chief Reactor Projects Branch 5

l 9702040119 970129 PDR ADOCK 05000331 G PDR

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EXECUTIVE SUMMARY Duane Arnold Energy Center NRC inspection Report 50-331/96011 This inspection report included resident and regional inspectors' evaluation of aspects of licensee operations, engineering, maintenance, and plant suppor Ooerations i

e in two cases, operators did not perform surveillance activities according to i procedures. See Sections M1.3 and M1.6 for detail l I

Maintenance e The "A" RRMG tripped while operators were conducting a test. Poor pre-job  ;

planning resulted in the decision to perform this work and post maintenance testing l on-line without considering the effects of a failed test on plant operation. (Section I M1.2) i i

e The inspectors waro concerned with the recent examples of problems with document change forms (DCFs). Plant operators failed to implement requirements !

of a DCF into a surveillance. This was a violation. (Section M1.3)

l e Average Power Range Monitor (APRM) 15% scram setpoint was rendered l

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inoperable when maintenance was performed that replaced Local Power Range Monitors (LPRMs). The root cause was determined to be an inadequate procedure for LPRM replacement. This was a violation. (Section M1.4)

e The inspectors identified loose lock nuts on a drywell stabilizer. The inspectors concluded that the surveillance procedure was weak. (Sectica M1.5)

e Operators used incorrect acceptance criteria during a surveillance test. This was an unresolved item. (Section M1.6)

e The inspectors were concerned about material condition, especially since the plant had just completed a refueling outage. (Section M2.1)

Enaineerino e The inspectors determined that two events that occurred during the inspection period, were not reported according to 10 CFR Parts 50.72 and 50.73. This was an unresolved item. (Section E8.1)

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e The inspectors were concerned that a weakness in pre-job planning resulted in

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unnecessary additional dose while mechanically cleaning two drywell coolers. This is an unresolved inspection itern. (Section E1.1)

e The licensee identified that the residual heat removal inject check valve was chattering. This was an inspection followup item. (Section E1.2)

e One drywell seismic monitor was damaged due to heat. According to the UFSAR,

the instrumentation was to be constructed so that it will perform within the range of environmental corditions expected at the plant site. This was an unresolved

inspection item. (Section E2)
Plant Suonort i e No concerns were identified in the plant support area.

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Reoort Details Summarv of Plant Status j At the beginning of the inspection period, the plant was in a shutdown condition for '

j refueling outage fourteen (RFO-14). Startup from RFO-14 was on November 14,1996,

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with full power reached on November 24,1996. On December 2, power was reduced to approximately 85 percent for several hours when the "A" reactor recirculann motor i generator set tripped due to a breaker malfunction during post-maintenance, testing. On

December 13, operators reduced power to 50 percent to remove the "A" feedwater  ;

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regulating valve from service due to fluctuations in valve position and feedwater flow. The '

plant was restored to full power on December 14. The plant operated at full power for the ,

, remainder of the inspection perio i

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l. Operations i

j 01 Conduct of Operations k 0 General Comments (71707)

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The inspectors conducted frequent reviews of plant operations. This included

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observing routine control room activities, accompanying in-plant operators on daily rounds, attending shift turnovers and crew briefings, and performing panel walkdowns. The conduct of operations was professional. Noteworthy

observations are detailed in the sections below.

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01.2 Reactor Plant Startun From Refuelino Out=a=

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l j k November 14,1996, the licensee commenced a reactor plant startup following

, RK' 14. On November 16,1996, the main generator was synchronized to the electrical grid. The inspectors observed prestartup evolution briefings. The j inspectors also observed in-plant and main control room startup activities.

i Observations and Findinas

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) The inspectors observed the following during the startup: effective shift

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management oversight of the activities, formal communications between operators,

and strict procedural adherence. The plant had just reached criticality and operators l were maintaining power low in the intermediate range when a shift turnover was
scheduled to occur. Extra people entered the control room to prepare for turnover

{ activities. The inspectors conciaded that the presence of extra personnel was an unnecessary distraction to the operators while at an important point in the startu ,

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i The lead control room operator independently determined a distraction existed and

directed unnecessary people to leave the control. The turnover was appropriately j delayed until the plant was in a stable condition. The inspectors observed that the j shift turnover occurred smoothly. The startup continued without problems.

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Conclusions The inspectors concluded that the startup was well controlled and conducted in a

slow and conservative manner. The inspectors noted excellent coordination existed

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between control room operators and in-plant operators while bringing systems on '

line to support plant startup activitie l i

02 Operational Status of Focilities and Equipment 02.1 Ennineered Safety Feature System Walkdowns (71707)

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' Insoection Scone

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The inspectors used Inspection Procedure 71707 to walk down accessible portions of the following Engineered Safety Feature systems:

I e residual heat 9moval

{ e standby gas treatment

, e cwe sgay

e standby liquid control i e standby diesel generators  !

4 e safety related batteries Conclusions Equipment operability, material condition, and housekeeping were acceptable in all cases. Minor discrepancies were brought to the licensee's attention and were corrected. The inspectors identified no substantive concerns as a result of these walkdown II. Maintenance M1 Conduct of Maintenance M1.1 General Comments Insoection Scone (62703) (61726)

l The inspectors observed or reviewed portions of the following testing and work l activities:

o Control Rod Scram Time Testing l

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e High Pressure Coolant injection Simulated Automatic Actuation Test e Reactor Core isolation Cooling Simulated Automatic Actuation Test e Reactor Core isolation Cooling Quarterly Operability Test e Feedwater Regulating Valve Modification Testing

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e Standby Diesel Generator Operability Test e Fuel Movement / Core Alterations

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e "A" Standby Diesel Generator 18 Month Preventive Maintenance

, Activities e V-20-0082 Chack Valve Repairs

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e Loss of Offsite Power and Loss of Coolant Accident (LOOP-LOCA) Testing

, e Drywell-Suppression Chamber Vacuum Breaker Test i e Residual Heat Removal (RHR) Motor Operated Valve, MOV-1904 replacement of worn gear o "D" RHR Pump Breaker Lubrication and Inspection

e "A" Control Rod Drive Pump Seal Repair
  • Thermolag removal

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  • Crosstie Breaker 180505 Preventive Maintenance

M1.2 Breaker Failure to Close Durina Testina Results in Trio of "A" Reactor Recirculation

Motor GeneratorJRRMG1 i Insoection Scone (62703)

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On December 2,1996, the "A" RRMG tripped while operators were condu'cting a test. The inspectors followed up on the event and vedfied that the plant was in a stable condition.

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Operators we. e performing post-maintenance testing on breaker 180505 according
to Preventive Maintenance Action Request 1096166 and Operating Instruction

! 304.1. Breaker 1B0505 is a cross-tie between two non-essential 480 volt buses, 1B5 and 186. During the test, breaker 1B0505 did not close as expected.

j Because breaker 1B0505 did not close, power was temporarily lost to the 1B5 bus.

This resulted in a lost of power to two RRMG lube oil pumps and the RRMG tripped

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on low lube oil pressure.

i Corrective actions included: 1) documenting the event on Action Request (AR) I 1 962790, which initiated a root cause analysis, 2) restarting the "A" RRMG, 3) !

. repair of 1B0505, and 4) plans to review of the appropriateness of performing maintenance and testing of cross-tie breakers on-line. The inspectors considered the corrective actions to be appropriat Conclusions  !

There was no violation of NRC requirements because the 1B0505 breaker and the RRMG are not safety related. However, the inspectors were concerned with ineffective work planning being a contributor to the event. The inspectors concluded that poor pre-job planning resulted in the decision to perform this work and the associated post maintenance testing on-line without considering the effects that a failed test would have on plant operatio l l

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M1.3 Document Chanoe Form (DCF) Not incarnorated Durina SurW!!ance I

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On November 5,1996, operators identified that instructions on DCF 96-T-0313 j j were not incorporated into Surveillance Test Procedure (STP) 48AOO1-SA,  !

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" Standby Diesel Generator Semi-Annual Operability Test," Revision 22. As a result, l l vibration data was not obtained following the two hour run as required. The

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inspectors independently reviewed this issue and compared it to other DCF problems discussed in two recent NRC inspection report Observations and Findinas On November 5,1996, at the completion of STP 48AOO1 SA, operators realized that the required vibration data had not been obtained. The instructions on DCF 96-T-0313 were not incorporated into the STP due to personnel erro l The licensee documented the issue on AR 962553. Corrective actions included,1) l review by engineering of the acceptability of the November 5,1996 test without t the vibration data,2) revising Operations Department Instruction ODI-5 to emphasize that the Operations Shift Supervisor is responsibio for ensuring DCFs are incorporated before authorizing the STP, and 3) AR 961838 was issued to require a solutions team to address the recant problem with DCFs not beir:g incorporated into procedures, Conclusions The inspectors were concerned with the recent examples of problems with DCF See NRC inspection reports 50-331/96-06 and 96-07 for details. The inspectors concluded that the licensee's plan to address this problem more broadly was appropriat Duane Arnold Technical Specification (TS) 6.8.1 requires that written procedures covering areas such as testing requirements of equipment that could have an effect on the nuclear safety of the facility be implemented. Surveillance Test Procedure (STP) 48AOO1-SA, " Standby Diesel Generator Semi-Annual Operability Test,"

Revision 22 was modified by DCF 96-T-0313. DCF 96-T-0313 added a requirement to obtain vibration data following the two hour run at rated load. The plant operators' failure to obtain the required vibration data is considered a violation of TS (50-331/96011-01).

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i l M1.4 Non-conservative Averaae Power Ranae Monitor (APRM) 15% Scram Setooint Due

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to inadaanate Pracadure

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The inspectors reviewed the details of Licensee Event Report (LER) 96-06. The !

inspectors independently investigated TS requirements, and reviewed the facts I surrounding the event, licensee corrective actions, and root caus Observations and Findinas As discussed in LER 96-06-00, the licensee identified on October 26,1996, that the APRM 15% scram setpoint was rendered inoperable when the Local Power R.snge iv%.'itors (LPRMs) were replaced. The cause of the evwnt was a failure to bypass the 24 LPRMs when they were replaced on October 21,1996. Since the selector switches were left in " Operate," this caused the APRMs to indicate a neutron power level lower than actual. As a result, the APRM Neutron Flux 15 percent power trip function was inoperabl Upon identification of this issue, the licensee promptly stopped moving fuel, verified all control rods were full in, and requested further evaluation. The root cause was determined to be an inadequate procedure for LPRM replacement. Refueling Procedure RFP-504, "LPRM Replacement," Revision 2, did not contain instructions to bypass LPRMs. The licensee's corrective actions included 1) placing affected LPRMs in bypass,2) revision of RFP-504 and other associated procedures, and 3) l plans to emphasize this event during training for appropriate personne ! Conclusions The inspectors concluded that the corrective actions were appropriate. The inspectors also concluded that technical specification requirements were violate Technical Specification Table 3.1-1, 2.a requires action to be taken to suspend all operations involving core alterations and to insert all insertable control rods within one hour when the APRM Neutron Flux 15 percent power trip function is inoperable. From October 25,1996, at 0558 hours0.00646 days <br />0.155 hours <br />9.22619e-4 weeks <br />2.12319e-4 months <br /> until October 26,1996, at 0625 hours0.00723 days <br />0.174 hours <br />0.00103 weeks <br />2.378125e-4 months <br />, core alterations were in progress while the APRM Neutron Flux 15 percent power trip function was inoperable. This was considered a violation (50-331/96011-02).

M1.5 Loose Drvwell Stabilizer Fasteners identified After Comolation of Surveillance Insoection Scone On November 1,1996, during a drywell inspection, the inspectors identified loose lock nuts on a drywell stabilizer. The licensee documented this nonconformance on AR 96127 _. ._ ._ _ __ _ _ _ . ___ _ _ . _ _ _ _ _ . _ _ _ _ . _ _ _

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Observations and Findinas f
After the inspectors identified two loose nuts on the drywell stabilizer, the licensee

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initiated a change to surveillance test procedure (STP) 47AOO1, " Suppression Chamber and Drywell Visual Inspection," to add requirements for inspection of drywell stabilizers. The STP was completed on October 24,1996. STP 47AOO1 required only a visual inspection of stabilizers and did not specifically require examining the fasteners. The licensee planned to revise the STP to add inspection requirements Dr bolts and lock nut The licensee subsequently inspected other fasteners on the stabilizers and repaired additional loose fasteners. The licensee concluded that the effect of the loose fasteners was minor, based on previous experience with evaluating loose fastener Conclusions The inspectors concluded that the surveillance procedure was inadequate. The inspectors concluded that the safety significance was minor and that corrective actions were appropriate. The inadequate procedure was in violation of 10 CFR Part 50, Appendix B, Criterion V. However, because the licensee identified that the procedure was inadequate and appropriate revisions are planned, this is a Non-Cited Violation (NCV) (50-331/96011-03).

M1.6 Incorrect Accentance Criteria Used for Comolation of Daily Surveillances insoection Scone

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On December 8,1996, operators identified that acceptance criteria used in STP 48AOO1, " Daily Instrument Checks," had not been correct since October 25,199 The inspectors reviewed this issue in parallel with the licensee's investigatio Observations and Findinas The quarterly performance of Emergency Service Water (ESW) STP 48EOO1-Q determined the maximum allowable river water temperature that would support ESW system operability. The daily STP 42AOO1 compared actual river water temperature to this maximum allowable value. On October 25,1996, operators failed to record the data on the " Emergency Service Water Temperature" log shee Subsequently, operators transferred the incorrect data to the daily STI 42AOO As a result, the acceptance criteria used in the STP 42AOO1 (91.8 F for "A" and 93.O'F for "B") were not the actual values (90.5 F for "A" and 94.3 F for "B"). -

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c. Conclusions

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The inspe : tors were concerned with the practice of using the "ESW Temperature" log sheet and transferring data from one STP to the next, rather than referencing the source dowment. The inspectors planned to review other similar checks made during the performance of STP 42AOO1 to determine whether this was an isolated case. Pending further NRC review, this is an unresolved item (50-331/96011-04).

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M2 Maintenance and Material Condition of Facilities and Equipment M2.1 Plant Material Condition

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a. Inspection Scone

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The inspectors noted that there were several material condition issues and self-revealing equipment failures during the report period. The inspectors reviewed the failures to determine if there was any affect on plant safety, in each case, the inspectors observed appropriate licensee efforts to determine root cause and schedule repair. T he examples are listed below:

e On November 1,1996, the inspectors identified loose lock nuts on a drywell stabilizer as discussed in Section M o On November 2,1996, the low pressure coolant injection swing bus transfer

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breaker closed in five minutes instead of five seconds as expected. See

Section E8.1 for detail l

'j e On November 7,1996, a drywell seismic monitor was found damaged by l excessive heat. See Section E.2 for detail o On November 24,1996, operators identified a banging noise in the RHR valve room. The cause was later determined to be chattering of the RHR check valve V20-82. See Section E1.2 for detail o From November 24 until December 2,1996, there were intermittent alarms of high flow on the "B" reactor recirculation pump seal flow switch. Based 1 on alternate indication, the alarms were determined to be invalid. This is documented on AR 962385. The inspectors independently verified alternate control room indication, such as identified leakage rate, seal pressure, and drywell temperatures and found no concern e Beginning November 25,1996, control room chart recorders indicated higher than expected drywell particulates. This is documented on AR 96263 o On November 26,1996, the "B" river water supply pump breaker would not close in from the control room. The breaker was subsequently replaced and the original will be sent to the manufacturer to determine the root cause per AR 96277 __ . - . _.._ _ _ _ _ _ _ ._ _ . _ . _ _ _ . . . _ _ . _ _- __

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l e On December 2,1996, the "A" RRMG set tripped when cross-tie breaker 180505 failed to close during post-maintenance testing. See Section M1.2

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e On December 3,1996, the licensee identified that 5 out of 8 main steam relief and safety valves failed the as-found setpoint test. See Section E8.1

for details.

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e On December 13,1996, operators reduced power to 50 percent due to

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fluctuations on the "A" feedwater regHating valve. The cause was j determined to be a cracked solder joint in the positioner assembly, which i was subsequently repaired.

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i e Throughout the inspection period, unidentified drywell leakage continued to increase slightly. Although the value of 0.40 gallons per minute (gpm) on

December 20,1996, was well below TS limit of 5 gpm, the licensee was j monitoring to attempt to determine the source of the leakag Conclusions The inspectors were concerned about the equipment problems discussed above, i especially since the plant had just completed a refueling outage. For example, j drywell unidentified leakage was at 0.40 gpm, which was greater than the value of
0.18 gpm at the end of the previous cycle. In each case, the inspectors concluded

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that the licensee's response to the issue was appropriate.

M8 Miscellaneous Maintenance issues (92902)

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M8.1 (Closed) Insoection Follow-un item 50-331/96003-08: Discrepancy between l UFSAR and licensee's test method for secondary containment. The licensee

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i previously closed both sets of secondary containment isolation dampers before  ;

'. testing to ensure cepability to maintain 1/4 inch of water vacuum. Test procedure l

! STP 47JOO1-CY was revised before refuel outage fourteen (October 1996) to test i

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with only one set of dampers closed at a time. The inspectors verified the results

of STP 47JOO1-CY performed on October 16 and October 18,1996. The tests j were satisfactory. This item is closed.

! M8.2 (Closed) Licensee Event Reoort (LER) 50-331/96-06-00: Non-conservative APMA 15% scram setpoint due to inadequate procedure. The inspectors reviewed this  ;

j LER and determined that a violation occurred as discussed in Section M1.4. The

, licensee's corrective actions will be reviewed as part of the NOV closure. This item

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is closed.

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111 Engineering
E1 Conduct of Engineering

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7 insoection Scone (37551)

l The inspectors evaluated engineering involvement in resolution of emergent material j condition problems and other routine activities. The inspectors reviewed areas such i as operability evaluations, root cause analyses, safety committees, and self

assessments. The effectiveness of the licensee's controls for the identification, resolution, and prevention of problems was also examine I

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E Weak Pre-Job Plannina for Cleanina of Drvwell Coolers

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i l On October 25,1996, the licensee identified that two drywell cooler isolation I

valves that were doenergized open as part of a temporary modification, (TM)95-148 were found closed. AR 962053 was written to document the issue. The

, inspectors reviewed the licensee's resolution of this issue and conducted

independent interviews.

i l Observations and Findinas i

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The licensee had installed TM 95-148 in April 1995 after 'eentification of low

, resistance short circuits in drywell penetration JX105C. The purpose of the TM i was to deenergize open drywell cooling valves to prevent undesired operation or continued insulation breakdown within the penetratio As a part of resolution of AR 962053, the licensee concluded that the drywell

{ cooling valves may have been closed during the installation of the TM due to cross

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connection of circuits to the valve. This allowed the valves to be powered closed j after the fuses had been pulled. The licensee subsequently relocated the control i

circuits to spare conductors within the penetration. These spare conductors had good insulatio The inspectors reviewed another aspect of the incorrect position of the drywell cooler isolation valves. During RFO-14, chemical cleaning of drywell coolers was planned to resolve a long term material condition problem with drywell coolers (IR 50-331,96-04). The engineer planning the job did not establish a valve line-up before the flush. Instead, the engineer assumed the valves would be open since

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TM 95-148, which failed valves open, was still in effect. Tne isolation valves for coolers 3A and 5A were actually closed during the chemical cleaning. Subsequent

mechanical cleaning of the coolers was required and workers received an additional
1.6 Rem of dose as a result of this error.

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! Conclusions The inspectors concluded that the problem with inadequate cable insulation within penetration JX105C was resolved. This was accomplished when the control circuits for drywell cooling valves were re-routed to spara cables with good

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! insulations. The inspectors had no concams with the licensee's additional efforts to resolve problems with the penetration. The inspectors were concerned that a

' weakness in pre-job planning resulted in unnecessary additional dose to

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mechanically clean the two drywell coolers. The review of this event was not completed prior to the end of the inspection. The inspectors will review the

licensee's processes for configuration control of TMs. In addition, the inspectors will review the licensee's operability evaluation. This is an unresolved inspection

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item (50-331/96011-05) pending the inspectors' revie E1.2 RHR Check Valve Chatterina

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1 Insoection Scone

On November 24,1996, the licensee identified a banging sound in the RHR valve i room. Through extensive troubleshooting efforts, engineering determined that the

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"A" RHR loop inject check valve was chattering. The inspectors reviewed the l i

licensee's initial operability evaluation, the details of the work done on the check I

valve at the end of the outage, and walked down the acceptable portion of the i syste j l Observations and Findinas

Through discussions with the valve manufacturer, the licensee concluded that the

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chattering did not affect RHR system operability. The licensee commenced a

detailed operability evaluation in January 1997. The licensee also determined

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through discussion with the valve manufacturer that repairs performed on the check valve during RFO-14 were appropriat Conclusions

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The inspectors determined that further review was required by NRC valve specialists. This is an inspection follow up item (50-331/96011-06) pending review of the licensee's operability determination.

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E1.3 Conclusions on Conduct of Enaineerina

The inspectors considered engineering efforts to investigate or resolve material
condition issues discussed in Section M2.1 to be appropriat ;

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! E2 Engineering Support of Facilities and Equipment L

Insoection Scone a

j The inspectors reviewed plant equipment and activities against the UFSAR i descriptions. Two discrepancies were identified.

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l Observations and Findinas i

j e As discussed in Section E8.1, below, the inspectors identified a difference i between an analysis described in the UFSAR and the Reload Analysis for j relief valve and safety valve allowable set-points.

! e On November 7,1996, the licensee identified that drywell seismic monitor

! QROOO8 was damaged due to excessive heat. The design temperature of j the monitor was 300 degrees Fahrenheit. Although ambient temperatures in j the drywell were well below 300 F, the licensee indicated that this monitor,

installed on the reactor pressure vessel, may be exposed to temperatures

! greater than 3OO'F. The monitor was subsequently replaced and high j

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temperature film was installed. The licensee installed temperature indicators to monitor the equipment during the cycle and initiated preventiva i maintenance to be done each refuel outage.

l The inspectors reviewed the licensee's response to Regulatory Guide 1.12, Instrumentation for Earthquakes, contained in UFSAR Section 1.8.12.

l Regulatory Position 7 states that the instrumentation should be designed to

. perform its function over the appropriate range of environmental conditions,

such as temperature, in responase to this Regulatory Position, the licensee

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stated that the instrumentation was constructed in such a way that it will

. perform in a satisfactory manner within the range of environmental j conditions expected at the plant site.

) Conclusions

! The inspectors were concerned that seismic monitor QROOO8 was not designed to perform its function over actual temperature ranges as discussed in the UFSAR.

, This discrepancy will be reviewed further as an unresolved inspection item l (50-331/96011-07).

j E8 Miscellaneous Engineering lasues (37551, 92902)

E Reportability of Events under 10 CFR 50.72 and 50.73 Insoection Scone

! The inspectors identified two events that appeared to be not reported according to 1 10 CFR Parts 50.72 and 50.73. In both cases, the licensee determined that the events were not reportable. The inspectors reviewed the licensee's operability i

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! evaluations, independently verified the facts of the events, and held discussions with the licensee on their justification for the events not being reportabl b. Observations and Findinas

j e During surveillance testing on November 2,1996, low pressure coolant

, injection swing bus transfer breaker 184401 failed to close within five

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seconds as expected. Instead, the breaker took approximately five minutes

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to close. The cause was determined to be an oil leak that affected the l undervoltage trip time delay and this was subsequently repaired and tested j satisfactorily.

The licensee originally reported the event under 10 CFR Part 50.72 (b)(2)(i)

! based upon the scenario of a LOOP-LOCA with worst single failure of one division of 125 VDC. In this scenario, the failure of the bus to transfer for 5 l minutes would have resulted in only one train of core spray being available.

l According to licensee analysis, a single core spray pump, at rated flow, is

! not sufficient to maintain the peak cladding temperature below the l regulatory limit during the initial 5 minute period post-LOCA.

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i The notification was subsequently retracted based on licensee's review of reportability requirements. Since only a single component,1B4401, was

inoperable, with no other indications of other component problems, the j licensee considered that this event was not reportable.

! * On December 3,1996, the licensee received as-found testing results which j revealed that 4 out of 6 main steam relief valves (MSRVs) and 1 out of 2

main steam safety valves (MSSVs) failed to meet the requirements of a Technical Specifications (TS) 2.2.1.B and 2.2.1.D, respectively. This was a

! repetitive problem at Duane Arnold in that setpoint testing results since

! 1980 indicated an as-found failure rate of 48 % for MSRVs and 65 % for

{' MSSVs. The TS specified an allowable range of plus or minus 11 psi for l MSRVs and plus or minus 12 psi for MSSVs (plus or minus approximately i 1%) and Section 5.4.13.3 of the UFSAR stated that the transient analysis j assumed that the valves operated at the setpoints plus 1 %.

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The licensee based their decision that the results were not reportable to the i NRC on the Reload Analysis, which assumed each of the valves was set 3%

j above the nominal settings. All eight pilot valves were subsequently

$ replaced with valves that were set within TS requirements. The licensee planned to submit a " voluntary" LER in the near futur c. Conclusions Part 50.73(a)(2)(ii) of 10 CFR requires licensees to report events or conditions that resulted in the condition of the nuclear power plant being in a condition that was outside the design basis of the plant. The inspectors were not able to resolve this issue during the inspection period and will review further to determine whether 10

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CFR 50 reportability requirements were violated. Pending further NRC review, this item is considered an unresolved item (50-331/96011-08).

IV Mant Suncort R1 Radiological Protection and Chemistry Controls Insoection Scone (71750)

The inspectors observed radiological postings and evaluated radiological work practices while observing maintenance and test activities. One concern was noted with poor communications during a High Pressure Coolant injection draining evolution, which is discussed in detailin NRC inspection report 96-09. The inspectors had no other concerns in the plant support are V. Manaaement Meetings X1 Exit Meeting Summary The inspectors presented the !:ispection results to members of licensee management at the conclusion of the inspection on December 20,1996. The licensee acknowledged the findings presente The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identifie . . _ . _ _ -_ ._ __ _ . _ _ . _ . _ . _ . _ _ _ _ _ _ _ ___

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PARTIAL LIST OF PERSONS CONTACTED l

l Licensee j J. Franz, Vice President Nuclear j G. Van Middlesworth, Plant Manager i R. Anderson, Manager, Outage and Support

] P. Bessette, Manager, Engineering i

J. Bjorseth, Maintenance Superintendent 1 D. Curtland, Operations Manager i R. Hite, Manager, Radiation Protection j K. Peveler, Manager, Regulatory Performance i  ;

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l INSPECTION PROCEDURES USED i l i IP 37551: Engineering

! IP' 40500: Effectiveness of Licensee Controls in identifying, Resolving, and ;

Preventing Problems '

j IP 61726: Surveillance Observation l IP 62703: Maintenance Observation IP 62707: Maintenance Observation I-IP 71707: Plant Operations IP 71750: Plant Support

IP 92700: Onsite Followup of Written Reports of Nonroutine Events at Power Reactor Facilities l IP 92901: Followup - Operations i IP 92902: Followup - Engineering l IP 92903: Followup - Maintenance i IP 93702: Prompt Onsite Response to Events at Operating Power Reactors

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. ITEMS OPENED, CLOSED, AND DISCUSSED

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Opened a

. 50 331/96011-01 NOV DCF Not incorporated During Diesel STP

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50-331/96011-02 NOV APRM 15% Trip Function inoperable During Core Alterations 50-331/96011-03 NCV Inadequate surveillance procedure i 50-331/90011-04 URI Incorrect Acceptance Criteria in Daily STP 50-331/96011-05 URI Configuration control of temporary modifications 50-351/96011-06 IFl RHR Check Valve Chattering 50-331/96011-07 URI Drywell Seismic Monitor Design Temperature Exceeded 50-331/96011-08 URI Reportability of Events Under 10 CFR 50.72 and 50.73

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Closed I 50-331/96003-08 IFl Discrepancy Between UFSAR and Secondary Containment Test Method i 50-331/96006-00 LER Non-conservative APRM 15% Scram Setpoint Due to l

inadequate procedure

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LIST OF ACRONYMS USED

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l APRM Average power range monitor j AR Action Request l CFR Code of Federal Regulations

DAEC Duane Arnold Energy Center. DCF Document Chango Form

! ESW Emergency service water

IFl inspection followup item i IP inspection procedure

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IR inspection report LCO Limiting Condition for Operation

LER Licensee Event Report

! LOCA Loss of Coolant Accident LOOP Loss of Offsite Power LPRM Local power range monitors NOV Notice of Violation

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NRR Office of Nuclear Reactor Regulation RFP Refueling Procedure RHR Residual heat removal

! RRMG Reactor recirculation motor generator STP Surveillance Test Procedure TI Temporary instruction

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TS Technical Specification UFSAR Updated Final Safety Analysis Report

URI Unresolved item j

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\' t NGC Form 8-C (4-79)

NRCM 0240 i

COVER SHEET FOR CORRESPONDENCE Use this Cover Sheet to Protect Originals of Multi-Page Correspondenc l

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