IR 05000305/1990017

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Forwards Safety Insp Rept 50-305/90-17 on 900909-1020.No Violations Noted.Record Copy
ML20197H453
Person / Time
Site: Kewaunee Dominion icon.png
Issue date: 11/05/1990
From: Knop R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To: Evers K
WISCONSIN PUBLIC SERVICE CORP.
References
NUDOCS 9011140271
Download: ML20197H453 (2)


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Dco/DuM Aros)

WO 51990

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Docket No. 50-305 Wisconsin Public Service

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Corporation

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ATTN: 'Mr. K..H. Evers Manager

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Nuclear Power

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700 North Adams

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Post Office Box 19002

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Green Bay, WI 54307-9002 Gentlemen:

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.This refers to the routine safety inspection conducted by Mr. P. I. Castleman

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and others of this office during the period from September 9 through October 20, 1990, of activities at Kewaunee Nuclear Power Plant authorized by NRC Operating

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License No. DPR-43 and to the discussion of our findings with Mr. M. L. Marchi

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at the conclusion'of the inspection.

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'The enclosed copy of our inspection report identifies areas examined during-the inspection. Within these areas, the inspection consisted of a selective

. examination'of procedures and representative records, observations, and interviews with personnel.

No violations of NRC requirements were identified during the course of this

inspection.

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In accordance with 10 CFR 2.790 of the Commission's regulations, a copy of this letter and the enclosed inspection report will be placed in.the NRC

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Public Document Room.

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We will gladly discuss any questions you nave concerning this inspection.

Sincerely, E

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R. C. Knop, Chief Reactar Projects Branch 3 E

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Enclosure:

Inspection Report

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No. 50-305/90017(DRP)

See Attached Distribution

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REGION III==

Report No. 50-305/90017(DRP)

Docket No.'50-305

License No. DPR-43

Licensee:. Wisconsin Fablic Service Corporation

P. O. Box 19002

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Green Bay, WI - 54307-9002

Facility Name:.Kewaunee Nuclear Power Plant

Inspect' ion At:

Kewaunee Site, Kewaunee, Wisconsin

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Inspection Conducted:

September 9 through October 20, 1990

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Inspectors:

P. I. Castleman

M. J. Davis

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. Approved By:

J. McCormick-Barger, Chief

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' Reactor Projects Section-3C

Date

Inspection Summary

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-Inspection from Se)tember 9 through October 20, 1990 (Report

No. - 50-305/90017( D RP) )

. Areas-Inspected: Routine unannounced inspection by resident and headquarters

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based inspectors of:

previous inspection findings; operational safety and

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ESF walkdown; surveillance; maintenance; and followup of written reports of

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nonroutine events.

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Results: Li_censee performance, overall, has been good,

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Operations:

No significant issues.

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Maintenance /Surveillbnce:

A reportable event occurred 'during this inspection

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aeriod due to both emergency diesel generators being out of service for one -

lour and forty minutes. The.1B EDG was removed from service for surveillance

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. testing at the same time that the 1A EDG was inoperable. The cause of the

inoperability of the 1A EDG was improper installation of a retaining clip

in a. fuel. injector assembly during the.1990 refueling outage.

This event is

particularly significant because the licensee failed to vigorously pursue an

investigation into the cause of anomalous behavior of the 1A EDG when their

initial assumption of the cause was disproven.

Details contained in

paragraph 4.

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Engineering and Technical: Supporti. ; A-design: deficiency associated with

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- equipment upgradesi.totthe plant" security system manifested. itself during.

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the' inspection period. :This': deficiency wasjan. inadequate evaluation of the -

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'electrica1' characteristics of new equipment, which resulted in/an overcurrent

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trip of a supply breaker, ands.in'a 20% reduction in line voltage to the -loads -

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-in question <-under full current conditions. Details. contained in paragraph 5.

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DETAILS

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Persons Contacted

  • M. L. Marchi, Plant Manager-

.D. -J.LRopson, Assistant Manager, Plant Maintenance

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C. A. Schrock, Assistant Manager, Plant Operations

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R. E. Draheim,: Assistant Manager, Plant Services

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'd. J. Wallace, Superintendent, Plant Instrument and Control

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C. S. Smoker, Supervisor, Plant Quality Programs

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D. R. Berg, Superintendent, Plant.Information Systems

Di T. Braun, Superintendent, Plant Operations-

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M. T. Reinhart, Superintendent, Plant Radiation Protection

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'*D. S. Nalepka, Plant: Licensing Supervisor

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G. J. Youngwirth,, Plant Electrical Maintenance Supervisor

F..D; Evitch Plant l Security Supervisor

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T. J.-Webb,-Plant Nuclear Engineer

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  • D. J. Will, Assistant Superintendent, Nuclear Design Change

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The inspectors' also talked with and interviewed members of the

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Operations, Maintenance, Health Physics, Instrument and Control, Quality.

Control, Chemistry, Design. Change, and Security groups.

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  • Denotes personnel attending exit interview.;

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Followup on-Previous Inspection Findings (92702)

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.(CLOSED) Violation (305/89012-02):

Failure to Document Emergency

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Operating Frocedures -(E0P) Setpoint Calculations.

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'Thiscseverity level IV violation was issued as< a result of the E0P.

inspection performed in 1989 at Kewaunee, during which it was found

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'thatithe licensee's: lack:;of setpoint1 calculations would make it-

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impossible' for an independent verification that theLappropriate~ data =

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. base and calculational methodology had been used in the development.

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.of the setpoints.- In their response to the Notice of Violation (NOV)-,

.the' licensee committed to develop a detailed setpoint-documert which

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twould present:the data and calculations used to-determine the setpoints

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included in the EOPs.

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,The setpoint;; document was published in: September 1990. The inspectors

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determined-that the calculations presented in the _ document apoeared to be

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idotailed and properly based. The licensee' plans;to maintain.the setpoint

document in a controlled manner, updating-it as revisions are made to the

E0Ps. : The; document appeared to address the concerns' expressed.in the

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NOV. We-have;no further questions regarding this issue, and this

. violation is closed.

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Operational Safety Verification (71707), (71710)

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The inspectors. observed control room operations, reviewed applicable logs

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and conducted discussions with control room operators throughout the

inspection period.

The inspectors verified the operability of selected

safety-related systems, reviewed tagout records, and verified proper

return to service of affected components.

The inspectors observed a

number of control room shif t turnovers.

The turnovers were conducted in

a professional manner and included log reviews, panel walkdowns,

discussions of maintenance and surveillance activities in progress or

planned, and associated LC0 time restraints, as applicable.

Tne inspectors conducted tours of the auxiliary and turbine buildings.

During these tours, observations were made regarding plant equipment

conditions, fire hazards, fire protection, adherence to procedures,

radiological controls and conditions, housekeeping, tagging of equipment,

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ongoing maintenance and surveillance activities, containment integrity,

and availability of safety-related equipment.

The overall material

condition of plant systems and equipment was noted to be good, as were

the observed housekeeping and fire protection practices.

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On October 3, the licensee conducted their monthly containment

inspection.

During the inspection, it was noted that the insuletion

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around check valve SI-304B, on the train B safety injection line to the

reactor vessel, was wet.

A followup containment entry was performed to

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remove the insulation and inspect the valve for leakage and potential

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boric acid induced bolt corrosion.

This inspection showed that the

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wetted insulation was due to a body to connet leak at a rate of four

drops per minute.

No degradation of the valve bolts was noted.

The

resident inspector, who acc'mpanied licensee personnel into the

containment, noted the valve to be in good material conditior..

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appeared to be uniform leakage from around the circumference of the valve

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body to bonnet joint.

The licensee installed a catch basin beneath the

valve to contain the flow of water.

A followup inspection was performed

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ten days later, with no increase in leek rate noted. The control room

operators have noted no detectable increase in reactor coolant system

leakage.

The licensee intends to continue monitoring the leakage for any

further degradation in the integrity of the body to bonnet joint.

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During the inspection period, the inspectors walked down the accessible

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portions of the Auxiliary Feedwater (AF( Rystem.

Items checked

included:

an operational valve lineup; proper housekeeping including

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control of flammable materials; normal pump seal and valve stem

leakages; proper electrical breaker and switch lineup; the required

instrumentation, including pressure monitors and valve position

indicators, were operable, and; proper lineup of the service water

and condensate storage support systems. Overall, the system, including

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both the motor driven and turbine driven pumps, appeared to be in a sound

state of operational readiness and no problems were identified.

During routine tours of the facility, the inspectors observed the

licensee's security activities including badging of personnel, access

control, escorting of visitors, security staff attentiveness and

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operation of security equipment.

All activities were conducted in a satisfactory manner and no violetions

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or deviations wern i M *ified.

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Monthly Surveillance Observation (61726)

The inspectors reviewed / observed the following Technical Specification

required surveillance testing:

Surveillance Procedure

Test

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SP 47-010A

Reactor Coolant Temperature and Pressurizer Pressure

Instrument Channel Test - Channel 1

SP 35-038A-

Boric Acid Tank 1A Level Instrument Calibration

SP 42-047

Diesel Generator Combined Monthly Test

SP 54-058

Turbine First Stage Pressure Instrument Channel Test

SP 24-107

Shield Building Vent Monthly Test

SP 42-109

Diesel Generatoi Manual Test

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The following items were considered during the inspection:

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testing was performed in accordance with approved procedures; that

test instrumentation was calibrated; that-test results conformed with

technical specifications and procedure requirements and were reviewed

by personnel other than the individual directing the test, and; that any

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deficiencies identified during the testing were reviewed and resolved by

appropriate management personnel.

At 1825 on Friday, September 14, 1990, while shutting down the 1A Emergency

Diesel Generator (EDG) at the. completion of SP 42-047, " Diesel Generator-

Combined Monthly -Test," the control room operators observed the-EDG resume

full speed operation.

To ensure shutdown of the EDG, the operators placed

-its control switch in the pullout position, and the unit successfully

coasted to a complete stop.

In evaluating this malfunction, on-shift

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personnel assumed that the EDG. shutdown timing solenoid had failed, and

that the operability of the EDG was not affected.

Based on this assumption,

the licensee elected to not pursue an investigation of the EDG shutdown

anomaly over the weekend of September 15-16.

On Monday, September 17, at 0935, the licensee removed the 1A EDG from-

service to' investigate the assumed solenoid-failure, and to conduct

a surveillance test on the carbon dioxide deluge system. Prior to

removing the 1A EDG from service, the licensee performed 'an operability

demonstration of'the IB EDG in accordance with their standard practice-

for doing so when taking the opposite train EDG out of service. This

operability demonstration, conducted under SP 42-109, " Diesel Generator

Manual Test," consisted of a local manual start of the EDG, with-

verification that the unit was able to reach a speed of 900-950 RPM,

frequency of 60-63 Hz, and voltage of 4200 V, in less than 10 seconds.

In 'accordance with the licensee's standard practice for EDG demonstration

- testing, this operability test did not include loading the EDG,

As a result of their investigation, licensee personnel determined

that the 1A EDG timing solenoid was performing satisfactorily.

The

licensee then investigated the engine's governor, but no indications

of malfunction were found. The licensee concluded that there must have

been a problem with the engine itself, and they contacted the EDG vendor,

who dispatched a technical representative.

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When t'he troubleshooting and surveillance testing performed on the.1A EDG

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were completed, the licensee conducted a demonstration test of the 1A EDG

- per SP 42-109 prior to removing the-1B EDG from service for the completion

of-the surveillance-testing on the carbon dioxide deluge system. The

1A EDG was started manually, and satisfactorily attained the required

. operating parameters of engine speed and generator frequency and voltage.

Thus, _the.1A EDG was declared operable, and the IB EDG was removed from

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service for'a total of one hour and forty minutes.

The EDG vendor technical representative arrived two days later, on

September 19. During his inspection of the 1AL EDG, he discovered that a

retaining spring was not installed on a clevis pin connecting the engine

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fuel rack to one of the fuel injectors. The clevis pin had vibrated out

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of its proper position, thereby allowing the injector linkage to jam the

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fuel rack and limit its range _ of motion to no more than 50% open from the

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"not-fully-closed" position. The malfunction observed in the diesel's

performance was, at that time, determined to be caused by the fuel rack-

not being able to close completely, which allowed continued injection

of, fuel to the engine during its coastdoun to a complete stop. The

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inoperability of the EDG, however, resulted from the fuel rack's

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, inability to open more than 50%, a condition which would have prevented

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the EDG from being able to attain its continuous full load rating of

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2600 KW, Hence, when.the 1B EDG was removed from service for one hour and

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forty minutes on September 17, both EDGs were inoperable for that time

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period,'a condition which was outside the plant's design basis.

The most probable root cause of this event was determined to be the

incorrect installation of the fuel injector linkage retaining clip while

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-overhauling the 1A EDG during the plant's 1990 refueling outage.

-This event could have been averted had the licensee removed the 1A EDG

from service on Monday, September 17, to vigorously pursue their

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investigation once the initial assumption of the cause of the anomalous

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EDG_ behavior was proven incorrect.

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As immediate corrective action, the licensee repaired the 1A EDG and

returned-it to service. Additionally, to address the generic concern

that other fuel injectors might be similarly affected, all injector

linkage retaining clips for both EDG's were verified to be properly

installed. Long term.::orrective actions will include training of plant

maintenance mechanics on the details of this event, and the licensee will

re-evaluate their practice of not loading an EDG during demonstration

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testing. The licensee also plans to conduct operations personnel

training regarding.this event, focusing on conservatism in operability

assessment.-

This issue vill be evaluated further upon the inspectors' review of the

licensee event report documenting the circumstances surrounding the

event.

All activities were conducted in a satisfactory manner and no violations

or deviations were identified.

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Monthly Maintenance Observation (62703)

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Station maintenance activities of-safety related systems and components-

listed below were observed / reviewed to ascertain if they were conducted

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in accordance with approved procedures, regulatory guides, industry codes

-or; standards, and in conformance with technical specifications.=

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The following items were considered during this review:

the limiting-

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conditions of operation were met while components or systems were _ removed

from service;. approvals were obtained prior to initiating the work;

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-activities were accomplished using approved procedures and were. inspected

- as' applicable; functional testing and/or calibrations were performed

prior to returning components or systems to service; parts and materials

used were properly certified; radiological controls were implemented; and

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fire prevention' controls were implemented.

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LThe following maintenance activities were observed / reviewed:

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DCR_2483

Design Change Request (DCR) to Upgrade Auxiliary Building

Special Ventilation Zone Fan Inlet and Outlet Damper

Limit' Switch Wires

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-PMP 8-1

Preventive Maintenance on IB Fire Pump

MWR 48333

Replace 1A Charging Pump Power _ Supply Breaker

MWR.49175

Changeout 1A2 Service Water Pump

LMWR 49410-

Repair IB Emergency Diesel. Generator Vibration Monitoring

-Unit

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MWR_49451

' Repair Security Multiplexer

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During-the inspection period, the circuit breaker supplying:a multiplexer

-in the plant security system tripped open, resulting in the loss of some-

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security monitoring capabili_ ties.- The plant security force implemented

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appropriate compensatory measures for the-lost capabilities. As a result

of the licensee's investigation into the tripping open of the multiplexer

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.sapply breaker, it was determined that the total loads supplied by the.

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breaker were.significantly_ greater than the breaker's current interrupt

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rating. -This condition resulted from the :recent installation of several

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upgrades to the plant's-security system.

In particular, the design of-

the upgrades failed ~to account for the doubling of load due to the

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addition ~~of heaters in newly installed outdoor. equipment, so that, when -

.the heaters' energized on the first. cold night following. installation of.

the upgrades, the breaker in question tripped open due to an ovarcurrent '

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condition.- The licensee also determined that,'uncer full load current,

the line, voltage to'the multiplexer would be reduced by about 20%. This

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voltage reduction would adversely impact the operation of the equipment

supplied by the multiplexer.

The root cause of the mismatch between the multiplexer loads and the

rating of the supply breaker was the licensee's failure to adequately

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evaluate the. changes in electrical loading resulting from the-

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modifications to the lecurity system. : Corrective actions by the licensee

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included development of a desinn change that would install;a'new-supply

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breaker with double tie _ interrupting capacity of the old breaker, and the

installation of a' constant output voltage transformer to correct the

voltage degradation problem.

All other activities were conducted in a satisfactory manner and no

' violations or deviations were identified,

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Followup of Written Reports of Nonroutine Events-(92700)

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-The inspectors, through observations, discussions with licensee

personnel, and review of records, reviewed the following event-reports

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to determine that reportability requirements were satisfied, that

corrective action was implemented, and that the response to the event

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was adequate and met regulatory requirements,-license conditions, and

commitments, as applicable.

-(CLOSED) LER 90004 - ' Temporary Change to a Procedure Causes the

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Generator Main Output Breaker to Open, Resulting in an ESF Actuation

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On March 18,c1990, during a refueling shutdown, a generator trip and

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lockout signal was : initiated, causing the main generator output breaker

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.(G-1) to open. The 4160V non-safeguards buses, l'-3 and 1-4, and-

safeguards bus 1-6 were being backfed through breaker G-1, and were-

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.d6 energized. The event occurred during performance of an instrumentation

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and controls: procedure (ICP) that calibrated a pressure. indicator with a

sensing 'line common to a pressure switch in the turbine / generator motoring

' protection circuitry.

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To provide grid electrical power to in-plant busses ~through G-1 during

refueling outages, the licensee'sinormal practice was to lift several

electrical leads in. order to disable the generator's motoring protection

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circuitry. ' Prior to the'1990 refueling outage, however, the licensee's'

substation and transmission group requested a change to the' practice of-

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_ lifting the leads ~because of a concern with disabling generator

protection circuitry.

In response' to this request, a temporary change to

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the preventive maintenance procedure-(PMP) by which the leads were lifted

was approved to leave the leads terminated during the outage.

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the pressure indicator calibration ICP was based on the asssmption that

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the leads'were lifted. When the instrumentation and contrals group

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calibrated _the pressure indicator, the pressure switch actuated,

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initiating ~ a generator trip signal, which caused G-1 to open_. The loss

of voltage on safeguards bus 1-6 caused various ventilation dampers and

.two containe,an. ' solation valves to close, constituting a reportable ESF

actuation

The ruot cause'of the event was determined to be the failure

to recognize the impact of the temporary change to the PMP'on the

pressure indicator ICP.

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Corrective actions included completion of the calibration with the

appropriate leads lifted, discussions with the groups involved, and

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Lprocedure-changes ~to PMP 39.8 ICP--54.07 and--ICP.54.30

The effect of

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the procedure changes was to group the three pressure sensing and

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indication components that share the common sensing;1ine under:the same

calibration procedurc, and tc ensure lifting of leads when required.to

bypass protection circuitry. The i.7spectors found that the, licensee's

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corrective actions' for thislLER are complete. - This LER 1s closed.

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(CLOSED)' LER 90005 -- Eddy Current Results Cause Both Steam Generators

_(SGs) Being Categorized as C-3

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On April :4 1990, at the completion of eddy current testing during the

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1990 refueling outage, 97 tubes in SG A and 75 tubes in SG B were

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' declared defective.:'With the number of defective tubes. exceeding one

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. percent of Use total number of tubes, both SGs were categorized as C-3,

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and the licensee made the notifications required by the plant technical

specifications.

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All' defective tubes were plugged and, as a preventive measure,'59 other

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tubes exhibiting degradation were plugged.

Sludge lancing was conducted:

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during the outage to reduce the accumulated sludge inventory within'the:

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SGs. To minimize the rate _ of SG tube degradation, a secondary system

boric acid addition program has been implemented to reduce the caustic

environment :in the tube crevice area. Additionally, portions of two

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- defective tubes were removed for laboratory analysis.

The results of-

this analysis will be forwarded for informational purposes to che NRC'_s

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Office of Nuclear Reactor' Regulation. The inspectors hadino'further

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questions regarding this issue. This LER is closed.-

-(CLOSED) LER 90008 -- Quality Assurance Audit of the Siemens Energy and

- Automation-Facility in. Raleigh, NC Finds Inadequaw 10 CFR 50 Appendix B

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Pr ogram

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Or May 2,1990, the licensee received the resul ;s of an audit of.the

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quality assurance program at the Siemens Energy and Automation-Facility.

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- ;The audit found that this -facility had been accapting purchase orders for

saf aty related equipment and services' while it' had failed to implement a

squality +;surance program meeting the requirements: of Appendix B to.10 CFR

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50. A similar audit conducted in March 1987, found that the Siemens

facility had an effective.' quality assurance program for safety related-

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equipment.in' place.

Licen'see corrective actions included removal of the facility from its

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list of-suppliers qualified to provide safety related equipment and

services. Also, the licensee identified all equipment procured from the

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facility since March, 1987, and reviewed the dispositions of those. items.

. All of the equipment procured from Siemens.had either been installed in

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non-safety related applications or was still in the warehouse. The.

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equipment in the warehouse was placed in a. hold status, and was tagged

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with quality. assurance non-conformance tags pending.either commercial

grade dedication or redesignation of the equipment for non-safety related

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application;only.

The licensee determined that the provisions of 10 CFR 21'did not apply to this event.

However, since the results of the

quality assurance audit could potentially affect other licensees, the

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L i,.l censee electedito~ promulgate:those results in the' form of a licensee '

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i. Jeventireport issued:for information.only. This LER.is considered closed.-

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7. -- iExitInterview(307031-

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- The inspectors met with-licenseecrepresentatives (denoted in Paragraph '1)

throughout;the period and on October 23, 1990, and summarized-the'scoper

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andl findings.,of:the inspection activities.-

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The-inspe'ctorsl also ' dis;ussed the likely informational content of "th'e

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Linspection: report with regard to. documents or processes reviewed by the-

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' inspectors during.the.inspectlon.

The licensee did~not identify any-such

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