IR 05000285/1989038

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Insp Rept 50-285/89-38 on 891011-31.Violation Noted.Major Areas Inspected:Ler Followup,Operational Safety Verification,Plant Tours,Monthly Maint Observations,Monthly Surveillance Observations & Security Observations
ML20005D718
Person / Time
Site: Fort Calhoun Omaha Public Power District icon.png
Issue date: 12/01/1989
From: Westerman T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20005D716 List:
References
50-285-89-38, NUDOCS 8912140336
Download: ML20005D718 (22)


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APPENDIX B V.S. NUCLEAR REGULATORY COMMISSION

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REGION IV

NRC Inspection-Report:

50-285/89-38 Licensee:

DPR-40 i

Docket: 50-285

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' Licensee:. Omaha Public Power District (OPPD)

F 444 South 16th Street Mall

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Omaha, Nebraska 68102-2247

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I Facility Name:

Fort * Calhoun Station (FCS)

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_ Inspection ~At:

FCS,. Blair, Nebraska Inspection Conducted: October 11-31, 1989 l

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Inspectors:

P. Harrell, Senior Resident-Inspector L

T. Reis, Resident inspector R. Mu111 kin, Project Engineer

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e Approved:

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T, F. Westerman, Chief,- Pro 3 Pet Section B Date'

Division of Reactor Projects Inspection Summary

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Inspection Condutted October 11-31, 1989 (Report 50-285/89-38)

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Areas Inspectedi P.outine,-unannounced._inspectionsincluding review of previously identified items; licensee event report followup; operational safety

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verification; plant tours; monthly maintenance observations; monthly i

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surveillance observations; security observations; radiological protection observationsi in-office review of periodic, special, and nonroutine event-

. reports;. review of'10 CFR Part 21 reports; and review of onsite events.

-Results: Of the 11 areas inspected,1 violation (failure to comply with the TS LCO for two inoperable RPS channels, paragraph 13.c) of NRC requirements was identified.

The: inspectors reviewed the areas discussed below.

The discussion provides an

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overall evaluation of each-area.

'The inspectors reviewed the actions taken by the licensee in response to

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previously identified items and licensee event reports, and it appeared j

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8912140336 891204 PDR ADOCK 05000295 a

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that the licensee had appropriately implemented both short-and long-term actions to prevent recurrence of the identified problems.

During observations of activities and evolutions performed by the

operations staff, the inspectors noted no problems with the performance of the staff.

It appeared that the licensee's operations staff performed their duties in an adequate manntr to ensure safe plant operation.

  • The licensee discovered a nonconservatism in the value of a factor used to compute a RPS trip setpoint.

Due to existing margins, no potential safety concern resulted. Analysis of the root cause of the error is considered an unresolved item.

The inspectors performed numerous tours of the plant during this

inspection period. During the tours, no significant problems were noted.

  • During observation and review of maintenance and surveillance activities, the inspectors noted no problems with the procedures, documentation, or activities reviewed.

In the area of security operations, the inspectors noted a potential

weakness in the area of escort responsibilities.

The licensee took prompt corrective action. Progress continues in the security upgrade program.

During numerous tours of the radiologically controiled area, the

inspectors found no problems with the implement.ation of the radiological protection program.

  • The inspector reviewed the actions taken by the licensee te review potential problems identified in 10 CFR Part 21 raports.

It appeared the licensee's review program was adequate.

During review of onsite events, the inspector noted that the licensee too;'

proactive measures in preparation for a planned outage of the 161-kV offsite power supply. The licensee's actions related to the inoperability of two RPS channels was found to be inadequate. The licensee failed to comply, in a timely manner, with the appropriate TS LCO, resulting in the issuance of a violation.

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H DETAILS

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Persons Contacted i

J. Bobba, Supervisor, Radiation Protection

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I C. Brunnert, Supervisor, Operations Quality Assurance J. Chase, Manager, Nuclear Licensing and Industry Affairs

  • M. Core, Supervisor, Maintenance
  • D. Dale, Supervisor, Quality Control
  • R. DeMeu1meester, Acting Supervisor, Operations

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'J. Dyer, Senior Quality Control Inspector

  • S. Ferguson, Construction Manager
  • W. Gates, Executive Assistant to the President
  • J. Geschwender, Licensing Engineer
  • R. Jaworski, Manager, Station Engineering

J. Kecy, Supervisor, Systems Engineering

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  • T. Mathews, Station Licensing Engineer
  • D. Matthews, Supervisor, Station Licensing
  • T. Mcivor, Manager, Nuclear Projects
  • K. Morris, Division Manager, Nuclear Operations
  • W. Orr, Manager, Quality Assurance and Quality control
  • G. Peterson, Manager Fort Calhoun Station A. Richard, Assistant Manager, Fort Calhoun Station
  • J. Sefick, Manager, Security Services
  • P. Septenko, Supervisor, Outage Projects
  • C. Simmons, Station Licensing Engineer
  • F. Smith, Plant Chemist
  • K Stuitz, Supervisor, Radiological Services D. Trausch, Supervisor, Operations
  • S. W111 rett, Manager, Administrative Services
  • Denotes attendance at the monthly exit interview.

The inspectors also contacted other plant personnel, including operators, technicians, and administrative personnel.

2.

Plant Status During this inspection period, the plant operated at 100 percent power.

No plant perturbations or challenges to safety systems were experienced.

3.

Review of Previously Identified items (92701 and 92702)

a.

(Closed) Open Item 28S/8836-03: Cracks found in the gear housing of Limitorque motor-operated valves (MOVs).

Cracks in Limitorque gear housings were identified during the performance of preventive maintenance activities by the licensee.

The cracks were located axially along the bolt holes in the gear

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housing in four valve operators, which are in the high pressure

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safety injection (HPSI) system.

In addition, in one of the four

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operators, multiple cracks were found in the upper housing of the I

operator.

The cracks were found only in Model SMB-00 Limitorque

MOVc.

This item was reviewed in NRC Inspection Report 50-285/89-05.

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F inspector was satisfied with all of the-licensee's corrective action taken to date.

Howeser, tht5 item remained open pending the

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completion of the licensee's documentation of the final root cause

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analysis and the reason for the valve operator gear housing cracks.

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i The licensee, in an internal memorandum (PED-SSE-89-6735), dated

. August 31, 1989, documented the results of their root cause analysis.

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The licensee concluded that the four valve actuators cracked due to the effects of overthrusting.

Historically, the valves experienced repeated challenges to the capacity of the valve motor operator. The thrust requirements for the actuator application.were high into the range of the capacity of the actuator.

Performance requirements at

this level placed the motor operator at risk for overthrust.

The HPSI valve actuators were unique to the group of the installed (

safety-related, motor-operated valves because the HPSI actuators were

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required to operate at the high end of their capacity. These were the only operators required to perform near their maximum capacity.

The licensee's analysis resulted in the following recommendations:

Perform a design review of HPSI motor operator requirements-

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Establish testing procedure restraints to prevent overthrusting

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possibilities.

  • Develop testing procedures and/or acquisition of a more accurate l

set of MOV test equipment.

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Install four rotor switching in each MOV.

The actions taken by the licensee were sufficient to close this open h

item.

However, the four recommendations listed above are considered an open item pending disposition by the licensee.

(285/8938-01)

b.

(Closed) Unresolved Item 285/88201-09 (Violation B.4):

Failure to L

use procedures for operation of the CCW and resin transfer systems.

This violation involved the following examples of the licensee's inattention to procedural requirements:

An operator pe* formed the steps of Procedure 01-CC-4, " Component

Cooling Systems Outage for Maintenance," without having the procedure in hand.

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An. operator failed to follow the procedure during the spent resin transfer.

Procedure 01-CH-6, "CVCS Resin Transfer,"

provided certain steps in the prerequisite section, rather than as clearly defined steps in the procedure. The problem was compounded when the individual involved continued on his own rather than stopping work and obtaining an approved b

on-the-spot-change before proceeding.

  • An auxiliary operator returned the dechromating system for the CCW system to service without the use of a procedure.

In addition, the operator was apparently unfamiliar with the installation.

The licensee's corrective actions included revising Procedure 50-0-29 " Conduct of Operations," to provide additional guidance on procedure use.

It defined when personnel were required

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L to have the procedure in hand and what actions can be taken outside of the scope of procedures, such as during an emergency. The procedure revision also emphasized the requirements for verbatim compliance with procedures.

In addition, Procedure OI-CH-6 was revised to correct identified deficiencies.

p The corrective actions taken by the licensee appeared to adequately address the problems identified by this violation.

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(Closed) Followup Item 285/8928-02:

Administrative controls for raw water (RW) flow.

Due to concerns with elevated Missouri river temperatures, the licensee performed an analysis to verify that the design basis upper limit of 85'F could be raised..It was determined that the design basis accident (DBA) cooling capability could be maintained above a river temperature of 85'F, proviced there was adequate raw water flow.

The licensee generated a curve of river temperature'versus flow requirements necessary to maintain DBA cooling capabilities',

The curve was included in Safety Analysis for Operability (SAO)89-012, " Elevated Ccmponent Cooling Water Temperature." The licensee incorporated a verification of the required RW conditions into the official control room log, Form FC-75. This verification is performed on a daily basis to verify that adequate RW flow exists for a given river temperature.

Based'on the above, it appeared that the licensee had implemented adequate administrative controls to ensure that sufficient RW flow was continuously provided to meet DBA conditions, d.

(Closed) Unresolved item 285/8932-01:

Potential problems with the electrical supply breakers for Pumps DW-46A and DW-46B.

This item was related to the identification of potential problems with the breakers for Pumps DW-46A and DW-46B.

The breakers were l

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-6-r supplied by the Satin American Company and the types of potential defects with the breakers were described in NRC Information Notice 89-45, Supplement 1, "Metalclad, Low-Voltage Power Circuit Breakers With Substandard Parts." Pumps DW-46A and DW-46B are used as deareating pumps in the pure water system. The pumps are not safety-related equipment; however, the pumps are connected to

safety related electrical buses and must be isolated during an

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accident.

In the event that offsite power is lost, the emergency F

11esel generator would provide power to all safety-related loads, but

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the DW-46A and DW-46B breakers may not trip due to defects in the breaker. The emergency diesel generator may be subsequently lost due

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to an overload on the bus since the generator can not supply the E

engineered safeguards equipment and a deareator pump, Therefore, it was necessary to ensure that the breakers for Pumps DW-46A and DW-46B trip to protect the integrity of these vital buses. The potential problems were identified by personnel from the NRC's Vendor Program Branch during an onsite inspection of the breakers.

The licensee tested the breakers and found that they satisfactorily passed all tests.

However, the NRC identified to the licensee that tht types of latent d'.tfects found in the breakers may not be

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detectable during testing.

To address this problem, the licensee replaced the breaker for Pump DW-46A with an unused spare breaker that was installed in a motor control center. The licensee obtained a spare breaker from the warehouse and used it to replace the breaker for Pump DW-46B.

Prior to installation of the breakers, the licensee verified that none of the conditions identified in Information Notice 89-45 existed.

Based on the actions taken by the licensee to replace the apparent deficient breakers, it appeared that the licensee had adequately resolved the breaker problem.

The inspector reviewed the actions-taken by the licensee and noted no-problems.

During review of the actions taken by the licensee to address previously identified items, the inspectors noted that appropriate actions had been taken to resolve the identified concerns, The actions taken by the licensee appear to be conservative and provide adequate controls to prevent recurrence of previously identified problems.

No violations or deviations were identified.

4, Qcensee Event Report (LER) Followup (92700)

Through direct observation, discussions with licensee personnel, and review of records, the following event reports were reviewed to determine l

that reportability requirements were fulfilled, immediate corrective

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action was accomplished, and corrective action to prevent recurrence had l

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The LERs listed below are closed:

88-032 Design Deficiency in the Safety Injection / Containment Spray Recirculation Piping l

!89-018'

Failure to Perform an Hourly Firewatch

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89-019 Manual Reactor Trip Due to High Temperature Indication on the

Thrust Bearing for Reactor Coolant. Pump (RCP) RC-3C L

A discussion of the review performed by the inspectors for each LER is

provided below:

a.

LER 88-032 reported a design deficiency in the safety

injection / containment spray recirculation piping.

The deficiency was that, under conditions in which all safety injection (SI) and containment spray (CS) pumps were running in the recirculation mode, calculations indicated that the recirculation line would not be able to pass the minimum flow required for all the pumps. The licensee's corrective actions were reviewed in NRC Inspection Report 50-285/89-05 during the closure of Open Item 285/8836-04. A portion of the corrective action was that a modification to the electrical circuitry was made such that the CS pumps would start only after receipt of a CS actuation signal. This would present the CS pumps from being run in the recirculation mode when the SI pumps were running.

Region IV requested that the NRC's Office of Nuclear Rear. tor Regulation (NRR) review the design modification since the start of the CS pumps was modified so the pumps started 30 seconds after an actuation signal was received.

This delay ensured that sufficient time was available for the CS valves to open.

By letter dated September 12, 1989, NRR concluded that the licensee's analyses were in conformance with NRR staff guidelines and satisfactorily indicated that peak containment pressure was within the design limits with the delayed start of the CS pumps.

This LER is considered closed, b.

LER 89-018 reported an event where an hourly firewatch patrol was not performed for a nonfunctional fire barrier in accordance with TS 2.19(7). The patrol was missed for approximately 5 days due to a fire door being removed from the firewatch patrol log.

The licensee attributed the cause of the event to inadequate procedural control over the release of firewatches, ineffective communications between involved personnel, and procedural noncompliance.

The inadequate procedural control occurred when the firewatch was i

released per a telephone conversation between a security sergeant and a licensed operator.

The miscommunication occurred when the fire door that the operator wanted removed from the firewatch log was not the door the security sergeant understood it to be. The applicable procedure stated that the shif t supervisor and the fire protection

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I system engineer (or their designees) were the only persons authorized to terminate an hourly firewatch patrol.

In addition, the shift

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security supervisor was required to be notified. These procedural l

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requirements were not performed.

The missing of firewatch patrols has been an ongoing problem at FCS.

t Previous corrective actions, such as procedure changes, have not been

totally effective. The licensee, due to this event, implemented the i

following corrective actions to prevent recurrence of the problem:

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Revised Form FC-1140, " Current Fire Protection Impairments Log,"

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prior to terminating an hourly firewatch.

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Revised Procedure 50-G-58, " Control of Fire Protection System Impairments," to reflect the above requirements, Revised Form FC-1006, " Hourly Fire Watch Log," and its a

associated procedure to require that the signature of the fire protection system engineer or the operations shift supervisor be

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obtained to clear a firewatch. -Telephone approval is no longer i

permitted.

The actions taken by the licensee should significantly reduce the

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probability of missed firewatches due to the erroneous terminating of firewatches.

This LER is considered closed.

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LER 89-019 reported an event where the plant was manually scrammed due to a high temperature indication on the thrust bearing for RCP RC-3C.

Subsequent investigation by the licensee indicated that the high temperature problem was due to faulty wiring connected to the bearing resistance temperature indicator. The licensee replaced

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the wiring and restarted the plant.

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The inspector reviewed the actions taken by the licensee's operating staf f in response to this event immediately af ter the occurrence.

As noted in NRC Inspection Report 50-285/89-33, the inspector noted that the operations staff performed their duties and responded to the

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event in a professional manner. Based on the review previously performed by the inspector, this LER is considered closed.

Based on the reviews performed by the inspectors, as described above, it appeared that the licensee took appropriate actions in response to the identified events to provide timely corrective actions and implementation

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of controls to prevent recurrence of the event.

No violations or deviations were identified.

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0perational Safety Verification (71707)

The inspectors conducted reviews and observations of selected activities to verify that facility operations were performed in conformance with the requirements established under 10 CFR, the licensee's administrative procedures, and the TS. The inspectors made several contr)1 room observations to verify the following:

Proper shift staffing was maintained and conduct of control raom

personnel was appropriate.

Operater adherence to approved procedures and TS requirements was

evident.

Operability of reactor protective system, engineered safeguards

equipment, and the safety parameter display system was maintained.

If not, the appropriate TS LCO was met.

Logs, records, recorder traces, annunciators, panel indications, and

switch positions complied with the appropriate requirements,

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Proper return to service of components was performed.

  • Maintenance work orders (MdO) were initiated for equipment in need of

maintenance.

Management personnel toured the control room on a regular basis.

  • Control room access was properly controlled.

Control room annunciator status was reviewed to verify operator

awareness of plant conditions.

Mechanical and electrical temporary modification logs were properly

maintained, Engineered safeguards systems were properly aligned for the specific

plant condition.

During review of this area, the inspectors identified the following items:

a.

On October 18, 1989, the licensee confirmed that the value of 1.8 for the total integrated radial peaking f actor upper limit given by TS 2.10.4(2) and Figure 2.9 of the TS was nonconservative. The total integrated radial peaking f actor (FrT) ic a component of the equation used to calculate the RPS setpoint for the thermal margin / low pressure (TM/LP) trip function. The licensee found that if the Cycle 12 core were allowed to develop an FrT of 1.8 in a depressurization scenario, the reactor would not trip until primary plant pressure dropped to 46 psia below the required setpoint. The licensee investigated and found that the current core arrangement was

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p not' capable of producing an Fri of 1.8 and the highest value to date had been 1.65, Therefore, a safety concern did not result from the error in the TS.

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In performing the recalculation, the licensee determined, with h

concurrence from. Combustion Engineering, that the appropriate upper

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. limit of Fri was:1.77..The licensee implemented administrative L

controls to restrict FrT to a value of 1.75 or less for the remainder of the cycle._ Operations Memorandum 89-03 was issued by tne licensee to provide' explicit instructions that clearly modify the TS-

requirements in a-conservative manner.

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-The inspector-verified that the operations memorandum was approved by-the plant review committee, the memorandum was placed in the control

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room copy of the TS, and training was provided to operations

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personnel.

The inspector considered that the actions taken by the i

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licensee were appropriate, conservative, and satisfactory for the remainder of the current fuel cycle.

The is value will be changed when the licensee submits its license amendment request for the

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g upcoming Cycle 13, if necessary.

F In June 1988 the licensee discovered that the actual setpoint of the TM/LP trip function was set nonconservatively.

NRC Inspection l

p-Report 50-285/88-22 discussed this error, its cause, the safety-related implications, and the corrective actions taken by the i

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Severity Level III Violation 285/8822-01 was issued as a result of the NRC followup inspection on this occurrence.

It was determined that an inadequate' design control program caused the

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setpoint to be' incorrectly. determined. Additional review is required to determine if the present incorrect value of FrT resulted from design control inadequacy or another programmatic problem.

Additional review of this problem is considered an unresolved item.

(285/8938-02)

'b.

.On October 24, 1989, the licensee requested'an extension of a commitment made to the NRC in response to Violation 285/8725-01. The violation involved the licensee's failure to correct deficiencies with safety-related fire doors.

-The licensee's response to the violation stated that the safety-related fire doors located in the auxiliary building would be replaced by October 31, 1989. The licensee requested an extension of the commitment until January 31, 1990.

On October 27.. 1989, the Chief, Project Section B, Division of Reactor Projects, Region IV, approved the extension of the commitment based on the licensee's problems encountered with purchasing the necessary materials.

The licensee was notified of the approval on October 27, 1989.

No violations or deviations were identified, i

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Plant Tours' (71707_)

-The-inspector _' conducted plant tours at various times 'to assess plant and c-

' equipnient conditions.' The following items were observed during the tours:

Genuil plant condit1'ons, including operability of standby equipment,

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'Eouipmentiwas_beingmaintainedinpropercondition,withoutfluid

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o Naks and excessive vibration.

  • Valves and/or switches for safety-related systems were in the. proper position.

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Plant. housekeeping and cleanliness practices were observed, including no fire hazards and the control of combustible material,

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Performance of work act Nities was in accordance with approved procedures.

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Portable gas cylinders were properly stored to prevent possible missile' hazards.

  • Tag-out'of equipment was' performed properly.

Management personnel toured the operating spaces on a regular basis.

During' tours of the plant, the inspector noted the items listed below:

The results of the-. plant tours performed by the ' inspector indicated that the licensee was providing-adequate attention to the physical condition of

.the plant. Work continued on painting and clean up of the. plant to

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improve the-overall appearance.

Plant housekeeping has been very good.

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a.

On~0ctober 24, 1989, the inspector accompanied a cognizant licensee employee on a comprehensive tour of the warehouse.

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personnel were in the process of segregating, safety-related from nonsafety-related material. 'The inspector considered the new system a significant improvement which will further reduce the likelihood of

interchanging nonsafety-for' safety-related components'.

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The inspector toured the chemical storage area-to gain a working knowledge of how the lit.ensee implements its chemical control program in accordance with Procedure'S0-G-70, " Chemical Control." No problems were noted.

c.

On October 6, 1989, it was observed that the licensee used an absorbent material to soak up spilled diesel fuel and lube oil in the

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emergency diesel generator rooms.

The flame retardancy of the material was questioned.

The station fire protection engineer was 3.. - -......,,

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aware of its use and provided the inspector with the manufacturer's literature verifying the flame retardancy of the material, it appeared that the material was being appropriately used.

No violations or deviations were identified.

7.

Monthly Maintenance Observations (62703)

The inspector reviewed selected station maintenance activities on safety-related systems and components to verify that maintenance was conducted in accordance with approved procedures, regulatory requirements, and the TS.

The following items were considered during the reviews:

-The TS LCGs were met while systems or components were removed from

service.

Approvals were obtained prior to initiating the work.

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Activities were accomplished using approved MW0s and were inspected,

as applicable.

Functional testing and/or calibrations were performed prior to

returning components or systems to service.

Quality control records were maintained.

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Activities were accomplished by qualified personnel.

Parts and materials used were properly certified.

Radiological and fire prevention controls were. implemented.

T:.c inspector examined the following MW0s f rom a random selection to verify compliance with licensee Procedure 50-M-101, " Conduct of Maintenance."

Adjustment of the flow for the containment stack monitor flow

(MWO 894853)

Projected oil leak from RCp RC-3D motor (MWO 894516)

Alarm trouble on plant security Door 1007-5 (MWO 894390)

Installation of the compressed air temporary air dryer (MWO 894262)

As a result of the review of the sample of MW0s, it appeared that licensee was implementing its maintenance program in accordance with approved procedures resulting in documentation that was fully auditable.

For each of the MW0s reviewed, the attributes listed above appeared to be met.

No violations or deviations were identified.

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8.

Monthly Surveillance Observations (61726)

The inspector observed selected portions of the performance of the TS-required serveillance testing on safety-related systems and components.

.The inspector verified the following items during the testing:

Testing was performed by qualified personnel using approved

. procedures.

Test instrumentation was calibrated.

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The TS LCOs-were met.

Removal and restoration of the affected system and/or component were

accomplished.

Test results conformed with TS and procedure requirements.

  • Test results were reviewed by personnel other than the individual directing the test.

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Deficiencies identified during the testing were properly reviewed and resolved by appropriate management personnel.

Test was performed on schedule and complied with the TS required frequency, The inspector observed the following surveillance test activities. The procedures used for the test activities are noted in parenthesis:

Monthly check of the high containment pressure channels (ST-RpS-8)

Monthly check of the high containment pressure channels (ST-ESF-3)

A' discussion of each surveillance observed is provided below:

a.

On October 23, 1989, the inspector observed a technician perform Procedure ST-RPS-8, " Monthly Check of the High Containment Pressure Channels." The test verified the proper operation of the channels within each of four RPS trip units.

This was done by electronically inputting pressure signals to the respective pressure switches associated with each channel and verifying that each channel tripped and provided the appropriate alarms.and indications. No problems were noted with either system performance or execution of the test.

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On October 23, 1989,'the inspector observed the performance of Procedure ST-ESF-3, " Monthly Check of the Containment Pressure Channels." This' test verified the operability of the containment pressure channel inputs to the engineered safeguards features system.

The technician properly executed the test and the system performed as designed.

No problems were noted.

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Based on' the observations made by the inspector it appeared that_ the licensee was-adequately implementing an effective surveillance testing program.- In each test observed, the inspector noted that licensee

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personnel were performing the-testing evolutions in accordance with the

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. appropriate procedure, as written.

No violations or deviations were identified.

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9.

Security Observations (71707)

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The inspectors verified that the physical security plan was being

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The. security organization was properly manned.

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Personnel within the protected area (PA) displayed their

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identification badges.

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Vehicles were properly authorized, searched, and escorted or

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controlled within the;PA.

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Persons and packages were properly cleared and checked before entry

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into the PA was ; permitted.'

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The effectiveness of_the securit9 program was. maintained when security equipment failure or' impairment required compensatory b

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measures to.be' employed.

The PA barrier was maintained and the isolation zone kept free of-

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transient material,

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t The vital' area. barriers were maintained and not compromised by

breaches or weaknesses; Illumination in the PA was adequate to observe the appropriate areas

at night.

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Security monitors at the secondary and central alarm stations were

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  • On Octcber. 12, 1989, the inspector observed activities in the construction area within the PA.

The inspector noted at least two contract workers,

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who were in the PA on visitor passes, were possibly out of the line-of-sight of their designated escorts. The inspector summoned a

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nearby member of the security force who took prompt action by escorting several persons in question off site for retraining in security

- requirements and escort responsibilities.

Additionally, the licensee issued Security Communications Notice 029-89 on October 19, 1989, reinforcing ways in which the security force can help prevent escort / visitor violations. Also, a statement reiterating the h

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vulnerability of escort / visitor violations in the construction area was

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~ published in the station plan-of-the-day and will remain there until the end of the year, i All badged personnel will be made aware of their escort responsibilities in their annual general employee training.

Visitors are made aware of their responsibilities upon processing in.

On October 20, 23, and 25, 1989, the inspector revisited the area, found no violations, and noticed an increased security presence to protect against this vulnerability.

It appeared the licensee took aggressive actions to correct what was perceived as a weakness.

It appeared, based on the observations made by the inspector, that'the licensee's guard force was adequately performing its duties. The security system is currently being extensively modified and the extent of the modifications require extensive compensatory measures be taken.

The inspector noted that the compensatory measures have been very good and compensate for all security system degradations.

No violations or deviations were identified.

10.

Radiological Protection Observations (71707)

The inspector verified that selected activities of the licensee's radiological protection program were implemented in conformance with the facility policies and procedures and in compliance with regulatory requirements. The activities listed below were observed and/or reviewed:

Health physics (HP) supervisory personnel conducted plant tours to

check on activities in progress.

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HP technicians were using calibrated instrumentation.

Radiation work permits contained the appropriate information to ensure that work was performed in a safe and controlled manner, Personnel in radiation controlled areas (RCA) were wearing the required-personnel monitoring equipment and protective clothing, and were properly frisked prior to exiting an RCA.

Radiation and/or contaminated areas were properly posted and

controlled based on the activity levels within the area.

Based on the observations and reviews performed by the inspector, it appeared that the licensee was implementing an effective radiological protection program.

No violations or deviations were identified.

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i 11..In-Office Review of Periodic, Special, and Nonroutine Event Reports

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(90712 and 90713)

In-office review of periodic, special, and nonroutine event reports was performed by the inspectors to verify the following, as appropriate:

Correspondence included the information requ1 red by appropriate NRC

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requirements.

Test results and supporting i.nformation were consistent with design

predictions and specifications.

Planned corrective actions were adequate for resolution of identified

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problems.

Whether or not any information contained in the correspondence report

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should be classified as an abnormal occurrence or additional reactive inspection is warranted.

Correspondence did'not contain incorrect, inadequate, or incomplete

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information.

The. inspectors reviewed the following correspondence:

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Inservice Testing Program for Pumps and Valves, dated October 2, 1989 Failure to Maintain Compensatory Action Due to Inattentive Security Officer (LER 89-S07), dated' September 21, 1989 Auxiliary Feedwater Panel Instrumentation Outside Design Basis

(LER 89-014, Revision 1), dated ~ September 29, 1989 Failure' to Maintain Compensatory Action (LER 89-S08), dated September 20, 1989 Followup to Special Reports-on Inoperability of Fire Barriers and

Fire Detection Systems, dated September 19, 1989

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Monthly Operations Report for September 1989, undated September Monthly Operating Report, dated October 13, 1989 Feedwater Valve HCV-1386 Inoperable Due to Maintenance Program Deficiency (LER 89-012, Revision 1), dated October 13, 1989 Manual Unit Trip Due to High ludicated Reactor Coolant Pump Motor Bearing Temperature (LER 89-019), dated October 24, 1989

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Update'to' Revision 4 of-the Inservice Testing Program, dated

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No' violations or deviations were identified.

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Review of 10 CFR Part 21 Reports (36100)'

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-The-inspector reviewed the licensee's activities related to the processing

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.of Part 21 reports. l The review was performed to verify that the licensee

.had processed, in accordance with the appropriate procedures,-the Part 21'

q reports-that had been provided to the licensee by the inspector.'The-Part 21 reports were identified by a regicnal specialist as potentially affecting the safety of the FCS.

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The Part 21 reports reviewed by the inspector are listed below:

- The Foxboro Company issued a Part 21 report (Region IV Log No. 87-03)-

on problems with E-Line and H-Line instruments. The' manufacturer's

- letter was dated June 4, 1986.

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During previous inspection activities, the concern with the-

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instruments was identified as Open Item 285/8523-02 in NRC Inspection =

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Report 50-285/85-23. This.open item was reviewed and closed by an

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inspector as-the actions taken by the licent.ee to address this item

g were adequate.

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Gibbs and Hill identified a potential problem with the containment spray system recirculation lines not being classified as safety-related piping. The Part 21 report (Region IV Log No. 87-13)

was issued on March 17, 1986.

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The licensee reviewed this potential problem and noted that the problem did not exist-at the FCS, since the recirculation lines had

- been fabricated, installed': and maintained as a safety-related

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installation.

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Morrison-Knudsen identified a potential problem with saturable core

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transformers installed on emergency diesel generators and submitted a Part 21 report (Region'IV Log No' 87-83) on September ~ 29, 1987. -The transformers with potential problems were manufa'ctured-by the-Bassler Electric Company.

The licensee reviewed this report and noted, that it did not apply to FCS since saturable core transformers were not installed on the licensee's emergency diesel' generators.

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1The. Westinghouse Company issued a Part 21 report (Region IV Log

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No. 87-82) on October.16, 1987 3The report described problems that

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p, were. identified with Westinghouse W-2 type circuit'. breaker cell switches.

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- The. licensee reviewed the appropriate documentation and noted that b[..

the type of cell switches installed at'FCS were not the ones identified by the Part 21 report.

  • On October 19, 1987, the Peach. Bottom Atomic Power Station issued a

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Part 21 report (Region IV Log No. 87-81) regarding nondestructive L

examination services provided by Eastern Testing and Inspection

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(ETI).

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- By review of-purchasing documents, the licensee determined that ETI

.had not performed any activities at-FCS,

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' The Gamma-Metrics Company issued a Part 21 report (Region IV Log No. 88-07.) that described prublems with leaking cable assemblies.

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The report, dated May 10= 1988,; stated that the. solder-joints for the

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connectors for the RPS cabling;may leak.

The licensee performed a leak-test en the connectors and noted that

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leakage occurred. To address this deficiency, the licensee generated

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- SA0 88-01:to address continued plant operation:with the leaking

connectors.

The results of the evaluation provided by SA0 88-01

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indicated that continued plant = operation was. acceptable.

The inspector performed a review'of the, actions"taken by the licensee with respect to this problemi The results of the review are documented in NRC Inspection-Report 50-285/88-46.

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On October 18, 1988, the Automatic Switch Company issued.a Part 21

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report (Region IV Log No. 88-16) to document a problem identified with ASCO NP-8314 series solenoid valves.

The specific problem identified in the report was that the' solenoid may not shift positions when deenergized if'the solenoid had been energized for a long period of time.

The licensee performed a review of the types of ASCO solenoids installed at FCS. The review identified three valves that had solenoids installed that were the subject of the report.

The valves were' replaced.- The licensee also reviewed the stock supplies in the warehouse and removed the appropriate solenoid-operated valves.

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On November 3, 1988, the Limitorque Corporation generated a Part 21 report (Region IV Log No. 88-18) that addressed inadequate starting

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torque at elevated temperatures for RH-insulated motors.

The report stated that the motors were operated by dc power.

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The licensee reviewed the report and noted that no de Limitorque motors were installed at FCS.

The inspector reviewed the actions taken by the licensee to address the Part 21 reports listed above.

Based on the review, it appeared that the licensee had taken the appropriate actions to address these identified potential problems. The review of the Part 21 reports listed above is considered closed.

No violationslor deviations'were identified.

13.

Review of Onsite Events (93702)

During-this inspection period, the inspector reviewed the onsite events

. discussed below; a.

On October 11, 1989, the licensee removed the 161-kV offsite power supply from service for maintenance. The 161-kV supply is one of the two offsite power sources available to the plant.

The 161-kV line was removed from service so three transmission line poles could be replaced prior to the onset of the harsh winter months. The poles had been slightly damaged by a grass range fire during the summer months. The actions taken by the licensee were preventive measures to maximize the reliability of the 161-kV power supply.

Prior-to removal of the offsite power supply, the licensee took prnactive measures to ensure that guidance was given to operations personnel on what actions to take in the event that the ramaining offsite power supply was lost.

Loss of the second power supply would cause the plant to enter the natural circulation mode of operation.

The guidance provided to the operations staff included items such as no work was to be conducted on electrical equipment, operability of both emergency diesel generators was to be verified, routine rotation

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of electrical equipment in service was not to be performed, and review of the appropriate emergency and abnormal operating procedures was to be performed.

The inspector reviewed the actions.taken by the licensee and it appeared that the actions were adequate. The inspector also verified that the licensee took.the actions specified by the LC0 for a loss of the 161-kV power supply as specified by TS 2.7(2)n.

No problems were noted.

b.

On October 12, 1989, the licensee determined that the component cooling water (CCW) inlet and outlet valves (HCV-489A and HCV-489B)

for CCW Heat Exchanger (HX) AC-1A could not be operated f rom the control room. The inoperability of the valves resulted in the inoperability of CCW HX AC-1A. At the time of discovery, CCW HX AC-1B was also inoperable due to maintenance activities being performed on the HX.

Based on the inoperability of two CCW HXs, it

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appeared that;the licenseeldid not comply with TS 2.3, which requires

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the plant to be'placed-in a cold shutdown condition.

' The. inspector's review of the apparent f ailure to comply with TS 2.3 is discussed in NRC Inspection Report 50-285/89-48,

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At approximately 9:45 a.m. on September 13, 1989, 'the licensee.

experienced a problem where a-power level deviation between the t

E-delta TLpower and nuclear power meters on the RPS was as.high as D

4 percent.' For Channels A and B, the_ delta T power meter indicated

.up to 4 percent less than nuclear power.

For Channels C and D, the

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delta T meter indicated up to 4 percent above nuclear power. Due to

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the magnitude of the deviation, an annunciator alarm was received on L

the control board to alert the operations. staff of the problem. The operations: staff,-in conjunction with the reactor engineer and

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engineering support personnel, reviewed the status of the appropriate

' plant systems to verify that no system problems existed..The review included an' analysis of core performance, reactor coolant system flow b

rates, and a. plant walkdown to verify no systems were leaking. After reviewing the appropriate data, the licensee's staff determined that

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the alarm was most likely caused by instrumentation problems and no actual plant problem existed.

Based on the data available,-the operations shift supervisor declared all RPS channels operable and continued to operate the~ plant at 100 percent power.

The operability

, determination was made. by the shift supervisor at approximately 16:30 a.m.

At approximately 12:20 p.m., the acting plant manager, who was in a

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meeting at the corporate offices in Omaha, Nebraska, was notified of

'the problem.

Subsequent discussions were held between plant

supervision, the acting plant manager, and the plant manager over the telephone. The plant manager was attending a-meeting in

. Washington,1D.C.

Based lon discussions between licensee management, it was decided to declare-RPS Channels A and B inoperable since the

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delta T meter on these channels provided a nonconservative indication of reactor. power. At;2:25 p.m.,

the channels were officially declared inoperable.

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The action specified by the.LC0 in Table 2-2 of TS 2.15 requires that one-inoperable channel be placed in the tripped condition within I hour and the other channel be placed in' bypass.

The LC0 also states that, if two channels are inoperable, load shall be reduced to-70 percent or less of rated power.

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Within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />, the licensee placed one RPS channel in bypass and one in the tripped condition. An actual power reduction was not initiated until I hour after the RPS channels were declared i noperabl e.'

During this 1-hour period, it was not evident that the licensee initiated timely actions to reduce the power. Although the licensee took actions to prepare for the power reduction, the actions appe'ared to be directed toward allowing technicians to take

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-21-measurements of the RPS input rignals before power.was reduced. At

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the end of_ the-1-hour requirement for placing one channel in bypass

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.and one channel in trip, the operations shift supervisor directed the

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technicians to stop the measurement activities so that the power

L reduction could be initiated.

It appeared that the licensee complied with the TS requirement for

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placing one RPS channel in bypass and one channel in trip. However, it did not appear that the licensee's actions in complying with the TS requirement for reducing power to'70 percent or less was timely.

This is an apparent violation for failure to meet a TS LCO.

(285/8938-03)

At approximately 3:33 p.m.,

the operations staff initiated injection of boric acid to reduce the power level. A power level of less than 70 percent was achieved at approximately 6:55.p.m.

Table 2-2 of TS 2.15 states that plant power must be reduced to le than 70 percent of rated power; however, the TS does not state a time period in which the power reduction must be achieved.

In discussions

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with licensee management, the inspector determined that an assumption was made by management that since no time requirement was specified, the power reduction should be performed conservatively. ' Management decided that a power reduction over a 4-hour period was satisfactory to comply with the TS. This interpretation of the TS appeared to be inappropriate since the TS did not specify a time period when the power reduction should be initiated.

On October 5, 1989, licensee management met with NRC management in the Region IV office to discuss the event and the actions taken by the licensee in response to the event. At this meeting, the licensee stated that the items listed below contributed to the problems i-experienced during response to this event:

Final operability determination of the RPS was not timely.

  • Power reduction was not commenced immediately after the

inoperability determination.

n A procedure did not exist to address TS. interpretation.

A procedure upgrade is required to define the specific line of authority during the' absence of the plant manager.

The licensee has initiated actions to implement requirements to address the items listed above.

In a letter to the NRC dated October 31, 1989, the licensee committed to taking actions to resolve their identified problems.

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[14; Exit Interview:

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y The inspectors met:with Mr.~ K. J,. Morris, (Division Manager : Nuclear-

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= Operations).;and other members -of:the' licensee staf f.on. November 13,1989.

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- The meeting-attendees are listed in.: paragraph 1 of this inspection report.

?E, At:this meeting the' inspectors summarized,tbe scope of.the-. inspection and

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. the" finding!.. - During the exit meetingp the licensee didLnot identify any -

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proprietary;.information to the-inspectors,

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