ML20217G566

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Insp Repts 50-413/98-01 & 50-414/98-01 on 980111-0221. Violations Noted.Major Areas Inspected:Operation,Maint, Engineering & Plant Support
ML20217G566
Person / Time
Site: Catawba  Duke Energy icon.png
Issue date: 03/23/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20217G543 List:
References
50-413-98-01, 50-413-98-1, 50-414-98-01, 50-414-98-1, NUDOCS 9804020423
Download: ML20217G566 (33)


See also: IR 05000413/1998001

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U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos: 50-413. 50-414

License Nos: NPF-35. NPF-52

Report Nos.-: 50-413/98-01. 50-414/98-01

Licensee: Duke Energy Corporation

Facility: Catawba Nuclear Station. Units 1 and 2

-Location: 422 South Church Street

Charlotte. NC 28242

Dates: January 11 -' February 21, 1998

Inspectors: D. Roberts. Senior Resident Inspector

R. Franovich, Resident Inspector

M. Giles. Resident Inspector.(In Training)

N. Economos.-Reactor Inspector RII (Sections M1.1, M1.2)

M. Widmann Resident Inspector. Vogtle (Sections 04.1. F2.1)

Approved by: C. Ogle. Chief

Reactor' Projects Branch 1

Division of Reactor Projects

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Enclosure 2

9804020423 '900323

,. . PDR ADOCK 05000413

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EXECUTIVE SUMMARY

Catawba Nuclear Station. Units 1 and 2

, NRC Inspection Report 50-413/98-01. 50-414/98-01

This. integrated inspection included aspects of licensee operations,

maintenance, engineering, and plant support. The report covers a 6-week '

period of resident ins)ection: in addition, it includes the results of I

announced inspections )y a regional reactor inspector and a visiting resident

inspector.

Doerations.

- -A Unit 1 shutdown on January 18, 1998, and power reduction activities on

February 20. 1998, were conducted well. On February 20. 1998. operators

particularly did well during the coordinated effort to swap 0-ring leak

detection paths, including the establishment of effective communications

between the control room and containment building, and the monitoring of -

diverse leak detection sources. (Section 01.1)

- Control-room operators appropriately identified and corrected a fault in

the control room ventilation system. An Unresolved Item was opened

pending NRC review of the basis for assuming that the control room

ventilation system is allowed to be inoperable for five minutes

following a safety injection, radiation release within the plant or a

chlorine leak. (Section 01.2)

. A Violation with four examples of failure to follow plant operating and

administrative procedures was identified. These included two separate

events resulting in the inadvertent injection 6f emergency core cooling

system water into the reactor coolant system, and inappropriate actions

regarding the by]assing of an automatic feature following a manual reactor trip wit 1 the plant already shutdown. Procedural weaknesses

contributed to the fourth example regarding containment chilled water .

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pump operation. (Sections 04.1. 08.1. 08.2. and 08.3)

- The Plant Operations Review Committee meeting which was convened to

discuss plans to swap the Unit 1 reactor vessel flange 0-ring leak

detection from the inner 0-ring to the outer one was conducted in

accordance with commitments contained in the Updated Final Safety

Analysis Report Chapter 16. Selected License Commitments, with adequate

representation and a quorum present. The committee exhibited good

questioning attitude regarding issues associated with the leak detection

capability while aligned to the outer 0-ring. (Section 07.1)

Maintenance

  • Cleaning of.the 2 B component coolirg water heat exchanger was well

planned, managed and executed with sufficient oversight from the

cognizant engineer who displayed a good working knowledge of the

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personnel, including welders, were adequately trained to perform their ,

assigned tasks. Procedures were followed tests were performed and )

records were complete and accurate. (Section M1.1) j

. Replacement of certain isolation valves on the service water system used

on the control room air chillers was consistent with applicable code

requirements for material and processes. Engineering overview was

adequate. Welders assigned on the job lacked adequate knowledge in the

licensee's welding process control program which resulted in a work

stoppage. The licensee's inability to establish a strong working

program to address these problems was regarded as a weakness. (Section

M1.2)

. An Unresolved Item was open pending further NRC review of a Technical

Specifications compliance issue associated with containment valve

injection water system valve 2NW-190A. (Section M2.1)

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. The licensee's scaffolding program was in compliance with the

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requirements of Title 29 Code of Federal Regulations Part (CFR) 1926.

Safety Standards for Scaffolds Used in the Construction: Final Rule.

With the exception of a discrepancy identified between actual internal

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contamination levels and the amount posted radiological handling and

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storage of scaffolding material was adequate. (Section M2.2)

. One Non-Cited Violation was identified for the failure to follow

maintenance procedures which resulted in an unapproved aluminum packing

spacer being installed in the Unit 1 B steam generator main feedwater

regulating valve. (Section M2.3)

Enaineerina.

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. An Inspector Followup Item was opened to assess the licensee's dose

analysis calculation for emergency core cooling system leakage outside

containment after discrepancies were identified between assumptions made

by the licensee and those discussed in the Updated Final Safety Analysis

Report. (Section E3.1)

- The licensee's identification of a refueling water storage tank level

transmitter design deficiency was commendable. Their initial inspcction

of the level transmitter boxes failed to reveal moisture in one of them.

The licensee's corrective efforts to address the inadequacy of their

initial inspections were appropriate. (Section E7.1)

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A-Violation of 10 CFR 50.59 was identified for the licensee's failure to

perform a. safety evaluation, including an unreviewed safety question

determination, for compensatory actions assot.iated with the realignment

of the auxiliary feedwater system pumps' normal suction sources. Inis

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issue also involved poor decision making in the licensee's

implementation of the clearance process (instead of the temporary

modification process). (Section E8.1)

Plant Sucoort

- Radiation protection activities were generally adequate. with minor

discrepancies identified in the radiological labeling of some

scaffolding containers. (Section R1.1)

- One Non-Cited Violation was identified for failure to establish

compensatory fire watches after several fire detection zone alarms

malfunctioned for greater than 14 days. The inspectors identified a

weakness concerning the lack of written guidance to operators on how to

effectively monitor the fire detection panel alarms. (Section F2.1)

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Reoort Details

Summary of Plant Status

Unit 1 operated at or near 100 percent power until January 16, 1998, when a

power reduction was initiated due to erratic operation of steam generator B

feedwater control valve ICF-37. Power was reduced to approximately 30 aercent

power for valve repair. Power escalation to 79 percent was completed w1en

continued erratic operation resulted in the unit being shutdown for valve

repairs. The unit entered Mode 2 and then Mode 3 on January 18, 1998.

Following repair of ICF-37, reactor startup (Mode 2) commenced on January 20,

1998. The unit was placed on-line January 20, 1998, and power was increased

to 100 percent on January 21. 1998. On February 20, 1998. reactor power was

reduced to approximately 15 percent power to realign the reactor vessel flange

0-ring leakoff valve leak detection from the inner 0-ring to the outer 0-ring.

Power escalation commenced on February 20. 1998, and the unit was returned to

100 percent power on February 21, 1998. The unit operated at or near 100

percent power for the remainder of the inspection period.

Unit 2 operated at or near 100 percent power until February 15, 1998. when

reactor power was reduced to approximately 90 percent power for main turbine

control valve movement testing. Following test completion, the unit was

returned to 100 percent power on February 16, 1998. The unit operated at or

near 100 percent power for the remainder of the inspection period.

Review of Uodated Final Safety Analysis Reoort (UFSAR) Commitments

While performing inspections discussed in this report. the inspectors reviewed j

the applicable portions of the UFSAR that were related to the areas inspected.

The inspectors verified that the UFSAR wording was consistent with the

observed plant practices, procedures, and/or parameters. One discrepancy

concerning assumptions made in accident dose calculations is discussed in

Section E3.1. Also, a 10 CFR 50.59 violation concerning changes made to the

plant affecting the normal suction source for the AFW pumps is detailed in

section E8.1.

I. Doerations

01 Conduct of Operations

01.1 General Comments (71707)

The inspectors conducted frequent control room tours to verify proper

staffing, operator attentiveness and communications, and adherence to i

approved procedures. The inspectors attended operations shift turnovers l

and site direction meetings to maintain awareness of overall plant j

status and operations. Sperator logs were reviewed to verify

operational safety and compliance with Technical Specifications (TS).

' Instrumentation, computer indications, and safety system lineups were

periodically reviewed, along with equipment removal and restoration

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tagouts, to assess system availability. The TS Action Item Log (TSAIL)

books for both units were reviewed daily for potential entries into

limiting conditions for operation (LCO). action statements. The

inspectors conducted plant tours to observe material condition and

housekeeping. Problem Identification Process (PIP) reports were

routinely reviewed to ensure that potential safety concerns and

equipment probler were resolved.

A Unit 1 shutdown on January 18, 1998, and power reduction activities on

. February 20, 1998, to support a feedwater regulating valve repair and

swapover to reactor vessel flange outer 0-ring leak detection path,

respectively, were conducted well. Operators particularly did well

during the coordinated effort to swap 0-ring leak detection paths,

including the establishment of effective communications between the

. control room and containment building, and the monitoring of diverse

leak detection sources.

. 01.2 Loss of Control Room Ventilation

a. Insoection Scoce (71707)

On February 4. 1998, following maintenance on the B-train control room

ventilation (VC) system, an open access door on a VC air handling unit

(AHU) compromised the ventilation system's pressure boundary when the

AHU was returned to normal alignment. To determine the subsequent

impact on system operability and reportability, the inspectors discussed

the issue with licensee personnel and reviewed the applicable TS,

reportability requirements, and station PIP 0-C98-0476.

b. Observations and Findinas

On February 4, 1998, maintenance activities were 3erformed on the B-

train VC system to replace access doors on AHU 2CR-AHU-1. Ventilation

dampers 2CR-D-1 and 2CR-D-4 were closed to isolate 2CR-AHU-1 for work

execution. The A-train VC system was o)erating to maintain a aositive

control room pressure in accordance wit 1 the VC system design ) asis.

Early on February 5.1998, after maintenance was completed ventilation

dampers 2CR-D-1 and 2CR-D-4 were reopened. and the air handling unit was

realigned to the system's flowpath.

Soon afterwards, control room operators noticed a change in the noise

level and temperature in the control room. A control room access door

was opened to determine if the control room was pressurized. Air flow

into the control room from the opened door indicated that positive

pressure may have been lost. Ventilation dampers 2CR-D-1 and 2CR-D-4

were closed.~and control room pressure returned to normal.

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The licensee determined that an access Janel to the air handling unit.

located in the auiliary building, had )een o)ened.during the .

maintenance activity. - At the completion of t1e maintenance activities.

the access door was not latched closed. When the isolation dampers were

opened, flow from the operating A-train of VC was diverted through the

open access door and into the auxiliary building. The opened access

door to the air handling unit compromised the control room pressure . .

boundary. The licensee estimated that the faulted air handling unit had

been in the system alignment for approximately five minutes.

Later that day, the licensee determined that both trains of the VC

system were inoperable with the breach in pressure boundary. As a

result, both units had entered TS 3.0.3 for approximately five minutes.

At approximately 4:30 p.m. the licensee determined that the occurrence

was reportable and submitted a 10 CFR 50.72 one-hour notification to the-

NRC. The NRC and licensee discussed the cimeliness of issuing the 50.72

report. No violations were identified. However, the licensee stated

that a compensatory action existed for maintaining the VC system

operable during maintenance activities that compromise the control room

pressure boundary. The compensatory action allows the VC system to

remain operable provided the pressure boundary can be restored within

five minutes of a safety injection signal. a radiation release within

.the plant, a high chlorine alarm at a VC intake, or the sensing of

chlorine in the work area. The inspectors requested information

pertaining to the basis for the 5-minute window during which VC

. operability was not assumed for accident mitigation, a chlorine leak, or

offsite dose calculations. Pending the receipt and further inspector

review of this information, this issue is characterized as Unresolved

Item 50-413,414/98-01-01: Basis for Five-Minute Period of VC System-

Inoperability with Compensatory Actions. This inspector review will

include a review of the adequacy of the licensee's post-maintenance

testing of the access door.

c. Conclusions

Control room operators appropriately identified and corrected a fault in

the control room ventilation system. An Unresolved Item was opened

pending NRC review of the basis for assuming that the control room

ventilation system is allowed to be inoperable for five minutes

following a safety injection, radiation release within the plant, or a

chlorine leak.

01;3 Doerations Clearances - General Comments (71707)

The inspectors reviewed the following clearances during the inspection

period:

  • Tagout 17-643 Unit 1 CA Pumps Suction from CA CST

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- Tagout 27-1139. Unit 2 CA Pumps Suction from CA CST

The inspectors observed that the clearances were properly prepared and

authorized and that the tagged components were in the required positions

with the appropriate tags in place. The inspectors were concerned with

the length of time these clearances had been in place to maintain the

auxiliary feedwater system operable. -The clearances were first' alaced

on May 15, 1997, and had been in place ever since. Aspects of tais

concern are discussed further in Section E8.1 of this report.

04 Operator Knowledge and Performance

04.1 Containment Chill Water Pumo Trio

a. Insoection Scone (71707)

The inspectors reviewed PIP 2-C98-0447 and the circumstances surrounding

the trips of the operating Unit 2 containment chilled water pumps on

February 3. 1998. The inspectors reviewed the PIP and Procedure

OP/2/A/6450/020. Containment Chilled Water System. Revision 32. The

inspectors also interviewed the operator involved and discussed with

licensee management their review of this issue.

b. Observations and Findinas

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On February 3. 1998. an operator attempted to place in service

containment chilled water pump number 3 which resulted in the operating

pumps being automatically tripped due to low flow. During performance

of OP/2/A/6450/020. Enclosure 4.5. Swapping Operating Chiller Units, the

operator inadvertently performed Section 2.1 One Chiller Operation,

rather than Section 2.2. Swapping a Chiller with Two Chillers in

Operation. Although chiller system temperature increased from 42

degrees Fahrenheit to the high alarm setpoint of 60 degrees, containment

temperature was not effected by this error and two chillers were

subsequently placed in service without incident.

Based on discussions with the operator. the inspectors determined that

performance of the improper section of the arocedure occurred due to

personnel error. The operator stated that le concentrated on steps

necessary to support placing the number 3 chiller pum) in service and

did not recognize that he was in the wrong section. ) lacing a third

pump in service required securing one of the operating chiller units and

the subsequent opening of a hot gas bypass valve that was recently

installed as part of a modification. The o)erator stated that

maintenance personnel normally mani Julate t1e valve: however, on this

day he was requested to place the cailler Jump in service and manipulate

the valve. Due.to being unfamiliar with tie valve, the operator failed

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to recognize what section of the procedure he initiated and, as a

result, the chiller pumps tripped.

The inspectors determined that the failure of the operator to perform

the proper section of Procedure OP/2A/6450/020 was primarily due to

personnel error. The inspectors also noted that the format of the

procedure contributed to the event. The procedure's structure lent to

the error by having multiple sections together in one enclosure rather

than in separate attachments. This aspect was discussed with plant

management who indicated that, in light of this and other recent

procedure adherence and format problems, a further review would be

considered. The failure to follow procedure on behalf of the operator

in this case was of minor safety consequence since plant equipment was

not rendered inoperable nor was the long term operation affected.

However, this incident was one of four examples of operators failing to

follow procedures noted throughout this report and is characterized as

Violation 50-413.414/98-01-02: Failure to Follow Plant Operating and

Administrative Procedures.

c. Conclusion 1

One example of a violation was identified for failing to follow the

appropriate section of a procedure for placing a containment chilled

water pump in service.

07 Quality Assurance in Operations

07.1 Plant Ooerations Review Committee (PORC) Meetina

a. Insoection Scoce (40500)

The inspectors attended a PORC meeting on February 19, 1998, which was

convened to discuss plans to reduce reactor Jower on Unit 1 the next day

to swa) the reactor vessel flange 0-ring leat detection valve lineup

from 11e inner to the outer 0-ring. The inspectors attended this

meeting to verify that the required representatives and quorum were

present, and that safety aspects associated with the planned swapover

evolution were covered adequately.

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b. Observations and Findinos

Since the beginning of the current fuel operating cycle for Unit 1 in

January 1998, operators in the control room had been receiving

intermittent indications of a reactor vessel flange inner 0-ring leak.

Approximately once every two or three days, the reactor vessel flange 0-

ring leak detection high temperature alarm would enunciate when the

tell-tale leak-off line temperature spiked to approximately 250 degrees

Fahrenheit, then decayed quickly to normal temperatures. The ar,ount of

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. leakage caused slight increases in reactor coolant. drain tank levels,

none of which, however, indicated leakage greater than Technical

Specification limits. As a result of the inner 0-ring leak, plant

management decided to isolate the inner 0-ring leak detection path and

. swap to the outer 0-ring.

Because the outer.0-ring differed from the inner 0-ring in that it was

not provided with the same notched groove in the reactor vessel which

would channel 0-ring leakage directly to the tell-tale piaing, a 10 CFR

50.59 safety evaluation was performed to evaluate the pro) ability and

consequences of a potential outer 0-ring leak not being detected. The

engineering staff determined that an unreviewed safety question did not

exist based primarily on the _ belief that some of the potential leakage

would end up in the tell-tale piping and cause a control room alarm.

After discussions of various design aspects of the reactor vessel flange

to support this belief, and logistical details of the swapover evolution

. including communications between the control room operators and those in

containment, and diverse methods to be used to detect any 0-ring

leakage. the PORC ap3 roved the safety evaluation and the plan to swap to

the outer 0-ring leac detection path.

The inspectors observed that the PORC exhibited good questioning

attitude concerning the various aspects of this issue.

-c. Conclusions

The PORC meeting which was convened to discuss plans to swap the Unit 1

reactor vessel flange 0-ring leak detection from the inner 0-ring to the

outer one was conducted in accordence with commitments contained in the

UFSAR Chapter 16. Selected License Commitments. with adequate

representation and a quorum present. The committee exhibited good

questioning attitude regarding issues associated with the leak detection

capability while aligned to the outer 0-ring.

08 Miscellaneous Operations Issues (92700. 92901)

08.1 (Closed) Licensee Event Reoort (LER) 50-414/96-07: Cold Leg Accumulator

Discharge.

This LER documented an inadvertent discharge of the Unit 2 cold leg

accumulators (part of the emergency core cooling system) into the RCS

cold legs. The discharge occurred on December 16. 1996, during a

shutdown to Mode 5 when RCS pressure decreased to the accumulator

discharge setpoint of.600 pounds per square inch gauge (psig). The

accumulator discharge isolation valves had been o)ened following RCS

pressure boundary check valve testing, although t1ey should have been

closed in accordance with Step 2.31 of OP/2/A/6100/02. Controlling

Procedure for Unit Shutdown, approved November 25, 1996 (see NRC

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Inspection Report 50-413.414/96-20 for additional information).

Operator activities associated with this event were contrary to the

requirements of TS 6.8.1.a. and Regulatory Guide 1.33. Appendix A: and

constituted a second example of failure to follow procedure,

characterized as Violation 50-413.414/98-01-02: Failure to Follow Plant

Operating and Administrative Procedures.

This LER is closed and the licensee's corrective actions will be tracked'

with the response to the Notice of Violation.

08.2 (Closed) URI 50-413.414/97-15-01: Failure to Follow Procedures Resulting

in Inadvertent Injections of ECCS Fluid into the Reactor Coolant System

(RCS).

On December 29, 1997. an inadvertent Unit 1 safety injection pump

discharge into the RCS occurred during cold leg accumulator filling.

The licensee attributed the event to failure to follow the cold leg

accumulator operating procedure. Unresolved item 50-413.414/97-15-01

was opened pending further NRC review of the human performance issues

associated with the event. The evolution was governed by Procedure

OP/1/A/6200/009, Cold Leg Accumulator Operation, Revision 61. Step

2.3.3 which directed the operator to close valve 1NI-118A, safety

injection Jump 1A cold leg injection isolation valve-, was inadvertently

missed. T1is was contrary to requirements contained in TS 6.8.1.a and

Regulatory Guide 1.33. Appendix A. and constituted a third example of

failure to follow 3rocedure, characterized as Violation 50-413.414/98-

01-02: Failure to rollow Plant Operating and Administrative Procedures.

08.3 (Closed) URI 50-413/97-15-02: Appropriateness of Operator Actions

During Control Rod Testing.

This item involved concerns associated with operator response to a Unit

1 manual reactor trip following a loss of rod position indication during

rod manipulations on December 29, 1997. While manually tripping the

reactor, which was already shut down to Mode 4. control room operators

held in the Main Feedwater (MF) Isolation reset pushbuttons on the main

control board to prevent an unnecessary secondary plant transient.

Following the reactor trip. Abnormal Operating Procedure AP/1/A/5500/05.

' Reactor Trip or Inadvertent Safety Injection Below P-10. Revision 16.

Step 29.a. directed control room operators to manually initiate

feedwater isolation. Again, operators decided to avoid a secondary

plant transient and skipped Step 29.a. The inspectors questioned the

rocedure

ap)ropriateness

-(A)). Operations of deviating Procedure

Management from the abnormal [ operating] p/ Abnormal

(0MP) 1-7. Emergency

Procedure Implementation Guidelines. Revision 13. provided guidance for

deviating from Emergency Procedures. However, deviation from APs was

not addressed. A separate procedure. OMP 1-4. Use of Procedures.

Revision 59. Section 8.1.N stated "Unless specified by a procedure, an

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automatic signal shall Dat be defeated from performing its intended

function." According to OMP 1-4. Section 8.4.E. if there is reason to

believe that a procedure step does Dat have to be performed and is not

applicable (N/A), then several criteria must be met: (1) two operators.

one of whom is a supervisor who holds a senior reactor operator (SRO)

license, shall approve the decision to deviate from the procedure: (2)

the performer of the step shall initial'the step marked N/A: and (3) the

initials of the approving SR0 shall be documented on the working copy of

the )rocedure beside the applicable step along with a brief description

of tie reason for the deviation. Step 9.6 of OMP 1-4 also states that,

whenever an AP is used, a Procedure Evaluation Form shall be completed

and forwarded along with the completed procedure to the 0)erations

Support Manager. The form is intended to provide feedbacc to ensure

that APs are kept current and usable.

The inspectors reviewed the procedure that was in use the night of the

manual trip and post-trip response. Step 29.a had not been marked N/A:

nor had the initials of the procedure performer or an approving SRO.

along with a descri] tion of the reason for the deviation. been provided

on the procedure.- r eedback provided in the Procedure Evaluation Form

was "None - or No Comments. The person who filled out the form began

to provide additional information but struck it out. No reference to

the appropriateness of MF isolation could be gleaned.

The inspectors did not identify plant safety concerns associated with

the decision to bypass MF isolation during and after the manual reactor trip from Mode 4. However, defeating the MF isolation function and

failing to document the decision to deviate from the AP indicating the

persons accountable and their justifr.ation in accordance with the OMP.

exhibited in this case an informal regard for the AP as well as the

administrative requirements governing deviation from it. This failure

to comply with OMP 1-4 constituted a fourth example of Violation 50-413.

414/98-01-02: Failure to Follow Plant Operating and Administrative

Procedures.

II. Maintenance

M1 Conduct of Maintenance

M1.1 Comoonent Coolina Water (KC) 2B Heat Exchance (HX) Tube Cleanina

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(Unit 2)

a. Insoection Stone (62700/62707/55050)

The inspectors determined by work observation and document review. the

adequacy of maintenance activities relative to cleaning the 2B KC HX

tubing and replacement of vent and drain lines associated with this

heat exchanger. Cleaning of tubes was performed under Work Order 97111777-01. Replacement of vent and drain lines was done under Work

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Orders 97013977-01 and 97013976-01. The two-inch line on isometric

Drawing 2RN-424. was safety-related QA Condition 1. Duke Class C and the

3/4-inch diameter line was noncode, nonsafety. Duke Class G

classification. The controlling procedure for cleaning was

MP/0/A/7650/056 C. Heat Exchanger Corrective Maintenance. Revision 5.

b. Observations and Findinas

Cleanina of 2B KC HX Tubina - At the time of this inspection, cleaning

of the 2B KC HX tubes was in )rogress. The inspectors noted that the

tubes were cleaned by using tie propelled brush method during which

individual cleaner brushes are inserted in the tube-ends and shot

through the tubes with a specially designed lance-gun, under sufficient

water pressure to achieve the desired cleaning. The inspectors verified

that technicians were adhering to procedural requirements including

installation of individual brushes in each tube; establishment of good

communication on the inlet and outlet ends of the HX: a clean full tube

stream of water followed the brush and the muddy water: sufficient light

was provided at both ends of the HX to assure good visibility: and

procedure sign-offs were in line with job completion. Through

discussions with the cognizant component engineer, the inspectors

ascertained that in 1995, the 2B KC HX was re-tubed with stainless steel

Type 316 tubing as a protective measure against copper contamination in

the system. However, the licensee indicated that out of a maximum of

800 tubes that could be plugged. 318 of the original tubes were plugged

and left in the HX.

For the most Jart, these tubes were located in the periphery of the HX's

tubesheet. T1ese tubes were made from brass material and were allowed  ;

to remain in the HX because of the difficulty in removing and replacing i

them from that location of the tubesheet. l

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Reolacement of 28 KC HX Vent and Drain Lines - The vent and drain lines

in the 2B KC HX were replaced due to pipe wall degradation from general

corrosion. The replacement pipe sections were made of seamless carbon l

steel pipe, two-inch and 3/4-inch diameter schedule 40 Type 106 Grade l

B. material. This material was the same as the piping replaced. The 1

inspectors observed welding in progress on the 3/4-inch line: observed

completed welds: and reviewed quality records for the filler metal,

replacement piping, welder qualifications and in-process control

documentation. Weld appearance was satisfactory and the documents and

records were complete and accurate.

c. Conclusions

Cleaning of the 2B KC HX was well planned managed and executed with l

sufficient oversight by the cognizant engineer who displayed a good l

working knowledge of the components and took an active role in the '

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activity. Technical personnel. including welders, were adequately

trained to perform their assigned tasks. Procedures were followed.

tests were performed and records were complete and accurate.

M1.2 Reolacement of Certain Isolation Valves on the Nuclear Service Water  ;

(RN) System. Associated with the Control Room Air Chillers (Unit 1) l

a. Insoection Scone (62700/62707/55050)

The inspectors determined by work observation and document review the

adequacy of work activities with regards to the replacement of certain

manually operated isolation valves associated with the control room air

chillers. The governing codes for this activity were the American

Society of Mechanical Engineers (ASME) Sections III and XI. Editions

1974 and 1989 respectively. The replacement was being handled as minor

modification CE-8790 which was executed using work orders 97042493. -94.

-95. -96. -97, and -99. l

b. Observation and Findinas

At the time of this inspection, sections of the RN piping were

undergoing modification to facilitate installation of the replacement

valves. Through discussions with the cognizant engineer and a review

of controlling documents, the inspectors ascertained the following

information: five manually operated butterfly isolation valves;

identified by tags 1RN-238. -243. -247. -298, and -303: were being

removed from service due to material deterioration which precluded them

from performing their intended functions. The replacement valves were

similar in size except that they were manufactured from stainless steel ,

material which provided improved performance in their applications. The i

inspectors' review of the licensee's valve replacement evaluation,

verified that the stress calculation CNC-1206.02-84-2010. Revision 14

for these valves was acceptable, and that the 10 CFR 50.59 safety

evaluation was satisfactory. Also, because the replacement was regarded

as a routine valve maintenance and re)lacement activity, it did not

require inclusion in the Catawba UFSA1. Through this document review,

the inspectors ascertained that existing piping would have to be cut ,

back slightly and rewelded to accommodate a three-inch difference in i

valve take-out dimensions.

Welding was being controlled by requirements of the applicable code and

the licensee's Procedure SM/0/A/8100/001. Revision 1. Welding of 0A

Piping and Valves. The piping system was rated as ASME Class "C."

Replacement piping was made from eight-inch diameter pipe Schedule 40.

carbon. steel material Type SA-105. Grade B. The inspectors reviewed

-material certification reports, personnel qualification records, weld

process control records, and observed welding of certain welds during

. fabrication and others which had been completed. Through this work

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11

effort, the inspectors verified that on February 4.1998, a. welding QC-

inspector had quizzed certain welders who were working on this job to

determine their knowledge of welding process control practices at

Catawba. Based on his questions, the welding OC inspector determined

that the welders' responses indicated that their knowledge of weld

process control practice.s was not fully adequate and stopped work on the

job. The licensee's immediate corrective action was to conduct training

to assure that supervisors and welding personnel had a good

understanding of the process control program before returning to the

job.

The licensee documented this finding with PIP 0-C98-0479 and initiated a

root cause investigation to address the long-term questions and

corrective measures to address this problem. Through discussions with

technical personnel, the inspectors determined that the probable cause

of this problem was a lack of adequate screening of incoming welders and

appropriate pre-job training to ensure that welders had a good working

knowledge of the licensee's weld process control program. The welders

involved in this problem were from the licensee's Electrical System

Support (ESS) organization, and had been brought in to weld on this

modification. The welders were qualified to applicable code

requirements and the quality of welds they had fabricated was not in

question. An example of inadequate screening and training of welders

brought in to weld on safety-related main feedwater piping had been

previously identified as a weakness in NRC Inspection Report 50-

413.414/97-15. The problem identified by the liceasee during the

present inspection was another example of inadecuate site screening and

training of welders before allowing them to welc on safety-related QA

Condition 1 components. In response to these problems, the licensee

took certain corrective measures'that will provide for screening and

pre-job training of welders before assigning them to the jobs where

superior skills and knowledge of the program were required.

c. Conclusions

Replacement of certain isolation valves on the RN system used on the

control room air chillers was consistent with applicable code.

requirements for materia, and processes. Engineering's overview was

adequate. We'ders assigned on the job lacked adequate knowledge in the

licensee's welding process control program which resulted in a work

stoppage. The licensee's inability to establish a strong working

program to address these type of welding problems. was regarded as a

weakness.

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~ 12

M2 .Haintenance and Haterial Condition of Facilities and Equipment.

M2.1 Seal Water Valve Iniection Inservice Testina

a. Insoection Scone (61726)

On; January 28, 1998. troubleshooting activities were performed.to

determine the cause of indication problems associated with 2NW-190A.

Seal Water Supply Isolation Valve to 2NI-121A. which is the A-train

Safety Injection Pump Discharge to RCS Loops B and C Hot Legs Isolation

Valve. The licensee determined that 2NW-190A was unable to open due to

a large differential pressure across the valve. The inspectors

discussed the valve's safety function with engineering and operations

personnel.

b. Observations and Findinas-

~The containment valve injection water (NW) system prevents leakage of

containment atmosphere past certain gate valves used for containment

isolation following a loss of coolant accident. This is accomplished by

injecting seal water at a pressure (150 asig) that exceeds the peak

containment accident 3ressure (15 psig) Jetween the two seating surfaces

of the flex-wedge dis (s. In October 1997, the licensee encountered a '

position indication problem associated with 2NW-190A. Specifically.

with the valve in the closed position and receiving an open demand

signal. an open indication light would come on, but the closed

indication light would not go out. The licensee suspected that the

problem was limited to indication only.

On January-28, 1998, the licensee was aerforming troubleshooting

activities to determine the cause of tie indication problem. During

troubleshooting, technicians encountered difficulty in opening the

valve. The valve was removed from the system and bench tested. The

valve stroked on the test bench with no difficulty and no signs of

foreign material were identified. The valve was reinstalled in the

system the~ evening of the January 29, 1998, and the next day, failed an

inservice valve stroke test. The maintenance technicians determined

that the valve was not opening. The cause was attributed to reactor

coolant system leakage past two safety injection check valves and two

containment valve water injection system check valves. The licensee

hypothesized that the associated back pressure had caused the valve to

become unable to open due to a large differential pressure across the

. valve. To verify this hypothesis the licensee vented the piping and

attempted to open the valve. The valve opened without difficulty. and

an inservice valve stroke test was successfully performed several hours

later.

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The inspectors questioned the valve's ability to perform its safety

function. which was to provide containment valve injection water to 2NI-

121A (a containment isolation valve) on a containment isolation signal.

Valve 2NI-121A is normally closed. The valve is opened for hot leg

recirculation following the injection and cold leg recirculation phases

of ECCS operation. The licensee responded that the valve would not be

required to perform a containment isolation function until the

associated section of piping had depressurized (some time after accident

initiation). The inspectors asked if the containment isolation signal

to 2NW-190A that is generated early in the accident would still be

present at the point when the valve would no longer be pressure-bound.

The licensee provided electrical diagrams demonstrating that a seal-in

circuit' ensured that a containment isolation signal would be maintained

to 2NW-190A (and other_ valves in the system) as long as the valve

injection water signal is not reset. The inspectors independently

verified that the seal-in circuit existed and that it was being tested

in accordance with monthly and quarterly slave relay testing

requirements. The' inspectors' review concluded that the valve injection

water signal could not be reset without resetting the Containment Phase

A signal first.

The licensee indicated that PT/2/A/4200/027, NW Valve Inservice Test.

Revision 28 would be revised to provide a step to vent 2NW-190A before

performing future in-service tests. The licensee r,tated that venting

does not establish " ideal conditions" for the test, but establishes the

design conditions to demonstrate its design function (to open at less

than 150 psig differential pressure). The licensee has addressed the

long-term resolution of NI and NW system check-valve leakage in station

PIP 2-C98-0391. The inspectors questioned whether or not the valve

would meet Technical Specification surveillance requirements. Pending

further NRC review, this is characterized as Unresolved Item 50-414/98-

01-07: Operability of Valve 2NW-190A.

c. Conclusions

An Unresolved Item was open pending further NRC review of a Technical

Specifications compliance issue associated with containment valve

injection water system valve 2NW-190A.

M2.2 Scaffoldina Proaram And Handlina Of Scaffoldina Material

a. Insoection Scone (62707)

The inspectors reviewed the licensee's scaffolding program and the

methods of handling scaffolding material. This included the-

review of station procedures for the erection and removal of

scaffolding and for the removal of items from radiation controlled

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14

areas. Discussions were conducted with health physics and

scaffolding crew personnel.

b .' Observations and Findinas

Discussions with the scaffolding supervisor indicated that three

scaffolding systems were used at Catawba; the wedge lock system,

the tube and coupler system, and the welded frame system. The

system normally selected for use to su] port maintenance activities

was the system that could be erected t1e fastest and could conform

to the physical limitations of the local area. Regardless which

scaffolding system'was chosen, com)leted scaffolding, ready for

use, was erected in accordance wit 1 the station's Power Group-

Scaffold Manual and MP/0/A/7650/115. Revision-004. Erection And

Removal Of Scaffolding. Inspectors verified the Power Group

Scaffold Manual was in compliance with OSHA standard 29 CFR Part

1926. Safety Standards for Scaffolds Used in the Construction

Industry: Final Rule, effective date November 29, 1996. The

licensee also indicated that all scaffolding was erected by

cualified builders who receive 80 hours9.259259e-4 days <br />0.0222 hours <br />1.322751e-4 weeks <br />3.044e-5 months <br /> of instructional training

curing the qualification process. The inspector did not observe

scaffolding being constructed or the cutting and prefabrication of

scaffolding material due to the limited amount of scaffolding work

being performed during the time of the inspection. Controlled

areas set up specifically for cutting and preparing scaffolding

material were also not available for inspection. However, the '

inspector noted from a review of licensee procedures that the

unconditional release of material from a radiologically controlled

area including material associated with scaffolding. included

surveys for potential contamination.

Scaffolding material is stored in the auxiliary building in one of

seven scaffolding storage boxes located on different elevations

and behind the auxiliary building in three large cargo-type i

storage boxes. According to the licensee, the storage boxes j

located in the auxiliary building are primarily used to store a

material for scaffolding jobs in the auxiliary building and the

large cargo-type storage boxes hold scaffolding material used

mostly in containment during refueling outages. The storage boxes

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contained various material and building hardware required for the

erection of scaffolding. Some of the material was wrapped but the

bulk of the material was unwrapped. Materials being transported '

.from one controlled area to another are required by station

. procedures to be wrapped. The inspector did not observe the .

transporting of scaffolding material but did observe scaffolding-

material that was being wrapped and stacked for transport as the

material was being taken out of a potentially contaminated area in

the radiation controlled area. The material was easily accessible

u . .. .. .. .. .. .. .. . .. .

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for ins)ection. The inspectors noted that all storage containers

were la)eled identifying the radiation levels and contamination

levels present. Random smear surveys were taken from different

materials from all storage boxes to verify that the stored

material were within the limits as specified on the storage

container and the method of storage was appropriate based on the

actual contamination levels. All smear surveys were counted and

.found to be less that 1000 dpm/100cm2. The inspectors noted

however that smear survey results from external surfaces of stored

material in two of the three large cargo type storage boxes

exceeded the contamination levels stated on the container label.

This discrepancy was considered to be of minor significance since

all survey results were less 1000 dam /100cm2, the level of loose

contamination which would require tie storage containers to be

posted as contaminated per 10 CFR Part 20.

c. Conclusions

The inspectors concluded that the scaffolding program was in

compliance with the requirements of 29 CFR Part 1926. Safety

Standards for Scaffolds Used in the Construction: Final Rule.

With the exception of the minor discrepancy identified between

actual internal contamination levels and the amount posted,

radiological handling and storage of scaffolding material was

adequate.

M2.3 Main Feedwater Reaulatino Valve 1CF-37 Problems

a. Insoection Scoce (62707)

The inspectors reviewed circumstances surrounding the forced Unit 1

shutdown associated with the erratic performance of main feedwater

regulating valve ICF-37. which controls feedwater flow to the B steam

generator,

b. Observations and Findinas

On January 16, 1998, control room operators experienced problems

controlling B steam generator (SG) level when valve ICF-37 responded

erratically to control input signals. The operators swapped from

automatic to manual valve control and were better able to maintain the

SG level within the normal operating band. Later, power was reduced to

approximately 20 percent ~ to allow the valve to~ be isolated for

' troubleshooting. Initially, the valve's packing was adjusted and

testing was performed demonstrating freedom of movement and that the

valve's pneumatic control system was functioning properly. After the

valve was returned to service and reactor power was increased on January

17, 1998, operators again experienced the same symptoms as before with

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16

erratic SG level control. Plant management elected to shut down the

plant to allow full draining and isolation of the piping associated with

ICF-37 for troubleshooting. Technicians discovered a galled aluminum

s)acer in the valve packing cavity which was im) acting stem movement.

T1e spacer had been replaced during the recent Jnit I refueling outage

following planned valve maintenance. Plant personnel determined that

the installation of the aluminum spacer (placed in the packing cavity.

below 5 graphite and rope packing rings) was unapproved for this. valve.

The controlling. Maintenance Procedure. MP/0/A/7600/83. Main Feedwater

Regulating Control Valves Corrective Maintenance.. Revision 4. specified

in step 11.1.10 to install a carbon spacer (if removed) in the packing

cavity. Licensee personnel generated PIP 1-C98-0218 to document the

problems with this valve. The aluminum spacer was replaced with a new

carbon one and the system and plant were successfully returned to

operation.

The inspectors reviewed Procedure MP/0/A/7600/83 and confirmed that it

specified using a carbon spacer instead of an aluminum one. The

inspectors discussed this issue with maintenance personnel and

management who indicated that on December 9.1997, during the refueling

outage, technicians working on the valve discovered that its original

carbon packing spacer was damaged and needed replacement. There was no

carbon spacer available and the technicians discussed with a maintenance

technical assistant the possibility of using an aluminum spacer instead

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of a carbon one. The decision was made to use the aluminum one. The

technician failed to bring the procedure with him during these

discussions which might have prompted the technical assistant to further

scrutinize the use of an aluminum spacer. The technician later failed

to annotate the spacer material deviation in the procedure.

The safety consequences of this error were minimized by the fact that

the feedwater regulating valve performs a backup isolation function to

the main feedwater motor-operated isolation valves located in the steam

doghouses. Additionally. )lant engineers performed an operability

evaluation (documented in )IP 1-C98-0218) demonstrating that valve ICF-

37 would have been able to perform its isolation function even with the

increased frictional forces caused by the galled packing spacer.

Licensee management appropriately addressed the human performance issues

associated with the aluminum spacer installation. The inspectors

considered the licensee's investigation and corrective actions to be

appropriate and thorough. The failure to properly follow MP/0/A/7600/83

on December 9. 1997 was contrary to the requirements of TS 6.8.1.a and

Regulatory Guide 1.33. Revision 2. This non-repetitive, licensee-

identified and corrected violation is being treated as a Non-Cited

Violation, consistent with Section VII.B.1 of the NRC Enforcement

Policy: and is identified as NCV 50-413/98-01-03. Failure to Install

Correct Packing Spacer in Feedwater Regulating Valve ICF-37.

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c. Conclusions

~

One Non-Cited Violation was identified for the-failure to follow

maintenance procedures which.resulted in an unapproved aluminum packing

spacer being installed in the Unit 1 B steam generator main feedwater

regulating valve.

III. Enaineerina

E3 Engineering Procedures and Documentation

E3.1 Calculation of Accentable Emeraency Core Coolina System (ECCS)

Leakaae Outside Containment

a. Insoection Scone (37551)

The inspectors reviewed the established program for monitoring

ECCS leakage outside containment and the methodology used for

determining acceptable leakage limits. This review included

discussions with operations and engineering personnel, and review

of plant procedures and aaplicable portions of the Updated Final

Safety Analysis Report (U SAR).

b. Observations and Findinas

On January 21, 1998. following an inservice surveillance test of

the 1A centrifugal charging pump. an inboard seal leak was

observed while the pump was in standby. The leakage was measured

by the licensee at approximately 350 milliliters per minute

(ml/ min). On January 23. 1998, a surveillance test was performed

on the 2A centrifugal charging pump. When this pump was secured.

an outboard seal leak was observed and later measured to be

greater than 400 ml/ min. Inspectors questioned when the pumas

were to be declared inoperable based on their respective leacage

contribution to the total ECCS leakage outside containment for

each individual unit. Discussions with engineering personnel

indicated that this amount of leakage did not render either

centrifugal charging pump inoperable. It was noted. however, that

no current dose analysis calculation had been performed to

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substantiate this operability determination.

ECCS leakage outside containment is monitored during normal

o)erations on each unit to ensure total leakage would not

clallenge the post-accident dose rates as specified in 10 CFR 100.

when in cold leg or hot leg recirculation alignment following a

large break loss of coolant accident. PT/1/A/4150/002. Revision

026. Visual-Inspection Of Radioactive Systems Outside Containment,

performed on a weekly basis, is the procedure used to monitor all

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ECCS systems, components, and related piping that could come in

contact with reactor coolant from the containment recirculation

sump. This procedure was reviewed by the inspectors and it was

verified that the seal leakage from the 1A and 2A centrifugal

charging pump was being monitored.

Upon further investigation and rev'N of Catawba's UFSAR, Section

15,6. Decrease in Reactor Coolant Inventory, the inspectors

identified various conservative assumptions that were outlined in

the Standard Review Plan 15.6.5. Appendix B, and required to be

included in the analysis of the offsite dose effects attributable

to Engineered Safety Features (ESF) leakage. Discussions with

engineering

methodology, personnel

and concerning

whether all current dose

required conservative analysis

assumptions

were included in current dose analysis calculations, revealed that

Catawba's dose analysis calculations were in the process of being

modified. Current dose analysis calculations were not consistent

in the assumptions used, and those as specified in the UFSAR.

Specifically, the UFSAR states that no credit was to be taken for

auxiliary building ventilation system for iodine removal. As

documented in existing PIP 0-C95-1938, current dose analysis

assumptions take credit for this factor. Proposed resolution of

this inconsistency was given an internal due date of May 31, 1998,

by the licensee.

Based on the inconsistency in the dose analysis assumption used

and the ongoing revision in the dose analysis calculation, the

inspectors could not verify the accuracy of the licensee's dose

analysis calculation and methodology used. The inspectors

therefore determined further review was warranted. This review

will be tracked under Inspector Followup Item (IFI) 50-413.414/98-

04: Assess the Licensee's Dose Analysis Calculation For ECCS

Leakage Outside Containment.

c. Conclusions

An Inspector Followup Item was identified to assess the licensee's

dose analysis calculation for ECCS leakage outside containment.

E7 Quality Assurance in Engineering Activities

E7.1 Environmental Qualification of Refuelina Water Storace Tank Level

Transmitters

a. Insoection Scoce (37551)

On January 27, 1998, the licensee discovered that the Refueling Water

Storage Tank (RWST) level transmitters were not qualified for a

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19

postulated submerged environment. The inspectors discussed the issue

with plant personnel and NRC subject matter experts: inspected a sample

of RWST level transmitter boxes: reviewed station PIPS 0-C97-0190 and 0-

C98-361: reviewed design basis documentation: and reviewed construction

records'and cable conduit dam installation procedures.

b. Observations and Findinas

During a recent review of a possible modification to eliminate sources

of RWST level instrument inaccuracy, plant engineers determined that the

RWST level transmitters were not qualified for a submerged environment.

The licensee assumed that these transmitters (which are located between

.the outer tank wall and a missile shield which surrounds the tank) will

be submerged under water during a specific design basis event. The

accident scenario involves a tornado-generated missile that is assumed

to puncture the tank. The RWST inventory would issue from the resulting-

hole, and the surrounding enclosure would then flood. The transmitters,

which are located just above ground level outside the tank and inside

the missile shield, would be submerged under approximately 12 feet of

water. The tornado also is assumed to damage one main steam line. The

main steam line break would cause a safety injection on low pressurizer

pressure.

Since the RWST level transmitters were assumed to be submerged during

this tornado event, and the transmitters were not qualified for a

submerged environment, the licensee identified a concern that instrument

failure might give a false low RWST level indication. The auto-swapover

level setpoint is 37 percent, and emergency procedures direct control

room o

pumps)perators to secure

when the RWST all operating

level indicates ECCS

less than pumps (including

5 percent. The concerncharging

was that an instrument failure would occur prior to safety injection

system termination, thereby resulting in either a premature swap to the

containment sump or loss of reactor coolant pump seal injection.

To address the concern, the licensee devised a plan to verify that cable

penetrations into the transmitter boxes, which also were not qualified

for a submerged environment, were sealed. The licensee reasoned that if

the seal dams (which had been installed during construction) were

present, then they would provide a suitable barrier to water inleakage.

An acceptance criterion for a maximum hole diameter was calculated, and

on January 29, 1998, the licensee inspected the RWST instrument boxes to

identify visible holes: to ensure the gasket sealing around the box

doors was intact: and to verify that the dams were present. The

inspection results were that all enclosures and transmitters were in

sound condition with no apparent leaks or holes. Based upon the

inspection, the licensee concluded that all Unit 1 and Unit 2 RWST level

transmitters were operable (eight transmitters in total).

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The inspectors conducted an independent inspection of the transmitter

boxes'on January. 30 and identified water droplets and moisture around a

cable 3enetration in one of the Unit 2 boxes (2TB0X0010). Noting that

there lad been no precipitation for two days, the inspectors asked why

the moisture had not been identified during the licensee's inspection

the previous day. On February 2. Engineering personnel verified that

moisture was present in 2TB0X0010: on February 3. the associated level

channel 3 was declared inoperable, appropriate TS action was taken, and

PIP 2-C98-0434 was generated to document the inspectors' observation.

The inspectors determined that the licensee failed to identify the

degraded condition during initial inspections, and the licensee

initiated a root cause evaluation to address the adequacy of their

initial-inspections. The licensee refurbished 2TBOX0010 and declared it

operable on February 7.

Within their corrective action program, the licensee is considering

several alternatives to address the design deficiency for long-term

resolution.

c. Conclusions

The licensee's identification of the design deficiency was commendable.

Their initial inspection of the RWST level transmitter boxes failed to

reveal moisture in one of the boxes. The licensee's corrective efforts

to assess the adequacy of their initial inspections were appropriate.

E8 Miscellaneous Engineering Issues

E8.1 (Ocen) LER 50-413.414/97-003-00: Auxiliary Feedwater System Found

Outside Design Basis.

(Ocen) URI 50-413.414/97-300-02: Catawba UFSAR Discrepancies

a. Insoection Scooe (37551. 92700. 92903)

The inspectors reviewed the licensee's activities to address the

potential design discreaancy associated with air entrainment caused by

aligning the Auxiliary reedwater Condensate Storage Tank (CACST) to.the

suction of the auxiliary feedwater (AFW) pumps in Units 1 and 2. The

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licensee had identified in LER 50-413/97-003 that the normal system

alignment could potentially place each unit outside of its design basis,

and that further engineering analysis from an outside contractor would

be performed to confirm or refute the degraded condition. This issue

was also raised as part of Unresolved Item 50-413.414/97-300-02.

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b. Observations and Findinas

On May 15. 1997, the licensee identified a potential design deficiency

associated with the normal configuration of aligning each AFW pump to

the CACST (shared by both units) to provide condensate quality water at

sufficient head to operate the pumps. The CACST was one of three

nonsafety-related, condensate water sources tied to a common header

feeding the aumps. The other two sources included each unit's upper

surge tank (JST) and each unit's main condenser hotwell. All of these

sources were normally aligned but capable of being isolated from the

common header by motor-operated isolation valves: check valves were

provided to prevent volume exchange between the three condensate quality

water sources. Because of its elevation and the amount of suction head

provided, the CACST would initially provide pump suction until its level

decreased to a predetermined value at which time the UST would begin to

supply the AFW pumps.

The licensee determined that because of the nonsafety-grade tanks'

piping configurations, air could be introduced into the suction of all

three of the AFW pumps during the transition from the CACST to the UST

with a failure of the nonsafety-related 1(2)CA-6 to close on low level.

This could potentially disable the pumps during a loss of offsite power

(LOOP) event coincident with a steam line or feedwater line break prior

to the transfer of AFW pump suction to its safety-related assured

source, the non-condensate quality nuclear service water system. The

licensee performed an initial operability determination given the above

identified condition and determined that further engineering analysis

would be required from a vendor. In the interim, the licensee closed

the suction valves from the CACST (Valves ICA-6 and 2CA-6) to eliminate

the potential for air entrainment.

The inspectors learned that the valves were closed using the clearance

]rocess; specifically. Tagout 17-643 for Unit 1 and Tagout 27-1139 for

Jnit 2. In addition to tagging the valves closed, the clearances (dated

May 15. 1997) removed power from the valves by opening their breakers,

and removed an Operator Aid Computer and control board annunciator alarm

for "CA CST lo level" from service in each unit. As a result of these

actions, licensee personnel generated an Operations Technical Memorandum

(#97-01) dated May 15, 1997, assigning " action items" to designated

individuals ("normally a balance of plant licensed reactor operator")

until a permanent resolution of the AFW/CACST suction problem could be

obtained. The technical memorandum stated that shutting the CACST

suction valves would prevent the low level alarm from enunciating which

normally prompted certain actions in abnormal operating procedure.

AP/1(2)/A/5500/06. Loss of S/G Feedwater. Revision 17. To compensate

for the two CA-6 valve closures and the removal of the CACST low level

alarms, the technical memorandum included actions to maintain the UST

full, and to inform the control room SRO upon any AFW system automatic

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start to implement the abnormal procedure. The temporary melnorandum was

given an expiration date of April 30, 1998.

The licensee performed a 10 CFR 50.59 screening (also on May 15, 1997)

of the technical memorandum in accordance with Nuclear System Directive

(NSD) 209.10 CFR 50.59 Evaluations. Revision 6. to determine-if an

unreviewed safety question determination would be required. The

-screening determined that the activities described in the technical

memorandum related to the implementation of the abnormal operating

3rocedure and did not change the facility as described in the [ Updated

rinal) Safety Analysis Report (UFSAR). nor did it change procedures.

methods of operation, or alter a test or experiment as described in the

UFSAR: and, therefore did not recuire a US0 determination. This

screening did not specifically adcress the action to close the valves.

As of the end of this inspection aeriod, approximately nine months

later, the clearance tags and tec1nical memorandum were still active.

The inspectors reviewed the UFSAR. Section 10.4.9. Auxiliary Feedwater

System, subsection 10.4.9.2. which described the suction sources for the

AFW system. The UFSAR stated that "all of the preferred sources of

condensate quality water are normally aligned to the CA pump suctions."

The CACST was listed first among the three condensate-quality sources.

It further stated "to maintain steam generator water chemistry,

especially for such fast recovery events as [ station) blackout, loss of

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normal feedwater. or main steam system malfunction. the AFW pumps should

be normally aligned to condensate quality water. All necessary means to

prevent inadvertent injection of out-of-chemistry nuclear service water

to the steam generators must be employed."

The inspectors evaluated the licensee *s actions against the UFSAR

comments and determined that the licensee incorrectly concluded on May

15. 1997, that shutting the valves and issuing additional instructions

to operators regarding the implementation of Procedure

AP/1(2)/A/5500/06, did not involve a change to the facility or its

procedures as described in the UFSAR As a result, the licensee failed

to meet the 10 CFR 50.59 requirement to perform an evaluation

determining whether or not shutting the valves resulted in a US0. The

inspectors discussed this issue with licensee personnel who indicated

that the following factors influenced its decision not to pursue a

safety evaluation for closing the valves:

.

The clearance process and not the temporary or permanent

modification process, was used to implement the change. The

-temporary modification process was ruled out as a method to

implement the valve closure, because of its expected short

duration.

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23

The inspectors questioned whether or not the clearances had been

reviewed and dispositioned per the licensee's quarterly clearance

review program outlined in Procedure PT/0/B/4700/058. Operations

Quarterly Safety Tag Audit. Plant personnel indicated that the

clearances had been identified as requiring further evaluation due

to their age, but it was decided that the ongoing engineering

analysis would be due soon and that the clearances should remain

in place pending its completion.

The ins)ectors noted that the licensee had identified several

times tiroughout the nine-month period that the ongoing

engineering analysis would not be due until late winter 1998,

including a CA-6 engineering update documented for a November 10.

1997 Site Direction Meeting. During that meeting, plant

management was informed that preliminary results of the detailed

analysis verified the problem of AFW pump air entrainment and that

the isolation of the CACST was an appropriate decision. The

inspectors also noted that the clearance extended beyond a

refueling outage for Unit 1. The inspectors concluded that the

temporary or permanent modification process would have been the

appropriate vehicle to implement this change.

- No procedures were physically changed to implement the valve

closure or the actions described in the Operations Technical

-

Memorandum. The licensee considered the specific operator actions

described in the memorandum as typical actions that would have

been performed anyway (except for the action to enter AP-06 on any

AFW actuation). The inspectors contended that the disabling of

the low level alarm affected performance of emergency and abnormal

o)erating procedures which allowed certain actions despite the

a)sence of the alarm.

.

The licensee did not consider the actions to close the valves as

compensatory actions (described in NRC Generic Letter 91-18.

Revision 1. and its implementing program. NSD-203. Operability.

Revision 9).

10 CFR 50.59 states that the licensee may make changes to the facility

as described in the safety analysis report, or make changes in the

procedures as described in the safety analysis report without prior

Commission approval unless the )roposed change involves a change in the

technical specifications or an JSQ. It also requires that the licensee  ;

maintain records of changes in the facility and of changes in procedures '

made pursuant to this section, to the extent that these changes

constitute changes in the facility as described in the safety analysis

report (or the procedures as described therein). The records must  !

include a written safety evaluation which provides the bases for the J

determination that the change does not involve a US0. The licensee's

1

I

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24

failure to perform a USQ determination for the above compensatory

actions affecting the normal source of suction for the AFW system as

described in the UFSAR (and hence the failure to maintain associated

records of such determination) was contrary to 10 CFR 50.59 and is

identified as Violation 50-413.414/98-01-05: Failure to Conduct 10 CFR

50.59 Safety Evaluation for Operable but Degraded Condition and Related

Changes Involving the Normal AFW Pump Suction Source.

At the end of the inspection period. licensee management stated that it

recognized the weaknesses in its program implementation resulting in the

violation and intended to correct those in the near term since

preliminary results from the offsite engineering analysis confirm the

outside design basis condition with valves 1CA-6 and 2CA-6 open to the

AFW pumps' suction header.

The LER will remain open pending the licensee's permanent resolution of

the AFW design basis condition.

c. ' Conclusions

One violation of 10 CFR 50.59 was identified regarding the failure to

perform a safety evaluation with an unreviewed safety question

determination for compensatory actions associated with the realignment

of the auxiliary feedwater system pumps' normal suction sources. This

issue also involved poor decision making in the licensee's

implementation of the clearance process instead of the temporary

modification process.

IV. Plant Sucoort

R1 Radiological Protection

RI.1 General Comments (71750)

As noted in Section M2.2 above. the inspectors found minor discrepancies

between radiological postings on scaffolding containers located behind

the auxiliary building and the actual contamination levels on equipment

contained therein. The results of inspector-initiated smear analyses

demonstrated that contaminated levels were well below NRC regulatory

requirements for posting contaminated radioactive material: however, the

inspectors concluded that the minor discrepancies between postings and

actual contaminant levels warranted additional attention from site

management.

Other radiation protection activities were determined by the inspectors

to be adequate. No violations or deviations were identified.

_

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25

F2 Status of Fire Protection Facilities and Equipment

F2.1. Malfunction of Fire Detection Comouter

a. Insoection Scone (71750)

The inspectors reviewed an issue involving the failure of the fire

detection system to monitor a series of alarm points (i.e., fire zones).

The inspectors reviewed the 10 CFR 50.72 NRC Notification of non-

' compliance with Facility Operating License Conditions 2.C(8) (Unit 1),

and 2.C.(6) (Unit 2): Procedore RP/0/B/5000/013. NRC Notification

Requirements. Revision 21: Operations Management Procedure 2-22.

Attachment 7. Non-Licensed Operator Turnover Sheet. Revision 48: the

Unit 1 Facility Operating License: UFSAR Selected License Commitments

(SLC) Section 16.9. Auxiliary Systems - Fire Protection Systems:

Procedure IP/0/A/3350 003. Fire Detection System (EFA) Channel

Operational Test Procedure Revision 4: and the fire panel All Points

Log. The inspectors discussed with operations supervision the

expectations and training of the fire protection console operators

(FPCO) responsible for monitoring the fire alarm computer.

b. Observations and Findinas

On February 4. 1998, during troubleshooting of the fire detection system

the licensee determined that a series of alarm points were not

functioning properly. Alarms from the affected detectors would not have

'

been received in the main control room. The fire detectors were

declared inoperable and fire watches were established for the affected

zones in accordance with the fire protection program requirements. A

total of 36 zones were affected. Subsecuent to the discovery. the

licensee replaced three power supply anc computer logic cards associated

with the fire Janel and verified that all zones were being monitored

properly. On rebruary 7. 1998, a separate, unrelated card failure

resulted in the loss of fire zone monitoring. Appropriate compensatory

measures were established and the panel repaired.

Following the February 4 incident, licensee personriel identified that

the fire panel computer previously had not been monitoring all fire

zones based on a review of an All Points Log printout. During this

'

review, the licensee identified that specific series alarm zones had not

been monitoring since January 21, 1998. Further, some single zone

alarms committed to as part of the UFSAR, Chapter 16. Selected License

Conditions (SLC). Section 16.9. were not being monitored since December

24, 1997. Licensee personnel determined that compensatory fire watches

had not been posted within one hour for the affected fire zones during

the above dates. which was contrary to Facility Operating License

Condition 2.C.(8) for Unit 1. and 2.C.(6)- for Unit 2: along with

commitments contained in UFSAR SLC, Section 16.9-6, Fire Detection

,

,.l . i . ..i... -. . . ..

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26

Instrumentation. SLC Remedial action 16.9-6.a stipulated with any, but

not more than one-half the total in any fire zone Function A fire

detection instruments shown in Table 16.9-3 ino>erable, restore the

inoperable instrument (s) to operable status witlin 14 days or within 1

hour establish a fire watch patrol to inspect the zone (s) with the

ino)erable instrument at least once per hour...". The licensee made a

24-lour notification to the NRC for the non-compliances per License

Condition 2F (both Units) and 10 CFR 50.72.

.The inspectors' inde)endent review of the All Points Log printout

indicated that on Fe)ruary 4,1998, the 300 and 700-series fire detector

points were the zones involved, which affected various zones included in

Table 16.9-3. Fire Detection Instruments. A review of the non-licensed

operator turnover logs indicated that operators were reviewing and

turning over the res)onsibility to monitor the fire panel to subsequent I

operating shifts wit 1out recognizing that the series and single fire

zone alarms had been disabled since December 24, 1997.

The inspectors * review of operator logs, procedural guidance for fire j

alarm panel operation, and training lesson plans, found that there were

no written instructions or guidance for the operators to compare the All

Points Log printout to fire zones designated to be monitored. The 3

inspectors considered that this was a weakness and a significant

contributor to the problems with the fire detection panels not being

-

identified earlier.

Plant personnel documented these problems in PIPS 0-C98-0474 and 0-C98-

0499, which included proposed corrective actions to provide the FPC0

with better guidance on incorporating a review of the All Points Log

once per shift. Increased surveillance of the alarm panels was provided

until confidence in the system's performance could be regained.

The failure to identify.the deleted fire zones before February 4.1998,

and failure to establish compensatory fire watch )atrols within one hour

(after 14 days had expired) was contrary to Catawaa Facility Operating

LMense condition 2.C.(8). Technical Specification 6.8.1.1, and

commitments contained in SLC. Section 16.9 (of the UFSAR). This failure

affected single zones dating back to December 24, 1997, and the entire

300 and 700 series alarms deleted as far back as January 21, 1998. In

-

addition, during that time the operators inadequately performed their

turnovers without recognizing the non-functioning fire panel alarm

points. Licensee management has appropriately addressed the factors

-that caused the above non-compliances in its corrective actions as

described-in PIP 0-C98-0499. This non-repetitive, licensee-identified

and corrected violation is being treated as a Non-Cited Violation,

consistent with Section VII.B.1 of the NRC Enforcement Policy, and is

identified as NCV 50-413,414/98-01-06. Failure to Establish Fire Watch

Patrol Within 1 Hour for Non-Functioning Fire-Zone Detectors.

_-_ _ __-___ - _ _

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i

c. Cont'_.sions

One non-cited violation was identified for failure to establish l

compensatory fire watches after several fire detection zone alarms i

malfunctioned for greater than 14 days. The inspectors identified a

weakness concerning the lack of written guidance to operators on how to

effectively monitor the fire detection panel alarms, i

V. Mananamant Meetinas i

l

X1 Exit.Heeting Summary j

The inspectors ) resented the ins ection results to members of licensee

management at t1e conclusion of he inspection on February 25, 1998. l

The licensee acknowledged the~ findings presented. No proprietary

information was identified.

1

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28

PARTIAL LIST OF PERSONS CONTACTED

Licensee

M. Birch, Safety Assurance Manager

M. Boyle. Radiation Protection Manager

R.: Glover.. Operations Superintendent

-J. Forbes.' Engineering Manager

R. Jones. Station Manager-

M. Kitlan. Regulatory Compliance Manager

G. Peterson. Catawba Site Vice-President

R. Propst. Chemistry Manager

INSPECTION PROCEDURES USED

IP 37550: Engineering

IP.37551: Onsite Engineering

IP 55050: ASME Welding

IP 61726: Surveillance Observation

IP 62700: Maintenance

'IP 62707: Maintenance Observation -]

l

IP 71707: Plant Operations 1

IP 71750: Plant Sup) ort Activities

IP 92700: Licensee Event Reports l

IP 92901: Followup - Operations

IP 92903: Followup - Engineering

IP 40500: Effectiveness of Licensee Controls in Identifying and Preventing

Problems

ITEMS OPENED. CLOSED. AND DISCUSSED

ODEDe.d

50-413.414/98-01-01 URI Basis For Five-Minute Period

of VC System Inoperability

with Compensatory Action

(Section 01.2)

50-413.414/98-01-02 VIO Failure to Follow Plant

Operating and Administrative

Procedures (Sections 04.1.

08.1. 08.2. and 08.3)

50-413/98-01-03 NCV -ailure to Install Correct

N king Spacer in Feedwater

)

. .

4

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29

Regulating Valve ICF-37

(Section M2.3)

50-413.414/98-01-04 IFI Assess the Licensee's Dose

Analysis Calculation for ECCS

Leakage Outside Containment

(Section E3.1)

50-413.414/98-01-05 VIO Failure to Conduct 10 CFR

50.59 Safety Evaluation for

Operable but Degraded

Condition and Releted Changes

Involving the Normal AFW Pump

Suction Source (Section E8.1)

- 50-413.414/98-01-06 NCV Failure to Establish Fire

Watch Patrol Within 1 Hour for

Non-Functioning Fire Zone

Detectors (Section F2.1)

50-414/98-01-07 URI Operability of Valve 2NW-190A.

(Section M1.2)

Closed

50-414/96-07 LER Cold Leg Accumulator Discharge

(Section 08.1)

50-413.414/97-15-01 URI Failure to Follow Procedures

Resulting in Inadvertent

Injections of ECCS Fluid into

the Reactor Coolant System

(Section 08.2)

50-413/97-15-02 URI Appropriateness of Operator

Actions During Control Rod

Testing (Section 08.3)

Discussed

50-413.414/97-003-00 LER Auxiliary Feedwater System

Found Outside Design Basis

(Section E8.1)

50-413,414/97-300-02 URI Catawba UFSAR Discrepancies-

(Section E8.1)

l' )

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30

LIST OF ACRONYMS USED

AHU - Air Handling Unit

AP .- Abnormal Procedure

CFR -

Code of Federal Regulations

CLA -

Cold Leg Accumulator

DBD -

Design Basis Documentation

EFA -

Fire Detection System

ESF -

Engineered Safety Feature

FPCD -

Fire Protection Console Operators

IFI -

Inspector Followup Item

LER -

Licensee Event Report

NCV -

Non-Cited Violation

OMP -

Operations Management Procedure

PIP -

Problem Investigation Report

PDR -

Public Document Room

RCS -

Reactor Coolant System

RWST -

Refueling Water Storage Tank

SLC -

Selected Licensee Commitments

UFSAR - Updated Final Safety Analysis Review ,

URI -

Unresolved Item

VC - Control Room Ventilation System

VIO -

Violation

WO -

Work Order

YV -

Containment Chilled Water