ML20134G123

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Insp Repts 50-254/96-17 & 50-265/96-17 on 961027-1206.No Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML20134G123
Person / Time
Site: Quad Cities  Constellation icon.png
Issue date: 02/04/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20134G109 List:
References
50-254-96-17, 50-265-96-17, NUDOCS 9702100289
Download: ML20134G123 (30)


See also: IR 05000254/1996017

Text

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U. S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos: 50-254, 50-265

License Nos: DPR-29, DPR-30

Report No: 50-254/96017(DRP), 50-265/96017(DRP)

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Licensee: Commonwealth Edison Company (Comed)

Facility: Quad Cities Nuclear Power Station, Units 1 and 2

Location: 22710 206th Avenue North

Cordova, IL 61242

Dates: October 27 - December 6, 1996

, Inspectors: C. Miller, Senior Resident Inspector

K. Walton, Resident Inspector

L. Collins, Resident Inspector

R. Ganser, Illinois Department of Nuclear Safety

Approved by: Patrick Hiland. Chief

Reactor Projects Branch 1

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9702100289 970204

PDR ADOCK 05000254

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! EXECUTIVE SUMMARY i

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. Quad Cities Nuclear Power Station, Units 1 & 2

j NRC Inspection Report 50-254/96017(DRP), 50-265/96017(DRP)

! This inspection included aspects of licensee operations, engineering,

L maintenance, and plant support. The report covers a 6-week period of resident

l inspection.

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Doerations

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. The inspectors determined that winterizing preparations had improved

j. over last year. However, certain equipment, including the auxiliary

, boiler, were not ready for the onset of cold weather. This was a repeat

finding from last year. In addition, the inspectors determined that the

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lack of special precautions or corrective actions for the low

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temperature alarms was a weakness in the annunciator .wponse procedures

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(Section 01.2).

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i . The shift engineer took a conservative approach in the conduct of I

switchyard work to repair the backup battery power supply for switchyard '

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breakers (Section 01.4).

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. The inspectors concluded that Operations and Engineering had failed

! fully to evaluate the effect a degraded check valve would have had on

! the low pressure coolant injection system during an accident. l'

Operations had not initially characterized the degraded check valve as a

. significant operator workaround (Section 01.5).

l . The inspectors concluded that the work effort on the circulating water

traveling screens was necessary, but not well coordinated from a risk

. perspective. . As a result, one of the two sup) lies to all safety-related ,

! cooling water was unavailable for over a monti with both units operating i

i at full power (Section 02.1).

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j Maintenance

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i . The preparation, communications, and the general performance of the high

pressure coolant injection (HPCI) surveillance test were acceptable.

Shift management allowed operators to continue the high pressure coolant

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injection (HPCI) surveillance without documenting problems arising in

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the procedure and without documenting a clarification of a step in the

procedure. Weaknesses in planning and schedule adherence led to an

l extended surveillance period for HPCI (for an administratively increased ,

. surveillance). (Section M1.1).

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. The licensee identified that incorrect bolt material was installed in

the 1C and 2C residual heat removal service water (RHRSW) pumps due to

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inadequate control of vendor processes. A violation was issued for

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failure to ensure correct materials were used in safety-related

equipment. The use of the incorrect bolt material resulted in a non-

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cited violation for the 2C RHRSW pump being inoperable in excess of

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Technical Specification (TS) limits. The licensee's failure to report a

condition prohibited by TS resulted in a violation of 10 CFR 50.73.

Other examples involving inaaequate control of vendor processes and

materials were also identified by the licensee (Section M2.1).

. During overhaul and modification of the 2D RHRSW pump. the licensee

identified and corrected a number of problems including deficiencies in

vendor supplied parts. Final test results indicated that the overhaul

effort was successful (Section M2.2).

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Various material . equipment deficiencies resulted in increased personnel

radiation exposure and impacted plant operations (Section M2.3).

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!

Enaineerina

. The licensee identified that the control room emergency ventilation

system was inoperable. Post modification and surveillance testing

! failed to ensure the system met requirements specified in the updated

final safety analysis report (UFSAR). The licensee had not performed a

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required 10 CFR 50.59 evaluation. These three issues were being

considered Apparent Violations (Section E2.1).

. The inspectors identified a violation for failure to incorporate

Technical Specification requirements into station surveillance

procedures (Section E3.1).

l . The inspectors identified weaknesses in the licensee's approach for

determining control room operability for post accident conditions

(Section E3.2). l

Plant Sucoort i

. The inspectors noted additional radiation exposures were received in an >

effort either to repair deficient material condition issues or to

continue operating the unit with the deficient material condition

(Section R1.1).

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Reoort Details i

Summary of Plant Status

! Unit 1 operated at or near full power throughout the inspection aeriod,

with the except M of the first full week in November. On Novem)er 1.

load was dropped to approximately 500 MWe to repair the level control

valve for the "B" steam packing exhauster. The load was further dropped

to approximately 340 MWe due to a seal leak on the 1A reactor feedwater

pump. The unit was returned to full power on November 7 and continued 1

to operate at or near full power through the remainder of the inspection  !

period.

Unit 2 started the period by increasing to full power following repairs l

l to the main turbine bypass valve control system. Problems with the

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moisture separator drain tank level ~ control valves, followed by J

continued main turbine bypass valve control system problems, caused the

unit to be taken off-line on October 27. The unit was brought back on-

line on October 30. and held at 200 MWe for testing of the main turbine

control systems. On November 1, the unit was taken to full power. On  !

December 2, operators reduced Unit 2 power to 200 MWe to repair a l

packing leak on a reactor water cleanup valve. The unit operated at or

near full power the remainder of the inspection period.

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I. Operations

l 01 Conduct of Operations

l 01.1 General Comments (71707)

l Using Inspection Procedure 71707, the inspectors conducted frequent

i reviews of ongoing plant operations.

l During the inspection period, several events occurred which required

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prompt notification of the NRC pursuant to 10 CFR 50.72. The events and

dates are listed below.

October 27 Operators reduced Unit 1 power due to reactor feed pump

ventilation fan return damper failing closed.

October 27 Operators tripped Unit 2 main turbine due to problems with

moisture separator drain tank level control valves. Foreign

material caused two valves to stick open.

October 28 Emergency Notification System (ENS) call. Safety train of

control room ventilation system declared inoperable due to

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Topical headings such as 01, M8, etc., are used in accordance with the

i NRC standardized reactor inspection report outline. Individual reports are

i not expected to address all outline topics.

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inability to maintain sufficient positive pressure in the

control room.

November 1 Operators reduced Unit 1 power due to problems with "B"  !

gland steam condenser level control valve air operator.

November 24 Control room emergency filtration system declared inoperable

since operators were not assured that-a surveillance test  :

was performed correctly. Subsequent testing verified system !

operability.

November 26 Operators declared the shared standby diesel generator r

inoperable to Unit 2 due to a relay problem.

December 2 Operators reduced Unit 2 power to less than 15 percent power  !

due to problems with reactor water cleanup isolation valve ,

packing leak.

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01.2 Winterizino Checklist (71714)

a. Insoection Scoce l

The inspectors observed performance of scheduled cold weather  !

preparation activities including use of Quad Cities Operating Procedure

(OCOP) 0010-01, " Winterizing Checklist." '

b. ' Observations and Findinos l

The inspectors reviewed the licensee's progress of completing the  !

checklist throughout the period and found that a majority of items were  :

completed prior to the expected date of October 30. A notable exception  :

to the licensee's expectations was that the heating boilers were not i

available for use by the first cold spell of the season or by l

October 30.

The inspectors identified several periods when supply air low I

temperature annunciators (panel 912-5, B1 through B5) were lit in the l

control room for the reactor building, the turbine building, and the '

radwaste building. The annunciator response procedures for these alarms

guided the operators to check for valid indication and take corrective

action as necessary. There were no specific actions identified in the

procedures.

The inspectors questioned operators as to the special precautions being

taken during the time when low intake temperature alarms were

annunciated. The operators indicated that only normal rounds were being

performed and that maintenance actions to repair the boilers were

underway. The inspectors noted that the potential for colder than

normal equipment temperatures existed during this time, especially in

the vicinity of su)

conditions during )uilding

ply air inspections.

duct outlets, but found no unacceptable

c. Conclusions

The inspectors determined that use of the winterization checklist had

improved from the previous year. P vever, the licensee still failed to

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) lace the auxiliary boiler and other items on the cNcklist in service

l Jefore the arrival of cold weather. This was a repeat problem from

l 1995. In addition, the inspectors determined that the lack of special

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precautions or corrective actions for the low temperature alarms was a

weakness in the annunciator response procedures.

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01.3 Conservative Ooerations Control of Work Activities

l The inspectors attended a meeting conducted by the shift engineer to

l address switchyard work that had the potential to remove backup battery

l power for the switchyard breaker trip circuits. The shift engineer

directed that the engineers )erform a 10 CFR 50.59 safety evCuation to

address a design condition tlat would be controlled by temporary I

alteration. The meeting was concise, and resulted in o. i parties

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knowing their roles and actions. There was good inter-departmental

communication. Shift management's conservative approach was

demonstrated in the pursuit of a safe and effective corrective action

for a problem that could have adversely affected the units.

01.4 Unit 2 Low Pressure Coolant Iniection (LPCI) System Inocerable Due to

Loss of Discharge Header Pressure

a. Insoection Scone (71707)

The inspectors responded to a licensee report on November 12 in which

the LPCI system was declared inoperable after losing keep fill pressure

on the common discharge header from the residual heat removal (RHR)

pumps. The inspectors interviewed licensed operators and the system

engineer, and reviewed the system configuration and previously completed

surveillance tests.

b. Observations and Findings

The licensee had started the "2D" RHR pump in order to verify proper

breaker operation after maintenance. After stopping the pump, the

discharge check valve (2-1001-67D) failed to fully reseat. This failure

allowed water in the discharge header to drain back to the torus through

the normally open pump suction valve. Since the discharge header was

common to all four RHR pum)s the entire LPCI system was affected.

Under normal conditions, t1e keep fill system maintained pressure in the

discharge header for both LPCI and the core spray system. However, the

keep fill system could not maintain the discharge header pressure with

the discharge check valve stuck open.

The licensee entered a 7-day shutdown limiting condition for o)eration

(LCO) according to Technical Specification (TS) 3.5.A.2 when t1e Unit 2

LPCI system was declared inoperable. Operators shut the suction valve

for the "20" RHR pump which allowed the keep fill system to repressurize

the discharge header. Operators then filled and vented the system in

l accordance with the operating procedure. The "2C" RHR pump was started

l to reseat the discharge check valve on the "2D" pump. Once the "2C" RHR

l pump stopped, header pressure remained constant: and operators

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determined-that the "20" pump discharge check had reseated. The LPCI

system was then determined to be operable and the LCO was exited.

Operators generated problem identification form (PIF) 96-3196 that

referenced a 3revious similar event and mentioned a caution card on the-

control switc 1 for the "2D" RHR pump. The inspectors found that the

caution card on the control panel was dated July 3,1996, and referenced

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an action request from May 21, 1996. The inspectors reviewed the

previous event and found it was similar to the current event, except the-

unit was in cold shutdown. The system engineer told the inspectors that

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this check valve had been replaced during the 1995 Unit 2 refueling

outage and that he had been aware of the leak since May 1996 when the

RHR system was operating in the shutdown cooling mode.

i The inspectors viewed the degraded condition of the check valve as a

{ significant operator work around since failure of the valve to seat

could affect the LPCI function during an accident. However, the

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inspectors found that this work around was not documented on the

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operator work around list and that no specific information or

, instructions had been given to operators regarding this potential

failure mode. Although the caution card existed on the control switch

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for the pump, inspectors determined that some control room operators did

not recognize the impact of the condition on accident response, and some-

l were not even aware of the degraded condition. )

! The licensee agreed that the degraded check valve met the criteria for  !

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an operator work around. At the end of the inspection period, the i

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licensee had ordered a new valve and was evaluating whether to perform

the maintenance on-line or during the upcoming refueling outage. In

, addition. Operations issued a standing order with special instructions

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to operators regarding this valve.

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c. Conclusion

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l The inspectors concluded that Operations and Engineering had failed to

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fully evaluate the impact the degraded check valve would have had on

LPCI during accident. Even after the second instance of a check valve

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failing to reseat, the licensee was slow to consider this a significant

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operator work around. The inspectors found the licensee's plans for

future replacement of the valve and the issuance of the standing order

to operators to be acceptable cc' *ective actions and compensatory

measures for this degraded condim in,

j 02 Operational Status of Facilities and Equipment

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02.1 Circulating Water Bay Conditions

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a. Inspection Scope (71707)

! The inspectors observed maintenance activities on the Unit 1 circulating

j water bay to assess the licensee's evaluation of risk significant

l activities.

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b. Observations and Findinas

Poor Risk Persoective and Prioritization

The inspectors observed maintenance activities associated with repairs

on the 1A circulating water pump and motor, and the 1A and 18 traveling

screens. Repairs to the traveling screens required the 1A circulating

water bay to be dewatered. This was accomplished by placing stop logs

upstream of the 1A and 1B traveling screens and at the Unit 1 water

supply to the safety-related cooling water bay at the crib house, and

Jumping the water out of the 1A bay. The safety-related cooling water

Jay was the suction source for all trains of emergency diesel generator

cooling water (EDGCW), residual heat removal service water (RHRSW) for

both units, and one of two diesel fire pumps for both units.

The inspectors determined that the repairs to the circulating water

system were necessary and appeared to be aimed at correcting long

standing problems identified with the traveling screens. However, the

limited risk considerations given to this work were troubling.

Dewatering the 1A bay left only one supply of water to the safety-

related water bay (through the PE and 2F traveling screens and the fixed

screen from the 2C circulating water bay). Normally there were two

sources of water to this safety-related water bay, from the ultimate

heat sink (VHS) through the 1A and the 2C circulating water bays. The

second supply to the safety-related water bay was unavailable since

October 28, 1996.

The inspectors asked what processes were used to evaluate the risk

3riorities of )erfcrming work which required circulating water bay 1A to

]e drained witi both units at 100 percent power instead of with one or

both units shut down. The licensee indicated that the risk priorities

of various plant conditions were not considered, and that the work was

always scheduled for on-line maintenance. The inspectors found that the

work requests had been generated in 1995, and since that time both units

had been shut down simultaneously for several months. Additionally, the

inspectors found that the process described in Quad Cities

Administrative Procedure (0 CAP) 2200-07 "Probabilistic Risk Assessment

of On-Line Maintenance Activities" was used, but was not detailed enough

to model items such as the circulating water bay supply to RHRSW in the

station probabilistic risk assessment driven operational safety

predictor program.

The inspectors had previously identified opportunities for better

planning of on-line shared diesel generator work that could have been

performed during the sam dual unit outage period (see Inspection Report

(IR) 50-254/265-96014). Licensee management indicated the potential

weaknesses in scheduling risk significant work would be evaluated.

Lead Unit Planners reviewed the risk significance of circulating water

bay dewatering efforts. However, only the risk effects of making a

circulating water and service water pump inoperable were considered.

The loss of redundancy to the RHRSW water supply from the UHS was not

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modeled in the operational safety predictor or considered by planners or

operations supervision. Since the work was not considered risk

significant, planners scheduled the work only on day shift for about the

first 2 weeks of the job. Later, a limited sized evening shift crew was

added. At times, all crews were pulled away to work on other emergent

work for 1 to 2 day periods.

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Poor Understanding and Control of Licensing Basis

The inspectors were concerned that the licensee modified an UHS flowpath

of water to safety-related cooling components without performing an

evaluation for the modification. Technical Specification recuirement

3.8.A specified that during plant operation at power, two incependent

subsystems of RHRSW be available with an operable flow path capable of

taking suction from the UHS. On November 24 the inspectors questioned

the licensee about the operability of the RHRSW subsystems when only one l

path from the UHS to the safety-related water bay was available, and it '

was common to all trains. Operations management indicated that the

safety-related water bay was considered part of the UHS, and there was i

no restriction to operations with only one pathway. l

The inspectors determined that the updated final safety analysis report

(UFSAR) descriation of the UHS and of RHRSW was not detailed enough to i

determine the )oundary of the UHS and what flow requirements were needed i

for intake into the safety-related water bay. The inspectors pointed

out that the licensee had used stop logs to modify the safety-related

water bay without evaluating the potential impact. For example, the

licensee had not initially considered if the flow capacity of the single I

fixed screen was sufficient, and had not considered the risk impact of

the loss of the redundant water supply. The inspectors also questioned  :

the ability of the stop logs to maintain an acceptable water level at j

all times during a seismic event. The licensee was evaluating the '

design requirements for the UHS at the close of the period. The

inspector's planned assessment of the licensee's evaluation of the

design requirements of the VHS and review of scheduling of risk

significant activities is considered an Unresolved Item (50 254/265- ,

96017-01). I

c. Conclusions

The inspectors concluded that the work effort on the circulating water

traveling screens was necessary, but was not well coordinated from a

risk perspective. As a result, one of two supplies to all safety-

related cooling water was unavailable for over a month with both units

operating at full power. In addition, the design basis for the sup) lies

to safety-related cooling water were not well known or considered w1en

stop logs isolated one of the pathways for safety-related cooling water

from the UHS.

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08 Hiscellaneous Operations Issues (92700)

08.1 (Closed) Unresolved Item (50-254/265-94004-23): Reactor Vessel

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Temperatures Not Recorded During Cooldown. The Diagnostic Evaluation

Team (DET) noted that the licensee previously identified operators

failed to verify reactor vessel temperature limits during unit cooldown

1 as required by TS 3.6. This was addressed-in licensee event report t

(LER) 50-254-92011 and LER 50-265-92010. These LERs were previously

reviewed and closed. The inspectors noted the licensee adequately

l verified temperature limits during unit heat ups and cool downs. .

! The DET also identified the licensee had no procedural requirements to

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log or monitor inoperability of instruments to ensure compliance with TS

l during surveillance testing. The licensee subsequently established

procedural controls in this area. The inspectors noted the licensee

. continued to implement these administrative controls while complying

i- with TS LCOs for ecuipment unavailability during surveillance testing.

This item 1.s closec .

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08.2 (Closed) Licensee Event ReDort (LER) 50-254/94011: Control Rod L-11

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Failed to Scram During Rod Time Testing. A maintenance activity during

i the Unit 11994 refueling outage installed a pipe plug into a solenoid

3 valve exhaust port during maintenance testing but the plug was not

i removed until detected by operators during rod testing. The licensee

! attributed this event to maintenance workers failing to adhere to

i procedures. The licensee trained maintenance personnel on temporary

alterations and maintenance on hydraulic control units. The licensee

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changed procedures and performed rod testing during the primary plant

i hydrostatic test in lieu of testing rods during startup from a refuel

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outage. The inspectors reviewed the changed procedures.and verified

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compliance with TS. Maintenance craft procedure adherence has been

i enhanced by the station requirement to sign each line item of a

1 procedure. Some sequencing and procedure adherence problems have

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continued, to a lesser extent, and will be addressed on an individual

basis. This event resulted in a Level III Violation and Civil Penalty.

See inspection reports 50-254/94017 and 94027 for additional

information. This item is closed.

l 08.3 IC.losed) Violation 50-254/265-94017-01: Violation of Procedure

i Adherence, Test Control, and Corrective Actions Associated with Failure

] of a Control Rod to Scram During Testing. This violation was the same

event described in Section 08.2 above. Corrective actions for the

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procedural adherence violation were described above. Licensee actions

for test control and corrective action violations included counseling of

appropriate nuclear engineering personnel. The licensee hired an

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experienced nuclear engineer to provide oversight of nuclear engineering

issues. Corrective actions taken by the licensee to address delayed

i start of rod motion included replacement of scram solenoid pilot valve

diaphragms with models less prone to the phenomena. The licensee also

reinforced the use of the nuclear tracking system to ensure documented

problems were tracked to resolution. The-inspectors reviewed the

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licensee's corrective actions. This item is closed.

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II. Maintenance

M1 Conduct of Maintenance (62707)

M1.1 High Pressure Coolant Iniection (HPCI) System Surveillance Test

a. Insoection Scone

The inspectors observed performance of scheduled activities including a

monthly surveillance test run of Unit 2 HPCI system Quad Cities

Operating Surve111ance (0C05) 2300-5, " Quarterly HPCI Pump Operability

Test."

b. Observations and Findings

0)erations stopped at one point to make a )rocedure field change when

tie normal pressure indication listed in tie procedure was not available

due to maintenance. However, the inspectors identified one instance

where operators could not properiy verify the requirements of the

procedure. Step H.31.b. required operators to verify turbine speed

increased to approximately 3900 rpm. When the turbine speed reached

only 3100 rpm, operators appro)rlately notified the system engineer.

The system engineer informed t1e operating crew that this was acceptable

performance for the present system condition, and to continue the test.

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The inspectors identified that the system engineer was not aware of the

origin of the test requirement or why previous crews had not had trouble

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meeting the requirement. The system engineer felt confident that the

3900 rpm requirement was related to the high speed stop setting of the

HPCI motor speed changer circuitry and was not a critical parameter.

The inspectors reviewed the completed procedure and identified that

operators had not documented the inability to meet the 3900 rpm

requirement, and that no procedure change was made, even though the i

actual rpm during the test was about 20 percent lower than required.

The system engineer indicated that the rpm seen could be considered l

approximately equal to that required by the procedure. Based on the

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magnitude of the s)eed difference, the inspectors believed that

documentation of t1e speed difference would clarify the step during

future testing. The surveillance results indicated that all TS l

requirements for rated flow were met. 1

The inspectors noted that the next performance of the surveillance was

scheduled for November 28: however, the test was not performed until

December 7. The licensee had postponed the test due to Thanksgiving

holiday work schedule conflicts. Although this test was only required

to be performed quarterly by TS, the licensee scheduled it monthly

because previous performance problems had reduced confidence in the ,

system. The licensee sought to improve performance through increased  !

testing and troubleshooting.  ;

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c. Conclusions

The inspectors noted that the preparation, communications, a'nd the

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general performance of the' surveillance test were acceptable. An

opportunity to document 3roblems and clarify the meaning of steps in the

procedure was missed. S11ft management allowed operators to continue

the HPCI surveillance without documenting problems arising in the

procedure and without documenting a clarification for the step for lower

than expected rpm. Weaknesses in planning and schedule adherence led to

an extended surveillance period for HPCI.

M2 Maintenance and Haterial Condition of Facilities and Equipment

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M2.1 Use of Incorrect Bolt Material in RHRSW Low Pressure (LP) Pumos (IP

92700)

a. Insoection ScoDe

The ins)ectors investigated the licensee's use of incorrect bolts in the

RHRSW L) Pumps.

b. Observations and Findinas

Incorrect Bolt Material on 1C and 2C RHRSW LP Pumos

On May 3. 1996, the RHRSW Jump vendor notified Comed (Ref: 073-

61152/503284XX348/XX275) t1at the ) art number for the bolts used in the

RHRSW LP pumps was not current. T1e recommendation from Ingersoll-

Dresser Pump Co. was to change the bolt material from SAE Grade 8 to

A193-75 Class 2 Grade B8. The vendor certified that the recommended

parts had not affected the form, fit, or function of the original parts,

when in fact, the substitution bolts had a lower yield strength limit

than the original Grade 8 material. On May 24, 1996. Comed's Corporate i

Materials Engineering Group, performed an evaluation. M-1996-0454-0. l

agreeing with the vendor's incorrect substitution recommendation (PIF '

96-3039).

On October 25. 1996, during assembly of a sJare RHRSW LP Pump.

Mechanical Maintenance Department (MMD) worcers were torquing the pump  ;

casing flange bolts. One bolt broke and several others showed signs of 1

stretching. The licensee stopped the work and began an investigation of

the cause of the failures (PIF 96-3025). The licensee inspected all LP

pump casing bolts and discovered that lower yield strength A193-75 Class

2 Grade 88 bolt material had been installed in the 1C RHRSW LP Pump (PIF i

96-3029) on October 8. 1996, and in the 2C RHRSW LP Pump (PIF 96-3030)  !

in July 1996. A torque value of 375 ft/lbs applying to the original

"high yield strength" limit for the SAE Grade 8 bolts, was used to

assemble the pump casings. Consequently, the yield strength limit for

all of the LP pump casing bolts on the 1C and 2C RHRSW LP Pumps was

exceeded during assembly,

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The licensee's corrective actions included validating (through the

vendor) that the high yield strength SAE Grade 8 bolt material or

equivalent was the correct replacement. The torque value was verified

to be correct at 375 ft/lbs lubricated with N5000 Antiseize for the SAE

Grade 8 bolts. Additionally, the vendor recommended a "one-time-use-

only," for the high yield strength SAE Grade 8 bolts. Following

replacement of the incorrect LP pump casing bolts with the correct

bolts, the 1C pump was tested and declared operable on October 27, 1996,

and the 2C pump was declared operable on October 28, 1996. The licensee

was assessing the condition of other RHRSW LP pumps using the correct

SAE Grade 8 bolts which have been torqued more than once. Past practice

allowed reuse of the bolts.

A)pendix B of 10 CFR Part 50, Criterion III, " Design Control." requires

tlat measures shall be established for the selection and review for

suitability of application of parts that are essential to the safety-

related functions of the structures, systems and components. The

licensee's failure to assure that the correct a] plication of bolt

material was used in the safety-related RHRSW L) pumps was a Violation

(50 254/265-96017-02) of 10 CFR Part 50 Appendix B, Criteria III.

The licensee took good corrective actions at the station level following

the discovery of a broken bolt. However, this condition appeared to be

similar to other 2roblems related to the control and issuance of safety-

related parts. W1ile the short term corrective actions were aggressive,

long term actions which included both station and corporate actions,

have not been demonstrated. Based on this lack of comprehensive

corrective action to prevent recurrence, the NRC chose not to exercise

the discretion outlined in Section VII.B.1 of the Enforcement Policy.

2C RHRSW Pumo InoDerable in Excess of TS LCO

Technical Specifications 3.5.B.2 required that with one RHR$W pump

inoperable, continued reactor operation is permissible only during the

succeeding 30 days provided that all other active components of the

containment cooling mode of the RHR system are operable. Technical

Specifications 3.5.B.5 stated that: "If the requirements of 3.5.B

cannot be met, an orderly shutdown shall be initiated, and the reactor

shall be in a cold shutdown condition within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />." The 1C and 2C

RHRSW pumps were declared inoperable on October 26, 1996, when the

licensee recognized the potential impact of the installation of

incorrect bolt material that was discovered late on October 25, 1996.

It was established that the correct bolt material for use in the LP

pumps was the original SAE GRADE 8 material. The 2C RHRSW Pump was

inoperable from July 12, 1996, when incorrect bolts were installed in

the LP ) ump casing, until October 28, 1996. The 1C RHRSW Pump was

inopera)le from the period following October 8, 1996, when incorrect

bolts were installed in the LP pump casing, until October 27, 1996.

Unit 2 was started on August 15, 1996, and the incorrect bolt condition

, was discovered on October 25, 1996. Unit 2 was operated past the

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30 days allowed by TS. This licensee-identified and corrected violation j

l is being treated as a Non-cited Violation 50-254/265 96017 03 consistent l

l with Section VII.B.1 of the NRC Enforcement Policy. I

Failure to ReDort a Condition Prohibited by TS

l

'

The 10 CFR 50.73 Section (a)(2)(B). " License Event Report System,"

required the licensee to report any condition prohibited by the plant's

l TS within 30 days after the discovery of the event. However, the l

licensee failed to report by November 24, 1996, in accordance with j

10 CFR 50.73, operation of Unit 2 in a condition prohibited by plant

TS 3.5.B.2 and 3.5.B.5 following discovery of the incorrect bolts on

October 25, 1996, which is a Violation (50 254/265 96017-04) of i

10 CFR 50.73. '

Other Problems Identified Durino RHRSW LP Pumo Maintenance

On October 26. 1996, due to a separate incorrect recommendation from the i

vendor (PIF 96-3043), a single incorrect bolt was found to have been '

installed on the 2A RHRSW LP Pump. A substitute bolt material, A193

Grade B7, was installed. This material has a yield strength between the

correct SAE Grade 8 material and that of the lower yield A193-75 Class 2

Grade B8 material. This single bolt was replaced.

Another PIF (96-3253) was written to address two spare bearing housings  !

for the RHRSW LP Pumps that did not have all of the bolt holes tapped. l

There were dimensional problems with two new LP pump shafts drawn from

stores for future rebuilds (PIF 96-3000). Several other problems

involving inadequate control of vendor supplied materials for LP pumps

are described in section M2.2 below.

During overhaul of the 1C RHRSW Pump in the previous inspection period

(NRC Inspection Re3 ort 50-254/265-96014), the LP pump casing flanges

were found not to 1 ave met a critical dimension and the pump failed the

post maintenance leak test. In response, the licensee's Site Quality

Verification Department has initiated a "stop work" to the vendor in

order to identify the root cause and take effective corrective actions

for the relatively high number of quality control issues from one

vendor. The licensee initiated a 10 CFR Part 21 internal and/or

external report to address the generic and potential industry

implications of the materials issues.

c. Conclusions

The licensee had not assured adequate quality assurance measures for

control of some vendor materials and processes. This resulted in

incorrect bolt material being installed in the 1C and 2C RHRSW LP pumps,

rendering the pumps inoperable. A separate incorrect bolt

recommendation resulted in the installation of one incorrect bolt in the

2A RHRSW LP pump.

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The licensee's response to the broken bolt while rebuilding the spare

pump'in the shop was appropriate. Stopping the job and )erforming

timely inspections of all the other pumps demonstrated tlat MMD workers

were alert to conditions adverse to quality. The licensee's

-identification and timely correction of the incorrect bolt material was

an adequate immediate response. While the short term corrective actions

were aggressive, long term actions which include both station and

corporate actions, have not been demonstrated.

The inspectors will continue to monitor the licensee's performance in

determining the root cause of inadequate quality assurance of materials

and processes supplied by a vendors.

M2.2 Observation of MMD Work Activities for Overhaul of the 20 RHRSW Pumn

a. Insoection Scooe

The inspectors observed the MMD during portions of the overhaul of the

20 RHRSW Pump. This was the seventh of eight pump overhauls to perform

modifications (cutwater modification) to improve the overall pump

performance characteristics and increase reliability.

b. Observations and Findinas

The inspectors noted that spare components and tools were staged in an

orderly fashion. Foreign material exclusion (FME) barriers were

appropriately placed and FME practices were adhered to. Job supervision

was adequate and workers coordinated the tasks with each other. A

number of issues described below were identified during the overhaul

effort.

Erosion of Flance

E2cessive erosion was found at the 2D RHRSW LP pump discharge flange.

The cause of the erosion was determined to be a weld dam used to

initially construct the pipe. The weld dam allowed excess turbulence at

the discharge flange, resulting in accelerated erosion. The repair i

consisted of building up the eroded area inside the pipe and machining j

the added material to form a smooth surface (ER 9606131). The pump 1

engineer stated that the condition had not been detected during

ultrasonic testing. The eroded condition had been noted on one or more

of the other RHRSW pumps during overhaul, but was not as advanced as on

the 2D pump.

Bearina Housina i

One of the bearing housings for the 2D RHRSW high pressure (HP) pump was

dimensionally incorrect (PIF 96-3203). These housings, although

supplied as new, had a thick paint-like coating on the inner surface.

Some of this coating had flaked off and was lose in places, such that it i

posed a potential for introducing foreign material into the bearings

'

during operation. The licensee replaced the faulty housings.  !

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Rework

Maintenance workers initially positioned the 2D RHRSW HP pump seal ,

housings 180 degrees out of the correct orientation. This was  :

attributed to a performance error on the part of the MMD worker who '

!

failed to check the proper orientation prior to assembly. Following the

licensee's evaluation of the PIF, an additional work instruction was

added to the work package, specifying the orientation of the seal

housings to minimize the potential for recurrence. The licensee

j initially. indicated that the orientation of the seal-housing was within

the skill of the craft.

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The second issue arose during post maintenance testing (PMT) of the pump

when minor leakage occurred at the HP Jump outboard seal. Engineering

recommended that the HP' pump be re-worced. The cause of the leak was

found to be an improperly seated "0" ring in the pump seal assembly.

The licensee determined that this was due to im)recise dimensional

specifications on the threaded portion of the slaft as it was delivered

by the vendor. Maintenance Engineering recommended dimensional

l adjustments to the shaft assembly to eliminate the potential for the

.

interference between the "0" ring and the threaded portion of the pump

! shaft. Resultant changes were implemented into the work instructions

for future reference.

c. Conclusions

l

Weaknesses were identified in quality assurance of vendor supplied

components. The licensee's work procedure was inadequate for the skill

level of the workers as indicated by the incorrect installation of the

2D RHRSW HP Pump seal housings. In spite of a number of problems which

the licensee resolved, the work was successfully completed and the pump

was returned to service within the original schedule. Test data

,

indicated that the pump performance had improved significantly over the

!

prior-to-overhaul condition. The efficiency of the overhaul process was

improved, in part, due to using many of the same 3ersonnel for each

overhaul job. The knowledge and skill level of t1e alignment and

vibration team has increased with the experience on the RHRSW pumps.

Some lessons learned from previous RHRSW pump overhaul efforts were

effectively implemented.

M2.3 Material Condition of the Facility

a. Insoection Scone (71707. 62707)

The inspectors reviewed operator logs, PIFs, interviewed operations and

,

maintenance personnel, and observed activities in progress.

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b. Observations and Findinas

Reactor Water Clean UD (RWCU) System Problems - Unit 1

Maintenance personnel, troubleshooting a pump low flow candition,

discovered an installed orifice in the discharge nozzle of the 1A RWCU i

Jump. A modification performed in 1986 (M04-1-85-065) was supposed to

lave removed the orifice. In the work package impleme iting M04-1-85-

065, workers documented the orifice could not be located. and

l reassembled the discharge piping without removing the arifice. As

I corrective actions, the licensee removed the orifice from the 1A RWCU

pump, and wrote a work request to remove the orifice from the 2B RWCU

j pump.

l

After removing the orifice from the 1A RWCU pump, old weld deficiencies

on the pump delayed the return to service. Concurrent with work

performed on the 1A pump, the IB RWCU pump was removed from service due

to high vibrations.

Delay in olanned maintenance of the 1A pump coupled with an emergent

material condition concern with the 1B pump resulted in operating Unit 1

without a functioning RWCU system. The licensee classified this as a

maintenance rule functional failure. Workers repaired the 1B RWCU pump

within 3 days and returned the RWCU system to service.

, Removing the RWCU system from service was not desirable since some

chemistry parameters can be adversely affected. The length of time the

'

RWCU system was removed from service did not result in any chemistry

parameters exceeding TS limits.

.

RWCU System Problems - Unit 2

In late October, operators detected a packing leak on the Unit 2 RWCU

containment outboard isolation valve (2-1201-5). Subsequent cycling of

the valve and tightening of valve packing reduced the leakage to

acceptable levels. However, on December 1, operators noted steam

emitting from the 2-1201-5 valve packing.

Seat leakage of the RWCU containment inboard isolation valve (2-1201-2)

coupled with the Jacking leak on 2-1201-5 resulted in a degraded

condition of the RWCU system. In order to perform repairs at power,

operators reduced Unit 2 power and removed RWCU from service. The valve

packing leak was temporarily corrected and Unit 2 returned to full power

operations. Action requests were written to address both material

condition issues for the upcoming outage. The RWCU system was out of

service for about 37 hours4.282407e-4 days <br />0.0103 hours <br />6.117725e-5 weeks <br />1.40785e-5 months <br /> and TS li. dts of chemistry parameters were

not exceeding .

l Gland Seal Condenser Level Control Valve (LCV) Problems

On November 1, operators received control room alarms indicating a

failure of the "B" gland steam condenser LCV (1-5404B). The operators

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reduced Unit 1 power and placed the "A" (1-5404A) LCV in service.

Workers replaced a ri) ped diaphragm in the "B" LCV air operator and

identified that both _CV controllers had 3roblems maintaining the proper

level in the condenser. Also, the drain leader from the "A" gland seal

condenser was found to have been plugged.

Workers repaired the controller and returned the "B" LCV to service.

The "A" LCV remained out of service until an inspection of the drain

header could be performed. However, on November 27, o]erators received

control room alarms indicating additional problems wit 1 the "B" LCV.

Workers identified the "B" LCV air operator had broken hold down bolts.

4

This resulted in the air operator being displaced from the valve yoke

, and caused the LCV to close. Workers replaced the broken bolts. ,

,

The failures of the Unit 1 gland steam condenser LCVs although not

safety significant, required operators attention to be diverted from

,

monitoring the unit. This condition had the potential to spread

contamination from the main turbine seals. On several occasions,

operators were re

condenser level. quired to take manual control of the gland seal

The local control station was in the feedwater heater

bay: an area of elevated radiation dose.

Foreion Material Found in Feedwater Heater System - Unit 2

l

~ On November 26, control room operators received feedwater heater drain l

le/e1 alarms indicating problems with the system LCVs during an increase

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in Unit 2 power. Operators discovered two air operated valves (A02- i

3508C and A02-3509A) were stuck open. Operators removed Unit 2 main

turbine from service to allow inspection of all six feedwater heater

drain LCVs.

The inspection identified that foreign material caused the two valves to

stick open. Foreign material was found in a third LCV. The foreign

i

material was believed to have originated from decaying grid work inside

moisture separator drain tanks upstream of the LCVs.

To effect repairs, the licensee was required to remove the unit from

operation affecting operational performance of the unit and some

increased dose to the workers.

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c. Conclusions

During the inspection period, the licensee experienced numerous

equipment performance problems. The licensee was still evaluating the

causes of the above equipment failures.

'

The equipment mentioned above was not classified as safety-related.

However, poor equipment performance necessitated operator intervention

prior to further equipment degradation. Additionally, the degraded

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equipment performance caused increased personnel radiation exposure to

repair and/or restore the affected equipment, re-directed maintenance

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! resources, delayed the start of scheduled maintenance activities. and

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impacted the operation of the units.

M8 Miscellaneous Maintenance Issues (92902)

M8.1 (Closed) Violation (50-254/265-96011-04): Three Examples of Workers Not

Properly Executing Work. The inspectors reviewed the licensee's

corrective actions for the personnel errors leading to this violation.

.

This item is closed.

I M8.2 (Closed) Violation (50-254/265-96002-08): Improper Storage of Emergency

Diesel Generator Air Start Motors. The cause of the improper storage of

! the air start motors was that the motors were not effectively coded to

, have planned maintenance (PM) performed on them. This PM would have

i

assured storage in a. moisture-free environment to prevent moisture

. buildup. In response to the NOV. the licensee performed an expanded

1- scope inspection of safety-related spare parts that were coded for PM

! activities to be performed while in stores. Of over 400 items screened,

the licensee identified approximately 35 items which were not coded

i

properly for a PM action. There were no cases in the sample inspected

j in which installation of faulty parts occurred, or failures of safety-

related ecuipment due to s Jare parts PM deficiencies. The licensee

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identifiec and corrected tle PM deficiencies and another administrative

{ weakness whereby the PM code was inappropriately ap)1ied to discontinued

,

or redesignated items. The inspectors determined t1e corrective action

j was adequate. This item is closed.

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III. Enaineerina '

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I E2 Engineering Support of Facilities and Equipment (IP 37551) '

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E2.1 Control Room Emeraency Ventilation System (CREVS)lnocerable and Outside

of the Desian Basis as Described in the UFSAR.

.

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a. Inspection Scone (IP 37551)

The inspectors reviewed the CREVS ino)erability which was reported to

the NRC on October 28, 1996, via the ENS phone line. The inspectors

used the TS, the UFSAR, the licensee's operability assessment, various

regulatory guides, the standard review plan on control room

habitability, and completed surveillance tests in the review. In

addition, the inspectors interviewed system engineers and licensee

management and attended plant on-site review committee (PORC) meetings

on the subject. The inspectors also observed portions of the

maintenance and surveillance activities during repair and restoration of

the system to an operable status.

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b. Observations and Findinas

On October 8, 1996, the licensee initiated PIF 96-2892 to document an

issue found at Dresden for review at Quad Cities. The issue concerned

TS surveillance requirement 4.8.D.5.c which required that once every

18 months, verification that the control room Jositive pressure was

maintained at greater than or equal to 1/8 inc1 water gauge relative to

adjacent areas during system operation at a flow rate less than or equal ,

to 2000 scfm. This particular surveillance requirement was new as of I

September 24, 1996, when new TS for Quad Cities were implemented. At i

the time of implementation, all new TS requirements for surveillance  !

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were required to be current and completed. l

l

After taking differential pressure measurements supplemental to the

measurements of the current surveillance procedure, the licensee

identified that the surveillance procedure was inadequate because the

control room differential pressure with respect to all adjacent areas I

was not measured. Engineers found that the required 1/8 inch positive

pressure in the control room was not met with respect to the cable

<

s3 reading room. The licensee identified eight additional adjacent areas

i

t1at needed to be included in the surveillance. On October 28, 1996,

the CREVS was declared inoperable, reported the condition to the NRC,

and entered the 7-day Limiting Condition for Operation. The inspectors

determined that the system had been inoperable since at least the

implementation of the new TS on September 24, 1996, since the as-found

condition was not in conformance with the TS and the required test had

not been performed prior to November 3, 1996. The inspectors concluded

that this was an Apparent Violation of TS 3.8.D.1, since the system was

inoperable for a period greater than allowed by the 7-day LCO while both

units were in Mode 1.

The licensee identified a discrepancy between the requirements of the TS

surveillance and the UFSAR description. Technical Specification 4.8.D.5.c required verification of the differential pressure between the

control room and adjacent areas, while the UFSAR (Section 6.4) stated

that the control room emeraency zene should be maintained at a 1/8 inch

Jositive pressure. The control room emergency zone was defined in the

JFSAR as the main control room, cable spreading room, auxiliary electric

equipment room, and the train "B" heating, ventilation, and air

conditioning (HVAC) equipment room. Differential pressure measurements

taken between the control room emergency zone and the adjacent areas

revealed that some areas were at a negative pressure and that some

areas, while positive, could not meet 1/8 inch design basis.

The inspectors reviewed the original design modification that installed

the CREVS and determined that testing for Modification M04-1/2-82-02

completed on April 16,1985, had not measured differential pressure

between the control room emergency zone and adjacent areas and therefore

failed to ensure UFSAR Section 6.4.4.1 criteria were met. The

inspectors concluded that both the modification test and subsequent

surveillance tests of the CREVS were inadequate to ensure that the

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. system would perform'its design basis function as described in the
UFSAR. The inspectors consider this an Apparent Violation of  !'

l 10 CFR Part 50, Appendix B, Criterion XI, " Test Control."

The UFSAR stated that the purpose of maintaining Jositive pressure in i

.

the control room emergency zone was to minimize t1e transfer of toxic or  !

i

!

radioactive gases into the control room (Section 6.4.2.4). Chapter 15 ,

of the UFSAR described the control- room dose calculation which assumed  !

the in-leakage into the control room emergency zone was 259.3 standard

cubic feet per minute (scfm).  !

The licensee sealed the CREVS ductwork and plugged leakage pathways into

the control room eme m ncy zone. A final set of differential pressure

readings concluded that while the control room had been restored to

1/8 inch positive pressure with respect to all adjacent areas, other

sections of the control room emergency zone remained at a negative  !

pressure. I

In addition to the repairs, the licensee performed a control room dose

calculation to determine how much in-leakage into the control room

emergency zone would result in failure to meet General Design Criteria (GDC) 19 of 10 CFR Part 50, Appendix A which sets limits for the

radiation dose operators can receive during an accident. Concurrently, ,

the licensee performed a test to measure the in-leakage. The measured' '

in-leakage was 275 plus or minus 99 scfm. an amount greater than that

assumed in the UFSAR.

The licensee performed a new control -room dose calculation (NUS

calculation number 6200.001-M-04) using the measured in-leakage. The

calculation methodology was different from that described in the UFSAR

Section 15.6.5. It used dose conversion factors from International

Committee on Radiation Protection (ICRP) 30. took credit for suppression

pool scrubbing of iodine (Standard Review Plan (SRP) 6.5.5), and used a

different secondary containment effluent leakage rate (4 volumes per

day). The combined effect of these differences resulted in a lower

calculated dose to the thyroid (12.5 rem) for control room personnel

when compared to the UFSAR calculation (29.4 rem).

The licensee used the results of the new control room dose calculation

and the completed control room differential pressure surveillance tesi

as the basis to declare the CREVS operable and exit the LCO on

November 3, 1996. The written operability assessment declared the

system fully operable and not degraded. Corrective actions described in

LER 50-254/96-022, dated November 25, 1996, included a revision of the

control room habitability study and new submittal to the NRC but had not

included plans to restore the plant to the original design basis as

described in the UFSAR.

The inspectors concluded that several discrepancies continued to exist

between the UFSAR and plant conditions after the licensee determined

that the CREVS was operable on November 3. On November 27, 1996, the

licensee informed the inspectors that as of November 26. the licensee

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planned to restore the system to its original design basis, while  !

pursuing an update to the control room habitability study. At the end
of the inspection period, the licensee developed a schedule for l

3 restoring the CREVS to its design bases, l

i

From November 3, when the CREVS was declared operable, to November 26, 1

4

the licensee did not plan to restore the CREVS to correct the identified l

UFSAR discrepancies. This de facto change in the facility was subject  !

to 50.59 review. Failure to perform this required evaluation was an-

i

,

Apparent Violation of 10 CFR 50.59, " Changes, Tests, and Experiments."

i

c. Conclusion

'

The inspectors concluded that the licensee had failed to ensure that I

!

i testing associated with the CREVS was adequate to verify that the system -  ;

could perform as described in the UFSAR. The licensee's actions after

identifying this inadequacy appeared to be technically adequate to

ensure operability of the system in that radiation exposure to control  !

rcom operators would not have exceeded GDC 19 limits. However, the i

i licensee had not properly im]lemented the procedures re  !

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regulations for evaluating clanges to the design basis. quired by the

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E2.2 Engineerino Review of Post Modification Testino Reveals Deficiencies )

.

, a. Insoection Scoce

The inspectors reviewed the circumstances surrounding the licensee's

1

f failure to adeguately test equipment after design modification. The l

inspectors reviewed PIFs and licensee reports, interviewed engineers and

]; engineering management, and attended several PORC meetings.

b. Observations and Findings

.

In November 1996, the licensee identified an issue regarding improper

i closure of a review of modifications conducted in 1993. In response to

a violation cited by the NRC in inspection report 50-254/265-93012, the

licensee committed to review a sample of old modifications for  !

i appropriate post modification testing. That review of 31 modifications l

was completed in October 1993 but produced 6 operability concerns and

! numerous other issues. The review questioned whether the operability

concerns were properly closed and if the scope had been expanded.

4

The licensee formed a team to review the issue. Three PIFs (96-3199,

-

96-3612, 96-3229) were generated which identified modifications that had

testing deficiencies. The licensee wrote and performed tests to address
the deficiencies. In addition, the licensee expanded the scope of the

1 review of old modifications.

,

The ins)ectors planned to inspect the results of the licensee's review

after t1e completion of the additional scope. This is considered to be

Inspector Followup Item (50 254/265-96017 05(DRS)).

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c. Conclusion  !

The inspectors noted that the licensee's response to the issue was

prompt and appeared to be comprehensive. The inspectors will review the

licensee's corrective actions to the identified deficiencies upon

completion.

E3 Engineering Procedures and Documentation

E3.1 Technical Soecification Review

a. Insoection Scooe (37551)

The inspectors compared the licensee's surveillance procedures to I

Section 4.8.D of TS to determine if all TS surveillance requirements for 1

the CREVS were implemented into procedures. l

,

b. Observations and Findinos

In answering the inspectors' questions concerning testing Jerformed to

meet the requirements of TS' 4.8.0, the licensee informed t1e inspectors

that a procedure was not in place to meet requirement TS 4.8.D.4. Quad l

Cities Technical Staff procedure (0 CTS) 440-03, " Control Room Emergency

Filtration System (CREFS) Removal of Charcoal Adsorber Test Canister,"

Revision 3, had not adequately addressed the TS. Specifically, TS  ;

4.8.D.4 required the licensee to remove a sample of charcoal adsorber  :

for testing after CREFS exceeded 720-hours operating time. I

I

However, the licensce had not tracked the o)erating hours of the CREFS

and was not readily able to determine the CREFS operating history. The

licensee documented this condition on PIF 96-3413 and were attempting to 1

determine the operating time of CREFS using operating logs. The i

licensee confirmed the 720-hour operating history was not exceeded.

c. Conclusions

The ins)ectors identified a failure to incorporate TS requirements into

applica)le surveillance procedures which is a Violation (50 254/265-

96017-06) of 10 CFR Part 50, Appendix B, Criterion XI, " Test Control."

E3.2 Control Room Emeroency Ventilation System Ooerability Determination

a. Insoection Scoce (37551)

The inspectors reviewed the licensee's operability evaluation for the

CREVS, including portions of the control room habitability study

calculation. The inspectors also reviewed licensee documentation used

for testing in-leakage into the control room emergency zone, operating

procedures and applicable regulatory guides. The inspectors also

reviewed Section 6.4.1.1 of the UFSAR.

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b. Observations and Findinas

Or October 27, engineering determined the existing control room

configuration was unable to meet Section 6.4.1.1 of the UFSAR. This

section required the control room emergency zone be pressurized to at

least +1/8 inch differential pressure (d/p) with respect to adjacent i

areas. Engineering determined the CREVS could not meet the design  !

functions and operations declared the CREVS inoperable on October 28.

The inspectors reviewed various documents associated with this issue and

noted weaknesses in the licensees approach for determining operability

of the CREVS.

i. Iodine Scrubbino Methodoloav

The licensee performed an operability evaluation and determined

4

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the CREVS was operable based on a calculation of thyroid dose to

o)erators and measured control room emergency zone in-leakage.

Tie measured in-leakage was greater than the in-leakage assumed in

the UFSAR. The calculation concluded thyroid doses were below

10 CFR Part 50 Appendix A, Criterion 19 limits. The calculation

adopted new methodologies not previously utilized in the original

control room habitability study referenced in the UFSAR, including

removal of iodine by the torus.

I

Standard Review Plan (SRP) 6.5.5 allowed licensees to utilize

iodine scrubbing by the torus provided specific criteria were met.

Criterion II.3 of SRP 6.5.5, required licensees maintain charcoal

filters to the minimum level in Regulatory Guide (RG) 1.52,

Table 2. Table 2 required laboratory tests for a representative

filter sample meet less than 1 percent penetration. However,

TS 4.7.P.2.b. required the standby gas treatment system (SBGTS)

filter sample meet less than 10 percent penetration. The

inspectors considered the licensee had not met the provisions

allowed by SRP 6.5.5 for the iodine removal methodology. This is

considered an Inspector Followup Item (50 254/265-96017-07)

pending further NRC review.

ii. Station Buildino Ventilation Status Post-Accident

The licensee determined that a positive d/p could not be

maintained in the control room emergency zone without securing

Service Building Ventilation (SBV). The licensee changed OCOP

5750-09, "CREVS Operating Procedure," and OCOS 5750-02, "CREFS

Monthly Test," to ensure SBV was secured to maintain a positive

d/p in the control room emergency zone.

The inspectors questioned whether the licensee could take credit

for conditions established by manual intervention of a nonsafety-

related piece of equipment if it can affect safety-related

equipment during post accident conditions. The inspectors noted

SBV will be lost during a loss of offsite power (LOOP) concurrent

24

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.

,

with a loss of coolant accident (LOCA) but not during a LOCA

without LOOP unless secured by manual intervention. The

i

inspectors consider this an Inspector Followup Item (50-254/265-

96017-08) pending further NRC review.

iii. Reactor Power level Assumed in the Control Room Dose Calculation

"

The inspectors noted that the control room dose calculation had

, assumed that the reactor power level at the time of the accident

was 100 percent core thermal power. Both the calculation

.

' described in the UFSAR and the calculation performed for the

o)erability determination used 100 percent core thermal power.

i-

T1e inspectors questioned the licensee if the evaluation should

-

be done under the assumption that the reactor was operating at

-

'

102 percent core thermal )ower, as done in the LOCA analysis. The

licensee responded that t1is particular assumption would be re-

evaluated prior to performing the calculations for submittal to

.

the NRC. The inspectors consider this an Inspector Followup Item

(50 254/265-96017 09) pending further NRC review.
c. Conclusions

I The ins)ectors identified the above weaknesses in the licensee's

!

approac1 for determining control room operability in post accident -

situations. These issues were considered Inspector Followup Items i

"

pending further NRC review.

E8 Hiscellaneous Engineering Issues (92902)

.1

l E8.1 (Closed) Licensee Event Report (LER) (50-265/95006): Motor Control

i Center 29-2 Main Feed Breaker Tripped Due to Inadequate Trip Setting.

As documented in Inspection Reports 50-254/265-95007 and 95011, the
events which resulted in generation of LER 50-265/95006 were the subject

j of an NRC enforcement conference held on November 25, 1995. This LER is

l closed.

,

, E8.2 (Closed) Insoection Followuo Item (50-254/265-94004-07): Prioritization

of Work Requests. As documented in IR 50-254/265-94004, the work

. control process was burdened by such a large number of nuclear work

j requests (NWRs) that only high priority corrective maintenance items

.

could be worked. In addition, there was no central focus on

establishing equipment priorities.

t

As documented in IR 50-254/265-96010, the inspectors reviewed the

licensee s work control process and determined that a revised work

control rocess was in place which utilized both system engineers and

lead uni planners to prioritize corrective maintenance activities.

This Inspection Followup Item is closed.

i

E8.3 (Closed) LER (50-254/94017): Banked Position Withdrawal Sequence Rules

J Violated Since October 1991 Due To Training, Procedure, and Work

Practice Deficiencies In The Nuclear Engineering Group. As discussed in

$ 25

,

-d

'

+

-

-

1

\

IR 50-254/265-94028. Unresolved Item (URI) 50-254/265-94028-01 was

opened following discovery by the licensee that some control rods were

withdrawn in the incorrect sequence during reactor startups since

October 1991. This LER is administratively closed due to tracking it as

URI 94028-01. The URI is still open pending inspector review.

E8.4 (Closed) Unresolved Item 50-254/265-96014-05): Torus Baseplate Bolt

Inconsistencies Identified by the Inspector. The inspectors had

)

identified inconsistencies in the bolting on the torus system saddle'

sup) ort baseplates. The licensee engineers performed additional system

walcdowns and consulted with Duke Engineering and Services to provide an

engineering assessment to determine whether the existing conditions were

acceptable. Duke Engineering and Services Document 1598.00043.014 was i

submitted to the licensee design engineering supervisor on November 4, i

1996. The inspectors reviewed this document and discussed the contents

'

with the engineers. In conclusion the documentation provided by the

licensee verified that the as-found condition had not invalidated the

design basis of the torus bolting. The inspectors verified that all

observed inconsistencies were bounded by the design calculations. This

item is closed.

IV. Plant Sucoort

R1 Radiological Protection and Chemistry Controls

R1.1 Material Condition Isst'es Mfoctina ExDosures

The inspectors revie%ed operator logs, PIFs, and viewed activities in

progress. The inspectors interviewed operators maintenance personnel,

and radiological protection staff.

Due to various material condition concerns (See Section M2.3), the

inspectors noted additlonal radiation exposures were received in an

effort to either repair deficient material condition issues or to

continue operating the unit with the deficient material condition. For

example, operators were required to manually control gland seal

condenser level when both level control valves for Unit 1 were

inoperable. The local control station was in the feedwater heater bay;

an area of elevated radiation dose. This dose plus the dose to workers .I

attempting repairs on the valves may have been avoided with better {

repair efforts to these valves which have a history of problems. Dose

rates in the area of the valves were much lower with the Unit shut down.

The licensee did take efforts to reduce dose once both level control

valves failed by lowering power in order to make the repairs. Operators

were also required to enter the Unit 2 containment at power to manually

isolate a reactor water cleanup valve because the remotely operated

valve had not provided proper isolation when a leak on another valve

occurred.

26

l

1

.

.

V. Manaaement Meetinos

X1 Exit Meeting Summary

The inspectors 3 resented the inspection results to members of licensee

management at t1e conclusion of the inspection on December 6, 1996. The

licensee acknowledged the findings presented. <

!

The inspectors asked the licensee whether any materials examined during the

inspection should be considered proprietary. No proprietary information was

identified. ]

,

I

l

1

1

1

27

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.- -..,

, *

,

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t

.

i

l PARTIAL LIST OF PERSONS CONTACTED

l

!

Comed

,

B. Pearce Station Manager ,

F. Famulari, Site OV Director r

4

J. Hutchinson, Engineering Manager -

.

F. Tsakeres, Radiation Chemistry Superintendent  :

l M. Wayland.. Maintenance Superintendent

i

1

INSPECTION PROCEDURES USED l

!

>

IP 40500: Effectiveness of Licensee Controls in Identifying, Resolving, and l

. Preventing Problems . l

IP 62703: Maintenance Observation

j

'

IP 64704: Fire Protection Program

IP 71707: Plant Operations

! IP 71714: Cold Weather Preparations

. IP 73051: Inservice Inspection - Review of Program

IP 73753: Inservice Inspection

-

IP 83729: Occupational Exposure During Extended Outages

i

IP 83750: Occupational Exposure

IP 92700: Onsite Followup of Written Reports of Nonroutine Events at Power

Reactor Facilities

IP 92902: Followup - Engineering

. IP 92903: Followup - Maintenance

j IP 93702: Prompt Onsite Response to Events at Operating Power Reactors

!

!

, 2

i

28

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.

}

!

ITEMS OPENED, CLOSED. AND DISCUSSED

Opened

50-254/265-96017-01 URI Joor understanding and control of licensing

] asis

50-254/265-96017-02 VIO use of incorrect bolt material in RHRSW LP pumps

50-254/265-96017-03 NCV Unit 2 operated past 30 days allowed by TS

50-254/265-96017-04 VIO failure to report prohibited plant condition

within 30 days

50-254/265-96017-05 IFI engineering review of post modification testing

reveals deficiencies

50-254/265-96017-06 VIO failure to incorporate TS requirements into  ;

applicable surveillance procedures

50-254/265-96017-07 IFI iodine scrubbing methodology

50-254/265-96017-08 IFI station building ventilation status post-

accident

50-254/265-96017-09 IFI reactor power level assumed in the control room

dose calculation

_C_l? sed

50-254/265-94004-23 URI reactor vessel temperatures not recorded during

cooldown

50-254-94011 LER control cod L-11 failed to scram during rod time

testing i

50-254/265-94017-01 VIO violation of procedure adherence, test control,  !

and corrective actions associated with failure

of a control rod scram during testing

50-254/265-96011-04 VIO three examples of workers not properly executing

work

50-254/265-96002-08 VIO improper storage of EDG air start motors

50-265/95006 LER MCC 29-2 main feed breaker tripped due to

inadequate trip setting

50-254/265-94004-07 IFI 3rioritization of work requests ,

50-254/94017 LER Janked position withdrawal sequence rules  !

violated since October 1991 due to training,  ;

procedure, and work practice deficiencies in the

nuclear engineering group

50-254/265-96014-05 URI torus baseplate bolt inconsistencies identified

by the inspector

29

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'

.

i

.

LIST OF ACRONYMS USED

'

CFR - Code of Federal Regulations

'

CREFS - Control Room Filtration System

CREVS - Control Room Emergency Ventilation System

4 CST - Central Standard Time

d/p -

differential pressure

DET -

Diagnostic Evaluation Team

DRP - Division of Reactor Projects

EA -

Enforcement Action

'

EDGCW - Emergency Diesel Generator Cooling Water

ENS - Emergency Notification System
FME -

Foreign Material Exclusion

! GDC - General Design Criteria

! HP - High Pressure

. HPCI - High Pressure Coolant Injection System

-

HVAC - Heating, ventilation, and air conditioning

,

IDNS - Illinois Department of Nuclear Safety

i IR -

Inspection Report

i LC0 -

Limiting Condition for Operation

LCV - Level Control Valve

LER - Licensee Event Report

i LOCA -

Loss of Cooling Accident

i LOOP - Loss of Offsite Power

,

'

LP - Low Pressure

LPCI -

Low Pressure Coolant Injection

4 MMD - Mechanical Maintenance Department

i MWe - Megawatts Electric

NRR - NRC Office of Nuclear Reactor Regulation

. NWR - Nuclear Work Request

PDR -

Public Document Room

. PIF - Problem Identification Form

1

' PM - Planned Maintenance

PMT -

Post Maintenance Testing

PORC -

Plant On-site Review Committee

i

OCOP -

Quad Cities Operating Procedure

QCOS - Quad Cities Operating Surveillance

'

.

OCTS - Quad Cities Technical Staff Procedure

t RG -

Regulatory Guide

. RHR - Residual Heat Removal

!

RHRSW - Residual Heat Removal Service Water

i RPM -

revolutions per minute

2

RWCU - Reactor Water Clean Up

! SBV - Service Building Ventilation

SCFM -

Standard Cubic Feet per Minute

SRP - Standard Review Plan
TS - Technical Specification

i

'

UFSAR - Updated Final Safety Analysis Report

UHS - Ultimate Heat Sink

j URI -

Unresolved Item

i

$

) 30

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