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Category:Inspection Report
MONTHYEARIR 05000352/20240122024-10-17017 October 2024 Commercial Grade Dedication Inspection Report 05000352/2024012 and 05000353/2024012 IR 05000352/20244202024-09-16016 September 2024 – Security Baseline Inspection Report 05000352/2024420 and 05000353/2024420 IR 05000352/20250102024-09-10010 September 2024 Information Request for Quadrennial Baseline Comprehensive Engineering Team Inspection; Notification to Perform Inspection 05000352/2025010 and 05000353/2025010 IR 05000352/20230022024-09-0404 September 2024 Reissued Integrated Inspection Report 05000352/2023002 and 05000353/2023002 IR 05000352/20240052024-08-29029 August 2024 Updated Inspection Plan for Limerick Generating Station, Units 1 and 2 (Report 05000352/2024005 and 05000353/2024005) IR 05000352/20240022024-08-12012 August 2024 Integrated Inspection Report 05000352/2024002 and 05000353/2024002 IR 05000352/20243022024-05-20020 May 2024 Revised Initial Operator Licensing Examination Report 05000352/2024302 and 05000353/2024302 IR 05000352/20240012024-05-0707 May 2024 Integrated Inspection Report 05000352/2024001 and 05000353/2024001 IR 05000352/20244012024-03-19019 March 2024 Security Baseline Inspection Report 05000352/2024401 and 05000353/2024401 IR 05000352/20240102024-03-18018 March 2024 Biennial Problem Identification and Resolution Inspection Report 05000352/2024010 and 05000353/2024010 IR 05000352/20230062024-02-28028 February 2024 Annual Assessment Letter for Limerick Generating Station, Units 1 and 2 (Reports 05000352/2023006 and 05000353/2023006) IR 05000352/20243012024-02-0202 February 2024 Initial Operator Licensing Examination Report 05000352/2024301 and 05000353/2024301 IR 05000352/20240112024-01-31031 January 2024 Information Request to Support Post-Approval Site Inspection for License Renewal; Inspection Report 05000352/2024011 IR 05000352/20230042024-01-31031 January 2024 Integrated Inspection Report 05000352/2023004 and 05000353/2023004 IR 05000352/20230102024-01-11011 January 2024 Age-Related Degradation Report 05000352/2023010 and 05000353/2023010 IR 05000352/20234012023-12-21021 December 2023 Cybersecurity Inspection Report 05000352/2023401 and 05000353/2023401 IR 05000352/20230032023-10-27027 October 2023 Integrated Inspection Report 05000352/2023003 and 05000353/2023003 and Independent Spent Fuel Storage Installation Inspection 07200065/2023001 ML23297A1722023-10-24024 October 2023 Request for Information for a Biennial Problem Identification and Resolution Inspection; Inspection Report 05000352/2024010 and 05000353/2024010 IR 05000352/20235012023-10-17017 October 2023 Emergency Preparedness Biennial Exercise Inspection Report 05000352/2023501 and 05000353/2023501 IR 05000352/20230052023-08-31031 August 2023 Updated Inspection Plan for Limerick Generating Station, Units 1 and 2 (Report 05000352/2023005 and 05000353/2023005) IR 05000352/20230012023-04-28028 April 2023 Integrated Inspection Report 05000352/2023001 and 05000353/2023001 IR 05000352/20220062023-03-0101 March 2023 Annual Assessment Letter for Limerick Generating Station, Units 1 and 2 (Reports 05000352/2022006 and 05000353/2022006) IR 05000352/20220042023-02-13013 February 2023 Integrated Inspection Report 05000352/2022004 and 05000353/2022004 IR 05000352/20234022023-02-0707 February 2023 Security Baseline Inspection Report 05000352/2023402 and 05000353/2023402 IR 05000352/20233012023-01-26026 January 2023 Initial Operator Licensing Examination Report 05000352/2023301 and 05000353/2023301 IR 05000352/20220032022-11-0707 November 2022 Integrated Inspection Report 05000352/2022003 and 05000353/2022003 IR 05000352/20224022022-10-18018 October 2022 Security Baseline Inspection Report 05000352/2022402 and 05000353/2022402 IR 05000352/20220052022-08-31031 August 2022 Updated Inspection Plan for Limerick Generating Station, Units 1 and 2 (Report 05000352/2022005 and 05000353/2022005) IR 05000352/20224012022-08-0303 August 2022 Material Control and Accounting Inspection Report 05000352/2022401 and 05000353/2022401 (Cover Letter Only) IR 05000352/20220022022-08-0101 August 2022 Integrated Inspection Report 05000352/2022002 and 05000353/2022002 IR 05000352/20220112022-06-30030 June 2022 Triennial Fire Protection Inspection Report 05000352/2022011 and 05000353/2022011 IR 07200065/20210012022-06-0909 June 2022 Independent Spent Fuel Storage Installation (ISFSI) NRC Inspection Report No. 07200065/2021001 and Exercise of Enforcement Discretion IR 05000352/20220012022-05-0404 May 2022 Integrated Inspection Report 05000352/2022001 and 05000353/2022001 IR 05000352/20220102022-03-0909 March 2022 Biennial Problem Identification and Resolution Inspection Report 05000352/2022010 and 05000353/2022010 IR 05000352/20210062022-03-0202 March 2022 Annual Assessment Letter for Limerick Generating Station, Units 1 and 2 (Reports 05000352/2021006 and 05000353/2021006) IR 05000352/20214012022-02-15015 February 2022 Security Baseline Inspection Report 05000352/2021401 and 05000353/2021401 IR 05000352/20210042022-02-0909 February 2022 Integrated Inspection Report 05000352/2021004 and 05000353/2021004 IR 05000352/20215012021-11-29029 November 2021 Emergency Preparedness Biennial Exercise Inspection Report 05000352/2021501 and 05000353/2021501 IR 05000352/20210032021-11-0404 November 2021 Integrated Inspection Report 05000352/2021003 and 05000353/2021003 IR 05000352/20214202021-10-0404 October 2021 NRC Inspection Report 05000352/2021420 and 05000353/2021420 IR 05000352/20213012021-09-16016 September 2021 Initial Operator Licensing Examination Report 05000352/2021301 and 05000353/2021301 IR 05000352/20210052021-09-0101 September 2021 Updated Inspection Plan for the Limerick Generating Station, Units 1 and 2 (Report 05000352/2021005 and 05000353/2021005) IR 05000352/20214022021-08-24024 August 2021 Security Baseline Inspection Report 05000352/2021402 and 05000353/2021402 IR 05000352/20210022021-08-10010 August 2021 Integrated Inspection Report 05000352/2021002 and 05000353/2021002 IR 05000352/20210012021-04-30030 April 2021 Integrated Inspection Report 05000352/2021001 and 05000353/2021001 IR 05000352/20210102021-03-0909 March 2021 Design Basis Assurance Inspection (Teams) Inspection Report 05000352/2021010 and 05000353/2021010 IR 05000352/20200062021-03-0303 March 2021 Annual Assessment Letter for Limerick Generating Station, Units 1 and 2 (Reports 05000352/2020006 and 05000353/2020006) IR 05000352/20200042021-02-0202 February 2021 Integrated Inspection Report 05000352/2020004 and 05000353/2020004 and Independent Spent Fuel Storage Installation Inspection Report 07200065/2020002 IR 05000352/20200152021-01-0404 January 2021 Temporary Instruction 2515/194 Inspection Report 05000352/2020015 and 05000353/2020015 IR 05000352/20200032020-11-0404 November 2020 Integrated Inspection Report 05000352/2020003 and 05000353/2020003 2024-09-04
[Table view] Category:Letter
MONTHYEARML24303A0902024-10-29029 October 2024 Operator Licensing Examination Approval IR 05000352/20240122024-10-17017 October 2024 Commercial Grade Dedication Inspection Report 05000352/2024012 and 05000353/2024012 RS-24-093, Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-10-10010 October 2024 Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests ML24274A2372024-10-0707 October 2024 – Supplemental Information Needed for Acceptance of Requested Licensing Action Regarding Primary Containment Leakage Technical Specifications ML24278A3022024-10-0404 October 2024 Supplement to License Amendment Request to Revise Technical Specifications and Exemption Request from Requirements of 10 CFR 50.62 ATWS Rule to Support the Digital Modernization Project Installation - Rev Unit 2 Technical Spec ML24275A2442024-10-0303 October 2024 Reassignment of the U.S. Nuclear Regulatory Commission Branch Chief, Division of Operating Reactor Licensing ML24263A0032024-09-27027 September 2024 Generation Station, Units 1 and 2 – Regulatory Audit Plan Supporting Review of the Component Interface Module System of the Limerick Digital Instrumentation and Controls License Amendment Request (EPID L-2022-LLA-0140) (Redacted) ML24243A0482024-09-19019 September 2024 Generation Station, Unit Nos. 1 and 2 - Schedule Update for License Amendment Request to Replace Existing Safety-Related Analog Control Systems with a Single Digital Plant Protection System ML24215A4042024-09-18018 September 2024 Request for Withholding Information from Public Disclosure IR 05000352/20244202024-09-16016 September 2024 – Security Baseline Inspection Report 05000352/2024420 and 05000353/2024420 RS-24-090, Response to Request for Additional Information - Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds2024-09-12012 September 2024 Response to Request for Additional Information - Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds IR 05000352/20250102024-09-10010 September 2024 Information Request for Quadrennial Baseline Comprehensive Engineering Team Inspection; Notification to Perform Inspection 05000352/2025010 and 05000353/2025010 ML24255A8642024-09-0606 September 2024 Rscc Wire & Cable LLC Dba Marmon Industrial Energy & Infrastructure - Part 21 Retraction of Final Notification IR 05000352/20230022024-09-0404 September 2024 Reissued Integrated Inspection Report 05000352/2023002 and 05000353/2023002 IR 05000352/20240052024-08-29029 August 2024 Updated Inspection Plan for Limerick Generating Station, Units 1 and 2 (Report 05000352/2024005 and 05000353/2024005) ML24241A1952024-08-28028 August 2024 License Amendment Request for Modification to Technical Specification 3.6.1.2 and Main Steam Isolation Valve Leakage Rate Requirements ML24239A3972024-08-23023 August 2024 Rssc Wire & Cable LLC Dba Marmon - Part 21 Final Notification - 57243-EN 57243 ML24163A3902024-08-14014 August 2024 Request for Withholding Information from Public Disclosure IR 05000352/20240022024-08-12012 August 2024 Integrated Inspection Report 05000352/2024002 and 05000353/2024002 ML24220A2392024-08-12012 August 2024 Correction to Technical Specification Page 3/4 3-11 in Amendment No. 225 ML24222A6772024-08-0909 August 2024 Response to Request for Additional Information for Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition ML24204A0712024-07-29029 July 2024 Issuance of Amendment Nos. 263 and 225 Technical Specifications for Main Steam Line Tunnel Temperature ML24208A1592024-07-25025 July 2024 Regulatory Audit Plan Supporting Review of the System Development Portion of Limerick Digital Instrumentation and Controls License Amendment Request (EPID L-2022-LLA-0140) - Non-Proprietary ML24208A0962024-07-25025 July 2024 57243-EN 57243 - Rssc Wire & Cable LLC, Dba Marmon - Part 21 Notification ML24201A1662024-07-19019 July 2024 Response to Request for Additional Information for License Amendment Request for Proposed Changes to the Technical Specification Isolation Actuation Instrumentation Tables and New Turbine Enclosure Main Steam L ML24199A1842024-07-15015 July 2024 RAI-LAR for Limerick EPID: L-2024-LLA-0079- Use This Version RS-24-070, Independent Spent Fuel Storage Installation, Nine Mile Point, Units 1 and 2, Quad Cities, Units 1 and 2, R. E. Ginna - Nuclear Radiological Emergency Plan Document Revisions2024-07-12012 July 2024 Independent Spent Fuel Storage Installation, Nine Mile Point, Units 1 and 2, Quad Cities, Units 1 and 2, R. E. Ginna - Nuclear Radiological Emergency Plan Document Revisions ML24180A1572024-06-28028 June 2024 Request to Return and Replace WEC Documents (EQ-EV-386-GLIM, EQ-QR- 433-GLIM, and APP-GW-GLR-611), to Meet 10CFR2.390 Request to Withdraw from Public Disclosure Requirements ML24170A7702024-06-20020 June 2024 Individual Notice of Consideration of Issuance of Amendments to Renewed Facility Operating Licenses, Proposed No Significant Hazards Consideration Determination, Opportunity for Hearing(Epid L-2024-LLA-0079) LTR 05000352/LER-2024-003, Core Operating Limits Report Thermal Limit Exceeded for Unit 1 Fuel Bundle GGK1232024-06-18018 June 2024 Core Operating Limits Report Thermal Limit Exceeded for Unit 1 Fuel Bundle GGK123 ML24166A1142024-06-14014 June 2024 Response to Requests for Additional Information (RAIs 15 Through 23) for License Amendment Request to Revise the Licensing and Design Basis to Incorporate the Replacement of Existing Safety-Related Analog Control Systems RS-24-061, Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations2024-06-14014 June 2024 Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations ML24165A2642024-06-13013 June 2024 License Amendment Request for Proposed Changes to the Technical Specification Isolation Actuation Instrumentation Tables and New Turbine Enclosure Main Steam Line Tunnel Temperature TS 3/4.7.9 05000352/LER-2024-001, Leakage for the Unit 1 `B Outboard Main Steam Isolation Valve Exceeded Technical Specification Limit2024-06-10010 June 2024 Leakage for the Unit 1 `B Outboard Main Steam Isolation Valve Exceeded Technical Specification Limit 05000352/LER-2024-002, Invalid Actuation Due to a Trip of 1B Reactor Protection System Circuit Breaker2024-06-10010 June 2024 Invalid Actuation Due to a Trip of 1B Reactor Protection System Circuit Breaker ML24151A2012024-06-10010 June 2024 Request for Withholding Information from Public Disclosure ML24151A2882024-06-10010 June 2024 Request for Withholding Information from Public Disclosure ML24150A0242024-05-29029 May 2024 Notification of Commercial Grade Dedication Inspection (05000352/2024012 and 05000353/2024012) and Request for Information ML24149A2112024-05-28028 May 2024 Supplement to License Amendment Request to Revise Technical Specifications and Exemption Request from Requirements of 10CFR50.62 ATWS Rule to Support the Digital Modernization Project Installation ML24079A0762024-05-23023 May 2024 Issuance of Amendments to Adopt TSTF 264 IR 05000352/20243022024-05-20020 May 2024 Revised Initial Operator Licensing Examination Report 05000352/2024302 and 05000353/2024302 RS-24-055, 2023 Corporate Regulatory Commitment Change Summary Report2024-05-17017 May 2024 2023 Corporate Regulatory Commitment Change Summary Report IR 05000352/20240012024-05-0707 May 2024 Integrated Inspection Report 05000352/2024001 and 05000353/2024001 ML24124A0432024-05-0303 May 2024 Response to Requests for Additional Information (RAIs 9 Through 14) for License Amendment Request to Revise the Licensing and Design Basis to Incorporate the Replacement of Existing Safety-Related Analog Control Systems with RS-24-038, Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds2024-05-0202 May 2024 Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds RS-24-041, Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-04-30030 April 2024 Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests ML24114A3222024-04-23023 April 2024 Supplement to License Amendment Request to Revise the Licensing and Design Basis to Incorporate the Replacement of Existing Safety-Related Analog Control Systems with a Single Digital Plant Protection System (PPS) - Pivot to Unit ML24109A0702024-04-18018 April 2024 Supplement to License Amendment Request to Revise Technical Specifications and Exemption Request from Requirements of 10CFRC50.52 ATWS Rule to Support the Digital Modernization Project Installation . ML24093A0912024-04-17017 April 2024 Revised Estimated Review Completion Date Concerning License Amendment Request to Replace Existing Safety-Related Analog Control Systems with a Single Digital Plant Protection System ML24106A1832024-04-15015 April 2024 Submittal of Changes to Technical Specifications Bases 2024-09-06
[Table view] |
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{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION ary 5, 2013
SUBJECT:
LIMERICK GENERATING STATION - NRC INTEGRATED INSPECTION REPORT 05000352/2012005 AND 05000353/2012005
Dear Mr. Pacilio:
On December 31, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Limerick Generating Station, Units 1 and 2. The enclosed inspection report documents the inspection results, which were discussed on January 11, 2013 with Mr. T.
Dougherty, Site Vice President, and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
This report documents two findings of very low safety significance (Green). One of these findings was determined to involve a violation of NRC requirements. Additionally, two licensee-identified violations, which were determined to be of very low safety significance, are listed in this report. However, because of the very low safety significance, and because they are entered into your corrective action program, the NRC is treating these findings as non cited violations (NCVs), consistent with Section 2.3.2 of the NRC Enforcement Policy. If you contest any NCVs in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.:
Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Limerick Generating Station. In addition, if you disagree with the cross-cutting aspect assigned to any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC Resident Inspector at Limerick Generating Station.
In accordance with 10 Code of Federal Regulations (CFR) 2.390 of the NRCs Rules of Practice, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). ADAMS is accessible from the NRC website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Mel Gray, Chief Reactor Projects Branch 4 Division of Reactor Projects Docket Nos.: 50-352, 50-353 License Nos.: NPF-39, NPF-85
Enclosure:
Inspection Report 05000352/2012005 and 05000353/2012005 w/Attachment: Supplemental Information
REGION I==
Docket Nos.: 50-352, 50-353 License Nos.: NPF-39, NPF-85 Report No.: 05000352/2012005 and 05000353/2012005 Licensee: Exelon Generation Company, LLC Facility: Limerick Generating Station, Units 1 & 2 Location: Sanatoga, PA 19464 Dates: October 1, 2012 through December 31, 2012 Inspectors: E. DiPaolo, Senior Resident Inspector J. Hawkins, Resident Inspector A. Rosebrook, Senior Project Engineer J. Caruso, Senior Operations Engineer R. Nimitz, Senior Health Physicist P. Kaufman, Senior Reactor Inspector S. Barr, Senior Emergency Preparedness Specialist C. Newport, Operations Engineer J. DeMarshall, Senior Operations Engineer (In-Training)
Approved By: Mel Gray, Chief Reactor Projects Branch 4 Division of Reactor Projects Enclosure
SUMMARY OF FINDINGS
IR 05000352/2012005; 05000353/2012005; 10/01/2012 - 12/31/2012; Limerick Generating
Station, Units 1 and 2; Licensed Operator Requalification and Post-Maintenance Testing.
This report covered a three-month period of inspection by resident inspectors and announced inspections performed by regional inspectors. The inspectors identified two findings of very low safety significance, one of which was a non-cited violation (NCV). The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). The cross-cutting aspects for the findings were determined using IMC 0310, Components Within Cross-Cutting Areas. Findings for which the SDP does not apply may be Green, or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NRC Technical Report Designation (NUREG)-1649,
Reactor Oversight Process, Revision 4, dated December 2006.
Cornerstone: Mitigating Systems
- Green.
The inspectors identified a Green finding of Exelon procedure TQ-AA-150,
Operator Training Programs, and TQ-AA-155, Conduct of Simulator Training and Evaluation, based on a determination that the minimum number of scenarios required for simulator re-examination was not administered following a crew failure of the dynamic simulator scenario portion of the annual operating exam during week two of the 2012 Licensed Operator Requalification Training (LORT) Annual Operating Test. Exelon staff entered this finding into their corrective action program (CAP) (IR 1437839), conducted a prompt investigation, assigned an action to complete the annual operating exam scenario set for the crew in question, and initiated an Apparent Cause Evaluation (ACE).
The inspectors determined that the finding was more than minor because it was associated with the Human Performance attribute of the Mitigation Systems cornerstone and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage).
The risk importance of this issue was evaluated using IMC 0609, Appendix I, Licensed Operator Requalification Significance Determination Process (SDP). Based on this screening criteria, the finding (inadequate retest) was characterized by the SDP as having very low safety significance (Green) because crew remediation was conducted and a partial re-evaluation performed. This finding had a cross-cutting aspect in the area of Human Performance, Work Practices, because Exelon did not ensure that personnel followed procedures [H.4(b)]. Specifically, the simulator scenario re-exam administered following a failed Annual Operating Test did not meet procedure requirements for number of scenarios.
[H.4(b)]. (Section 1R11.3)
- Green.
A self-revealing Green NCV of Technical Specification 6.8.1, Administrative Controls-Procedures, was identified because Exelon did not implement procedure use and adherence requirements when workers changed the scope of work on emergency diesel generator (EDG) fuel oil day tanks and did not revise the work instructions when they determined that work could not be performed as written. This resulted in EDG D13 accruing approximately 40 hours of unplanned unavailability between December 14 and 16, 2012.
Exelon entered the issue into their CAP as IR 1453737, conducted a human performance review board, drained and flushed the tank to restore fuel oil quality, and initiated an ACE.
This finding was more than minor because it was associated with the Human Performance attribute of the Mitigating Systems cornerstone and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The finding was determined to be self-revealing because it was revealed through the receipt of alarms during operation which required no active and deliberate observation by the Exelon staff. The finding was determined to be of very low safety significance (Green) in accordance with Section A of Exhibit 2 of IMC 0609,
Appendix A, The Significance Determination Process for Findings at Power, because the finding did not represent an actual loss of function a single train for greater than the TS allowed outage time.
This finding had a cross-cutting aspect in the area of Human Performance, Work Practices, because Exelon did not ensure that personnel followed procedures [H.4(b)]. Specifically, work order procedural steps to clean the fuel oil tank were not completed as directed by the work order and a procedurally required change to written work instructions was not implemented when station personnel determined that the fuel oil tank cleaning would be based on the need to clean the tank as determined by tank inspection results. (Section 1R19)
Other Findings
Two violations of very low safety significance that were identified by Exelon personnel were reviewed by the inspectors. Corrective actions taken or planned by Exelon have been entered into Exelons CAP. These violations and corrective action tracking numbers are listed in Section 4OA7 of this report.
REPORT DETAILS
Summary of Plant Status
Unit 1 began the inspection period at 100 percent power. On October 29, during a period of high winds due to Storm Sandy, operators reduced power to approximately 49 percent in response to lowering main condenser vacuum and high grid voltage. Operators returned the unit to 100 percent power on October 30. Power was reduced to approximately 87 percent on October 31 to facilitate a follow-up control rod pattern adjustment. Power was returned to 100 percent on November 1. An additional power reduction to 93 percent and follow-up control rod pattern adjustment was performed on November 3. Operators returned power to 100 percent on November 4. On November 12, power automatically reduced to approximately 70 percent when single loop operation was entered following the trip of the A reactor recirculation pump.
The cause of the trip was the loss of the pumps adjustable speed drive (ASD) due to solid state controller failures. Operators further reduced power to approximately 36 percent per procedural requirements. Following troubleshooting and repair of the adjustable speed drive, operators restarted the A reactor recirculation pump on November 15 and restored power to 100 percent later that day. A power reduction to approximately 80 percent was performed on November 16 to facilitate a follow-up control rod pattern adjustment and power was returned to 100 percent later that day. On December 7, operators reduced power to approximately 20 percent to remove the main turbine from service (Maintenance Outage 1M53) to facilitate repairs to stop a steam leak on the 1A2 moisture separator manway cover, repairs to the main generator hydrogen seal system and repairs to a low pressure turbine bleeder trip valve. Following the repairs, the main turbine was returned to service and the generator was synchronized to the grid on December 9. Unit 1 was returned to 100 percent power on December 10. Unit 1 remained at or near 100 percent power for the remainder of the inspection period.
Unit 2 began the inspection period at 100 percent power. On October 5, operators reduced power to approximately 65 percent to facilitate planned main condenser circulating water box cleaning, control rod scram time testing, and a control rod pattern adjustment. Operators returned power to 100 percent on October 6. Power was reduced to approximately 90 percent on October 12 to facilitate a follow-up control rod pattern adjustment. Power was returned to 100 percent later that day. On October 29, during a period of high winds due to Storm Sandy, operators reduced power to approximately 21 percent in response to lowering main condenser vacuum and high grid voltage. Operators returned the unit to 100 percent power on October 31.
An additional power reduction to approximately 80 percent and follow-up control rod pattern adjustment was performed on November 1. Power was returned to 100 percent later that day.
Operators reduced power to approximately 90 percent on November 16 to facilitate a control rod pattern adjustment. Operators restored power to 100 percent later that day. On December 16, operators reduced power to approximately 81 percent facilitate main turbine valve testing, control rod fuel channel distortion testing, and to perform a control rod exercise. Unit 2 was returned to 100 percent on December 17. Unit 2 remained at or near 100 percent power for the remainder of the inspection period.
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
1R01 Adverse Weather Protection
Main article: IP 71111.01
Site Imminent Weather Conditions
a. Inspection Scope
During the approach of Storm Sandy to Montgomery County area, the inspectors attended storm preparation status meetings, reviewed site preparations for adverse weather, and reviewed preparations for plant damage assessment. The inspectors toured risk-significant and susceptible plant areas to verify the implementation of adverse weather preparation procedures and compensatory measures before the onset of adverse weather conditions. From October 29 until October 30, the inspectors observed plant response to the adverse weather and monitored Exelons damage assessment, review of emergency response capabilities, and corrective actions as a result of the storm. Documents reviewed for each section of this inspection report are listed in the Attachment.
b. Findings
No findings were identified.
==1R04 Equipment Alignment
.1 Partial System Walkdowns
Main article: IP 71111.04Q ==
a. Inspection Scope
The inspectors performed partial walkdowns of the following systems:
EDG D14 following return-to-service for a two year overhaul B control room emergency fresh air system when A control room emergency fresh air system was out-of-service for testing on December 11, 2012 Unit 1 scram discharge volume level transmitters with LT-047-1N012C found out-of-calibration (Issue Report (IR) 1447377)
Unit 1 seismic monitoring accelerometers with channel 1 failed (IR 1449120)
The inspectors selected these systems based on their risk-significance relative to the reactor safety cornerstones at the time they were inspected. The inspectors reviewed applicable operating procedures, system diagrams, the Updated Final Safety Analysis Report (UFSAR), technical specifications (TS), work orders, IRs, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have impacted system performance of their intended safety functions. The inspectors also performed field walkdowns of accessible portions of the systems to verify system components and support equipment were aligned correctly and were operable.
The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no deficiencies. The inspectors also reviewed whether Exelon staff had properly identified equipment issues and entered them into the CAP for resolution with the appropriate significance characterization.
b. Findings
No findings were identified.
.2 Full System Walkdown
Main article: IP 71111.04S
a. Inspection Scope
The inspectors performed a complete system walkdown of accessible portions of the Unit 2 fuel pool cooling system to verify the existing equipment lineup was correct. The inspectors reviewed operating procedures, surveillance tests, drawings, equipment line-up check-off lists, and the UFSAR to verify the system was aligned to perform its required safety functions. The inspectors also reviewed electrical power availability, component lubrication and equipment cooling, hangar and support functionality, and operability of support systems. The inspectors performed field walkdowns of accessible portions of the systems to verify system components and support equipment were aligned correctly and operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no deficiencies. Additionally, the inspectors reviewed a sample of related IRs and work orders to ensure Exelon appropriately evaluated and resolved any deficiencies.
b. Findings
No findings were identified.
==1R05 Fire Protection
.1 Resident Inspector Quarterly Walkdowns
Main article: IP 71111.05Q