ML18043A338

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Forwards LER#78-040/01X-1
ML18043A338
Person / Time
Site: Palisades Entergy icon.png
Issue date: 12/18/1978
From: Hoffman D
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To: James Keppler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML18043A339 List:
References
NUDOCS 7812210230
Download: ML18043A338 (3)


Text

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consumers Power company General Offices: 212 West Michigan Avenue, .Jackson, Michigan 49201

  • Area Code 517 788-0550 December 18, 1978 Mr James G Keppler Office of Inspection and Enforcement Region III US Nuclear Regulatory Commission 799 Roo.sevel t Road Glen Ellyn, IL 60137 DOCKET 50-255 - LICENSE DPR PALISADES PLANT - LER 78-040 On the reverse side is Revision 1 of Licensee Event Re-oort 78-040 which is reportable under Technical Specification 6.9.2.a.(2).

David P Hoffman (Signed)

David P Hoffman Assistant Nuclear Licensing Administrator CC: Director, Office of Nuclear Reactor Regulation Director, Office of Inspection and Enforcement REGULATO,n.v

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'* v.i -~~ b Jt--L COPY 781.221. Od--SC

~JPDATE' REPOR- PREVIOUS REPOR'I' DATE 12/12,.:78 Palisades NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (7*77)

LICENSEE EVENT REPORT CONTROi. BLOCK: ._I I

_....__._-------'--'-..,jj 6

0 (PLEASE PRINT OR TYPE ALI. REQUIRED INFORMATION!

CLl2J I I PI A I 1 I 1 101 o Io I - I oIo I o Io I o I . Io I o 101 4 I 1 1 J 1 1 1 101 I l

~S MJ I 7 8 9 LICENSEE COOE 14 LICENSE NUMBER 25 26 LICENSE TYPE JO 57 CAT SB ©s CON'T 0JJ 7 8

~~~;~~ L1.J© I 60 61 Cl 5 I oI o I o 12 I 5 I 5 (VI DOCKET NUMBER 68 69 1 I l  ! 2 I 81 7 I 8 EVENT DATE 74 I© I 11 2 I 1 I 8 I 7 18 10 75 REPORT DATE BO EVENT DESCRIPTION AND PROBABLE CONSEQUENCES (,°Q)

[§Jl] I During load reduction in prepa~tion for plant shutdown, the volume control tank was being vented to the waste gas surge tank in order to degas the PCS. Leakage from the surge tank resuJ,.ted in a gaseous release without the 15-day holdup time required by TS 3.9.17. Upon discovery VCT venting was stopped. Total activity release was 4.314 curie which

~I is 5,7 percent of the average annual release rate. No hazard to public

.I r;;"'l01 health or safety resulted.

7 s 9'----------------------------------------------~~~----~----------__J L..2...L!..J 80 s~5~~M c.\ cc"ou~i (,':;\ s3:~J.3e(,':;\ COMPONENT CODE COMP.

SUBC.QDE VALVE SUBl=,DDE IIill I Ml El~ IX I~ ~~ I A!C I CjU I Mj u1e 121@ ~@

7 8 9 10 ,, 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION*

~ LEAIRQ CVENTYEAR I 7 I 81 I I REPORT NO.

I 0141 01 1.....-1

. COOE

1. o I l! ~

TYPE

'to.

\:.Y REPORT NUMBER L=l L::J ACTION TAKEN FUTURE ACTION 21 22 oW:eiJT 23 s~~~~i~N 24 26 HOURS 27

$) Al.J:~iw~~T 28 29 F~~~B.

30 PRIME COMP.

SUPPLIER 31 32 COMPONENT 0

..

MANUFACTURE'CJ W@l.x.J@ W@) W Io 10 Io ft) I L!J@ l2!J~ ~@ I z I 9 I 91 _, I@

33 34 35 36 37 *o 41 42 ~ 4J " *7 CAUSE DESCRIPTION AND COAREC"rlVE ACTIONS @. An updated I The cause of this occurrence is still under evaluation.

report will be submitted by January 5, 1979.

1 o:ma ~9---------------------------------------------------------------------------------_j 80 .

METHOD OF

. 9THER STATUS @

FACILITY STATUS '!.POWER DISCOVERY A , .._DISCOVERY DESCRIPTION tJ2'

[ill] I DI@ I 019 10 l@I NtA I t...:J@I nnuruca1,,or l::::J 7

S AJTIVITY cd~TENT  !:2 13 45 46 80 l,'"'T;jRELEASEO OF RELEASE

~ LQJ@ ~@13* 01~

,<\MOUNT PF AC;pvrry curie

.

.x..e-.ij.) I Waste gas s~ 1 <le!S!iJlEL~E ~osphere 1 a 9 10 PERSONNEL EXPOSURES 11 f.:;\

....I 45 -co stack. ao NUMBER (.;°::;\TYPE DESCRIPTION CTE]8 9 ol o I o11lLZJ@  ::

rr /A 1~3....._________________~----------..,....--------------------------------...J PERSONNEL INJURl!;S r;"'.;\ 50 NUMBER DESCRIPTION~

i:D:!] lo I ol ol@)...__N~/_A________________________~--~~~-----------------~

1 a s 11 12 80 LOSS OF OR CAMAGE TO FACILITY t4J'I TYPE DESCRIPTIO!\I '.;:;;J rr::TIJa IZ l@):n-_N_/fa_.___________________,,.._,_~~-,--------~----------------__J 1 9 10 * *:.}

  • ao PUBLICITY f.:\ NRC USE ONLY 1sa\JE!:'c.\ DESC~J'(JON ~

III1J U!j~...__.1_1 _A_______________________~----~----~-----~-.l I I I I !! I I I I I )

8 s 10 ' 68 69 80

-- -~-- - - - - - - - -- ~--

consumers Power company General Offices: 212 West Michigan Avenue, Jackson, Michigan 49201

  • Area Code 517 788-0550 December 18, 1978 Mr James G Keppler Office of Inspection and Enforcement Region III US Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137 DOCKET 50-255 - LICENSE DPR PALISADES PLANT - LER 78-040 On the reverse side is Revision 1 of Licensee Event Report 78-040 which is reportable under Technical Specification 6.9.2.a.(2).

David P Hoffman Assistant Nuclear Licensing Administrator CC: Director, Office of Nuclear Reactor Regulation Director, Office of Inspection and Enforcement