ML17292A361

From kanterella
Revision as of 23:09, 18 June 2019 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
Jump to navigation Jump to search
Monthly Operating Rept for June 1996 for WNP-2.W/960712 Ltr
ML17292A361
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 06/30/1996
From: Kasko B, Galen Smith
WASHINGTON PUBLIC POWER SUPPLY SYSTEM
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
GO2-96-137, NUDOCS 9607170076
Download: ML17292A361 (10)


Text

REGULATO INFORMATION DISTRIBUTION STEM (RIDS)ACCESSION NBR:9607170076 DOC.DATE: 96/06/30 NOTARIZED:

NO DOCKET I FACIL:50-397-WPPSS Nuclear Project, Unit 2, Washington Public Powe 05000397 AUTH.NAME AUTHOR AFFILIATION KASKO,B.Washington Public Power Supply System SMITHiG.O.

Washington Public Power Supply System RECIP.NAME RECIPIENT'AFFILIATION

SUBJECT:

Monthly operating rept for June 1996 for WNP-2.W/960712 ltr.DISTRIBUTION CODE: IE24D COPIES RECEIVED:LTR ENCL SIZE: TITLE: Monthly Operating Report (per Tech Specs)NOTES: RECIPIENT ID CODE/NAME PD4-2 PD INTERNAL: AC ILE CENT Ol N COPIES LTTR ENCL 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME COLBURN,T AEOD/SPD/RRAB NRR/DRPM/PECB COPIES LTTR ENCL 1 1 1 1 1 1 EXTERNAL: LITCO BRYCE,J H NRC PDR 1 1 1 1 NOAC 1 1 NOTE TO ALL"RIDSl'ECIPIENTS:

PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESKi ROOM OWFN 5D-5(EXT~415-2083)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED(TOTAL NUMBER OF COPIES REQUIRED: LTTR 10 ENCL 10 o I'4~\t'I WASHINGTON PUBLIC POWER SUPPLY SYSTEM PO.Box 968~3000 George Washington Way~Richland, Washington 99352-0968

~(509)372-5000 July 12, 1996 G02-96-137 Docket No.50-397 U.S.Nuclear Regulatory Commission Document Control Desk Washington, D.C.20555 Gentlemen:

Subject:

WNP-2 OPERATING LICENSE NPF-21 MONTHLY OPERATING REPORT JUNE 1996 Transmitted herewith is the Monthly Operating Report for the month of June 1996 as required by Technical Specification 6.9.1.6.Respectfully, G.O.Smith Plant General Manager (Mail Drop 9270)cc: LJ Callan-NRC RIV TG Colburn-NRR KE Perkins, Jr.-NRC RIV, WCFO NRC Sr.Resident Inspector-927N NS Reynolds-Winston&Strawn INPO ANI Library Utility Data Institute;-DLWilliams

-BPA/399 f v~o7i7oo7s 9sosso PDR~"ADGCK 0500039'7 R PDR.~~>/i l 4%'1'W 8=%N P 4'I t C l H OPERATING STATUS REPORT for WNP-2 Date: July 1, 1996 2.3.4.5.6.7.8.9.Outage+On-line Hours: 720.0 3486 1199 1153 1153 1107 none Docket: 50-397 Reporting Period: JUNE 1996 Utility Contact: Bernice Kasko (509)377-4473 Licensed Thermal Power (MW,): Nameplate Rating (Gross MW,): Design Electrical Rating (Net MW,): Maximum Dependable Capacity-summer (Gross MW,): Maximum Dependable Capacity-summer (Net MW,): If changes occur above since last report, give reasons: 10.Power to which restricted, if any (Net MW,): 11.Reasons for restrictions, if any: none 12.13.14.15.16.17.18.19.20.21.22.23.24.25.Report Period Hours Hours Reactor Critical Rx Reserve Shutdown Hours Hours Generator On-Line Unit Reserve Shutdown Hours Gross Thermal Energy (MwH)Gross Electrical Energy (MWH)Net Electrical Energy (MWH)Unit Service Factor Unit Availability Factor Unit Capacity Factor (MDC Net)Unit Capacity Factor (DER Net)Unit Forced Outage Rate Forced Outage Hours ONT 720.0 334.7 0.0 109.0 0.0 121,343 17,980 6,312 15.1%15.1%0.8%0.8%53.3%123.3 YEAR 4,367.0 1,819.8 985.9 1,582.6 997.4 4,546,703 1,523,270 1,435,103 36.2%59.1%29.7%28.5%7.3%123.3 CUMULATllUg 101,215.2 71,455.6 1,730.8 68,833.1 1,956.2 205,004,253 69,100,750 66,193,421 68.0%69.9%59.9%59.0%10.9%8,443.0 26.Shutdowns scheduled over the next 6 months (type, date, duration):

None 27.If currently shutdown, estimated startup date: Note: Cumulative Unit Capacity Factors (MDC&DER)are calculated with weighted averages.

4 I~4 0 I Lv 4v-Iv%1 v vh'l4 Iv iv 44 v 4 r~t t AVERAGE DAILY UNIT POWER LEVEL C~REPORT PERIOD: JUNE 1996 DOCKET NO.: 50-397 UNIT: WNP-2 DATE: July 1, 1996 COMPLETED BY: B Kasko TELEPHONE:

(509)377-4473 DAY AVERAGE DAILY POWER LEVEL (Net MWe)AVERAGE DAILY POWER LEVEL DAY (Net MWe)10 12 13 14 15-14-14-14-14-15-15-14-14-14-14-14-14-14-14 16'17 18 19 20 21 22 23 24 25 26 27 28 29 30-17-16-16-16-16 69 136 160 145-18-18-17-18-16 136 INSTRUCTIONS On this form, list the average daily unit power level in MWe (net)for each day in the reporting month.Compute to the nearest whole megawatt.These figures will be used to plot a graph for each reporting month.Note that when maximum dependable capacity is used for the net electrical rating of the unit, there may be occasions when the daily average power level exceeds the 100%line (or the restricted power level line).In such cases, the average daily unit power output sheet should be footnoted to explain the apparent anomaly.

1 k e E 4 il l UNIT SHUTDOWNS AND POWER REDUCTIONS REPORT PERIOD: JUNE 1996 DOCKET NO.: 50-397 UNIT NAME: WNP-2 DATE: July 1, 1996 COMPLETED BY B Kasko TELEPHONE:

(509)377M73 No.Date Type Hours Reason Method LER Number System, Component Cause and Corrective Action To Prevent Recurrence 96-08 4/13/96 S 487.7 NA RC t FUELXX Continuation from previous month-Plant entered annual refueling and maintenance outage (R-11)on April 13, 1996.96-09 6/25/96 F 124.3 A 96~3 CH INSTRU Digital feedwater controller error, change made to the controller software to prevent recurrence.

SUMMARY

WNP-2 exited the annual refueling and maintenance outage (R-11)on June 21.The reactor was manually scrammed on June 24 due to an unexpected plant response during testing of the new adjustable speed drives.At the end of the month WNP-2 was operating at 25%power and continuing with startup testing.TYPE F-Forced S-Scheduled REASON A-Equipment Failure B-Maintenance or Test C-Refueling D-Regulatory Restriction E-Operator Training&License Examination F-Administration G-Operational Error H-Other METHOD 1-Manual 2-Manual Scram 3-Auto Scram 4-Continued 5-Reduced Load 9-Other SYSTEM&COMPONENT NUREG%161 Exhibits F&H 0~'P D