NRC 2005-0034, February 2005 Monthly Operating Report for Point Beach Units 1 & 2

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February 2005 Monthly Operating Report for Point Beach Units 1 & 2
ML050810578
Person / Time
Site: Point Beach  NextEra Energy icon.png
Issue date: 03/14/2005
From: Koehl D
Nuclear Management Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
NRC 2005-0034, TS 5.6.3
Download: ML050810578 (6)


Text

Committed to Nuclear Excellence Point Beach Nuclear Plant Operated by Nuclear Management Company, LLC March 14, 2005 NRC 2005-0034 TS 5.6.3 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555 Point Beach Nuclear Plant, Units 1 and 2 Dockets 50-266 and 50-301 License Nos. DPR-24 and DPR-27 Monthly Operatinq Report In accordance with Technical Specification 5.6.3, Enclosure 1 contains the Monthly Operating Report for February 2005 for the Point Beach Nuclear Plant, Units 1 and 2.

This letter contains no new commitments and no revisions to existing commitments.

Dennis L. Koehl Site Vice-President, Point Beach Nuclear Plant Nuclear Management Company, LLC Enclosure cc: Administrator, Region ll, USNRC Project Manager, Point Beach Nuclear Plant, USNRC Resident Inspector, Point Beach Nuclear Plant, USNRC PSCW INPO Records Center 6590 Nuclear Road

  • Two Rivers, Wisconsin 54241 Telephone: 920.755.2321

ENCLOSURE I MONTHLY OPERATING REPORT 4 pages follow

OPERATING DATA REPORT DOCKET NO. 50-266 UNIT NAME POINT BEACH NUCLEAR PLANT - UNIT 1 DATE 03/04/05 COMPLETED BY Kim M. Locke TELEPHONE 920-755-7655 REPORTING PERIOD February - 2005

1. DESIGN ELECTRICAL RATING (MWE-NET) 522.0
2. MAXIMUM DEPENDABLE CAPACITY (MWE-NET) 516.0 MONTH YEAR TO DATE CUMULATIVE
3. NUMBER OF HOURS REACTOR WAS CRITICAL 672.0 1,416.0 248,786.3
4. NUMBER OF HOURS THE GENERATOR WAS ON LINE 672.0 1,416.0 245,199.4
5. UNIT RESERVED SHUTDOWN HOURS 0.0 0.0 846.9
6. NET ELECTRICAL ENERGY (MWH) 337,868.0 718,951.5 114,242,341.0 DATA REPORTED AND FACTORS CALCULATED AS REQUESTED IN NRC GENERIC LETTER 97-02 DATED MAY 15, 1997

UNIT SHUTDOWNS DOCKET NO. 50-266 UNIT NAME POINT BEACH NUCLEAR PLANT - UNIT 1 DATE 03/14/05 COMPLETED BY Kim M. Locke TELEPHONE 920-755-7655 REPORTING PERIOD: Februa!1/2005 (Month/Year)

TYPE METHOD OF CAUSE/CORRECTIVE NO. DATE F: FORCED DURATION REASON (1) SHUTTING ACTIONS S: SCHEDULED (HOURS) DOWN (2) COMMENTS N/A N/A N/A N/A N/A N/A N/A (1) Reason (2) Method A. Equipment Failure (Explain) 1. Manual B. Maintenance or Test 2. Manual Trip/Scram C. Refueling 3. Automatic Trip/Scram D. Regulatory Restriction 4. Continuation E. Operator Training/license Examination 5. Other (Explain)

F. Administrative G. Operational Error (Explain)

H. Other (Explain)

SUMMARY

Unit I average daily power for the month of February was 510.2 MWe.

There were no LERs issued in February for Unit 1.

e OPERATING DATA REPORT DOCKET NO. 50-301 UNIT NAME POINT BEACH NUCLEAR PLANT - UNIT 2 DATE 03/04/05 COMPLETED BY Kim M. Locke TELEPHONE 920-755-7655 REPORTING PERIOD February - 2005

1. DESIGN ELECTRICAL RATING (MWE-NET) 522.0
2. MAXIMUM DEPENDABLE CAPACITY (MWE-NET) 518.0 MONTH YEAR TO DATE CUMULATIVE
3. NUMBER OF HOURS REACTOR WAS CRITICAL 672.0 1,416.0 243,374.2
4. NUMBER OF HOURS THE GENERATOR WAS ON LINE 672.0 1,416.0 240,213.2
5. UNIT RESERVED SHUTDOWN HOURS 0.0 0.0 302.2
6. NET ELECTRICAL ENERGY (MWH) 339,135.0 724,718.5 113,610,683.5 DATA REPORTED AND FACTORS CALCULATED AS REQUESTED IN NRC GENERIC LETTER 97-02 DATED MAY 15, 1997

UNIT SHUTDOWNS DOCKET NO. 50-301 UNIT NAME POINT BEACH NUCLEAR PLANT - UNIT 2 DATE 03/14/05 COMPLETED BY Kim M. Locke TELEPHONE 920-755-7655 REPORTING PERIOD: Februar/2005 (Month/Year)

TYPE METHOD OF CAUSE/CORRECTIVE NO. DATE F: FORCED DURATION REASON (1) SHUTTING ACTIONS S: SCHEDULED (HOURS) DOWN (2) COMMENTS N/A N/A N/A N/A N/A N/A N/A (1) Reason (2) Method A. Equipment Failure (Explain) 1. Manual B. Maintenance or Test 2. Manual Trip/Scram C. Refueling 3. Automatic Trip/Scram D. Regulatory Restriction 4. Continuation E. Operator Training/license Examination 5. Other (Explain)

F. Administrative G. Operational Error (Explain)

H. Other (Explain)

SUMMARY

Unit 2 average daily power for the month of February was 512.1 MWe.

There were no LERs on Unit 2 for the month of February.

On February 27, PBNP experienced a loss of 345KV Line 151. Unit 2 was in a condition where the loss of 345KV, bus tie breaker 4-5, resulted in separating from the grid. Based on this scenario, Unit 2 was required to reduce load to <50%. On February 28, ATCo personnel notified PBNP that repairs were complete on Line 151; Unit 2 commenced load increase to 100%.