ML17223A875

From kanterella
Revision as of 08:04, 19 June 2019 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
Jump to navigation Jump to search
Responds to Violations Noted in Insp Rept 50-335/90-14. Corrective Actions:Rcs Flow Determination by Calorimetric Procedure Repeated W/Supervisor of Individual Observing & Individual Counseled by Supervisor
ML17223A875
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 08/09/1990
From: Goldberg J
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
L-90-291, NUDOCS 9008140504
Download: ML17223A875 (5)


See also: IR 05000335/1990014

Text

(ACCELERATED

DISTRIBUTION

DEMONSTRATION

SYSTEM I~~'REGULATORY

INFORMATION

DISTRIBUTION

SYSTEM (R1DS)ACCESSION NBR:9008140504

DOC.DATE: 90/08/09 NOTARIZED:

NO FACIL:50-335

St.Lucie Plant, Unit 1, Florida Power 6 Light Co.AUTH.NAME AUTHOR AFFILIATION

GOLDBERG,J.H.

Florida Power&Light, Co.RECIP.NAME

RECIPIENT AFFIL1ATION

Document Control Branch (Document Control Desk)SUBJECT: Responds to violations

noted in Insp Rept 50-335/90-14.

DISTRIBUTION

CODE: IEOID COPIES RECEIVED:LTR

i ENCL j SIZE: TITLE: General (50 Dkt)-Insp Rept/Notice

of VioTation Response NOTES: DOCKET ,05000335 D RECIPIENT ID CODE/NAME PD2-2 PD INTERNAL: ACRS AEOD/DEIIB

DEDRO NRR SHANKMAN,S

NRR/DOEA DIR 11 NRR/DRIS/DIR

.NRR/PMAS/ILRB12

OE.D EXTERNAL: LPDR NSIC COPIES LTTR ENCL 1 1 2 2 1 1 1 1 1 1 1.1 1 1'1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME NORRIS,J AEOD AEOD/TPAD NRR MORISSEAU,D

NRR/DLPQ/LPEB10

NRR/DRE P/PE PB9 D NRR/DST/DIR

8E2 NUDOCS-ABSTRACT

OGC/HDS2 RGN2 FILE 01 NRC PDR COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 A D D S D NOTE TO ALL"RIDS" RECIPIENTS:

D D PLEASE HELP US TO REDUCE O'ASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOiiI Pl-37 (EXT.20079)TO ELIMINATE YOUR NAME FROiv!DISTRIBUTIOiV

LISTS FOR DOCUi>IENTS

YOU DON'T NEED!TOTAL NUMBER OF COPIES REQUIRED: LTTR 24 ENCL 24

PO.Box 14000,Juno

Beach,FL 33408 0420 AUGUST.9 1990 L-90-291 10 CFR 2.201 U.S.Nuclear Regulatory

Commission

Attn: Document Control Desk Washington, D.C.20555 Gentlemen:

Re: St.Lucie Unit 1 Docket Nos.50-335 Response to Notice of Violation Ins ection Re ort 90-14 Florida Power and Light Company has reviewed the subject inspection

report and pursuant to 10 CFR 2.201 the response is attached.Very truly yours,":.b WX~~:~J;H.Goldberg President-Nuclear Division JHG/GRM Attachment

A cc: Stewart D.Ebneter, Regional Administrator, USNRC Region II Senior Resident Inspector, USNRC, St.Lucie Plant900-:;,40.".;Ot'C>r>80a>

F'1:<AZ>GCc,'-C~i>j>.".:;:

>-D>".an FPL Grov>>compacv+/

Re: St.Lucie Units 1 Docket Nos.50-335 Response to Notice of Violation Ins ection Re ort 90-14 FINDING:.Unit 1 Technical Specification (TS)6.8.1.a requires that written procedures

shall be established, implemented

and maintained

covering the activities

recommended

in Appendix A of Regulatory

Guide 1.33, Revision 2, February 1978.Appendix A, paragraph 1.d, includes procedures

addressing

procedure adherence and temporary change method.Procedure QI 5-PR/PSL-l, Rev 37, Preparation, Revision, Review/Approval

of Procedures, section 5.5, implemented

TS 6.8.1 and required that procedures

be strictly adhered to.It also provided the method to obtain approved temporary procedure changes and, if appropriate, subsequent

permanent changes.Procedure OP-1-0120051, Rev 10, RCS Flow Determination

by Calorimetric

Procedure, steps 8.3 through 8.6, directed certain action sequences involving coordination

with the Reactor Control Operator at the control board, control board loop temperature

meter function selection using switches, and confirmation

that measurements

were being made=only on channels that had the meter switched out and isolated.Cont'rary to the above, on May 14, 1990, During the performance

of procedure OP 1-0120051, the licensee's

staff did not follow instruction

steps 8.3 through 8.6 The test persons instead utilized an unapproved

method to isolate all the meters to simultaneously

isolate the involved loop temperature

meters and complete the data collection

without.the described coordination.

RESPONSE: 2~3~Florida Power and Light Company concurs with the violation.

The reason for the violation was failure to follow QI 5-PR/PSL-1.Test personnel failed to process a Procedure Change Request (PCR)prior to,implementing

an improved method of collecting

the temperature

data.The Reactor Coolant System flow determination

by calorimetric

.procedure was repeated with the individual's

supervisor

observing.

4, The following actions have been implemented

to avoid further violations:

a.The individual

was counselled

by his supervisor.'.

A PCR was submitted to clarify and authorize the'improved method of data collection.

Re: St.Lucie Units 1 Docket Nos.50-335 Response to Notice of Violation Ins ection Re ort 90-14 c.All individuals

in the Test Group were reminded of the importance

of following procedures

and the need for processing

a PCR and/or a Temporary Change (TC)followed by a PCR prior to implementation

of the change.5.All the corrective

actions were completed by August 1, 1990.