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MONTHYEARML13120A1582013-04-25025 April 2013 License Amendment Request to Revise Technical Specification 6.8.4.F for Peak Calculated Containment Internal Pressure Project stage: Request ML13150A2292013-05-28028 May 2013 Acceptance Review Results Regarding Millstone 3 - Revised Peak Calculated Containment Internal Pressure LAR (MF1731) Project stage: Acceptance Review ML13218A3102013-08-0808 August 2013 Request for Additional Information Regarding Amendment for a Revised Calculated Peak Containment Internal Pressure Project stage: RAI ML13275A2402013-09-19019 September 2013 Response to Request for Additional Information Regarding License Amendment Request to Revise Technical Specification 6.8.4.F for Peak Calculated Containment Internal Pressure Project stage: Response to RAI ML13305B0052013-11-0606 November 2013 Request for Additional Information Regarding License Amendment Request to Revise Technical Specification for Calculated Peak Containment Internal Pressure Project stage: RAI ML13353A2962013-12-11011 December 2013 Response to Request for Additional Information Regarding License Amendment Request to Revise Technical Specification 6.8.4.F for Peak Calculated Containment Internal Pressure Project stage: Response to RAI ML14073A0552014-04-0808 April 2014 Issuance of Amendment Calculated Containment Internal Pressure Project stage: Approval ML14142A0962014-06-10010 June 2014 Correction Letter to License Amendment No. 259 Project stage: Other 2013-05-28
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Category:Letter
MONTHYEARML24240A1692024-09-18018 September 2024 Cy 2023 Summary of Decommissioning Trust Fund Status ML24260A2192024-09-16016 September 2024 Decommissioning Trust Fund Disbursement - Revision to Previous Thirty-Day Written Notification ML24260A1952024-09-16016 September 2024 Response to Request for Additional Information Regarding Proposed Amendment to Support Implementation of Framatome Gaia Fuel ML24248A2272024-09-0404 September 2024 Operator Licensing Examination Approval ML24240A1532024-09-0303 September 2024 Summary of Regulatory Audit Supporting the Review of License Amendment Request for Implementation of Framatome Gaia Fuel IR 05000336/20240052024-08-29029 August 2024 Updated Inspection Plan for Millstone Power Station, Units 2 and 3 (Reports 05000336/2024005 and 05000423/2024005 IR 05000336/20240022024-08-13013 August 2024 Integrated Inspection Report 05000336/2024002 and 05000423/2024002 ML24221A2872024-08-0808 August 2024 Independent Spent Fuel Storage Installation (ISFSI) - Submittal of Cask Registration for Spent Fuel Storage IR 05000336/20244412024-08-0606 August 2024 Supplemental Inspection Report 05000336/2024441 and 05000423/2024441 and Follow-Up Assessment Letter (Cover Letter Only) ML24212A0742024-08-0505 August 2024 Request for Withholding Information from Public Disclosure - Millstone Power Station, Unit No. 3, Proposed Alternative Request IR-4-13 to Support Steam Generator Channel Head Drain Modification ML24211A1712024-07-25025 July 2024 Associated Independent Spent Fuels Storage Installation, Revision to Emergency Plan - Report of Change IR 05000336/20244032024-07-22022 July 2024 Information Request for the Cybersecurity Baseline Inspection, Notification to Perform Inspection 05000336/2024403 and 05000423/2024403 IR 05000336/20245012024-07-0101 July 2024 Emergency Preparedness Biennial Exercise Inspection Report 05000336/2024501 and 05000423/2024501 ML24180A0932024-06-28028 June 2024 Readiness for Additional Inspection: EA-23-144 IR 05000336/20240102024-06-26026 June 2024 Biennial Problem Identification and Resolution Inspection Report 05000336/2024010 and 05000423/2024010 ML24178A2422024-06-25025 June 2024 2023 Annual Report of Emergency Core Cooling System (ECCS) Model, Changes Pursuant to the Requirements of 10 CFR 50.46 IR 05000336/20244402024-06-24024 June 2024 Final Significance Determination for Security-Related Greater than Green Finding(S) with Assessment Follow-up; IR 05000336/2024440 and 05000423/2024440 and Notice of Violation(S), NRC Investigation Rpt 1-2024-001 (Cvr Ltr Only) ML24177A2792024-06-20020 June 2024 Preparation and Scheduling of Operator Licensing Examinations ML24170B0532024-06-10010 June 2024 DOM-NAF-2-P/NP-A, Revision 0.5, Reactor Core Thermal-Hydraulics Using the VIPRE-D Computer Code ML24162A0882024-06-10010 June 2024 Control Room Air Conditioning Unit Inoperable Due to Refrigerant Overcharge Resulting in a Condition Prohibited by Technical Specifications ML24165A1292024-06-0505 June 2024 ISFSI, 10 CFR 50.59 Annual Change Report for 2023 Annual Regulatory Commitment Change Report for 2023 ML24128A2772024-06-0404 June 2024 Issuance of Amendment No. 290 to Revise TSs for Reactor Core Safety Limits, Fuel Assemblies, and Core Operating Limits Report for Use of Framatome Gaia Fuel (EPID L-2023-LLA-0074) (Non-Proprietary) ML24151A6482024-06-0303 June 2024 Changes in Reactor Decommissioning Branch Project Management Assignments for Some Decommissioning Facilities ML24110A0562024-05-21021 May 2024 Exemption from the Requirements of 10 CFR Part 50, Section 50.46, and Appendix K Regarding Use of M5 Cladding Material (EPID L-2023-LLE-0013) (Letter) ML24109A0032024-05-21021 May 2024 Issuance of Amendment No. 289 to Revise Technical Specifications to Use Framatome Loss of Coolant Accident Evaluation Methodologies for Establishing Core Operating Limit (EPID L-2023-LLA-0065) (Non-Proprietary) ML24141A2432024-05-20020 May 2024 Response to Request for Additional Information Regarding Alloy 600 Aging Management Program Submittal Related to License Renewal Commitment No. 15 ML24141A1502024-05-20020 May 2024 Pressurizer Power Operated Relief Valve Failed to Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications ML24142A0952024-05-20020 May 2024 End of Cycle 22 Steam Generator Tube Inspection Report IR 05000336/20240012024-05-14014 May 2024 Integrated Inspection Report 05000336/2024001 and 05000423/2024001 and Apparent Violation ML24123A2272024-05-0202 May 2024 Pressurizer Power Operated Relief Valve Failed to Stroke Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications ML24123A2042024-05-0202 May 2024 Pre-Decisional Replay to EA-23-144 IR 05000336/20244012024-04-30030 April 2024 Security Baseline Inspection Report 05000336/2024401 and 05000423/2024401 (Cover Letter Only) ML24123A1222024-04-30030 April 2024 Inservice Inspection Program - Owners Activity Report, Refueling Outage 22 ML24116A0452024-04-25025 April 2024 Special Inspection Follow-Up Report 05000336/2024440 and 05000423/2024440 and Preliminary Finding(S) of Greater than Very Low Significance and NRC Investigation Report No. 1-2024-001 (Cover Letter Only) ML24116A1742024-04-24024 April 2024 Annual Radiological Environmental Operating Report ML24114A2662024-04-24024 April 2024 Submittal of 2023 Annual Radioactive Effluent Release Report ML24103A0202024-04-22022 April 2024 Summary of Regulatory Audit in Support of License Amendment Request to Use Framatome Small Break and Realistic Large Break Loss of Coolant Accident Evaluation Methodologies for Establishing Core Operating Limits ML24106A2032024-04-15015 April 2024 2023 Annual Environmental Operating Report ML24088A3302024-04-0404 April 2024 Regulatory Audit Plan in Support of License Amendment Request to Implement Framatome Gaia Fuel ML24093A1022024-04-0101 April 2024 Alternative Request IR-4-13, Proposed Alternative Request to Support Steam Genera Tor Channel Head Drain Modification ML24093A2162024-04-0101 April 2024 Response to Request for Additional Information Regarding License Amendment Request to Use Framatome Small Break and Realistic Large Break Loss of Coolant Accident Evaluation Methodologies for Establishing Core Operating Limits IR 05000336/20240112024-04-0101 April 2024 Comprehensive Engineering Team Inspection - Inspection Report 05000336/2024011 and 05000423/2024011 ML24092A0752024-03-28028 March 2024 3R22 Refueling Outage Inservice Inspection (ISI) Owners Activity Report Extension ML24088A2352024-03-26026 March 2024 Decommissioning Funding Status Report ML24086A4762024-03-22022 March 2024 Application for Technical Specification Change to Extend the Inspection Interval for Reactor Coolant Pump Flywheels Using the Consolidated Line-Item Improvement Process ML24086A4802024-03-22022 March 2024 Alternative Request IR-4-14, Proposed Alternative Request to Defer ASME Code Section XI Inservice Inspection Examination for Pressurizer and Steam Generator Pressure-Retaining Welds and Full Penetration Welded Nozzles ML24051A1922024-03-0808 March 2024 – Exemption from Select Requirements of 10 CFR Part 73 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting) IR 05000336/20230062024-02-28028 February 2024 Annual Assessment Letter for Millstone Power Station, Units 2 and 3, (Reports 05000336/2023006 and 05000423/2023006) ML24053A2632024-02-21021 February 2024 Unit 3, and Independent Spent Fuel Storage Installation, Notification Pursuant to 10 CFR 72.212(b)(1) Prior to First Storage of Spent Fuel Under a General License ML24057A0612024-02-19019 February 2024 and Virgil C. Summer Power Nuclear Stations - Nuclear Property Insurance Coverage 2024-09-04
[Table view] Category:Technical Specification
MONTHYEARML24086A4762024-03-22022 March 2024 Application for Technical Specification Change to Extend the Inspection Interval for Reactor Coolant Pump Flywheels Using the Consolidated Line-Item Improvement Process ML24030A7522024-01-30030 January 2024 Technical Specification Bases Pages ML23153A1732023-06-16016 June 2023 Correction to Amendment Nos. 346 & 286 Millstone, 294 & 277 North Anna, 311 & 311 Surry, and 225 Summer to Revise Technical Specifications to Adopt TSTF-554,Rev Reactor Coolant Leakage Requirement ML23013A2242023-01-13013 January 2023 Proposed License Amendment Request to Revise the Applicability Term for Reactor Coolant System Heatup and Cooldown Pressure Temperature Limitation Figures ML22095A1072022-07-11011 July 2022 Issuance of Amendment Nos. 120, 344, & 284, 293 & 276, & 307 & 307 to Relocate Requirements to the QAPD ML22096A2212022-04-0606 April 2022 Application for Technical Specification Change Regarding Mode Change Limitations Using the Consolidated Line Item Improvement Process ML22032A2702022-01-28028 January 2022 Technical Specification Bases Pages ML22032A2692022-01-28028 January 2022 Technical Specification Bases Pages ML22027A7362022-01-27027 January 2022 Request for Enforcement Discretion from Technical Specification 3.5.2 ECCS Subsystems and Technical Specification 3.7.3 Reactor Plant Component Cooling Water System ML21294A3382021-10-21021 October 2021 Proposed Amendment to Relocate Unit Staff Qualification Requirements from Technical Specifications to Nuclear Facility Quality . ML21047A4332021-02-15015 February 2021 Attachment 2: MPS3 Technical Specification Bases Pages ML21047A4322021-02-15015 February 2021 Attachment 1: MPS2 Technical Specification Bases Pages ML20252A1912020-09-0404 September 2020 Response to Request for Additional Information Regarding License Amendment Request for a One-Time Deferral of the Millstone Unit 3 Steam Generator Inspections ML20224A4572020-08-11011 August 2020 Connecticut. Inc. Millstone Power Station Unit 3, Proposed License Amendment Request for a One-Time Extension of the Millstone Unit 3 Steam Generator Inspections ML20063L8232020-03-0303 March 2020 License Amendment Request to Revise Technical Specification Table 3.3-11, Accident Monitoring Instrumentation ML20065K9762020-03-0303 March 2020 License Amendment Request to Revise Technical Specification Table 3.3-11, Accident Monitoring Instrumentation ML20063L2872020-02-26026 February 2020 Technical Specification Bases Pages ML19304A2942019-10-22022 October 2019 Supplement to Proposed License Amendment Request to Revise TS 3.8.1.1, A.C. Sources - Operating, to Support Maintenance and Replacement of the Millstone Unit 3 'A' Reserve Station Service Transformer and 345 Kv South Bus Switchyard Componen ML19109A1002019-04-11011 April 2019 Application to Revise Technical Specifications to Adopt TSTF-522, Revise Ventilation System Surveillance Requirements to Operate for 10 Hours Per Month. ML19052A1612019-02-14014 February 2019 Changes to Technical Specification Bases ML16257A5632016-09-19019 September 2016 Correction Letter to Amendment No. 327 - Technical Specification Changes for Spent Fuel Storage ML16258A1442016-09-0101 September 2016 Administrative Correction to License Amendment 327, Technical Specification Changes to Spent Fuel Pool Storage ML16061A0732016-02-23023 February 2016 Changes to Technical Specification Bases ML16034A3582016-01-26026 January 2016 License Amendment Request, Spent Fuel Pool Heat Load Analysis ML15342A0282015-12-0101 December 2015 Supplement to License Amendment Request to Adopt TSTF-523, Revision 2, Generic Letter 2008-01, Managing Gas Accumulation ML15246A1172015-08-31031 August 2015 Supplement to License Amendment Request to Revise TS 6.19, Containment Leakage Testing Program ML15065A3342015-02-26026 February 2015 Changes to Technical Specification Bases ML14188B1892014-06-30030 June 2014 License Amendment Request to Revise Technical Specifications to Adopt TSTF-426, Revise or Add Actions to Preclude Entry Into LCO 3.0.3 - RITSTF Initiatives 6B & 6C. ML14093A0272014-03-28028 March 2014 License Amendment Request for Administrative Changes and Corrections to the Technical Specifications ML14093A0262014-03-28028 March 2014 License Amendment Request for Administrative Changes and Corrections to the Technical Specifications ML14070A3462014-03-0606 March 2014 Changes to Technical Specification Bases ML13281A8092013-10-0202 October 2013 Response to Request for Additional Information Regarding License Amendment Request for Changes to Technical Specification 3/4.7.11, Ultimate Heat Sink ML13281A8042013-10-0202 October 2013 Response to Request for Additional Information Regarding License Amendment Request for Changes to Technical Specification 3/4.7.5, Ultimate Heat Sink ML13198A2712013-06-27027 June 2013 Supplement to License Amendment Request for Changes to Technical Specification 3/4.7.11, Ultimate Heat Sink. ML13120A1582013-04-25025 April 2013 License Amendment Request to Revise Technical Specification 6.8.4.F for Peak Calculated Containment Internal Pressure ML13079A2262013-03-0606 March 2013 Submittal of Changes to Technical Specification Bases ML12362A0122012-12-17017 December 2012 License Amendment Request to Revise Surveillance Requirement 4.4.3.2 Reactor Coolant System Relief Valves ML12081A1292012-03-0909 March 2012 Changes to Technical Specification Bases ML12032A2242012-01-25025 January 2012 License Amendment Request to Relocate TS Surveillance Frequencies to License Controlled Program in Accordance with TSTF-425, Revision 3 ML11193A2242011-07-0505 July 2011 License Amendment Request to Relocate TS Surveillance Frequencies to Licensee Controlled Program in Accordance with TSTF-425, Revision 3, Attachment 3 Through Attachment 6, Marked-up TS Pages and TS Bases Pages ML1023904032010-08-19019 August 2010 Changes to Technical Specification Bases ML0925806592009-09-0909 September 2009 Changes to Technical Specification Bases ML0826104492008-09-0808 September 2008 Transmittal of Changes to Technical Specification Bases ML0723303092007-08-15015 August 2007 Reactor Coolant System Leakage Detection Systems (Lbdcrs 07-MP2-012 and 07-MP3-032) ML0720003962007-07-13013 July 2007 Attachment 4, Millstone Power Station Unit 3, License Amendment Request, Stretch Power Uprate, Mark-Up of Associated Technical Specifications Bases Pages ML0715605312007-05-31031 May 2007 Tech Spec Pages for Amendment 299 Steam Generator Tube Integrity ML0711002192007-04-12012 April 2007 Changes to Technical Specifications Bases ML0708807052007-03-28028 March 2007 License Amendment Request (LBDCR 07-MP2-007) Re Containment Spray Nozzle Surveillance ML0703101462007-01-30030 January 2007 Technical Specification, Pressurizer Water Level Limits ML0700300722007-01-0202 January 2007 Supplement to Proposed Technical Specification Change (LBDCR 04-MP3-011) Auxiliary Feedwater System Allowed Outage Time 2024-03-22
[Table view] Category:Amendment
MONTHYEARML24086A4762024-03-22022 March 2024 Application for Technical Specification Change to Extend the Inspection Interval for Reactor Coolant Pump Flywheels Using the Consolidated Line-Item Improvement Process ML23153A1732023-06-16016 June 2023 Correction to Amendment Nos. 346 & 286 Millstone, 294 & 277 North Anna, 311 & 311 Surry, and 225 Summer to Revise Technical Specifications to Adopt TSTF-554,Rev Reactor Coolant Leakage Requirement ML23013A2242023-01-13013 January 2023 Proposed License Amendment Request to Revise the Applicability Term for Reactor Coolant System Heatup and Cooldown Pressure Temperature Limitation Figures ML22095A1072022-07-11011 July 2022 Issuance of Amendment Nos. 120, 344, & 284, 293 & 276, & 307 & 307 to Relocate Requirements to the QAPD ML22027A7362022-01-27027 January 2022 Request for Enforcement Discretion from Technical Specification 3.5.2 ECCS Subsystems and Technical Specification 3.7.3 Reactor Plant Component Cooling Water System ML21294A3382021-10-21021 October 2021 Proposed Amendment to Relocate Unit Staff Qualification Requirements from Technical Specifications to Nuclear Facility Quality . ML20252A1912020-09-0404 September 2020 Response to Request for Additional Information Regarding License Amendment Request for a One-Time Deferral of the Millstone Unit 3 Steam Generator Inspections ML20224A4572020-08-11011 August 2020 Connecticut. Inc. Millstone Power Station Unit 3, Proposed License Amendment Request for a One-Time Extension of the Millstone Unit 3 Steam Generator Inspections ML20063L8232020-03-0303 March 2020 License Amendment Request to Revise Technical Specification Table 3.3-11, Accident Monitoring Instrumentation ML19304A2942019-10-22022 October 2019 Supplement to Proposed License Amendment Request to Revise TS 3.8.1.1, A.C. Sources - Operating, to Support Maintenance and Replacement of the Millstone Unit 3 'A' Reserve Station Service Transformer and 345 Kv South Bus Switchyard Componen ML16257A5632016-09-19019 September 2016 Correction Letter to Amendment No. 327 - Technical Specification Changes for Spent Fuel Storage ML15246A1172015-08-31031 August 2015 Supplement to License Amendment Request to Revise TS 6.19, Containment Leakage Testing Program ML14093A0272014-03-28028 March 2014 License Amendment Request for Administrative Changes and Corrections to the Technical Specifications ML14093A0262014-03-28028 March 2014 License Amendment Request for Administrative Changes and Corrections to the Technical Specifications ML13281A8092013-10-0202 October 2013 Response to Request for Additional Information Regarding License Amendment Request for Changes to Technical Specification 3/4.7.11, Ultimate Heat Sink ML13281A8042013-10-0202 October 2013 Response to Request for Additional Information Regarding License Amendment Request for Changes to Technical Specification 3/4.7.5, Ultimate Heat Sink ML13120A1582013-04-25025 April 2013 License Amendment Request to Revise Technical Specification 6.8.4.F for Peak Calculated Containment Internal Pressure ML12362A0122012-12-17017 December 2012 License Amendment Request to Revise Surveillance Requirement 4.4.3.2 Reactor Coolant System Relief Valves ML0715605312007-05-31031 May 2007 Tech Spec Pages for Amendment 299 Steam Generator Tube Integrity ML0703101462007-01-30030 January 2007 Technical Specification, Pressurizer Water Level Limits ML0518101502005-06-28028 June 2005 Technical Specification Bases Pages ML0506706622005-02-25025 February 2005 Administrative Changes in Technical Specifications ML0326913862003-09-17017 September 2003 Amended TS Pages Reactivity Control Systems, Power Distribution Limits, and Special Test Exceptions ML0302805422003-01-16016 January 2003 Response to a Request for Additional Information, License Basis Document Change Request 2-1-02 Limiting Safety System Settings & Instrumentation ML0221201682002-07-19019 July 2002 Application for Amendment to NPF-49 to Modify Technical Specification Requirements for Missed Surveillances in Specification 4.0.3 & Modify Associated Technical Specification Bases ML0212901372002-05-0808 May 2002 Technical Specifications for Amendments Relocating Various Reactor Coolant System Technical Specifications to the Respective Unit'S Technical Requirements Manual ML0209200232002-03-29029 March 2002 Corrected TS Pages 3/4 3-39 & 3/4 3-41 ML0203701252002-02-0101 February 2002 Technical Specifications Pages Amendment 264 Revising the TSs and Bases Related to Reactor Coolant Pump Flywheel Inspection Requirements and Reactor Coolant System Structural Integrity ML0201103752002-01-11011 January 2002 Technical Specifications Pages for Amendment 263 Changes to TS Definitions for Core Alteration & Refueling Operations ML0201004062002-01-0808 January 2002 TS Pages for Amendment 262 Elimination of Requirements for Post-Accident Sampling ML0135202902002-01-0808 January 2002 Issuance of Amendment Elimination of Requirements for Post-Accident Sampling ML0135202162002-01-0808 January 2002 Issuance of Amendment Elimination of Requirements for Post-Accident Sampling ML0200702602002-01-0404 January 2002 Amendment 261 to TS Pages Emergency Diesel Generator Allowed Outage Time ML18088A9471976-04-19019 April 1976 Proposed Revisions to Environmental Technical Specifications ML17037B7791974-02-0707 February 1974 Letter Regarding Petition for Derating of Certain Boiling Water Reactors and Enclosed Before the Atomic Safety and Licensing Appeal Board in the Matter of Vermont Yankee Nuclear Power Corporation - Vermont Yankee Nuclear ... 2024-03-22
[Table view] Category:License-Application for Facility Operating License (Amend/Renewal) DKT 50
MONTHYEARML23226A0052023-09-26026 September 2023 Issuance of Amendment No. 287 Supplement to Spent Fuel Pool Criticality Safety Analysis ML23123A2792023-05-0202 May 2023 License Amendment Request to Use Framatome Small Break and Realistic Large Break Loss of Coolant Accident Evaluation Methodologies for Establishing Core Operating Limits and Exemption Request for Use of M5 Cladding ML23013A2242023-01-13013 January 2023 Proposed License Amendment Request to Revise the Applicability Term for Reactor Coolant System Heatup and Cooldown Pressure Temperature Limitation Figures ML22362A1022022-12-28028 December 2022 Proposed License Amendment Request to Supplement Spent Fuel Pool Criticality Safety Analysis ML22146A0272022-05-25025 May 2022 Application to Revise Technical Specifications to Adopt TSTF-554, Revise Reactor Coolant. ML22096A2212022-04-0606 April 2022 Application for Technical Specification Change Regarding Mode Change Limitations Using the Consolidated Line Item Improvement Process ML21294A3382021-10-21021 October 2021 Proposed Amendment to Relocate Unit Staff Qualification Requirements from Technical Specifications to Nuclear Facility Quality . ML21053A3422021-02-22022 February 2021 Proposed License Amendment Request to Clarify Shutdown Bank Technical Specification Requirements and Add Alternative Control Rod Position Monitoring Requirements ML20343A2432020-12-0808 December 2020 Proposed License Amendment Request Revise Reactor Core Safety Limit to Reflect WCAP-17642-P-A, Revision 1 ML20343A2592020-12-0808 December 2020 Supplement to Proposed License Amendment Request to Revise the Millstone Unit 2 Technical Specifications for Steam Generator Frequency ML20324A7032020-11-19019 November 2020 Proposed License Amendment Request Measurement Uncertainty Recapture Power Uprate ML20310A3242020-11-0505 November 2020 Proposed License Amendment Request, Addition of Analytical Methodology to the Core Operating Limits Report for a Large Break Loss of Coolant Accident (LBLOCA) ML20282A5942020-10-0808 October 2020 Proposed License Amendment Request to Revise the Millstone Unit 2 Technical Specifications for Steam Generator Inspection Frequency ML20224A4572020-08-11011 August 2020 Connecticut. Inc. Millstone Power Station Unit 3, Proposed License Amendment Request for a One-Time Extension of the Millstone Unit 3 Steam Generator Inspections ML20121A2172020-04-30030 April 2020 Proposed Technical Specifications Change Battery Surveillance Requirements ML20105A0782020-04-14014 April 2020 Supplement to License Amendment Request to Revise TS 3.8.1.1, A.C. Sources - Operating, to Support Maintenance and Replacement of the 'A' Reserve Station Service Transformer and 345 Kv South Bus Switchyard Components ML20065K9762020-03-0303 March 2020 License Amendment Request to Revise Technical Specification Table 3.3-11, Accident Monitoring Instrumentation ML20063L8232020-03-0303 March 2020 License Amendment Request to Revise Technical Specification Table 3.3-11, Accident Monitoring Instrumentation ML19353A0222019-12-17017 December 2019 License Amendment Request to Revise TS 6.25, Pre-Stressed Concrete Containment Tendon Surveillance Program ML19304A2942019-10-22022 October 2019 Supplement to Proposed License Amendment Request to Revise TS 3.8.1.1, A.C. Sources - Operating, to Support Maintenance and Replacement of the Millstone Unit 3 'A' Reserve Station Service Transformer and 345 Kv South Bus Switchyard Componen ML19217A2082019-07-30030 July 2019 Proposed License Amendment Request to Revise Integrated Leak Rate Test (Type a) and Type C Test Intervals ML19109A1002019-04-11011 April 2019 Application to Revise Technical Specifications to Adopt TSTF-522, Revise Ventilation System Surveillance Requirements to Operate for 10 Hours Per Month. ML19023A4272019-01-17017 January 2019 Application to Adopt 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems and Components for Nuclear Power Reactors ML18128A0492018-05-0303 May 2018 License Amendment Request Regarding Proposed Technical Specifications Changes for Spent Fuel Storage and New Fuel Storage ML18100A0552018-04-0404 April 2018 License Amendment Request to Revise Technical Specification Action Statement for Loss of Control Building Inlet Ventilation Radiation Monitor Instrumentation Channels ML17284A1792017-10-0404 October 2017 Proposed License Amendment Request to Revise Integrated Leak Rate Test (Type a) and Type C Test Intervals ML17171A2322017-06-15015 June 2017 License Amendment Request to Revise the Company Name ML17018A0002017-02-0707 February 2017 Issuance of Amendment Technical Specification Surveillance Requirement 4.1.3.1.2 for Control Element Assembly 39 ML16354A4242016-12-14014 December 2016 License Amendment Request to Revise Technical Specification Surveillance Requirement 4.1.3.1.2 for Control Element Assembly 39 for the Remainder of Cycle 24 ML16159A2592016-09-0606 September 2016 Enclosure 1 Millstone Power Station, Unit No. 1 Issuance of Amendment Administrative Changes and Corrections to the Technical Specifications ML16153A0262016-05-25025 May 2016 Proposed License Amendment Request Realistic Large Break Loss of Coolant Accident Analysis ML16153A0272016-05-25025 May 2016 ANP-3316(NP), Revision 0, Millstone, Unit 2, M5 Upgrade, Realistic Large Break Loca Analysis Licensing Report. ML16153A2342016-05-23023 May 2016 Supplement to License Amendment Request for Administrative Changes to the Permanently Defueled Technical Specifications ML16034A3582016-01-26026 January 2016 License Amendment Request, Spent Fuel Pool Heat Load Analysis ML16029A1682016-01-25025 January 2016 License Amendment Request to Revise ECCS TS 3/4.5.2 and FSAR Chapter 14 to Remove Charging ML15246A1172015-08-31031 August 2015 Supplement to License Amendment Request to Revise TS 6.19, Containment Leakage Testing Program ML15246A1182015-08-31031 August 2015 License Amendment Request to Revise Technical Specification 5.6.3, Fuel Storage Capacity ML15246A1242015-08-27027 August 2015 Connecticut, Inc. Millstone Power Station Unit 2 Supplement to License Amendment Request to Relocate TS Surveillance Frequencies to Licensee Controlled Program in Accordance with TSTF-425, Revision 3 ML15183A0222015-06-30030 June 2015 License Amendment Request for Removal of Severe Line Outage Detection from the Offsite Power System ML15134A2442015-05-0808 May 2015 License Amendment Request to Adopt Dominion Core Design and Safety Analysis Methods and to Address the Issues Identified in Westinghouse Documents NSAL-09-5, Rev. 1, NSAL-15-1, and 06-IC-03 ML15065A3342015-02-26026 February 2015 Changes to Technical Specification Bases ML15021A1282015-01-15015 January 2015 Proposed License Amendment Requests to Adopt TSTF-523, Revision 2, Generic Letter 2008-01, Managing Gas Accumulation ML14310A1872014-10-31031 October 2014 License Amendment Request to Revise the Final Safety Analysis Report - Examination Requirements for ANSI B31.1.0 Piping Welds ML14301A1122014-10-22022 October 2014 License Amendment Request to Relocate TS Surveillance Frequencies to Licensee Controlled Program in Accordance with TSTF-425, Revision 3 ML14188B1892014-06-30030 June 2014 License Amendment Request to Revise Technical Specifications to Adopt TSTF-426, Revise or Add Actions to Preclude Entry Into LCO 3.0.3 - RITSTF Initiatives 6B & 6C. ML14133A0092014-05-0808 May 2014 License Amendment Request, Implementation and Engineered WCAP-15376, Reactor Trip System Instrumentation Test Times and Engineered Safety Feature Actuation System Instrumentation Test and Completion Times ML14093A0282014-03-28028 March 2014 License Amendment Request for Administrative Changes to the Permanently Defueled Technical Specifications ML14093A0262014-03-28028 March 2014 License Amendment Request for Administrative Changes and Corrections to the Technical Specifications ML14093A0272014-03-28028 March 2014 License Amendment Request for Administrative Changes and Corrections to the Technical Specifications ML14070A3462014-03-0606 March 2014 Changes to Technical Specification Bases 2023-09-26
[Table view] |
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Dominion Nuclear Connecticut, Inc. FDominion 5000 Dominion Boulevard, Glen Allen, VA 23060 Web Address: www.dom.com April 25, 2013 U.S. Nuclear Regulatory Commission Serial No.13-225 Attention:
Document Control Desk NSSL/MLC RO Washington, DC 20555 Docket No. 50-423 License No. NPF-49 DOMINION NUCLEAR CONNECTICUT, INC.MILLSTONE POWER STATION UNIT 3 LICENSE AMENDMENT REQUEST TO REVISE TECHNICAL SPECIFICATION 6.8.4.F FOR PEAK CALCULATED CONTAINMENT INTERNAL PRESSURE Pursuant to 10 CFR 50.90, Dominion Nuclear Connecticut, Inc. (DNC) requests an amendment to Operating License NPF-49 for Millstone Power Station Unit 3 (MPS3). The proposed license amendment would revise the peak calculated containment internal pressure for the design basis loss of coolant accident described in Technical Specification (TS) 6.8.4.f, "Containment Leakage Rate Testing Program." The peak calculated containment internal pressure, Pa, would increase from 41.4 psig to 41.9 psig.Attachment 1 provides the description and assessment of the proposed change. As discussed in this attachment, the proposed amendment does not involve a significant hazards consideration pursuant to the provisions of 10 CFR 50.92. Attachment 2 contains the marked-up TS page to reflect the proposed change. The proposed change has been reviewed and approved by the Facility Safety Review Committee.
DNC requests approval of the proposed license amendment by April 25, 2014. Once approved, the license amendment will be implemented within 60 days.In accordance with 10 CFR 50.91(b), a copy of this license amendment request is being provided to the State of Connecticut.
If you have any questions regarding this submittal, please contact Ms. Wanda Craft at (804) 273-4687.Sincerely, Notary Public Eugene S. Grecheck I Commonwealth of Virgania Vice President-Nuclear Engineering and Development 140542 my commision Expires May 31. 2014 COMMONWEALTH OF VIRGINIA COUNTY OF HENRICO The foregoing document was acknowledged before me, in and for the County and Commonwealth aforesaid, today by Eugene S. Grecheck, who is Vice President
-Nuclear Engineering and Development of Dominion Nuclear Connecticut, Inc. He has affirmed before me that he is duly authorized to execute and file the foregoing document in behalf of that Company, and that the statements in the document are true to the best of his knowledge and belief.Acknowledged before me this 4.X- of d y of 2013.My Commission Expires: -5 A , A, Notary Public Serial No.13-225 Docket No. 50-423 Page 2 of 2 Commitments made in this letter: None Attachments:
- 1. Evaluation of Proposed Change to Revise Technical Specification 6.8.4.f for Peak Calculated Containment Internal Pressure 2. Marked-up Technical Specifications Page cc: U.S. Nuclear Regulatory Commission Region I 2100 Renaissance Blvd, Suite 100 King of Prussia, PA 19406-2713 J. S. Kim Project Manager U.S. Nuclear Regulatory Commission One White Flint North, Mail Stop 08-C2A 11555 Rockville Pike Rockville, MD 20852-2738 NRC Senior Resident Inspector Millstone Power Station Director, Radiation Division Department of Energy and Environmental Protection 79 Elm Street Hartford, CT 06106-5127 Serial No.13-225 Docket No. 50-423 ATTACHMENT I EVALUATION OF PROPOSED CHANGE TO REVISE TECHNICAL SPECIFICATION 6.8.4.F FOR PEAK CALCULATED CONTAINMENT INTERNAL PRESSURE DOMINION NUCLEAR CONNECTICUT, INC.MILLSTONE POWER STATION UNIT 3 Serial No.13-225 Docket No. 50-423 Attachment 1, Page 1 of 9 EVALUATION OF PROPOSED CHANGE TO REVISE TECHNICAL SPECIFICATION 6.8.4.F FOR PEAK CALCULATED CONTAINMENT INTERNAL PRESSURE
1.0 DESCRIPTION
Pursuant to 10 CFR 50.90, Dominion Nuclear Connecticut, Inc. (DNC) requests an amendment to Operating License NPF-49 for Millstone Power Station Unit 3 (MPS3).The proposed license amendment would revise the peak calculated containment internal pressure for the design basis loss of coolant accident (LOCA) described in Technical Specification (TS) 6.8.4.f, "Containment Leakage Rate Testing Program." The peak calculated containment internal pressure, Pa, would increase from 41.4 pounds per square inch gauge (psig) to 41.9 psig.The increase in Pa for MPS3 is due to an increase in the calculated mass and energy (M&E) released into containment during the blowdown phase of the design basis LOCA event. DNC has reanalyzed MPS3's Final Safety Analysis Report (FSAR) Chapter 6 containment analyses with corrected large break LOCA M&E data and is requesting NRC review and approval to change the TS 6.8.4.f value for Pa from 41.4 psig to 41.9 psig.The large break LOCA containment pressure analysis uses NRC-approved methods already described in the MPS3 FSAR, uses mass and energy inputs from an analysis that uses NRC-approved methods, meets the containment design pressure limit of 45 psig, and satisfies the Environmental Qualification and Containment Leakage Rate Testing Programs.2.0 PROPOSED CHANGE The proposed change to TS 6.8.4.f, "Containment Leakage Rate Testing Program," is shown below.TS 6.8.4.f currently states: The peak calculated containment internal pressure for the design basis loss of coolant accident, Pa, is 41.4 psig.The proposed change would revise TS 6.8.4.f, by replacing the Pa value of 41.4 psig with a value of 41.9 psig.The revised TS 6.8.4.f would read as follows: The peak calculated containment internal pressure for the design basis loss of coolant accident, Pa, is 41.9 psig.
Serial No.13-225 Docket No. 50-423 Attachment 1, Page 2 of 9 3.0 BACKGROUND Four errors have been identified in the MPS3 FSAR Chapter 6 analyses for large break LOCA M&E releases.
The M&E releases are calculated by Westinghouse and input to the MPS3 FSAR Chapter 6 containment response analyses that are performed by DNC.Three of the errors were identified in Westinghouse Nuclear Safety Advisory Letter (NSAL)-1 1-5, "Westinghouse LOCA Mass and Energy Release Calculation Issues," dated July 25, 2011. The fourth error was independent of NSAL-1 1-5 and specific to MPS3 (see Item 1 below). DNC has reanalyzed the FSAR Chapter 6 containment response analyses with corrected large break LOCA M&E data and is requesting NRC review and approval to change the TS 6.8.4.f value for Pa from 41.4 psig to 41.9 psig.Specifically, the four errors applicable to the MPS3 LOCA M&E analysis are: 1. Steam generator (SG) pressure was incorrectly input as 948 pounds per square inch absolute (psia) rather than the correct value of 984 psia. This error under predicted the initial stored energy in the four SGs. This error was specific to the MPS3 analysis of record and was discovered independent of the issues identified in NSAL-11-5.
- 2. The reactor vessel modeling did not include the appropriate reactor vessel metal mass available from the component drawings.
The discrepancy results in an inaccurate reactor vessel metal mass that affects the amount of reactor vessel stored energy initially available in the M&E model. This error was identified in NSAL-1 1-5.3. The reactor vessel modeling did not include the appropriate reactor vessel metal mass in the reactor vessel barrel/baffle downcomer region. Differences were identified in the calculated metal mass and surface area input values between upflow and downflow barrel/baffle configurations, with more significant differences noted in plants that were converted to an upflow barrel/baffle configuration.
Increases in the barrel/baffle metal mass impact the initial energy stored within the reactor vessel. MPS3 is an upflow plant. This error was identified in NSAL-1 1-5.4. The large break LOCA M&E release analysis was initialized at a non-conservative (low) SG secondary pressure condition.
This input value determines the initial SG secondary side temperature and pressure used in the large break LOCA M&E release calculations.
The pressure at the exit of the SG outlet nozzle was incorrectly used as the SG secondary side pressure, as opposed to the correct higher tube bundle pressure.
The initial SG energy is under estimated; therefore, the correction results in an increase in the calculated large break LOCA M&E release. This error was identified in NSAL-1 1-5.
Serial No.13-225 Docket No. 50-423 Attachment 1, Page 3 of 9 The Westinghouse errors only affected large break LOCA M&E releases.
Steam line break and small break LOCA M&E releases are unaffected.
Westinghouse reanalyzed the large break LOCA M&E releases with the errors corrected and no design input changes. The large break LOCA M&E analysis methods that were applied are consistent with those referenced in MPS3 FSAR Section 6.2.1.3 (see below).* WCAP-8264-P-A, Revision 1, "Topical Report: Westinghouse Mass and Energy Release Data for Containment Design," August 1975." WCAP-10325-P-A, "Westinghouse LOCA Mass and Energy Release Model for Containment Design -March 1979 Version," May 1983 (Proprietary).
4.0 TECHNICAL ANALYSIS Using the revised large break LOCA M&E data, DNC reanalyzed the FSAR Chapter 6 containment pressure and temperature response calculations using the NRC-approved GOTHIC containment analysis methodology documented in topical report DOM-NAF 0.0-P-A, Revision 0, "GOTHIC Methodology for Analyzing the Response to Postulated Pipe Ruptures Inside Containment," dated September 2006. This methodology is described in MPS3 FSAR Chapter 6.The peak calculated containment internal pressure following a large break LOCA is obtained for the double-ended hot leg guillotine break. Table A compares the new analysis results to the analysis of record. In the new analysis, correction of the large break LOCA M&E errors produced an increase in containment peak pressure of 0.44 psig and a reduction of 0.1 seconds in the peak pressure time. Consistent with the analysis of record, the containment peak pressure occurs near the end of the initial RCS blowdown.The magnitude of the peak pressure is independent of the emergency core cooling and containment heat removal systems, because these systems actuate after the peak pressure occurs. The large break LOCA containment peak pressure is less than the containment design pressure of 45 psig; however, the rounded result of 41.9 psig is an increase compared to the value for Pa of 41.4 psig currently reported in TS 6.8.4.f.
Serial No.13-225 Docket No. 50-423 Attachment 1, Page 4 of 9 Table A LOCA Peak Calculated Containment Internal Pressure Results Analysis of Record Revised Analysis LOCA Containment Peak Pressure 56.09 psia 56.53 psia Time of Peak Pressure 21.2 seconds 21.1 seconds Peak Pressure for TS 6.8.4.f Pa* 41.4 psig 41.9 psig* Determined by rounding the peak calculated containment internal pressure up to the nearest 0.1 psig.Containment Leaka-ge Review The total containment leakage, (La), for MPS3 consists of both filtered and bypass leakage. Per TS 6.8.4.f, the maximum allowable containment leakage rate La, at Pa, is 0.3 percent by weight of the containment air per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Until the supplementary leak collection and release system (SLCRS) drawdown is effective at 2 minutes post-LOCA, 100% of the containment leak rate is assumed to bypass the secondary containment and release unfiltered at ground level directly from containment.
After SLCRS drawdown at 2 minutes, the bypass leak rate, defined per TS 6.8.4.f, is 0.06 of La or 0.018 percent by weight per day; the remaining containment leakage (0.3 -0.018) is filtered and released through SLCRS. The containment leak rate, La, is reduced from 0.3 to 0.15 percent by weight at 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> for offsite dose calculations, and at one hour for control room (CR) and technical support center (TSC) dose calculations.
This assumption of a reduction in the containment leak rate by 50 percent after one hour for the CR and TSC habitability analyses was used in calculations supporting Amendment No. 59 (ADAMS No.ML01 1790140), which eliminated the post-LOCA negative containment pressure requirement.
This assumption was also referenced in the description of calculations provided as supplemental information supporting Amendment No. 211 (ADAMS No.ML023290568 and ML022470399), which changed the licensing basis for the post-accident operation of the SLCRS. The assumption of a 50 percent reduction in containment leakage after one hour is based on the fact that the MPS3 post-LOCA containment pressure is rapidly reduced compared to typical pressurized water reactors because the MPS3 containment was originally designed to be operated at sub-atmospheric pressure.
The initial containment design pressure for MPS3 was for a range of 8.9 psia -12 psia. In Amendment No. 59, the limiting condition for operation for TS 3.6.1.4 for containment initial pressure was changed from a range of 8.9 psia -12 psia to the current range of 10.6 psia -14.0 psia.The long-term LOCA containment response analysis demonstrates that the containment pressure meets the FSAR requirement for the radiological analysis of a 50 percent reduction in containment leakage after one hour. Resolution of the errors in the Westinghouse-generated LOCA M&E release analysis does not modify the intrinsic characteristic of the MPS3 containment.
The containment was originally designed as a negative pressure containment that allows a rapid pressure reduction following a
Serial No.13-225 Docket No. 50-423 Attachment 1, Page 5 of 9 design basis LOCA event as compared to typical pressurized water reactor containments.
The LOCA offsite radiological dose consequence analyses assume containment leakage rates based on percent by weight of the containment air. Therefore, the increase in the peak calculated containment internal pressure does not impact the offsite, CR and TSC radiological consequences of the LOCA accident analysis, as described in the MPS3 FSAR Section 15.6.5.4.10 CFR 50 Appendix J Program Review The containment leakage rate "Type A" test is performed in accordance with the requirements of 10 CFR 50 Appendix J to demonstrate that leakage of systems and components penetrating the primary containment do not exceed the allowable leakage rates specified in MPS3 TS 6.8.4.f. Specifically, the Type A test verifies that the measured containment leakage rate at Pa does not exceed the maximum allowable leakage rate, La, which is used to calculate the dose consequences following a postulated LOCA.The MPS3 Type A test was last completed on November 7, 2011. The containment pressure during the test was measured at 42.5 psig, which exceeds the peak calculated containment internal pressure of 41.9 psig that was calculated following resolution of the errors in the Westinghouse-generated large break LOCA M&E release analyses.
The containment leakage rate during the test was calculated to correspond to 0.0531 weight percent per day, which is less than the maximum containment leakage rate of 0.30 weight percent of the containment air per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> specified in TS 6.8.4.f and used for the offsite dose calculations.
The increase in peak calculated containment internal pressure does not affect systems and components in containment because these are designed for a containment design pressure limit of 45 psig, as referenced in FSAR Sections 6.2.1 and 3.8.1.Equipment Environmental Qualification Review The change in Pa does not affect environmentally qualified equipment within containment.
This equipment is qualified for the containment design pressure of 45 psig. Therefore, an increase in peak calculated containment internal pressure to 41.9 psig does not affect the environmental qualification of equipment within containment.
The containment temperatures, using the corrected large break LOCA M&E releases, remain within the bounding containment temperature profile used to qualify equipment.
Therefore, the post-accident operating time of the environmentally qualified equipment is unaffected.
Serial No.13-225 Docket No. 50-423 Attachment 1, Page 6 of 9 5.0 REGULATORY SAFETY ANALYSIS 5.1 Applicable Regulatory Requirements/Criteria The proposed change has been evaluated to determine whether applicable regulations and requirements continue to be met.General Design Criterion 4, "Environmental and dynamic effects design bases," states that structures, systems and components important to safety shall be designed to accommodate the effects of, and to be compatible with, the environmental conditions associated with normal operation, maintenance, testing, and postulated accidents including LOCAs.General Design Criterion 16, "Containment design," states that reactor containment and associated systems shall be provided to establish an essentially leak-tight barrier against the uncontrolled release of radioactivity to the environment and to assure that the containment design conditions important to safety are not exceeded for as long as postulated accident conditions require.General Design Criterion 19, "Control room," states that a control room shall be provided from which actions can be taken to operate the nuclear power unit safely under normal conditions and to maintain it in a safe condition under accident conditions, including LOCAs, and that adequate radiation protection shall be provided.General Design Criterion 38, "Containment heat removal," states that a system to remove heat from the reactor containment shall be provided that rapidly reduces, consistent with the functioning of other associated systems, the containment pressure and temperature following any LOCA and maintain them at acceptable low levels.These general design criteria continue to be met with the change in peak calculated containment internal pressure.
The environmental qualification of equipment within containment is not affected by the change in peak calculated containment internal pressure following a LOCA. The change in peak calculated containment internal pressure will be reflected in future 10 CFR 50 Appendix J, Type A containment leakage rate testing, so containment integrity is not impacted by the change. The change in peak calculated containment internal pressure does not impact the maximum allowable containment leakage rate and therefore does not impact control room operator dose. The peak calculated containment internal pressure remains below the containment design pressure.Based on the considerations above, (1) there is reasonable assurance that the health and safety of the public will not be endangered by operation in the proposed manner, (2) such activities will continue to be conducted in accordance with the MPS3 licensing basis, and Serial No.13-225 Docket No. 50-423 Attachment 1, Page 7 of 9 (3) the approval of the proposed change will not be inimical to the common defense and security or to the health and safety of the public.In conclusion, DNC has determined that the proposed change does not require any exemptions or relief from regulatory requirements, other than the TS, and does not affect conformance with any regulatory requirements or criteria.5.2 No Significant Hazards Consideration DNC is proposing a license amendment to MPS3 TS 6.8.4.f, "Containment Leakage Rate Testing Program." The proposed amendment would increase the calculated peak containment internal pressure for the design basis loss of coolant accident, Pa, from 41.4 psig to 41.9 psig.DNC has evaluated whether or not a significant hazards consideration is involved with the proposed amendment by focusing on the three standards set forth in 10 CFR 50.92,"Issuance of Amendment," as discussed below: 1. Does the proposed change involve a significant increase in the probability or consequences of an accident previously evaluated?
Response:
No.The proposed change to Pa does not alter the assumed initiators to any analyzed event.The probability of an accident previously evaluated will not be significantly increased by this proposed change.The change in Pa will not affect radiological dose consequence analyses.
MPS3 radiological dose consequence analyses assume a certain containment atmosphere leak rate based on the maximum allowable containment leakage rate, which is not affected by the change in peak calculated containment internal pressure.
The Appendix J containment leakage rate testing program will continue to ensure that containment leakage remains within the leakage assumed in the offsite dose consequence analyses.The consequences of an accident previously evaluated will not be significantly increased by this proposed change.Therefore, operation of the facility in accordance with the proposed change to Pa will not involve a significant increase in the probability or consequences of an accident previously evaluated.
- 2. Does the proposed change create the possibility of a new or different kind of accident from any accident previously evaluated?
Response:
No.
Serial No.13-225 Docket No. 50-423 Attachment 1, Page 8 of 9 The proposed change provides a higher Pa than currently described in TS 6.8.4.f. This change is a result of an increase in the M&E release input for the LOCA containment response analysis.
The peak calculated containment pressure remains below the containment design pressure of 45 psig. This change does not involve any alteration in the plant configuration (no new or different type of equipment will be installed) or make changes in the methods governing normal plant operation.
The change does not create the possibility of a new or different kind of accident from any accident previously evaluated.
Therefore, operation of the facility in accordance with the proposed change to TS 6.8.4.f would not create the possibility of a new or different kind of accident from any previously evaluated.
- 3. Does the proposed change involve a significant reduction in a margin of safety?Response:
No.The calculated peak containment internal pressure remains below the containment design pressure of 45 psig. Since the MPS3 radiological consequence analyses are based on the maximum allowable containment leakage rate, which is not being revised, the change in the calculated peak containment internal pressure does not represent a significant change in the margin of safety.Therefore, operation of the facility in accordance with the proposed change to TS 6.8.4.f does not involve a significant reduction in the margin of safety.6.0 ENVIRONMENTAL CONSIDERATION The proposed amendment would change a requirement with respect to installed facility components located within the restricted area of the plant, as defined in 10 CFR 20.However, as detailed below, the proposed amendment does not involve 1) a significant hazards consideration, 2) a significant change in the types or significant increase in the amounts of any effluent that may be released offsite, or 3) a significant increase in individual or cumulative occupational radiation exposure.
Accordingly, the proposed amendment meets the eligibility criterion for categorical exclusion set forth in 10 CFR 51.22(c)(9).
Therefore, pursuant to 10 CFR 51.22(b), no environmental impact statement or environmental assessment need be prepared in connection with the proposed amendment.
- 1. The amendment involves no significant hazards consideration.
As demonstrated in Section 5.2 above, "No Significant Hazards Consideration," the proposed change does not involve any significant hazards consideration.
Serial No.13-225 Docket No. 50-423 Attachment 1, Page 9 of 9 2. There is no significant change in the types or significant increase in the amounts of any effluent that may be released offsite.The proposed change will revise TS 6.8.4.f, "Containment Leakage Rate Testing Program." The proposed change does not result in an increase in power level, and does not increase the production nor alter the flow path or method of disposal of radioactive waste or byproducts; thus, there will be no change in the amounts of radiological effluents released offsite.Based on the above evaluation, the proposed change will not result in a significant change in the types or significant increase in the amounts of any effluent released offsite.3. There is no significant increase in individual or cumulative occupational radiation exposure.The proposed change will revise TS 6.8.4.f, "Containment Leakage Rate Testing Program." The proposed change will not result in any changes to the configuration of the facility.
The proposed change will not cause a change in the level of controls or methodology used for the processing of radioactive effluents or handling of solid radioactive waste, nor will the proposed amendment result in any change in the normal radiation levels in the plant. Therefore, there will be no increase in individual or cumulative occupational radiation exposure resulting from this change.7.0 PRECEDENCE This request is similar to the license amendment authorized by the NRC on January 19, 2012, for the Palisades Nuclear Plant (TAC No. ME6875, ADAMS Accession Numbers ML113220370 and ML120600415).
Serial No.13-225 Docket No. 50-423 Attachment 2 Marked-Up Technical Specifications Page DOMINION NUCLEAR CONNECTICUT, INC.MILLSTONE POWER STATION UNIT 3 ADMINISTRATIVE CONTROLS PROCEDURES AND PROGRAMS (Continued)
- 2) Pre-planned operating procedures and backup instrumentation to be used if one or more monitoring instruments become inoperable, and 3) Administrative procedures for returning inoperable instruments to OPERABLE status as soon as practicable.
- f. Containment Leakage Rate Testing Program A program shall be established to implement the leakage rate testing of the containment as required by 10 CFR 50.54(o) and 10 CFR 50, Appendix J, Option B, as modified by approved exemptions*.
This program shall be in accordance with the guidelines contained in Regulatory Guide 1.163, "Performance-Based Containment Leak-Test Program," dated September 1995, as modified by the following exception to NEI 94-01, Rev. 0, "Industry Performance Based Option of 10 CFR Part 50 Appendix J": The first Type A test performed after the January 6, 1998 Type A test shall be performed no later than January 6, 2013.9-1 The peak calculated contai ien--internal pressure for the design basis loss of coolant accident, Pa, is 41.4 psig.The maximum allowable containment leakage rate La, at Pa, shall be 0.3 percent by weight of the containment air per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.Leakage rate acceptance criteria are: 1) Containment overall leakage rate acceptance criterion is _< 1.0 La. During the first unit startup following testing in accordance with this program, the leakage rate acceptance criteria are < 0.60 La for the combined Type B and Type C tests, and _ 0.06 La for all penetrations that are Secondary Containment bypass leakage paths, and < 0.75 La for Type A tests;2) Air lock testing acceptance criteria are: a. Overall air lock leakage rate is _ 0.05 La when tested at > Pa.b. For each door, seal leakage rate is < 0.01 La when pressurized to >_ Pa.The provisions of Specification 4.0.2 do not apply to the test frequencies specified in the Containment Leakage Rate Testing Program.The provisions of Specification 4.0.3 are applicable to the Containment Leakage Rate Testing Program.* An exemption to Appendix J, Option A, paragraph III.D.2(b)(ii), of 10 CFR Part 50, as approved by the NRC on December 6, 1985.MILLSTONE
-UNIT 3 6-17 Amendment No. 69, 4-86, 2-32, 239, 24-2