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#REDIRECT [[IR 05000413/1997009]]
{{Adams
| number = ML20210N734
| issue date = 08/18/1997
| title = Insp Repts 50-413/97-09 & 50-414/97-09 on 970608-0719. Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support
| author name =
| author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
| addressee name =
| addressee affiliation =
| docket = 05000413, 05000414
| license number =
| contact person =
| document report number = 50-413-97-09, 50-413-97-9, 50-414-97-09, 50-414-97-9, NUDOCS 9708260105
| package number = ML20210N708
| document type = INSPECTION REPORT, NRC-GENERATED, TEXT-INSPECTION & AUDIT & I&E CIRCULARS
| page count = 32
}}
See also: [[see also::IR 05000413/1997009]]
 
=Text=
{{#Wiki_filter:.
                                                                                      . . . . . . . _ ,
        Notice of Violation                    3
        withholding of such material, you muit tpecifically identify the portions of
        your response that you seek to have witkield and provide in detail the bases
l
'
        for your claim of withholding (e.g., explain why the disclosure of information
        will create an unwarranted invasion of personal privacy or provide the
,
        confidential commercial or financial information). If safeguards information
l      1s necessary to provide an acceptable response, please provide the level of
        protection described in 10 CFR 73.21.
        Dated at Atlanta, Georgia
        this 18th day of August, 1997
l
                                                                          Enclosure 1
    .
      .
                        .
                                              __  .
                                                              ..  .
                                                                                -  ..
 
                                                                                  1
                        U. S. NUCLEAR REGULATORY COMMISSION
                                        REGION 11
    Docket Nos:    50-413, 50 414
    License Nos:    NPF-35. NPF-52
    Report Nos..    50-413/97 09. 50 414/97-09
    Licensee:      Duke Power Company
    Facility:      Catawba Nuclear Station. Units 1 and 2
    Location:      422 South Church Street
l                  Charlotte. NC 28242
    Dates:          June 8 - July 19, 1997
    Inspectors:    J. Zeiler. Acting Senior Resident inspector
                    R. L. Franovich, Resident inspector
                    M. Giles. Resident inspector (In Training)
                    N. Economos Region 11 Inspector (Sections M8.1. 2. 3. 4)
                    R. M. Moore. Region 11 Inspector (Sections 08.1. E2.1 )
    Approved by:    S. M. Shaeffer. Acting Chief
                    Reactor Projects Branch 1
                    Division of Reactor Projects
l
I
                                                                    Enclosure 2
  9708260105 970818
  PDR  ADOCK 05000413
  0              PDR
          .  .
                            .
                                .    .
                                                                                -
 
. _ .  __    _. _ _ _ _ _ _ _
                                  _____ - _ _ __ -
                                                          EXECUTIVE SUMMARY
                                                  Catawba Nuclear Station. Units 1 & 2
                                NRC Inspection Report 50 413/97-09, 50 414/97 09
      This integrated inspection included aspects of licensee operations.
      maintenance, engineering, and plant support. The report covers a 6-week
      period of resident ins)ection; in addition, it includes the results of
      announced inspections ay Regional reactor safety inspectors.
      Doerations
      e
            A Non Cited Violation (NCV) was identified for failure to declare three
            ice condenser intermediate deck doors inoperable and log an associated
            Technical Specification Action item Log entry after identifying ice
            buildup on the doors. This item along with several other minor human
            performance weaknesses indicated a need for greater attention to detail
            and questioning attitude by operations personnel during the performance
            of routine activities (Section 01.1).
      e
            The root cause evaluations of a reactor coolant pump trip and subsequent
            reactor trip were adequatel
            involve human error or nonconservative            y performed.  The cause
                                                                          decision      of theThe
                                                                                    making.    trip protective
                                                                                                    did not
            relaying associated with the short bus of 2TB functioned as designed.
            However, a delay in troubleshooting activities to locate the source of
            the associated ground indicated that the ground received a low priority
            status in the work schedule and that trained personnel were not readily
            available to troubleshoot ground indications in a timely manner (Section
            w.2).
      *
            Control room operators were effective in precluding a turbine runback by
            reducing reactor power to 50% before the 28 Main Generator Power Circuit
            Breaker opened on low air pressure. The licensee's root cause
            evaluation was detailed, and actions to prevent recurrence were
            considered adequate (Section 01.3).
      *
            The decision to deviate from the preferred normal alignment of
            Lower Containment Ventilation Unit (LCVU) operation to support
            planned maintenance exhibited non-conservative work scheduling and
            operatorjudgement. This resulted in lower containment air
            temperature increasing slightly above the adjusted Technical
            Specification limit for a brief period of time.                          The LCVU
            operating procedures did not address the adverse impact of
            removing two LCVUs from service simultaneously, nor did the
            procedure address the interaction between LCVU operation and
            integrated containment ventilation systems. These procedural
            inadequacies were identified as a NCV (Section 01.4).
      *
            A violation (first example) for failure to follow procedure was
            identified related to Operations failure to adequately document 10 CFR
            50.59 screening evaluations (Section 08.1).
                                                                                                  Enclosure 2
 
                                                    _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
                                          2
Maintenance
e      A Failure In!estigation Process (FIP) team was thorough in investigating
        the cause of an electrical flash in a 600 Volt breaker cubicle
        associated with Motor Control Center 2MXM. The root cause indicated
        configuration and procedure weaknesses in the method of locking out 600
        Volt breaker cubicles to the maintenance position. Adaquate corrective
        actions to prevent recurrence of this incident were implemented (Section
        M1.1).
e
        The licensee's identification of a technician's failure to follow a leak
        rate test procedure that resulted in an invaild test of valve 2NV-874
        during the previous refueling outage was an example of good questioning
        attitude: however, the procedure completion review was untimely. The
        Plant Operations Review Committee performed a thorough review of
        subsequent activities to aroperly retest the valve. Good engineering
        support was arovided, bot 1 in developing a leak rate test procedure and
      briefing paccage for the evolution. The failure to follow the leak rate
      test procedure was identified as a Violation (Section M1.2).
Enaineerina
e      The licensee's identification of a discrepancy between primary and
      secondary thermal power indication exhibited attention to detail in the
      review of plant data. Actions to initiate a FIP team to investigate the
      root cause were appropriate and steps to reduce reactor power until the
      discrepancy was understood were conservative. Replacement of a faulty
      T,,, card was well-planned, coordinated and controlled and executed in
      an expediticas manner (Section El.1).
o      Resolution of Design Base Document (DBD) open items was generally
      adequate.    However, a violation (second example) for failure to follow
      procedure was identified related to Engineering's failure to enter DBD
      open items into the Problem identification Process as required by
      procedure and stated in the licensee's response to the Des'.gn Basis
      50.54f letter (Section E2.1).
e      The licensee's corrective action audit that assessed the resolution of
      Self-N iated Technical Audit findings was identified as a strength in
      correc " ve action performance (Section E2.1).
e      The licensee adequately addressed the Emergency Diesel Generator 10 CFR
      Part 21 issue related to potentially defective intake / exhaust springs
      (Section E2.1).
*      Based on in-office review of the licensee *s March 31, 1997, annual
      summary on 10 CFR 50.59 changes, onsite review of the licensee's 10 CFR
      50.59 evaluations, and audit of the licensee's procedures, the inspector
      concluded that the licensee had complied with t1e provisions of the
      regulation for the changes listed in the annual summary (Section E3.1).
                                                                                                                          Enclosure 2
 
                                                                                  -
                                                                                      ,
                                        3
  Plant Suncort
  e    Radiological control practices observed during the inspection period
        were considered to b(. proper (Section R1.1).
l
l
                                                                    Enclosure 2
                            ,
                                            .
                                                            -
                                                                                -  _
 
                  _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
I
                                                    Reoort Details
; Summary of Plant Status
,
  Unit 1 operated at or near 100% power during the inspection period.
l On June 26, a Unit 2 reactor trip occurred on low Reactor Coolant System loop
l
i
  flow as a result of an electrical ground fault which de energized the
  electrical bus that powers the "2B' Reactor Coolant Pump (RCP). The unit was
  returned to 100% power operation on June 29. Power was reduce 1 to 50% on July
  2 to preclude a turbine trip / reactor trip u)on the anticipated failure of                    ;
  Main Generator Power Circuit Breaker (PCB) 23.                    A solenoid (or pilot) valve  '
  associated with the air supply to all three main generator PCB poles had
  failed, rendering the air system unable to deliver air to the breaker. The
  solenoid valve was replaced, and the unit was returned to 100% power the
  following day. Reactor power was reduced to 99.3% on July 15 in response to a
  discrepancy between primary and secondary thermal power indications. The
  discrepancy was attributed to feedwater venturi defouling and hot leg
  streaming, and did not reflect an actual temperature difference. The unit
  returned to 100% power on July 17 and operated at or near 100% power for the
  remainder of the inspection period.
  Review of UDdated Final Safety Analysis Report (UFSAR) Commitm_gn_t1
  While performing inspections discussed in this report, the inspector reviewed
  the applicable portions of the UFSAR that were related to the areas ins)ected.
  The inspector verified that the UFSAR wording was consistent with the o) served
  plant practices, procedures, and/or parameters.
                                                    I. Operations
  01    Conduct of Operations
  01.1 General Comments (71707)
        The inspector conducted frequent control room tours to verify proper
        staffing operator attentiveness and communications. and adherence to
        approved )rocedures. The inspector attended daily operations turnover
        and Site )irection meetings to maintain awareness of overall plant
        operations. Operator logs were reviewed to verify operational safety
        and compliance with Technical Specifications (TS). Instrumentation,
        computer indications, and safety system lineups were periodically
        reviewed from the Control Room to assess o)erability. Plant tours were
        conducted to observe equipment status and Jousekeeping.                  Problem
        Identification Process (PIP) reports were routinely reviewed to assure
        that potential safety concerns and equipment problems were reported and-
        resolved,
        in general, the conduct of operations was professional and safety
        conscious. Good )lant equipment material conditions ar.d housekee ing
        were noted througaout the report period. However, as addressed b low,
        sevcral minor operator human performance deficiencies were identified
                                                                                      Enclosure 2
 
_ _ _ _ _ _ _
                                                                    .
                                                                                        ,
                                                  2
                involving a failure to enter a TS Action Statement, failure to identify
                equipment status anomalies, and failure to properly document a Technical
              Specification Action item Log (TSAIL) entry.
              Failure to Declare Unit 2 Ice Condenser Intermediate Deck Doors
                inoDerable and Enter ADolicable TS Action Statement
              On June 17 at 2:38 p.m., while performing the weekly TS surveillance on
              the intermediate deck doors the licensee identified that three doors
              had ice buildup (reported to be less than one half inch thick). The
                function of these doors is to open during a des.gn basis accident to
              ensure that the containment loss Of Coolant Accident (LOCA) atmos)here      l
              would be diverted through the ice condenser. Upon discovery of t1e ice,
              a test procedure discrepancy was entered and a work request was
                initiated to remove the ice. However, work to remove the ice or
                investigate the extent of the impact on the door opening function was
              not initiated due to problems with personnel accessing containment
              through the containment airlock door. Later that night, the oncoming
              Shift Work Manager became aware of the previces day's problem and
              -contacted engineering personnel to perform an operability evaluation of
              the condition. The following morning, the inspector reviewed the
              results of this evaluation. The evaluation concluded that the " ice
              condenser" was operable. This was based primarily-on a previous McGuire
              Nuclear Station analysis that showed up to one-third of the intermediate
              deck doors could fail to open and there would still be enough ice
              condenser flow area for LOCA heat removal. The inspector determined the
              evaluation focused to narrowly on the ice condenser system operability
              and failed to adequately evaluate the operability of the intermediate
              deck doors, especially with regard to consideration of information in
              the applicable TS and Bases.
              TS 3.6.5.3 requires the intermediate deck doors be operable in Modes 1-
              4. TS Surveillance Recuirement 4.6.5.3.2 requires a 7-day verification
              that the intermediate ceck doors be closed and free of frost
              accumulation. The TS Bases also states that impairment by ice, frost.
              or debris is considered to render the doors inoperable, but capable of
              opening. Based on this, the inspector concluded that operations
              personnel had failed to declare the three doors inopera]le and follow
              the Action Statement of TS 3.6.5.3.a when the problem was initially
              identified. This action statement allowed power operation to continue
              for up to 14 days provided ice bed temperature was monitored at least
              once per four hours and the maximum ice bed temperature was maintained
              less than or equal to 27*F. The licensee initiated PIP 2-C97-2014-to
              investigate this incident.
              On June 18. after repairing the containment airlock, ice was removed
              from the three intermediate deck doors. The cause of the ice buildup
              was found to be the failure of heat tracing on an ice condenser air
              handling fan drain line, which prevented adequate draining of defrost
              condensate. The heat tracing was subsequently repaired. The licensee
                                                                            Enclosure 2
                                                                        -
 
,
                                    3
i
  determined during activities to remove the ice that all three doors were
l not blocked to the extent that would have prevented their opening during
'
  a LOCA. The inspector also noted that the ice bed monitoring system was
  operational during the period that ice was on the doors and control room
  annunciator alarms would have alerted the operators of anomalous ice bed
  temperatures. Therefore, the ins)ector considered the safety
  consequences of this incident to )e minimal.
  The inspector reviewed Operations Management Procedure (OMP) 2-29.
  Technical Specifications Action Item Log. Step 3.4 requires that non-
  compliance with a Limiting Condition For Operation requiring operation
  in a TS Action Statement, be logged in TSAll. The ins)ector determined
  that a TSAll entry was not logged for this condition w1en ice was
  identified on the doors rendering them inoperable. The failure to
  declare the doors inoperable and enter a TSAll entry for t % applicable
  TS Action Statement in accordance with OMP 2-29 was identitied as a
  Violation of TS 6.8.1. Procedures and Programs. This failure to follow
  procedures constitutes a violation of minor significance and is being
  treated as a Non-Cited Violation (NCV). consistent with Section IV of
  the NRL Enforcement Policy. This item is identified as NCV 50 414/97-
  09 01:  Failure to Declare Ice Condenser Intermediate Deck Doors
  Inoperable and Log Appropriate TSAll Entry.
  Auxiliary Shutdown Panel Volume Control Tank (VCT) Instrumentation Drift
  During a walkdown of the four Motor Driven Auxiliary Feedwater Shutdown
  Panels, the inspector identified that three of the four VCT level
  indications were not reading accurately. There is one VCT gauge on each
  Shutdown Panel. Gauge indications differed from control room
  indications by as much as 20 percent level. The ins)ector alerted
  operations-personnel to-the problem and noted that t1ey were very
  responsive in initiating corrective actions. Due to subsequent problems
  in calibrating the gauges and unavailability of like parts, engineering
  modifications were developed and implemented to replace the gauges with
  more accurate models. Based on discussions with Instrumentation and
  Electrical (IAE) personnel, it was indicated that most likely, the
  gauges had drifted out of accuracy over a long period of-time.
  The inspector reviewed periodic surveillance test procedures associated
  with verifying Shutdown Panel instrumentation indications. VCT level
  was not among the indications checked periodically. The inspector
  noted. however, that VCT level was not required by TS to be o)erable
  from the Shutdown Panels. However, the VCT indication could )e
  potentially used during operation from the Shutdown Panels. It was also
  apparent that-there had been opportunities to have identified the gauge
  output drift during the periodic surveillances of other Shutdown Panel
  instrumentation.
                                                                Enclosure 2
 
  _________ __- _ _                          .
                                                            -
l                                                              4
                          Unit 2 Power Rance Channel NI-42 Soare Window Illuminated
                          On June 27. 1997, the day after Unit 2 tripped on low Reactor Coolant
                          System flow, the inspector noticed an annunciator window on the Nuclear
                          Instrument (N1) 42 Power Range drawer that was illuminated. The
                          annunciator window was labeled " spare" and appeared to serve no
                          function. The inspector questioned the control room operators about the
                          illuminated window. The window apparently first illuminated following
                          the trip; however, the operators were not aware that the window was
                          illuminated, nor the reason for the condition. Based on subsequent
                          discussions with reactor engineering personnel, the inspector learned
                          that this spare annunciator window was previously used as the negative
                          rate trip indication light. During the previous refueling outage. this
                          trip function was isolated from the reactor protection logic, the
                          modification that implemented the rate trip change was supposed to have
                          removed the bulb from these windows on all of the N1 drawers. .It was
                          believed that the bulb in the NI-42 drawer was removed, but may have
                          been reinstalled by lAE personnel by mistake during subsequent NI
                          maintenance activities following the refueling outage. The light was
                          extinguished once the rate trip function was reset and the bulb. removed.
                          The licensee initiated a PIP to address this problem.
                          TS Loaaina Error for Trackina Containment Airlock Door Seal Surveillance
                          lRR
                          On July 11, 1997, during review of the Unit 2 TSAIL. the inspector
                          noticed an incorrect entry that was made on July 9. The entry was for
                          tracking a TS required 72 hour airlock door seal test following opening
                          of the airlock door on July 9. The time required for the test to be
                          performed was listed in TSAIL as July 16 instead of July 12. The
                          inspector discussed the error with operations personnel who corrected
                          the entry. It was also indicated that the seal test was scheduled to be
                          performed that same day. Based on this, the inspector determined the
                          test would not have been missed even though the TSAll was incorrect.
                          The inspector was concerned that the TSAll error had not been identified
                          over the two previous two days that the problem existed.
                          Individually, the above problems had little actual safety consequences.
                          however, in the aggregate represented the need for greater attention to
                          detail and questioning attitude by operations personnel during the
                          performance of routine activities.
                    01.2 Unit 2 Reactor Trio on low Reactor Coolant System Flow-
                      a.  Insoection Scope (71707. 937,01).
                          On June 26 a Unit 2 reactor trip from 100% power occurred when the 2B
                          Reactor Coolant Pump (RCP) tripped and caused a loss of flow signal in
                          the associated loop. The inspector discussed the unit trip with
                          engineering, operations and maintenance personnel, as well as reviewed
                          the associated electrical diagrams. Unit Trip Report and Pl? 2-C97-2221.
                                                                                        Enclosure 2
 
l                                        5
i b, Observations and Findinas
i
!
    On June 21. a negative leg ground was detected on ron vital distribution
    bus 2CDB.    The ground subsequently was traced to tre 125 VDC control
l    power circuit of breaker 2T6 6. On June 26. the b"eaker was opened to
'
    facilitate troubleshooting the cause of the ground. The Instrument and      .
    Electrical (IAE) technicians noticed that the breaker failure initiation    l
    relay in 2TB 6 control cubicle was chattering, but continued with their      i
    troubleshooting activities. Shortly thereafter, a reactor trip
    occurred.
    The licensee determined that. the source of the ground fault was the
    breaker pushbutton, a Cutler-Hammer E30 model,    lhe pushbutton had        '
    failed and created a negative leg-to ground fault on 2CDB. The
    pushbutton internals had changed state when 2TB 6 was tripped open
    during troubleshooting, introducing a fault path to the positive leg.
    Noise from the cabinet ground was induced through the switch and the
    breaker failure initiation relay (94B) coil, causing it to chatter and
    eventually actuate to trip the incoming breaker on the short bus of 2TB.
    The auto close function of the 2TB tie breaker was blocked by a lockout
    rela
    bus,y, and the bus de-energized. The 2B RCP. which is supplied from the
          tripped, and the subsequent low flow in the B loop caused a reactor
    trip.
    The inspector discussed the reactor trip with operations and engineering
    personnel to determine if the root cause involved a human error. The
    chattering of the relay, generated when 2TB 6 was opened, could have
    been stop)ed if the IAE technicians had reclosed the breaker when they
    noticed tlat relay chattering. However, they did not understand what
    was causing the chattering at the time. The inspector concluded that
    the IAE technicians responded appropriately by leaving the breaker in
    the opened position since the cause and impact of the relay chattering
    were not understood.
    The inspector inquired about the time delay between ground detection
    (identified on a Saturday) and troubleshooting activities (initiated the
    following Wednesday).    l.icensee personnel indicated that Single Point Of
    Contact (SPOC) technicians were not trained and qualified to use the
    ground chasing equipment. As a result a'stempts to locate the ground
    could not be made until the following Monday when a trained IAE
    technician would be available. Also, priority status was not associated
    with troubleshooting the ground indication early in the week. In
    addition, the inspector determined that only two techniciant on site
    were fully qualified to use the ground-chasing equipment to locate the
    source of a ground, and that_one of those technicians had been offsite
    since February and was not scheduled to return until October of this
    year. A shortage of trained personnel available to perform the
    troubleshooting contributed to the delay. At the end of the ins)ection
    period, the delay in investigating the ground, associated contri)uting
    factors, and appropriate corrective actions were not addressed within
    the licensee's corrective action program.
                                                                    Enclosure 2
 
.
                                            6
        The unit was restarted on June 28 after trip list activities were
        performed and minor equipment problems were corrected. The licensee is          '
        planning to document the reactor trip in a Licensee Event Report.
l  c.  Conclusions
        The inspector concluded that root cause evaluations of the reactor trip
        were adequately performed.    The cause of the tt!p did not involve human
        error or non conservative decision making. The protective relaying
        associated with the short bus of 2TB functioned as designed. The
        inspector determined that, although the delay in troubleshooting
        activities to locate the source of the ground did not affect the outcome
          (reactor trip), challenges existed in the following areas: (1)
        associating appropriate priority to locating ground indications in a
        timely manner, and (2) ensuring that trained personnel are avullable to
        troubleshoot ground indications. At the end of the inspection period,
        efforts to address the delay, understand its causes, and identify
        corrective actions were not evident in the licensee's corrective action
        program.
'
  01.3 Unit 2 Downoower in Response to Generator Outout Breaker Trouble
    a.  insoection Scone (71707)
        On July 2. Unit 2 control room operators received a generator breaker
        trouble alarm and identified a continuous decrease in minimum close air
          3ressure on 28 Main G2nerator Power Circuit Breaker (PCB). Operators
        Jegan a rapid load reduction, and the PCB automatically tripped after
        reactor power reached 50%. The inspector reviewed PIP 2 C97 2177 and
        discussed the downpower and associated equipment failure with licensee
        personnel.
    b.  Observations and Findinos
        On July 2, the Main Generator PCB 2B Trouble annunciator alarmed in the
        control room. Control room operators determined that there was a
        continuous decrease in air 3ressure on the 28 Main Generator PCB,
        indicating an approach to 11e minimum air pressure is required to open
        the breaker. Air
      ' the resulting arc. pressure  is required
                              Since the          to openofthe
                                          safety function    thebreaker andtodissipate
                                                                  PCB was      open, it
        was designed to automatically open before the minimum pressure required
        for this function is reached.    The minimum tri
        Generator PCB 2B is between 446 and 452 psig. p pressure on Main
        To preclude an automatic turbine runback on the potential automatic
        opening of the PCB operators began a rapid load reduction, The PCB
        automatically tripped after reactor power reached 50%. No overcurrent
        alarms were received on Main Transformer 2A.
        The license deternJned that a solenoid (or )ilot) valve associated with            I
s
        the air sup)1y to a:1 three main generator )CB poles had failed,
        rendering t1e air system unable to deliver air to the breaker.
        Normally, the solenoid valve receives signals from the breaker poles to
                                                                          Enclosure 2
                                                V
 
i
                                            7
,
        supply air to them. When the air pressure on any pole reaches
        a> proximately 485 psi.-a pressure switch actuates and the solenoid valve
        sluttles to pneumatically control a regulator that delivers air to the
        breaker poles. When air pressure is restored to 500 psi the signal
'
        from the pole to the solenoid is terminated.
        Station PIP 2-C97-2177 documented the root cause of the solenoid
        failure. The failed solenoid was new and had been installed during the
        April 1997 refueling outage. The component failure was attributed to a
        deformed nylon bushing. The valve had been assembled to compensate for
        the defect which initially allowed the valve to operate as designed.
        However, the valve's internal components drifted from their assembled
        positions over time and eventually were unable to engage with the
        valve's lower assembly, thereby preventing air flow to the poles.
        To address the potential that newly purchased solenoid valves could be
        installed with problems, the licensee had revised procedure
        IP/0/B/4974/01, Main Generator PCB Maintenance. - Revision 5 of the
        procedure included a Note between Steps 10.3.7 and 10.3.8. The-Note
        read: "If pilot valve is replaced, ensure pilot valve has been
        disassembled and inspected for pro >er assembly and components. or
        rebuilt prior to installation." T1e inspector verified that this
        procedure change had been made,
    c.  Conclusions
        The inspector concluded that control room operators were effective in
          )recluding a turbine runback by reducing reactor power to 50% before the
          3CB opened. The licensee's root cause evaluation was detailed and
        actions to prevent recurrence were adequate.
  01.4 Lower Containment Air Temoerature Exceeded for Short Duration
    a.  Insnection Stone (71707)
        On June 30. the licensee was performing maintenance on the Unit 2
        Lower Containment Ventilation Units (LCVUs). While the 2A and 20
        LCVUs were out of service, the lower containment temperature
        increased to 117.4'F. The inspector reviewed apalicable operating
        procedures. TS. the FSAR, tagout requirements, tie innage work
        schedule, and PIP 2 C97-2127. The inspector also discussed the
        -issue with operations, engineering and work control personnel.
    b.  Observations-and Findinas
        During normal operation. the Containment Chilled Water (YV)
        chillers service various containment loads including the LCt!Us and
        the Reactor Coolant Pump (RCP) Motor Air Coolers. 0_n June 30,
        preventive maintenance (PM) and electrical motor testing were
        scheduled for the 2A and 20 LCVUs. The 2A LCVU was removed from
                                                                      Enclosure 2
 
                                                                                                                      I
                                                                                                                      !
                                                                                                                        l
                                                              8
                                                                                                                        l
  service first. After the PM for the 2A LCVU was completed, but                                                        i
before motor testing was completed, operations personnel decided
to remove the 2D LCVU for PM.                              The 2D LCVU was removed from                              ,
service at 10:55 a.m.            While both LCVUs were out of service, lower
containment temperature increased. To compensate for the
temperature increase, control room operators adjusted the
o)eration of the remaining inservice LCVUs (2B and 2C) from
  "iormal" to "High Speed." and then to " Max Cool." However, for a                                                      !
brief period of time lower containment temperature had exceeded
the high high temperature Operator Aid Computer (0AC) alarm
setpoint of 115.6'F and the adjusted TS limit of 117.2*F.
ultimately reaching 117.4'F. Lower containment temperature was                                                        ,
                                                                                                                      '
above 117'F for approximately 3 minutes before it was restored to
within TS limits. The Action required by TS 3.6.1.5 was to
                                                                                                                        ,
                                                                                                                        i
restore the air temperature to within the limits within 8 hours or
be in at least hot standby within the next 6 hours. Since the
                                                                                                                        .
                                                                                                                      !
bich lower containment temperature existed for only a few minutes.                                                    -
th6 licensee was in compliance with the TS action.                                                                    .
At anroximately 11:10 a.m., operations personnel decided to post)one
the M on the 2D LCVU. recall the associated tags and return the _CVU to
service until the 2A LCVU was restored to operation. While operators                                                  i
were returning the 2D LCVU to service and all three LCVUs to normal
alignment, the YV chillers in service (A and C) trip >ed on low flow.
Based on a review of the circumstances surrounding t1e trip of the A and                                              ,
C YV chillers, the inspector discerned that the following took place.
When the B and C LCVUs were taken to " Max Cool" in an effort to reduce                                                !
lower containment temperature, the flow control valves in the chiller
loop fully opened as designed, and thermostatic control of,the chilled
water supply was lost. When operations subsequently restored the D LCVU
to service and returned the LCVUs to normal operation, thermostatic                                                      i
control of the flow control valves was reinstated. The existing
temperature caused the flow control valves to throttle closed, and the
chillers tripped on low load. Normal alignment with the A and B YV
chillers was established within 30 minutes of the chiller trips. The C
YV chiller had also been restarted, but tripped after running for 10
minutes.            Shortly thereafter, containment temperatures were restored to
normal levels.
Operations surveillance procedure PT/1/A/4600/02A. Mode 1 Periodic
Surveillance Items. Enclosure-13.1. Periodic Surveillance Items Data,
approved January 23, 1997, provides surveillance acceptance criteria in                                                -
accordance with the lower containment temperature limits imposed by TS
3.6.1.5. Lower containment minimum and maximum air temperature limits
are based on the average inlet temperatures of the operating LCVUs.
Temperature readings associated with non running LCVUs provide
indication of static air temperature and therefore, are not used to
determine average containment air temperature.                              Therefore. temperature
':mits are adjusted conservatively as a function of uncertainty (because
of the reduced sample size) in generalizing local indications to average
                                                                                          Enclosure 2
                                                                                                                      1
      ..-._..__ ,,
                  -
                              ,a..
                              -
                                    ._-..,....,--...--m.__-      -
                                                                                    -      - - _ _ - _ . . _ . . .-m.
 
                                  9
containment air temperature. As the number of LCVUs in service
decreases, the temperature limit decreases (becomes more conservative).
With two LCVUs running. the lower containment TS limit of 120*F was
adjusted to 117.2'F.
The Containment Lower Compartment Ventilation Subsystem as
described in the FSAR is designed to maintain a maximum
temperature of 120*F in the lower compartment during rnrmal plant
operation. During normal operation, three units (each providing
33.3% capacity) are in service, and one unit is on standby.
Technical Specification Interpretation 3.6.1.5 states that                  3
                                                                            !
containment air temperature can be maintained with one active
component out-of-service (i.e., three LCVUs in service).
Based upon a review of the FSAR and TS as well as discussions
with on-shift operators, the inspector determined that the                  4
decision to remove the D LCVU from service while preventive
maintenance (PM)s on the A LCVU were ongoing was non conservative
and caused lower containment temperature to exceed the adjusted TS
limit.
The inspector also determined that problems existed with procedure
OP/2/A/6450/01. Containment Ventilation Systems. dated June 15. 1994,
which controls the configuration of the LCVUs. The procedure did not
provide adequate guidance to address the impact of removing two LVCus
from service on lower containment temperature. Operations Management
Procedure 2-18. Tagout Removal and Restoration Procedure. Revision 46.
Responsibility 4.8. states that the person placing or removing tag (s)
shall check procedures affected and any outstanding tagouts associated
with that procedure / system for any adverse effects. Because the adverse
impact of removing 2 LCVUs from service was not addressed in the
procedure, this responsibility could not be effectively realized.
  n addition, procedure OP/2/A/6450/01 did not address the interaction
between LCVU operation and integrated Containment Ventilation (VV)
Systems. Step 2.7.3 of OP/2/A/6450/01. Enclosure 4.12. LCVU Additional
Cooling and YV Chiller Trip Prevention directs the operator to ensure
that three LCVUs are in the " NORM" position. The performance of this
step caused the A and C YV chillers to trip. Procedure
slowly reduce the demand on the system was not provided,      guidance
                                                          nor was  a      to
precaution or note provided to warn of the potential to induce a chiller
trip as a function of load demand changes.
The inspector also noted that no procedure guidance was available for
swapping between running and_non running LCVU units. OP/2/A/6450/01.
Enclosure 4.2. Lower Containment Ventilation Unit Startup and Normal
Operation, provided procedural guidance for starting up the system by
placing three LCVUs in operation. Enclosure 4.7. Lower Containment
Ventilation Unit Shutdown provides procedural guidance for shutdown of
the system by placing all four LCVU switches in the OFF position.
                                                              Enclosure 2
                                                -
 
l
                                              10
          However, no procedural guidance existed for stopping an individual LCVU
          and subsequently restarting it or making other required alignment
          changes needed to facilitate the performance of the PM. The inspector
          recognized that this lack of procedural guidance was unrelated to the
l
          lower co'itainment temperature increase and the YV chiller trips.
          The inspector also identified a minor discrepancy in the planned
l        innage work schedule.    The 2A LCVU had two work items planned to
          be worked which included a PM and electrical motor testing.      The
          PM on the 2A LCVU was scheduled to be completed at 12:00 p.m. on
          June 30, 1997. The motor electrical testing on the 2A LCVU was
          scheduled to be completed at 1:00 p.m. on June 30. The PM on the
          20 LCVU was scheduled to commence at 12:00 p.m. on June 30.
          immediately following the scheduled completion of the PM on the 2A
          LCVU.
                  This schedule allowed both the A and 0 LCVUs to be out of
          service for 1 hour, which was non conservative and not in
          accordance with the alignment described in the FSAR.
    c.  Conclusions
          The inspector concluded that the decision to deviate from the
          preferred normal alignment of LCVU operation to support planned
          maintenance exhibited non conservative work scheduling and
          operator judgement. As a result. lower containment temperature
          increased slightly above the adjusted TS limit for a brief period
          of time. However, temperatures were reduced below the adjusted TS
          limit within 8 hours as required by the TS action requirement.
          Therefore, exceeding the lower containment air temperature on
          plant equipment had minor safety significance and did not pose a
          threat to safety related equipment. The LCVU operating procedures
          did not address the adverse impact of removing two LCVUs from
          service. simultaneously. nor did the procedure address the
          interaction between LCVU operation and integrated containment
          ventilation systems. These procedural inadequacies constituh a
          violation of TS 6.8.1. Procedures and Programs. This failure
          constitutes a violation of minor significance and is being treated
          as  a NCV. consistent with Section IV of the NRC Enforcement
          Policy.  This item is identified as NCV 50-414/97-09-02:
          Inadequate LCVU Operating Procedure.
  08
        ,
          Hiscellaneous Operations Issues (92901)
  08.1    (Closed) Un.reigh.ed_Ltem (URI) 50-413.414/94-13-02: Emergency Operating
          Procedure (EOP) 50.59 Evaluations Not Reviewed by Nuclear Safety Review
          Board (NSRB) as Required by TS
          This item was related to an apparent failure to meet the TS requirement
          for the NSRB to review 50.59 evaluations for E0P changes. The
          inspector's review determined that the re
          being appropriately reviewed by the NSRBThe  quired  50.59 evaluations
                                                            licensee's            were
                                                                      procedures had
                                                                          Enclosure 2
 
  __-_______ __-_ - _ _ - .
                                                      11
  been inconsistent in defining the 10 CFR 50.59 screening evaluation and
  the 10 CFR 50.59 Unreviewed aafety Question (US0) evaluation. The TS
  requirement was intended for the NSRB to review the 10 CFR 50.59 U50
  evaluations. Nuclear Site Procedure NS0-209, 10 CFR 50.59 Evaluations.
  Revision 6. was revised after 1994 to clearly define the two
  evaluations. The licensee initiated a change to NSD 703. Administrative
  Instruction for Station Procedures, to clearly distinguish on the
  procedure change process documentation whether the evaluation performed
  was a screening evaluation or an USQ evaluation. The inspector reviewed
,
' three US0 evaluations for E0P changes and verified the US0 evaluation
i
  had been sent to the NSRB_for review. A 1995 evaluation had been
  reviewed and two 1997 evaluations were scheduled for review at the next
  NSRB meeting. The inspector concluded that this issue was adequately
;
  resolved and the TS requirements had been met by the licensee.
  During the invettigation of the above issue, the inspector reviewed
  a) proximately 20 examp',cs of 10 CFR 50.59 screening evaluations for E0P
  c1anges and identified a deficiency in the licensee's procedure
  implementation of this activity. Specifically, the justifications for
  the screening questions were inadequate in many changes.                      The
  justifications were inadequate in that they only repeated the screening
  question as a negative statement. NSD 209, 10 CFR 50.59 Evaluations.
  Revision 5. required the doca,3ntation of justification for responses to
  50.59 screening questions. It further stated that justifications should
  be complete enough so that an independent reviewer cculd come to the
  same conclusion. The following E0P change 50.59 screening evaluations
  were inadequate and did not meet the applicable procedure requirements:
  o                          EP/2/A/5000/FR 1.2 dated November 17, 1995
  e                          EP/1/A/5000/FR-1.1 dated September 19. 1996
  *                          OF/1/A/6350/08 dated February 28. 1996
  e                          EP/2/A/5000/F-0 dated March 26, 1997
  e                          EP/1/A/5000/FR H.1 dated August 16, 1996
  *                          EP/1/A/5000/FR-H.1 dated January 30, 1995
  This failure to follow NSD 209 for 10 CFR 50.59 screening evaluations,
  is identified as the first example of Violation (VIO) 50 413.414/9/-09-
  04:                      Failure to Follow Procedure. The inspector did not identify any
  US0 condition related to the inadequate 50.59 screening evaluations.
  The inspector noted that the 50.59 screening evaluations for E0P changes
  were performed by the Operations organization. Previous inspections of
  50.59 evaluation performance have concluded that the Engineering
  organization performed to a high standard in this area for 50.59
  evaluations related to modifications. Although both organizations
                                                                                  Enclosure 2
 
                                          12
        receive the same training and use the same procedures. Operation's
        performance in this activity was deficient as previously noted. The
        inspector reviewed a 1997 50.59 USO evaluation for an E0P change.    This
        evaluation was good in that it included a well detailed justification
        for responses to the USQ evaluation questions. This indicated that the
>
        Operations deficient performance was related only to the 50.59 screening
        evaluations.
                                    II. Maintenance
l
  M1    Conduct of Maintenance
1
  M1.1 Electrical Flash Durinn Breaker Preventive Maintem nte
    a. Inspection Stone (62707)
        The inspector reviewed the circumstances and the licensee's corrective
        actions associated with an electrical flash that occurred inside a 600
        Volt non safety-related breaker cubicle while periodic breaker PM was
        being performed. The electrical flash resulted in a minor personnel
        injury and extensive damage to the breaker cubicle.
    b. Observations and Findinas
        On June 3. 1997, an Instrumentation and Electrical (IAE) technician was
        aerforming PM on 600 Volt breakers 2MXM-F09C and 2MXM-F090.    These
        areakers supplied power to two Unit 2 ice condenser refrigeration air
        handling fans. The PM activity involved testing the overcurrent
        protective devices associated with the breakers. The technician had
        removed breaker F09C from its cubicle and was in the process of removing
        breaker F090 from its cubicle. While removing F090, an electrical ficsh
        occurred in the F09C cubicle, which was located directly above F09D.
        The technician received minor facial burns. but was not seriously
        injured. Breaker F09C was electrically welded in its cubicle as a
        result of the electrical fault, The inspector responded to the breaker
        work location and noted good licensee immediate actions in response to
        the incident. These actions included terminati'      11 PM work, roping
        off the area for personnel safety consideratior . nd initiating a
        Failure Investigative Process (FIP) to determine the root cause of the
        electrical fav a.
        On June 6, 1997. Motor Control Center 2MXM was de energized, and the
        breaker cubicle for F09C inspected. The damage to the bus was minimal;
        however, the stabs for F09C were badly damaged and recuired replacement.
        Both breakers F09C and F09D were repaired, tested, anc returned to
        service. The inspector attended the PORC meeting conducted to discuss
        the repair plans and noted that management performed a thorough review
        of the plans with good discussions on the impact of the work planned on
        the plant. The repairs were completed without incident.
                                                                      Enclosure 2
 
  _____                -
                                                13
              The FlP team was thorough in their investigations and determined that
              the stabs b? hind breaker F09C had come in contact with the energized
              bus.  Since the breaker power connecting cables had been determed and
              left untaped in the bottom of the breaker cubicle. an electrical ground
              path was created when the cables were re energized. The FIP determined
              the method for racking the breaker out in the maintenance position was
              inadequate.    In the maintenance position a lock tab on the front of the
              breaker cubicle had been used to position the breaker away from the bus;
l              however this method did not provide sufficient distance between the bus
              and stabs. While this method had not resulted in any problems in the
              past, the result of having two breakers in the maintenance position,
              located one above the other, created an even smaller bus / stab distance
              that resulted in electrical flash over.
              As a result of the FlP investigations, instrumentation procedures
              governing work on 600 Volt breakers were revised to change the method of
              racking out these breakers for maintenance. Instead of using the lock
              tab, procedures directed that a padlock be placed on the breaker or the
              bteaker be removed completely to ensure adequate stab / bus distance is
              maintained. In addition, IAE personnel involved with breaker work were
              to be provided training on this new method of racking 600 Volt breakers
              out to the maintenance position.
        c.  Conclusions
              The inspector concluded that the FlP team was thorough in investigating
              the cause of the electrical flash. The root cause evaluation revealed
              configuration weaknesses in the method of locking out 600 Volt breaker
              cubicles to the maintenance position. The inspector determined that the
              licensee adecuately implemented corrective actions to prevent recurrence
              of this incicent.
        M1.2 'Jngdeounte Leak Rate lest of Unit 2 Containment Isolation Valve
        a,    insoection Scope (40500. 61726. 62707)
              On June 4,1997, the licensee identified that Unit 2 containment
              isolation valve 2NV 874 had not been properly Type C leak rate tested in
              accordance with 10 CFR 50. Appendix J during the previous. refueling
              outage. On June 6. the valve was properly tested and failed the Type C
              leak rate test. -The valve disc was replaced, and the valve was
              successfully tested on June 7. The licensee submitted LER 50 414/97-004
            . to document the inadecuate leak cate test conducted during the outage.
              The inspector reviewec the circumstances associated with the inadequate
              testing, attended PORC meetings to discuss retesting valve 2NV-874
              online, witnessed aspects of the June 6 retest, reviewed leak rate test
              results, and discussed the incident with engineering and Operations Test
              Group (OTG) personnel,
                                                                            Enclosure 2
                                                                  _          -
 
i
                                      14
  b. Observations and Findinas
    On &ne 4.1997 the OTG Suaervisor was conducting a procedure
    completion verification of Jnit 2 Periodic Test (PT) procedure
    PT/2/A/4200/01C. Containment Isolation Valve t.eak Rate Test. This
    procedure had been performed during the previous refueling outage in
1
    April 1997. During the review, the supervisor idcntified that Step
    2.2.3 of Enclosure 13.7. Penetration No. M228 Type C 1.eak Rate Test had
    been marked "Not Applicable'' by the OTG technician performing the test.
                                                                                ,
                                                                                I
    resulting in the step not being performed. This step required test vent    I
    flow path valve 2NV 873 to be opened while testing inside containment
    isolation check valve 2NV 874 (associated with the Standby Makeup System    '
    flowpath to the reactor coolant pump seals). Without an open test vent
    flowpath, the leak rate test on 2NV 874 had been invalid.
    The inspector verified that appropriate actions were implemented upon
    identification of the invalid lea ( rate test. These actions included
    2NV 874 being declared inoperable and in accordance with TS 3.6.3, the
    outboard containment isolation valve (2NV 872A) in the penetration was
    closed and power was removed from the valve operator within four hours.
    The inspector attended the June 5 and 6 PORC meetings conducted to
    discuss activities to retest 2NV-874. Management thoroughly discussed
    the impact on the plant with testing the valve while online. In
    addition engineering developed a special leak rate test procedure and a
    detailed briefing package explaining the necessary actions for
    controlling the retest activities.
    On June 6. the inspector witnessed aspects of the leak rate test on 2NV-
    874. The inspector noted that testing was well controll?d and performed
    in accordance with the test procedure.- The valve was not able to be-
    pressurized and resulted in-a failed leak rate test. Valve maintenance
    was performed resulting in replacement of the valve disc and disc
    spring. A subsequent leak rate test was performed following the
    maintenance activity. The inspector reviewed the results of this
    testing which verified that leakage was within acceptable limits.
    Following successful testing 2NV 874 was declared operable and the
    penetration was returned to its normal configuration,
  c.    n
    C_Qn.clusions
    The inspector concluded the identification by the OTG Supervisor of a
    procedure discrepancy that resulted in an invalid leak rate test of nD-
    874 was an example of good questioning attitude. The PORN performed a
    thorough review of subsequent activities to properly perform the leak
    rate test. Good engineering support was )rovided, both in developing a
    leak rate test procedure and briefing paccage for the evolution.
    The inspector noted that the procedure completion review was not
    performed by the OTG Supervisor following actual completion of all
    testing or prior to plant startup from the refueling outage. Since this
                                                                  Enclosure 2
            _ _ _ _
                                                                              -
 
  . . - _ .    __-          --_          ---            - -            -    - - . . - - _-                    _.
                                                      15
l                  was the only review that was recuired following test procedure
                    completion, the inspector consicered the review untimely. Had this
                    review been completed prior to plant startup, this problem may have been
                    identified and corrected arior to the unit entering a mode recuiring
                    containment integrity. T1e failure to open test vent valve 2hV-873
                    during/4200/01C
                    PT/2/A              was identified as a violation of TS 6.8.1.          leak
                                                                                          This    rate testing of
                                                                                                issue
                    is identified as Violation E0-414/97-09 03: Failure to Follow Procedure
                    Results in Invalid Local Leak Rate Test of Valve 2NV 874.
            M8      Miscellaneous Maintenance Issues (92902.
l          M8.1 (Closed) VIO 50 413. 414/97-01-01: Failure to Include all Structures.
                    S stems and Components in the Scope of the Maintenance Rule as Required
                    b 10 CFR 50.65
                    This violation was identified when the inspectors determined that the
                    licensee had incorrectly excluded a number of structures. systems and
                    components from the scope of the Maintenance Rule. The licensee
                    acknowledged the violation and issued a Problem Investigation Process
;                  (PIP) report PIP No. 0 C97-0419. to document correctivo actions taken
!                  and, track the progress made in addressing the issues. The systems
                    affected included Nuclear Sampling (NM). Main Steam to Auxiliary
                    Equi) ment (SA). Auxiliary Building Chilled Water (YN) and Ice Condenser
l
'
                    Hitti Pins (NF). Following a review by the site Expert Panel these
                    systems or components were added to the scope of the Maintenance Rule.
                    Corrective actions taken or planned included a review of the 239
'
                    functions that had been excluded from the Maintenance Rule scope. This
                    review was scheduled for completion in December 1997.- and will be
                    documented in PIP No. 0-C97-0419, In addition, structures and functions
                    excluded from the Maintenance Rule will be reviewed for Generic Scoping
                    applicability. The due date for this review is also December 1997. The
                    inspectors concluded the licensee's corrective actions were appropriate.
,
            M8.2. (Closed V10 50-413.414/97 01-04: Failure to implement the Requirements
                    of (a)(1) and (a)(2) of the Maintenance Rule
l                  This violation was identified when the inspectors determined that the
l                  licensee was using Forced Outage Rate (FOR) instead of Unplanned
l                  Capability loss Factor (UCLF) as a Plant Level Performance Criteria for
'                  monitoring A2 systs....; 3er 10 CFR 50.65. The concern was that FOR was
                    not as sensitive as UC F in detecting declining performance in some
                    systems.
                    The licensee acknowledged the violation and took appropriate action to
                    correct the problem. The licensee incorporated the Plant Transient
                    Criteria as part of the Forced Outage Criteria. This combination of
                    criteria was intended to provide appropriate equivalent defense in depth
                    monitoring as the Unplanned Capability Loss Factor. A Plant level
                                                                                          Enclosure 2
l
                                                      ._                                -      --      -
 
                                                                                          1
;
                                              16
l
            Performance Criteria called Plant Transients, which defined unacceptable
            performance was added to Engineering Directives Manual (EDM)-210 as Rev.
i
'
            4.    The inspectors concluded the licensee's corrective actions were
            appropriate.                                                                  l
                                                                                          I
      M8.3 (Closed) Insoector Followuo item (IFI) 50 413.414/97-01-02: Followup and
                                                                                          '
            Review of Licensee Procedure to implement the Requirements of (a)(1) and
            (a)(2) of the Maintenance Rule after issuance of Regulatory Guide 1.160,
            Rev.2
i
            EDM-210." Requirements for Monitoring the Effectiveness of Maintenance
            at Nuclear Power Plants or the Maintenance Rule " Rev. 5. revised the
            definition of Maintenance such that it was now in agreement with
            Regulatory Guide 1.160. Rev. 2, dated March 1997. Revision 5 of the EDM
            now considers any operator action performed in support of Maintenance as
            a Maintenance Preventable Function Failure (MPff) candidate. In
            addition, the flow gra)h of Appendix A to the subject EDM, were revised
            for clarity. One of tie two was revised from Vendor Error to Off-site
            Vendor Services while the other from Operations or Plant configuration
            control to Operation or Plant Configuration Control not associated with
            a maintenance activity. The inspectors concluded the licensee's
i
            corrective actions were appropriate.
      M8.4 (Closed) IFT 50-413.414/97-OL-01 Followup on Licensee Actions to
            Provide Performance Criteria for Structures After Resolution of this
            Issue
            EDM-210. " Requirements for Monitoring the Effectiveness of Maintenance
:          at Nuclear Power Plants or the Maintenance Rule." Rev. 5. changed the
            3erformance criteria for all Maintenance Rule structures to comply with
            legulatory Guide 1.160. Rev. 2. This criteria applies to both risk and
            non-risk significant Maintenance Rule structures.
            EDM 410. " Ins)ection Program for Civil Engineering Structures and
            Components." Rev. 1. dated June 16, 1997, is the controlling document
            for monitoring and assessing civil engineering structures and' components
            to the requirements of 10 CFR 50.65 and Regulatory Guide 1.160,.Rev. 2.
            dated March 1997. It provides examination guidelines, acceptance
            criteria and documentation requirements. As such. Catawba civil
,
            engineering was responsible for implementing the ins)ection program for
l          structures and components. The inspectors reviewed EDM-410. Rev. 1 for
            content and adequacy. The inspectors noted that the procedure provided
            adequate guidelines and the acceptance criteria contained within,
            followed Regulatory Guide 1.160. Rev. 2 guidelines for acceptable and
.          unacceptable performance criteria.
l
l          Through discussions and document review, the inspectors ascertained that
            the inspection program for structures was adequately administered and
            implemented. Responsible engineers had received training and were
            familiar with Maintenance Rule requirements as they applied to their
            area of responsibility.
5
                                                                          Enclosure 2
L ___  _--      _ . _ _      _.          ..  . _ __..      _    _  _        _  __  , /
 
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _                                                __                - _ __                _________
                                                                                      17
                                                  At the close of this inspection. 39 structures had been inspected and an
                                                  additional 120 were scheduled for inspection by year's end. Ins)ection
                                                  per the revised EDMs -210 and -410 commenced on July 1, 1997.                  T1e
                                                  inspectors reviewed the licensee's classroom training material. ES-CN-
                                                  97-21. used to cormiunicate Regulatory Guide 1.160. Rev. 2 guidelines.
                                                  Training of personnel was held between June 9 and 18. 1997. The
                                                  inspectors concluded the licensee's corrective actions were ap]ropriate.
                                                                              III. Enaineerina
                                          El      Conduct of Engineering
                                          El.1 Primary and Secondary Thermal Power DiscreDancy
                                            a. -Insoection Stone (37551)
                                                  On July 15 the licensee discovered a discrepancy of approximately 0.6%
                                                  between the Unit 2 primary and secondary thermal power indications.
                                                  Secondary thermal
                                                  was reduced to 99.7%)power
                                                                          andwas  immediately
                                                                                a FIP  team was reduced
                                                                                                    initiated to  to determine
                                                                                                                      99.3% (reactor
                                                                                                                                  the power
                                                  cause of the discreaancy. The inspector attended management briefings
                                                  by the FIP team mem)ers on the progress of their investigation: reviewed
                                                  associated TS and TS Interpretations: and discussed the issue with
                                                  Operations. Engineering and Maintenance personnel.
                                            b.  Observations and Findinas
                                                  On July 15. Operations personnel were notified by the reactor
                                                  engineering group that there was a 0.6% discrepancy between primary and
                                                  secondary thermal power indications, and that actual thermal Jower might
                                                  be greater than the secondary thermal power (the designated tiermal
                                                  power best estimate) indication. The reactor engineering group
                                                  discovered, during a routine review of secondary plant parameters, that
                                                  primary thermal power had slowly increased over time since the Unit 2
                                                  restart from the April 1997 refueling outage. A FIP team was initiated
                                                  to determine the cause of the discrepancy, and control room operators
                                                  decreased reactor aower to 99.3%. Tae reactor was operated at 99.3%
                                                  power until the FI) team could determine the cause of the discrepancy.
                                                  The FIP team determined, during the course of their investigation, that
                                                  theT,Yto586.9F.
                                                  587.3              indication  had responded
                                                                        Operations  been drifting    downward T,,,
                                                                                                by decreasing            since May 11, 1997, from
                                                                                                                            to minimize
                                                  the T * /T error. Lowering T,,, caused the reactor to increase AT to
                                                  maint'aIn,r,,actorpowerequaltosecondarypower.
                                                            e                                                    The drift in the T,,,
                                                  indication resulted in changes in T        Tm T,,, and AT but did not
                                                  cause a change in indicated or actud3 primary and secondary thermal
                                                  power. Although the FIP team could not attribute this indication drift
                                                  to the primary / secondary thermal power indication discrepancy they
                                                  determined that a degraded 7300 process card was responsible for the
                                                                                                                              Enclosure 2
                                                                                                _.                .    -                  . -  . . _ .
 
                                                                                          }
                                                                                          l
                                  18
drift and initiated plans to have the card replaced after the root cause
of the power indication discrepancy was identified.
The FIP team also determined that indicated feedwater flow had decreased
while steam flow had remained constant. This was attributed to
feedwater venturi defouling as a function of the new cycle (restart from
the April refueling outage was in early May). the recent reactor trip
(June 26), and was the recent rapid downpower (July 2). The result of
defouling was a decrease in indicated feedwater flow with a
consequential decrease in indicated secondary thermal                Operations
maintains secondary Thermal Power Best Estimate (TPBE) power.
                                                          near 100% by
periodically opening flow control valves, which in turn causes primary
power to increase to maintain T
defouling caused an increase in.,,    for and
                                  actual 100%  power level.
                                              indicated      The
                                                        primary        gradual
                                                                  thermal
power, as well as actual secondary thermal power. However, the
resultant discrepancy between indicated and actual secondary thermal
)ower accounted for approximately 0.10% to 0.15% of the 0.6% discrepancy
)etween primary and secondary indicated thermal power.
The major contributor (0.3% to 0.4%) to the discreaancy between primary
and secondary thermal power was determined by the IP team on July 16 as
hot leg streaming. According to Westinghouse, hot leg streaming refers
to the inability to accurately characterize bulk hot leg temperature.
The licensee examined data from the Unit 2 Beginning of C.rcle and
identified changes in the behavior of this phenomenon from previous
cycles. S)ecifically. calculations revealed that indicated Tw had
increased ay 0.2*F and caused indicated primary thermal power to
increase. As discussed above these changes were originally masked by
the decrease in primary tem                                                            -
T,,,/T,,, as a function of T,,,peratures  accompanying the decrease in
                              indication drift.
Hot leg streaming has occurred in previous cycles on both units and has
resulted in as high as a 1.0% difference between primary and secondary
thermal power. To account for this, an adjustment factor in the OAC
calculation corrects the discrepancy.
The FIP team concluded that sea:dary thermal power had always been
accurately and correctly indicated, and that primary thermal power
indication did not reflect an actual increase in power level above TS
limits. The inspector discussed the impact of the primary thermal power
indication on Reactor Protection System setpoints and functions.
According to the reactor engineering group, the venturi defouling and
hot leg streaming factors did not constitute a sufficient temperature
error to warrant adjustment via the Reactor Coolant System (RCS)
Temperature Calibration Procedure, which is run quarterly. The OPAT and
OTAT trip strings remained within their TS limits. In addition, the
nuclear instrumentation system is calibrated to secondary thermal power,
so the associated overpower trip setpoints were unaffected.
                                                                Enclosure 2
                                                                                          ,
                                                                _,
                                                                    -
                                                                        -.-.-.c. _. ---
 
                  _ _ _ _ - _ _ _ _ - - - - _ _ _ _ - - - - -
                                                                - - - - - -
                                                                                            -
                                                              19
            Reactor Power was increased to 99.5% on July 16 and the degraded T,q
            card was replaced on July 17. The inspector attended the prejob brief
            for the card replacement and observed the work activity in the control
            room. The replacement was successfully completed within less than 1
            hour and without incidence. At the end of the inspection period, the
3a          license was considering either performina periodic manual calculations
            to the correct the thermal power aiscrepancy, or conducting a full
            calorimetric to account for the deviation.
        c. Conclusiqn_q
                                                                                              ,
*          The inspector concluded that the licensee's identification of the
E          thermal power discrepancy exhibited attention to detail and a thm
            review of plant data. Actions to initiate a FlP team to invr a
g          root cause were appropriate, and steps to reduce reactor po'
            discrepancy was understood were conservative and indicative
            positive nuclear safety ethic. Replacement of the faulty T,            ,a was
            well-planned. coordinated and controlled, and executed in an expeditious
            manner.
      E2    Engineering Support of Facilities and Equipment
    .
      E2.1 Review of Corrective Actions
        a. Inspedjon Scooe (37550. 92903)
            The inspector reviewed Engineering corrective actions to resolve open
            itens identified during the development of the station Design Base
            Documents (DBDs) and findings from Self-initiated Technical Audits
            (SITAs). Also reviewed were the licensee's actions to address a 10 CFR
            Part 21 issue related to a defective Emergency Diesel Generator (EDG)
            intake / exhaust valve spring. Anplicable regulatory requirements
            included 10 CFR 50 Appendix B. ESAR. Technical Specifications and
            implementing licensee procedures.
        b. Observations and Findinos
            DS_Qs
            Developed between 1990 and 1994. DBDs consolidated design and licensing
            documentation for selected station systems and programs. The ]rocedure
            guidance for development and maintenance of DBDs was provided ay
            Enoineering Directives Manual . EDM-170. Design Specifications, revision
'
            5. Open items were evaluhed for operability during the DBD development
            and Licensee Event Reports (LERs) initiated as required. EDM-170
            required the remaining items to be entered into the Problem
            Investigation Process (PIP) for tracking and resolution. Additionally,
            the l u ensee's February 10. 1997. response to the 10 CFR 50.54f letter
            related to the Adequacy and Availability of Design Basis Information.
  P        stated that DBD open items woeli be ente 1 4 into the PIP for trackir.g
N          and resolution.
                                                                                Enclosure 2
  .
                                                                            Mi
 
                                  20
TM inspector reviewed the resolution of open item in the Reactor
coolant System DBD to sample the adecuacy of item resolution activity.
Approximately 20 items were evaluatec to verify that the PIP and
interfacing station programs evaluated and resolved the open item
issues.  The items were adequately resolved.
An independent industry audit of Catawba in late 1996, identified as a
finding the numerous lon9-term unresolved DBD open items. The response
to the finding was to initiate a blanket PIP (PIP 0-C97-0595 dated
March 5,1997) to cover the systems with the identified open items.
Many of these open items were not previously in the PIP process. The
PIP corrective actions established a schedule to resolve and close the
referenced DBD open items by September 1. 1997,
During this inspection, the inspector identified additional E      'en
items which were not entered into the PIP process nor incluau .d the
blanket PIP. The open items.were included in DBD CNS-1435.00-0002. Post
Fire Safe Shutdown, revision 4. and DBD CNS-1465.00-00-0018. Station
Blackout (SBO) Rule, revision 2. Although not entered into the PIP
3rocess. the licensee provided meeti g documentation indicating the Post
rire Safe Shutdown open items were being evaluated. These items were
identified by a November 1995 electrical post fire shutdown review
performeo after the initial DBD development and entered into the DBD by
revision 4 at that time. There was no c: :umented evaluation of
o)erability  or A
tie PIP process.ppendix    R commitments
                    Following            which
                                the inspector's    would haveof
                                                identification been
                                                                this addressed
                                                                    issue    by
the licensee initiated PIP 0-C97-1918 to track resolution of these open
items. The inspector identified no significant safety concerns related
to the open items reviewed. This failure to follow procedure for
resolution of DBD open items is identified as the second example of
Violation 50-413.414/97-09-04: Failure to Follow Procedure.
                                                                                  *
SITAS
The ins)ector reviewed a recently comp'eted SITA report dated June 11.
1997, w11ch reviewed the adequacy of resolution of SITA findings. The
scope of the audit was good in that it reviewed the resolution of 80
findings from four previous SITAs. The depth of the audit was good in
that corrective act ans were verified through the extent of station
programs (e.g. . PIP work requests, modification etc. .) involved in the
resolution. The findings were well defined and demonstrated an
independent and objective audit. Corrective actions for the findings
hcd not yet been developed.
EDG 10 CFR Part 21 Notice
The inspector ruiewed the licensee's actions to address a Cooper
Industries 10 CFR Part 21 notice regarding potentially defective EDG
intake / exhaust valve springs which was applicable to Catawba. The
notice was initiated in 1991 and revised on May 1. 1997. The licensee
had included an inspection for the spring defect into the EDG
maintenance procedure. A defective spring was identified at Catawba in
1996. The spring was replaced. analyzed, and sent to the vendor for
                                                                                  '
                                                              Encloture 2
                .                                                      _
 
    ._.            _ _ _ _        ..      ..
                                                          .      .    ..  .
                                                                              .      ..
                                                  21
              further analysis.      The licensee's respon.e to the notice on this issue
              was appropriate,
          c. Conclusions
              Resolution of DBD open items was generally adequate in that no safety
              significant issues were identifieo in the open items. A violation was
              identified for failure to follow licensee procedure requirements to
              enter open DBD open items into the station PIP process for tracking and
.            resolution. The audit of SITA corrective actions demonstrated that the
              licensee was aggressively following SITA findings and is identified as a
              strength in corrective action performance. Additionally, the licensee
              adequately addressed the EDG 10 CFR Part 21 issue related to potentially
              defective intake / exhaust springs.
        E3    Engineering Procedures and Documentation
        E3.1 Chanaes. Tests. and Exneriments Performed in Accordance With
              10 CFR 50.59 (thru December 31. 1996)
          a. Insoection Scone (37551)
                                                                                          '
f
              By letter dated March 31, 1997. Duke Power Company (the licer.see)
              submitted its annual summary of all changes, tests, and experiments,
              which were completed under the provisions of 10 CF,150.59 for the period
              through December 31. 1996. The licensee's March 31, 1997, summary
              included approximately 380 changes made during the subject period. The
              inspector evaluated these changes against the p,avisions of the
              regulation.
                                                                                          <
          b. Observations and Findinas
              In accordance with 10 CFR 50.59, a licensee may:      (1) make changes in
              the facility as described in the safety analysis report, (2) make
              changes -in the procedures as described in the safety analysis report,
              and (3) corduct tests or experiments not described in the safety
              analysis report, without prior Commission approval, unless the change
              involvy a changc in the Technical Specifications or an Unreviewed
              Safety duestion (US0). The regulation defines an US0 as a proposed
              action that: (a) may increase the probability of occurrence or
              consequences of an accident or malfunction of equipment important to
              safety previously evaluated in the safety analysis report, or (b) may
              create a possibility for an accident or malfunction of a different type
              than any previously evaluated in the safety analysis report or (c) may
              reduce the margin of safety as defined in the basis for any Technical
              Specification.
              The inspector reviewed the licensee's current (dated March 10. 1997)
              version of Nuclear System Directive 209. "10 CFR 50.59 Evaluations."
              which is patterned after NSAC-125. " Guidelines for 10 CFR 50.59 Safety
                                                                              Enclosure 2
  .
 
      _ _ _ _        _--  __      --
                                        22
Evaluations." June 1989. This document requires that changes be
evaluated against the appropriate Final Safety Analysis Report (FSAR).
Technical Specifications, end NRC Safety Evaluation Report sections to
determine if there is need for revision.          Specifically, the criteria
specified by 10 CFR 50.59 are broken down into seven (7) questions. For
a change to be qualified for 10 CFR 50.59, the answers to all seven
questions must be "no". Based on review of this document, and the
review of the licensee's 10 CFR 50.59 evaluations. the inspector
concluded that the licensee's directive appropriately reflects the
criteria of this regulation and that. if followed accordingly, should
ensure that a change would be correctly performed under this regulation.
The inspector performed an in-office review of the licensee's summary to
determine the nature and safety significance of each change. Through
this review, the inspector selected the following changes for more
detailed review onsite:
e            Exempt Changes:
              Exempt Change CE-3176
              Exempt Change CE-3705
              Exempt Change CE-3759
              Exempt Change CE-4745
              Exempt Charge CE-4746
              Exempt Change CE-4821
              Exempt Change CE-4822
              Exempt Change CE-7416
              Exempt Change CE-7977
              Exempt Change CE-8126
              Exempt Change CE-8182
              Exempt Change CE-8245
              Exempt Change CE-8410
              Exempt Change CE-61008
              Exempt Change CE-61162
e            Miscellaneous Changes:
              SIMULATE (a computer code) Version 4
*            Modifications:
              NSM CN-11371
              NSM CN-20396
o            0:?rable But Degraded Evaluations:
              PIF 2-C97-0157
              PIP 2-096-3250
e            Operability Evaluations:
                                                                    Enclosure 2
                                        _
                                                                                ~
 
  . - _ _ _ _ _ _ _ _ _ _ - _ -
                                                              23
                                Operability Evaluation dated 2/15/94
                                Operability Evaluation dated 2/18/94
                                Operability Evaluation dated 6/28/94
  e                              Procedure Channes:
                                OP/1/A/6200/11
                                AM/2/A/5100/07
                                OP/2/B/6200/33. Change 4 Rev. 4
                                OP/1/A/6550/14
                                PT/1/B/4700/82
  The ins ector determined that these changes were correctly evaluated
  under t e provisions of 10 CFR 50.59
  During the in-office and onsite reviews, the inspector made a number of
  observations and has communicated them to licensee personnel:
  *                              The use of nuke-specific system identifiers in the annual summary
                                (which is submitted to the NRC and is thus available to the
l
                                public) is discouraged unless the licensee provides a key in the
l                                summary. These identifiers do not bear any apparent correlation
l                                to the actual systems (e.g. , NC = reactor coolant system. KC =
l                                component cooling system, etc..). The inspector made a similar
                                observation on the summary submitted on March 2~. 1996 (see
                                Inspection Report 50-413.414/96-10).
'
  o                              The licensee's corresponding revision of the UFSAR. per 10 CFR
                                50.71. lags behind 10 CFR 50.59 evaluations. The next u)date of
                                the UFSAR. scheduled for late 1997. should capture all tie changes
                                that are within the scope of the UFSAR.
  e                              While the licensee had acceptably evaluated all the changes
                                audited by the inspector, a number of them eppeared in the summary
                                with insufficient information for a reader to even determine what
                                system was involved, or what change was made. The inspector
                                recommended a several-sentence description. identifying the
                                system, the component, and the nature of the change, and
                                accompanied by a several-sentence evaluation. Despite this
                                problem with the summary, the evaluations were found to be
                                thorough and in compliance with 10 CFR 50.59. The licensee was
                                aware of this aroblem with the summary and has initiated actions
                                to correct suc1 weakness by revising its guidance document. NSD
                                209 (see Problem Investigation Process Form 0-C97-2027. dated June
                                19. 1997).
  *                              The term " Exempt Changes" may cause confusion in the context of 10
                                CFR 50.59.    It is a term internal to the licensee's docunentation.
                                It pertains to changes that "do not require the Modification
                                                                                          Enclosure 2
 
                            - _ _ _ _
                                                                                  1
                                                                                  b
                                                  24
              Program controls for configuration management and therefore are
              specifically exempted from the requirements to process an
              editorial NM or NSM." According to licensee personnel, an " exempt
              change" is essentially a minor change.
        e    The summary contained a significant number of errors, which stated
              the opposite of the actual facts. For example, test procedure
              TT/1/A/9200/88 states "there are Unreviewed Safety Questions
              associated with this test procedure" when the onsite evaluation
              shows that there was no unreviewed safety question. The licensee
              submitted a letter on July 9, 1997, correcting such errors.
    c.  Crnclusions
        Based on in-office review of the licensee's March 31, 1997, annual
        summary on 10 CFR 50.59 changes, onsite review of the licensee's 10 CFR
        50.59 evaluatius, and audit of the licensee's 3rocedures, the inspector
        concluded that the licensee had complied with t1e provisions of the
        regulation for the changes listed in the annual summary.
l
                                          IV. Plant Suocort
  R1    Radiological Protection and Chemistry Controls
  R1.1 Tours of the Radiolooical Control Area (RCA) (71750)
        The inspectors periodically toured the RCA during the inspection period.
t        Radiological control practices were observed and discussed with
!
        radiological control personnel, including RCA entry and exit, survey
        postings locked high radiation areas, and radiological area material
        conditions. The inspector concluded that radiological control practices
        were proper.
                                      V. Management Meetinas
  X1    Exit Meeting Summary
  The inspectors ) resented the inspection results to members of licensee
  management at t1e conclusion of the inspection on July 11 and July 23. 1997.
  The licensee acknowledged the findings presented. No proprietary information
  was identified. Dissenting comments were not received from the licensee.
                                                                      Enclosure 2
 
          _ - _ _ _ . - - - _
                                                                                  .,
                              -.    -
                                  t
                                                    25
                                    PARTIAL LIST OF PERSONS CONTACTED
  Licensee
  Bhatnager. A. . Operations Su>erintendent
  Birch. M. . Safety Assurance ianager
  Coy., S., Radiation Protection Manager
  Forbes. J., Engineering Manager
  Jones. R.. Station Manager
  Harrall. T., Instrument and Electrical Maintenance Superintendent
  Kelly. C.. Mainteriance Manager
  Kimball . D. , Safety Review Group Manager
  Kitlan. M., Regulatory Compliance Manager
'
  Nicholson. K., Compliance Specialist
  Peterson. G., Catawba Site Vice-President
  Tower. D., Regulatory Compliance
l
                                                                                      ,
4
                                                                      Enclosure 2
                                                                                    u
 
                _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ - _                      __
                                                                                            26
                                                                              INSPECTION PROCEDURES USED
  IP 37551:  Onsite Engineering
  IP 40500:  Effectiveness of Licensee Controls in Identifying. Resolving, and
              Preventing Problems                                                                                                    i
  IP 61726:  Surveillance Observation
  IP 37550:  Engineering
  IP 62707:  Maintenance Observation
  IP 71707:  Plant Operations
  IP 71750:  Plant Support Activitia
  IP 92901:  Followup - Operations
  IP 92902:  Followup - Maintenance
  IP 92903:  Followup - Engineering
  IP 93702:  Prompt Onsite Respense to Events
                                                                        ITEMS OPENED, CLOSED, AND DISCUSSED
  Opened
i
  50-414/97-09-01                                                          NCV          Failure to Declare Ice Condenser
                                                                                          Intermediate Deck Doors Inoperable and Log
                                                                                        Appropriate TSAIL Entry (Section C1.1)
  50-414/97-09-02                                                          NCV          Inadequate Lower Containment Ventilation
                                                                                        Unit Operating Procedure (Section 01.4)
'
  50-414/97-09-03                                                          VIO          Failure to Follow Procedure Results in
                                                                                          Invalid Local Leak Rate Test of Valve 2NV-
                                                                                        874 (Section M1.2)
  50-413.414/97-09-04                                                      VIO          Failure to Follow Procedure - Two Examples
                                                                                          (Sections 08.1. E2.1)
  Closed
  50-413.414/97-01-01                                                      VIO          Failure to Include All Structures Systems
                                                                                        and Components in the Scope of the
                                                                                        Maintenance Rule as Required by 10 CFR
                                                                                        50.65(b) (Section M8.1)
  50-414.414/97-01-02                                                      IFI          Followup and review of licensee procedure
                                                                                        to implement the requirements of (a)(1)
                                                                                        and (a)(2) of the Maintenance Rule after
                                                                                        issuance of Revision 2 of Regulatory Guide
                                                                                        1.160 (Section M8.3)
  50-413.414/97-01-03                                                      IFl          Followup on Licensee Actions to Provide
                                                                                        Performance Criteria for Structures After
                                                                                        Resolution of this Issue (Section M8.4)
                                                                                                                        Enclosure 2
 
- _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _                        _
                                                                                                                  27
                                                                        50-413.414/97-01-04        VIO        Failure to implement the requirements of
                                                                                                              (a)(1) and (a)(2) of the Maintenance Rule
                                                                                                              (Section M3.2)
                                                                        50 413.414/94-13-02        URI        Emergency Operating Procedure 50.59
                                                                                                              Evaluations Not Reviewed by Nuclear Safety
                                                                                                  '
                                                                                                              Review Board as Required by TS (Section      l
                                                                                                              08.1)
<
l                                                                                                        List of Acronyms
!                                                                      CFR  -
                                                                                    Code of Federal Fagulations
                                                                        DBD  -
                                                                                    Design Basis Documents
                                                                        EDG  -
                                                                                    Emergency Diesel Generator
                                                                        EDM  -
                                                                                    Engineering Directives Manual
                                                                        E0P  -
                                                                                    Emergency Operating Procedure
                                                                        FIP  -
                                                                                    Failure Investigative Process
                                                                        FSAR  -
                                                                                    Final Safety Analysis Report
                                                                        IAE  -
                                                                                    Instrument and Electrical
                                                                        IFI  -
                                                                                    Inspector Followup Iten
                                                                        IST  -
                                                                                    Inservice Testing
                                                                        LCVU  -
                                                                                    Lower Containment Ventilation Unit
                                                                        LER  -
                                                                                    Licensee Event Report
                                                                        LLRT  -
                                                                                    Local Leak Rate Test
                                                                        MPFF  -
                                                                                    Maintenance Preventable Function Failure
                                                                        NCV  -
                                                                                    Non Cited Violation
                                                                        NM    -
                                                                                    Nuclear Sampling
                                                                        NRC  -
                                                                                    Nuclear Regulatory Commission
                                                                        NSD  -
                                                                                    Nuclear Site Directive
                                                                        NSRB  -
                                                                                    Nuclear Safety Review Board
                                                                        DAC  -
                                                                                    Operator Aid Com] uter
                                                                        POR  -
                                                                                    Public Document Room
                                                                        PIP  -
                                                                                    Problem Investigation Process
                                                                        PM    -
                                                                                    Preventive Maintenance
                                                                        asig  -
                                                                                    Pounds Per Square Inch Gauge
                                                                        RCA  -
                                                                                    Radiologically Controlled Area
                                                                        RCP  -
                                                                                    Reactor Coolant Pump
                                                                        RCS  -
                                                                                    Reactor Coolant System
                                                                        RG    -
                                                                                    Regulatory Guide
                                                                        SA    --
                                                                                    Main Steam to Auxiliary Equipment
                                                                        SB0  -
                                                                                    Station Blackout Role
                                                                        SITA -      Self Initiated Technical Audit
                                                                        SPOC  -
                                                                                    Single Point of Contact
                                                                        TPBE -      Thermal Power Best Estimate
                                                                        TS    -
                                                                                    Technical Specifications
                                                                        TSAIL -    Tech Spec' Action Item Log
                                                                        UCLF -      Unplanned Capability loss Factor
                                                                        UFSAR -    Updated Final Safety Analysis Report
                                                                                                                                              Enclosure 2
                                                                                                                                                          _
 
                                    28
  URI- -
          Unresolved Item-
  USO  -
          Unreviewed Safety Question
  VDC' -
          Volts direct current
                .
  VIO  -
          Violation
  -VV  -
          Containment Ventilation
  WO  -
          Work Order
  YN  -
          Auxiliary Building Chilled Water
l
                                          Enclosure 2
                                                      _
}}

Latest revision as of 07:35, 19 December 2021

Insp Repts 50-413/97-09 & 50-414/97-09 on 970608-0719. Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support
ML20210N734
Person / Time
Site: Catawba  Duke Energy icon.png
Issue date: 08/18/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20210N708 List:
References
50-413-97-09, 50-413-97-9, 50-414-97-09, 50-414-97-9, NUDOCS 9708260105
Download: ML20210N734 (32)


See also: IR 05000413/1997009

Text

.

. . . . . . . _ ,

Notice of Violation 3

withholding of such material, you muit tpecifically identify the portions of

your response that you seek to have witkield and provide in detail the bases

l

'

for your claim of withholding (e.g., explain why the disclosure of information

will create an unwarranted invasion of personal privacy or provide the

,

confidential commercial or financial information). If safeguards information

l 1s necessary to provide an acceptable response, please provide the level of

protection described in 10 CFR 73.21.

Dated at Atlanta, Georgia

this 18th day of August, 1997

l

Enclosure 1

.

.

.

__ .

.. .

- ..

1

U. S. NUCLEAR REGULATORY COMMISSION

REGION 11

Docket Nos: 50-413, 50 414

License Nos: NPF-35. NPF-52

Report Nos.. 50-413/97 09. 50 414/97-09

Licensee: Duke Power Company

Facility: Catawba Nuclear Station. Units 1 and 2

Location: 422 South Church Street

l Charlotte. NC 28242

Dates: June 8 - July 19, 1997

Inspectors: J. Zeiler. Acting Senior Resident inspector

R. L. Franovich, Resident inspector

M. Giles. Resident inspector (In Training)

N. Economos Region 11 Inspector (Sections M8.1. 2. 3. 4)

R. M. Moore. Region 11 Inspector (Sections 08.1. E2.1 )

Approved by: S. M. Shaeffer. Acting Chief

Reactor Projects Branch 1

Division of Reactor Projects

l

I

Enclosure 2

9708260105 970818

PDR ADOCK 05000413

0 PDR

. .

.

. .

-

. _ . __ _. _ _ _ _ _ _ _

_____ - _ _ __ -

EXECUTIVE SUMMARY

Catawba Nuclear Station. Units 1 & 2

NRC Inspection Report 50 413/97-09, 50 414/97 09

This integrated inspection included aspects of licensee operations.

maintenance, engineering, and plant support. The report covers a 6-week

period of resident ins)ection; in addition, it includes the results of

announced inspections ay Regional reactor safety inspectors.

Doerations

e

A Non Cited Violation (NCV) was identified for failure to declare three

ice condenser intermediate deck doors inoperable and log an associated

Technical Specification Action item Log entry after identifying ice

buildup on the doors. This item along with several other minor human

performance weaknesses indicated a need for greater attention to detail

and questioning attitude by operations personnel during the performance

of routine activities (Section 01.1).

e

The root cause evaluations of a reactor coolant pump trip and subsequent

reactor trip were adequatel

involve human error or nonconservative y performed. The cause

decision of theThe

making. trip protective

did not

relaying associated with the short bus of 2TB functioned as designed.

However, a delay in troubleshooting activities to locate the source of

the associated ground indicated that the ground received a low priority

status in the work schedule and that trained personnel were not readily

available to troubleshoot ground indications in a timely manner (Section

w.2).

Control room operators were effective in precluding a turbine runback by

reducing reactor power to 50% before the 28 Main Generator Power Circuit

Breaker opened on low air pressure. The licensee's root cause

evaluation was detailed, and actions to prevent recurrence were

considered adequate (Section 01.3).

The decision to deviate from the preferred normal alignment of

Lower Containment Ventilation Unit (LCVU) operation to support

planned maintenance exhibited non-conservative work scheduling and

operatorjudgement. This resulted in lower containment air

temperature increasing slightly above the adjusted Technical

Specification limit for a brief period of time. The LCVU

operating procedures did not address the adverse impact of

removing two LCVUs from service simultaneously, nor did the

procedure address the interaction between LCVU operation and

integrated containment ventilation systems. These procedural

inadequacies were identified as a NCV (Section 01.4).

A violation (first example) for failure to follow procedure was

identified related to Operations failure to adequately document 10 CFR

50.59 screening evaluations (Section 08.1).

Enclosure 2

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

2

Maintenance

e A Failure In!estigation Process (FIP) team was thorough in investigating

the cause of an electrical flash in a 600 Volt breaker cubicle

associated with Motor Control Center 2MXM. The root cause indicated

configuration and procedure weaknesses in the method of locking out 600

Volt breaker cubicles to the maintenance position. Adaquate corrective

actions to prevent recurrence of this incident were implemented (Section

M1.1).

e

The licensee's identification of a technician's failure to follow a leak

rate test procedure that resulted in an invaild test of valve 2NV-874

during the previous refueling outage was an example of good questioning

attitude: however, the procedure completion review was untimely. The

Plant Operations Review Committee performed a thorough review of

subsequent activities to aroperly retest the valve. Good engineering

support was arovided, bot 1 in developing a leak rate test procedure and

briefing paccage for the evolution. The failure to follow the leak rate

test procedure was identified as a Violation (Section M1.2).

Enaineerina

e The licensee's identification of a discrepancy between primary and

secondary thermal power indication exhibited attention to detail in the

review of plant data. Actions to initiate a FIP team to investigate the

root cause were appropriate and steps to reduce reactor power until the

discrepancy was understood were conservative. Replacement of a faulty

T,,, card was well-planned, coordinated and controlled and executed in

an expediticas manner (Section El.1).

o Resolution of Design Base Document (DBD) open items was generally

adequate. However, a violation (second example) for failure to follow

procedure was identified related to Engineering's failure to enter DBD

open items into the Problem identification Process as required by

procedure and stated in the licensee's response to the Des'.gn Basis

50.54f letter (Section E2.1).

e The licensee's corrective action audit that assessed the resolution of

Self-N iated Technical Audit findings was identified as a strength in

correc " ve action performance (Section E2.1).

e The licensee adequately addressed the Emergency Diesel Generator 10 CFR

Part 21 issue related to potentially defective intake / exhaust springs

(Section E2.1).

  • Based on in-office review of the licensee *s March 31, 1997, annual

summary on 10 CFR 50.59 changes, onsite review of the licensee's 10 CFR

50.59 evaluations, and audit of the licensee's procedures, the inspector

concluded that the licensee had complied with t1e provisions of the

regulation for the changes listed in the annual summary (Section E3.1).

Enclosure 2

-

,

3

Plant Suncort

e Radiological control practices observed during the inspection period

were considered to b(. proper (Section R1.1).

l

l

Enclosure 2

,

.

-

- _

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

I

Reoort Details

Summary of Plant Status

,

Unit 1 operated at or near 100% power during the inspection period.

l On June 26, a Unit 2 reactor trip occurred on low Reactor Coolant System loop

l

i

flow as a result of an electrical ground fault which de energized the

electrical bus that powers the "2B' Reactor Coolant Pump (RCP). The unit was

returned to 100% power operation on June 29. Power was reduce 1 to 50% on July

2 to preclude a turbine trip / reactor trip u)on the anticipated failure of  ;

Main Generator Power Circuit Breaker (PCB) 23. A solenoid (or pilot) valve '

associated with the air supply to all three main generator PCB poles had

failed, rendering the air system unable to deliver air to the breaker. The

solenoid valve was replaced, and the unit was returned to 100% power the

following day. Reactor power was reduced to 99.3% on July 15 in response to a

discrepancy between primary and secondary thermal power indications. The

discrepancy was attributed to feedwater venturi defouling and hot leg

streaming, and did not reflect an actual temperature difference. The unit

returned to 100% power on July 17 and operated at or near 100% power for the

remainder of the inspection period.

Review of UDdated Final Safety Analysis Report (UFSAR) Commitm_gn_t1

While performing inspections discussed in this report, the inspector reviewed

the applicable portions of the UFSAR that were related to the areas ins)ected.

The inspector verified that the UFSAR wording was consistent with the o) served

plant practices, procedures, and/or parameters.

I. Operations

01 Conduct of Operations

01.1 General Comments (71707)

The inspector conducted frequent control room tours to verify proper

staffing operator attentiveness and communications. and adherence to

approved )rocedures. The inspector attended daily operations turnover

and Site )irection meetings to maintain awareness of overall plant

operations. Operator logs were reviewed to verify operational safety

and compliance with Technical Specifications (TS). Instrumentation,

computer indications, and safety system lineups were periodically

reviewed from the Control Room to assess o)erability. Plant tours were

conducted to observe equipment status and Jousekeeping. Problem

Identification Process (PIP) reports were routinely reviewed to assure

that potential safety concerns and equipment problems were reported and-

resolved,

in general, the conduct of operations was professional and safety

conscious. Good )lant equipment material conditions ar.d housekee ing

were noted througaout the report period. However, as addressed b low,

sevcral minor operator human performance deficiencies were identified

Enclosure 2

_ _ _ _ _ _ _

.

,

2

involving a failure to enter a TS Action Statement, failure to identify

equipment status anomalies, and failure to properly document a Technical

Specification Action item Log (TSAIL) entry.

Failure to Declare Unit 2 Ice Condenser Intermediate Deck Doors

inoDerable and Enter ADolicable TS Action Statement

On June 17 at 2:38 p.m., while performing the weekly TS surveillance on

the intermediate deck doors the licensee identified that three doors

had ice buildup (reported to be less than one half inch thick). The

function of these doors is to open during a des.gn basis accident to

ensure that the containment loss Of Coolant Accident (LOCA) atmos)here l

would be diverted through the ice condenser. Upon discovery of t1e ice,

a test procedure discrepancy was entered and a work request was

initiated to remove the ice. However, work to remove the ice or

investigate the extent of the impact on the door opening function was

not initiated due to problems with personnel accessing containment

through the containment airlock door. Later that night, the oncoming

Shift Work Manager became aware of the previces day's problem and

-contacted engineering personnel to perform an operability evaluation of

the condition. The following morning, the inspector reviewed the

results of this evaluation. The evaluation concluded that the " ice

condenser" was operable. This was based primarily-on a previous McGuire

Nuclear Station analysis that showed up to one-third of the intermediate

deck doors could fail to open and there would still be enough ice

condenser flow area for LOCA heat removal. The inspector determined the

evaluation focused to narrowly on the ice condenser system operability

and failed to adequately evaluate the operability of the intermediate

deck doors, especially with regard to consideration of information in

the applicable TS and Bases.

TS 3.6.5.3 requires the intermediate deck doors be operable in Modes 1-

4. TS Surveillance Recuirement 4.6.5.3.2 requires a 7-day verification

that the intermediate ceck doors be closed and free of frost

accumulation. The TS Bases also states that impairment by ice, frost.

or debris is considered to render the doors inoperable, but capable of

opening. Based on this, the inspector concluded that operations

personnel had failed to declare the three doors inopera]le and follow

the Action Statement of TS 3.6.5.3.a when the problem was initially

identified. This action statement allowed power operation to continue

for up to 14 days provided ice bed temperature was monitored at least

once per four hours and the maximum ice bed temperature was maintained

less than or equal to 27*F. The licensee initiated PIP 2-C97-2014-to

investigate this incident.

On June 18. after repairing the containment airlock, ice was removed

from the three intermediate deck doors. The cause of the ice buildup

was found to be the failure of heat tracing on an ice condenser air

handling fan drain line, which prevented adequate draining of defrost

condensate. The heat tracing was subsequently repaired. The licensee

Enclosure 2

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,

3

i

determined during activities to remove the ice that all three doors were

l not blocked to the extent that would have prevented their opening during

'

a LOCA. The inspector also noted that the ice bed monitoring system was

operational during the period that ice was on the doors and control room

annunciator alarms would have alerted the operators of anomalous ice bed

temperatures. Therefore, the ins)ector considered the safety

consequences of this incident to )e minimal.

The inspector reviewed Operations Management Procedure (OMP) 2-29.

Technical Specifications Action Item Log. Step 3.4 requires that non-

compliance with a Limiting Condition For Operation requiring operation

in a TS Action Statement, be logged in TSAll. The ins)ector determined

that a TSAll entry was not logged for this condition w1en ice was

identified on the doors rendering them inoperable. The failure to

declare the doors inoperable and enter a TSAll entry for t % applicable

TS Action Statement in accordance with OMP 2-29 was identitied as a

Violation of TS 6.8.1. Procedures and Programs. This failure to follow

procedures constitutes a violation of minor significance and is being

treated as a Non-Cited Violation (NCV). consistent with Section IV of

the NRL Enforcement Policy. This item is identified as NCV 50 414/97-

09 01: Failure to Declare Ice Condenser Intermediate Deck Doors

Inoperable and Log Appropriate TSAll Entry.

Auxiliary Shutdown Panel Volume Control Tank (VCT) Instrumentation Drift

During a walkdown of the four Motor Driven Auxiliary Feedwater Shutdown

Panels, the inspector identified that three of the four VCT level

indications were not reading accurately. There is one VCT gauge on each

Shutdown Panel. Gauge indications differed from control room

indications by as much as 20 percent level. The ins)ector alerted

operations-personnel to-the problem and noted that t1ey were very

responsive in initiating corrective actions. Due to subsequent problems

in calibrating the gauges and unavailability of like parts, engineering

modifications were developed and implemented to replace the gauges with

more accurate models. Based on discussions with Instrumentation and

Electrical (IAE) personnel, it was indicated that most likely, the

gauges had drifted out of accuracy over a long period of-time.

The inspector reviewed periodic surveillance test procedures associated

with verifying Shutdown Panel instrumentation indications. VCT level

was not among the indications checked periodically. The inspector

noted. however, that VCT level was not required by TS to be o)erable

from the Shutdown Panels. However, the VCT indication could )e

potentially used during operation from the Shutdown Panels. It was also

apparent that-there had been opportunities to have identified the gauge

output drift during the periodic surveillances of other Shutdown Panel

instrumentation.

Enclosure 2

_________ __- _ _ .

-

l 4

Unit 2 Power Rance Channel NI-42 Soare Window Illuminated

On June 27. 1997, the day after Unit 2 tripped on low Reactor Coolant

System flow, the inspector noticed an annunciator window on the Nuclear

Instrument (N1) 42 Power Range drawer that was illuminated. The

annunciator window was labeled " spare" and appeared to serve no

function. The inspector questioned the control room operators about the

illuminated window. The window apparently first illuminated following

the trip; however, the operators were not aware that the window was

illuminated, nor the reason for the condition. Based on subsequent

discussions with reactor engineering personnel, the inspector learned

that this spare annunciator window was previously used as the negative

rate trip indication light. During the previous refueling outage. this

trip function was isolated from the reactor protection logic, the

modification that implemented the rate trip change was supposed to have

removed the bulb from these windows on all of the N1 drawers. .It was

believed that the bulb in the NI-42 drawer was removed, but may have

been reinstalled by lAE personnel by mistake during subsequent NI

maintenance activities following the refueling outage. The light was

extinguished once the rate trip function was reset and the bulb. removed.

The licensee initiated a PIP to address this problem.

TS Loaaina Error for Trackina Containment Airlock Door Seal Surveillance

lRR

On July 11, 1997, during review of the Unit 2 TSAIL. the inspector

noticed an incorrect entry that was made on July 9. The entry was for

tracking a TS required 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> airlock door seal test following opening

of the airlock door on July 9. The time required for the test to be

performed was listed in TSAIL as July 16 instead of July 12. The

inspector discussed the error with operations personnel who corrected

the entry. It was also indicated that the seal test was scheduled to be

performed that same day. Based on this, the inspector determined the

test would not have been missed even though the TSAll was incorrect.

The inspector was concerned that the TSAll error had not been identified

over the two previous two days that the problem existed.

Individually, the above problems had little actual safety consequences.

however, in the aggregate represented the need for greater attention to

detail and questioning attitude by operations personnel during the

performance of routine activities.

01.2 Unit 2 Reactor Trio on low Reactor Coolant System Flow-

a. Insoection Scope (71707. 937,01).

On June 26 a Unit 2 reactor trip from 100% power occurred when the 2B

Reactor Coolant Pump (RCP) tripped and caused a loss of flow signal in

the associated loop. The inspector discussed the unit trip with

engineering, operations and maintenance personnel, as well as reviewed

the associated electrical diagrams. Unit Trip Report and Pl? 2-C97-2221.

Enclosure 2

l 5

i b, Observations and Findinas

i

!

On June 21. a negative leg ground was detected on ron vital distribution

bus 2CDB. The ground subsequently was traced to tre 125 VDC control

l power circuit of breaker 2T6 6. On June 26. the b"eaker was opened to

'

facilitate troubleshooting the cause of the ground. The Instrument and .

Electrical (IAE) technicians noticed that the breaker failure initiation l

relay in 2TB 6 control cubicle was chattering, but continued with their i

troubleshooting activities. Shortly thereafter, a reactor trip

occurred.

The licensee determined that. the source of the ground fault was the

breaker pushbutton, a Cutler-Hammer E30 model, lhe pushbutton had '

failed and created a negative leg-to ground fault on 2CDB. The

pushbutton internals had changed state when 2TB 6 was tripped open

during troubleshooting, introducing a fault path to the positive leg.

Noise from the cabinet ground was induced through the switch and the

breaker failure initiation relay (94B) coil, causing it to chatter and

eventually actuate to trip the incoming breaker on the short bus of 2TB.

The auto close function of the 2TB tie breaker was blocked by a lockout

rela

bus,y, and the bus de-energized. The 2B RCP. which is supplied from the

tripped, and the subsequent low flow in the B loop caused a reactor

trip.

The inspector discussed the reactor trip with operations and engineering

personnel to determine if the root cause involved a human error. The

chattering of the relay, generated when 2TB 6 was opened, could have

been stop)ed if the IAE technicians had reclosed the breaker when they

noticed tlat relay chattering. However, they did not understand what

was causing the chattering at the time. The inspector concluded that

the IAE technicians responded appropriately by leaving the breaker in

the opened position since the cause and impact of the relay chattering

were not understood.

The inspector inquired about the time delay between ground detection

(identified on a Saturday) and troubleshooting activities (initiated the

following Wednesday). l.icensee personnel indicated that Single Point Of

Contact (SPOC) technicians were not trained and qualified to use the

ground chasing equipment. As a result a'stempts to locate the ground

could not be made until the following Monday when a trained IAE

technician would be available. Also, priority status was not associated

with troubleshooting the ground indication early in the week. In

addition, the inspector determined that only two techniciant on site

were fully qualified to use the ground-chasing equipment to locate the

source of a ground, and that_one of those technicians had been offsite

since February and was not scheduled to return until October of this

year. A shortage of trained personnel available to perform the

troubleshooting contributed to the delay. At the end of the ins)ection

period, the delay in investigating the ground, associated contri)uting

factors, and appropriate corrective actions were not addressed within

the licensee's corrective action program.

Enclosure 2

.

6

The unit was restarted on June 28 after trip list activities were

performed and minor equipment problems were corrected. The licensee is '

planning to document the reactor trip in a Licensee Event Report.

l c. Conclusions

The inspector concluded that root cause evaluations of the reactor trip

were adequately performed. The cause of the tt!p did not involve human

error or non conservative decision making. The protective relaying

associated with the short bus of 2TB functioned as designed. The

inspector determined that, although the delay in troubleshooting

activities to locate the source of the ground did not affect the outcome

(reactor trip), challenges existed in the following areas: (1)

associating appropriate priority to locating ground indications in a

timely manner, and (2) ensuring that trained personnel are avullable to

troubleshoot ground indications. At the end of the inspection period,

efforts to address the delay, understand its causes, and identify

corrective actions were not evident in the licensee's corrective action

program.

'

01.3 Unit 2 Downoower in Response to Generator Outout Breaker Trouble

a. insoection Scone (71707)

On July 2. Unit 2 control room operators received a generator breaker

trouble alarm and identified a continuous decrease in minimum close air

3ressure on 28 Main G2nerator Power Circuit Breaker (PCB). Operators

Jegan a rapid load reduction, and the PCB automatically tripped after

reactor power reached 50%. The inspector reviewed PIP 2 C97 2177 and

discussed the downpower and associated equipment failure with licensee

personnel.

b. Observations and Findinos

On July 2, the Main Generator PCB 2B Trouble annunciator alarmed in the

control room. Control room operators determined that there was a

continuous decrease in air 3ressure on the 28 Main Generator PCB,

indicating an approach to 11e minimum air pressure is required to open

the breaker. Air

' the resulting arc. pressure is required

Since the to openofthe

safety function thebreaker andtodissipate

PCB was open, it

was designed to automatically open before the minimum pressure required

for this function is reached. The minimum tri

Generator PCB 2B is between 446 and 452 psig. p pressure on Main

To preclude an automatic turbine runback on the potential automatic

opening of the PCB operators began a rapid load reduction, The PCB

automatically tripped after reactor power reached 50%. No overcurrent

alarms were received on Main Transformer 2A.

The license deternJned that a solenoid (or )ilot) valve associated with I

s

the air sup)1y to a:1 three main generator )CB poles had failed,

rendering t1e air system unable to deliver air to the breaker.

Normally, the solenoid valve receives signals from the breaker poles to

Enclosure 2

V

i

7

,

supply air to them. When the air pressure on any pole reaches

a> proximately 485 psi.-a pressure switch actuates and the solenoid valve

sluttles to pneumatically control a regulator that delivers air to the

breaker poles. When air pressure is restored to 500 psi the signal

'

from the pole to the solenoid is terminated.

Station PIP 2-C97-2177 documented the root cause of the solenoid

failure. The failed solenoid was new and had been installed during the

April 1997 refueling outage. The component failure was attributed to a

deformed nylon bushing. The valve had been assembled to compensate for

the defect which initially allowed the valve to operate as designed.

However, the valve's internal components drifted from their assembled

positions over time and eventually were unable to engage with the

valve's lower assembly, thereby preventing air flow to the poles.

To address the potential that newly purchased solenoid valves could be

installed with problems, the licensee had revised procedure

IP/0/B/4974/01, Main Generator PCB Maintenance. - Revision 5 of the

procedure included a Note between Steps 10.3.7 and 10.3.8. The-Note

read: "If pilot valve is replaced, ensure pilot valve has been

disassembled and inspected for pro >er assembly and components. or

rebuilt prior to installation." T1e inspector verified that this

procedure change had been made,

c. Conclusions

The inspector concluded that control room operators were effective in

)recluding a turbine runback by reducing reactor power to 50% before the

3CB opened. The licensee's root cause evaluation was detailed and

actions to prevent recurrence were adequate.

01.4 Lower Containment Air Temoerature Exceeded for Short Duration

a. Insnection Stone (71707)

On June 30. the licensee was performing maintenance on the Unit 2

Lower Containment Ventilation Units (LCVUs). While the 2A and 20

LCVUs were out of service, the lower containment temperature

increased to 117.4'F. The inspector reviewed apalicable operating

procedures. TS. the FSAR, tagout requirements, tie innage work

schedule, and PIP 2 C97-2127. The inspector also discussed the

-issue with operations, engineering and work control personnel.

b. Observations-and Findinas

During normal operation. the Containment Chilled Water (YV)

chillers service various containment loads including the LCt!Us and

the Reactor Coolant Pump (RCP) Motor Air Coolers. 0_n June 30,

preventive maintenance (PM) and electrical motor testing were

scheduled for the 2A and 20 LCVUs. The 2A LCVU was removed from

Enclosure 2

I

!

l

8

l

service first. After the PM for the 2A LCVU was completed, but i

before motor testing was completed, operations personnel decided

to remove the 2D LCVU for PM. The 2D LCVU was removed from ,

service at 10:55 a.m. While both LCVUs were out of service, lower

containment temperature increased. To compensate for the

temperature increase, control room operators adjusted the

o)eration of the remaining inservice LCVUs (2B and 2C) from

"iormal" to "High Speed." and then to " Max Cool." However, for a  !

brief period of time lower containment temperature had exceeded

the high high temperature Operator Aid Computer (0AC) alarm

setpoint of 115.6'F and the adjusted TS limit of 117.2*F.

ultimately reaching 117.4'F. Lower containment temperature was ,

'

above 117'F for approximately 3 minutes before it was restored to

within TS limits. The Action required by TS 3.6.1.5 was to

,

i

restore the air temperature to within the limits within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> or

be in at least hot standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. Since the

.

!

bich lower containment temperature existed for only a few minutes. -

th6 licensee was in compliance with the TS action. .

At anroximately 11:10 a.m., operations personnel decided to post)one

the M on the 2D LCVU. recall the associated tags and return the _CVU to

service until the 2A LCVU was restored to operation. While operators i

were returning the 2D LCVU to service and all three LCVUs to normal

alignment, the YV chillers in service (A and C) trip >ed on low flow.

Based on a review of the circumstances surrounding t1e trip of the A and ,

C YV chillers, the inspector discerned that the following took place.

When the B and C LCVUs were taken to " Max Cool" in an effort to reduce  !

lower containment temperature, the flow control valves in the chiller

loop fully opened as designed, and thermostatic control of,the chilled

water supply was lost. When operations subsequently restored the D LCVU

to service and returned the LCVUs to normal operation, thermostatic i

control of the flow control valves was reinstated. The existing

temperature caused the flow control valves to throttle closed, and the

chillers tripped on low load. Normal alignment with the A and B YV

chillers was established within 30 minutes of the chiller trips. The C

YV chiller had also been restarted, but tripped after running for 10

minutes. Shortly thereafter, containment temperatures were restored to

normal levels.

Operations surveillance procedure PT/1/A/4600/02A. Mode 1 Periodic

Surveillance Items. Enclosure-13.1. Periodic Surveillance Items Data,

approved January 23, 1997, provides surveillance acceptance criteria in -

accordance with the lower containment temperature limits imposed by TS 3.6.1.5. Lower containment minimum and maximum air temperature limits

are based on the average inlet temperatures of the operating LCVUs.

Temperature readings associated with non running LCVUs provide

indication of static air temperature and therefore, are not used to

determine average containment air temperature. Therefore. temperature

':mits are adjusted conservatively as a function of uncertainty (because

of the reduced sample size) in generalizing local indications to average

Enclosure 2

1

..-._..__ ,,

-

,a..

-

._-..,....,--...--m.__- -

- - - _ _ - _ . . _ . . .-m.

9

containment air temperature. As the number of LCVUs in service

decreases, the temperature limit decreases (becomes more conservative).

With two LCVUs running. the lower containment TS limit of 120*F was

adjusted to 117.2'F.

The Containment Lower Compartment Ventilation Subsystem as

described in the FSAR is designed to maintain a maximum

temperature of 120*F in the lower compartment during rnrmal plant

operation. During normal operation, three units (each providing

33.3% capacity) are in service, and one unit is on standby.

Technical Specification Interpretation 3.6.1.5 states that 3

!

containment air temperature can be maintained with one active

component out-of-service (i.e., three LCVUs in service).

Based upon a review of the FSAR and TS as well as discussions

with on-shift operators, the inspector determined that the 4

decision to remove the D LCVU from service while preventive

maintenance (PM)s on the A LCVU were ongoing was non conservative

and caused lower containment temperature to exceed the adjusted TS

limit.

The inspector also determined that problems existed with procedure

OP/2/A/6450/01. Containment Ventilation Systems. dated June 15. 1994,

which controls the configuration of the LCVUs. The procedure did not

provide adequate guidance to address the impact of removing two LVCus

from service on lower containment temperature. Operations Management

Procedure 2-18. Tagout Removal and Restoration Procedure. Revision 46.

Responsibility 4.8. states that the person placing or removing tag (s)

shall check procedures affected and any outstanding tagouts associated

with that procedure / system for any adverse effects. Because the adverse

impact of removing 2 LCVUs from service was not addressed in the

procedure, this responsibility could not be effectively realized.

n addition, procedure OP/2/A/6450/01 did not address the interaction

between LCVU operation and integrated Containment Ventilation (VV)

Systems. Step 2.7.3 of OP/2/A/6450/01. Enclosure 4.12. LCVU Additional

Cooling and YV Chiller Trip Prevention directs the operator to ensure

that three LCVUs are in the " NORM" position. The performance of this

step caused the A and C YV chillers to trip. Procedure

slowly reduce the demand on the system was not provided, guidance

nor was a to

precaution or note provided to warn of the potential to induce a chiller

trip as a function of load demand changes.

The inspector also noted that no procedure guidance was available for

swapping between running and_non running LCVU units. OP/2/A/6450/01.

Enclosure 4.2. Lower Containment Ventilation Unit Startup and Normal

Operation, provided procedural guidance for starting up the system by

placing three LCVUs in operation. Enclosure 4.7. Lower Containment

Ventilation Unit Shutdown provides procedural guidance for shutdown of

the system by placing all four LCVU switches in the OFF position.

Enclosure 2

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l

10

However, no procedural guidance existed for stopping an individual LCVU

and subsequently restarting it or making other required alignment

changes needed to facilitate the performance of the PM. The inspector

recognized that this lack of procedural guidance was unrelated to the

l

lower co'itainment temperature increase and the YV chiller trips.

The inspector also identified a minor discrepancy in the planned

l innage work schedule. The 2A LCVU had two work items planned to

be worked which included a PM and electrical motor testing. The

PM on the 2A LCVU was scheduled to be completed at 12:00 p.m. on

June 30, 1997. The motor electrical testing on the 2A LCVU was

scheduled to be completed at 1:00 p.m. on June 30. The PM on the

20 LCVU was scheduled to commence at 12:00 p.m. on June 30.

immediately following the scheduled completion of the PM on the 2A

LCVU.

This schedule allowed both the A and 0 LCVUs to be out of

service for 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />, which was non conservative and not in

accordance with the alignment described in the FSAR.

c. Conclusions

The inspector concluded that the decision to deviate from the

preferred normal alignment of LCVU operation to support planned

maintenance exhibited non conservative work scheduling and

operator judgement. As a result. lower containment temperature

increased slightly above the adjusted TS limit for a brief period

of time. However, temperatures were reduced below the adjusted TS

limit within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> as required by the TS action requirement.

Therefore, exceeding the lower containment air temperature on

plant equipment had minor safety significance and did not pose a

threat to safety related equipment. The LCVU operating procedures

did not address the adverse impact of removing two LCVUs from

service. simultaneously. nor did the procedure address the

interaction between LCVU operation and integrated containment

ventilation systems. These procedural inadequacies constituh a

violation of TS 6.8.1. Procedures and Programs. This failure

constitutes a violation of minor significance and is being treated

as a NCV. consistent with Section IV of the NRC Enforcement

Policy. This item is identified as NCV 50-414/97-09-02:

Inadequate LCVU Operating Procedure.

08

,

Hiscellaneous Operations Issues (92901)

08.1 (Closed) Un.reigh.ed_Ltem (URI) 50-413.414/94-13-02: Emergency Operating

Procedure (EOP) 50.59 Evaluations Not Reviewed by Nuclear Safety Review

Board (NSRB) as Required by TS

This item was related to an apparent failure to meet the TS requirement

for the NSRB to review 50.59 evaluations for E0P changes. The

inspector's review determined that the re

being appropriately reviewed by the NSRBThe quired 50.59 evaluations

licensee's were

procedures had

Enclosure 2

__-_______ __-_ - _ _ - .

11

been inconsistent in defining the 10 CFR 50.59 screening evaluation and

the 10 CFR 50.59 Unreviewed aafety Question (US0) evaluation. The TS

requirement was intended for the NSRB to review the 10 CFR 50.59 U50

evaluations. Nuclear Site Procedure NS0-209, 10 CFR 50.59 Evaluations.

Revision 6. was revised after 1994 to clearly define the two

evaluations. The licensee initiated a change to NSD 703. Administrative

Instruction for Station Procedures, to clearly distinguish on the

procedure change process documentation whether the evaluation performed

was a screening evaluation or an USQ evaluation. The inspector reviewed

,

' three US0 evaluations for E0P changes and verified the US0 evaluation

i

had been sent to the NSRB_for review. A 1995 evaluation had been

reviewed and two 1997 evaluations were scheduled for review at the next

NSRB meeting. The inspector concluded that this issue was adequately

resolved and the TS requirements had been met by the licensee.

During the invettigation of the above issue, the inspector reviewed

a) proximately 20 examp',cs of 10 CFR 50.59 screening evaluations for E0P

c1anges and identified a deficiency in the licensee's procedure

implementation of this activity. Specifically, the justifications for

the screening questions were inadequate in many changes. The

justifications were inadequate in that they only repeated the screening

question as a negative statement. NSD 209, 10 CFR 50.59 Evaluations.

Revision 5. required the doca,3ntation of justification for responses to

50.59 screening questions. It further stated that justifications should

be complete enough so that an independent reviewer cculd come to the

same conclusion. The following E0P change 50.59 screening evaluations

were inadequate and did not meet the applicable procedure requirements:

o EP/2/A/5000/FR 1.2 dated November 17, 1995

e EP/1/A/5000/FR-1.1 dated September 19. 1996

  • OF/1/A/6350/08 dated February 28. 1996

e EP/2/A/5000/F-0 dated March 26, 1997

e EP/1/A/5000/FR H.1 dated August 16, 1996

  • EP/1/A/5000/FR-H.1 dated January 30, 1995

This failure to follow NSD 209 for 10 CFR 50.59 screening evaluations,

is identified as the first example of Violation (VIO) 50 413.414/9/-09-

04: Failure to Follow Procedure. The inspector did not identify any

US0 condition related to the inadequate 50.59 screening evaluations.

The inspector noted that the 50.59 screening evaluations for E0P changes

were performed by the Operations organization. Previous inspections of

50.59 evaluation performance have concluded that the Engineering

organization performed to a high standard in this area for 50.59

evaluations related to modifications. Although both organizations

Enclosure 2

12

receive the same training and use the same procedures. Operation's

performance in this activity was deficient as previously noted. The

inspector reviewed a 1997 50.59 USO evaluation for an E0P change. This

evaluation was good in that it included a well detailed justification

for responses to the USQ evaluation questions. This indicated that the

>

Operations deficient performance was related only to the 50.59 screening

evaluations.

II. Maintenance

l

M1 Conduct of Maintenance

1

M1.1 Electrical Flash Durinn Breaker Preventive Maintem nte

a. Inspection Stone (62707)

The inspector reviewed the circumstances and the licensee's corrective

actions associated with an electrical flash that occurred inside a 600

Volt non safety-related breaker cubicle while periodic breaker PM was

being performed. The electrical flash resulted in a minor personnel

injury and extensive damage to the breaker cubicle.

b. Observations and Findinas

On June 3. 1997, an Instrumentation and Electrical (IAE) technician was

aerforming PM on 600 Volt breakers 2MXM-F09C and 2MXM-F090. These

areakers supplied power to two Unit 2 ice condenser refrigeration air

handling fans. The PM activity involved testing the overcurrent

protective devices associated with the breakers. The technician had

removed breaker F09C from its cubicle and was in the process of removing

breaker F090 from its cubicle. While removing F090, an electrical ficsh

occurred in the F09C cubicle, which was located directly above F09D.

The technician received minor facial burns. but was not seriously

injured. Breaker F09C was electrically welded in its cubicle as a

result of the electrical fault, The inspector responded to the breaker

work location and noted good licensee immediate actions in response to

the incident. These actions included terminati' 11 PM work, roping

off the area for personnel safety consideratior . nd initiating a

Failure Investigative Process (FIP) to determine the root cause of the

electrical fav a.

On June 6, 1997. Motor Control Center 2MXM was de energized, and the

breaker cubicle for F09C inspected. The damage to the bus was minimal;

however, the stabs for F09C were badly damaged and recuired replacement.

Both breakers F09C and F09D were repaired, tested, anc returned to

service. The inspector attended the PORC meeting conducted to discuss

the repair plans and noted that management performed a thorough review

of the plans with good discussions on the impact of the work planned on

the plant. The repairs were completed without incident.

Enclosure 2

_____ -

13

The FlP team was thorough in their investigations and determined that

the stabs b? hind breaker F09C had come in contact with the energized

bus. Since the breaker power connecting cables had been determed and

left untaped in the bottom of the breaker cubicle. an electrical ground

path was created when the cables were re energized. The FIP determined

the method for racking the breaker out in the maintenance position was

inadequate. In the maintenance position a lock tab on the front of the

breaker cubicle had been used to position the breaker away from the bus;

l however this method did not provide sufficient distance between the bus

and stabs. While this method had not resulted in any problems in the

past, the result of having two breakers in the maintenance position,

located one above the other, created an even smaller bus / stab distance

that resulted in electrical flash over.

As a result of the FlP investigations, instrumentation procedures

governing work on 600 Volt breakers were revised to change the method of

racking out these breakers for maintenance. Instead of using the lock

tab, procedures directed that a padlock be placed on the breaker or the

bteaker be removed completely to ensure adequate stab / bus distance is

maintained. In addition, IAE personnel involved with breaker work were

to be provided training on this new method of racking 600 Volt breakers

out to the maintenance position.

c. Conclusions

The inspector concluded that the FlP team was thorough in investigating

the cause of the electrical flash. The root cause evaluation revealed

configuration weaknesses in the method of locking out 600 Volt breaker

cubicles to the maintenance position. The inspector determined that the

licensee adecuately implemented corrective actions to prevent recurrence

of this incicent.

M1.2 'Jngdeounte Leak Rate lest of Unit 2 Containment Isolation Valve

a, insoection Scope (40500. 61726. 62707)

On June 4,1997, the licensee identified that Unit 2 containment

isolation valve 2NV 874 had not been properly Type C leak rate tested in

accordance with 10 CFR 50. Appendix J during the previous. refueling

outage. On June 6. the valve was properly tested and failed the Type C

leak rate test. -The valve disc was replaced, and the valve was

successfully tested on June 7. The licensee submitted LER 50 414/97-004

. to document the inadecuate leak cate test conducted during the outage.

The inspector reviewec the circumstances associated with the inadequate

testing, attended PORC meetings to discuss retesting valve 2NV-874

online, witnessed aspects of the June 6 retest, reviewed leak rate test

results, and discussed the incident with engineering and Operations Test

Group (OTG) personnel,

Enclosure 2

_ -

i

14

b. Observations and Findinas

On &ne 4.1997 the OTG Suaervisor was conducting a procedure

completion verification of Jnit 2 Periodic Test (PT) procedure

PT/2/A/4200/01C. Containment Isolation Valve t.eak Rate Test. This

procedure had been performed during the previous refueling outage in

1

April 1997. During the review, the supervisor idcntified that Step

2.2.3 of Enclosure 13.7. Penetration No. M228 Type C 1.eak Rate Test had

been marked "Not Applicable by the OTG technician performing the test.

,

I

resulting in the step not being performed. This step required test vent I

flow path valve 2NV 873 to be opened while testing inside containment

isolation check valve 2NV 874 (associated with the Standby Makeup System '

flowpath to the reactor coolant pump seals). Without an open test vent

flowpath, the leak rate test on 2NV 874 had been invalid.

The inspector verified that appropriate actions were implemented upon

identification of the invalid lea ( rate test. These actions included

2NV 874 being declared inoperable and in accordance with TS 3.6.3, the

outboard containment isolation valve (2NV 872A) in the penetration was

closed and power was removed from the valve operator within four hours.

The inspector attended the June 5 and 6 PORC meetings conducted to

discuss activities to retest 2NV-874. Management thoroughly discussed

the impact on the plant with testing the valve while online. In

addition engineering developed a special leak rate test procedure and a

detailed briefing package explaining the necessary actions for

controlling the retest activities.

On June 6. the inspector witnessed aspects of the leak rate test on 2NV-

874. The inspector noted that testing was well controll?d and performed

in accordance with the test procedure.- The valve was not able to be-

pressurized and resulted in-a failed leak rate test. Valve maintenance

was performed resulting in replacement of the valve disc and disc

spring. A subsequent leak rate test was performed following the

maintenance activity. The inspector reviewed the results of this

testing which verified that leakage was within acceptable limits.

Following successful testing 2NV 874 was declared operable and the

penetration was returned to its normal configuration,

c. n

C_Qn.clusions

The inspector concluded the identification by the OTG Supervisor of a

procedure discrepancy that resulted in an invalid leak rate test of nD-

874 was an example of good questioning attitude. The PORN performed a

thorough review of subsequent activities to properly perform the leak

rate test. Good engineering support was )rovided, both in developing a

leak rate test procedure and briefing paccage for the evolution.

The inspector noted that the procedure completion review was not

performed by the OTG Supervisor following actual completion of all

testing or prior to plant startup from the refueling outage. Since this

Enclosure 2

_ _ _ _

-

. . - _ . __- --_ --- - - - - - . . - - _- _.

15

l was the only review that was recuired following test procedure

completion, the inspector consicered the review untimely. Had this

review been completed prior to plant startup, this problem may have been

identified and corrected arior to the unit entering a mode recuiring

containment integrity. T1e failure to open test vent valve 2hV-873

during/4200/01C

PT/2/A was identified as a violation of TS 6.8.1. leak

This rate testing of

issue

is identified as Violation E0-414/97-09 03: Failure to Follow Procedure

Results in Invalid Local Leak Rate Test of Valve 2NV 874.

M8 Miscellaneous Maintenance Issues (92902.

l M8.1 (Closed) VIO 50 413. 414/97-01-01: Failure to Include all Structures.

S stems and Components in the Scope of the Maintenance Rule as Required

b 10 CFR 50.65

This violation was identified when the inspectors determined that the

licensee had incorrectly excluded a number of structures. systems and

components from the scope of the Maintenance Rule. The licensee

acknowledged the violation and issued a Problem Investigation Process

(PIP) report PIP No. 0 C97-0419. to document correctivo actions taken

! and, track the progress made in addressing the issues. The systems

affected included Nuclear Sampling (NM). Main Steam to Auxiliary

Equi) ment (SA). Auxiliary Building Chilled Water (YN) and Ice Condenser

l

'

Hitti Pins (NF). Following a review by the site Expert Panel these

systems or components were added to the scope of the Maintenance Rule.

Corrective actions taken or planned included a review of the 239

'

functions that had been excluded from the Maintenance Rule scope. This

review was scheduled for completion in December 1997.- and will be

documented in PIP No. 0-C97-0419, In addition, structures and functions

excluded from the Maintenance Rule will be reviewed for Generic Scoping

applicability. The due date for this review is also December 1997. The

inspectors concluded the licensee's corrective actions were appropriate.

,

M8.2. (Closed V10 50-413.414/97 01-04: Failure to implement the Requirements

of (a)(1) and (a)(2) of the Maintenance Rule

l This violation was identified when the inspectors determined that the

l licensee was using Forced Outage Rate (FOR) instead of Unplanned

l Capability loss Factor (UCLF) as a Plant Level Performance Criteria for

' monitoring A2 systs....; 3er 10 CFR 50.65. The concern was that FOR was

not as sensitive as UC F in detecting declining performance in some

systems.

The licensee acknowledged the violation and took appropriate action to

correct the problem. The licensee incorporated the Plant Transient

Criteria as part of the Forced Outage Criteria. This combination of

criteria was intended to provide appropriate equivalent defense in depth

monitoring as the Unplanned Capability Loss Factor. A Plant level

Enclosure 2

l

._ - -- -

1

16

l

Performance Criteria called Plant Transients, which defined unacceptable

performance was added to Engineering Directives Manual (EDM)-210 as Rev.

i

'

4. The inspectors concluded the licensee's corrective actions were

appropriate. l

I

M8.3 (Closed) Insoector Followuo item (IFI) 50 413.414/97-01-02: Followup and

'

Review of Licensee Procedure to implement the Requirements of (a)(1) and

(a)(2) of the Maintenance Rule after issuance of Regulatory Guide 1.160,

Rev.2

i

EDM-210." Requirements for Monitoring the Effectiveness of Maintenance

at Nuclear Power Plants or the Maintenance Rule " Rev. 5. revised the

definition of Maintenance such that it was now in agreement with

Regulatory Guide 1.160. Rev. 2, dated March 1997. Revision 5 of the EDM

now considers any operator action performed in support of Maintenance as

a Maintenance Preventable Function Failure (MPff) candidate. In

addition, the flow gra)h of Appendix A to the subject EDM, were revised

for clarity. One of tie two was revised from Vendor Error to Off-site

Vendor Services while the other from Operations or Plant configuration

control to Operation or Plant Configuration Control not associated with

a maintenance activity. The inspectors concluded the licensee's

i

corrective actions were appropriate.

M8.4 (Closed) IFT 50-413.414/97-OL-01 Followup on Licensee Actions to

Provide Performance Criteria for Structures After Resolution of this

Issue

EDM-210. " Requirements for Monitoring the Effectiveness of Maintenance

at Nuclear Power Plants or the Maintenance Rule." Rev. 5. changed the

3erformance criteria for all Maintenance Rule structures to comply with

legulatory Guide 1.160. Rev. 2. This criteria applies to both risk and

non-risk significant Maintenance Rule structures.

EDM 410. " Ins)ection Program for Civil Engineering Structures and

Components." Rev. 1. dated June 16, 1997, is the controlling document

for monitoring and assessing civil engineering structures and' components

to the requirements of 10 CFR 50.65 and Regulatory Guide 1.160,.Rev. 2.

dated March 1997. It provides examination guidelines, acceptance

criteria and documentation requirements. As such. Catawba civil

,

engineering was responsible for implementing the ins)ection program for

l structures and components. The inspectors reviewed EDM-410. Rev. 1 for

content and adequacy. The inspectors noted that the procedure provided

adequate guidelines and the acceptance criteria contained within,

followed Regulatory Guide 1.160. Rev. 2 guidelines for acceptable and

. unacceptable performance criteria.

l

l Through discussions and document review, the inspectors ascertained that

the inspection program for structures was adequately administered and

implemented. Responsible engineers had received training and were

familiar with Maintenance Rule requirements as they applied to their

area of responsibility.

5

Enclosure 2

L ___ _-- _ . _ _ _. .. . _ __.. _ _ _ _ __ , /

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ __ - _ __ _________

17

At the close of this inspection. 39 structures had been inspected and an

additional 120 were scheduled for inspection by year's end. Ins)ection

per the revised EDMs -210 and -410 commenced on July 1, 1997. T1e

inspectors reviewed the licensee's classroom training material. ES-CN-

97-21. used to cormiunicate Regulatory Guide 1.160. Rev. 2 guidelines.

Training of personnel was held between June 9 and 18. 1997. The

inspectors concluded the licensee's corrective actions were ap]ropriate.

III. Enaineerina

El Conduct of Engineering

El.1 Primary and Secondary Thermal Power DiscreDancy

a. -Insoection Stone (37551)

On July 15 the licensee discovered a discrepancy of approximately 0.6%

between the Unit 2 primary and secondary thermal power indications.

Secondary thermal

was reduced to 99.7%)power

andwas immediately

a FIP team was reduced

initiated to to determine

99.3% (reactor

the power

cause of the discreaancy. The inspector attended management briefings

by the FIP team mem)ers on the progress of their investigation: reviewed

associated TS and TS Interpretations: and discussed the issue with

Operations. Engineering and Maintenance personnel.

b. Observations and Findinas

On July 15. Operations personnel were notified by the reactor

engineering group that there was a 0.6% discrepancy between primary and

secondary thermal power indications, and that actual thermal Jower might

be greater than the secondary thermal power (the designated tiermal

power best estimate) indication. The reactor engineering group

discovered, during a routine review of secondary plant parameters, that

primary thermal power had slowly increased over time since the Unit 2

restart from the April 1997 refueling outage. A FIP team was initiated

to determine the cause of the discrepancy, and control room operators

decreased reactor aower to 99.3%. Tae reactor was operated at 99.3%

power until the FI) team could determine the cause of the discrepancy.

The FIP team determined, during the course of their investigation, that

theT,Yto586.9F.

587.3 indication had responded

Operations been drifting downward T,,,

by decreasing since May 11, 1997, from

to minimize

the T * /T error. Lowering T,,, caused the reactor to increase AT to

maint'aIn,r,,actorpowerequaltosecondarypower.

e The drift in the T,,,

indication resulted in changes in T Tm T,,, and AT but did not

cause a change in indicated or actud3 primary and secondary thermal

power. Although the FIP team could not attribute this indication drift

to the primary / secondary thermal power indication discrepancy they

determined that a degraded 7300 process card was responsible for the

Enclosure 2

_. . - . - . . _ .

}

l

18

drift and initiated plans to have the card replaced after the root cause

of the power indication discrepancy was identified.

The FIP team also determined that indicated feedwater flow had decreased

while steam flow had remained constant. This was attributed to

feedwater venturi defouling as a function of the new cycle (restart from

the April refueling outage was in early May). the recent reactor trip

(June 26), and was the recent rapid downpower (July 2). The result of

defouling was a decrease in indicated feedwater flow with a

consequential decrease in indicated secondary thermal Operations

maintains secondary Thermal Power Best Estimate (TPBE) power.

near 100% by

periodically opening flow control valves, which in turn causes primary

power to increase to maintain T

defouling caused an increase in.,, for and

actual 100% power level.

indicated The

primary gradual

thermal

power, as well as actual secondary thermal power. However, the

resultant discrepancy between indicated and actual secondary thermal

)ower accounted for approximately 0.10% to 0.15% of the 0.6% discrepancy

)etween primary and secondary indicated thermal power.

The major contributor (0.3% to 0.4%) to the discreaancy between primary

and secondary thermal power was determined by the IP team on July 16 as

hot leg streaming. According to Westinghouse, hot leg streaming refers

to the inability to accurately characterize bulk hot leg temperature.

The licensee examined data from the Unit 2 Beginning of C.rcle and

identified changes in the behavior of this phenomenon from previous

cycles. S)ecifically. calculations revealed that indicated Tw had

increased ay 0.2*F and caused indicated primary thermal power to

increase. As discussed above these changes were originally masked by

the decrease in primary tem -

T,,,/T,,, as a function of T,,,peratures accompanying the decrease in

indication drift.

Hot leg streaming has occurred in previous cycles on both units and has

resulted in as high as a 1.0% difference between primary and secondary

thermal power. To account for this, an adjustment factor in the OAC

calculation corrects the discrepancy.

The FIP team concluded that sea:dary thermal power had always been

accurately and correctly indicated, and that primary thermal power

indication did not reflect an actual increase in power level above TS

limits. The inspector discussed the impact of the primary thermal power

indication on Reactor Protection System setpoints and functions.

According to the reactor engineering group, the venturi defouling and

hot leg streaming factors did not constitute a sufficient temperature

error to warrant adjustment via the Reactor Coolant System (RCS)

Temperature Calibration Procedure, which is run quarterly. The OPAT and

OTAT trip strings remained within their TS limits. In addition, the

nuclear instrumentation system is calibrated to secondary thermal power,

so the associated overpower trip setpoints were unaffected.

Enclosure 2

,

_,

-

-.-.-.c. _. ---

_ _ _ _ - _ _ _ _ - - - - _ _ _ _ - - - - -

- - - - - -

-

19

Reactor Power was increased to 99.5% on July 16 and the degraded T,q

card was replaced on July 17. The inspector attended the prejob brief

for the card replacement and observed the work activity in the control

room. The replacement was successfully completed within less than 1

hour and without incidence. At the end of the inspection period, the

3a license was considering either performina periodic manual calculations

to the correct the thermal power aiscrepancy, or conducting a full

calorimetric to account for the deviation.

c. Conclusiqn_q

,

  • The inspector concluded that the licensee's identification of the

E thermal power discrepancy exhibited attention to detail and a thm

review of plant data. Actions to initiate a FlP team to invr a

g root cause were appropriate, and steps to reduce reactor po'

discrepancy was understood were conservative and indicative

positive nuclear safety ethic. Replacement of the faulty T, ,a was

well-planned. coordinated and controlled, and executed in an expeditious

manner.

E2 Engineering Support of Facilities and Equipment

.

E2.1 Review of Corrective Actions

a. Inspedjon Scooe (37550. 92903)

The inspector reviewed Engineering corrective actions to resolve open

itens identified during the development of the station Design Base

Documents (DBDs) and findings from Self-initiated Technical Audits

(SITAs). Also reviewed were the licensee's actions to address a 10 CFR

Part 21 issue related to a defective Emergency Diesel Generator (EDG)

intake / exhaust valve spring. Anplicable regulatory requirements

included 10 CFR 50 Appendix B. ESAR. Technical Specifications and

implementing licensee procedures.

b. Observations and Findinos

DS_Qs

Developed between 1990 and 1994. DBDs consolidated design and licensing

documentation for selected station systems and programs. The ]rocedure

guidance for development and maintenance of DBDs was provided ay

Enoineering Directives Manual . EDM-170. Design Specifications, revision

'

5. Open items were evaluhed for operability during the DBD development

and Licensee Event Reports (LERs) initiated as required. EDM-170

required the remaining items to be entered into the Problem

Investigation Process (PIP) for tracking and resolution. Additionally,

the l u ensee's February 10. 1997. response to the 10 CFR 50.54f letter

related to the Adequacy and Availability of Design Basis Information.

P stated that DBD open items woeli be ente 1 4 into the PIP for trackir.g

N and resolution.

Enclosure 2

.

Mi

20

TM inspector reviewed the resolution of open item in the Reactor

coolant System DBD to sample the adecuacy of item resolution activity.

Approximately 20 items were evaluatec to verify that the PIP and

interfacing station programs evaluated and resolved the open item

issues. The items were adequately resolved.

An independent industry audit of Catawba in late 1996, identified as a

finding the numerous lon9-term unresolved DBD open items. The response

to the finding was to initiate a blanket PIP (PIP 0-C97-0595 dated

March 5,1997) to cover the systems with the identified open items.

Many of these open items were not previously in the PIP process. The

PIP corrective actions established a schedule to resolve and close the

referenced DBD open items by September 1. 1997,

During this inspection, the inspector identified additional E 'en

items which were not entered into the PIP process nor incluau .d the

blanket PIP. The open items.were included in DBD CNS-1435.00-0002. Post

Fire Safe Shutdown, revision 4. and DBD CNS-1465.00-00-0018. Station

Blackout (SBO) Rule, revision 2. Although not entered into the PIP

3rocess. the licensee provided meeti g documentation indicating the Post

rire Safe Shutdown open items were being evaluated. These items were

identified by a November 1995 electrical post fire shutdown review

performeo after the initial DBD development and entered into the DBD by

revision 4 at that time. There was no c: :umented evaluation of

o)erability or A

tie PIP process.ppendix R commitments

Following which

the inspector's would haveof

identification been

this addressed

issue by

the licensee initiated PIP 0-C97-1918 to track resolution of these open

items. The inspector identified no significant safety concerns related

to the open items reviewed. This failure to follow procedure for

resolution of DBD open items is identified as the second example of

Violation 50-413.414/97-09-04: Failure to Follow Procedure.

SITAS

The ins)ector reviewed a recently comp'eted SITA report dated June 11.

1997, w11ch reviewed the adequacy of resolution of SITA findings. The

scope of the audit was good in that it reviewed the resolution of 80

findings from four previous SITAs. The depth of the audit was good in

that corrective act ans were verified through the extent of station

programs (e.g. . PIP work requests, modification etc. .) involved in the

resolution. The findings were well defined and demonstrated an

independent and objective audit. Corrective actions for the findings

hcd not yet been developed.

EDG 10 CFR Part 21 Notice

The inspector ruiewed the licensee's actions to address a Cooper

Industries 10 CFR Part 21 notice regarding potentially defective EDG

intake / exhaust valve springs which was applicable to Catawba. The

notice was initiated in 1991 and revised on May 1. 1997. The licensee

had included an inspection for the spring defect into the EDG

maintenance procedure. A defective spring was identified at Catawba in

1996. The spring was replaced. analyzed, and sent to the vendor for

'

Encloture 2

. _

._. _ _ _ _ .. ..

. . .. .

. ..

21

further analysis. The licensee's respon.e to the notice on this issue

was appropriate,

c. Conclusions

Resolution of DBD open items was generally adequate in that no safety

significant issues were identifieo in the open items. A violation was

identified for failure to follow licensee procedure requirements to

enter open DBD open items into the station PIP process for tracking and

. resolution. The audit of SITA corrective actions demonstrated that the

licensee was aggressively following SITA findings and is identified as a

strength in corrective action performance. Additionally, the licensee

adequately addressed the EDG 10 CFR Part 21 issue related to potentially

defective intake / exhaust springs.

E3 Engineering Procedures and Documentation

E3.1 Chanaes. Tests. and Exneriments Performed in Accordance With

10 CFR 50.59 (thru December 31. 1996)

a. Insoection Scone (37551)

'

f

By letter dated March 31, 1997. Duke Power Company (the licer.see)

submitted its annual summary of all changes, tests, and experiments,

which were completed under the provisions of 10 CF,150.59 for the period

through December 31. 1996. The licensee's March 31, 1997, summary

included approximately 380 changes made during the subject period. The

inspector evaluated these changes against the p,avisions of the

regulation.

<

b. Observations and Findinas

In accordance with 10 CFR 50.59, a licensee may: (1) make changes in

the facility as described in the safety analysis report, (2) make

changes -in the procedures as described in the safety analysis report,

and (3) corduct tests or experiments not described in the safety

analysis report, without prior Commission approval, unless the change

involvy a changc in the Technical Specifications or an Unreviewed

Safety duestion (US0). The regulation defines an US0 as a proposed

action that: (a) may increase the probability of occurrence or

consequences of an accident or malfunction of equipment important to

safety previously evaluated in the safety analysis report, or (b) may

create a possibility for an accident or malfunction of a different type

than any previously evaluated in the safety analysis report or (c) may

reduce the margin of safety as defined in the basis for any Technical

Specification.

The inspector reviewed the licensee's current (dated March 10. 1997)

version of Nuclear System Directive 209. "10 CFR 50.59 Evaluations."

which is patterned after NSAC-125. " Guidelines for 10 CFR 50.59 Safety

Enclosure 2

.

_ _ _ _ _-- __ --

22

Evaluations." June 1989. This document requires that changes be

evaluated against the appropriate Final Safety Analysis Report (FSAR).

Technical Specifications, end NRC Safety Evaluation Report sections to

determine if there is need for revision. Specifically, the criteria

specified by 10 CFR 50.59 are broken down into seven (7) questions. For

a change to be qualified for 10 CFR 50.59, the answers to all seven

questions must be "no". Based on review of this document, and the

review of the licensee's 10 CFR 50.59 evaluations. the inspector

concluded that the licensee's directive appropriately reflects the

criteria of this regulation and that. if followed accordingly, should

ensure that a change would be correctly performed under this regulation.

The inspector performed an in-office review of the licensee's summary to

determine the nature and safety significance of each change. Through

this review, the inspector selected the following changes for more

detailed review onsite:

e Exempt Changes:

Exempt Change CE-3176

Exempt Change CE-3705

Exempt Change CE-3759

Exempt Change CE-4745

Exempt Charge CE-4746

Exempt Change CE-4821

Exempt Change CE-4822

Exempt Change CE-7416

Exempt Change CE-7977

Exempt Change CE-8126

Exempt Change CE-8182

Exempt Change CE-8245

Exempt Change CE-8410

Exempt Change CE-61008

Exempt Change CE-61162

e Miscellaneous Changes:

SIMULATE (a computer code) Version 4

  • Modifications:

NSM CN-11371

NSM CN-20396

o 0:?rable But Degraded Evaluations:

PIF 2-C97-0157

PIP 2-096-3250

e Operability Evaluations:

Enclosure 2

_

~

. - _ _ _ _ _ _ _ _ _ _ - _ -

23

Operability Evaluation dated 2/15/94

Operability Evaluation dated 2/18/94

Operability Evaluation dated 6/28/94

e Procedure Channes:

OP/1/A/6200/11

AM/2/A/5100/07

OP/2/B/6200/33. Change 4 Rev. 4

OP/1/A/6550/14

PT/1/B/4700/82

The ins ector determined that these changes were correctly evaluated

under t e provisions of 10 CFR 50.59

During the in-office and onsite reviews, the inspector made a number of

observations and has communicated them to licensee personnel:

  • The use of nuke-specific system identifiers in the annual summary

(which is submitted to the NRC and is thus available to the

l

public) is discouraged unless the licensee provides a key in the

l summary. These identifiers do not bear any apparent correlation

l to the actual systems (e.g. , NC = reactor coolant system. KC =

l component cooling system, etc..). The inspector made a similar

observation on the summary submitted on March 2~. 1996 (see

Inspection Report 50-413.414/96-10).

'

o The licensee's corresponding revision of the UFSAR. per 10 CFR

50.71. lags behind 10 CFR 50.59 evaluations. The next u)date of

the UFSAR. scheduled for late 1997. should capture all tie changes

that are within the scope of the UFSAR.

e While the licensee had acceptably evaluated all the changes

audited by the inspector, a number of them eppeared in the summary

with insufficient information for a reader to even determine what

system was involved, or what change was made. The inspector

recommended a several-sentence description. identifying the

system, the component, and the nature of the change, and

accompanied by a several-sentence evaluation. Despite this

problem with the summary, the evaluations were found to be

thorough and in compliance with 10 CFR 50.59. The licensee was

aware of this aroblem with the summary and has initiated actions

to correct suc1 weakness by revising its guidance document. NSD

209 (see Problem Investigation Process Form 0-C97-2027. dated June

19. 1997).

  • The term " Exempt Changes" may cause confusion in the context of 10

CFR 50.59. It is a term internal to the licensee's docunentation.

It pertains to changes that "do not require the Modification

Enclosure 2

- _ _ _ _

1

b

24

Program controls for configuration management and therefore are

specifically exempted from the requirements to process an

editorial NM or NSM." According to licensee personnel, an " exempt

change" is essentially a minor change.

e The summary contained a significant number of errors, which stated

the opposite of the actual facts. For example, test procedure

TT/1/A/9200/88 states "there are Unreviewed Safety Questions

associated with this test procedure" when the onsite evaluation

shows that there was no unreviewed safety question. The licensee

submitted a letter on July 9, 1997, correcting such errors.

c. Crnclusions

Based on in-office review of the licensee's March 31, 1997, annual

summary on 10 CFR 50.59 changes, onsite review of the licensee's 10 CFR

50.59 evaluatius, and audit of the licensee's 3rocedures, the inspector

concluded that the licensee had complied with t1e provisions of the

regulation for the changes listed in the annual summary.

l

IV. Plant Suocort

R1 Radiological Protection and Chemistry Controls

R1.1 Tours of the Radiolooical Control Area (RCA) (71750)

The inspectors periodically toured the RCA during the inspection period.

t Radiological control practices were observed and discussed with

!

radiological control personnel, including RCA entry and exit, survey

postings locked high radiation areas, and radiological area material

conditions. The inspector concluded that radiological control practices

were proper.

V. Management Meetinas

X1 Exit Meeting Summary

The inspectors ) resented the inspection results to members of licensee

management at t1e conclusion of the inspection on July 11 and July 23. 1997.

The licensee acknowledged the findings presented. No proprietary information

was identified. Dissenting comments were not received from the licensee.

Enclosure 2

_ - _ _ _ . - - - _

.,

-. -

t

25

PARTIAL LIST OF PERSONS CONTACTED

Licensee

Bhatnager. A. . Operations Su>erintendent

Birch. M. . Safety Assurance ianager

Coy., S., Radiation Protection Manager

Forbes. J., Engineering Manager

Jones. R.. Station Manager

Harrall. T., Instrument and Electrical Maintenance Superintendent

Kelly. C.. Mainteriance Manager

Kimball . D. , Safety Review Group Manager

Kitlan. M., Regulatory Compliance Manager

'

Nicholson. K., Compliance Specialist

Peterson. G., Catawba Site Vice-President

Tower. D., Regulatory Compliance

l

,

4

Enclosure 2

u

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26

INSPECTION PROCEDURES USED

IP 37551: Onsite Engineering

IP 40500: Effectiveness of Licensee Controls in Identifying. Resolving, and

Preventing Problems i

IP 61726: Surveillance Observation

IP 37550: Engineering

IP 62707: Maintenance Observation

IP 71707: Plant Operations

IP 71750: Plant Support Activitia

IP 92901: Followup - Operations

IP 92902: Followup - Maintenance

IP 92903: Followup - Engineering

IP 93702: Prompt Onsite Respense to Events

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

i

50-414/97-09-01 NCV Failure to Declare Ice Condenser

Intermediate Deck Doors Inoperable and Log

Appropriate TSAIL Entry (Section C1.1)

50-414/97-09-02 NCV Inadequate Lower Containment Ventilation

Unit Operating Procedure (Section 01.4)

'

50-414/97-09-03 VIO Failure to Follow Procedure Results in

Invalid Local Leak Rate Test of Valve 2NV-

874 (Section M1.2)

50-413.414/97-09-04 VIO Failure to Follow Procedure - Two Examples

(Sections 08.1. E2.1)

Closed

50-413.414/97-01-01 VIO Failure to Include All Structures Systems

and Components in the Scope of the

Maintenance Rule as Required by 10 CFR

50.65(b) (Section M8.1)

50-414.414/97-01-02 IFI Followup and review of licensee procedure

to implement the requirements of (a)(1)

and (a)(2) of the Maintenance Rule after

issuance of Revision 2 of Regulatory Guide

1.160 (Section M8.3)

50-413.414/97-01-03 IFl Followup on Licensee Actions to Provide

Performance Criteria for Structures After

Resolution of this Issue (Section M8.4)

Enclosure 2

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27

50-413.414/97-01-04 VIO Failure to implement the requirements of

(a)(1) and (a)(2) of the Maintenance Rule

(Section M3.2)

50 413.414/94-13-02 URI Emergency Operating Procedure 50.59

Evaluations Not Reviewed by Nuclear Safety

'

Review Board as Required by TS (Section l

08.1)

<

l List of Acronyms

! CFR -

Code of Federal Fagulations

DBD -

Design Basis Documents

EDG -

Emergency Diesel Generator

EDM -

Engineering Directives Manual

E0P -

Emergency Operating Procedure

FIP -

Failure Investigative Process

FSAR -

Final Safety Analysis Report

IAE -

Instrument and Electrical

IFI -

Inspector Followup Iten

IST -

Inservice Testing

LCVU -

Lower Containment Ventilation Unit

LER -

Licensee Event Report

LLRT -

Local Leak Rate Test

MPFF -

Maintenance Preventable Function Failure

NCV -

Non Cited Violation

NM -

Nuclear Sampling

NRC -

Nuclear Regulatory Commission

NSD -

Nuclear Site Directive

NSRB -

Nuclear Safety Review Board

DAC -

Operator Aid Com] uter

POR -

Public Document Room

PIP -

Problem Investigation Process

PM -

Preventive Maintenance

asig -

Pounds Per Square Inch Gauge

RCA -

Radiologically Controlled Area

RCP -

Reactor Coolant Pump

RCS -

Reactor Coolant System

RG -

Regulatory Guide

SA --

Main Steam to Auxiliary Equipment

SB0 -

Station Blackout Role

SITA - Self Initiated Technical Audit

SPOC -

Single Point of Contact

TPBE - Thermal Power Best Estimate

TS -

Technical Specifications

TSAIL - Tech Spec' Action Item Log

UCLF - Unplanned Capability loss Factor

UFSAR - Updated Final Safety Analysis Report

Enclosure 2

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28

URI- -

Unresolved Item-

USO -

Unreviewed Safety Question

VDC' -

Volts direct current

.

VIO -

Violation

-VV -

Containment Ventilation

WO -

Work Order

YN -

Auxiliary Building Chilled Water

l

Enclosure 2

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