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{{#Wiki_filter:UNITED NUCLEAR REGULATORY  
{{#Wiki_filter:UNITED STATES
REGION 475 ALLENDALE KING OF PRUSSIA, PA  
                                  NUCLEAR REGULATORY COMMISSION
October 15, 2009 Mr. Paul Harden Site Vice President  
                                                      REGION I
FirstEnergy  
                                                475 ALLENDALE ROAD
Nuclear Operating  
                                          KING OF PRUSSIA, PA 19406-1415
Company Beaver Valley Power Station P. O. Box 4, Route 168 Shippingport, PA 15077  
                                        October 15, 2009
BEAVER VALLEY POWER STATION -NRC PROBLEM IDENTIFICATION  
Mr. Paul Harden
AND RESOLUTION  
Site Vice President
INSPECTION  
FirstEnergy Nuclear Operating Company
REPORT 05000334/2009008  
Beaver Valley Power Station
AND 05000412/2009008  
P. O. Box 4, Route 168
Dear Mr. Harden: On September  
Shippingport, PA 15077
3,2009, the U.S. Nuclear Regulatory  
SUBJECT:        BEAVER VALLEY POWER STATION - NRC PROBLEM IDENTIFICATION
Commission (NRC) completed  
                AND RESOLUTION INSPECTION REPORT 05000334/2009008 AND
an inspection  
                05000412/2009008
at your Beaver Valley Power Station Units 1 and 2. The enclosed report documents  
Dear Mr. Harden:
the inspection  
On September 3,2009, the U.S. Nuclear Regulatory Commission (NRC) completed an
results, which were discussed  
inspection at your Beaver Valley Power Station Units 1 and 2. The enclosed report documents
on September  
the inspection results, which were discussed on September 3,2009, with Mr. Roy Brosi and
3,2009, with Mr. Roy Brosi and other members of your staff. This inspection  
other members of your staff.
was an examination  
This inspection was an examination of activities conducted under your license as they relate to
of activities  
the identification and resolution of problems, and compliance with the Commission's rules and
conducted  
regulations and the conditions of your operating license. Within these areas, the inspection
under your license as they relate to the identification  
involved examination of selected procedures and representative records, observations of
and resolution  
activities, and interviews with personnel.
of problems, and compliance  
Based on the samples selected for review, the inspection team concluded that FirstEnergy
with the Commission's  
Nuclear Operating Company (FENOC) was generally effective in identifying, evaluating and
rules and regulations  
resolving problems. FENOC personnel identified problems at a low threshold and entered them
and the conditions  
into the Corrective Action Program (CAP). FENOC personnel screened issues appropriately for
of your operating  
operability and reportability, and prioritized issues commensurate with the safety significance of
license. Within these areas, the inspection  
the problems. Root and apparent cause analyses appropriately considered extent of condition,
involved examination  
generic issues, and previous occurrences. Corrective actions addressed the identified causes
of selected procedures  
and were typically implemented in a timely manner. However, the inspectors noted several
and representative  
examples for improvement in the identification of plant issues, and examples where evaluations
records, observations  
lacked rigor to fully explore the corrective actions needed to address the issue.
of activities, and interviews  
This report documents one NRC-identified finding of very low safety significance (Green). The
with personnel.  
finding was determined to involve a violation of NRC requirements. However, because of its
Based on the samples selected for review, the inspection  
very low safety significance and because it has been entered into your CAP, the NRC is
team concluded  
treating this finding as a non-cited violation (NCV), in accordance with Section VI.A.1 of the
that FirstEnergy  
NRC's Enforcement Policy. If you deny this NCV, you should provide a response with the basis
Nuclear Operating  
for your denial, within 30 days of the date of this inspection report, to the U.S. Nuclear
Company (FENOC) was generally  
effective  
in identifying, evaluating  
and resolving  
problems.  
FENOC personnel  
identified  
problems at a low threshold  
and entered them into the Corrective  
Action Program (CAP). FENOC personnel  
screened issues appropriately  
for operability  
and reportability, and prioritized  
issues commensurate  
with the safety significance  
of the problems.  
Root and apparent cause analyses appropriately  
considered  
extent of condition, generic issues, and previous occurrences.  
Corrective  
actions addressed  
the identified  
causes and were typically  
implemented  
in a timely manner. However, the inspectors  
noted several examples for improvement  
in the identification  
of plant issues, and examples where evaluations  
lacked rigor to fully explore the corrective  
actions needed to address the issue. This report documents  
one NRC-identified  
finding of very low safety significance (Green). The finding was determined  
to involve a violation  
of NRC requirements.  
However, because of its very low safety significance  
and because it has been entered into your CAP, the NRC is treating this finding as a non-cited  
violation (NCV), in accordance  
with Section VI.A.1 of the NRC's Enforcement  
Policy. If you deny this NCV, you should provide a response with the basis for your denial, within 30 days of the date of this inspection  
report, to the U.S. Nuclear
P. 2 Regulatory
Commission, ATTN.: Document Control Desk, Washington
DC 20555-0001, with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, U.S. Nuclear Regulatory
Commission, Washington, DC 20555-0001;
and the NRC Senior Resident Inspector
at the Beaver Valley Power Station. In addition, if you disagree with the characterization
of any finding in this report, you should provide a response within 30 days of the date of this inspection
report, with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC Senior Resident Inspector
at the Beaver Valley Power Station. The information
you provide will be considered
in accordance
with Inspection
Manual Chapter 0305. In accordance
with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available
electronically
for public inspection
in the NRC Public Document Room or from the Publicly Available
Records (PARS) component
of the NRC's document system (ADAMS). ADAMS is accessible
from the NRC Web Site at (the Public Electronic
Reading Room). Sincerely, IRA! Raymond J. Powell, Chief Technical
Support & Assessment
Branch Division of Reactor Projects Docket Nos.: 50-334, 50-412 License Nos: DPR-66, NPF-73
Inspection
Report 05000334/2009008;
05000412/2009008
w/Attachment:
Supplemental
Information
cc w/encls: Distribution
via ListServ 
P. 3 copies to the Regional Administrator, Region I; the Director, Office of Enforcement, U.S. Nuclear Regulatory
Commission, Washington, DC 20555-0001;
and the NRC Senior Resident Inspector
at the Beaver Valley Power Station. In addition, if you disagree with the characterization
of any finding in this report, you should provide a response within 30 days of the date of this inspection
report, with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC Senior Resident Inspector
at the Beaver Valley Power Station. The information
you provide will be considered
in accordance
with Inspection
Manual Chapter 0305. In accordance
with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available
electronically
for public inspection
in the NRC Public Document Room or from the Publicly Available
Records (PARS) component
of the NRC's document system (ADAMS). ADAMS is accessible
from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html(the
Public Electronic
Reading Room). Sincerely, IRAJ Raymond J. Powell, Chief Technical
Support & Assessment
Branch Division of Reactor Projects Docket Nos.: 50-334, 50-412 License Nos: DPR-66, NPF-73
Inspection
Report 05000334/2009008;
05000412/2009008
w/Attachment:
Supplemental
Information
Distribution
w/encl: (via e-mail) S. Collins, RA (R10RAMAILRESOURCE)
M. Dapas, DRA
D. Spindler, DRP, RI D. Lew, DRP (R1
P. Garrett, DRP, OA J. Clifford, DRP (R1DRPMAIL
RESOURCE)
L. Trocine, RI OEDO R. Bellamy, RIDSNRRPMBEAVERVAllEY
RESOURCE G. Barber, ROPreportsResource@nrc.qov
C. Newport, Region I Docket Room (with concurrences)
J. Greives, DRP D. Werkheiser, DRP, SRI SUNSI Review Complete:
tcs (Reviewer's
ML092920008
DOCUMENT NAME: G:\DRP\BRANCH
TSAB\lnspection
Reports\Beaver
Valley PI&R 2009\BV
After declaring
this document "An Official Agency Record" it will be released to the To receive a copy of this document, indicate In the box: 'C' =Copy without attachment/enclosure
'E" =Copy with attachment/enclosure "N" =No OFFICE: RI/DRP NAME: TSetzer/tcs
RBeliamy/rjp
for DATE: 10/13109 10/14/09 
Docket License Report Team
Approved 1 U.S. NUCLEAR REGULATORY
REGION 50-334, DPR-66, 05000334/2009008
and
FirstEnergy
Nuclear Operating
Company Beaver Valley Power Station, Units 1 and Post Office Box Shippingport, PA August 17 through September
3, Thomas Setzer, PE, Senior Project
Division of Reactor Projects (DRP) Jeffery Bream, Project Engineer, DRP Elizabeth
Keighley, Reactor Inspector, DRP David Spindler, Beaver Valley Resident Inspector, DRP Raymond J. Powell, Chief Technical
Support &Assessment
Branch Division of Reactor Projects Enclosure 
2 SUMMARY OF FINDINGS IR 05000334/2009008, IR 05000412/2009008;
08/17/2009
-09/03/2009;
Beaver Valley Power Station, Units
1 & 2; Biennial Baseline Inspection
of the Identification
and Resolution
of Problems.
One finding was identified
in the area of prioritization
and evaluation
of issues. This team inspection
was performed
by three NRC regional inspectors
and one resident inspector.
One finding of very low safety significance (Green) was identified
during this inspection
and was classified
as a non-cited
violation (NCV). The significance
of most findings is indicated
by their color (Green, White, Yellow, Red) using NRC Inspection
Manual Chapter (IMC) 0609, "Significance
Determination
Process" (SOP). The cross-cutting
aspect was determined
using IMC 0305, "Operating
Reactor Assessment
Program." Findings for which the SOP does not apply may be Green or be assigned a severity level after NRC management
review. The NRC's program for overseeing
the safe operation
of commercial
nuclear power reactors is described
in NUREG-1649, "Reactor Oversight
Process," Revision 4, December 2006. Identification
and Resolution
of Problems The inspectors
concluded
that FENOC was, in general, effective
in identifying, evaluating, and resolving
problems.
Beaver Valley personnel
identified
problems at a low threshold
and entered them into the Corrective
Action Program (CAP). The inspectors
determined
that Beaver Valley personnel
screened issues appropriately
for operability
and reportability, and prioritized
issues commensurate
with the safety significance
of the problems.
Root and apparent cause analyses appropriately
considered
extent of condition, generic issues, and previous occurrences.
The inspectors
determined
that corrective
actions addressed
the identified
causes and were typically
implemented
in a timely manner. However, the inspectors
noted one NCV of very low safety significance
in the area of prioritization
and evaluation
of issues. This issue was entered into FENOC's CAP during the inspection.
FENOC's audits and self-assessments
reviewed by the inspectors
were thorough and probing. Additionally, the inspectors
concluded
that FENOC adequately
identified, reviewed, and applied relevant industry operating
experience (OE) to the Beaver Valley Power Station. Based on interviews, observations
of plant activities, and reviews of the CAP and the Employees
Concerns Program (ECP), the inspectors
did not identify any concerns with site personnel
willingness
to raise safety issues, nor did the inspectors
identify conditions
that could have had a negative impact on the site's safety conscious
work environment (SCWE). Cornerstone:
Mitigating
Systems Green. The inspectors
identified
an NCV of very low safety significance (Green) of 10 CFR 50.65(a)(2), "Requirements
for Monitoring
the Effectiveness
of Maintenance
at Nuclear Power Plants," due to FENOC personnel's
failure to demonstrate
that the 10 CFR 50.65(a)(2)
performance
of the containment
isolation
valve limit switches was effectively
controlled
through the performance
of appropriate
preventive
maintenance.
Specifically, as evidenced by
repeat dual position indications
of containment
isolation
valves in the control room between 2007 and 2009 resulting
in 21 unplanned
entries into Technical
Specification
3.6.3, the containment
isolation
valve system 10 CFR 50.65(a)(2)
performance
demonstration
was no longer justified
in accordance
with Maintenance
Rule Enclosure 
implementing
procedure
guidance.
This should have resulted in placement
of the containment
isolation
valve system in 10 CFR 50.65(a)(1)
for goal setting and monitoring.
FENOC entered this issue into the CAP (CR 09-64040).
The inspectors
determined
the finding was more than minor because it is associated
with the Equipment
Performance
attribute
of the Mitigating
Systems cornerstone
and adversely
affected the cornerstone
objective
of ensuring the reliability
of systems that respond to initiating
events to prevent undesirable
consequences.
The finding was determined
to be of very low safety significance (Green) because the finding did not involve a design or qualification
deficiency
resulting
in loss of operability
or functionality, did not result in a loss of system safety function, and did not screen as potentially
risk significant
due to external initiating
events. The inspectors
determined
that this finding had a cross-cutting
aspect in the "Corrective
Action Program" component
of the Problem Identification
and Resolution
cross-cutting
area because FENOC did not take appropriate
corrective
actions to address safety issues and adverse trends associated
with faulty containment
isolation
valve limit switches in a timely manner, commensurate
with their safety significance
and complexity
[P.1(d)]. (Section 40A2.1c) Enclosure 
.1 REPORT DETAILS 4. OTHER ACTIVITIES (OA) 40A2 Problem Identification
and Resolution (PI&R) (71152B) Assessment
of the Corrective
Action Program Effectiveness
a. Inspection
Scope The inspectors
reviewed FENOC's procedures
that describe the CAP at the Beaver Valley Power Station. FENOC personnel
identified
problems by initiating
condition
reports (CRs) for conditions
adverse to quality, plant equipment
deficiencies, industrial
or radiological
safety concerns, and other significant
issues. Condition
reports were subsequently
screened for operability
and reportability, and categorized
by significance, which included levels SR (significant
condition
adverse to quality, root cause), AR (adverse condition, root cause), AA (adverse condition, full apparent cause), AL (adverse condition, limited apparent cause), AF (adverse condition, fix), and AC (adverse condition, close). CRs were assigned to personnel
for evaluation
and resolution
or trending.
The inspectors
evaluated
the process for assigning
and tracking issues to ensure that issues were screened for operability
and reportability, prioritized
for evaluation
and resolution
in a timely manner commensurate
with their safety significance, and tracked to identify adverse trends and repetitive
issues. In addition, the inspectors
interviewed
plant staff and management
to determine
their understanding
of, and involvement
with, the CAP. The inspectors
reviewed CRs selected across the seven cornerstones
of safety in the NRC's Reactor Oversight
Process (ROP) to determine
if site personnel
properly identified, characterized, and entered problems into the CAP for evaluation
and resolution.
The inspectors
selected items from functional
areas that included physical security, emergency
preparedness, engineering, maintenance, operations, and radiation
safety to ensure that FENOC appropriately
addressed
problems identified
in these functional
areas. The inspectors
selected a risk-informed
sample of CRs that had been issued since the last NRC Problem Identification
and Resolution (PI&R) inspection
conducted
in April 2007. Insights from the station's
risk analyses were considered
to focus the sample selection
and plant walkdowns
on risk-significant
systems and components.
The corrective
action review was expanded to five years for evaluation
of identified
concerns within CRs relative to radiation
monitors.
The inspectors
selected items from various processes
at Beaver Valley to verify that they were appropriately
considered
for entry into the CAP. Specifically, the inspectors
reviewed a sample of Maintenance
Rule functional
failure evaluations, operability
determinations, system health reports, work orders (WOs), and issues entered into the Employee Concerns Program (ECP). The inspectors
inspected
plant areas including
the turbine buildings, safeguards
buildings, intake structure, emergency
diesel generator
buildings, yard areas, security areas, and control room. Enclosure 
The inspectors
reviewed CRs to assess whether FENOC personnel
adequately
evaluated
and prioritized
issues. The CRs reviewed encompassed
the full range of evaluations, including
root cause analyses, full apparent cause evaluations, limited apparent cause analyses, and common cause analyses.
A sample of CRs that were assigned lower levels of significance
which did not include formal cause evaluations (AF and AC significance
levels) were also reviewed by the inspectors
to ensure they were appropriately
classified.
The inspectors'
review included the appropriateness
of the assigned significance, the scope and depth of the analysis, and the timeliness
of resolution.
The inspectors
assessed whether the evaluations
identified
likely causes for the issues and identified
appropriate
corrective
actions to address the identified
causes. As part of this review, the inspectors
interviewed
various station personnel
to fully understand
details within the evaluations
and the proposed and completed
corrective
actions. The inspectors
observed management
review board (MRB) meetings in which FENOC personnel
reviewed new CRs for prioritization
and assignment.
Further, the inspectors
reviewed equipment
operability
determinations
and extent-of-condition
reviews for selected CRs to verify these specific reviews adequately
addressed
equipment
operability
and the extent of problems.
The inspectors'
review of CRs also focused on the associated
corrective
actions in order to determine
whether the actions addressed
the identified
causes of the problems.
The inspectors
reviewed CRs for adverse trends and repetitive
problems to determine
whether corrective
actions were effective
in addressing
the broader issues. The inspectors
reviewed FENOC's timeliness
in implementing.
corrective
actions and effectiveness
in precluding
recurrence
for significant
conditions
adverse to quality. Lastly, the inspectors
reviewed CRs associated
with NRC non-cited
violations (NCV) and findings since the last PI&R inspection
to determine
whether FENOC personnel
properly evaluated
and resolved the issues. Specific documents
reviewed during the inspection
are listed in the Attachment
to this report. b. Assessment
Effectiveness
of Problem Identification
Based on the selected samples reviewed, plant walkdowns, and interviews
of site personnel, the inspectors
determined
that, in general, FENOC personnel
identified
problems and entered them into the CAP at a low threshold.
For the issues reviewed, the inspectors
noted that problems or concerns had been appropriately
documented
in enough detail to understand
the issues. Approximately
19,000 CRs had been written by FENOC personnel
since January 2007. The inspectors
noted that the Security department
had generated
significantly
less CRs when compared to the rest of the site. Interviews
with Security personnel
revealed that they had received adequate training, displayed
a willingness
to raise issues, and had ample access to computers;
however, there was a reliance on the shift Captain to enter issues into the CAP. The inspectors
observed managers and supervisors
at MRB meetings appropriately
questioning
and challenging
CRs to ensure clarity of the issues. The inspectors
determined
that FENOC personnel
trended equipment
and programmatic
issues, and CR descriptions
appropriately
included reference
to repeat occurrences
of issues. The Enclosure 
inspectors
concluded
that personnel
were identifying
trends at low levels. The inspectors
toured plant areas including
the turbine buildings, safeguards
buildings, intake structure, emergency
diesel generator
buildings, yard areas, security areas and control room to determine
if FENOC personnel
identified
plant issues at the proper threshold.
Housekeeping
in all areas, with the exception
of the Unit 2 intake structure, was noted to be improved since the 2007 NRC PI&R inspection.
During the plant walkdown, the inspectors
identified
three examples of adverse conditions
that had not been identified
by FENOC. The following
issues were entered into the CAP for evaluation
and resolution: During an inspection
of the east end of the main intake structure, the inspectors
identified
an oxygen bottle strapped to an Appendix R ladder (a ladder used by plant personnel
for implementing the
site fire protection
program).
Restraining
the oxygen bottle and Appendix R ladder together in this fashion represented
a minor procedure
violation
of Beaver Valley procedure, 1/2-PIP-G01, "Securing
Transient/Temporary/Stored
Equipment
in Safety-Related
Areas." This issue is minor because there was no adverse impact to plant safety equipment, and there was only minimal impact on operator fire response times. FENOC entered this into the CAP (CR 09-63536). During an inspection
of the 'D' intake structure
cubicle, the inspectors
identified
rigging scaffolding
with a chainfall
that had been left draped over a safety related component.
Scaffold contacting
plant equipment
represented
a minor procedure
violation
of Beaver Valley procedure, 1/2-ADM-0810, "Scaffold
Erection and Tagging." The component
was not damaged nor had any reduced capability
as a result of the contact with the chainfall.
This issue is minor because there was no loss of operability
or adverse impact to the safety related component.
FENOC entered this into the CAP (CR 09-63532). During an inspection
of the Unit 2 Safeguards
Building, the inspectors
identified
four plastic buckets filled with lubricating
oil totaling 20 gallons. The unattended
oil in a safety related fire area represented
a minor procedure
violation
of Beaver Valley procedure, 1/2-ADM-1906, "Control of Transient
Combustible
and Flammable
Materials." This issue is minor because the increase in combustible
loading in the room as a result of the unattended
oil did not violate the plant fire hazard analysis.
FENOC entered this into the CAP (CR 09-63441).
In accordance
with NRC Inspection
Manual Chapter 0612, "Power Reactor Inspection
Reports," the above issues constitute
violations
of minor significance
that are not subject to enforcement
action in accordance
with the NRC's Enforcement
Policy. Effectiveness
of Prioritization
and Evaluation
of Issues The inspectors
determined
that, in general, FENOC personnel
appropriately
prioritized
and evaluated
issues commensurate
with their safety significance.
CRs were screened for operability
and reportability, categorized
by significance, and assigned to a department
for evaluation
and resolution.
The CR screening
process considered
human performance
issues, radiological
safety concerns, repetitiveness
and adverse trends. The inspectors
observed managers and supervisors
at MRB meetings appropriately
questioning
and challenging
CRs to ensure appropriate
prioritization.
Enclosure 
CRs were categorized
for evaluation
and resolution
commensurate
with the significance
of the issues. Based on the sample of CRs reviewed, the guidance provided by the FENOC implementing procedures appeared
sufficient
to ensure consistency
in categorization
of the issues. Operability
and reportability
determinations
were performed
when conditions
warranted
and the evaluations
supported
the conclusions.
Causal analyses appropriately
considered
extent of condition, generic issues, and previous occurrences.
During this inspection, the inspectors
noted that, in general, FENOC's root cause analyses were thorough, and corrective
and preventive
actions addressed
the identified
causes. Additionally, the identified
causes were well supported.
An NCV was identified
for FENOC's failure to demonstrate
that the 10 CFR 50.65(a)(2)
performance
of the containment
isolation
valve limit switches was effectively
controlled
through the performance
of appropriate
preventive
maintenance.
This NCV is discussed
in the findings section of this assessment
area. The inspectors
identified
the following
two examples of issues that were not fully evaluated
or prioritized
for corrective
action: A root cause evaluation (CR 08-39835)
associated
with a 2.5 inch drain down of the Unit 2 reactor coolant system during refueling
outage 2R13 did not identify all corrective
actions necessary
to address all failed barriers.
The inspectors
noted that the root cause evaluation
had not included corrective
actions to address the communication
failure within operations
shifts, and the work management
scheduling
issues which contributed
to a component
tagoutlctearance
being inappropriately
implemented.
The issue is minor because while corrective
actions were not assigned to address all failed barriers, FENOC had discussed
communication
expectations
with each operating
crew and there have not been any repeat issues. FENOC entered these issues into the CAP (CR 09-63454 and 09-63479). The inspectors
identified
three CRs describing
component
mispositioning
events (CR 09-59541, CR 09-58355, and CR 09-57224)
that were prioritized
as CR level OlAF." The failure to prioritize
these CRs as a limited apparent cause (CR level "AL") represented
a minor procedure
violation
of Beaver Valley procedure, OP-0004, "Component
Mispositioning." The inspectors
reviewed NRC Inspection
Manual Chapter 0612, Appendix E, "Minor Examples," and determined
this issue was minor because there
was no loss of operability
or safety impact. FENOC entered this issue into the CAP (CR 09-64004 and CR 09-63975).
In accordance
with NRC Inspection
Manual Chapter 0612, "Power Reactor Inspection
Reports," these issues constitute
violations
of minor significance
that are not subject to enforcement
action in accordance
with the NRC's Enforcement
Policy. Effectiveness
of Corrective
Actions The inspectors
concluded
that corrective
actions for identified
deficiencies
were generally
timely and adequately
implemented.
For significant
conditions
adverse to quality, corrective
actions were identified
to prevent recurrence.
The inspectors
concluded
that corrective
actions to address NCVs and findings since the last PI&R inspection
were timely and effective.
The inspectors
identified
the following
example where corrective
actions were not fully effective
in addressing
an issue: Enclosure 
The inspectors
reviewed corrective
actions taken in response to an NCV documented
in NRC report 05000334/05000412
2007004. CR 07-24074 was written to ensure bearing temperatures
would be monitored
when performing
surveillance
testing on the turbine driven auxiliary
feedpumps (TDAFWP).
The inspectors
found that the comprehensive
surveillance
tests for Unit 1 and Unit 2 (Beaver Valley procedures
10ST-24.9
and 20ST-24.4A, respectively)
did not have a precaution
stating that this surveillance
was not suitable to be used for post maintenance
testing as there is no guidance prescribed
to monitor and achieve steady bearing temperatures.
The inspectors
determined
that the issue was minor because the preventive
maintenance
work order had contained
the appropriate
guidance.
FENOC entered this issue into the CAP (CR 09-64015).
c. Findings Introduction:
The inspectors
identified
an NCV of very low safety significance (Green) of 10 CFR 50.65(a)(2), "Requirements
for Monitoring
the Effectiveness
of Maintenance
at Nuclear Power Plants," due to FENOC personnel's
failure to demonstrate
that the 10 CFR 50.65(a)(2)
performance
of the containment
isolation
valve limit switches was effectively
controlled
through the performance
of appropriate
preventive
maintenance.
Specifically, as evidenced
by repeat dual position indications
of containment
isolation
valves in the control room resulting
in 21 unplanned entries into
Technical
Specification
3.6.3, the containment
isolation
valve system 10 CFR 50.65(a)(2)
performance
demonstration
was no longer justified
in accordance
with Maintenance
Rule implementing
procedure
guidance.
Description:
The containment
isolation
valve system is a risk-significant
system that is scoped within the Maintenance
Rule because it is a system, structure, or component (SSC) required to mitigate accidents/transients
and is identified
in emergency
operating
procedures.
The primary Maintenance
Rule function of the containment
isolation
valve system is to provide a containment
isolation
function during an event to prevent offsite radiological
release. Additionally, limit switches associated
with each containment
isolation
valve are scoped within the Maintenance
Rule because they provide a function to indicate valve position
in the control room for operators
to use during emergency
operating
procedures.
In February 2009, during stroke-time
testing, an air-operated
containment
isolation
valve displayed
dual indication
in the control room, causing the stroke times of the valve to be indeterminate
and causing an unplanned
entry into Technical
Specification
3.6.3. Additionally, between January 2007 and July 2009, Technical
Specification
3.6.3 had 21 unplanned
entries as a result of faulty limit switches on similar containment
isolation
valves. This resulted in the FENOC established
containment
isolation
valve system Maintenance
Rule condition
monitoring
criteria being exceeded, which required FENOC to perform a Maintenance
Rule 10 CFR 50.65(a)(1)
evaluation.
The Maintenance
Rule (a)(1) evaluation
was completed
in February 2009 and concluded
that the containment
isolation
valve system should continue to be monitored
in accordance
with Maintenance
Rule 10 CFR 50.65(a)(2)., This reinforced
a similar decision made in 2007 based on a Maintenance
Rule (a)(1) evaluation
recommendation
to keep the system in (a)(2) despite Enclosure 
the condition
monitoring
criteria being exceeded due to multiple dual indications
in the control room. The basis of the decision was that the dual indication
issue was a result of faulty limit switches, and that this did not affect the valve's safety related function to close during an event to prevent offsite radiological
release. Site personnel
determined
the direct cause was the limit switch being out of adjustment
due to a problem with the required torque. Despite the repeat failures, FENOC failed to implement
or revise preventive
maintenance
practices
for these limit switches.
Subsequently, the Maintenance
Rule Steering Committee
approved a revision to clarify the monitoring
criteria for the containment
isolation
valve system, which would exclude future indication
problems that did not affect the valve's ability to isolate containment.
However, it failed to take into account the limit switches'
Maintenance
Rule function in emergency
operating
procedures, specifically, the ability to accurately
indicate valve position in the control room during an event. Following
the change to the condition
monitoring
criteria, the site had seven valves display dual indication
in the control room between February 2009 and June 2009 that FENOC concluded
did not affect valve operability.
The inspectors
concluded
that the numerous dual indications
of the limit switches should have been evaluated
against FENOC's Maintenance
Rule condition
monitoring
criteria and should have resulted in placement
of the containment
isolation
valve system in 10 CFR 50.65(a)(1)
for goal setting and monitoring.
FENOC performed
an extent of condition
review on two other valves of the same model, and determined
that the torque on the limit switch fasteners
needed to be adjusted.
FENOC corrected
the torque issue and has implemented
plans to install a button tab on the limit switches to minimize misalignment
causing dual indications.
Analysis:
The inspectors
determined
that the failure to demonstrate
that the 10 CFR 50.65{a)(2)
performance
of the containment
isolation
valve limit switches was effectively
controlled
through the performance
of appropriate
preventive
maintenance
was a performance
deficiency
within FENOC personnel's
ability to foresee and correct and should have been prevented.
Traditional
Enforcement
did not apply, as the issue did not have actual or potential
safety consequence, had no willful aspects, nor did it impact the NRC's ability to perform its regulatory
function.
A review of NRC Inspection
Manual Chapter (IMC) 0612, Appendix E, "Minor Examples," revealed that no minor examples were applicable
to this finding. The inspectors
determined
the finding was more than minor because it is associated
with the Equipment
Performance
attribute
of the Mitigating
Systems cornerstone
and adversely
affected the cornerstone
objective
of ensuring the reliability
of systems that respond to initiating
events to prevent undesirable
consequences.
Specifically, the dual indication
of containment
isolation
valves in the control room due to faulty limit switches presents a challenge
to the operators
during event response while implementing
emergency
operating
procedures, and has resulted in 21 unplanned
Technical
Specification
entries. The numerous dual indication
instances
should have caused the containment
isolation
valve system to be placed in 10 CFR 50.65(a)(1)
for goal setting and monitoring.
The inspectors
determined
the significance
of the finding using IMC 0609.04, "Phase 1 Initial Screening
and Characterization
of Findings." The finding was determined
to be of very low safety significance (Green) because the finding did not involve a design or qualification
deficiency
resulting
in loss of operability
or functionality, did not result in a loss of system Enclosure 
safety function, and did not screen as potentially
risk significant
due to external initiating
events. The inspectors
determined
that this finding had a cross-cutting
aspect in the "Corrective
Action Program" component
of the Problem Identification
and Resolution
cross-cutting
area because FENOC did not take appropriate
corrective
actions to address safety issues and adverse trends associated
with faulty containment
isolation
valve limit switches in a timely manner, commensurate
with their safety
significance
and complexity
[P.1 (d)). Enforcement:
10 CFR 50.65(a)(1)
requires, in part, that holders of an operating
license shall monitor the performance
or condition
of SSCs within the scope of the monitoring
program as defined in 10 CFR 50.65(b) against licensee-established
goals, in a manner sufficient
to provide reasonable
assurance
that such SSCs are capable of fulfilling
their intended functions.
10 CFR 50.65(a)(2)
states, in part, that monitoring
as specified
in 10 CFR 50.65(a)(1)
is not required where it has been demonstrated
that the performance
or condition
of an SSC is being effectively
controlled
through the performance
of appropriate
preventative
maintenance, such that the SSC remains capable of performing
its intended function.
Contrary to the above, between 2007 and 2009, FENOC personnel
failed to demonstrate
that the 10 CFR 50.65(a)(2)
performance
of the containment
isolation
valve limit switches was effectively
controlled
through the performance
of appropriate
preventive
maintenance.
FENOC has performed
an extent of condition
review and has initiated
corrective
actions to install a button tab on the limit switches to minimize misalignment
causing the dual indications.
Because this violation
was of very low safety significance
and has been entered into the CAP (CR 09-64040), this violation
is being treated as an NCV, consistent
with the NRC Enforcement
Policy (NCV 05000314,412/2009008-01:
Containment
Isolation
Valve System 10 CFR 50.65 (a)(2) Performance
Demonstration
Not Met) . . 2 Assessment
of the Use of Operating
Experience
a. Inspection
Scope The inspectors
selected a sample of CRs associated
with the review of industry Operating
Experience (OE) to determine
whether FENOC personnel
appropriately
evaluated
the OE information
for applicability
to Beaver Valley and had taken appropriate
actions, when warranted.
The inspectors
reviewed CR evaluations
of OE documents
associated
with a sample of NRC Generic Letters and Information
Notices to ensure that FENOC adequately
considered
the underlying
problems associated
with the issues for resolution
via their CAP. The inspectors
also observed plant activities
to determine
if industry OE was considered
during the performance
of routine activities.
Specific documents
reviewed during the inspection
are listed in the Attachment
to this report. b. Assessment
The inspectors
determined
that, in general, FENOC appropriately
considered
industry OE information
for applicability, and used the information
for corrective
and preventive
actions Enclosure 
to identify and prevent similar issues when appropriate.
The inspectors
determined
that OE was appropriately
applied and lessons learned were communicated
and incorporated
into plant operations.
The inspectors
observed that industry OE was routinely
discussed
and considered
during the performance
of plant activities.
The inspectors
reviewed a fleet-level
focused self-assessment
of OE performed
in May 2008. The self-assessment
identified
a number of weaknesses, specifically: OE was not discussed
in system health reports; Roles and responsibilities
of Section OE Coordinators
were not clearly defined; Familiarization
with SAP, the database used to manage OE, was low at the Management
and Section OE Coordinator
levels; and Procedures
describing
the requirements
to process OE were in need of revision to add clarity. Although the inspectors
noted that corrective
actions were not completed
until June 2009, since that time Beaver Valley has made progress in addressing
OE program needs. This has included clearly defining the roles and responsibilities
of Section OE Coordinators.
Procedures
have been revised and a familiarization
guide has been completed
with guidance on how to use SAP efficiently.
Training has been completed
for Section OE Coordinators
and the backlog of unreviewed
OE items has decreased (currently
at 2 unreviewed
items as compared to over 12 items previously).
Finally, a higher level of accountability
has been placed on each department
to report backlogged
OE items at weekly plant meetings.
With respect to incorporating
OE in system health reports, the inspectors
identified
that OE continued
not to be incorporated
in the 2008 and 2009 reports. FENOC entered this issue into the CAP (CR 09-63999).
c. Findings No findings of significance
were identified . . 3 Assessment
of Self-Assessments
and Audits a. Inspection
Scope The inspectors
reviewed a sample of snapshot self-assessments, focused assessments, fleet-level
assessments, and a variety of self-assessments
focused on various plant programs.
These reviews were performed
to determine
if problems identified
through these assessments
were entered into the CAP, and whether corrective
actions were initiated
to address identified
deficiencies.
The effectiveness
of the assessments
was evaluated
by comparing
audit and assessment
results against self-revealing
and NRC-identified
observations
made during the inspection.
A list of documents
reviewed is included in the Attachment
to this report. b. Assessment
The inspectors
concluded
that QA audits and self-assessments
were critical, thorough, and effective
in identifying
issues. The inspectors
observed that these audits and self-Enclosure 
.4 12 assessments
were completed
by personnel
knowledgeable
in the subject areas and were completed
to a sufficient
depth to identify issues that were then entered into the CAP for evaluation.
Corrective
actions associated
with the issues were implemented
commensurate
with their safety significance.
FENOC managers evaluated
the results and initiated
appropriate
actions to focus on areas identified
for improvement.
c. Findings No findings of significance
were identified . Assessment
of Safety Conscious
Work Environment
a. Inspection
Scope The inspectors
performed
interviews
with station personnel
to assess the safety conscious
work environment (SCWE) at Beaver Valley. Specifically, the inspectors
interviewed
personnel
to determine
whether they were hesitant to raise safety concerns to their management
and/or the NRC. The inspectors
also interviewed
the station Employee Concerns Program (ECP) coordinator
to determine
what actions were implemented
to ensure employees
were aware of the program and its availability
with regard to raising concerns.
The inspectors
reviewed the ECP files to ensure that issues were entered into the CAP when appropriate.
The inspectors
reviewed site SCWE surveys from 2007 and 2008 to assess any adverse trends in department
and site safety culture. A list of documents
reviewed is included in the Attachment
to this report. b. Assessment
During interviews, plant staff expressed
a willingness
to use the CAP to identify plant issues and deficiencies, and stated that they were willing to raise safety issues. All persons interviewed
demonstrated
an adequate knowledge
of the CAP and ECP. Based on these limited interviews, the inspectors
concluded
that there was no evidence of SCWE concerns and no significant
challenges
to the free flow of information.
SCWE surveys in 2007 and 2008 showed that the overall SCWE health at Beaver Valley remained positive.
The surveys indicated
the staff understands
and accepts expectations
and responsibilities
for identifying
concerns.
The surveys indicated
FENOC personnel
feel free to approach management
with issues and management
expectations
on safety and quality are clearly communicated.
The surveys indicated
lower than average scores for Radiation
Protection, Chemistry, Security, and Site Projects departments.
CRs were generated
to help promote improvement
in the safety culture of these departments, and corrective
actions were implemented.
The inspectors
noted that when compared to the 2007 survey, the Operations
department
had an increase in negative responses
in the 2008 survey. This trend had not been entered into the CAP for evaluation
since the negative score averages did not exceed a ten percent cutoff "trigger" for CR generation.
The inspectors
questioned
this cutoff in that it appeared to potentially
limit FENOC's ability to fully explore year-to-year
trends in departments
that may not exceed ten percent negative responses, but decline significantly
from the previous survey_ FENOC entered this issue into the CAP (CR 09-63998).
Enclosure 
As a result of the survey review, the inspectors
completed
additional
SCWE interviews
with operators
to determine
if there was a reluctance
to raise safety issues. No individuals
expressed
any fear to raise issues. Findings No findings of significance
were identified.
40A6 Meetings, Including
Exit On September
3, 2009, the inspectors
presented
the inspection
results to Mr. Roy Brosi, Director of Site Performance
Improvement, and other members of the Beaver Valley staff. The inspectors
verified that no proprietary
information
was documented
in the report. ATTACHMENT:
SUPPLEMENTAL
INFORMATION
Enclosure 
A-1 SUPPLEMENTAL
KEY POINTS OF Licensee personnel
Harold Szklinski, Staff Nuclear Specialist
Fulton Schaffner, Staff Nuclear Specialist
Daniel Butor, Staff Nuclear Specialist
Robert Lubert, Supervisor, Nuclear Electrical
System Engineering
Francy Mantine, Staff Nuclear Engineer David Jones, Staff Nuclear Engineer Philip Slifkin, Staff Nuclear Engineer Giuseppe Cerasi, Senior Nuclear Specialist
Brian Goff, Supervisor, Nuclear Work Planning Michael Kienzle, Nuclear Engineering
Pat Pauvlinch, Supervisor, Nuclear Plant System Engineering
Robert Williams, Staff Nuclear Engineer Joann West, Staff Nuclear Engineer John Kaminskas, Nuclear Engineer David Hauser, Superintendent
Shift Operations, Unit 2 Christopher
Makowka, Root Cause Evaluator
Michael Mitchell, Superintendent
Nuclear Work Planning John Bowden, Superintendent
Nuclear Operations
Services Jim Mauck, Senior Nuclear Specialist
Brian Sepelak, Supervisor, Nuclear Compliance
Karl Wolfson, Supervisor, Nuclear Performance
Improvement
Colin Keller, Manager, Site Regulatory
Compliance
Rich Dibler, Security Support Supervisor
Sue Vincinie, Performance
Improvement
Senior Consultant
Darrel Batina, Employee Concerns Program Representative
Dutch Chancey, Manager, Employee Concerns (Fleet) Wayne Mcintire, Beaver Valley Site Safety Specialist
Gary Shildt, Supervisor, Nuclear Projects Engineering
Jack Patterson, Staff Nuclear Engineer Thomas King, Plant Engineer Robert Lubert, Plant
Engineering
Supervisor
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened and Closed 05000334, 412/2009008-01
Containment
Isolation
Valve System 10 CFR 50.65 (a)(2) Performance
Demonstration
Not Met. Attachment 
LIST OF DOCUMENTS
Condition
ReQorts 08-38146 09-60763 09-55789 08-50881 08-47439 08-46291 08-45288 08-42054 08-36772 07-26862 08-32856 07-14885
07-14208 09-62156 09-62106 09-61128 09-60432
09-59875 09-56773 09-54230
09-52736 08-39941 08-48160 09-57390
09-52275 08-49681 08-33109 07-28371 07-15761 09-61333 08-42790 09-62268
09-59641 09-58307 09-57580 09-57463
09-55267 09-52029 08-48296 09-57822 09-61026 09-60359 09-56525 09-61753 09-57743 08-51000 07-23937 09-59057 09-53803 08-41802
08-32965 03-01371 09-61679 09-62681 09-57726 08-39835 07-18191 07-21962 08-48581 08-50283 09-52719 09-61026 09-63451 09-61453 08-48268 08-44941 08-44947 08-37921 08-44960 07-24074 07-30275 09-63317
08-48482 09-52857 09-63269 09-57857 09-56402
08-34526 08-33776 09-55350 09-52043 07-28809 07-12360
07-14181 07-14185 07-14530
07-14761 07-14934 09-61430 09-61631 09-61878 09-62202 09-62810 07-15636 07-17006 07-17236 07-20147 07-20158
07-22189 07-24552 07-25283 07-28203
07-22004 07-29608 07-30073 09-57198
09-57688 09-57815 09-58598 09-60492 09-60672 09-59088 09-60547 09-61017
07-31483 07-28809 07-12120 08-35376 08-49694 08-43202
08-43205 09-62787 08-48664
08-49518 09-53081 09-53243 09-53762 09-54051 09-55146 09-55719 09-56851 09-56874 09-57268 09-57784 09-58142
07-26688 09-54051 08-48664 07-25046 07-30273 08-38146 07-13076
08-48581 09-60218 04-09895 07-30390 07-32095 08-40472 08-48688 09-60450
06-11217 07-30430 08-32447
08-40490 08-49073 09-60763 07-13021 07-30431 08-32887 08-40519
08-49368 09-61744 07-15001 07-30447 08-33126 08-40575
08-49750 09-62348 07-15444 07-30484 08-33306 08-40579 08-49983 09-62705
07-18894 07-30575 08-33398 08-40587 08-50137 08-37743
07-20907 07-30677 08-33725 08-40753
08-50151 08-37925 07-22891 07-30823 08-35048 08-40867 08-51024 08-38276 07-23543 07-30847 08-35517 08-40932 08-51136 08-38687
07-23933 07-30911 08-35674 08-40970 08-51385 08-38750
07-26020 07-30912 08-36383 08-41330 09-52096
08-39233 Attachment 
07-26065 07-30988 08-36471 08-41450 09-52351
07-26326 07-30999 08-36539
08-41691 09-53214 07-27423 07-31040 08-37026 08-41723 09-53275
07-27469 07-31083 08-37250
08-41801 09-53803 07-28007 07-31107 08-37304 08-42046 09-53938 07-28012 07-31110 08-37318 08-42627
09-54227
07-28471 07-31112 08-37320 08-42847 09-54737
07-28724 07-31221 08-37330 08-43510 09-54836 07-29217 07-31350 08-37373 08-44047
09-55439 07-30075 07-30383 08-37405 08-45833 09-56328
07-30318 08-37676 08-37450 08-46143 09-57224 07-30362 08-46883 08-37646 08-46662
09-57244 07-28652 08-38049 08-41776 08-47368 08-47539 09-53197 09-53372 09-53569 09-55916 09-57165 07-16667 07-17938 07-19218 07-20942
07-23163 07-24034 07-25474 07-27222 07-28474 08-34940
08-36384 08-37168 08-37252 08-40090 08-40292
08-48144 08-48160 08-49360 08-49836 09-51664
09-54942 09-55267 09-56250 09-56291 09-56315 09-57617 09-58071 09-58215 09-58481 09-58495
09-59654 09-60890 *09-63801
*09-63391
*09-63416 *09-63532 *09-63546
*09-63536
*09-63454
*09-63479
*09-63916
*09-63975
*09-63998
*09-63999
*09-64004
*CR written as a result of NRC inspection
Audits and Self-assessments
BV-SA-08-086, "BVPS Inservice
Testing (1ST) Program Snapshot Self-Assessment
Plan." BV-SA-08-007, "CAP Effectiveness." Fleet Self-assessment
of Use of Operating
Experience
at Beaver Valley, Perry and Davis Berry, May 2008. BV-SA-08-009, "Focused Self-Assessment
of Beaver Valley Work Management
Performance
Indicators" BV-SA-08-080
Operating
Experience
OE 28133 OE 24688 OE 24689 IN 2008-06 SEN 274, "Multiple
Reactor Coolant Pump Seal Failures During Cooldown" Attachment 
Procedures
NOP-LP-2001, Corrective
Action Program, Rev. 22 NOBP-LP-2011, FENOC Cause Analysis, Rev. 9 1/2-EPP-IP-7.1, Emergency
Equipment
Inventory
and Maintenance
Procedure, Rev. 22 1/2-EPP-IP-7.1, Emergency
Equipment
Inventory
and Maintenance
Procedure, Rev. 23 1/2-EPP-IP-7.1.F09, Emergency
Inventory
Checklist
-Primary Assembly Areas, Rev. 4 1/2-EPP-IP-7.1.F09, Emergency
Inventory
Checklist
-Primary Assembly Areas, Rev. 5 EPP-PLAN-SECTION-6, Emergency
Measures, Rev. 25 EPP-PLAN-SECTION-7, Emergency
Facilities
and Equipment, Rev. 25 NOP-LP-5004, Equipment
Important
to Emergency
Response, Rev. 0 BVRM-EP-5003, Equipment
Important
to Emergency
Response, Rev. 1 1/2-EPP-IP-7.2, Administration
of Emergency
Preparedness
Plan Drills and Exercises, Rev. 13 1/2-EPP-IP-3.2, Site Assembly and Personnel
Accountability, Rev. 18 10ST-15.1, [1CC-P-1A]
Quarterly
Test, Rev. 19 10ST-15.1, [1CC-P-1A]
Quarterly
Test, Rev. 20 10ST-15.1, [1CC-P-1A]
Quarterly
Test, Rev. 23 20ST-11.1, Low Head Safety Injection
Pump [2SIS*P21A]
Test, Rev. 25 20M-11.2.B, Setpoints, Rev. 4 2CMP-11SIS-P-21A-B-1M, Low Head Safety Injection
Pump Overhaul, Issue 4, Rev. 9 10ST-24.4, Steam Turbine Driven Auxiliary
Feed Pump Test [1 FW-P-2], Rev. 42 10ST-24.9, Turbine-Driven
AFW Pump [1 FW-P-2] Operability
Test, Rev. 40 20ST-24.4, Steam Driven Auxiliary
Feed Pump [2FWE*P22]
Quarterly
Test, Rev. 64 20ST-24.4A , Steam Driven Auxiliary
Feed Pump [2FWE*P22]
Full Flow Test, Rev. 20 NOBP-LP-1107, Security Operating
Experience
Guidelines, Rev. 0 20M-53A.1.A-0.11 , Beaver Valley Power Station Unit 2 Verification
of Automatic
Actions, Rev. 6 20M-53A.1.A-0.11 , Beaver Valley Power Station Unit 2 Containment
Isolation
Phase A Checklist, Issue 1 C Rev. 0 NOP-MS-4001, Warehousing, Rev. 6 NOBP-OM-2031, Outage Management
Scheduling
Process, Rev. 3 NOBP-OP-0004, Component
Mispositioning, Rev. 2 NOP-OP-1001, Clearance/Tagging
Program, Rev. 11 BVBP-OPS-0004, Operations
Clearance
Coordinator, Rev. 7 1/2-ADM-2017.F01, Beaver Valley Power Station Vendor Technical
Information
Review Form-Low Head Safety Injection
Pump Instruction
Manual, Rev. 5 NOBP-CC-7003, Structured
Spare Parts List, Rev. 5 BVPM-ER-3004, Maintenance
Rule (MR) Program Supplemental
Guidance, Rev. 0 BVBP-OPS-0008, Supplemental
Instructions
For the Control of Operating
Manual Procedures.
BVPS-OPS-0022, Operating
Procedure
Development
and Revision, Rev. 0 NOP-ER-3004, FENOC Maintenance
Rule Program, Rev. 1 SAP Orders/Notifications
600556345


600544389
P. Harden                                      2
200287486
Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001, with
600519950
copies to the Regional Administrator, Region I; the Director, Office of Enforcement, U.S.
200221237
Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Senior Resident
Attachment 
Inspector at the Beaver Valley Power Station. In addition, if you disagree with the
200309431
characterization of any finding in this report, you should provide a response within 30 days of
200287583
the date of this inspection report, with the basis for your disagreement, to the Regional
200276981
Administrator, Region I, and the NRC Senior Resident Inspector at the Beaver Valley Power
200042681
Station. The information you provide will be considered in accordance with Inspection Manual
Chapter 0305.
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its
enclosure, and your response (if any) will be available electronically for public inspection in the
NRC Public Document Room or from the Publicly Available Records (PARS) component of the
NRC's document system (ADAMS). ADAMS is accessible from the NRC Web Site at
~=:'::'~~~~=-'-=:::'!J..!.~~=~~",-= (the Public Electronic Reading Room).
                                                Sincerely,
                                                IRA!
                                                Raymond J. Powell, Chief
                                                Technical Support & Assessment Branch
                                                Division of Reactor Projects
Docket Nos.: 50-334, 50-412
License Nos: DPR-66, NPF-73
Enclosures:    Inspection Report 05000334/2009008; 05000412/2009008
                w/Attachment: Supplemental Information
cc w/encls: Distribution via ListServ


200172902
P. Harden                                                          3
200371419
copies to the Regional Administrator, Region I; the Director, Office of Enforcement, U.S.
200310030
Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Senior Resident
Inspector at the Beaver Valley Power Station. In addition, if you disagree with the
characterization of any finding in this report, you should provide a response within 30 days of
the date of this inspection report, with the basis for your disagreement, to the Regional
Administrator, Region I, and the NRC Senior Resident Inspector at the Beaver Valley Power
Station. The information you provide will be considered in accordance with Inspection Manual
Chapter 0305.
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its
enclosure, and your response (if any) will be available electronically for public inspection in the
NRC Public Document Room or from the Publicly Available Records (PARS) component of the
NRC's document system (ADAMS). ADAMS is accessible from the NRC Web Site at
http://www.nrc.gov/reading-rm/adams.html(the Public Electronic Reading Room).
                                                                    Sincerely,
                                                                    IRAJ
                                                                    Raymond J. Powell, Chief
                                                                    Technical Support & Assessment Branch
                                                                    Division of Reactor Projects
Docket Nos.: 50-334, 50-412
License Nos: DPR-66, NPF-73
Enclosures:          Inspection Report 05000334/2009008; 05000412/2009008
                      w/Attachment: Supplemental Information
Distribution w/encl: (via e-mail)
S. Collins, RA (R10RAMAILRESOURCE)
M. Dapas, DRA (R10RAMAILRESOURCE)                                                D. Spindler, DRP, RI
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OFFICE:      RI/DRP                        RI/DRP
NAME:        TSetzer/tcs                  RBeliamy/rjp for
DATE:        10/13109                      10/14/09


200254994
                                      1
600375319
                U.S. NUCLEAR REGULATORY COMMISSION
600422084
                                  REGION I
Docket Nos.  50-334, 50-412
License Nos. DPR-66, NPF-73
Report Nos.  05000334/2009008 and 05000412/2009008
Licensee:    FirstEnergy Nuclear Operating Company (FENOC)
Facility:    Beaver Valley Power Station, Units 1 and 2
Location:    Post Office Box 4
            Shippingport, PA 15077
Dates:      August 17 through September 3, 2009
Team Leader: Thomas Setzer, PE, Senior Project Engineer
            Division of Reactor Projects (DRP)
Inspectors:  Jeffery Bream, Project Engineer, DRP
            Elizabeth Keighley, Reactor Inspector, DRP
            David Spindler, Beaver Valley Resident Inspector, DRP
Approved by: Raymond J. Powell, Chief
            Technical Support & Assessment Branch
            Division of Reactor Projects
                                                                  Enclosure


600423831
                                                  2
200283954
                                      SUMMARY OF FINDINGS
Non-Cited
IR 05000334/2009008, IR 05000412/2009008; 08/17/2009 - 09/03/2009; Beaver Valley Power
Violations
Station, Units 1 & 2; Biennial Baseline Inspection of the Identification and Resolution of Problems.
and Findings NCV 05000334/2008003-01, Inadequate
One finding was identified in the area of prioritization and evaluation of issues.
Maintenance
This team inspection was performed by three NRC regional inspectors and one resident
Procedure
inspector. One finding of very low safety significance (Green) was identified during this
Results in Unexpected
inspection and was classified as a non-cited violation (NCV). The significance of most findings is
Terry Turbine Speed Increase NCV 05000334/2007004-02, Inadequate
indicated by their color (Green, White, Yellow, Red) using NRC Inspection Manual Chapter (IMC)
Procedure
0609, "Significance Determination Process" (SOP). The cross-cutting aspect was determined
and Monitoring
using IMC 0305, "Operating Reactor Assessment Program." Findings for which the SOP does
Program for Turbine Driven Auxiliary
not apply may be Green or be assigned a severity level after NRC management review. The
Feedwater
NRC's program for overseeing the safe operation of commercial nuclear power reactors is
Pump Turbine 1 FW-T-2 NCV 05000334/2008002-01, Incorrect
described in NUREG-1649, "Reactor Oversight Process," Revision 4, December 2006.
Jumper Placement
Identification and Resolution of Problems
during Testing Renders Quench Spray Chemical Addition Inoperable
The inspectors concluded that FENOC was, in general, effective in identifying, evaluating, and
NCV 05000334/2007005-05, Inadequate
resolving problems. Beaver Valley personnel identified problems at a low threshold and entered
Inspection
them into the Corrective Action Program (CAP). The inspectors determined that Beaver Valley
led to a subsequent
personnel screened issues appropriately for operability and reportability, and prioritized issues
failure of a Fuel Transfer Up-Ender Cable FIN 05000412/2008003-02, Deficient
commensurate with the safety significance of the problems. Root and apparent cause analyses
Control of Clearance
appropriately considered extent of condition, generic issues, and previous occurrences. The
Posting Interrupts
inspectors determined that corrective actions addressed the identified causes and were typically
Reactor Coolant Charging Path while Vessel Water Level Drained Below the Flange Surveillance
implemented in a timely manner. However, the inspectors noted one NCV of very low safety
Tests 20ST-11.1, Low Head Safety Injection
significance in the area of prioritization and evaluation of issues. This issue was entered into
Pump [2SIS-P21A]
FENOC's CAP during the inspection.
Test, Rev. 24, 07/28/08 20ST-11.1, Low Head Safety Injection
FENOC's audits and self-assessments reviewed by the inspectors were thorough and probing.
Pump [2SIS-P21A]
Additionally, the inspectors concluded that FENOC adequately identified, reviewed, and applied
Test, Rev. 24, 10/20/08 20ST-11.1, Low Head Safety Injection
relevant industry operating experience (OE) to the Beaver Valley Power Station. Based on
Pump [2SIS-P21A]
interviews, observations of plant activities, and reviews of the CAP and the Employees Concerns
Test, Rev. 24, 06/30/09 10ST-24.9, Turbine-Driven
Program (ECP), the inspectors did not identify any concerns with site personnel willingness to
AFW Pump [1 FW-P-2] Operability
raise safety issues, nor did the inspectors identify conditions that could have had a negative
Test, Rev. 36,10/23/07
impact on the site's safety conscious work environment (SCWE).
10ST-24.9, Turbine-Driven
        Cornerstone: Mitigating Systems
AFW Pump [1 FW-P-2] Operability
        Green. The inspectors identified an NCV of very low safety significance (Green) of
Test, Rev. 40,05/11/09
        10 CFR 50.65(a)(2), "Requirements for Monitoring the Effectiveness of Maintenance at
Vendor Manual 2502.290-001-001, Low Head Safety Injection
        Nuclear Power Plants," due to FENOC personnel's failure to demonstrate that the
Pump Instruction
        10 CFR 50.65(a)(2) performance of the containment isolation valve limit switches was
Manual, Rev. S 2502.290-001-001, Low Head Safety Injection
        effectively controlled through the performance of appropriate preventive maintenance.
Pump Instruction
        Specifically, as evidenced by repeat dual position indications of containment isolation
Manual, Rev. T Other WO 200287486
        valves in the control room between 2007 and 2009 resulting in 21 unplanned entries into
Feedback Form #2008-1448
        Technical Specification 3.6.3, the containment isolation valve system 10 CFR 50.65(a)(2)
PM Change Request BV-REV.-08-4731
        performance demonstration was no longer justified in accordance with Maintenance Rule
SAP Report -Bill of Materials
                                                                                          Enclosure
for Low Head Safety Injection
 
Pump 2SIS-P21A
                                            3
SAP Report -Bill of Materials
implementing procedure guidance. This should have resulted in placement of the
for Low Head Safety Injection
containment isolation valve system in 10 CFR 50.65(a)(1) for goal setting and monitoring.
Pump 2SIS-P21B
FENOC entered this issue into the CAP (CR 09-64040).
2SIS-P21A
The inspectors determined the finding was more than minor because it is associated with
Vibration
the Equipment Performance attribute of the Mitigating Systems cornerstone and adversely
Trend Data 03/24/1998
affected the cornerstone objective of ensuring the reliability of systems that respond to
-06/30/2009
initiating events to prevent undesirable consequences. The finding was determined to be
Beaver Valley System Health Report 2008-1 Beaver Valley System Health Report 2008-2 Beaver Valley System Health Report 2008-3 Beaver Valley System Health Report 2008-4 Attachment 
of very low safety significance (Green) because the finding did not involve a design or
Beaver Valley System Health Report 2009-1 Weekly Operating
qualification deficiency resulting in loss of operability or functionality, did not result in a
Experience
loss of system safety function, and did not screen as potentially risk significant due to
Summary -August 3, 2009 Maintenance
external initiating events. The inspectors determined that this finding had a cross-cutting
Rule System Basis Document Unit 2 System 47, Rev. 5 Maintenance
aspect in the "Corrective Action Program" component of the Problem Identification and
Rule System Basis Document Unit 2 System 47, Rev. 6 Licensing
Resolution cross-cutting area because FENOC did not take appropriate corrective actions
Requirements
to address safety issues and adverse trends associated with faulty containment isolation
Manual, Rev. 52 Protective
valve limit switches in a timely manner, commensurate with their safety significance and
Tagout 2BVP-CYC-013-1
complexity [P.1(d)]. (Section 40A2.1c)
2R13-07-EDS-00B
                                                                                        Enclosure
Unit 2 Shift Narrative
 
Logs May 5, 2008 to May 7, 2008 Beaver Valley Unit 2 System Health Report 2009-2, "System 43 -Unit 2 Radiation
                                                4
Monitoring
                                          REPORT DETAILS
System" Beaver Valley Unit 1 System Health Report 2009-2, "System 43 -Unit 1 Radiation
4.  OTHER ACTIVITIES (OA)
Monitoring
40A2 Problem Identification and Resolution (PI&R) (71152B)
System" ADAMS BV CAP CFR CR DRP ECP FENOC IMC IR 1ST MRB NCV NRC OA OE PARS
.1  Assessment of the Corrective Action Program Effectiveness
PI&R ROP SCWE SOP TDAFWP WO LIST OF ACRONYMS Agencywide
  a. Inspection Scope
Documents
    The inspectors reviewed FENOC's procedures that describe the CAP at the Beaver Valley
Access and Management
    Power Station. FENOC personnel identified problems by initiating condition reports (CRs)
System Beaver Valley Corrective
    for conditions adverse to quality, plant equipment deficiencies, industrial or radiological
Action Program Code of Federal Regulations
    safety concerns, and other significant issues. Condition reports were subsequently
Condition
    screened for operability and reportability, and categorized by significance, which included
Report Division of Reactor Projects Employee Concerns Program  
    levels SR (significant condition adverse to quality, root cause), AR (adverse condition, root
FirstEnergy
    cause), AA (adverse condition, full apparent cause), AL (adverse condition, limited
Nuclear Operating
    apparent cause), AF (adverse condition, fix), and AC (adverse condition, close). CRs
Company Inspection
    were assigned to personnel for evaluation and resolution or trending.
Manual Chapter Inspection
    The inspectors evaluated the process for assigning and tracking issues to ensure that
Report Inservice
    issues were screened for operability and reportability, prioritized for evaluation and
Test Management
    resolution in a timely manner commensurate with their safety significance, and tracked to
Review Board Non-Cited
    identify adverse trends and repetitive issues. In addition, the inspectors interviewed plant
Violation
    staff and management to determine their understanding of, and involvement with, the
Nuclear Regulatory
    CAP.
Commission
    The inspectors reviewed CRs selected across the seven cornerstones of safety in the
Other Activities
    NRC's Reactor Oversight Process (ROP) to determine if site personnel properly identified,
Operating
    characterized, and entered problems into the CAP for evaluation and resolution. The
Experience
    inspectors selected items from functional areas that included physical security,
Publicly Available
    emergency preparedness, engineering, maintenance, operations, and radiation safety to
Records System Problem Identification
    ensure that FENOC appropriately addressed problems identified in these functional areas.
and Resolution
    The inspectors selected a risk-informed sample of CRs that had been issued since the
Reactor Oversight
    last NRC Problem Identification and Resolution (PI&R) inspection conducted in April 2007.
Process Safety Conscious
    Insights from the station's risk analyses were considered to focus the sample selection
Work Environment
    and plant walkdowns on risk-significant systems and components. The corrective action
Significance
    review was expanded to five years for evaluation of identified concerns within CRs relative
Determination
    to radiation monitors.
Process Turbine Driven Auxiliary
    The inspectors selected items from various processes at Beaver Valley to verify that they
Feedwater
    were appropriately considered for entry into the CAP. Specifically, the inspectors
Pump Work Order Attachment
    reviewed a sample of Maintenance Rule functional failure evaluations, operability
    determinations, system health reports, work orders (WOs), and issues entered into the
    Employee Concerns Program (ECP). The inspectors inspected plant areas including the
    turbine buildings, safeguards buildings, intake structure, emergency diesel generator
    buildings, yard areas, security areas, and control room.
                                                                                        Enclosure
 
                                              5
  The inspectors reviewed CRs to assess whether FENOC personnel adequately evaluated
  and prioritized issues. The CRs reviewed encompassed the full range of evaluations,
  including root cause analyses, full apparent cause evaluations, limited apparent cause
  analyses, and common cause analyses. A sample of CRs that were assigned lower
  levels of significance which did not include formal cause evaluations (AF and AC
  significance levels) were also reviewed by the inspectors to ensure they were
  appropriately classified. The inspectors' review included the appropriateness of the
  assigned significance, the scope and depth of the analysis, and the timeliness of
  resolution. The inspectors assessed whether the evaluations identified likely causes for
  the issues and identified appropriate corrective actions to address the identified causes.
  As part of this review, the inspectors interviewed various station personnel to fully
  understand details within the evaluations and the proposed and completed corrective
  actions. The inspectors observed management review board (MRB) meetings in which
  FENOC personnel reviewed new CRs for prioritization and assignment. Further, the
  inspectors reviewed equipment operability determinations and extent-of-condition reviews
  for selected CRs to verify these specific reviews adequately addressed equipment
  operability and the extent of problems.
  The inspectors' review of CRs also focused on the associated corrective actions in order
  to determine whether the actions addressed the identified causes of the problems. The
  inspectors reviewed CRs for adverse trends and repetitive problems to determine whether
  corrective actions were effective in addressing the broader issues. The inspectors
  reviewed FENOC's timeliness in implementing. corrective actions and effectiveness in
  precluding recurrence for significant conditions adverse to quality. Lastly, the inspectors
  reviewed CRs associated with NRC non-cited violations (NCV) and findings since the last
  PI&R inspection to determine whether FENOC personnel properly evaluated and resolved
  the issues. Specific documents reviewed during the inspection are listed in the
  Attachment to this report.
b. Assessment
  Effectiveness of Problem Identification
  Based on the selected samples reviewed, plant walkdowns, and interviews of site
  personnel, the inspectors determined that, in general, FENOC personnel identified
  problems and entered them into the CAP at a low threshold. For the issues reviewed, the
  inspectors noted that problems or concerns had been appropriately documented in
  enough detail to understand the issues. Approximately 19,000 CRs had been written by
  FENOC personnel since January 2007. The inspectors noted that the Security
  department had generated significantly less CRs when compared to the rest of the site.
  Interviews with Security personnel revealed that they had received adequate training,
  displayed a willingness to raise issues, and had ample access to computers; however,
  there was a reliance on the shift Captain to enter issues into the CAP.
  The inspectors observed managers and supervisors at MRB meetings appropriately
  questioning and challenging CRs to ensure clarity of the issues. The inspectors
  determined that FENOC personnel trended equipment and programmatic issues, and CR
  descriptions appropriately included reference to repeat occurrences of issues. The
                                                                                      Enclosure
 
                                            6
inspectors concluded that personnel were identifying trends at low levels.
The inspectors toured plant areas including the turbine buildings, safeguards buildings,
intake structure, emergency diesel generator buildings, yard areas, security areas and
control room to determine if FENOC personnel identified plant issues at the proper
threshold. Housekeeping in all areas, with the exception of the Unit 2 intake structure,
was noted to be improved since the 2007 NRC PI&R inspection. During the plant
walkdown, the inspectors identified three examples of adverse conditions that had not
been identified by FENOC. The following issues were entered into the CAP for evaluation
and resolution:
    *  During an inspection of the east end of the main intake structure, the inspectors
        identified an oxygen bottle strapped to an Appendix R ladder (a ladder used by
        plant personnel for implementing the site fire protection program). Restraining the
        oxygen bottle and Appendix R ladder together in this fashion represented a minor
        procedure violation of Beaver Valley procedure, 1/2-PIP-G01, "Securing
        Transient/Temporary/Stored Equipment in Safety-Related Areas." This issue is
        minor because there was no adverse impact to plant safety equipment, and there
        was only minimal impact on operator fire response times. FENOC entered this
        into the CAP (CR 09-63536).
    *  During an inspection of the 'D' intake structure cubicle, the inspectors identified
        rigging scaffolding with a chainfall that had been left draped over a safety related
        component. Scaffold contacting plant equipment represented a minor procedure
        violation of Beaver Valley procedure, 1/2-ADM-0810, "Scaffold Erection and
        Tagging." The component was not damaged nor had any reduced capability as a
        result of the contact with the chainfall. This issue is minor because there was no
        loss of operability or adverse impact to the safety related component. FENOC
        entered this into the CAP (CR 09-63532).
    *  During an inspection of the Unit 2 Safeguards Building, the inspectors identified
        four plastic buckets filled with lubricating oil totaling 20 gallons. The unattended oil
        in a safety related fire area represented a minor procedure violation of Beaver
        Valley procedure, 1/2-ADM-1906, "Control of Transient Combustible and
        Flammable Materials." This issue is minor because the increase in combustible
        loading in the room as a result of the unattended oil did not violate the plant fire
        hazard analysis. FENOC entered this into the CAP (CR 09-63441).
In accordance with NRC Inspection Manual Chapter 0612, "Power Reactor Inspection
Reports," the above issues constitute violations of minor significance that are not subject
to enforcement action in accordance with the NRC's Enforcement Policy.
Effectiveness of Prioritization and Evaluation of Issues
The inspectors determined that, in general, FENOC personnel appropriately prioritized
and evaluated issues commensurate with their safety significance. CRs were screened
for operability and reportability, categorized by significance, and assigned to a department
for evaluation and resolution. The CR screening process considered human performance
issues, radiological safety concerns, repetitiveness and adverse trends. The inspectors
observed managers and supervisors at MRB meetings appropriately questioning and
challenging CRs to ensure appropriate prioritization.
                                                                                      Enclosure
 
                                            7
CRs were categorized for evaluation and resolution commensurate with the significance of
the issues. Based on the sample of CRs reviewed, the guidance provided by the FENOC
implementing procedures appeared sufficient to ensure consistency in categorization of
the issues. Operability and reportability determinations were performed when conditions
warranted and the evaluations supported the conclusions. Causal analyses appropriately
considered extent of condition, generic issues, and previous occurrences. During this
inspection, the inspectors noted that, in general, FENOC's root cause analyses were
thorough, and corrective and preventive actions addressed the identified causes.
Additionally, the identified causes were well supported. An NCV was identified for
FENOC's failure to demonstrate that the 10 CFR 50.65(a)(2) performance of the
containment isolation valve limit switches was effectively controlled through the
performance of appropriate preventive maintenance. This NCV is discussed in the
findings section of this assessment area. The inspectors identified the following two
examples of issues that were not fully evaluated or prioritized for corrective action:
    *  A root cause evaluation (CR 08-39835) associated with a 2.5 inch drain down of
        the Unit 2 reactor coolant system during refueling outage 2R13 did not identify all
        corrective actions necessary to address all failed barriers. The inspectors noted
        that the root cause evaluation had not included corrective actions to address the
        communication failure within operations shifts, and the work management
        scheduling issues which contributed to a component tagoutlctearance being
        inappropriately implemented. The issue is minor because while corrective actions
        were not assigned to address all failed barriers, FENOC had discussed
        communication expectations with each operating crew and there have not been
        any repeat issues. FENOC entered these issues into the CAP (CR 09-63454 and
        09-63479).
    *  The inspectors identified three CRs describing component mispositioning events
        (CR 09-59541, CR 09-58355, and CR 09-57224) that were prioritized as CR level
        OlAF." The failure to prioritize these CRs as a limited apparent cause (CR level
        "AL") represented a minor procedure violation of Beaver Valley procedure, NOBP
        OP-0004, "Component Mispositioning." The inspectors reviewed NRC Inspection
        Manual Chapter 0612, Appendix E, "Minor Examples," and determined this issue
        was minor because there was no loss of operability or safety impact. FENOC
        entered this issue into the CAP (CR 09-64004 and CR 09-63975).
    In accordance with NRC Inspection Manual Chapter 0612, "Power Reactor Inspection
    Reports," these issues constitute violations of minor significance that are not subject
    to enforcement action in accordance with the NRC's Enforcement Policy.
Effectiveness of Corrective Actions
The inspectors concluded that corrective actions for identified deficiencies were generally
timely and adequately implemented. For significant conditions adverse to quality,
corrective actions were identified to prevent recurrence. The inspectors concluded that
corrective actions to address NCVs and findings since the last PI&R inspection were
timely and effective. The inspectors identified the following example where corrective
actions were not fully effective in addressing an issue:
                                                                                    Enclosure
 
                                              8
      *  The inspectors reviewed corrective actions taken in response to an NCV
          documented in NRC report 05000334/05000412 2007004. CR 07-24074 was
          written to ensure bearing temperatures would be monitored when performing
          surveillance testing on the turbine driven auxiliary feedpumps (TDAFWP). The
          inspectors found that the comprehensive surveillance tests for Unit 1 and Unit 2
          (Beaver Valley procedures 10ST-24.9 and 20ST-24.4A, respectively) did not have
          a precaution stating that this surveillance was not suitable to be used for post
          maintenance testing as there is no guidance prescribed to monitor and achieve
          steady bearing temperatures. The inspectors determined that the issue was minor
          because the preventive maintenance work order had contained the appropriate
          guidance. FENOC entered this issue into the CAP (CR 09-64015).
c. Findings
  Introduction: The inspectors identified an NCV of very low safety significance (Green) of
  10 CFR 50.65(a)(2), "Requirements for Monitoring the Effectiveness of Maintenance at
  Nuclear Power Plants," due to FENOC personnel's failure to demonstrate that the
  10 CFR 50.65(a)(2) performance of the containment isolation valve limit switches was
  effectively controlled through the performance of appropriate preventive maintenance.
  Specifically, as evidenced by repeat dual position indications of containment isolation
  valves in the control room resulting in 21 unplanned entries into Technical Specification
  3.6.3, the containment isolation valve system 10 CFR 50.65(a)(2) performance
  demonstration was no longer justified in accordance with Maintenance Rule implementing
  procedure guidance.
  Description: The containment isolation valve system is a risk-significant system that is
  scoped within the Maintenance Rule because it is a system, structure, or component
  (SSC) required to mitigate accidents/transients and is identified in emergency operating
  procedures. The primary Maintenance Rule function of the containment isolation valve
  system is to provide a containment isolation function during an event to prevent offsite
  radiological release. Additionally, limit switches associated with each containment
  isolation valve are scoped within the Maintenance Rule because they provide a function to
  indicate valve position in the control room for operators to use during emergency
  operating procedures.
  In February 2009, during stroke-time testing, an air-operated containment isolation valve
  displayed dual indication in the control room, causing the stroke times of the valve to be
  indeterminate and causing an unplanned entry into Technical Specification 3.6.3.
  Additionally, between January 2007 and July 2009, Technical Specification 3.6.3 had 21
  unplanned entries as a result of faulty limit switches on similar containment isolation
  valves. This resulted in the FENOC established containment isolation valve system
  Maintenance Rule condition monitoring criteria being exceeded, which required FENOC to
  perform a Maintenance Rule 10 CFR 50.65(a)(1) evaluation. The Maintenance Rule
  (a)(1) evaluation was completed in February 2009 and concluded that the containment
  isolation valve system should continue to be monitored in accordance with Maintenance
  Rule 10 CFR 50.65(a)(2)., This reinforced a similar decision made in 2007 based on a
  Maintenance Rule (a)(1) evaluation recommendation to keep the system in (a)(2) despite
                                                                                      Enclosure
 
                                            9
the condition monitoring criteria being exceeded due to multiple dual indications in the
control room. The basis of the decision was that the dual indication issue was a result of
faulty limit switches, and that this did not affect the valve's safety related function to close
during an event to prevent offsite radiological release. Site personnel determined the
direct cause was the limit switch being out of adjustment due to a problem with the
required torque. Despite the repeat failures, FENOC failed to implement or revise
preventive maintenance practices for these limit switches. Subsequently, the
Maintenance Rule Steering Committee approved a revision to clarify the monitoring
criteria for the containment isolation valve system, which would exclude future indication
problems that did not affect the valve's ability to isolate containment. However, it failed to
take into account the limit switches' Maintenance Rule function in emergency operating
procedures, specifically, the ability to accurately indicate valve position in the control room
during an event. Following the change to the condition monitoring criteria, the site had
seven valves display dual indication in the control room between February 2009 and June
2009 that FENOC concluded did not affect valve operability.
The inspectors concluded that the numerous dual indications of the limit switches should
have been evaluated against FENOC's Maintenance Rule condition monitoring criteria
and should have resulted in placement of the containment isolation valve system in
10 CFR 50.65(a)(1) for goal setting and monitoring. FENOC performed an extent of
condition review on two other valves of the same model, and determined that the torque
on the limit switch fasteners needed to be adjusted. FENOC corrected the torque issue
and has implemented plans to install a button tab on the limit switches to minimize
misalignment causing dual indications.
Analysis: The inspectors determined that the failure to demonstrate that the
10 CFR 50.65{a)(2) performance of the containment isolation valve limit switches was
effectively controlled through the performance of appropriate preventive maintenance was
a performance deficiency within FENOC personnel's ability to foresee and correct and
should have been prevented. Traditional Enforcement did not apply, as the issue did not
have actual or potential safety consequence, had no willful aspects, nor did it impact the
NRC's ability to perform its regulatory function.
A review of NRC Inspection Manual Chapter (IMC) 0612, Appendix E, "Minor Examples,"
revealed that no minor examples were applicable to this finding. The inspectors
determined the finding was more than minor because it is associated with the Equipment
Performance attribute of the Mitigating Systems cornerstone and adversely affected the
cornerstone objective of ensuring the reliability of systems that respond to initiating events
to prevent undesirable consequences. Specifically, the dual indication of containment
isolation valves in the control room due to faulty limit switches presents a challenge to the
operators during event response while implementing emergency operating procedures,
and has resulted in 21 unplanned Technical Specification entries. The numerous dual
indication instances should have caused the containment isolation valve system to be
placed in 10 CFR 50.65(a)(1) for goal setting and monitoring. The inspectors determined
the significance of the finding using IMC 0609.04, "Phase 1 Initial Screening and
Characterization of Findings." The finding was determined to be of very low safety
significance (Green) because the finding did not involve a design or qualification
deficiency resulting in loss of operability or functionality, did not result in a loss of system
                                                                                        Enclosure
 
                                                10
    safety function, and did not screen as potentially risk significant due to external initiating
    events.
    The inspectors determined that this finding had a cross-cutting aspect in the "Corrective
    Action Program" component of the Problem Identification and Resolution cross-cutting
    area because FENOC did not take appropriate corrective actions to address safety issues
    and adverse trends associated with faulty containment isolation valve limit switches in a
    timely manner, commensurate with their safety significance and complexity [P.1 (d)).
    Enforcement: 10 CFR 50.65(a)(1) requires, in part, that holders of an operating license
    shall monitor the performance or condition of SSCs within the scope of the monitoring
    program as defined in 10 CFR 50.65(b) against licensee-established goals, in a manner
    sufficient to provide reasonable assurance that such SSCs are capable of fulfilling their
    intended functions. 10 CFR 50.65(a)(2) states, in part, that monitoring as specified in
    10 CFR 50.65(a)(1) is not required where it has been demonstrated that the performance
    or condition of an SSC is being effectively controlled through the performance of
    appropriate preventative maintenance, such that the SSC remains capable of performing
    its intended function.
    Contrary to the above, between 2007 and 2009, FENOC personnel failed to demonstrate
    that the 10 CFR 50.65(a)(2) performance of the containment isolation valve limit switches
    was effectively controlled through the performance of appropriate preventive
    maintenance. FENOC has performed an extent of condition review and has initiated
    corrective actions to install a button tab on the limit switches to minimize misalignment
    causing the dual indications. Because this violation was of very low safety significance
    and has been entered into the CAP (CR 09-64040), this violation is being treated as an
    NCV, consistent with the NRC Enforcement Policy (NCV 05000314,412/2009008-01:
    Containment Isolation Valve System 10 CFR 50.65 (a)(2) Performance
    Demonstration Not Met) .
.2  Assessment of the Use of Operating Experience
  a. Inspection Scope
    The inspectors selected a sample of CRs associated with the review of industry Operating
    Experience (OE) to determine whether FENOC personnel appropriately evaluated the OE
    information for applicability to Beaver Valley and had taken appropriate actions, when
    warranted. The inspectors reviewed CR evaluations of OE documents associated with a
    sample of NRC Generic Letters and Information Notices to ensure that FENOC
    adequately considered the underlying problems associated with the issues for resolution
    via their CAP. The inspectors also observed plant activities to determine if industry OE
    was considered during the performance of routine activities. Specific documents
    reviewed during the inspection are listed in the Attachment to this report.
  b. Assessment
    The inspectors determined that, in general, FENOC appropriately considered industry OE
    information for applicability, and used the information for corrective and preventive actions
                                                                                          Enclosure
 
                                                11
    to identify and prevent similar issues when appropriate. The inspectors determined that
    OE was appropriately applied and lessons learned were communicated and incorporated
    into plant operations. The inspectors observed that industry OE was routinely discussed
    and considered during the performance of plant activities.
    The inspectors reviewed a fleet-level focused self-assessment of OE performed in May
    2008. The self-assessment identified a number of weaknesses, specifically:
          *  OE was not discussed in system health reports;
          *  Roles and responsibilities of Section OE Coordinators were not clearly defined;
        *    Familiarization with SAP, the database used to manage OE, was low at the
              Management and Section OE Coordinator levels; and
          *  Procedures describing the requirements to process OE were in need of revision to
              add clarity.
    Although the inspectors noted that corrective actions were not completed until June 2009,
    since that time Beaver Valley has made progress in addressing OE program needs. This
    has included clearly defining the roles and responsibilities of Section OE Coordinators.
    Procedures have been revised and a familiarization guide has been completed with
    guidance on how to use SAP efficiently. Training has been completed for Section OE
    Coordinators and the backlog of unreviewed OE items has decreased (currently at 2
    unreviewed items as compared to over 12 items previously). Finally, a higher level of
    accountability has been placed on each department to report backlogged OE items at
    weekly plant meetings. With respect to incorporating OE in system health reports, the
    inspectors identified that OE continued not to be incorporated in the 2008 and 2009
    reports. FENOC entered this issue into the CAP (CR 09-63999).
c.  Findings
    No findings of significance were identified .
.3  Assessment of Self-Assessments and Audits
  a. Inspection Scope
    The inspectors reviewed a sample of snapshot self-assessments, focused self
    assessments, fleet-level assessments, and a variety of self-assessments focused on
    various plant programs. These reviews were performed to determine if problems
    identified through these assessments were entered into the CAP, and whether corrective
    actions were initiated to address identified deficiencies. The effectiveness of the
    assessments was evaluated by comparing audit and assessment results against
    self-revealing and NRC-identified observations made during the inspection. A list of
    documents reviewed is included in the Attachment to this report.
  b. Assessment
    The inspectors concluded that QA audits and self-assessments were critical, thorough,
    and effective in identifying issues. The inspectors observed that these audits and self-
                                                                                        Enclosure
 
                                              12
    assessments were completed by personnel knowledgeable in the subject areas and were
    completed to a sufficient depth to identify issues that were then entered into the CAP for
    evaluation. Corrective actions associated with the issues were implemented
    commensurate with their safety significance. FENOC managers evaluated the results and
    initiated appropriate actions to focus on areas identified for improvement.
  c. Findings
    No findings of significance were identified .
.4  Assessment of Safety Conscious Work Environment
a.  Inspection Scope
    The inspectors performed interviews with station personnel to assess the safety conscious
    work environment (SCWE) at Beaver Valley. Specifically, the inspectors interviewed
    personnel to determine whether they were hesitant to raise safety concerns to their
    management and/or the NRC. The inspectors also interviewed the station Employee
    Concerns Program (ECP) coordinator to determine what actions were implemented to
    ensure employees were aware of the program and its availability with regard to raising
    concerns. The inspectors reviewed the ECP files to ensure that issues were entered into
    the CAP when appropriate. The inspectors reviewed site SCWE surveys from 2007 and
    2008 to assess any adverse trends in department and site safety culture. A list of
    documents reviewed is included in the Attachment to this report.
  b. Assessment
    During interviews, plant staff expressed a willingness to use the CAP to identify plant
    issues and deficiencies, and stated that they were willing to raise safety issues. All
    persons interviewed demonstrated an adequate knowledge of the CAP and ECP. Based
    on these limited interviews, the inspectors concluded that there was no evidence of
    SCWE concerns and no significant challenges to the free flow of information.
    SCWE surveys in 2007 and 2008 showed that the overall SCWE health at Beaver Valley
    remained positive. The surveys indicated the staff understands and accepts expectations
    and responsibilities for identifying concerns. The surveys indicated FENOC personnel
    feel free to approach management with issues and management expectations on safety
    and quality are clearly communicated. The surveys indicated lower than average scores
    for Radiation Protection, Chemistry, Security, and Site Projects departments. CRs were
    generated to help promote improvement in the safety culture of these departments, and
    corrective actions were implemented. The inspectors noted that when compared to the
    2007 survey, the Operations department had an increase in negative responses in the
    2008 survey. This trend had not been entered into the CAP for evaluation since the
    negative score averages did not exceed a ten percent cutoff "trigger" for CR generation.
    The inspectors questioned this cutoff in that it appeared to potentially limit FENOC's ability
    to fully explore year-to-year trends in departments that may not exceed ten percent
    negative responses, but decline significantly from the previous survey_ FENOC entered
    this issue into the CAP (CR 09-63998).
                                                                                        Enclosure
 
                                              13
    As a result of the survey review, the inspectors completed additional SCWE interviews
    with operators to determine if there was a reluctance to raise safety issues. No individuals
    expressed any fear to raise issues.
c.  Findings
    No findings of significance were identified.
40A6 Meetings, Including Exit
    On September 3, 2009, the inspectors presented the inspection results to Mr. Roy Brosi,
    Director of Site Performance Improvement, and other members of the Beaver Valley staff.
    The inspectors verified that no proprietary information was documented in the report.
ATTACHMENT: SUPPLEMENTAL INFORMATION
                                                                                      Enclosure
 
                                              A-1
                                SUPPLEMENTAL INFORMATION
                                    KEY POINTS OF CONTACT
Licensee personnel
Harold Szklinski, Staff Nuclear Specialist
Fulton Schaffner, Staff Nuclear Specialist
Daniel Butor, Staff Nuclear Specialist
Robert Lubert, Supervisor, Nuclear Electrical System Engineering
Francy Mantine, Staff Nuclear Engineer
David Jones, Staff Nuclear Engineer
Philip Slifkin, Staff Nuclear Engineer
Giuseppe Cerasi, Senior Nuclear Specialist
Brian Goff, Supervisor, Nuclear Work Planning
Michael Kienzle, Nuclear Engineering
Pat Pauvlinch, Supervisor, Nuclear Plant System Engineering
Robert Williams, Staff Nuclear Engineer
Joann West, Staff Nuclear Engineer
John Kaminskas, Nuclear Engineer
David Hauser, Superintendent Shift Operations, Unit 2
Christopher Makowka, Root Cause Evaluator
Michael Mitchell, Superintendent Nuclear Work Planning
John Bowden, Superintendent Nuclear Operations Services
Jim Mauck, Senior Nuclear Specialist
Brian Sepelak, Supervisor, Nuclear Compliance
Karl Wolfson, Supervisor, Nuclear Performance Improvement
Colin Keller, Manager, Site Regulatory Compliance
Rich Dibler, Security Support Supervisor
Sue Vincinie, Performance Improvement Senior Consultant
Darrel Batina, Employee Concerns Program Representative
Dutch Chancey, Manager, Employee Concerns (Fleet)
Wayne Mcintire, Beaver Valley Site Safety Specialist
Gary Shildt, Supervisor, Nuclear Projects Engineering
Jack Patterson, Staff Nuclear Engineer
Thomas King, Plant Engineer
Robert Lubert, Plant Engineering Supervisor
                      LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened and Closed
05000334, 412/2009008-01                    Containment Isolation Valve System 10 CFR 50.65
                                            (a)(2) Performance Demonstration Not Met.
                                                                                  Attachment
 
                                    A-2
                        LIST OF DOCUMENTS REVIEWED
Condition ReQorts
08-38146      09-60763  09-55789    08-50881  08-47439 08-46291
08-45288      08-42054  08-36772    07-26862  08-32856 07-14885
07-14208      09-62156  09-62106    09-61128  09-60432 09-59875
09-56773      09-54230  09-52736    08-39941  08-48160 09-57390
09-52275      08-49681  08-33109    07-28371  07-15761 09-61333
08-42790      09-62268  09-59641    09-58307  09-57580 09-57463
09-55267      09-52029  08-48296    09-57822  09-61026 09-60359
09-56525      09-61753  09-57743    08-51000  07-23937 09-59057
09-53803      08-41802  08-32965    03-01371  09-61679 09-62681
09-57726      08-39835  07-18191    07-21962  08-48581 08-50283
09-52719      09-61026  09-63451    09-61453  08-48268 08-44941
08-44947      08-37921  08-44960    07-24074  07-30275 09-63317
08-48482      09-52857  09-63269    09-57857  09-56402 08-34526
08-33776      09-55350  09-52043    07-28809  07-12360 07-14181
07-14185      07-14530  07-14761    07-14934  09-61430 09-61631
09-61878      09-62202  09-62810    07-15636  07-17006 07-17236
07-20147      07-20158  07-22189    07-24552  07-25283 07-28203
07-22004      07-29608  07-30073    09-57198  09-57688 09-57815
09-58598      09-60492  09-60672    09-59088  09-60547 09-61017
07-31483      07-28809  07-12120    08-35376  08-49694 08-43202
08-43205      09-62787  08-48664    08-49518  09-53081 09-53243
09-53762      09-54051  09-55146    09-55719  09-56851 09-56874
09-57268      09-57784  09-58142    07-26688  09-54051 08-48664
07-25046      07-30273  08-38146    07-13076  08-48581 09-60218
04-09895      07-30390  07-32095    08-40472  08-48688 09-60450
06-11217      07-30430  08-32447    08-40490  08-49073 09-60763
07-13021      07-30431  08-32887    08-40519  08-49368 09-61744
07-15001      07-30447  08-33126    08-40575  08-49750 09-62348
07-15444      07-30484  08-33306    08-40579  08-49983 09-62705
07-18894      07-30575  08-33398    08-40587  08-50137 08-37743
07-20907      07-30677  08-33725    08-40753  08-50151 08-37925
07-22891      07-30823  08-35048    08-40867  08-51024 08-38276
07-23543      07-30847  08-35517    08-40932  08-51136 08-38687
07-23933      07-30911  08-35674    08-40970  08-51385 08-38750
07-26020      07-30912  08-36383    08-41330  09-52096 08-39233
                                                                Attachment
 
                                            A-3
07-26065        07-30988        08-36471    08-41450      09-52351        08-39304
07-26326        07-30999        08-36539    08-41691      09-53214        08-39946
07-27423        07-31040        08-37026    08-41723      09-53275        08-46995
07-27469        07-31083        08-37250    08-41801      09-53803        08-47282
07-28007        07-31107        08-37304    08-42046      09-53938        08-47455
07-28012        07-31110        08-37318    08-42627      09-54227        08-47767
07-28471        07-31112        08-37320    08-42847      09-54737        09-58483
07-28724        07-31221        08-37330    08-43510      09-54836        09-58878
07-29217        07-31350        08-37373    08-44047      09-55439        09-58985
07-30075        07-30383        08-37405    08-45833      09-56328        09-59541
07-30318        08-37676        08-37450    08-46143      09-57224        09-58355
07-30362        08-46883        08-37646    08-46662      09-57244        07-22603
07-28652        08-38049        08-41776    08-47368      08-47539        08-48966
09-53197        09-53372        09-53569    09-55916      09-57165        07-12368
07-16667        07-17938        07-19218    07-20942      07-23163        07-23960
07-24034        07-25474        07-27222    07-28474      08-34940        08-35010
08-36384        08-37168        08-37252    08-40090      08-40292        08-47830
08-48144        08-48160        08-49360    08-49836      09-51664        09-54128
09-54942        09-55267        09-56250    09-56291      09-56315        09-57553
09-57617        09-58071        09-58215    09-58481      09-58495        09-59460
09-59654        09-60890        *09-63801    *09-63391      *09-63416        *09-63982
*09-63532        *09-63546      *09-63536    *09-63454      *09-63479        *09-63441
*09-63916        *09-63975      *09-63998    *09-63999      *09-64004        *09-64015
*09-64040
*CR written as a  result of NRC inspection
Audits and Self-assessments
BV-SA-08-086, "BVPS Inservice Testing (1ST) Program Snapshot Self-Assessment Plan."
BV-SA-08-007, "CAP Effectiveness."
Fleet Self-assessment of Use of Operating Experience at Beaver Valley, Perry and Davis Berry,
      May 2008.
BV-SA-08-009, "Focused Self-Assessment of Beaver Valley Work Management Performance
      Indicators"
BV-SA-08-080
Operating Experience
OE 28133
OE 24688
OE 24689
IN 2008-06
SEN 274, "Multiple Reactor Coolant Pump Seal Failures During Cooldown"
                                                                                    Attachment
 
                                            A-4
Procedures
NOP-LP-2001, Corrective Action Program, Rev. 22
NOBP-LP-2011, FENOC Cause Analysis, Rev. 9
1/2-EPP-IP-7.1, Emergency Equipment Inventory and Maintenance Procedure, Rev. 22
1/2-EPP-IP-7.1, Emergency Equipment Inventory and Maintenance Procedure, Rev. 23
1/2-EPP-IP-7.1.F09, Emergency Inventory Checklist - Primary Assembly Areas, Rev. 4
1/2-EPP-IP-7.1.F09, Emergency Inventory Checklist - Primary Assembly Areas, Rev. 5
EPP-PLAN-SECTION-6, Emergency Measures, Rev. 25
EPP-PLAN-SECTION-7, Emergency Facilities and Equipment, Rev. 25
NOP-LP-5004, Equipment Important to Emergency Response, Rev. 0
BVRM-EP-5003, Equipment Important to Emergency Response, Rev. 1
1/2-EPP-IP-7.2, Administration of Emergency Preparedness Plan Drills and Exercises, Rev. 13
1/2-EPP-IP-3.2, Site Assembly and Personnel Accountability, Rev. 18
10ST-15.1, [1CC-P-1A] Quarterly Test, Rev. 19
10ST-15.1, [1CC-P-1A] Quarterly Test, Rev. 20
10ST-15.1, [1CC-P-1A] Quarterly Test, Rev. 23
20ST-11.1, Low Head Safety Injection Pump [2SIS*P21A] Test, Rev. 25
20M-11.2.B, Setpoints, Rev. 4
2CMP-11SIS-P-21A-B-1M, Low Head Safety Injection Pump Overhaul, Issue 4, Rev. 9
10ST-24.4, Steam Turbine Driven Auxiliary Feed Pump Test [1 FW-P-2], Rev. 42
10ST-24.9, Turbine-Driven AFW Pump [1 FW-P-2] Operability Test, Rev. 40
20ST-24.4, Steam Driven Auxiliary Feed Pump [2FWE*P22] Quarterly Test, Rev. 64
20ST-24.4A, Steam Driven Auxiliary Feed Pump [2FWE*P22] Full Flow Test, Rev. 20
NOBP-LP-1107, Security Operating Experience Guidelines, Rev. 0
20M-53A.1.A-0.11, Beaver Valley Power Station Unit 2 Verification of Automatic
      Actions, Rev. 6
20M-53A.1.A-0.11, Beaver Valley Power Station Unit 2 Containment Isolation Phase A
      Checklist, Issue 1C Rev. 0
NOP-MS-4001, Warehousing, Rev. 6
NOBP-OM-2031, Outage Management Scheduling Process, Rev. 3
NOBP-OP-0004, Component Mispositioning, Rev. 2
NOP-OP-1001, Clearance/Tagging Program, Rev. 11
BVBP-OPS-0004, Operations Clearance Coordinator, Rev. 7
1/2-ADM-2017.F01, Beaver Valley Power Station Vendor Technical Information Review Form-
      Low Head Safety Injection Pump Instruction Manual, Rev. 5
NOBP-CC-7003, Structured Spare Parts List, Rev. 5
BVPM-ER-3004, Maintenance Rule (MR) Program Supplemental Guidance, Rev. 0
BVBP-OPS-0008, Supplemental Instructions For the Control of Operating Manual Procedures.
BVPS-OPS-0022, Operating Procedure Development and Revision, Rev. 0
NOP-ER-3004, FENOC Maintenance Rule Program, Rev. 1
SAP Orders/Notifications
600556345
600544389
200287486
600519950
200221237
                                                                                  Attachment
 
                                              A-5
200309431
200287583
200276981
200042681
200172902
200371419
200310030
200254994
600375319
600422084
600423831
200283954
Non-Cited Violations and Findings
NCV 05000334/2008003-01, Inadequate Maintenance Procedure Results in Unexpected Terry
        Turbine Speed Increase
NCV 05000334/2007004-02, Inadequate Procedure and Monitoring Program for Turbine Driven
        Auxiliary Feedwater Pump Turbine 1FW-T-2
NCV 05000334/2008002-01, Incorrect Jumper Placement during Testing Renders
        Quench Spray Chemical Addition Inoperable
NCV 05000334/2007005-05, Inadequate Inspection led to a subsequent failure of a Fuel Transfer
        Up-Ender Cable
FIN 05000412/2008003-02, Deficient Control of Clearance Posting Interrupts Reactor Coolant
        Charging Path while Vessel Water Level Drained Below the Flange
Surveillance Tests
20ST-11.1, Low Head Safety Injection Pump [2SIS-P21A] Test, Rev. 24,    07/28/08
20ST-11.1, Low Head Safety Injection Pump [2SIS-P21A] Test, Rev. 24,    10/20/08
20ST-11.1, Low Head Safety Injection Pump [2SIS-P21A] Test, Rev. 24,    06/30/09
10ST-24.9, Turbine-Driven AFW Pump [1 FW-P-2] Operability Test, Rev.    36,10/23/07
10ST-24.9, Turbine-Driven AFW Pump [1 FW-P-2] Operability Test, Rev.    40,05/11/09
Vendor Manual
2502.290-001-001, Low Head Safety Injection Pump Instruction Manual, Rev. S
2502.290-001-001, Low Head Safety Injection Pump Instruction Manual, Rev. T
Other
WO 200287486
Feedback Form #2008-1448
PM Change Request BV-REV.-08-4731
SAP Report - Bill of Materials for Low Head Safety Injection Pump 2SIS-P21A
SAP Report - Bill of Materials for Low Head Safety Injection Pump 2SIS-P21B
2SIS-P21A Vibration Trend Data 03/24/1998 - 06/30/2009
Beaver Valley System Health Report 2008-1
Beaver Valley System Health Report 2008-2
Beaver Valley System Health Report 2008-3
Beaver Valley System Health Report 2008-4
                                                                                    Attachment
 
                                              A-6
Beaver Valley System Health Report 2009-1
Weekly Operating Experience Summary - August 3, 2009
Maintenance Rule System Basis Document Unit 2 System 47, Rev. 5
Maintenance Rule System Basis Document Unit 2 System 47, Rev. 6
Licensing Requirements Manual, Rev. 52
Protective Tagout 2BVP-CYC-013-1 2R13-07-EDS-00B
Unit 2 Shift Narrative Logs May 5, 2008 to May 7, 2008
Beaver Valley Unit 2 System Health Report 2009-2, "System 43 - Unit 2 Radiation Monitoring
        System"
Beaver Valley Unit 1 System Health Report 2009-2, "System 43 - Unit 1 Radiation Monitoring
        System"
                                      LIST OF ACRONYMS
ADAMS          Agencywide Documents Access and Management System
BV            Beaver Valley
CAP            Corrective Action Program
CFR            Code of Federal Regulations
CR            Condition Report
DRP            Division of Reactor Projects
ECP            Employee Concerns Program
FENOC          FirstEnergy Nuclear Operating Company
IMC            Inspection Manual Chapter
IR            Inspection Report
1ST            Inservice Test
MRB            Management Review Board
NCV            Non-Cited Violation
NRC            Nuclear Regulatory Commission
OA            Other Activities
OE            Operating Experience
PARS          Publicly Available Records System
PI&R          Problem Identification and Resolution
ROP            Reactor Oversight Process
SCWE          Safety Conscious Work Environment
SOP            Significance Determination Process
TDAFWP        Turbine Driven Auxiliary Feedwater Pump
WO            Work Order
                                                                                  Attachment
}}
}}

Latest revision as of 02:25, 14 November 2019

IR 05000334-09-008, IR 05000412-09-008; 08/17/2009 - 09/03/2009; Beaver Valley Power Station, Units 1 & 2; Biennial Baseline Inspection of the Identification and Resolution of Problems
ML092920008
Person / Time
Site: Beaver Valley
Issue date: 10/15/2009
From: Racquel Powell
NRC/RGN-I/DRP/PB7
To: Harden P
FirstEnergy Nuclear Operating Co
powell r j
References
IR-09-008
Download: ML092920008 (22)


See also: IR 05000334/2009008

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION I

475 ALLENDALE ROAD

KING OF PRUSSIA, PA 19406-1415

October 15, 2009

Mr. Paul Harden

Site Vice President

FirstEnergy Nuclear Operating Company

Beaver Valley Power Station

P. O. Box 4, Route 168

Shippingport, PA 15077

SUBJECT: BEAVER VALLEY POWER STATION - NRC PROBLEM IDENTIFICATION

AND RESOLUTION INSPECTION REPORT 05000334/2009008 AND

05000412/2009008

Dear Mr. Harden:

On September 3,2009, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Beaver Valley Power Station Units 1 and 2. The enclosed report documents

the inspection results, which were discussed on September 3,2009, with Mr. Roy Brosi and

other members of your staff.

This inspection was an examination of activities conducted under your license as they relate to

the identification and resolution of problems, and compliance with the Commission's rules and

regulations and the conditions of your operating license. Within these areas, the inspection

involved examination of selected procedures and representative records, observations of

activities, and interviews with personnel.

Based on the samples selected for review, the inspection team concluded that FirstEnergy

Nuclear Operating Company (FENOC) was generally effective in identifying, evaluating and

resolving problems. FENOC personnel identified problems at a low threshold and entered them

into the Corrective Action Program (CAP). FENOC personnel screened issues appropriately for

operability and reportability, and prioritized issues commensurate with the safety significance of

the problems. Root and apparent cause analyses appropriately considered extent of condition,

generic issues, and previous occurrences. Corrective actions addressed the identified causes

and were typically implemented in a timely manner. However, the inspectors noted several

examples for improvement in the identification of plant issues, and examples where evaluations

lacked rigor to fully explore the corrective actions needed to address the issue.

This report documents one NRC-identified finding of very low safety significance (Green). The

finding was determined to involve a violation of NRC requirements. However, because of its

very low safety significance and because it has been entered into your CAP, the NRC is

treating this finding as a non-cited violation (NCV), in accordance with Section VI.A.1 of the

NRC's Enforcement Policy. If you deny this NCV, you should provide a response with the basis

for your denial, within 30 days of the date of this inspection report, to the U.S. Nuclear

P. Harden 2

Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001, with

copies to the Regional Administrator, Region I; the Director, Office of Enforcement, U.S.

Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Senior Resident

Inspector at the Beaver Valley Power Station. In addition, if you disagree with the

characterization of any finding in this report, you should provide a response within 30 days of

the date of this inspection report, with the basis for your disagreement, to the Regional

Administrator, Region I, and the NRC Senior Resident Inspector at the Beaver Valley Power

Station. The information you provide will be considered in accordance with Inspection Manual

Chapter 0305.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of the

NRC's document system (ADAMS). ADAMS is accessible from the NRC Web Site at

~=:'::'~~~~=-'-=:::'!J..!.~~=~~",-= (the Public Electronic Reading Room).

Sincerely,

IRA!

Raymond J. Powell, Chief

Technical Support & Assessment Branch

Division of Reactor Projects

Docket Nos.: 50-334, 50-412

License Nos: DPR-66, NPF-73

Enclosures: Inspection Report 05000334/2009008; 05000412/2009008

w/Attachment: Supplemental Information

cc w/encls: Distribution via ListServ

P. Harden 3

copies to the Regional Administrator, Region I; the Director, Office of Enforcement, U.S.

Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Senior Resident

Inspector at the Beaver Valley Power Station. In addition, if you disagree with the

characterization of any finding in this report, you should provide a response within 30 days of

the date of this inspection report, with the basis for your disagreement, to the Regional

Administrator, Region I, and the NRC Senior Resident Inspector at the Beaver Valley Power

Station. The information you provide will be considered in accordance with Inspection Manual

Chapter 0305.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of the

NRC's document system (ADAMS). ADAMS is accessible from the NRC Web Site at

http://www.nrc.gov/reading-rm/adams.html(the Public Electronic Reading Room).

Sincerely,

IRAJ

Raymond J. Powell, Chief

Technical Support & Assessment Branch

Division of Reactor Projects

Docket Nos.: 50-334, 50-412

License Nos: DPR-66, NPF-73

Enclosures: Inspection Report 05000334/2009008; 05000412/2009008

w/Attachment: Supplemental Information

Distribution w/encl: (via e-mail)

S. Collins, RA (R10RAMAILRESOURCE)

M. Dapas, DRA (R10RAMAILRESOURCE) D. Spindler, DRP, RI

D. Lew, DRP (R1 DRPMAILRESOURCE) P. Garrett, DRP, OA

J. Clifford, DRP (R1DRPMAIL RESOURCE) L. Trocine, RI OEDO

R. Bellamy, DRP RIDSNRRPMBEAVERVAllEY RESOURCE

G. Barber, DRP ROPreportsResource@nrc.qov

C. Newport, DRP Region I Docket Room (with concurrences)

J. Greives, DRP

D. Werkheiser, DRP, SRI

SUNSI Review Complete: tcs (Reviewer's Initials) ML092920008

DOCUMENT NAME: G:\DRP\BRANCH TSAB\lnspection Reports\Beaver Valley PI&R 2009\BV PIR

IR2009008revO.doc

After declaring this document "An Official Agency Record" it will be released to the Public.

To receive acopy of this document, indicate In the box: 'C' = Copy without attachment/enclosure 'E" = Copy with attachment/enclosure "N" = No copy

OFFICE: RI/DRP RI/DRP

NAME: TSetzer/tcs RBeliamy/rjp for

DATE: 10/13109 10/14/09

1

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket Nos. 50-334, 50-412

License Nos. DPR-66, NPF-73

Report Nos. 05000334/2009008 and 05000412/2009008

Licensee: FirstEnergy Nuclear Operating Company (FENOC)

Facility: Beaver Valley Power Station, Units 1 and 2

Location: Post Office Box 4

Shippingport, PA 15077

Dates: August 17 through September 3, 2009

Team Leader: Thomas Setzer, PE, Senior Project Engineer

Division of Reactor Projects (DRP)

Inspectors: Jeffery Bream, Project Engineer, DRP

Elizabeth Keighley, Reactor Inspector, DRP

David Spindler, Beaver Valley Resident Inspector, DRP

Approved by: Raymond J. Powell, Chief

Technical Support & Assessment Branch

Division of Reactor Projects

Enclosure

2

SUMMARY OF FINDINGS

IR 05000334/2009008, IR 05000412/2009008; 08/17/2009 - 09/03/2009; Beaver Valley Power

Station, Units 1 & 2; Biennial Baseline Inspection of the Identification and Resolution of Problems.

One finding was identified in the area of prioritization and evaluation of issues.

This team inspection was performed by three NRC regional inspectors and one resident

inspector. One finding of very low safety significance (Green) was identified during this

inspection and was classified as a non-cited violation (NCV). The significance of most findings is

indicated by their color (Green, White, Yellow, Red) using NRC Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SOP). The cross-cutting aspect was determined

using IMC 0305, "Operating Reactor Assessment Program." Findings for which the SOP does

not apply may be Green or be assigned a severity level after NRC management review. The

NRC's program for overseeing the safe operation of commercial nuclear power reactors is

described in NUREG-1649, "Reactor Oversight Process," Revision 4, December 2006.

Identification and Resolution of Problems

The inspectors concluded that FENOC was, in general, effective in identifying, evaluating, and

resolving problems. Beaver Valley personnel identified problems at a low threshold and entered

them into the Corrective Action Program (CAP). The inspectors determined that Beaver Valley

personnel screened issues appropriately for operability and reportability, and prioritized issues

commensurate with the safety significance of the problems. Root and apparent cause analyses

appropriately considered extent of condition, generic issues, and previous occurrences. The

inspectors determined that corrective actions addressed the identified causes and were typically

implemented in a timely manner. However, the inspectors noted one NCV of very low safety

significance in the area of prioritization and evaluation of issues. This issue was entered into

FENOC's CAP during the inspection.

FENOC's audits and self-assessments reviewed by the inspectors were thorough and probing.

Additionally, the inspectors concluded that FENOC adequately identified, reviewed, and applied

relevant industry operating experience (OE) to the Beaver Valley Power Station. Based on

interviews, observations of plant activities, and reviews of the CAP and the Employees Concerns

Program (ECP), the inspectors did not identify any concerns with site personnel willingness to

raise safety issues, nor did the inspectors identify conditions that could have had a negative

impact on the site's safety conscious work environment (SCWE).

Cornerstone: Mitigating Systems

Green. The inspectors identified an NCV of very low safety significance (Green) of

10 CFR 50.65(a)(2), "Requirements for Monitoring the Effectiveness of Maintenance at

Nuclear Power Plants," due to FENOC personnel's failure to demonstrate that the

10 CFR 50.65(a)(2) performance of the containment isolation valve limit switches was

effectively controlled through the performance of appropriate preventive maintenance.

Specifically, as evidenced by repeat dual position indications of containment isolation

valves in the control room between 2007 and 2009 resulting in 21 unplanned entries into

Technical Specification 3.6.3, the containment isolation valve system 10 CFR 50.65(a)(2)

performance demonstration was no longer justified in accordance with Maintenance Rule

Enclosure

3

implementing procedure guidance. This should have resulted in placement of the

containment isolation valve system in 10 CFR 50.65(a)(1) for goal setting and monitoring.

FENOC entered this issue into the CAP (CR 09-64040).

The inspectors determined the finding was more than minor because it is associated with

the Equipment Performance attribute of the Mitigating Systems cornerstone and adversely

affected the cornerstone objective of ensuring the reliability of systems that respond to

initiating events to prevent undesirable consequences. The finding was determined to be

of very low safety significance (Green) because the finding did not involve a design or

qualification deficiency resulting in loss of operability or functionality, did not result in a

loss of system safety function, and did not screen as potentially risk significant due to

external initiating events. The inspectors determined that this finding had a cross-cutting

aspect in the "Corrective Action Program" component of the Problem Identification and

Resolution cross-cutting area because FENOC did not take appropriate corrective actions

to address safety issues and adverse trends associated with faulty containment isolation

valve limit switches in a timely manner, commensurate with their safety significance and

complexity P.1(d). (Section 40A2.1c)

Enclosure

4

REPORT DETAILS

4. OTHER ACTIVITIES (OA)

40A2 Problem Identification and Resolution (PI&R) (71152B)

.1 Assessment of the Corrective Action Program Effectiveness

a. Inspection Scope

The inspectors reviewed FENOC's procedures that describe the CAP at the Beaver Valley

Power Station. FENOC personnel identified problems by initiating condition reports (CRs)

for conditions adverse to quality, plant equipment deficiencies, industrial or radiological

safety concerns, and other significant issues. Condition reports were subsequently

screened for operability and reportability, and categorized by significance, which included

levels SR (significant condition adverse to quality, root cause), AR (adverse condition, root

cause), AA (adverse condition, full apparent cause), AL (adverse condition, limited

apparent cause), AF (adverse condition, fix), and AC (adverse condition, close). CRs

were assigned to personnel for evaluation and resolution or trending.

The inspectors evaluated the process for assigning and tracking issues to ensure that

issues were screened for operability and reportability, prioritized for evaluation and

resolution in a timely manner commensurate with their safety significance, and tracked to

identify adverse trends and repetitive issues. In addition, the inspectors interviewed plant

staff and management to determine their understanding of, and involvement with, the

CAP.

The inspectors reviewed CRs selected across the seven cornerstones of safety in the

NRC's Reactor Oversight Process (ROP) to determine if site personnel properly identified,

characterized, and entered problems into the CAP for evaluation and resolution. The

inspectors selected items from functional areas that included physical security,

emergency preparedness, engineering, maintenance, operations, and radiation safety to

ensure that FENOC appropriately addressed problems identified in these functional areas.

The inspectors selected a risk-informed sample of CRs that had been issued since the

last NRC Problem Identification and Resolution (PI&R) inspection conducted in April 2007.

Insights from the station's risk analyses were considered to focus the sample selection

and plant walkdowns on risk-significant systems and components. The corrective action

review was expanded to five years for evaluation of identified concerns within CRs relative

to radiation monitors.

The inspectors selected items from various processes at Beaver Valley to verify that they

were appropriately considered for entry into the CAP. Specifically, the inspectors

reviewed a sample of Maintenance Rule functional failure evaluations, operability

determinations, system health reports, work orders (WOs), and issues entered into the

Employee Concerns Program (ECP). The inspectors inspected plant areas including the

turbine buildings, safeguards buildings, intake structure, emergency diesel generator

buildings, yard areas, security areas, and control room.

Enclosure

5

The inspectors reviewed CRs to assess whether FENOC personnel adequately evaluated

and prioritized issues. The CRs reviewed encompassed the full range of evaluations,

including root cause analyses, full apparent cause evaluations, limited apparent cause

analyses, and common cause analyses. A sample of CRs that were assigned lower

levels of significance which did not include formal cause evaluations (AF and AC

significance levels) were also reviewed by the inspectors to ensure they were

appropriately classified. The inspectors' review included the appropriateness of the

assigned significance, the scope and depth of the analysis, and the timeliness of

resolution. The inspectors assessed whether the evaluations identified likely causes for

the issues and identified appropriate corrective actions to address the identified causes.

As part of this review, the inspectors interviewed various station personnel to fully

understand details within the evaluations and the proposed and completed corrective

actions. The inspectors observed management review board (MRB) meetings in which

FENOC personnel reviewed new CRs for prioritization and assignment. Further, the

inspectors reviewed equipment operability determinations and extent-of-condition reviews

for selected CRs to verify these specific reviews adequately addressed equipment

operability and the extent of problems.

The inspectors' review of CRs also focused on the associated corrective actions in order

to determine whether the actions addressed the identified causes of the problems. The

inspectors reviewed CRs for adverse trends and repetitive problems to determine whether

corrective actions were effective in addressing the broader issues. The inspectors

reviewed FENOC's timeliness in implementing. corrective actions and effectiveness in

precluding recurrence for significant conditions adverse to quality. Lastly, the inspectors

reviewed CRs associated with NRC non-cited violations (NCV) and findings since the last

PI&R inspection to determine whether FENOC personnel properly evaluated and resolved

the issues. Specific documents reviewed during the inspection are listed in the

Attachment to this report.

b. Assessment

Effectiveness of Problem Identification

Based on the selected samples reviewed, plant walkdowns, and interviews of site

personnel, the inspectors determined that, in general, FENOC personnel identified

problems and entered them into the CAP at a low threshold. For the issues reviewed, the

inspectors noted that problems or concerns had been appropriately documented in

enough detail to understand the issues. Approximately 19,000 CRs had been written by

FENOC personnel since January 2007. The inspectors noted that the Security

department had generated significantly less CRs when compared to the rest of the site.

Interviews with Security personnel revealed that they had received adequate training,

displayed a willingness to raise issues, and had ample access to computers; however,

there was a reliance on the shift Captain to enter issues into the CAP.

The inspectors observed managers and supervisors at MRB meetings appropriately

questioning and challenging CRs to ensure clarity of the issues. The inspectors

determined that FENOC personnel trended equipment and programmatic issues, and CR

descriptions appropriately included reference to repeat occurrences of issues. The

Enclosure

6

inspectors concluded that personnel were identifying trends at low levels.

The inspectors toured plant areas including the turbine buildings, safeguards buildings,

intake structure, emergency diesel generator buildings, yard areas, security areas and

control room to determine if FENOC personnel identified plant issues at the proper

threshold. Housekeeping in all areas, with the exception of the Unit 2 intake structure,

was noted to be improved since the 2007 NRC PI&R inspection. During the plant

walkdown, the inspectors identified three examples of adverse conditions that had not

been identified by FENOC. The following issues were entered into the CAP for evaluation

and resolution:

  • During an inspection of the east end of the main intake structure, the inspectors

identified an oxygen bottle strapped to an Appendix R ladder (a ladder used by

plant personnel for implementing the site fire protection program). Restraining the

oxygen bottle and Appendix R ladder together in this fashion represented a minor

procedure violation of Beaver Valley procedure, 1/2-PIP-G01, "Securing

Transient/Temporary/Stored Equipment in Safety-Related Areas." This issue is

minor because there was no adverse impact to plant safety equipment, and there

was only minimal impact on operator fire response times. FENOC entered this

into the CAP (CR 09-63536).

  • During an inspection of the 'D' intake structure cubicle, the inspectors identified

rigging scaffolding with a chainfall that had been left draped over a safety related

component. Scaffold contacting plant equipment represented a minor procedure

violation of Beaver Valley procedure, 1/2-ADM-0810, "Scaffold Erection and

Tagging." The component was not damaged nor had any reduced capability as a

result of the contact with the chainfall. This issue is minor because there was no

loss of operability or adverse impact to the safety related component. FENOC

entered this into the CAP (CR 09-63532).

  • During an inspection of the Unit 2 Safeguards Building, the inspectors identified

four plastic buckets filled with lubricating oil totaling 20 gallons. The unattended oil

in a safety related fire area represented a minor procedure violation of Beaver

Valley procedure, 1/2-ADM-1906, "Control of Transient Combustible and

Flammable Materials." This issue is minor because the increase in combustible

loading in the room as a result of the unattended oil did not violate the plant fire

hazard analysis. FENOC entered this into the CAP (CR 09-63441).

In accordance with NRC Inspection Manual Chapter 0612, "Power Reactor Inspection

Reports," the above issues constitute violations of minor significance that are not subject

to enforcement action in accordance with the NRC's Enforcement Policy.

Effectiveness of Prioritization and Evaluation of Issues

The inspectors determined that, in general, FENOC personnel appropriately prioritized

and evaluated issues commensurate with their safety significance. CRs were screened

for operability and reportability, categorized by significance, and assigned to a department

for evaluation and resolution. The CR screening process considered human performance

issues, radiological safety concerns, repetitiveness and adverse trends. The inspectors

observed managers and supervisors at MRB meetings appropriately questioning and

challenging CRs to ensure appropriate prioritization.

Enclosure

7

CRs were categorized for evaluation and resolution commensurate with the significance of

the issues. Based on the sample of CRs reviewed, the guidance provided by the FENOC

implementing procedures appeared sufficient to ensure consistency in categorization of

the issues. Operability and reportability determinations were performed when conditions

warranted and the evaluations supported the conclusions. Causal analyses appropriately

considered extent of condition, generic issues, and previous occurrences. During this

inspection, the inspectors noted that, in general, FENOC's root cause analyses were

thorough, and corrective and preventive actions addressed the identified causes.

Additionally, the identified causes were well supported. An NCV was identified for

FENOC's failure to demonstrate that the 10 CFR 50.65(a)(2) performance of the

containment isolation valve limit switches was effectively controlled through the

performance of appropriate preventive maintenance. This NCV is discussed in the

findings section of this assessment area. The inspectors identified the following two

examples of issues that were not fully evaluated or prioritized for corrective action:

  • A root cause evaluation (CR 08-39835) associated with a 2.5 inch drain down of

the Unit 2 reactor coolant system during refueling outage 2R13 did not identify all

corrective actions necessary to address all failed barriers. The inspectors noted

that the root cause evaluation had not included corrective actions to address the

communication failure within operations shifts, and the work management

scheduling issues which contributed to a component tagoutlctearance being

inappropriately implemented. The issue is minor because while corrective actions

were not assigned to address all failed barriers, FENOC had discussed

communication expectations with each operating crew and there have not been

any repeat issues. FENOC entered these issues into the CAP (CR 09-63454 and

09-63479).

  • The inspectors identified three CRs describing component mispositioning events

(CR 09-59541, CR 09-58355, and CR 09-57224) that were prioritized as CR level

OlAF." The failure to prioritize these CRs as a limited apparent cause (CR level

"AL") represented a minor procedure violation of Beaver Valley procedure, NOBP

OP-0004, "Component Mispositioning." The inspectors reviewed NRC Inspection

Manual Chapter 0612, Appendix E, "Minor Examples," and determined this issue

was minor because there was no loss of operability or safety impact. FENOC

entered this issue into the CAP (CR 09-64004 and CR 09-63975).

In accordance with NRC Inspection Manual Chapter 0612, "Power Reactor Inspection

Reports," these issues constitute violations of minor significance that are not subject

to enforcement action in accordance with the NRC's Enforcement Policy.

Effectiveness of Corrective Actions

The inspectors concluded that corrective actions for identified deficiencies were generally

timely and adequately implemented. For significant conditions adverse to quality,

corrective actions were identified to prevent recurrence. The inspectors concluded that

corrective actions to address NCVs and findings since the last PI&R inspection were

timely and effective. The inspectors identified the following example where corrective

actions were not fully effective in addressing an issue:

Enclosure

8

  • The inspectors reviewed corrective actions taken in response to an NCV

documented in NRC report 05000334/05000412 2007004. CR 07-24074 was

written to ensure bearing temperatures would be monitored when performing

surveillance testing on the turbine driven auxiliary feedpumps (TDAFWP). The

inspectors found that the comprehensive surveillance tests for Unit 1 and Unit 2

(Beaver Valley procedures 10ST-24.9 and 20ST-24.4A, respectively) did not have

a precaution stating that this surveillance was not suitable to be used for post

maintenance testing as there is no guidance prescribed to monitor and achieve

steady bearing temperatures. The inspectors determined that the issue was minor

because the preventive maintenance work order had contained the appropriate

guidance. FENOC entered this issue into the CAP (CR 09-64015).

c. Findings

Introduction: The inspectors identified an NCV of very low safety significance (Green) of

10 CFR 50.65(a)(2), "Requirements for Monitoring the Effectiveness of Maintenance at

Nuclear Power Plants," due to FENOC personnel's failure to demonstrate that the

10 CFR 50.65(a)(2) performance of the containment isolation valve limit switches was

effectively controlled through the performance of appropriate preventive maintenance.

Specifically, as evidenced by repeat dual position indications of containment isolation

valves in the control room resulting in 21 unplanned entries into Technical Specification 3.6.3, the containment isolation valve system 10 CFR 50.65(a)(2) performance

demonstration was no longer justified in accordance with Maintenance Rule implementing

procedure guidance.

Description: The containment isolation valve system is a risk-significant system that is

scoped within the Maintenance Rule because it is a system, structure, or component

(SSC) required to mitigate accidents/transients and is identified in emergency operating

procedures. The primary Maintenance Rule function of the containment isolation valve

system is to provide a containment isolation function during an event to prevent offsite

radiological release. Additionally, limit switches associated with each containment

isolation valve are scoped within the Maintenance Rule because they provide a function to

indicate valve position in the control room for operators to use during emergency

operating procedures.

In February 2009, during stroke-time testing, an air-operated containment isolation valve

displayed dual indication in the control room, causing the stroke times of the valve to be

indeterminate and causing an unplanned entry into Technical Specification 3.6.3.

Additionally, between January 2007 and July 2009, Technical Specification 3.6.3 had 21

unplanned entries as a result of faulty limit switches on similar containment isolation

valves. This resulted in the FENOC established containment isolation valve system

Maintenance Rule condition monitoring criteria being exceeded, which required FENOC to

perform a Maintenance Rule 10 CFR 50.65(a)(1) evaluation. The Maintenance Rule

(a)(1) evaluation was completed in February 2009 and concluded that the containment

isolation valve system should continue to be monitored in accordance with Maintenance

Rule 10 CFR 50.65(a)(2)., This reinforced a similar decision made in 2007 based on a

Maintenance Rule (a)(1) evaluation recommendation to keep the system in (a)(2) despite

Enclosure

9

the condition monitoring criteria being exceeded due to multiple dual indications in the

control room. The basis of the decision was that the dual indication issue was a result of

faulty limit switches, and that this did not affect the valve's safety related function to close

during an event to prevent offsite radiological release. Site personnel determined the

direct cause was the limit switch being out of adjustment due to a problem with the

required torque. Despite the repeat failures, FENOC failed to implement or revise

preventive maintenance practices for these limit switches. Subsequently, the

Maintenance Rule Steering Committee approved a revision to clarify the monitoring

criteria for the containment isolation valve system, which would exclude future indication

problems that did not affect the valve's ability to isolate containment. However, it failed to

take into account the limit switches' Maintenance Rule function in emergency operating

procedures, specifically, the ability to accurately indicate valve position in the control room

during an event. Following the change to the condition monitoring criteria, the site had

seven valves display dual indication in the control room between February 2009 and June

2009 that FENOC concluded did not affect valve operability.

The inspectors concluded that the numerous dual indications of the limit switches should

have been evaluated against FENOC's Maintenance Rule condition monitoring criteria

and should have resulted in placement of the containment isolation valve system in

10 CFR 50.65(a)(1) for goal setting and monitoring. FENOC performed an extent of

condition review on two other valves of the same model, and determined that the torque

on the limit switch fasteners needed to be adjusted. FENOC corrected the torque issue

and has implemented plans to install a button tab on the limit switches to minimize

misalignment causing dual indications.

Analysis: The inspectors determined that the failure to demonstrate that the

10 CFR 50.65{a)(2) performance of the containment isolation valve limit switches was

effectively controlled through the performance of appropriate preventive maintenance was

a performance deficiency within FENOC personnel's ability to foresee and correct and

should have been prevented. Traditional Enforcement did not apply, as the issue did not

have actual or potential safety consequence, had no willful aspects, nor did it impact the

NRC's ability to perform its regulatory function.

A review of NRC Inspection Manual Chapter (IMC) 0612, Appendix E, "Minor Examples,"

revealed that no minor examples were applicable to this finding. The inspectors

determined the finding was more than minor because it is associated with the Equipment

Performance attribute of the Mitigating Systems cornerstone and adversely affected the

cornerstone objective of ensuring the reliability of systems that respond to initiating events

to prevent undesirable consequences. Specifically, the dual indication of containment

isolation valves in the control room due to faulty limit switches presents a challenge to the

operators during event response while implementing emergency operating procedures,

and has resulted in 21 unplanned Technical Specification entries. The numerous dual

indication instances should have caused the containment isolation valve system to be

placed in 10 CFR 50.65(a)(1) for goal setting and monitoring. The inspectors determined

the significance of the finding using IMC 0609.04, "Phase 1 Initial Screening and

Characterization of Findings." The finding was determined to be of very low safety

significance (Green) because the finding did not involve a design or qualification

deficiency resulting in loss of operability or functionality, did not result in a loss of system

Enclosure

10

safety function, and did not screen as potentially risk significant due to external initiating

events.

The inspectors determined that this finding had a cross-cutting aspect in the "Corrective

Action Program" component of the Problem Identification and Resolution cross-cutting

area because FENOC did not take appropriate corrective actions to address safety issues

and adverse trends associated with faulty containment isolation valve limit switches in a

timely manner, commensurate with their safety significance and complexity [P.1 (d)).

Enforcement: 10 CFR 50.65(a)(1) requires, in part, that holders of an operating license

shall monitor the performance or condition of SSCs within the scope of the monitoring

program as defined in 10 CFR 50.65(b) against licensee-established goals, in a manner

sufficient to provide reasonable assurance that such SSCs are capable of fulfilling their

intended functions. 10 CFR 50.65(a)(2) states, in part, that monitoring as specified in

10 CFR 50.65(a)(1) is not required where it has been demonstrated that the performance

or condition of an SSC is being effectively controlled through the performance of

appropriate preventative maintenance, such that the SSC remains capable of performing

its intended function.

Contrary to the above, between 2007 and 2009, FENOC personnel failed to demonstrate

that the 10 CFR 50.65(a)(2) performance of the containment isolation valve limit switches

was effectively controlled through the performance of appropriate preventive

maintenance. FENOC has performed an extent of condition review and has initiated

corrective actions to install a button tab on the limit switches to minimize misalignment

causing the dual indications. Because this violation was of very low safety significance

and has been entered into the CAP (CR 09-64040), this violation is being treated as an

NCV, consistent with the NRC Enforcement Policy (NCV 05000314,412/2009008-01:

Containment Isolation Valve System 10 CFR 50.65 (a)(2) Performance

Demonstration Not Met) .

.2 Assessment of the Use of Operating Experience

a. Inspection Scope

The inspectors selected a sample of CRs associated with the review of industry Operating

Experience (OE) to determine whether FENOC personnel appropriately evaluated the OE

information for applicability to Beaver Valley and had taken appropriate actions, when

warranted. The inspectors reviewed CR evaluations of OE documents associated with a

sample of NRC Generic Letters and Information Notices to ensure that FENOC

adequately considered the underlying problems associated with the issues for resolution

via their CAP. The inspectors also observed plant activities to determine if industry OE

was considered during the performance of routine activities. Specific documents

reviewed during the inspection are listed in the Attachment to this report.

b. Assessment

The inspectors determined that, in general, FENOC appropriately considered industry OE

information for applicability, and used the information for corrective and preventive actions

Enclosure

11

to identify and prevent similar issues when appropriate. The inspectors determined that

OE was appropriately applied and lessons learned were communicated and incorporated

into plant operations. The inspectors observed that industry OE was routinely discussed

and considered during the performance of plant activities.

The inspectors reviewed a fleet-level focused self-assessment of OE performed in May

2008. The self-assessment identified a number of weaknesses, specifically:

  • OE was not discussed in system health reports;
  • Roles and responsibilities of Section OE Coordinators were not clearly defined;
  • Familiarization with SAP, the database used to manage OE, was low at the

Management and Section OE Coordinator levels; and

  • Procedures describing the requirements to process OE were in need of revision to

add clarity.

Although the inspectors noted that corrective actions were not completed until June 2009,

since that time Beaver Valley has made progress in addressing OE program needs. This

has included clearly defining the roles and responsibilities of Section OE Coordinators.

Procedures have been revised and a familiarization guide has been completed with

guidance on how to use SAP efficiently. Training has been completed for Section OE

Coordinators and the backlog of unreviewed OE items has decreased (currently at 2

unreviewed items as compared to over 12 items previously). Finally, a higher level of

accountability has been placed on each department to report backlogged OE items at

weekly plant meetings. With respect to incorporating OE in system health reports, the

inspectors identified that OE continued not to be incorporated in the 2008 and 2009

reports. FENOC entered this issue into the CAP (CR 09-63999).

c. Findings

No findings of significance were identified .

.3 Assessment of Self-Assessments and Audits

a. Inspection Scope

The inspectors reviewed a sample of snapshot self-assessments, focused self

assessments, fleet-level assessments, and a variety of self-assessments focused on

various plant programs. These reviews were performed to determine if problems

identified through these assessments were entered into the CAP, and whether corrective

actions were initiated to address identified deficiencies. The effectiveness of the

assessments was evaluated by comparing audit and assessment results against

self-revealing and NRC-identified observations made during the inspection. A list of

documents reviewed is included in the Attachment to this report.

b. Assessment

The inspectors concluded that QA audits and self-assessments were critical, thorough,

and effective in identifying issues. The inspectors observed that these audits and self-

Enclosure

12

assessments were completed by personnel knowledgeable in the subject areas and were

completed to a sufficient depth to identify issues that were then entered into the CAP for

evaluation. Corrective actions associated with the issues were implemented

commensurate with their safety significance. FENOC managers evaluated the results and

initiated appropriate actions to focus on areas identified for improvement.

c. Findings

No findings of significance were identified .

.4 Assessment of Safety Conscious Work Environment

a. Inspection Scope

The inspectors performed interviews with station personnel to assess the safety conscious

work environment (SCWE) at Beaver Valley. Specifically, the inspectors interviewed

personnel to determine whether they were hesitant to raise safety concerns to their

management and/or the NRC. The inspectors also interviewed the station Employee

Concerns Program (ECP) coordinator to determine what actions were implemented to

ensure employees were aware of the program and its availability with regard to raising

concerns. The inspectors reviewed the ECP files to ensure that issues were entered into

the CAP when appropriate. The inspectors reviewed site SCWE surveys from 2007 and

2008 to assess any adverse trends in department and site safety culture. A list of

documents reviewed is included in the Attachment to this report.

b. Assessment

During interviews, plant staff expressed a willingness to use the CAP to identify plant

issues and deficiencies, and stated that they were willing to raise safety issues. All

persons interviewed demonstrated an adequate knowledge of the CAP and ECP. Based

on these limited interviews, the inspectors concluded that there was no evidence of

SCWE concerns and no significant challenges to the free flow of information.

SCWE surveys in 2007 and 2008 showed that the overall SCWE health at Beaver Valley

remained positive. The surveys indicated the staff understands and accepts expectations

and responsibilities for identifying concerns. The surveys indicated FENOC personnel

feel free to approach management with issues and management expectations on safety

and quality are clearly communicated. The surveys indicated lower than average scores

for Radiation Protection, Chemistry, Security, and Site Projects departments. CRs were

generated to help promote improvement in the safety culture of these departments, and

corrective actions were implemented. The inspectors noted that when compared to the

2007 survey, the Operations department had an increase in negative responses in the

2008 survey. This trend had not been entered into the CAP for evaluation since the

negative score averages did not exceed a ten percent cutoff "trigger" for CR generation.

The inspectors questioned this cutoff in that it appeared to potentially limit FENOC's ability

to fully explore year-to-year trends in departments that may not exceed ten percent

negative responses, but decline significantly from the previous survey_ FENOC entered

this issue into the CAP (CR 09-63998).

Enclosure

13

As a result of the survey review, the inspectors completed additional SCWE interviews

with operators to determine if there was a reluctance to raise safety issues. No individuals

expressed any fear to raise issues.

c. Findings

No findings of significance were identified.

40A6 Meetings, Including Exit

On September 3, 2009, the inspectors presented the inspection results to Mr. Roy Brosi,

Director of Site Performance Improvement, and other members of the Beaver Valley staff.

The inspectors verified that no proprietary information was documented in the report.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Enclosure

A-1

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

Harold Szklinski, Staff Nuclear Specialist

Fulton Schaffner, Staff Nuclear Specialist

Daniel Butor, Staff Nuclear Specialist

Robert Lubert, Supervisor, Nuclear Electrical System Engineering

Francy Mantine, Staff Nuclear Engineer

David Jones, Staff Nuclear Engineer

Philip Slifkin, Staff Nuclear Engineer

Giuseppe Cerasi, Senior Nuclear Specialist

Brian Goff, Supervisor, Nuclear Work Planning

Michael Kienzle, Nuclear Engineering

Pat Pauvlinch, Supervisor, Nuclear Plant System Engineering

Robert Williams, Staff Nuclear Engineer

Joann West, Staff Nuclear Engineer

John Kaminskas, Nuclear Engineer

David Hauser, Superintendent Shift Operations, Unit 2

Christopher Makowka, Root Cause Evaluator

Michael Mitchell, Superintendent Nuclear Work Planning

John Bowden, Superintendent Nuclear Operations Services

Jim Mauck, Senior Nuclear Specialist

Brian Sepelak, Supervisor, Nuclear Compliance

Karl Wolfson, Supervisor, Nuclear Performance Improvement

Colin Keller, Manager, Site Regulatory Compliance

Rich Dibler, Security Support Supervisor

Sue Vincinie, Performance Improvement Senior Consultant

Darrel Batina, Employee Concerns Program Representative

Dutch Chancey, Manager, Employee Concerns (Fleet)

Wayne Mcintire, Beaver Valley Site Safety Specialist

Gary Shildt, Supervisor, Nuclear Projects Engineering

Jack Patterson, Staff Nuclear Engineer

Thomas King, Plant Engineer

Robert Lubert, Plant Engineering Supervisor

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000334, 412/2009008-01 Containment Isolation Valve System 10 CFR 50.65

(a)(2) Performance Demonstration Not Met.

Attachment

A-2

LIST OF DOCUMENTS REVIEWED

Condition ReQorts

08-38146 09-60763 09-55789 08-50881 08-47439 08-46291

08-45288 08-42054 08-36772 07-26862 08-32856 07-14885

07-14208 09-62156 09-62106 09-61128 09-60432 09-59875

09-56773 09-54230 09-52736 08-39941 08-48160 09-57390

09-52275 08-49681 08-33109 07-28371 07-15761 09-61333

08-42790 09-62268 09-59641 09-58307 09-57580 09-57463

09-55267 09-52029 08-48296 09-57822 09-61026 09-60359

09-56525 09-61753 09-57743 08-51000 07-23937 09-59057

09-53803 08-41802 08-32965 03-01371 09-61679 09-62681

09-57726 08-39835 07-18191 07-21962 08-48581 08-50283

09-52719 09-61026 09-63451 09-61453 08-48268 08-44941

08-44947 08-37921 08-44960 07-24074 07-30275 09-63317

08-48482 09-52857 09-63269 09-57857 09-56402 08-34526

08-33776 09-55350 09-52043 07-28809 07-12360 07-14181

07-14185 07-14530 07-14761 07-14934 09-61430 09-61631

09-61878 09-62202 09-62810 07-15636 07-17006 07-17236

07-20147 07-20158 07-22189 07-24552 07-25283 07-28203

07-22004 07-29608 07-30073 09-57198 09-57688 09-57815

09-58598 09-60492 09-60672 09-59088 09-60547 09-61017

07-31483 07-28809 07-12120 08-35376 08-49694 08-43202

08-43205 09-62787 08-48664 08-49518 09-53081 09-53243

09-53762 09-54051 09-55146 09-55719 09-56851 09-56874

09-57268 09-57784 09-58142 07-26688 09-54051 08-48664

07-25046 07-30273 08-38146 07-13076 08-48581 09-60218

04-09895 07-30390 07-32095 08-40472 08-48688 09-60450

06-11217 07-30430 08-32447 08-40490 08-49073 09-60763

07-13021 07-30431 08-32887 08-40519 08-49368 09-61744

07-15001 07-30447 08-33126 08-40575 08-49750 09-62348

07-15444 07-30484 08-33306 08-40579 08-49983 09-62705

07-18894 07-30575 08-33398 08-40587 08-50137 08-37743

07-20907 07-30677 08-33725 08-40753 08-50151 08-37925

07-22891 07-30823 08-35048 08-40867 08-51024 08-38276

07-23543 07-30847 08-35517 08-40932 08-51136 08-38687

07-23933 07-30911 08-35674 08-40970 08-51385 08-38750

07-26020 07-30912 08-36383 08-41330 09-52096 08-39233

Attachment

A-3

07-26065 07-30988 08-36471 08-41450 09-52351 08-39304

07-26326 07-30999 08-36539 08-41691 09-53214 08-39946

07-27423 07-31040 08-37026 08-41723 09-53275 08-46995

07-27469 07-31083 08-37250 08-41801 09-53803 08-47282

07-28007 07-31107 08-37304 08-42046 09-53938 08-47455

07-28012 07-31110 08-37318 08-42627 09-54227 08-47767

07-28471 07-31112 08-37320 08-42847 09-54737 09-58483

07-28724 07-31221 08-37330 08-43510 09-54836 09-58878

07-29217 07-31350 08-37373 08-44047 09-55439 09-58985

07-30075 07-30383 08-37405 08-45833 09-56328 09-59541

07-30318 08-37676 08-37450 08-46143 09-57224 09-58355

07-30362 08-46883 08-37646 08-46662 09-57244 07-22603

07-28652 08-38049 08-41776 08-47368 08-47539 08-48966

09-53197 09-53372 09-53569 09-55916 09-57165 07-12368

07-16667 07-17938 07-19218 07-20942 07-23163 07-23960

07-24034 07-25474 07-27222 07-28474 08-34940 08-35010

08-36384 08-37168 08-37252 08-40090 08-40292 08-47830

08-48144 08-48160 08-49360 08-49836 09-51664 09-54128

09-54942 09-55267 09-56250 09-56291 09-56315 09-57553

09-57617 09-58071 09-58215 09-58481 09-58495 09-59460

09-59654 09-60890 *09-63801 *09-63391 *09-63416 *09-63982

  • 09-63532 *09-63546 *09-63536 *09-63454 *09-63479 *09-63441
  • 09-63916 *09-63975 *09-63998 *09-63999 *09-64004 *09-64015
  • 09-64040
  • CR written as a result of NRC inspection

Audits and Self-assessments

BV-SA-08-086, "BVPS Inservice Testing (1ST) Program Snapshot Self-Assessment Plan."

BV-SA-08-007, "CAP Effectiveness."

Fleet Self-assessment of Use of Operating Experience at Beaver Valley, Perry and Davis Berry,

May 2008.

BV-SA-08-009, "Focused Self-Assessment of Beaver Valley Work Management Performance

Indicators"

BV-SA-08-080

Operating Experience

OE 28133

OE 24688

OE 24689

IN 2008-06

SEN 274, "Multiple Reactor Coolant Pump Seal Failures During Cooldown"

Attachment

A-4

Procedures

NOP-LP-2001, Corrective Action Program, Rev. 22

NOBP-LP-2011, FENOC Cause Analysis, Rev. 9

1/2-EPP-IP-7.1, Emergency Equipment Inventory and Maintenance Procedure, Rev. 22

1/2-EPP-IP-7.1, Emergency Equipment Inventory and Maintenance Procedure, Rev. 23

1/2-EPP-IP-7.1.F09, Emergency Inventory Checklist - Primary Assembly Areas, Rev. 4

1/2-EPP-IP-7.1.F09, Emergency Inventory Checklist - Primary Assembly Areas, Rev. 5

EPP-PLAN-SECTION-6, Emergency Measures, Rev. 25

EPP-PLAN-SECTION-7, Emergency Facilities and Equipment, Rev. 25

NOP-LP-5004, Equipment Important to Emergency Response, Rev. 0

BVRM-EP-5003, Equipment Important to Emergency Response, Rev. 1

1/2-EPP-IP-7.2, Administration of Emergency Preparedness Plan Drills and Exercises, Rev. 13

1/2-EPP-IP-3.2, Site Assembly and Personnel Accountability, Rev. 18

10ST-15.1, [1CC-P-1A] Quarterly Test, Rev. 19

10ST-15.1, [1CC-P-1A] Quarterly Test, Rev. 20

10ST-15.1, [1CC-P-1A] Quarterly Test, Rev. 23

20ST-11.1, Low Head Safety Injection Pump [2SIS*P21A] Test, Rev. 25

20M-11.2.B, Setpoints, Rev. 4

2CMP-11SIS-P-21A-B-1M, Low Head Safety Injection Pump Overhaul, Issue 4, Rev. 9

10ST-24.4, Steam Turbine Driven Auxiliary Feed Pump Test [1 FW-P-2], Rev. 42

10ST-24.9, Turbine-Driven AFW Pump [1 FW-P-2] Operability Test, Rev. 40

20ST-24.4, Steam Driven Auxiliary Feed Pump [2FWE*P22] Quarterly Test, Rev. 64

20ST-24.4A, Steam Driven Auxiliary Feed Pump [2FWE*P22] Full Flow Test, Rev. 20

NOBP-LP-1107, Security Operating Experience Guidelines, Rev. 0

20M-53A.1.A-0.11, Beaver Valley Power Station Unit 2 Verification of Automatic

Actions, Rev. 6

20M-53A.1.A-0.11, Beaver Valley Power Station Unit 2 Containment Isolation Phase A

Checklist, Issue 1C Rev. 0

NOP-MS-4001, Warehousing, Rev. 6

NOBP-OM-2031, Outage Management Scheduling Process, Rev. 3

NOBP-OP-0004, Component Mispositioning, Rev. 2

NOP-OP-1001, Clearance/Tagging Program, Rev. 11

BVBP-OPS-0004, Operations Clearance Coordinator, Rev. 7

1/2-ADM-2017.F01, Beaver Valley Power Station Vendor Technical Information Review Form-

Low Head Safety Injection Pump Instruction Manual, Rev. 5

NOBP-CC-7003, Structured Spare Parts List, Rev. 5

BVPM-ER-3004, Maintenance Rule (MR) Program Supplemental Guidance, Rev. 0

BVBP-OPS-0008, Supplemental Instructions For the Control of Operating Manual Procedures.

BVPS-OPS-0022, Operating Procedure Development and Revision, Rev. 0

NOP-ER-3004, FENOC Maintenance Rule Program, Rev. 1

SAP Orders/Notifications

600556345

600544389

200287486

600519950

200221237

Attachment

A-5

200309431

200287583

200276981

200042681

200172902

200371419

200310030

200254994

600375319

600422084

600423831

200283954

Non-Cited Violations and Findings

NCV 05000334/2008003-01, Inadequate Maintenance Procedure Results in Unexpected Terry

Turbine Speed Increase

NCV 05000334/2007004-02, Inadequate Procedure and Monitoring Program for Turbine Driven

Auxiliary Feedwater Pump Turbine 1FW-T-2

NCV 05000334/2008002-01, Incorrect Jumper Placement during Testing Renders

Quench Spray Chemical Addition Inoperable

NCV 05000334/2007005-05, Inadequate Inspection led to a subsequent failure of a Fuel Transfer

Up-Ender Cable

FIN 05000412/2008003-02, Deficient Control of Clearance Posting Interrupts Reactor Coolant

Charging Path while Vessel Water Level Drained Below the Flange

Surveillance Tests

20ST-11.1, Low Head Safety Injection Pump [2SIS-P21A] Test, Rev. 24, 07/28/08

20ST-11.1, Low Head Safety Injection Pump [2SIS-P21A] Test, Rev. 24, 10/20/08

20ST-11.1, Low Head Safety Injection Pump [2SIS-P21A] Test, Rev. 24, 06/30/09

10ST-24.9, Turbine-Driven AFW Pump [1 FW-P-2] Operability Test, Rev. 36,10/23/07

10ST-24.9, Turbine-Driven AFW Pump [1 FW-P-2] Operability Test, Rev. 40,05/11/09

Vendor Manual

2502.290-001-001, Low Head Safety Injection Pump Instruction Manual, Rev. S

2502.290-001-001, Low Head Safety Injection Pump Instruction Manual, Rev. T

Other

WO 200287486

Feedback Form #2008-1448

PM Change Request BV-REV.-08-4731

SAP Report - Bill of Materials for Low Head Safety Injection Pump 2SIS-P21A

SAP Report - Bill of Materials for Low Head Safety Injection Pump 2SIS-P21B

2SIS-P21A Vibration Trend Data 03/24/1998 - 06/30/2009

Beaver Valley System Health Report 2008-1

Beaver Valley System Health Report 2008-2

Beaver Valley System Health Report 2008-3

Beaver Valley System Health Report 2008-4

Attachment

A-6

Beaver Valley System Health Report 2009-1

Weekly Operating Experience Summary - August 3, 2009

Maintenance Rule System Basis Document Unit 2 System 47, Rev. 5

Maintenance Rule System Basis Document Unit 2 System 47, Rev. 6

Licensing Requirements Manual, Rev. 52

Protective Tagout 2BVP-CYC-013-1 2R13-07-EDS-00B

Unit 2 Shift Narrative Logs May 5, 2008 to May 7, 2008

Beaver Valley Unit 2 System Health Report 2009-2, "System 43 - Unit 2 Radiation Monitoring

System"

Beaver Valley Unit 1 System Health Report 2009-2, "System 43 - Unit 1 Radiation Monitoring

System"

LIST OF ACRONYMS

ADAMS Agencywide Documents Access and Management System

BV Beaver Valley

CAP Corrective Action Program

CFR Code of Federal Regulations

CR Condition Report

DRP Division of Reactor Projects

ECP Employee Concerns Program

FENOC FirstEnergy Nuclear Operating Company

IMC Inspection Manual Chapter

IR Inspection Report

1ST Inservice Test

MRB Management Review Board

NCV Non-Cited Violation

NRC Nuclear Regulatory Commission

OA Other Activities

OE Operating Experience

PARS Publicly Available Records System

PI&R Problem Identification and Resolution

ROP Reactor Oversight Process

SCWE Safety Conscious Work Environment

SOP Significance Determination Process

TDAFWP Turbine Driven Auxiliary Feedwater Pump

WO Work Order

Attachment