ML18139A529: Difference between revisions

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| issue date = 09/19/1980
| issue date = 09/19/1980
| title = LER 80-019/03L-0:on 800822,during Operation Trip Valve TV- SS-206B Would Not Stay Closed When Actuated from Control Room.Caused by Misadjusted Limit Switch.Valve Isolated & Position Limit Switch Readjusted
| title = LER 80-019/03L-0:on 800822,during Operation Trip Valve TV- SS-206B Would Not Stay Closed When Actuated from Control Room.Caused by Misadjusted Limit Switch.Valve Isolated & Position Limit Switch Readjusted
| author name = WILSON J L
| author name = Wilson J
| author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
| author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
| addressee name =  
| addressee name =  

Revision as of 07:04, 17 June 2019

LER 80-019/03L-0:on 800822,during Operation Trip Valve TV- SS-206B Would Not Stay Closed When Actuated from Control Room.Caused by Misadjusted Limit Switch.Valve Isolated & Position Limit Switch Readjusted
ML18139A529
Person / Time
Site: Surry Dominion icon.png
Issue date: 09/19/1980
From: Joshua Wilson
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML18139A527 List:
References
LER-80-019-03L-03, LER-80-19-3L-3, NUDOCS 8009240471
Download: ML18139A529 (2)


Text


\!Rt: FORM j5;,; (i-77} e LICENSEE EVENT REPORT .S. NUCL:AR R:'.:t.JL,HORY COMMISSION CONTi'iCL SLOCK: (PL:.ASE PRINT CR TYPE ALL REQUIRED ,FORMATION) Iv IA ls IP Isl 210)1 olo-1-\olo_l~l.~_J_o I-lo \o_l014 J 1J_.1_1_1J_1_l01

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!With the Unit at power, TV-SS-206B would not remain closed when actuated !Ii]] from the control room. Isolation of the sample system was available by another valve, ~* I therefore the health and safety of the general public were not affected.

This event C§:II] ~s contrary to Technical Spe,cification 3 .8. A. ( 1) and report ab le per Technical filD cation 6.6.2.b.(l)

[Iill 8 9 [I:ill 7 S SYSTEM CODE IP IB I@ 9 10 C\ U,R :;o c*VENT YE;>.R \:.!.) REP<?~' I 8 I O I NUMo::R 21 22 ACTION FUTURE TAK::N ACTION

  • Ei=FECT ON PL.O.NT CAUSE COOE CAL'SE SU6CODE CCMPCNENT CODE COMP. v;...._*,e SU6CD0E s* ,---.-..-u]@ w@ v\A IL Iv IE Ix ,e w@ fnf'@ 11 12 13 L=.J 23 SHUTDOWN METHOD SEQUENTIAL RE?CRT NO. I o 11 I 9 I 24 26 HOURS ;s OCCURRENC:

CODE \/j Io I 3 / 2i 28 29 19 F.Ei='ORT TY?: LJ,J JO 20 NPRD-4 FCRM ~us. PRIME cot-.-:=.

SU?PLIE:'.

~E\/ISION

'10. w w@L.Ll@ ~@ ~ Io 10 10 :i:i ~4 -:is 36 :i 1 {22) ATiACHMENT ll) SUBMITTi:D I I LU@) "-0 41 u ~@ CAUSE: 0::SCRl?TlON AND CORRECTIVE ACTIONS @ 42 :.J [ The initial action taken following the malfunction of the valve position indicator

[CO] I was to close the isolation valve down'stream of the trip valve. The isolation valve [LI}] remained closed until the position limit switch to TV-SS-206B was adjusted.

DE] a 9 FACILITY STATUS , % POWEF, OTHER S7ATUS L!J@ IO I 6 IO l@l,___NA

____ --,1 METHOD CF A DISCOVE? . .,. DISCOVERY oesc:= :-;-;cN 0 ~@I~ ___ O_p_e_r_a_t_o_r_s_-_o_b_s_e_r_v_a_t_i_o_n

__ _ 8 9 10 12 11 ACTIVITY CONTENT RELEASED c;: =tELEASE AMOUNT OF ACTIVITY w@ u.lL....I

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s s
a , , 45 46 44 NA _LOC..>.TION CF ;:;EL=.~.o::

@ 80 so 80 [QJ] 0:(~~~~8~:Ll@(~;~@

OESCRIPTICN

(§) a 9 11 12 ::-:3:--------------------------------------~;o NA ?ERSC/',;,EL INJURIES Q NUM6E;:> DESCRIPTICN 0 [L] I o I o I o I@ 3 9 11 ~12::------------------------------------------__Jao NA LOSS OF C? '.:AMAGE TO FACILITY G TYPE ::~CRIPTION

\:::.::) ~~@:I a s ~~:----------------------------------------------....J so NA PUS~IC:"'"Y C\ *o ISSUEDQ ")E5CRIPTICN CII2J LJ!Jc I B 9 *: s 009240 'f 7' ! I I I l i I I I I I NA == 5; ao ,, *;..:.),'.E

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__________

_ (804) 357-3184 ?WQ~I::: --------------

. . .. ATTACHMENT 1 SURRY POWER DOCK.ET NO: REPORT NO: EVENT DATE: __ -_-_-_-__ --e STATION, UNIT 2 50-:-281 80-019-03L-O 08-22-80 TITLE OF EVENT: TRIP VALVE Tv~ss-206B INOPERABLE

1. Des*cription of Event: With the Unit at power, TV-SS-206B.

would not remain' closed when actuated from the control room. This event is contrary to Technical Specification 3.8.A.l. and_reportable per Technical Specification 6.6.2.b.{1)

2. Probable Consequences of Event: Assuming total inoperability of the valve, the health and safety of the general public would not have been affected since automatic sample system isolation was available by series valve TV-,SS-206A located side of containment.
3. Cause of Event: The failure_of TV-SS-206B

.. to remain ciosed was due to a misadjusted limit switch. 4. Innnediate Corrective Action: The immediate corrective action was to -isolate TV-SS-206B, by a manual val \re down stream. 5. Scheduled Corrective Action: The-position limit switch to TV-SS-206B was readjusted.

6. Action Taken to Prevent Recurrence:

None 7. Generic Implications:

None