IR 05000277/2019010: Difference between revisions

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=Text=
=Text=
{{#Wiki_filter:August 26, 2019 Mr. Bryan Senior Vice President, Exelon Generation Company, LLC President and Chief Nuclear Officer, Exelon Nuclear
{{#Wiki_filter:ust 26, 2019


4300 Winfield Road
==SUBJECT:==
PEACH BOTTOM ATOMIC POWER STATION, UNITS 2 AND 3 - BIENNIAL PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000277/2019010 AND 05000278/2019010


Warrenville, IL 60555 SUBJECT: PEACH BOTTOM ATOMIC POWER STATION, UNITS 2 AND 3 - BIENNIAL PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT
==Dear Mr. Hanson:==
On July 12, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed a problem identification and resolution inspection at Peach Bottom Atomic Power Station, Units 2 and 3 and discussed the results of this inspection with Patrick Navin, Site Vice President and other members of your staff. The results of this inspection are documented in the enclosed report.


05000277/2019010 AND 05000278/2019010
The NRC inspection team reviewed the stations corrective action program and the stations implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for corrective action programs. Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.


==Dear Mr. Hanson:==
The team also evaluated the stations processes for use of industry and NRC operating experience information and the effectiveness of the stations audits and self-assessments.
On July 12, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed a problem identification and resolution inspection at Peach Bottom Atomic Power Station, Units 2 and 3 and discussed the results of this inspection with Patrick Navin, Site Vice President and other members of your staff. The results of this inspection are documented in the enclosed report.


The NRC inspection team reviewed the station's corrective action program and the station's implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for corrective action programs. Based on the samples reviewed, the team determined that your staff's performance in each of these areas adequately supported nuclear safety.
Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.


The team also evaluated the station's processes for use of industry and NRC operating experience information and the effectiveness of the station's audits and self-assessments. Based on the samples reviewed, the team determined that your staff's performance in each of these areas adequately supported nuclear safety.
Finally the team reviewed the stations programs to establish and maintain a safety conscious work environment, and interviewed station personnel to evaluate the effectiveness of these programs. Based on the teams observations and the results of these interviews the team found no evidence of challenges to your organizations safety conscious work environment.


Finally the team reviewed the station's programs to establish and maintain a safety conscious work environment, and interviewed station personnel to evaluate the effectiveness of these programs. Based on the team's observations and the results of these interviews the team found no evidence of challenges to your organization's safety conscious work environment. Your employees appeared willing to raise nuclear safety concerns through at least one of the several means available.
Your employees appeared willing to raise nuclear safety concerns through at least one of the several means available.


The NRC inspectors did not identify any finding or violation of more than minor significance. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, "Public Inspections, Exemptions, Requests for Withholding."
The NRC inspectors did not identify any finding or violation of more than minor significance. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.


Sincerely,
Sincerely,
/RA/ Jonathan E. Greives, Chief Reactor Projects Branch 4  
/RA/
 
Jonathan E. Greives, Chief Reactor Projects Branch 4 Division of Reactor Projects Docket Nos. 05000277 and 05000278 License Nos. DPR-44 and DPR-56
Division of Reactor Projects Docket Nos. 05000277 and 05000278 License Nos. DPR-44 and DPR-56  


===Enclosure:===
===Enclosure:===
As stated  
As stated


==Inspection Report==
==Inspection Report==
 
Docket Numbers: 05000277 and 05000278 License Numbers: DPR-44 and DPR-56 Report Numbers: 05000277/2019010 and 05000278/2019010 Enterprise Identifier: I-2019-010-0006 Licensee: Exelon Generation Company, LLC Facility: Peach Bottom Atomic Power Station, Units 2 and 3 Location: Delta, PA Inspection Dates: June 10, 2019 to July 12, 2019 Inspectors: A. Rosebrook, Senior Project Engineer (Team Lead)
Docket Numbers: 05000277 and 05000278  
E. Andrews, Health Physicist J. Cherubini, Senior Physical Security Inspector J. Dolecki, Resident Inspector J. Heinly, Senior Resident Inspector J. Rey, Physical Security Inspector Approved By: Jonathan E. Greives, Chief Reactor Projects Branch 4 Division of Reactor Projects Enclosure
 
License Numbers: DPR-44 and DPR-56  
 
Report Numbers: 05000277/2019010 and 05000278/2019010  
 
Enterprise Identifier: I-2019-010-0006  
 
Licensee: Exelon Generation Company, LLC  
 
Facility: Peach Bottom Atomic Power Station, Units 2 and 3  
 
Location: Delta, PA  
 
Inspection Dates: June 10, 2019 to July 12, 2019  
 
Inspectors: A. Rosebrook, Senior Project Engineer (Team Lead)
E. Andrews, Health Physicist J. Cherubini, Senior Physical Security Inspector J. Dolecki, Resident Inspector J. Heinly, Senior Resident Inspector J. Rey, Physical Security Inspector  
 
Approved By: Jonathan E. Greives, Chief Reactor Projects Branch 4  
 
Division of Reactor Projects  
 
2


=SUMMARY=
=SUMMARY=
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensee's performance by conducting a biennial problem identification and resolution inspection at Peach Bottom Atomic Power Station, Units 2 and 3 in accordance with the Reactor Oversight Process.
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a biennial problem identification and resolution inspection at Peach Bottom Atomic Power Station, Units 2 and 3 in accordance with the Reactor Oversight Process.


The Reactor Oversight Process is the NRC's pr ogram for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.


List of Findings and Violations No findings or violations of more than minor significance were identified.
List of Findings and Violations No findings or violations of more than minor significance were identified.


Additional Tracking Items None.
Additional Tracking Items None.
3


=INSPECTION SCOPES=
=INSPECTION SCOPES=


Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, "Light-Water Reactor Inspection Program - Operations Phase.The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.


==OTHER ACTIVITIES - BASELINE==
==OTHER ACTIVITIES - BASELINE==
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===71152B - Problem Identification and Resolution Biennial Team Inspection (IP Section 02.04) ===
===71152B - Problem Identification and Resolution Biennial Team Inspection (IP Section 02.04) ===
{{IP sample|IP=IP 71152|count=1}}
{{IP sample|IP=IP 71152|count=1}}
: (1) The inspectors performed a biennial assessment of the licensee's corrective action program, use of operating experience, self-assessments and audits, and safety conscious work environment.
: (1) The inspectors performed a biennial assessment of the licensees corrective action program, use of operating experience, self-assessments and audits, and safety conscious work environment.


Corrective Action Program Effectiveness: The inspectors assessed the corrective action program's effectiveness in identifying, prioritizing, evaluating, and correcting problems. The inspectors conducted a five-year review on the adjustable speed drives (ASDs) for the reactor recirculation pumps.
Corrective Action Program Effectiveness: The inspectors assessed the corrective action programs effectiveness in identifying, prioritizing, evaluating, and correcting problems. The inspectors conducted a five-year review on the adjustable speed drives (ASDs) for the reactor recirculation pumps.


Operating Experience, Self-Assessments, and Audits: The inspectors assessed the effectiveness of the station's processes for use of operating experience, audits, and self-assessments.
Operating Experience, Self-Assessments, and Audits: The inspectors assessed the effectiveness of the stations processes for use of operating experience, audits, and self-assessments.


Safety Conscious Work Environment: The inspectors assessed the effectiveness of the station's programs to establish and maintain a safety conscious work environment.
Safety Conscious Work Environment: The inspectors assessed the effectiveness of the stations programs to establish and maintain a safety conscious work environment.


==INSPECTION RESULTS==
==INSPECTION RESULTS==
Assessment 71152B The NRC inspection team reviewed the station's corrective action program and their implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for corrective action programs. Based on the samples selected for review, the team determined that the implementation of the corrective action program and overall performance related to evaluating and resolving problems was effective. In most cases, Exelon identified issues and entered them into the corrective action program at a low threshold, prioritized and evaluated concerns appropriately, and implemented corrective actions to resolve problems in a timely manner, commensurate with the safety significance of the issues. Notwithstanding this, the team identified weaknesses in some of Exelon's evaluations, the scheduling and implementation of corrective actions, and in the management of some station programs.
Assessment                                                                               71152B The NRC inspection team reviewed the stations corrective action program and their implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for corrective action programs. Based on the samples selected for review, the team determined that the implementation of the corrective action program and overall performance related to evaluating and resolving problems was effective. In most cases, Exelon identified issues and entered them into the corrective action program at a low threshold, prioritized and evaluated concerns appropriately, and implemented corrective actions to resolve problems in a timely manner, commensurate with the safety significance of the issues. Notwithstanding this, the team identified weaknesses in some of Exelon's evaluations, the scheduling and implementation of corrective actions, and in the management of some station programs.
 
In addition to implementation of the corrective action program, the inspectors also reviewed Exelon's use of operating experience, conduct of self-assessments, and safety conscious work environment at the station. Based on the samples selected for review, the inspectors concluded the use of operating experience and self-assessments were generally effective in identifying issues and improvement opportunities.


4 In addition to implementation of the corrective action program, the inspectors also reviewed Exelon's use of operating experience, conduct of self-assessments, and safety conscious work environment at the station. Based on the samples selected for review, the inspectors concluded the use of operating experience and self-assessments were generally effective in identifying issues and improvement opportunities.
Finally, the inspectors found no evidence of significant challenges to Peach Bottoms safety conscious work environment. Based on the inspectors observations, Peach Bottom staff are willing to raise nuclear safety concerns through at least one of the several means available.


Finally, the inspectors found no evidence of significant challenges to Peach Bottom's safety conscious work environment. Based on the inspectors' observations, Peach Bottom staff are willing to raise nuclear safety concerns through at least one of the several means available.
Observation: Corrective Action Program Effectiveness                                    71152B In the area of problem evaluation, inspectors identified two issues where plant operators did not adequately evaluate how degraded conditions should be treated per plant technical specifications (TSs) for emergency diesel generators (EDGs):
On May 29, 2019, the E-1 EDG tripped during surveillance testing due to a failed cable (IR 4252679). TS 3.8.1, Emergency Power Sources, was entered appropriately; however, neither Action Statement 3.8.1 B.4.1 or B.4.2, which require an evaluation to determine if the remaining EDGs were inoperable due to a common cause, or completion of Surveillance Requirement 3.8.2, respectively, were adequately completed within 24 hours. In this case, Exelon decided to evaluate the other EDGs to ensure they were not inoperable due to a common cause and made this determination based, in large part, on satisfactory performance of previous surveillance tests and review of maintenance history. Because all four EDGs have similar cables, with similar environmental conditions and maintenance/test history, the inspectors determined that Exelon's evaluation to satisfy Action Statement B.4.1 was inadequate. Because all EDGs subsequently completed Surveillance Requirement 3.8.2 satisfactorily and no operability concerns were identified with the remaining EDGs, inspectors determined this performance deficiency and associated violation were of minor significance in accordance with IMC 0612, Appendix B, Issue Screening.


Observation:  Corrective Action Program Effectiveness 71152B In the area of problem evaluation, inspectors identified two issues where plant operators did not adequately evaluate how degraded conditions should be treated per plant technical specifications (TSs) for emergency diesel generators (EDGs):  On May 29, 2019, the E-1 EDG tripped during surveillance testing due to a failed cable (IR 4252679). TS 3.8.1, Emergency Power Sources, was entered appropriately; however, neither Action Statement 3.8.1 B.4.1 or B.4.2, which require an evaluation to determine if the remaining EDGs were inoperable due to a common cause, or completion of Surveillance Requirement 3.8.2, respectively, were adequately completed within 24 hours. In this case, Exelon decided to evaluate the other EDGs to ensure they were not inoperable due to a common cause and made this determination based, in large part, on satisfactory performance of previous surveillance tests and review of maintenance history. Because all four EDGs have similar cables, with similar environmental conditions and maintenance/test history, the inspectors determined that Exelon's evaluation to satisfy Action Statement B.4.1 was inadequate. Because all EDGs subsequently completed Surveillance Requirement 3.8.2 satisfactorily and no operability concerns were identified with the remaining EDGs, inspectors determined this performance deficiency and associated violation were of minor significance in accordance with IMC 0612, Appendix B, Issue Screening. On February 11, 2019, electrical bus E434 failed to re-energize after a partial loss of offsite power due to a lightning strike (IR 4219461). Operators did not identify that this issue required the E-4 EDG to be considered inoperable. This was identified several hours later during an Exelon fleet call. This action delayed entry into a TS action statement; however, the systems were restored prior to the allowed outage time being exceed so there was no violation of TSs. This issue was documented in Licensee Event Report 2019-001-00 and was closed out in Inspection Report 2019002 (ML19109A097).
On February 11, 2019, electrical bus E434 failed to re-energize after a partial loss of offsite power due to a lightning strike (IR 4219461). Operators did not identify that this issue required the E-4 EDG to be considered inoperable. This was identified several hours later during an Exelon fleet call. This action delayed entry into a TS action statement; however, the systems were restored prior to the allowed outage time being exceed so there was no violation of TSs. This issue was documented in Licensee Event Report 2019-001-00 and was closed out in Inspection Report 2019002 (ML19109A097).


In the area of problem evaluation, inspectors identified several weakness in the quality of corrective action program evaluations. Specifically, the team identified the following examples of evaluations which were not technically accurate or performed in accordance with Exelon's corrective action program procedure: IR 4070302: The inspectors reviewed a cause evaluation for a Unit 3 primary containment isolation valve, AO-3523, which experienced elevated local leak rate testing results. Exelon determined that the cause of the elevated leakage was due to misalignment of the valve in the closed position as evidenced by a saw tooth pattern on the valve test data. The inspectors identified that the evaluation did not account for the reverse actuating actuator when the data was reviewed. This resulted in the data being assessed opposite of its actual stroke pattern and invalidated the cause of the 5 elevated leak rates. Furthermore, the inspectors determined that the leak rate values assessed in the evaluation were not consistent with the testing results and test acceptance criteria. The evaluation, as documented, showed AO-3523 2015 local leak rate testing as-left testing results were out of tolerance. Without an evaluation being performed, operability of the primary containment isolation valve function of AO-3523 would have been in doubt from 2015-2017. Exelon staff was able to promptly demonstrate to the team using the actual test data that the valve had been left in specification and no operability concerns existed. The licensee documented the issues with the evaluation under IR 4256962 and will re-perform the cause evaluation.
In the area of problem evaluation, inspectors identified several weakness in the quality of corrective action program evaluations. Specifically, the team identified the following examples of evaluations which were not technically accurate or performed in accordance with Exelon's corrective action program procedure:
IR 4070302: The inspectors reviewed a cause evaluation for a Unit 3 primary containment isolation valve, AO-3523, which experienced elevated local leak rate testing results. Exelon determined that the cause of the elevated leakage was due to misalignment of the valve in the closed position as evidenced by a saw tooth pattern on the valve test data. The inspectors identified that the evaluation did not account for the reverse actuating actuator when the data was reviewed. This resulted in the data being assessed opposite of its actual stroke pattern and invalidated the cause of the elevated leak rates. Furthermore, the inspectors determined that the leak rate values assessed in the evaluation were not consistent with the testing results and test acceptance criteria. The evaluation, as documented, showed AO-3523 2015 local leak rate testing as-left testing results were out of tolerance. Without an evaluation being performed, operability of the primary containment isolation valve function of AO-3523 would have been in doubt from 2015-2017. Exelon staff was able to promptly demonstrate to the team using the actual test data that the valve had been left in specification and no operability concerns existed. The licensee documented the issues with the evaluation under IR 4256962 and will re-perform the cause evaluation.


The inspectors determined that the cause evaluation did not accurately identify the cause of the elevated leakage; however, the corrective actions created to replace the valve and actuator assembly were reasonable to address the issues associated with the valve and/or actuator.
The inspectors determined that the cause evaluation did not accurately identify the cause of the elevated leakage; however, the corrective actions created to replace the valve and actuator assembly were reasonable to address the issues associated with the valve and/or actuator.


IR 4185296: The inspectors reviewed a cause evaluation which assessed a pile of metal shavings in the Unit 2 torus that were identified during the 2018 refuel outage. The inspectors reviewed the licensee's determination of the cause and determined it to be less than adequate. The cause of the metal shavings was determined to be from equipment degradation; however, no specificity of the equipment, location, or mechanism of degradation was provided. Upon further investigation, the inspectors determined that the metal shavings were likely caused by the 2K safety relief valve cycling at power in 2016 which resulted in residual rust on the tail pipe of the safety relief valve to become dislodged and enter the torus. The licensee documented the issue in the corrective action program under IR 4256326 and will update the cause evaluation.
IR 4185296: The inspectors reviewed a cause evaluation which assessed a pile of metal shavings in the Unit 2 torus that were identified during the 2018 refuel outage.
 
The inspectors reviewed the licensees determination of the cause and determined it to be less than adequate. The cause of the metal shavings was determined to be from equipment degradation; however, no specificity of the equipment, location, or mechanism of degradation was provided. Upon further investigation, the inspectors determined that the metal shavings were likely caused by the 2K safety relief valve cycling at power in 2016 which resulted in residual rust on the tail pipe of the safety relief valve to become dislodged and enter the torus. The licensee documented the issue in the corrective action program under IR 4256326 and will update the cause evaluation.


IR 4153095: Inspectors reviewed a cause evaluation which assessed thermal overloads that unexpectedly tripped on the E434 breaker. Exelon determined that the cause of the trip could not be identified; however, replacement of the breaker would address potential unknown failure modes. The inspectors reviewed the cause evaluation and determined that it adequately assessed the condition and that the corrective actions to replace the breaker was adequate. However, the inspectors identified that the Exelon failed to perform an ER-AA-2003 risk evaluation in accordance with PI-AA-125. Specifically, PI-AA-125 requires a risk evaluation when a cause of a failure cannot be determined. The licensee entered the issue into their corrective action program under IR 4256535 and created an assignment to complete the ER-AA-2003 risk evaluation and perform an extent of condition review. The inspectors did not identify any performance deficiencies greater than minor as a result of this observation. Two additional examples of failing to perform ER-AA-2003 risk assessment were subsequently identified during the onsite portion on the inspection.
IR 4153095: Inspectors reviewed a cause evaluation which assessed thermal overloads that unexpectedly tripped on the E434 breaker. Exelon determined that the cause of the trip could not be identified; however, replacement of the breaker would address potential unknown failure modes. The inspectors reviewed the cause evaluation and determined that it adequately assessed the condition and that the corrective actions to replace the breaker was adequate. However, the inspectors identified that the Exelon failed to perform an ER-AA-2003 risk evaluation in accordance with PI-AA-125. Specifically, PI-AA-125 requires a risk evaluation when a cause of a failure cannot be determined. The licensee entered the issue into their corrective action program under IR 4256535 and created an assignment to complete the ER-AA-2003 risk evaluation and perform an extent of condition review. The inspectors did not identify any performance deficiencies greater than minor as a result of this observation. Two additional examples of failing to perform ER-AA-2003 risk assessment were subsequently identified during the onsite portion on the inspection.


In the area of management and implementation of corrective actions, inspectors identified several corrective actions which were not appropriately managed or which did not effectively correct the problem: IR 4178845: On September 30, 2018, Unit 3 experienced a trip of the 'B' and 'C' condensate pumps which resulted in a low water level SCRAM of the unit. Exelon's evaluation determined that when the condensate pump cables were replaced in 2017, they were pulled thru a wet conduit allowing moisture intrusion into the cables. Post work testing in 2017 included performance of Tan-Delta testing on the new cables.
In the area of management and implementation of corrective actions, inspectors identified several corrective actions which were not appropriately managed or which did not effectively correct the problem:
IR 4178845: On September 30, 2018, Unit 3 experienced a trip of the B and C condensate pumps which resulted in a low water level SCRAM of the unit. Exelon's evaluation determined that when the condensate pump cables were replaced in 2017, they were pulled thru a wet conduit allowing moisture intrusion into the cables. Post work testing in 2017 included performance of Tan-Delta testing on the new cables.


The Tan-Delta test results on the 'B' cable showed abnormal results and additional actions were required by Exelon's cable monitoring program. However, no actions were taken prior to placing the cables back in service and the cable subsequently 6 failed. This was documented in NRC Inspection Report 05000277& 05000278/2018004 as Green FIN 05000278/2018-004-01.
The Tan-Delta test results on the 'B' cable showed abnormal results and additional actions were required by Exelon's cable monitoring program. However, no actions were taken prior to placing the cables back in service and the cable subsequently failed. This was documented in NRC Inspection Report 05000277&
05000278/2018004 as Green FIN 05000278/2018-004-01.


IR 3962563 and IR 3985185: In January 2017, a reverse closing relay (RCR) associated with a motor-operated valve in the reactor coolant isolation cooling (RCIC) failed, resulting in unplanned inoperability of the Unit 3 RCIC system. The relay was  
IR 3962563 and IR 3985185: In January 2017, a reverse closing relay (RCR)associated with a motor-operated valve in the reactor coolant isolation cooling (RCIC)failed, resulting in unplanned inoperability of the Unit 3 RCIC system. The relay was identified during an extent of condition for a 2013 RCR relay failure as being vulnerable to failure due to age and were to be replaced. This corrective action was never scheduled. This failure was documented as a Green NCV in Inspection Report 05000277 & 05000278/2017002. Following the January 2017 failure, AR 03977949 was written to risk-inform their corrective maintenance schedule for replacing all RCRs that currently exceeded their service life. Inspectors reviewed IR 03985185 and determined the condition report represented a second example of NCV 05000278/2017002-01. Specifically, in March 2017, another RCR relay associated with the Unit 2 RCIC system failed, rendering the system inoperable. The inspectors determined that it was not reasonable for this corrective action to be completed on Unit 2 RCIC during the short time between the 2017 failures. Therefore, the March 2017 failure is considered to be an additional example of the performance deficiency documented in NCV 05000278/2017002-01. In accordance with NRC Enforcement Manual Section 1.3.4, Documenting Multiple Examples of a Violation, multiple examples of a single violation are allowed to be documented as a single violation bounded by the characterization of the most significant example. NCV 05000278/2017002-01 is the most significant example because the motor-operated valve controlled by the failed relay is normally closed and would have been required to open to perform its safety function. As such, there is no additional enforcement actions, and the issue is not entered into the plant issues matrix. All 56 safety-related relays have since been replaced or are scheduled to be replaced during the next refueling outage.


identified during an extent of condition for a 2013 RCR relay failure as being vulnerable to failure due to age and were to be replaced. This corrective action was never scheduled. This failure was documented as a Green NCV in Inspection Report 05000277 & 05000278/2017002. Following the January 2017 failure, AR 03977949 was written to risk-inform their corrective maintenance schedule for replacing all RCRs that currently exceeded their service life. Inspectors reviewed IR 03985185 and determined the condition report represented a second example of NCV 05000278/2017002-01. Specifically, in March 2017, another RCR relay associated with the Unit 2 RCIC system failed, rendering the system inoperable. The inspectors determined that it was not reasonable for this corrective action to be completed on Unit 2 RCIC during the short time between the 2017 failures. Therefore, the March 2017 failure is considered to be an additional example of the performance deficiency documented in NCV 05000278/2017002-01. In accordance with NRC Enforcement Manual Section 1.3.4, "Documenting Multiple Examples of a Violation," multiple examples of a single violation are allowed to be documented as a single violation bounded by the characterization of the most significant example. NCV 05000278/2017002-01 is the most significant example because the motor-operated
IR 4181284: An issue with primary containment isolation valve testing was identified regarding not testing a function of the system as a result of a procedure change. The extent of condition identified additional systems which may have the same vulnerability and could result in having exceeding TS surveillance requirements.


valve controlled by the failed relay is normally closed and would have been required to open to perform its safety function. As such, there is no additional enforcement actions, and the issue is not entered into the plant issues matrix. All 56 safety-related relays have since been replaced or are scheduled to be replaced during the next refueling outage. IR 4181284:  An issue with primary containment isolation valve testing was identified regarding not testing a function of the system as a result of a procedure change. The extent of condition identified additional systems which may have the same vulnerability and could result in having exceeding TS surveillance requirements. Actions were created to evaluate the additional systems but were deferred for 9 months. No justification had been completed to determine why it was acceptable to defer evaluating whether a surveillance requirement was met. After inspectors brought this to Exelon's attention, the systems were evaluated and no issues were identified.
Actions were created to evaluate the additional systems but were deferred for 9 months. No justification had been completed to determine why it was acceptable to defer evaluating whether a surveillance requirement was met. After inspectors brought this to Exelon's attention, the systems were evaluated and no issues were identified.


In 2014 and 2016, cable testing results for four cables associated with the emergency auxiliary transformers were identified as abnormal. A work request was initiated to schedule enhanced monitoring and replacement of the cables in 2018. No work order was generated and the cables were neither monitored nor replaced. Upon discovery, a work order was generated and the cables are now scheduled for replacement. Inspectors also identified two minor violations associated with corrective actions either being cancelled or not implemented correctly. These issues are documented separately in Inspection Report 05000277 & 05000278/2019411 (ML19232A327).
In 2014 and 2016, cable testing results for four cables associated with the emergency auxiliary transformers were identified as abnormal. A work request was initiated to schedule enhanced monitoring and replacement of the cables in 2018. No work order was generated and the cables were neither monitored nor replaced. Upon discovery, a work order was generated and the cables are now scheduled for replacement.


Observation:  Operational Experience Program 71152B While the team identified that, in general, the station appropriately identified and implemented industry and NRC operating experience, there were a few equipment failures that properly
Inspectors also identified two minor violations associated with corrective actions either being cancelled or not implemented correctly. These issues are documented separately in Inspection Report 05000277 & 05000278/2019411 (ML19232A327).


evaluating operating experience could have prevented. Most notably was the E-3 EDG 7 failure and White Notice of Violation (EA-18-107) as discussed in NRC Supplemental Inspection Report 05000277 & 05000278/2019040 (ML19178A008). Other examples include main steam isolation valve 80B valve stroking issues and a high pressure coolant injection system pressure boundary leak. These failures and their associated performance deficiencies were dispositioned in Inspection Report 05000277 & 05000278/2019001 (ML19130A086). Exelon agreed with the team's observation and, as detailed in IRs 04243817 and 04195110, are performing corrective actions, including training personnel on effective search techniques of the operating experience database.
Observation: Operational Experience Program                                            71152B While the team identified that, in general, the station appropriately identified and implemented industry and NRC operating experience, there were a few equipment failures that properly evaluating operating experience could have prevented. Most notably was the E-3 EDG failure and White Notice of Violation (EA-18-107) as discussed in NRC Supplemental Inspection Report 05000277 & 05000278/2019040 (ML19178A008). Other examples include main steam isolation valve 80B valve stroking issues and a high pressure coolant injection system pressure boundary leak. These failures and their associated performance deficiencies were dispositioned in Inspection Report 05000277 & 05000278/2019001 (ML19130A086). Exelon agreed with the teams observation and, as detailed in IRs 04243817 and 04195110, are performing corrective actions, including training personnel on effective search techniques of the operating experience database.


Observation: Review of long term corrective actions for EA-18-107 71152B Per the requirements of NRC IP 71152B, the team reviewed Exelon's progress with long term corrective actions for EA-18-107, which were not completed by the end of the supplemental inspection (Inspection Report 05000277 & 05000278/2019040). The team verified that IRs 04249183, 04249340, and 04249874, documenting the supplemental inspection team's observations, had been properly screened and evaluations were performed as appropriate.
Observation: Review of long term corrective actions for EA-18-107                     71152B Per the requirements of NRC IP 71152B, the team reviewed Exelon's progress with long term corrective actions for EA-18-107, which were not completed by the end of the supplemental inspection (Inspection Report 05000277 & 05000278/2019040). The team verified that IRs 04249183, 04249340, and 04249874, documenting the supplemental inspection team's observations, had been properly screened and evaluations were performed as appropriate.


No major open corrective actions were completed from the end of the supplemental inspection until the completion of the problem identification and resolution team inspection. Corrective actions such as effectiveness reviews remain open as expected.
No major open corrective actions were completed from the end of the supplemental inspection until the completion of the problem identification and resolution team inspection. Corrective actions such as effectiveness reviews remain open as expected.
Line 140: Line 123:


On July 12, 2019, the inspectors presented the biennial problem identification and resolution inspection results to Patrick Navin, Site Vice President and other members of the licensee staff.
On July 12, 2019, the inspectors presented the biennial problem identification and resolution inspection results to Patrick Navin, Site Vice President and other members of the licensee staff.
8


=DOCUMENTS REVIEWED=
=DOCUMENTS REVIEWED=


Inspection
Inspection Type             Designation Description or Title                                   Revision or
Procedure Type Designation Description or Title Revision or
Procedure                                                                                      Date
Date 71152B Corrective Action Documents
71152B     Corrective Action             1264501, 1271575, 1483753, 1484815, 1556263, 1571377,
264501, 1271575, 1483753, 1484815, 1556263, 1571377, 1573040, 1573674, 1576515, 1649868, 2527605, 2568186,
Documents                    1573040, 1573674, 1576515, 1649868, 2527605, 2568186,
2608175, 3801443, 3962563, 3966838, 3977949, 3985974, 3993931, 3994000, 3994568, 3997923, 3999609, 4001804, 4003608, 4005630, 4008207, 4008476, 4009511, 4012756,
2608175, 3801443, 3962563, 3966838, 3977949, 3985974,
3993931, 3994000, 3994568, 3997923, 3999609, 4001804,
4003608, 4005630, 4008207, 4008476, 4009511, 4012756,
4013582, 4016856, 4019651, 4020294, 4020298, 4020301,
4013582, 4016856, 4019651, 4020294, 4020298, 4020301,
21001, 4021004, 4021006, 4021010, 4022441, 4030168,
21001, 4021004, 4021006, 4021010, 4022441, 4030168,
4031002, 403027, 4030367, 4034253, 4034266, 4035036, 4035409, 4036492, 4037363, 4038804, 4040629, 4042507, 4042954, 4042605, 4044373, 4044444, 4045487, 4047278,
4031002, 403027, 4030367, 4034253, 4034266, 4035036,
4035409, 4036492, 4037363, 4038804, 4040629, 4042507,
4042954, 4042605, 4044373, 4044444, 4045487, 4047278,
4052562, 4052566, 4054327, 4056699, 4057393, 4059720,
4052562, 4052566, 4054327, 4056699, 4057393, 4059720,
4065691, 4065757, 4067087, 4070302, 4070392, 4070745,
4065691, 4065757, 4067087, 4070302, 4070392, 4070745,
4070781, 4076103, 4071144, 4073299, 4077304, 4079959,
4070781, 4076103, 4071144, 4073299, 4077304, 4079959,
4083059, 4083518, 4083178, 4083714, 4085436, 4088290, 4090461, 4092287, 4092566, 4097059, 4097357, 4010888, 4101666, 4106618, 4107475, 4111840, 4116548, 4112720,
4083059, 4083518, 4083178, 4083714, 4085436, 4088290,
4090461, 4092287, 4092566, 4097059, 4097357, 4010888,
4101666, 4106618, 4107475, 4111840, 4116548, 4112720,
4112733, 4115309, 4118666, 4121224, 4123548, 4122474,
4112733, 4115309, 4118666, 4121224, 4123548, 4122474,
27608, 4128185, 4128201, 4128214, 4129583, 4141255,
27608, 4128185, 4128201, 4128214, 4129583, 4141255,
4142103, 4143007, 4144923, 4146926, 4153095, 4153350, 4162534, 4163735, 4163825, 4165672, 4171947, 4174830, 4175355, 4175404, 4175898, 4175920, 4176097, 4176229,
4142103, 4143007, 4144923, 4146926, 4153095, 4153350,
4162534, 4163735, 4163825, 4165672, 4171947, 4174830,
4175355, 4175404, 4175898, 4175920, 4176097, 4176229,
4177767, 4178993, 4181284, 4185296, 4186914, 4187727,
4177767, 4178993, 4181284, 4185296, 4186914, 4187727,
4194026, 4194514, 4194889, 4195447, 4197731, 4200142,
4194026, 4194514, 4194889, 4195447, 4197731, 4200142,
201953, 4020305, 4211923, 4212231, 4212758, 4213437, 4221542, 4221544, 4221559, 4235568, 4235573, 4236188, 4239989, 4240548, 4241393, 4241392, 4242421, 4244532,
201953, 4020305, 4211923, 4212231, 4212758, 4213437,
21542, 4221544, 4221559, 4235568, 4235573, 4236188,
239989, 4240548, 4241393, 4241392, 4242421, 4244532,
246563, 4248475, 4248688, 4249277, 4249284, 4256326,
246563, 4248475, 4248688, 4249277, 4249284, 4256326,
256535, 4256840*, 4256962, 4258087, 4258942, 4259050,
256535, 4256840*, 4256962, 4258087, 4258942, 4259050,
259331, 4259510, 4259562,
259331, 4259510, 4259562,
Drawings 6280-M-367, Sheet 2 P&I DIAGRAM CONTAINMENT ATMOSPHERIC CONTROL SYSTEM Revision 81 Miscellaneous
Drawings         6280-M-367, P&I DIAGRAM CONTAINMENT ATMOSPHERIC CONTROL           Revision 81
PLANT HEALTH COMMITTEE MEETING AGENDA, DATED  
Sheet 2    SYSTEM
 
Miscellaneous                 PLANT HEALTH COMMITTEE MEETING AGENDA, DATED
Inspection
Inspection Type       Designation Description or Title                         Revision or
Procedure Type Designation Description or Title Revision or
Procedure                                                                      Date
Date JUNE 19, 2019
JUNE 19, 2019
PEACH BOTTOM NRC INSPECTION - PROBLEM IDENTIFICATION AND RESOLUTION (2019) STATUS
PEACH BOTTOM NRC INSPECTION - PROBLEM       June 26,
REPORT June 26, 2019  MAINTENANCE FUNCTIONAL AREA AUDIT REPORT, NOSA-PEA-18-01 (AR 4090541) PBAPS
IDENTIFICATION AND RESOLUTION (2019) STATUS 2019
February 5
REPORT
to February
MAINTENANCE FUNCTIONAL AREA AUDIT REPORT,   February 5
16, 2018 SECURITY PROGRAMS AUDIT REPORT, NOSA-PEA-17-
NOSA-PEA-18-01 (AR 4090541) PBAPS           to February
  (AR 3958635), PBAPS
16, 2018
January 23
SECURITY PROGRAMS AUDIT REPORT, NOSA-PEA-17- January 23
to January
  (AR 3958635), PBAPS                       to January
27, 2017 NCV 50-277 & 50-278/2017-002-01 NCV 50-277 & 50-278/2017-003-01 NCV 50-277 & 50-278/2017-008-01 NCV 50-277 & 50-278/2017-008-02
27, 2017
NCV 50-277 & 50-278/2017-002-01
NCV 50-277 & 50-278/2017-003-01
NCV 50-277 & 50-278/2017-008-01
NCV 50-277 & 50-278/2017-008-02
NCV 50-277 & 50-278/2017-201-01
NCV 50-277 & 50-278/2017-201-01
NCV 50-277 & 50-278/2017-201-02
NCV 50-277 & 50-278/2017-201-02
NCV 50-277 & 50-278/2017-403-01 NCV 50-277 & 50-278/2017-403-01 NCV 50-277 & 50-278/2018-001-01
NCV 50-277 & 50-278/2017-403-01
NCV 50-277 & 50-278/2017-403-01
NCV 50-277 & 50-278/2018-001-01
NCV 50-277 & 50-278/2018-002-01
NCV 50-277 & 50-278/2018-002-01
NCV 50-277 & 50-278/2018-002-01
NCV 50-277 & 50-278/2018-002-01
NCV 50-277 & 50-278/2018-003-01
NCV 50-277 & 50-278/2018-003-01
NCV 50-277 & 50-278/2018-004-01 NCV 50-277 & 50-278/2018-010-01 NCV 50-277 & 50-278/2018-010-02
NCV 50-277 & 50-278/2018-004-01
NCV 50-277 & 50-278/2018-010-01
NCV 50-277 & 50-278/2018-010-02
NCV 50-277 & 50-278/2018-012-01
NCV 50-277 & 50-278/2018-012-01
NCV 50-277 & 50-278/2018-410-01
NCV 50-277 & 50-278/2018-410-01
NCV 50-277 & 50-278/2019-001-01 NCV 50-277 & 50-278/2019-001-02 NCV 50-277 & 50-278/2019-011-01
NCV 50-277 & 50-278/2019-001-01
NCV 50-277 & 50-278/2019-001-02
NCV 50-277 & 50-278/2019-011-01
EA-17-20 (Enforcement Discretion)
EA-17-20 (Enforcement Discretion)
EA-18-08 (Enforcement Discretion)
EA-18-08 (Enforcement Discretion)
ZONE ALARM HISTORY BY CLEAR CODE 06/24/2019 Procedures CC-AA-102 DESIGN INPUT AND CONFIGURATION CHANGE IMPACT Revision 32
ZONE ALARM HISTORY BY CLEAR CODE             06/24/2019
Inspection
Procedures CC-AA-102   DESIGN INPUT AND CONFIGURATION CHANGE IMPACT Revision 32
Procedure Type Designation Description or Title Revision or
Inspection Type Designation     Description or Title                       Revision or
Date SCREENING
Procedure                                                                  Date
EP-AA-112-200-
SCREENING
F-04 SECURITY COORDINATOR CHECKLIST Revision 32 MA-AA-716-008 FOREIGN MATERIAL EXCLUSION PROGRAM Revision 14
EP-AA-112-200- SECURITY COORDINATOR CHECKLIST             Revision 32
NO-AA-10 QUALITY ASSURANCE TOPICAL REPORT (QATR) Revision 94 NO-AA-210
F-04
NUCLEAR OVERSIGHT REGULATORY AUDIT PROCEDURE
MA-AA-716-008   FOREIGN MATERIAL EXCLUSION PROGRAM         Revision 14
Revision 10
NO-AA-10       QUALITY ASSURANCE TOPICAL REPORT           Revision 94
OP-AA-108-115
                                (QATR)
OPERABILITY DETERMINATIONS (CM-1) Revision 21
NO-AA-210       NUCLEAR OVERSIGHT REGULATORY AUDIT         Revision 10
OP-AA-108-115-
PROCEDURE
1001
OP-AA-108-115   OPERABILITY DETERMINATIONS (CM-1)           Revision 21
OPERABILITY EVALUATION PASSPORT ENGINEERING CHANGE DESKTOP GUIDE
OP-AA-108-115- OPERABILITY EVALUATION PASSPORT ENGINEERING Revision 1
Revision 1
1001            CHANGE DESKTOP GUIDE
OP-AA-108-115-
OP-AA-108-115- SUPPLEMENTAL CONSIDERATION FOR ON-SHIFT     Revision 3
1002
1002            IMMEDIATE
SUPPLEMENTAL CONSIDERATION FOR ON-SHIFT
IMMEDIATE
OPERABILITY DETERMINATIONS (CM-1)
OPERABILITY DETERMINATIONS (CM-1)
Revision 3 OP-PB-102-106 OPERATOR RESPONSE TIME PROGRAM AT PEACH
OP-PB-102-106   OPERATOR RESPONSE TIME PROGRAM AT PEACH     Revision 10
BOTTOM Revision 10
BOTTOM
PI-AA-101
PI-AA-101       CONDUCT OF PERFORMANCE IMPROVEMENT         Revision 1
CONDUCT OF PERFORMANCE IMPROVEMENT Revision 1 PI-AA-101-1001
PI-AA-101-1001 PERFORMANCE MONITORING AND ANALYSIS MANUAL Revision 2
PERFORMANCE MONITORING AND ANALYSIS MANUAL Revision 2 PI-AA-101-1002
PI-AA-101-1002 PI MANAGEMENT REVIEW MEETINGS AND REPORTING Revision 2
PI MANAGEMENT REVIEW MEETINGS AND REPORTING Revision 2 PI-AA-101-1003
PI-AA-101-1003 PERFORMANCE GAP RESOLUTION                 Revision 0
PERFORMANCE GAP RESOLUTION Revision 0
PI-AA-115       OPERATING EXPERIENCE PROGRAM               Revision 4
PI-AA-115
PI-AA-115-1001 PROCESSING OF LEVEL 1 OPEX EVALUATIONS     Revision 2
OPERATING EXPERIENCE PROGRAM Revision 4 PI-AA-115-1001
PI-AA-115-1001- PRIORITY OF LEGACY IER AND SOER             Revision 0
PROCESSING OF LEVEL 1 OPEX EVALUATIONS Revision 2 PI-AA-115-1001-
F-01            RECOMMENDATIONS
F-01 PRIORITY OF LEGACY IER AND SOER RECOMMENDATIONS
Inspection Type Designation     Description or Title                       Revision or
Revision 0
Procedure                                                                    Date
Inspection
PI-AA-115-1002   PROCESSING OF LEVEL 2 OPEX EVALUATIONS     Revision 3
Procedure Type Designation Description or Title Revision or
PI-AA-115-1003   PROCESSING OF LEVEL 3 OPEX EVALUATIONS     Revision 5
Date PI-AA-115-1002
PI-AA-115-1004   PROCESSING OF NER AND ICES REPORTS         Revision 6
PROCESSING OF LEVEL 2 OPEX EVALUATIONS Revision 3 PI-AA-115-1003
PI-AA-115-1004- ICES REPORT SCREENING FORM                  Revision 0
PROCESSING OF LEVEL 3 OPEX EVALUATIONS Revision 5 PI-AA-115-1004
PROCESSING OF NER AND ICES REPORTS Revision 6 PI-AA-115-1004-
F-03
F-03
ICES REPORT SCREENING FORM Revision 0
PI-AA-120       ISSUE IDENTIFICATION AND SCREENING PROCESS Revision 8
PI-AA-120
PI-AA-125       CORRECTIVE ACTION PROGRAM (CAP) PROCEDURE   Revision 6
ISSUE IDENTIFICATION AND SCREENING PROCESS Revision 8
PI-AA-125-001-F- CAPCO INDOCTRINATION GUIDE                 Revision 1
PI-AA-125
PI-AA-125-1001   ROOT CAUSE ANALYSIS MANUAL                 Revision 3
CORRECTIVE ACTION PROGRAM (CAP) PROCEDURE Revision 6 PI-AA-125-001-F-
PI-AA-125-1003   CORRECTIVE ACTION PROGRAM EVALUATION MANUAL Revision 4
CAPCO INDOCTRINATION GUIDE Revision 1 PI-AA-125-1001
PI-AA-125-1004   EFFECTIVENESS REVIEW MANUAL                 Revision 2
ROOT CAUSE ANALYSIS MANUAL Revision 3 PI-AA-125-1003
PI-AA-125-1006   INVESTIGATION TECHNIQUES MANUAL             Revision 4
CORRECTIVE ACTION PROGRAM EVALUATION MANUAL Revision 4 PI-AA-125-1004
PI-AA-126       SELF-ASSESSMENT AND BENCHMARK PROGRAM       Revision 2
EFFECTIVENESS REVIEW MANUAL Revision 2 PI-AA-125-1006
PI-AA-126-1001   SELF-ASSESSMENTS                           Revision 2
INVESTIGATION TECHNIQUES MANUAL Revision 4
PI-AA-126-1001- SELF-ASSESSMENT                            Revision 2
PI-AA-126
SELF-ASSESSMENT AND BENCHMARK PROGRAM Revision 2 PI-AA-126-1001
SELF-ASSESSMENTS Revision 2 PI-AA-126-1001-
F-01
F-01
SELF-ASSESSMENT Revision 2
Inspection Type       Designation     Description or Title                               Revision or
Inspection
Procedure                                                                                Date
Procedure Type Designation Description or Title Revision or
PI-AA-126-1006 BENCHMARK PROGRAM                                 Revision 2
Date PI-AA-126-1006
PI-AA-126-1006- BENCHMARK                                          Revision 2
BENCHMARK PROGRAM Revision 2 PI-AA-126-1006-
F-01
F-01
BENCHMARK Revision 2 PI-AA-126-1006-
PI-AA-126-1006- OPPORTUNITY FOR IMPROVEMENT BENCHMARK              Revision 0
F-03
F-03
OPPORTUNITY FOR IMPROVEMENT BENCHMARK Revision 0
PI-AA-127       PASSPORT ACTION TRACKING MANAGEMENT               Revision 2
PI-AA-127
PROCEDURE
PASSPORT ACTION TRACKING MANAGEMENT PROCEDURE
RT-S-045-911-2 Precautions, Limitations, and General Instructions Revision 24
Revision 2 RT-S-045-911-2 Precautions, Limitations, and General Instructions Revision 24
ST/LLRT         LOCAL LEAK RATE TEST DOCUMENTATION AND             REVISION 4
ST/LLRT 20.00.01 LOCAL LEAK RATE TEST DOCUMENTATION AND TRACKING REVISION 4
20.00.01       TRACKING
ST/LLRT 30.00.01 LOCAL LEAK RATE TEST DOCUMENTATION AND TRACKING Revision 4
ST/LLRT        LOCAL LEAK RATE TEST DOCUMENTATION AND             Revision 4
ST/LLRT 30.07B.16 D/W PURGE SUPPLY (AO-3-07B-3523, CHK-3-07B-
30.00.01        TRACKING
50095A, CHK-3-07B-50095B)
ST/LLRT         D/W PURGE SUPPLY (AO-3-07B-3523, CHK-3-07B-       Revision 9
Revision 9
30.07B.16      50095A, CHK-3-07B-50095B)
SY-AA-101-122-
SY-AA-101-122- Performance of Security System Tests               Revision 13
1001 Performance of Security System Tests Revision 13
1001
SY-PB-101-122-
SY-PB-101-122- Performance of Security System Tests               Revision 1
1001 Performance of Security System Tests Revision 1
1001
SY-PB-101-122-
SY-PB-101-122- Security Weekly Equipment Testing - CAS           REvision 1
1001-F-01 Security Weekly Equipment Testing - CAS REvision 1 WC-AA-106
1001-F-01
WORK SCREENING AND PROCESSING Revision 18
WC-AA-106       WORK SCREENING AND PROCESSING                     Revision 18
Work Orders
Work Orders                 0246671
246671
2
}}
}}

Latest revision as of 00:08, 8 October 2019

Biennial Problem Identification and Resolution Inspection Report 05000277/2019010 and 05000278/2019010
ML19232A305
Person / Time
Site: Peach Bottom  Constellation icon.png
Issue date: 08/26/2019
From: Jon Greives
Reactor Projects Region 1 Branch 4
To: Bryan Hanson
Exelon Generation Co, Exelon Nuclear
Greives J
References
IR 2019010
Download: ML19232A305 (15)


Text

ust 26, 2019

SUBJECT:

PEACH BOTTOM ATOMIC POWER STATION, UNITS 2 AND 3 - BIENNIAL PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000277/2019010 AND 05000278/2019010

Dear Mr. Hanson:

On July 12, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed a problem identification and resolution inspection at Peach Bottom Atomic Power Station, Units 2 and 3 and discussed the results of this inspection with Patrick Navin, Site Vice President and other members of your staff. The results of this inspection are documented in the enclosed report.

The NRC inspection team reviewed the stations corrective action program and the stations implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for corrective action programs. Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

The team also evaluated the stations processes for use of industry and NRC operating experience information and the effectiveness of the stations audits and self-assessments.

Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

Finally the team reviewed the stations programs to establish and maintain a safety conscious work environment, and interviewed station personnel to evaluate the effectiveness of these programs. Based on the teams observations and the results of these interviews the team found no evidence of challenges to your organizations safety conscious work environment.

Your employees appeared willing to raise nuclear safety concerns through at least one of the several means available.

The NRC inspectors did not identify any finding or violation of more than minor significance. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Jonathan E. Greives, Chief Reactor Projects Branch 4 Division of Reactor Projects Docket Nos. 05000277 and 05000278 License Nos. DPR-44 and DPR-56

Enclosure:

As stated

Inspection Report

Docket Numbers: 05000277 and 05000278 License Numbers: DPR-44 and DPR-56 Report Numbers: 05000277/2019010 and 05000278/2019010 Enterprise Identifier: I-2019-010-0006 Licensee: Exelon Generation Company, LLC Facility: Peach Bottom Atomic Power Station, Units 2 and 3 Location: Delta, PA Inspection Dates: June 10, 2019 to July 12, 2019 Inspectors: A. Rosebrook, Senior Project Engineer (Team Lead)

E. Andrews, Health Physicist J. Cherubini, Senior Physical Security Inspector J. Dolecki, Resident Inspector J. Heinly, Senior Resident Inspector J. Rey, Physical Security Inspector Approved By: Jonathan E. Greives, Chief Reactor Projects Branch 4 Division of Reactor Projects Enclosure

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a biennial problem identification and resolution inspection at Peach Bottom Atomic Power Station, Units 2 and 3 in accordance with the Reactor Oversight Process.

The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations No findings or violations of more than minor significance were identified.

Additional Tracking Items None.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

OTHER ACTIVITIES - BASELINE

71152B - Problem Identification and Resolution Biennial Team Inspection (IP Section 02.04)

(1) The inspectors performed a biennial assessment of the licensees corrective action program, use of operating experience, self-assessments and audits, and safety conscious work environment.

Corrective Action Program Effectiveness: The inspectors assessed the corrective action programs effectiveness in identifying, prioritizing, evaluating, and correcting problems. The inspectors conducted a five-year review on the adjustable speed drives (ASDs) for the reactor recirculation pumps.

Operating Experience, Self-Assessments, and Audits: The inspectors assessed the effectiveness of the stations processes for use of operating experience, audits, and self-assessments.

Safety Conscious Work Environment: The inspectors assessed the effectiveness of the stations programs to establish and maintain a safety conscious work environment.

INSPECTION RESULTS

Assessment 71152B The NRC inspection team reviewed the stations corrective action program and their implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for corrective action programs. Based on the samples selected for review, the team determined that the implementation of the corrective action program and overall performance related to evaluating and resolving problems was effective. In most cases, Exelon identified issues and entered them into the corrective action program at a low threshold, prioritized and evaluated concerns appropriately, and implemented corrective actions to resolve problems in a timely manner, commensurate with the safety significance of the issues. Notwithstanding this, the team identified weaknesses in some of Exelon's evaluations, the scheduling and implementation of corrective actions, and in the management of some station programs.

In addition to implementation of the corrective action program, the inspectors also reviewed Exelon's use of operating experience, conduct of self-assessments, and safety conscious work environment at the station. Based on the samples selected for review, the inspectors concluded the use of operating experience and self-assessments were generally effective in identifying issues and improvement opportunities.

Finally, the inspectors found no evidence of significant challenges to Peach Bottoms safety conscious work environment. Based on the inspectors observations, Peach Bottom staff are willing to raise nuclear safety concerns through at least one of the several means available.

Observation: Corrective Action Program Effectiveness 71152B In the area of problem evaluation, inspectors identified two issues where plant operators did not adequately evaluate how degraded conditions should be treated per plant technical specifications (TSs) for emergency diesel generators (EDGs):

On May 29, 2019, the E-1 EDG tripped during surveillance testing due to a failed cable (IR 4252679). TS 3.8.1, Emergency Power Sources, was entered appropriately; however, neither Action Statement 3.8.1 B.4.1 or B.4.2, which require an evaluation to determine if the remaining EDGs were inoperable due to a common cause, or completion of Surveillance Requirement 3.8.2, respectively, were adequately completed within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. In this case, Exelon decided to evaluate the other EDGs to ensure they were not inoperable due to a common cause and made this determination based, in large part, on satisfactory performance of previous surveillance tests and review of maintenance history. Because all four EDGs have similar cables, with similar environmental conditions and maintenance/test history, the inspectors determined that Exelon's evaluation to satisfy Action Statement B.4.1 was inadequate. Because all EDGs subsequently completed Surveillance Requirement 3.8.2 satisfactorily and no operability concerns were identified with the remaining EDGs, inspectors determined this performance deficiency and associated violation were of minor significance in accordance with IMC 0612, Appendix B, Issue Screening.

On February 11, 2019, electrical bus E434 failed to re-energize after a partial loss of offsite power due to a lightning strike (IR 4219461). Operators did not identify that this issue required the E-4 EDG to be considered inoperable. This was identified several hours later during an Exelon fleet call. This action delayed entry into a TS action statement; however, the systems were restored prior to the allowed outage time being exceed so there was no violation of TSs. This issue was documented in Licensee Event Report 2019-001-00 and was closed out in Inspection Report 2019002 (ML19109A097).

In the area of problem evaluation, inspectors identified several weakness in the quality of corrective action program evaluations. Specifically, the team identified the following examples of evaluations which were not technically accurate or performed in accordance with Exelon's corrective action program procedure:

IR 4070302: The inspectors reviewed a cause evaluation for a Unit 3 primary containment isolation valve, AO-3523, which experienced elevated local leak rate testing results. Exelon determined that the cause of the elevated leakage was due to misalignment of the valve in the closed position as evidenced by a saw tooth pattern on the valve test data. The inspectors identified that the evaluation did not account for the reverse actuating actuator when the data was reviewed. This resulted in the data being assessed opposite of its actual stroke pattern and invalidated the cause of the elevated leak rates. Furthermore, the inspectors determined that the leak rate values assessed in the evaluation were not consistent with the testing results and test acceptance criteria. The evaluation, as documented, showed AO-3523 2015 local leak rate testing as-left testing results were out of tolerance. Without an evaluation being performed, operability of the primary containment isolation valve function of AO-3523 would have been in doubt from 2015-2017. Exelon staff was able to promptly demonstrate to the team using the actual test data that the valve had been left in specification and no operability concerns existed. The licensee documented the issues with the evaluation under IR 4256962 and will re-perform the cause evaluation.

The inspectors determined that the cause evaluation did not accurately identify the cause of the elevated leakage; however, the corrective actions created to replace the valve and actuator assembly were reasonable to address the issues associated with the valve and/or actuator.

IR 4185296: The inspectors reviewed a cause evaluation which assessed a pile of metal shavings in the Unit 2 torus that were identified during the 2018 refuel outage.

The inspectors reviewed the licensees determination of the cause and determined it to be less than adequate. The cause of the metal shavings was determined to be from equipment degradation; however, no specificity of the equipment, location, or mechanism of degradation was provided. Upon further investigation, the inspectors determined that the metal shavings were likely caused by the 2K safety relief valve cycling at power in 2016 which resulted in residual rust on the tail pipe of the safety relief valve to become dislodged and enter the torus. The licensee documented the issue in the corrective action program under IR 4256326 and will update the cause evaluation.

IR 4153095: Inspectors reviewed a cause evaluation which assessed thermal overloads that unexpectedly tripped on the E434 breaker. Exelon determined that the cause of the trip could not be identified; however, replacement of the breaker would address potential unknown failure modes. The inspectors reviewed the cause evaluation and determined that it adequately assessed the condition and that the corrective actions to replace the breaker was adequate. However, the inspectors identified that the Exelon failed to perform an ER-AA-2003 risk evaluation in accordance with PI-AA-125. Specifically, PI-AA-125 requires a risk evaluation when a cause of a failure cannot be determined. The licensee entered the issue into their corrective action program under IR 4256535 and created an assignment to complete the ER-AA-2003 risk evaluation and perform an extent of condition review. The inspectors did not identify any performance deficiencies greater than minor as a result of this observation. Two additional examples of failing to perform ER-AA-2003 risk assessment were subsequently identified during the onsite portion on the inspection.

In the area of management and implementation of corrective actions, inspectors identified several corrective actions which were not appropriately managed or which did not effectively correct the problem:

IR 4178845: On September 30, 2018, Unit 3 experienced a trip of the B and C condensate pumps which resulted in a low water level SCRAM of the unit. Exelon's evaluation determined that when the condensate pump cables were replaced in 2017, they were pulled thru a wet conduit allowing moisture intrusion into the cables. Post work testing in 2017 included performance of Tan-Delta testing on the new cables.

The Tan-Delta test results on the 'B' cable showed abnormal results and additional actions were required by Exelon's cable monitoring program. However, no actions were taken prior to placing the cables back in service and the cable subsequently failed. This was documented in NRC Inspection Report 05000277&

05000278/2018004 as Green FIN 05000278/2018-004-01.

IR 3962563 and IR 3985185: In January 2017, a reverse closing relay (RCR)associated with a motor-operated valve in the reactor coolant isolation cooling (RCIC)failed, resulting in unplanned inoperability of the Unit 3 RCIC system. The relay was identified during an extent of condition for a 2013 RCR relay failure as being vulnerable to failure due to age and were to be replaced. This corrective action was never scheduled. This failure was documented as a Green NCV in Inspection Report 05000277 & 05000278/2017002. Following the January 2017 failure, AR 03977949 was written to risk-inform their corrective maintenance schedule for replacing all RCRs that currently exceeded their service life. Inspectors reviewed IR 03985185 and determined the condition report represented a second example of NCV 05000278/2017002-01. Specifically, in March 2017, another RCR relay associated with the Unit 2 RCIC system failed, rendering the system inoperable. The inspectors determined that it was not reasonable for this corrective action to be completed on Unit 2 RCIC during the short time between the 2017 failures. Therefore, the March 2017 failure is considered to be an additional example of the performance deficiency documented in NCV 05000278/2017002-01. In accordance with NRC Enforcement Manual Section 1.3.4, Documenting Multiple Examples of a Violation, multiple examples of a single violation are allowed to be documented as a single violation bounded by the characterization of the most significant example. NCV 05000278/2017002-01 is the most significant example because the motor-operated valve controlled by the failed relay is normally closed and would have been required to open to perform its safety function. As such, there is no additional enforcement actions, and the issue is not entered into the plant issues matrix. All 56 safety-related relays have since been replaced or are scheduled to be replaced during the next refueling outage.

IR 4181284: An issue with primary containment isolation valve testing was identified regarding not testing a function of the system as a result of a procedure change. The extent of condition identified additional systems which may have the same vulnerability and could result in having exceeding TS surveillance requirements.

Actions were created to evaluate the additional systems but were deferred for 9 months. No justification had been completed to determine why it was acceptable to defer evaluating whether a surveillance requirement was met. After inspectors brought this to Exelon's attention, the systems were evaluated and no issues were identified.

In 2014 and 2016, cable testing results for four cables associated with the emergency auxiliary transformers were identified as abnormal. A work request was initiated to schedule enhanced monitoring and replacement of the cables in 2018. No work order was generated and the cables were neither monitored nor replaced. Upon discovery, a work order was generated and the cables are now scheduled for replacement.

Inspectors also identified two minor violations associated with corrective actions either being cancelled or not implemented correctly. These issues are documented separately in Inspection Report 05000277 & 05000278/2019411 (ML19232A327).

Observation: Operational Experience Program 71152B While the team identified that, in general, the station appropriately identified and implemented industry and NRC operating experience, there were a few equipment failures that properly evaluating operating experience could have prevented. Most notably was the E-3 EDG failure and White Notice of Violation (EA-18-107) as discussed in NRC Supplemental Inspection Report 05000277 & 05000278/2019040 (ML19178A008). Other examples include main steam isolation valve 80B valve stroking issues and a high pressure coolant injection system pressure boundary leak. These failures and their associated performance deficiencies were dispositioned in Inspection Report 05000277 & 05000278/2019001 (ML19130A086). Exelon agreed with the teams observation and, as detailed in IRs 04243817 and 04195110, are performing corrective actions, including training personnel on effective search techniques of the operating experience database.

Observation: Review of long term corrective actions for EA-18-107 71152B Per the requirements of NRC IP 71152B, the team reviewed Exelon's progress with long term corrective actions for EA-18-107, which were not completed by the end of the supplemental inspection (Inspection Report 05000277 & 05000278/2019040). The team verified that IRs 04249183, 04249340, and 04249874, documenting the supplemental inspection team's observations, had been properly screened and evaluations were performed as appropriate.

No major open corrective actions were completed from the end of the supplemental inspection until the completion of the problem identification and resolution team inspection. Corrective actions such as effectiveness reviews remain open as expected.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On July 12, 2019, the inspectors presented the biennial problem identification and resolution inspection results to Patrick Navin, Site Vice President and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection Type Designation Description or Title Revision or

Procedure Date

71152B Corrective Action 1264501, 1271575, 1483753, 1484815, 1556263, 1571377,

Documents 1573040, 1573674, 1576515, 1649868, 2527605, 2568186,

2608175, 3801443, 3962563, 3966838, 3977949, 3985974,

3993931, 3994000, 3994568, 3997923, 3999609, 4001804,

4003608, 4005630, 4008207, 4008476, 4009511, 4012756,

4013582, 4016856, 4019651, 4020294, 4020298, 4020301,

21001, 4021004, 4021006, 4021010, 4022441, 4030168,

4031002, 403027, 4030367, 4034253, 4034266, 4035036,

4035409, 4036492, 4037363, 4038804, 4040629, 4042507,

4042954, 4042605, 4044373, 4044444, 4045487, 4047278,

4052562, 4052566, 4054327, 4056699, 4057393, 4059720,

4065691, 4065757, 4067087, 4070302, 4070392, 4070745,

4070781, 4076103, 4071144, 4073299, 4077304, 4079959,

4083059, 4083518, 4083178, 4083714, 4085436, 4088290,

4090461, 4092287, 4092566, 4097059, 4097357, 4010888,

4101666, 4106618, 4107475, 4111840, 4116548, 4112720,

4112733, 4115309, 4118666, 4121224, 4123548, 4122474,

27608, 4128185, 4128201, 4128214, 4129583, 4141255,

4142103, 4143007, 4144923, 4146926, 4153095, 4153350,

4162534, 4163735, 4163825, 4165672, 4171947, 4174830,

4175355, 4175404, 4175898, 4175920, 4176097, 4176229,

4177767, 4178993, 4181284, 4185296, 4186914, 4187727,

4194026, 4194514, 4194889, 4195447, 4197731, 4200142,

201953, 4020305, 4211923, 4212231, 4212758, 4213437,

21542, 4221544, 4221559, 4235568, 4235573, 4236188,

239989, 4240548, 4241393, 4241392, 4242421, 4244532,

246563, 4248475, 4248688, 4249277, 4249284, 4256326,

256535, 4256840*, 4256962, 4258087, 4258942, 4259050,

259331, 4259510, 4259562,

Drawings 6280-M-367, P&I DIAGRAM CONTAINMENT ATMOSPHERIC CONTROL Revision 81

Sheet 2 SYSTEM

Miscellaneous PLANT HEALTH COMMITTEE MEETING AGENDA, DATED

Inspection Type Designation Description or Title Revision or

Procedure Date

JUNE 19, 2019

PEACH BOTTOM NRC INSPECTION - PROBLEM June 26,

IDENTIFICATION AND RESOLUTION (2019) STATUS 2019

REPORT

MAINTENANCE FUNCTIONAL AREA AUDIT REPORT, February 5

NOSA-PEA-18-01 (AR 4090541) PBAPS to February

16, 2018

SECURITY PROGRAMS AUDIT REPORT, NOSA-PEA-17- January 23

(AR 3958635), PBAPS to January

27, 2017

NCV 50-277 & 50-278/2017-002-01

NCV 50-277 & 50-278/2017-003-01

NCV 50-277 & 50-278/2017-008-01

NCV 50-277 & 50-278/2017-008-02

NCV 50-277 & 50-278/2017-201-01

NCV 50-277 & 50-278/2017-201-02

NCV 50-277 & 50-278/2017-403-01

NCV 50-277 & 50-278/2017-403-01

NCV 50-277 & 50-278/2018-001-01

NCV 50-277 & 50-278/2018-002-01

NCV 50-277 & 50-278/2018-002-01

NCV 50-277 & 50-278/2018-003-01

NCV 50-277 & 50-278/2018-004-01

NCV 50-277 & 50-278/2018-010-01

NCV 50-277 & 50-278/2018-010-02

NCV 50-277 & 50-278/2018-012-01

NCV 50-277 & 50-278/2018-410-01

NCV 50-277 & 50-278/2019-001-01

NCV 50-277 & 50-278/2019-001-02

NCV 50-277 & 50-278/2019-011-01

EA-17-20 (Enforcement Discretion)

EA-18-08 (Enforcement Discretion)

ZONE ALARM HISTORY BY CLEAR CODE 06/24/2019

Procedures CC-AA-102 DESIGN INPUT AND CONFIGURATION CHANGE IMPACT Revision 32

Inspection Type Designation Description or Title Revision or

Procedure Date

SCREENING

EP-AA-112-200- SECURITY COORDINATOR CHECKLIST Revision 32

F-04

MA-AA-716-008 FOREIGN MATERIAL EXCLUSION PROGRAM Revision 14

NO-AA-10 QUALITY ASSURANCE TOPICAL REPORT Revision 94

(QATR)

NO-AA-210 NUCLEAR OVERSIGHT REGULATORY AUDIT Revision 10

PROCEDURE

OP-AA-108-115 OPERABILITY DETERMINATIONS (CM-1) Revision 21

OP-AA-108-115- OPERABILITY EVALUATION PASSPORT ENGINEERING Revision 1

1001 CHANGE DESKTOP GUIDE

OP-AA-108-115- SUPPLEMENTAL CONSIDERATION FOR ON-SHIFT Revision 3

1002 IMMEDIATE

OPERABILITY DETERMINATIONS (CM-1)

OP-PB-102-106 OPERATOR RESPONSE TIME PROGRAM AT PEACH Revision 10

BOTTOM

PI-AA-101 CONDUCT OF PERFORMANCE IMPROVEMENT Revision 1

PI-AA-101-1001 PERFORMANCE MONITORING AND ANALYSIS MANUAL Revision 2

PI-AA-101-1002 PI MANAGEMENT REVIEW MEETINGS AND REPORTING Revision 2

PI-AA-101-1003 PERFORMANCE GAP RESOLUTION Revision 0

PI-AA-115 OPERATING EXPERIENCE PROGRAM Revision 4

PI-AA-115-1001 PROCESSING OF LEVEL 1 OPEX EVALUATIONS Revision 2

PI-AA-115-1001- PRIORITY OF LEGACY IER AND SOER Revision 0

F-01 RECOMMENDATIONS

Inspection Type Designation Description or Title Revision or

Procedure Date

PI-AA-115-1002 PROCESSING OF LEVEL 2 OPEX EVALUATIONS Revision 3

PI-AA-115-1003 PROCESSING OF LEVEL 3 OPEX EVALUATIONS Revision 5

PI-AA-115-1004 PROCESSING OF NER AND ICES REPORTS Revision 6

PI-AA-115-1004- ICES REPORT SCREENING FORM Revision 0

F-03

PI-AA-120 ISSUE IDENTIFICATION AND SCREENING PROCESS Revision 8

PI-AA-125 CORRECTIVE ACTION PROGRAM (CAP) PROCEDURE Revision 6

PI-AA-125-001-F- CAPCO INDOCTRINATION GUIDE Revision 1

PI-AA-125-1001 ROOT CAUSE ANALYSIS MANUAL Revision 3

PI-AA-125-1003 CORRECTIVE ACTION PROGRAM EVALUATION MANUAL Revision 4

PI-AA-125-1004 EFFECTIVENESS REVIEW MANUAL Revision 2

PI-AA-125-1006 INVESTIGATION TECHNIQUES MANUAL Revision 4

PI-AA-126 SELF-ASSESSMENT AND BENCHMARK PROGRAM Revision 2

PI-AA-126-1001 SELF-ASSESSMENTS Revision 2

PI-AA-126-1001- SELF-ASSESSMENT Revision 2

F-01

Inspection Type Designation Description or Title Revision or

Procedure Date

PI-AA-126-1006 BENCHMARK PROGRAM Revision 2

PI-AA-126-1006- BENCHMARK Revision 2

F-01

PI-AA-126-1006- OPPORTUNITY FOR IMPROVEMENT BENCHMARK Revision 0

F-03

PI-AA-127 PASSPORT ACTION TRACKING MANAGEMENT Revision 2

PROCEDURE

RT-S-045-911-2 Precautions, Limitations, and General Instructions Revision 24

ST/LLRT LOCAL LEAK RATE TEST DOCUMENTATION AND REVISION 4

20.00.01 TRACKING

ST/LLRT LOCAL LEAK RATE TEST DOCUMENTATION AND Revision 4

30.00.01 TRACKING

ST/LLRT D/W PURGE SUPPLY (AO-3-07B-3523, CHK-3-07B- Revision 9

30.07B.16 50095A, CHK-3-07B-50095B)

SY-AA-101-122- Performance of Security System Tests Revision 13

1001

SY-PB-101-122- Performance of Security System Tests Revision 1

1001

SY-PB-101-122- Security Weekly Equipment Testing - CAS REvision 1

1001-F-01

WC-AA-106 WORK SCREENING AND PROCESSING Revision 18

Work Orders 0246671

2