ML17223A875: Difference between revisions

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See also: [[followed by::IR 05000335/1990014]]


=Text=
=Text=
{{#Wiki_filter:(ACCELERATED
{{#Wiki_filter:ACCELERATED DISTRIBUTION DEMONSTRATION SYSTEM I (
DISTRIBUTION
            ~
DEMONSTRATION
'                         REGULATORY INFORMATION DISTRIBUTION SYSTEM (R1DS)
SYSTEM I~~'REGULATORY
ACCESSION NBR:9008140504                   DOC.DATE: 90/08/09     NOTARIZED: NO             DOCKET FACIL:50-335 St. Lucie Plant, Unit 1, Florida Power 6 Light Co.
INFORMATION
                                  ~
DISTRIBUTION
                                                                                              ,05000335 AUTH. NAME               AUTHOR AFFILIATION GOLDBERG,J.H.           Florida Power & Light, Co.
SYSTEM (R1DS)ACCESSION NBR:9008140504
RECIP.NAME               RECIPIENT AFFIL1ATION Document Control Branch (Document Control Desk)
DOC.DATE: 90/08/09 NOTARIZED:
 
NO FACIL:50-335
==SUBJECT:==
St.Lucie Plant, Unit 1, Florida Power 6 Light Co.AUTH.NAME AUTHOR AFFILIATION
Responds         to violations noted in Insp Rept 50-335/90-14.
GOLDBERG,J.H.
DISTRIBUTION CODE: IEOID TITLE: General        (50 COPIES RECEIVED:LTR     i ENCL Dkt)-Insp Rept/Notice of VioTation Response   j  SIZE:              D NOTES:
Florida Power&Light, Co.RECIP.NAME
RECIPIENT                COPIES            RECIPIENT             COPIES ID  CODE/NAME            LTTR ENCL        ID CODE/NAME         LTTR ENCL          A PD2-2 PD                     1    1      NORRIS,J                  1    1 INTERNAL: ACRS                               2     2     AEOD                      1   1           D AEOD/DEIIB                    1     1     AEOD/TPAD                1   1 DEDRO                        1     1     NRR MORISSEAU,D          1   1           D NRR SHANKMAN,S                1     1     NRR/DLPQ/LPEB10           1    1 NRR/DOEA DIR 11              1. 1      NRR/DRE P/PE PB9 D       1    1            S NRR/DRIS/DIR                  1    1'    NRR/DST/DIR 8E2          1    1
RECIPIENT AFFIL1ATION
              . NRR/PMAS/ILRB12                    1      NUDOCS-ABSTRACT           1   1 OE .D                        1     1     OGC/HDS2                  1   1 1     1     RGN2    FILE    01      1   1 EXTERNAL: LPDR                              1     1     NRC PDR NSIC                          1     1 D
Document Control Branch (Document Control Desk)SUBJECT: Responds to violations
D D
noted in Insp Rept 50-335/90-14.
NOTE TO ALL "RIDS" RECIPIENTS:
DISTRIBUTION
PLEASE HELP US TO REDUCE O'ASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOiiI Pl-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROiv! DISTRIBUTIOiV LISTS FOR DOCUi>IENTS YOU DON'T NEED!
CODE: IEOID COPIES RECEIVED:LTR
TOTAL NUMBER OF COPIES REQUIRED: LTTR                   24   ENCL     24
i ENCL j SIZE: TITLE: General (50 Dkt)-Insp Rept/Notice
 
of VioTation Response NOTES: DOCKET ,05000335 D RECIPIENT ID CODE/NAME PD2-2 PD INTERNAL: ACRS AEOD/DEIIB
PO.Box 14000,Juno Beach,FL 33408 0420 AUGUST.     9 1990 L-90-291 10 CFR 2.201 U. S.     Nuclear Regulatory Commission Attn:         Document Control Desk Washington,             D. C. 20555 Gentlemen:
DEDRO NRR SHANKMAN,S
Re:       St. Lucie Unit 1 Docket Nos. 50-335 Response to Notice of Violation Ins ection Re ort 90-14 Florida Power and Light Company has reviewed the subject inspection report and pursuant to 10 CFR 2.201 the response is attached.
NRR/DOEA DIR 11 NRR/DRIS/DIR
Very     truly yours,
.NRR/PMAS/ILRB12
":.b WX~~:~
OE.D EXTERNAL: LPDR NSIC COPIES LTTR ENCL 1 1 2 2 1 1 1 1 1 1 1.1 1 1'1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME NORRIS,J AEOD AEOD/TPAD NRR MORISSEAU,D
J; H. Goldberg President Nuclear Division JHG/GRM Attachment                           A cc: Stewart D. Ebneter, Regional Administrator, USNRC Region Senior Resident Inspector, USNRC, St. Lucie Plant II 900-:;,40.".;Ot'C>r>80a>
NRR/DLPQ/LPEB10
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NRR/DRE P/PE PB9 D NRR/DST/DIR
                              >- D>".
8E2 NUDOCS-ABSTRACT
                                                                            +/
OGC/HDS2 RGN2 FILE 01 NRC PDR COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 A D D S D NOTE TO ALL"RIDS" RECIPIENTS:
an FPL Grov>> compacv
D D PLEASE HELP US TO REDUCE O'ASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOiiI Pl-37 (EXT.20079)TO ELIMINATE YOUR NAME FROiv!DISTRIBUTIOiV
 
LISTS FOR DOCUi>IENTS
Re:   St. Lucie Units 1 Docket Nos. 50-335 Response to Notice of Violation Ins ection Re ort 90-14 FINDING:
YOU DON'T NEED!TOTAL NUMBER OF COPIES REQUIRED: LTTR 24 ENCL 24  
.Unit 1 Technical Specification (TS) 6.8.1.a requires that written procedures shall be established,           implemented and maintained covering the activities recommended in Appendix A of Regulatory Guide 1.33, Revision 2, February 1978. Appendix A, paragraph 1.d, includes procedures addressing procedure adherence and temporary change method.
PO.Box 14000,Juno
Procedure     QI   5-PR/PSL-l,     Rev   37,   Preparation,               Revision, Review/Approval of Procedures, section 5.5, implemented TS 6.8.1 and required that procedures be strictly adhered to.
Beach,FL 33408 0420 AUGUST.9 1990 L-90-291 10 CFR 2.201 U.S.Nuclear Regulatory
provided the method to obtain approved temporary procedure changes It also and,   if appropriate, subsequent permanent changes.
Commission
Procedure     OP- 1-0120051,   Rev   10, RCS   Flow               Determination   by Calorimetric Procedure, steps 8.3 through 8.6, directed certain action sequences involving coordination with the Reactor Control Operator at the control board, control board loop temperature meter function selection using switches,               and               confirmation that measurements were being made =only on channels that had the meter switched out and isolated.
Attn: Document Control Desk Washington, D.C.20555 Gentlemen:
Cont'rary to the above, on May 14, 1990, During the performance of procedure OP 1-0120051, the licensee's staff did not follow instruction steps 8.3 through 8.6 The test persons instead utilized an unapproved method to isolate all the meters to simultaneously isolate the involved loop temperature meters and complete the data collection without. the described coordination.
Re: St.Lucie Unit 1 Docket Nos.50-335 Response to Notice of Violation Ins ection Re ort 90-14 Florida Power and Light Company has reviewed the subject inspection
 
report and pursuant to 10 CFR 2.201 the response is attached.Very truly yours,":.b WX~~:~J;H.Goldberg President-Nuclear Division JHG/GRM Attachment
===RESPONSE===
A cc: Stewart D.Ebneter, Regional Administrator, USNRC Region II Senior Resident Inspector, USNRC, St.Lucie Plant900-:;,40.".;Ot'C>r>80a>
Florida   Power and Light   Company   concurs with the               violation.
F'1:<AZ>GCc,'-C~i>j>.".:;:
2 ~  The reason   for the violation was failure to follow QI 5-PR/PSL-1. Test personnel failed to process a Procedure Change Request (PCR) prior to,implementing an improved method of collecting the temperature data.
>-D>".an FPL Grov>>compacv+/
3 ~  The Reactor Coolant System flow     determination by calorimetric               .
Re: St.Lucie Units 1 Docket Nos.50-335 Response to Notice of Violation Ins ection Re ort 90-14 FINDING:.Unit 1 Technical Specification (TS)6.8.1.a requires that written procedures
procedure was repeated with         the individual's supervisor observing.
shall be established, implemented
4,   The following actions have     been implemented               to avoid further violations:
and maintained
: a. The individual   was   counselled by his   supervisor.'.
covering the activities
A PCR was submitted to clarify and authorize the 'improved method of data collection.
recommended
 
in Appendix A of Regulatory
Re: St. Lucie Units 1 Docket Nos. 50-335 Response to Notice of Violation Ins ection Re ort 90-14
Guide 1.33, Revision 2, February 1978.Appendix A, paragraph 1.d, includes procedures
: c. All individuals in the Test Group were reminded of the importance of following procedures and the need for processing a PCR and/or a Temporary Change (TC) followed by a PCR prior to implementation of the change.
addressing
: 5. All the corrective actions were completed by August 1, 1990.}}
procedure adherence and temporary change method.Procedure QI 5-PR/PSL-l, Rev 37, Preparation, Revision, Review/Approval
of Procedures, section 5.5, implemented
TS 6.8.1 and required that procedures
be strictly adhered to.It also provided the method to obtain approved temporary procedure changes and, if appropriate, subsequent
permanent changes.Procedure OP-1-0120051, Rev 10, RCS Flow Determination
by Calorimetric
Procedure, steps 8.3 through 8.6, directed certain action sequences involving coordination
with the Reactor Control Operator at the control board, control board loop temperature
meter function selection using switches, and confirmation
that measurements
were being made=only on channels that had the meter switched out and isolated.Cont'rary to the above, on May 14, 1990, During the performance
of procedure OP 1-0120051, the licensee's
staff did not follow instruction
steps 8.3 through 8.6 The test persons instead utilized an unapproved
method to isolate all the meters to simultaneously
isolate the involved loop temperature
meters and complete the data collection
without.the described coordination.
RESPONSE: 2~3~Florida Power and Light Company concurs with the violation.
The reason for the violation was failure to follow QI 5-PR/PSL-1.Test personnel failed to process a Procedure Change Request (PCR)prior to,implementing
an improved method of collecting
the temperature
data.The Reactor Coolant System flow determination
by calorimetric
.procedure was repeated with the individual's
supervisor
observing.
4, The following actions have been implemented
to avoid further violations:
a.The individual
was counselled
by his supervisor.'.
A PCR was submitted to clarify and authorize the'improved method of data collection.  
Re: St.Lucie Units 1 Docket Nos.50-335 Response to Notice of Violation Ins ection Re ort 90-14 c.All individuals
in the Test Group were reminded of the importance
of following procedures
and the need for processing
a PCR and/or a Temporary Change (TC)followed by a PCR prior to implementation
of the change.5.All the corrective
actions were completed by August 1, 1990.
}}

Latest revision as of 22:50, 29 October 2019

Responds to Violations Noted in Insp Rept 50-335/90-14. Corrective Actions:Rcs Flow Determination by Calorimetric Procedure Repeated W/Supervisor of Individual Observing & Individual Counseled by Supervisor
ML17223A875
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 08/09/1990
From: Goldberg J
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
L-90-291, NUDOCS 9008140504
Download: ML17223A875 (5)


Text

ACCELERATED DISTRIBUTION DEMONSTRATION SYSTEM I (

~

' REGULATORY INFORMATION DISTRIBUTION SYSTEM (R1DS)

ACCESSION NBR:9008140504 DOC.DATE: 90/08/09 NOTARIZED: NO DOCKET FACIL:50-335 St. Lucie Plant, Unit 1, Florida Power 6 Light Co.

~

,05000335 AUTH. NAME AUTHOR AFFILIATION GOLDBERG,J.H. Florida Power & Light, Co.

RECIP.NAME RECIPIENT AFFIL1ATION Document Control Branch (Document Control Desk)

SUBJECT:

Responds to violations noted in Insp Rept 50-335/90-14.

DISTRIBUTION CODE: IEOID TITLE: General (50 COPIES RECEIVED:LTR i ENCL Dkt)-Insp Rept/Notice of VioTation Response j SIZE: D NOTES:

RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL A PD2-2 PD 1 1 NORRIS,J 1 1 INTERNAL: ACRS 2 2 AEOD 1 1 D AEOD/DEIIB 1 1 AEOD/TPAD 1 1 DEDRO 1 1 NRR MORISSEAU,D 1 1 D NRR SHANKMAN,S 1 1 NRR/DLPQ/LPEB10 1 1 NRR/DOEA DIR 11 1. 1 NRR/DRE P/PE PB9 D 1 1 S NRR/DRIS/DIR 1 1' NRR/DST/DIR 8E2 1 1

. NRR/PMAS/ILRB12 1 NUDOCS-ABSTRACT 1 1 OE .D 1 1 OGC/HDS2 1 1 1 1 RGN2 FILE 01 1 1 EXTERNAL: LPDR 1 1 NRC PDR NSIC 1 1 D

D D

NOTE TO ALL "RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE O'ASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOiiI Pl-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROiv! DISTRIBUTIOiV LISTS FOR DOCUi>IENTS YOU DON'T NEED!

TOTAL NUMBER OF COPIES REQUIRED: LTTR 24 ENCL 24

PO.Box 14000,Juno Beach,FL 33408 0420 AUGUST. 9 1990 L-90-291 10 CFR 2.201 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Gentlemen:

Re: St. Lucie Unit 1 Docket Nos. 50-335 Response to Notice of Violation Ins ection Re ort 90-14 Florida Power and Light Company has reviewed the subject inspection report and pursuant to 10 CFR 2.201 the response is attached.

Very truly yours,

":.b WX~~:~

J; H. Goldberg President Nuclear Division JHG/GRM Attachment A cc: Stewart D. Ebneter, Regional Administrator, USNRC Region Senior Resident Inspector, USNRC, St. Lucie Plant II 900-:;,40.".;Ot'C>r>80a>

F'1: < AZ>GCc,'- C~i>j>.".:;:

>- D>".

+/

an FPL Grov>> compacv

Re: St. Lucie Units 1 Docket Nos. 50-335 Response to Notice of Violation Ins ection Re ort 90-14 FINDING:

.Unit 1 Technical Specification (TS) 6.8.1.a requires that written procedures shall be established, implemented and maintained covering the activities recommended in Appendix A of Regulatory Guide 1.33, Revision 2, February 1978. Appendix A, paragraph 1.d, includes procedures addressing procedure adherence and temporary change method.

Procedure QI 5-PR/PSL-l, Rev 37, Preparation, Revision, Review/Approval of Procedures, section 5.5, implemented TS 6.8.1 and required that procedures be strictly adhered to.

provided the method to obtain approved temporary procedure changes It also and, if appropriate, subsequent permanent changes.

Procedure OP- 1-0120051, Rev 10, RCS Flow Determination by Calorimetric Procedure, steps 8.3 through 8.6, directed certain action sequences involving coordination with the Reactor Control Operator at the control board, control board loop temperature meter function selection using switches, and confirmation that measurements were being made =only on channels that had the meter switched out and isolated.

Cont'rary to the above, on May 14, 1990, During the performance of procedure OP 1-0120051, the licensee's staff did not follow instruction steps 8.3 through 8.6 The test persons instead utilized an unapproved method to isolate all the meters to simultaneously isolate the involved loop temperature meters and complete the data collection without. the described coordination.

RESPONSE

Florida Power and Light Company concurs with the violation.

2 ~ The reason for the violation was failure to follow QI 5-PR/PSL-1. Test personnel failed to process a Procedure Change Request (PCR) prior to,implementing an improved method of collecting the temperature data.

3 ~ The Reactor Coolant System flow determination by calorimetric .

procedure was repeated with the individual's supervisor observing.

4, The following actions have been implemented to avoid further violations:

a. The individual was counselled by his supervisor.'.

A PCR was submitted to clarify and authorize the 'improved method of data collection.

Re: St. Lucie Units 1 Docket Nos. 50-335 Response to Notice of Violation Ins ection Re ort 90-14

c. All individuals in the Test Group were reminded of the importance of following procedures and the need for processing a PCR and/or a Temporary Change (TC) followed by a PCR prior to implementation of the change.
5. All the corrective actions were completed by August 1, 1990.