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| issue date = 12/31/1996
| issue date = 12/31/1996
| title = Monthly Operating Repts for Dec 1996 for Surry Power Station Units 1 & 2.W/970110 Ltr
| title = Monthly Operating Repts for Dec 1996 for Surry Power Station Units 1 & 2.W/970110 Ltr
| author name = FANGUY M J, MASON M J, SARVER S P
| author name = Fanguy M, Mason M, Sarver S
| author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
| author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
| addressee name =  
| addressee name =  
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:-*~ l -*----. . . t.., VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 January 10, 1997 United States Nuclear Regulatory Commission Attention:
{{#Wiki_filter:*~
Document Control Desk Washington, D.C. 20555 Gentlemen:
l -*----. .. t..,
VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION UNITS 1 AND 2 MONTHLY OPERATING REPORT Serial No. 97-020 NURPC Docket Nos. 50-280 50-281 License Nos. DPR-32 DPR-37 Enclosed is the Monthly Operating Report for Surry Power Station Units 1 and 2 for the month of December 1996. If you have any questions or require additional information, please contact us. Very truly yours, S. P. Sarver, Acting Manager Nuclear Licensing and Operations Support Enclosure cc: U. S. Nuclear Regulatory Commission Region II 101 Marietta Street, N.W. Suite 2900 Atlanta, Georgia 30323 Mr. R. A. Musser NRC Senior Resident Inspector Surry Power Station .,-----9701220318 961231 ' PD R ADOCK 05000280 ~---~-I I R PDR l 0~)on "-*-u39
VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 January 10, 1997 United States Nuclear Regulatory Commission                       Serial No. 97-020 Attention: Document Control Desk                                 NURPC Washington, D.C. 20555                                           Docket Nos. 50-280 50-281 License Nos. DPR-32 DPR-37 Gentlemen:
-VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION MONTHLY OPERATING REPORT REPORT No. 96-12 Approved:  
VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION UNITS 1 AND 2 MONTHLY OPERATING REPORT Enclosed is the Monthly Operating Report for Surry Power Station Units 1 and 2 for the month of December 1996.
~S)G_{l Station Manager TABLE OF CONTENTS Section tl'8urry-Monthly Operating Report No. 96-12 Page 2 of 22 Page Operating Data Report -Unit No. 1 ............................................................................................................................
If you have any questions or require additional information, please contact us.
3 Operating Data Report -Unit No. 2 ............................................................................................................................
Very truly yours, S. P. Sarver, Acting Manager Nuclear Licensing and Operations Support Enclosure cc:     U. S. Nuclear Regulatory Commission Region II 101 Marietta Street, N.W.
4 Unit Shutdowns and Power Reductions  
Suite 2900 Atlanta, Georgia 30323 Mr. R. A. Musser NRC Senior Resident Inspector Surry Power Station
-Unit No. 1 ..................................................................................................
                                                    ~---~-
5 Unit Shutdowns and Power Reductions  
                .,-----9701220318 961231 '
-Unit No. 2 ..................................................................................................
I PD R
6 Average Daily Unit Power Level -Unit No. 1 .............................................................................................................
ADOCK 05000280 PDR I
7 Average Daily Unit Power Level -Unit No. 2 .............................................................................................................
l 0~)on
8 Summary of Operating Experience  
          "-*-       u39
-Unit No. 1 .........................................................................................................
 
9 Summary of Operating Experience  
VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION MONTHLY OPERATING REPORT REPORT No.     96-12 Approved:
-Unit No. 2 .........................................................................................................
          ~S)G_{l Station Manager
9 Facility Changes That Did Not Require NRC Approval ............................................................................................
 
10 Procedure or Method of Operation Changes That Did Not Require NRC Approval.  
tl'8urry-Monthly Operating Report No. 96-12 Page 2 of 22 TABLE OF CONTENTS Section                                                                                                                                                          Page Operating Data Report - Unit No. 1 ............................................................................................................................ 3 Operating Data Report - Unit No. 2 ............................................................................................................................ 4 Unit Shutdowns and Power Reductions - Unit No. 1 .................................................................................................. 5 Unit Shutdowns and Power Reductions - Unit No. 2 .................................................................................................. 6 Average Daily Unit Power Level - Unit No. 1 ............................................................................................................. 7 Average Daily Unit Power Level - Unit No. 2 ............................................................................................................. 8 Summary of Operating Experience - Unit No. 1 ......................................................................................................... 9 Summary of Operating Experience - Unit No. 2 ......................................................................................................... 9 Facility Changes That Did Not Require NRC Approval ............................................................................................ 10 Procedure or Method of Operation Changes That Did Not Require NRC Approval. ................................................ 16 Tests and Experiments That Did Not Require NRC Approval .................................................................................. 18 Chemistry Report ..................................................................................................................................................... 19 Fuel Handling - Unit No. 1 ........................................................................................................................................ 20 Fuel Handling - Unit No. 2 ........................................................................................................................................ 20 Description of Periodic Test(s) Which Were Not Completed Within the Time Limits Specified in Technical Specifications ....................................................................................................................... 22
................................................
 
16 Tests and Experiments That Did Not Require NRC Approval ..................................................................................
                                                                                                - Surry Monthly Operating Report No. 96-12 Page 3 of 22 OPERATING DATA REPORT Docket No.:  50-280 Date:  01/01/97 Completed By:   D. K. Mason Telephone:    (804) 365-2459
18 Chemistry Report .....................................................................................................................................................
: 1. Unit Name: ........................................................... Surry Unit 1
19 Fuel Handling -Unit No. 1 ........................................................................................................................................
: 2. Reporting Period: ................................................ . December, 1996
20 Fuel Handling -Unit No. 2 ........................................................................................................................................
: 3. Licensed Thermal Power (MWt): ......................... .                   2546
20 Description of Periodic Test(s) Which Were Not Completed Within the Time Limits Specified in Technical Specifications  
: 4. Nameplate Rating (Gross MWe): ........................ .                    847.5
.......................................................................................................................
: 5. Design Electrical Rating (Net MWe): ................... .                   788
22 OPERATING DATA REPORT -Surry Monthly Operating Report Docket No.: Date: 50-280 01/01/97 No. 96-12 Page 3 of 22 Completed By: D. K. Mason (804) 365-2459 1. Unit Name: .......................................................... . 2. Reporting Period: ................................................ . 3. Licensed Thermal Power (MWt): ......................... . 4. Nameplate Rating (Gross MWe): ........................ . 5. Design Electrical Rating (Net MWe): ................... . 6. Maximum Dependable Capacity (Gross MWe): .. . 7. Maximum Dependable Capacity (Net MWe): ...... . Surry Unit 1 December, 1996 2546 847.5 788 840 801 Telephone:
: 6. Maximum Dependable Capacity (Gross MWe): .. .                               840
: 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons: 9. Power Level To Which Restricted, If Any (Net MWe): 10. Reasons For Restrictions, If Any: This Month YTD Cumulative
: 7. Maximum Dependable Capacity (Net MWe): ...... .                             801
: 11. Hours In Reporting Period ...............................
: 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
744.0 8784.0 210624.0 12. Number of Hours Reactor Was Critical ...........
: 9. Power Level To Which Restricted, If Any (Net MWe):
744.0 8784.0 146834.7 13. Reactor Reserve Shutdown Hours ..................
: 10. Reasons For Restrictions, If Any:
0.0 0.0 3774.5 14. Hours Generator On-Line ................................
This Month             YTD               Cumulative
744.0 8784.0 144531.0 15. Unit Reserve Shutdown Hours ........................
: 11. Hours In Reporting Period ...............................                   744.0             8784.0             210624.0
0.0 0.0 3736.2 16. Gross Thermal Energy Generated (MWH) ...... 1892818.6 22237651.3 338635443.8
: 12. Number of Hours Reactor Was Critical ...........                             744.0             8784.0             146834.7
: 17. Gross Electrical Energy Generated (MWH) ..... 633235.0 7395635.0 110972818.0
: 13. Reactor Reserve Shutdown Hours ..................                             0.0                 0.0             3774.5
: 18. Net Electrical Energy Generated (MWH) .........
: 14. Hours Generator On-Line ................................                     744.0             8784.0             144531.0
610120.0 7137776.0 105593749.0
: 15. Unit Reserve Shutdown Hours ........................                           0.0                 0.0             3736.2
: 19. Unit Service Factor ..........................................
: 16. Gross Thermal Energy Generated (MWH) ......                             1892818.6         22237651.3           338635443.8
100.0% 100.0% 68.6% 20. Unit Availability Factor. ....................................
: 17. Gross Electrical Energy Generated (MWH) .....                           633235.0           7395635.0         110972818.0
100.0% 100.0% 70.4% 21. Unit Capacity Factor (Using MDC Net) ............
: 18. Net Electrical Energy Generated (MWH) .........                         610120.0           7137776.0         105593749.0
102.4% 101.4% 64.5% 22. Unit Capacity Factor (Using DER Net) ............
: 19. Unit Service Factor ..........................................               100.0%             100.0%                 68.6%
104.1% 103.1% 63.6% 23. Unit Forced Outage Rate ................................
: 20. Unit Availability Factor. ....................................               100.0%             100.0%                 70.4%
0.0% 0.0% 15.2% 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each): Refueling, March 6, 1997, 37 Days 25. If Shut Down at End of Report Period, Estimated Date of Start-up:
: 21. Unit Capacity Factor (Using MDC Net) ............                           102.4%             101.4%                 64.5%
N/A 26. Unit In Test Status (Prior to Commercial Operation):
: 22. Unit Capacity Factor (Using DER Net) ............                           104.1%             103.1%                 63.6%
FORECAST ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION
: 23. Unit Forced Outage Rate ................................                       0.0%                 0.0%               15.2%
'-* OPERATING DATA REPORT -Surry Monthly Operating Report Docket No.: Date: 50-281 01-01-97 No. 96-12 Page 4 of 22 Completed By: D. K. Mason {804) 365-2459 1. Unit Name: .......................................................... . 2. Reporting Period: ................................................ . 3. Licensed Thermal Power (MWt): ......................... . 4. Nameplate Rating (Gross MWe): ........................ . 5. Design Electrical Rating (Net MWe): ................... . 6. Maximum Dependable Capacity (Gross MWe): .. . 7. Maximum Dependable Capacity (Net MWe): ...... . Surry Unit 2 December, 1996 2546 847.5 788 840 801 Telephone:
: 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
: 8. If Changes Occur in Capacity Ratings {Items Number 3 Through 7) Since Last Report, Give Reasons: 9. Power Level To Which Restricted, If Any (Net MWe): 10. Reasons For Restrictions, If Any: This Month YTD Cumulative
Refueling, March 6, 1997, 37 Days
: 11. Hours In Reporting Period ...............................
: 25. If Shut Down at End of Report Period, Estimated Date of Start-up:                                       N/A
744.0 8784.0 207504.0 12. Number of Hours Reactor Was Critical ...........
: 26. Unit In Test Status (Prior to Commercial Operation):
502.5 7572.7 143075.6 13. Reactor Reserve Shutdown Hours ..................
FORECAST             ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION
0.0 0.0 328.1 14. Hours Generator On-Line ................................
 
493.6 7541.7 141097.8 15. Unit Reserve Shutdown Hours ........................
                                      *                                                           - Surry Monthly Operating Report No. 96-12 Page 4 of 22 OPERATING DATA REPORT Docket No.:   50-281 Date:  01-01-97 Completed By:   D. K. Mason Telephone:    {804) 365-2459
0.0 0.0 0.0 16. Gross Thermal Energy Generated (MWH) ...... 1238394.8 18939202.8 331474256.8
: 1. Unit Name: .......................................................... . Surry Unit 2
: 17. Gross Electrical Energy Generated (MWH) ..... 415495.0 6295155.0 108450799.0
: 2. Reporting Period: ................................................ . December, 1996
: 18. Net Electrical Energy Generated (MWH) .........
: 3. Licensed Thermal Power (MWt): ......................... .                   2546
401148.0 6081464.0 103191879.0
: 4. Nameplate Rating (Gross MWe): ........................ .                      847.5
: 19. Unit Service Factor ..........................................
: 5. Design Electrical Rating (Net MWe): ................... .                     788
66.3% 85.9% 68.0% 20. Unit Availability Factor .....................................
: 6. Maximum Dependable Capacity (Gross MWe): .. .                                 840
66.3% 85.9% 68.0% 21. Unit Capacity Factor (Using MDC Net) ............
: 7. Maximum Dependable Capacity (Net MWe): ...... .                               801
67.3% 86.4% 63.7% 22. Unit Capacity Factor (Using DER Net) ............
: 8. If Changes Occur in Capacity Ratings {Items Number 3 Through 7) Since Last Report, Give Reasons:
68.4% 87.9% 63.1% 23. Unit Forced Outage Rate ................................
: 9. Power Level To Which Restricted, If Any (Net MWe):
0.0% 1.7% 12.5% 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each): 25. If Shut Down at End of Report Period, Estimated Date of Start-up:
: 10. Reasons For Restrictions, If Any:
N/A 26. Unit In Test Status (Prior to Commercial Operation):
This Month             YTD               Cumulative
FORECAST ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION
: 11. Hours In Reporting Period ...............................                     744.0             8784.0             207504.0
-Surry Monthly Operating Report No. 96-12 Page 5 of 22 UNIT SHUTDOWN AND POWER REDUCTION (1) (2) (EQUAL To OR GREATER THAN 20%) REPORT MONTH: December, 1996 (3) Method (4) (5) Docket No.: 50-280 Unit Name: Surry Unit 1 Date: 01-02-97 Completed by: M. J. Fanguy Telephone:
: 12. Number of Hours Reactor Was Critical ...........                             502.5             7572.7             143075.6
(804) 365-2155 Duration of LER . System _ Component Cause & Corrective Action to Date Type Hours Reason Shutting No. Code Code Prevent Recurrence (1) F: Forced S: Scheduled (4) (2) REASON: Down Rx None During the Reporting Period A -Equipment Failure (Explain)
: 13. Reactor Reserve Shutdown Hours ..................                             0.0                 0.0               328.1
B Maintenance or Test C Refueling D Regulatory Restriction E Operator Training & Licensing Examination F Administrative G Operational Error (Explain)
: 14. Hours Generator On-Line ................................                     493.6             7541.7             141097.8
Exhibit G -Instructions for Preparation of Data Entry Sheets for Licensee Event Report (LER) File (NU REG 0161) (3) METHOD: 1 -Manual 2 -Manual Scram 3 -Automatic Scram 4 -Other (Explain)
: 15. Unit Reserve Shutdown Hours ........................                           0.0                 0.0                   0.0
(5) Exhibit 1 -Same Source (1) --(2) Surry-Monthly Operating Report No. 96-12 Page 6 of 22 UNIT SHUTDOWN AND POWER REDUCTION
: 16. Gross Thermal Energy Generated (MWH) ......                             1238394.8         18939202.8           331474256.8
{EQUAL To OR GREATER THAN 20%} REPORT MONTH: December, 1996 (3) Method (4) Docket No.: 50-281 Unit Name: Surry Unit 2 Date: 01-02-97 Completed by: M. J. Fanguy Telephone:
: 17. Gross Electrical Energy Generated (MWH) .....                             415495.0           6295155.0           108450799.0
(804) 365-2155 (5) Duration of LER No. System Component Cause & Corrective Action to Date Type Hours Reason Shutting Code Code Prevent Recurrence 12/12/96 s 250.4 (1) F: Forced S: Scheduled B (2) REASON: Down Rx 3 96-006 A Equipment Failure (Explain)
: 18. Net Electrical Energy Generated (MWH) .........                           401148.0           6081464.0           103191879.0
B Maintenance or Test C Refueling D Regulatory Restriction SJ E Operator Training & Licensing Examination F Administrative G Operational Error (Explain)
: 19. Unit Service Factor ..........................................                 66.3%               85.9%               68.0%
(4) Exhibit G -Instructions for Preparation of Data Entry Sheets for Licensee Event Report (LER) File (NU REG 0161) NA Scheduled maintenance outage to repair the letdown line (had automatic Rx trip from 11 % power due to steam flow/feed flow mismatch with low level on "A" SG). (3) METHOD: 1 -Manual 2 -Manual Scram 3 -Automatic Scram 4 -Other (Explain)
: 20. Unit Availability Factor .....................................                 66.3%               85.9%               68.0%
(5) Exhibit 1 -Same Source 
: 21. Unit Capacity Factor (Using MDC Net) ............                             67.3%               86.4%               63.7%
'* --. Surry Monthly Operating Report No. 96-12 Page 7 of 22 AVERAGE DAILY UNIT POWER LEVEL Docket No.: 50-280 Unit Name: Surry Unit 1 Date: 01-05-97 Completed by: J. D. Kilmer Telephone:
: 22. Unit Capacity Factor (Using DER Net) ............                             68.4%               87.9%               63.1%
(804) 365-2792 MONTH: December, 1996 Average Daily Power Level Average Daily Power Level Day (MWe -Net) Day (MWe -Net) 824 17 821 2 824 18 819 3 813 19 819 4 821 20 813 5 822 21 802 6 826 22 799 7 824 23 815 8 824 24 820 9 821 25 823 10 824 26 820 11 823 27 822 12 825 28 823 13 820 29 823 14 820 30 824 15 822 31 824 16 822 INSTRUCTIONS On this format, list the average daily unit power level in MWe -Net for each day in the reporting month. Compute to the nearest whole megawatt.
: 23. Unit Forced Outage Rate ................................                       0.0%               1.7%               12.5%
_____J J ~urry Monthly Operating Report No. 96-12 Page 8 of 22 AVERAGE DAILY UNIT POWER LEVEL MONTH: December, 1996 Average Daily Power Level Day 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 INSTRUCTIONS (MWe -Net) 822 821 824 826 827 827 828 828 827 827 828 801 5 0 0 0 Day 17 18 19 20 21 22 23 24 25 26 27 28 29 30 31 Docket No.: 50-281 Unit Name: Surry Unit 2 Date: 01-05-97 Completed by: John D. Kilmer Telephone:
: 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
(804) 365-2792 Average Daily Power Level (MWe -Net) 0 0 0 0 0 0 203 818 825 826 826 825 825 825 825 On this format, list the average daily unit power level in MWe -Net for each day in the reporting month. Compute to the nearest whole megawatt. 
: 25. If Shut Down at End of Report Period, Estimated Date of Start-up:                                         N/A
: 26. Unit In Test Status (Prior to Commercial Operation):
FORECAST             ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION
 
                                                                                  - Surry Monthly Operating Report No. 96-12 Page 5 of 22 UNIT SHUTDOWN AND POWER REDUCTION (EQUAL To OR GREATER THAN   20%)
REPORT MONTH:   December, 1996 Docket No.:   50-280 Unit Name:   Surry Unit 1 Date: 01-02-97 Completed by:   M. J. Fanguy Telephone:   (804) 365-2155 (1)                  (2)        (3)                  (4)        (5)
Method Duration                  of      LER    . System _Component      Cause & Corrective Action to Date     Type     Hours     Reason     Shutting     No.       Code       Code       Prevent Recurrence Down Rx None During the Reporting Period (1)                           (2)                                                    (3)
F:   Forced                 REASON:                                              METHOD:
S:   Scheduled               A - Equipment Failure (Explain)                       1 - Manual B     Maintenance or Test                             2 - Manual Scram C     Refueling                                       3 - Automatic Scram D     Regulatory Restriction                         4 - Other (Explain)
E     Operator Training & Licensing Examination F     Administrative G     Operational Error (Explain)
(4)                                                                                  (5)
Exhibit G - Instructions for Preparation of Data Entry Sheets                     Exhibit 1 - Same Source for Licensee Event Report (LER) File (NU REG 0161)
 
                                -                                               - Surry-Monthly Operating Report No. 96-12 Page 6 of 22 UNIT SHUTDOWN AND POWER REDUCTION
{EQUAL To OR GREATER THAN 20%}
REPORT MONTH: December, 1996 Docket No.:   50-281 Unit Name:   Surry Unit 2 Date: 01-02-97 Completed by:   M. J. Fanguy Telephone:   (804) 365-2155 (1)                (2)        (3)                (4)        (5)
Method Duration                 of     LER No. System Component Cause & Corrective Action to Date     Type     Hours     Reason     Shutting             Code       Code       Prevent Recurrence Down Rx 12/12/96       s     250.4       B           3       96-006     SJ        NA        Scheduled        maintenance outage to repair the letdown line (had automatic Rx trip from 11 % power due to steam      flow/feed    flow mismatch with low level on "A" SG).
(1)                          (2)                                                  (3)
F:  Forced                  REASON:                                            METHOD:
S:  Scheduled              A    Equipment Failure (Explain)                  1 - Manual B    Maintenance or Test                          2 - Manual Scram C     Refueling                                     3 - Automatic Scram D     Regulatory Restriction                       4 - Other (Explain)
E     Operator Training & Licensing Examination F     Administrative G     Operational Error (Explain)
(4)                                                                                 (5)
Exhibit G - Instructions for Preparation of Data Entry Sheets                   Exhibit 1 - Same Source for Licensee Event Report (LER) File (NU REG 0161)
 
                                    -                                                  -  Surry Monthly Operating
                                                                                                                . Report No. 96-12 Page 7 of 22 AVERAGE DAILY UNIT POWER LEVEL Docket No.:   50-280 Unit Name:  Surry Unit 1 Date:  01-05-97 Completed by:    J. D. Kilmer Telephone:  (804) 365-2792 MONTH:      December, 1996 Average Daily Power Level                        Average Daily Power Level Day                    (MWe - Net)                 Day                  (MWe - Net) 824                      17                        821 2                        824                      18                        819 3                        813                      19                        819 4                        821                      20                        813 5                        822                      21                        802 6                        826                      22                       799 7                        824                      23                        815 8                        824                      24                        820 9                        821                      25                        823 10                        824                      26                        820 11                        823                      27                        822 12                        825                      28                        823 13                        820                      29                        823 14                        820                      30                        824 15                        822                      31                        824 16                        822 INSTRUCTIONS On this format, list the average daily unit power level in MWe - Net for each day in the reporting month. Compute to the nearest whole megawatt.
_____J
 
                                                                                      ~urry Monthly Operating Report J                                                                                                             No. 96-12 Page 8 of 22 AVERAGE DAILY UNIT POWER LEVEL Docket No.:   50-281 Unit Name:  Surry Unit 2 Date: 01-05-97 Completed by:    John D. Kilmer Telephone:  (804) 365-2792 MONTH:      December, 1996 Average Daily Power Level                         Average Daily Power Level Day                   (MWe - Net)                 Day                 (MWe - Net) 822                      17                         0 2                        821                     18                         0 3                       824                      19                         0 4                       826                      20                         0 5                       827                      21                         0 6                       827                      22                         0 7                       828                      23                       203 8                       828                      24                       818 9                       827                      25                       825 10                       827                      26                       826 11                       828                      27                       826 12                       801                      28                        825 13                         5                      29                       825 14                         0                      30                       825 15                         0                      31                       825 16                         0 INSTRUCTIONS On this format, list the average daily unit power level in MWe - Net for each day in the reporting month. Compute to the nearest whole megawatt.
 
                                                                                  . .urry Monthly Operating Report No. 96-12 Page 9 of 22


==SUMMARY==
==SUMMARY==
OF OPERATING EXPERIENCE MONTHNEAR:
OF OPERATING EXPERIENCE MONTHNEAR:   December, 1996 The following chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents.
December, 1996 .. urry Monthly Operating Report No. 96-12 Page 9 of 22 The following chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents.
UNIT ONE:
UNIT ONE: 12/01/96 12/03/96 12/31/96 UNIT Two: 12/01/96 12/03/96 12/12/96 12/13/96 12/23/96 12/24/96 12/31/96 0000 0925 The reporting period began with the unit operating at 100% power, 850 MWe. Start power reduction to change out E/P controller for 1-FW-FCV-1478.
12/01/96       0000       The reporting period began with the unit operating at 100% power, 850 MWe.
1017 Stopped power reduction at 90%, 770 MWe. 1206 Started power increase.
12/03/96        0925        Start power reduction to change out E/P controller for 1-FW-FCV-1478.
1345 Stopped power increase at 100%, 850 MWe. 2400 0000 1538 2102 0235 0255 The reporting period ended with the unit operating at 100% power, 855 MWe. The reporting period began with the unit operating at 99% power, 850 MWe. Unit returned to 100% power, Computer calorimetric operable after failed Feedwater RTD replaced.
1017       Stopped power reduction at 90%, 770 MWe.
Started power reduction in preparation for planned outage to repair the letdown line. Auto Reactor Trip from 11 % power due to steam flow/feed flow mismatch with low steam generator water level in the "A" steam generator.
1206       Started power increase.
Commence Reactor Startup. 0348 Reactor critical.
1345       Stopped power increase at 100%, 850 MWe.
1243 Unit on line, start power increase.
12/31/96        2400       The reporting period ended with the unit operating at 100% power, 855 MWe.
1548 2400 Stopped power increase at 100%, 858 MWe. The reporting period ended with the unit operating at 100% power, 855 MWe.
UNIT Two:
FS 96-44 TM S2-96-28 FS 96-47 FS 96-49 -urry Monthly Operating Report No. 96-12 Page 10 of 22 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR:
12/01/96        0000        The reporting period began with the unit operating at 99% power, 850 MWe.
December, 1996 Updated Final Safety Analysis Report Change (Safety Evaluation 96-150) 12-02-96 Section 14.3.2 of the UFSAR discusses the rupture of a main steam pipe. Questions have been raised about what is meant by the term "main steam lines." This change adds information to clarify what is meant by the term "main steam lines." Since this change is clarification of existing information only, no change to the meaning or intent of the UFSAR will be made. Therefore, an unreviewed safety question does not exist. Temporary Modification 12-3-96 (Safety Evaluation No. 95-005 Rev.1) Temporary Modification (TM) S2-96-28 installed a replacement resistance temperature device (RTD) in the local temperature indicator thermowell to provide the Unit 2 Steam Generator (SG) "8" inlet feedwater temperature.
12/03/96        1538        Unit returned to 100% power, Computer calorimetric operable after failed Feedwater RTD replaced.
The local temperature indicator thermowell is of the same design as the main RTD thermowell, except for length. An evaluation of this difference concluded, based on a comparison of previous temperature data, that a reliable and accurate indication of the SG "B" inlet feedwater temperature can be obtained.
12/12/96        2102        Started power reduction in preparation for planned outage to repair the letdown line.
This modification did not reduce the Technical Specifications margin of safety. Therefore, an unreviewed safety question does not exist. -Updated Final Safety Analysis Report Change (Safety Evaluation 96-154) 12-5-96 Currently, a note in UFSAR Table 6.2-2 and Section 6.2.2.1.1 states "any of the listed motor operated valves will actuate a combination light and alarm when one or more SIS valves are out of position." This does not accurately reflect actual plant control room indication, since not all of the SIS valves listed will actuate the "SIS Valves Out Of Position" alarm. A review of the SI Design Basis Document and the applicable General Design Criteria for control room indication did not indicate any specific requirement for all SIS valves listed in Table 6.2-2 or those implied in Section 6.2.2.1.1 to actuate an alarm when out of position.
12/13/96        0235        Auto Reactor Trip from 11 % power due to steam flow/feed flow mismatch with low steam generator water level in the "A" steam generator.
12/23/96        0255        Commence Reactor Startup.
0348       Reactor critical.
1243       Unit on line, start power increase.
12/24/96        1548       Stopped power increase at 100%, 858 MWe.
12/31/96        2400        The reporting period ended with the unit operating at 100% power, 855 MWe.
 
                                                                        -urry Monthly Operating Report No. 96-12 Page 10 of 22 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: December, 1996 FS 96-44      Updated Final Safety Analysis Report Change                                         12-02-96 (Safety Evaluation 96-150)
Section 14.3.2 of the UFSAR discusses the rupture of a main steam pipe. Questions have been raised about what is meant by the term "main steam lines."
This change adds information to clarify what is meant by the term "main steam lines."
Since this change is clarification of existing information only, no change to the meaning or intent of the UFSAR will be made. Therefore, an unreviewed safety question does not exist.
TM S2-96-28  Temporary Modification                                                               12-3-96 (Safety Evaluation No. 95-005 Rev.1)
Temporary Modification (TM) S2-96-28 installed a replacement resistance temperature device (RTD) in the local temperature indicator thermowell to provide the Unit 2 Steam Generator (SG) "8" inlet feedwater temperature.
The local temperature indicator thermowell is of the same design as the main RTD thermowell, except for length. An evaluation of this difference concluded, based on a comparison of previous temperature data, that a reliable and accurate indication of the SG "B" inlet feedwater temperature can be obtained. This modification did not reduce the Technical Specifications margin of safety. Therefore, an unreviewed safety question does not exist.
FS 96-47    - Updated Final Safety Analysis Report Change                                         12-5-96 (Safety Evaluation 96-154)
Currently, a note in UFSAR Table 6.2-2 and Section 6.2.2.1.1 states "any of the listed motor operated valves will actuate a combination light and alarm when one or more SIS valves are out of position." This does not accurately reflect actual plant control room indication, since not all of the SIS valves listed will actuate the "SIS Valves Out Of Position" alarm.
A review of the SI Design Basis Document and the applicable General Design Criteria for control room indication did not indicate any specific requirement for all SIS valves listed in Table 6.2-2 or those implied in Section 6.2.2.1.1 to actuate an alarm when out of position.
Sufficient monitoring exists to ensure that the SI valves are in their correct positions.
Sufficient monitoring exists to ensure that the SI valves are in their correct positions.
Therefore, an unreviewed safety question does not exist. Updated Final Safety Analysis Report Change (Safety Evaluation 96-152) 12-5-96 Due to limited space, a change to the UFSAR is required to allow storage of QA records offsite at an approved facility.
Therefore, an unreviewed safety question does not exist.
FS 96-49      Updated Final Safety Analysis Report Change                                         12-5-96 (Safety Evaluation 96-152)
Due to limited space, a change to the UFSAR is required to allow storage of QA records offsite at an approved facility.
Records will continue to be stored in accordance with the applicable ANSI commitments.
Records will continue to be stored in accordance with the applicable ANSI commitments.
This change is administrative in nature with no modification to plant systems or components.
This change is administrative in nature with no modification to plant systems or components. Therefore, an unreviewed safety question does not exist.
 
                                                                    .,,urry Monthly Operating Report No. 96-12 Page 11 of 22 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/VEAR: December, 1996 FS 96-41      Updated Final Safety Analysis Report Change                                      12-5-96 (Safety Evaluation 96-153)
This UFSAR change moves the stated numerical value of the auxiliary feedwater flow for the licensing basis Loss Of Normal Feedwater {LONF) event from Section 10.3.5.3 to Section 14.2.11.1.3 where the other analysis assumptions are located. The statement in Section 10.3.5.3 will be changed from "a minimum of 500 gpm of auxiliary feedwater flow''
to "adequate auxiliary feedwater flow."
This change is administrative in nature with no modification to plant systems or components. Therefore, an unreviewed safety question does not exist.
FS 96-54      Updated Final Safety Analysis Report Change                                      12-5-96 (Safety Evaluation 96-155)
This UFSAR change updates Section 3.2.1 to be consistent with the current plant configuration. When the plant configuration was changed in 1984, Section 6.2 Safety Injection System and Section 14.3.2 accident analysis were updated but Section 3.2.1 was overlooked.
This UFSAR change updates Section 3.2.1 for consistency and has no physical impact on any plant system or component. Therefore, an unreviewed safety question does not exist.
DCP 95-023    Design Change Package                                                            12-5-96
          * * (Safety Evaluation 95-129)
Design Change Package 95-023 replaced existing fire pump 1-FP-P-3 with a pump which meets the specified design requirements and provides the required pressure and flow capacity. Therefore, an unreviewed safety question does not exist.
SE 96-0021    Safety Evaluation                                                                12-11-96 (Safety Evaluation 96-0021)
The NRC has approved the TN-32 Dry Storage Cask Topical Safety Analysis Report and a Surry ISFSI Technical Specification amendment for the use of this cask. This safety evaluation is performed to incorporate the use of the TN-32 storage cask into the Surry ISFSI Safety Analysis Report, Environmental Report and License Application.
The design and operation of the TN-32 cask is similar to that of the four cask designs already approved for use at the Surry ISFSI. There is no reduction in the margin of safety as defined in the basis for any Technical Specification. The current design basis for the Surry ISFSI was evaluated and remains bounding. Therefore, an unreviewed safety question does not exist.
 
e  Surry Monthly Operating Report No. 96-12 Page 12 of 22 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: December, 1996 SE 96-0031  Safety Evaluation                                                                  12-11-96 (Safety Evaluation 96-0031)
This safety evaluation is performed to allow the revision of the ISFSI Safety Analysis Report for the storage of burnable poison rod assemblies and thimble plugging devices with the spent fuel in dry storage casks at the Surry ISFSI. The NRC issued a draft Standard Review Plan for Dry Cask Storage Systems which indicated that the:storage of "non-fuel core components" or "control assemblies" in dry storage casks is allowed, if they are described in the cask Topical Safety Analysis Report and included in the structural and shielding analyses.
The casks have been analyzed and it has been determined that the margin of safety has not been reduced by the storage of these core components since the cask and basket stresses remain below the allowable values during a cask end drop or tipover event.
Additionally, the existing surface dose rate limits in Technical Specification 3.3 still apply
              - to ensure compliance with the dose rate limits for the ISFSI perimeter fence and nearest resident. Therefore, an unreviewed safety question does not exist.
SE 96-0041  Safety Evaluation                                                                  12-11-96 (Safety Evaluation 96-0041)
This safety evaluation assesses the as-built conditions of ISFSI Surry Pad 2 to determine whether this pad meets the criteria established by the NRC in their Safety Evaluation Report (SER) for cask drops or tipover of the Transnuclear TN-32 cask. A review of the pad design criteria was performed. The results of the review determined that the pad meets the criteria established by the NRC SER.
This change is administrative in nature with no modification to plant systems or components. Therefore, an unreviewed safety question does not exist.
SE 96-161    Safety Evaluation                                                                  12-11-96 (Safety Evaluation 96-161)
This safety evaluation assesses the update to the Small Break Loss of Coolant Accident (SBLOCA) analysis which is being incorporated into the licensing analysis basis for Surry Units 1 and 2.
The reanalysis of the SBLOCA was performed using Westinghouse LOCA-ECCS SBLOCA Evaluation Model. The analytical techniques are in full compliance with 10CFR50, Appendix K. The evaluation model is an approved methodology in the COLR list. This reanalysis used conservative assumptions with respect to existing limits and plant capabilities. The analysis results show that the emergency core cooling system will meet the acceptance criteria in 10CFR50.46. Therefore, an unreviewed safety question does not exist.
 
e                      .
* Surry Monthly Operating Report
.. "                                                                                            No. 96-12 Page 13 of 22 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTHIYEAR: December, 1996 FS 96-59  Updated Final Safety Analysis Report Change                                      12-12-96 (Safety Evaluation 96-158)
Currently, UFSAR Sections 4.1.2.6 and 4.2.7.1 reference humidity indication as a method of monitoring containment coolant leakage. In 1978, the containment humidity monitoring instrumentation was abandoned in place.
Primary coolant system leakage is most readily detected by increased makeup requirements and by c secondary coolant system leak. Therefore, an unreviewed safety question does not exist.
FS 96-53  Updated Final Safety Analysis Report Change                                      12-12-96 (Safety Evaluation 96-157)
Currently, UFSAR Section 4.3.4.2 contains a statement "Two additional bottles charged to 2200 psig are connected to the system but isolated as spares" may lead to misinterpretation of the requirements associated with maintaining ready spares. A revision is needed to clarify current operating practices associated with the pressurizer PORV backup air supply system. The change will state "The two bottles that are not aligned to the manifold are initially fully charged and used as installed spare bottle capacity. The intent is to reduce the time required to reestablish bottle pressure when a low pressure alarm occurs with the unit at load. Instead of changing out bottles, the spare bottles need only be valved in." The intent of this change is to minimize the radiation exposure personnel would receive changing depleted bottles during power operations.
The backup air bottle pressure limits are set by the low temperature overpressure mitigating system, based on the assumption that no operator action is required for ten minutes. The air supply should be capable of providing 100 cycles. Two high pressure bottles are normally valved in with each bottle capable of 115 cycles at 1000 psig. The low pressure backup air annunicator alarms at 1000 psig. Therefore, an unreviewed safety question does not exist.
SE 96-158 Safety Evaluation                                                                12-16-96 (Safety Evaluation No. 96-159)
This safety evaluation assesses the impact of the "B" Circulating Water (CW) Pump being out of service for greater than 30 days. The purpose of the pump is to provide the water required to condense the turbine exhaust steam and supply water to the Service Water System by transferring water from the James River into a common intake canal for Units 1 and 2.
There are four CW pumps for each unit. The minimum requirement per Technical Specification (TS) 3.14 to support plant operation is two CW pumps. The TS requirement is satisfied and adequate canal level is maintained by the remaining operable CW pumps.
Therefore, an unreviewed safety question does not exist.
Therefore, an unreviewed safety question does not exist.
FS 96-41 FS 96-54 DCP 95-023 SE 96-0021 .,,urry Monthly Operating Report No. 96-12 Page 11 of 22 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/VEAR:
December, 1996 Updated Final Safety Analysis Report Change (Safety Evaluation 96-153) 12-5-96 This UFSAR change moves the stated numerical value of the auxiliary feedwater flow for the licensing basis Loss Of Normal Feedwater
{LONF) event from Section 10.3.5.3 to Section 14.2.11.1.3 where the other analysis assumptions are located. The statement in Section 10.3.5.3 will be changed from "a minimum of 500 gpm of auxiliary feedwater flow'' to "adequate auxiliary feedwater flow." This change is administrative in nature with no modification to plant systems or components.
Therefore, an unreviewed safety question does not exist. Updated Final Safety Analysis Report Change (Safety Evaluation 96-155) 12-5-96 This UFSAR change updates Section 3.2.1 to be consistent with the current plant configuration.
When the plant configuration was changed in 1984, Section 6.2 Safety Injection System and Section 14.3.2 accident analysis were updated but Section 3.2.1 was overlooked.
This UFSAR change updates Section 3.2.1 for consistency and has no physical impact on any plant system or component.
Therefore, an unreviewed safety question does not exist. Design Change Package * * (Safety Evaluation 95-129) 12-5-96 Design Change Package 95-023 replaced existing fire pump 1-FP-P-3 with a pump which meets the specified design requirements and provides the required pressure and flow capacity.
Therefore, an unreviewed safety question does not exist. Safety Evaluation 12-11-96 (Safety Evaluation 96-0021) The NRC has approved the TN-32 Dry Storage Cask Topical Safety Analysis Report and a Surry ISFSI Technical Specification amendment for the use of this cask. This safety evaluation is performed to incorporate the use of the TN-32 storage cask into the Surry ISFSI Safety Analysis Report, Environmental Report and License Application.
The design and operation of the TN-32 cask is similar to that of the four cask designs already approved for use at the Surry ISFSI. There is no reduction in the margin of safety as defined in the basis for any Technical Specification.
The current design basis for the Surry ISFSI was evaluated and remains bounding.
Therefore, an unreviewed safety question does not exist. 
,_, SE 96-0031 SE 96-0041 SE 96-161 e Surry Monthly Operating Report No. 96-12 Page 12 of 22 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR:
December, 1996 Safety Evaluation 12-11-96 (Safety Evaluation 96-0031) This safety evaluation is performed to allow the revision of the ISFSI Safety Analysis Report for the storage of burnable poison rod assemblies and thimble plugging devices with the spent fuel in dry storage casks at the Surry ISFSI. The NRC issued a draft Standard Review Plan for Dry Cask Storage Systems which indicated that the:storage of "non-fuel core components" or "control assemblies" in dry storage casks is allowed, if they are described in the cask Topical Safety Analysis Report and included in the structural and shielding analyses.
The casks have been analyzed and it has been determined that the margin of safety has not been reduced by the storage of these core components since the cask and basket stresses remain below the allowable values during a cask end drop or tipover event. Additionally, the existing surface dose rate limits in Technical Specification


===3.3 still===
                                                                      .,,urry Monthly Operating Report No. 96-12 Page 14 of 22 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: December, 1996 TM 82-96-030 Temporary Modification                                                            12-17-96 (Safety Evaluation No. 96-113 Rev. 1)
apply -to ensure compliance with the dose rate limits for the ISFSI perimeter fence and nearest resident.
This Temporary Modification (TM) adds spray shields to protect the RCP flange studs from boric acid spray and reduce the amount of boric acid spray being drawn into the RCP motor. Additionally, this TM will provide remote monitoring of the RCP flange from the Main Control Room by the installation of a camera and lights in the "C" RCP Loop Room.
Therefore, an unreviewed safety question does not exist. Safety Evaluation 12-11-96 (Safety Evaluation 96-0041) This safety evaluation assesses the as-built conditions of ISFSI Surry Pad 2 to determine whether this pad meets the criteria established by the NRC in their Safety Evaluation Report (SER) for cask drops or tipover of the Transnuclear TN-32 cask. A review of the pad design criteria was performed.
The spray shields will not affect the original configuration of the Reactor Coolant System or the loading on the primary loop piping supports. The shields will be secured in order to prevent them from becoming missiles during postulated earthquakes or high energy line breaks. The camera has no ties to existing station protection or control systems. The installation of equipment by this TM will not create an unreviewed safety question as described in 10CFR50.59. Therefore, an unreviewed safety question does not exist.
The results of the review determined that the pad meets the criteria established by the NRC SER. This change is administrative in nature with no modification to plant systems or components.
FS 96-55    Updated Final Safety Analysis Report Change                                      12-19-96 (Safety Evaluation 96-164)
Therefore, an unreviewed safety question does not exist. Safety Evaluation 12-11-96 (Safety Evaluation 96-161) This safety evaluation assesses the update to the Small Break Loss of Coolant Accident (SBLOCA) analysis which is being incorporated into the licensing analysis basis for Surry Units 1 and 2. The reanalysis of the SBLOCA was performed using Westinghouse LOCA-ECCS SBLOCA Evaluation Model. The analytical techniques are in full compliance with 1 OCFR50, Appendix K. The evaluation model is an approved methodology in the COLR list. This reanalysis used conservative assumptions with respect to existing limits and plant capabilities.
UFSAR Section 9.9.1.3 is being revised to delete some details on specific times when actions would be taken prior to the arrival of a hurricane on site and the specified hurricane wind speed. UFSAR Section 9.10.4.18 will be revised to reflect the Circulating Water (CW) isolation valves as safety-related. This Section incorrectly identifies the valves as non safety-related.
The analysis results show that the emergency core cooling system will meet the acceptance criteria in 1 OCFR50.46.
The details removed from Section 9.9.1.3 are not vital to the hurricane actions. Important actions as described in Technical Report 0032 will remain in the UFSAR. The CW isolation valves that were described as non safety-related were installed and maintained as safety-related. These changes are administrative in nature with no modification to plant systems or components. Therefore, an unreviewed safety question does not exist.
Therefore, an unreviewed safety question does not exist.
FS 96-58    Updated Final Safety Analysis Report Change                                       12-19-96 (Safety Evaluation 96-163)
. . " FS 96-59 FS 96-53 SE 96-158 e .
Currently, UFSAR Section 10.3.7.3 contains a statement indicating the non-safety related turbine generator DC bearing oil pump is required to function during a LOCA or loss of station power. Additionally, Section 10.3.7.4 contains a statement that the DC bearing oil pump will be tested on a monthly basis. Changes to the UFSAR Section 10.3.7.3 will state the DC bearing oil pump is designed to function during a loss of station power.
* Surry Monthly Operating Report No. 96-12 Page 13 of 22 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTHIYEAR:
Section 10.3.7.4 will change the frequency of DC oil pump testing from "monthly" to "periodically."
December, 1996 Updated Final Safety Analysis Report Change (Safety Evaluation 96-158) 12-12-96 Currently, UFSAR Sections 4.1.2.6 and 4.2.7.1 reference humidity indication as a method of monitoring containment coolant leakage. In 1978, the containment humidity monitoring instrumentation was abandoned in place. Primary coolant system leakage is most readily detected by increased makeup requirements and by c secondary coolant system leak. Therefore, an unreviewed safety question does not exist. Updated Final Safety Analysis Report Change (Safety Evaluation 96-157) 12-12-96 Currently, UFSAR Section 4.3.4.2 contains a statement "Two additional bottles charged to 2200 psig are connected to the system but isolated as spares" may lead to misinterpretation of the requirements associated with maintaining ready spares. A revision is needed to clarify current operating practices associated with the pressurizer PORV backup air supply system. The change will state "The two bottles that are not aligned to the manifold are initially fully charged and used as installed spare bottle capacity.
Although the turbine generator DC bearing oil pump is designed to operate during a loss of station power, there is no design basis assumption that requires it to be operable during a LOCA or loss of station power. The testing frequency is governed by industry good practice and insurance carrier requirements. There are no Technical Specification or design basis assumption requirements for the monthly testing of the pump. Therefore, an unreviewed safety question does not exist.
The intent is to reduce the time required to reestablish bottle pressure when a low pressure alarm occurs with the unit at load. Instead of changing out bottles, the spare bottles need only be valved in." The intent of this change is to minimize the radiation exposure personnel would receive changing depleted bottles during power operations.
 
The backup air bottle pressure limits are set by the low temperature overpressure mitigating system, based on the assumption that no operator action is required for ten minutes. The air supply should be capable of providing 100 cycles. Two high pressure bottles are normally valved in with each bottle capable of 115 cycles at 1000 psig. The low pressure backup air annunicator alarms at 1000 psig. Therefore, an unreviewed safety question does not exist. Safety Evaluation 12-16-96 (Safety Evaluation No. 96-159) This safety evaluation assesses the impact of the "B" Circulating Water (CW) Pump being out of service for greater than 30 days. The purpose of the pump is to provide the water required to condense the turbine exhaust steam and supply water to the Service Water System by transferring water from the James River into a common intake canal for Units 1 and 2. There are four CW pumps for each unit. The minimum requirement per Technical Specification (TS) 3.14 to support plant operation is two CW pumps. The TS requirement is satisfied and adequate canal level is maintained by the remaining operable CW pumps. Therefore, an unreviewed safety question does not exist.
                                                                        ~urry Monthly Operating Report No. 96-12 Page 15 of 22 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: December, 1996 SE 96-167  Safety Evaluation                                                                12-20-96 (Safety Evaluation No. 96-167)
TM 82-96-030 FS 96-55 FS 96-58 .,,urry Monthly Operating Report No. 96-12 Page 14 of 22 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR:
This safety evaluation assesses continued Unit 2 power operation with a single Unit 2 RCP~1 C flange bolt preload stretch below the minimum required by the vendor. The flange bolts provide a structural connection between the flange and the pump casing and provide adequate preload and compression to the gasketed joint. The bolt has full thread engagement which meets the structural requirements. However, with the bolt preload below the required minimum some leakage may occur at the casing joint. A temporary modification was installed to monitor the flange area using a camera.
December, 1996 Temporary Modification 12-17-96 (Safety Evaluation No. 96-113 Rev. 1) This Temporary Modification (TM) adds spray shields to protect the RCP flange studs from boric acid spray and reduce the amount of boric acid spray being drawn into the RCP motor. Additionally, this TM will provide remote monitoring of the RCP flange from the Main Control Room by the installation of a camera and lights in the "C" RCP Loop Room. The spray shields will not affect the original configuration of the Reactor Coolant System or the loading on the primary loop piping supports.
The probability of a rapid propagation type failure is not credible based on an evaluation performed by the vendor.        The RC System pressure boundary will continue to accommodate the temperatures and pressures attained under all expected modes of station operations or anticipated transients, as well as maintain integrity without catastrophic rupture. Therefore, an unreviewed safety question does not exist.
The shields will be secured in order to prevent them from becoming missiles during postulated earthquakes or high energy line breaks. The camera has no ties to existing station protection or control systems. The installation of equipment by this TM will not create an unreviewed safety question as described in 1 OCFR50.59.
SE 96-0051 Safety Evaluation                                                                12-20-96 (Safety Evaluation No. 96-0051)
Therefore, an unreviewed safety question does not exist. Updated Final Safety Analysis Report Change (Safety Evaluation 96-164) 12-19-96 UFSAR Section 9.9.1.3 is being revised to delete some details on specific times when actions would be taken prior to the arrival of a hurricane on site and the specified hurricane wind speed. UFSAR Section 9.10.4.18 will be revised to reflect the Circulating Water (CW) isolation valves as safety-related.
This safety evaluation assesses the continued storage of TN-32 Cask No.1 on the ISFSI pad with a pinhole leak in a weld. The weld connects the outer shell to the body of the cask. The cask is to remain on the ISFSI pad until appropriate procedures can be developed for the repair of the pinhole leak.
This Section incorrectly identifies the valves as non safety-related.
The function of the weld is to attach the outer skin to the cask body. The outer skin encloses the resin boxes which provide the primary neutron shielding for the cask. The presence of the pinhole could potentially allow the contents of the atmosphere inside the resin chamber to escape as the cask reaches equilibrium temperature. The gases given off by the resin during heatup could include carbon dioxide, carbon monoxide and other hydrocarbons.     Gas samples taken from the leakage site determined that no radioisotopes were present and that the primary constituents of the sample were nitrogen and oxygen in the percentages that would indicate that the leaking gas was air. No helium was detected and a smear taken of the area was not contaminated. The release of a small amount of these gases will not result in any detrimental environmental or radiological conditions. Therefore, an unreviewed safety question does not exist.
The details removed from Section 9.9.1.3 are not vital to the hurricane actions. Important actions as described in Technical Report 0032 will remain in the UFSAR. The CW isolation valves that were described as non safety-related were installed and maintained as safety-related.
 
These changes are administrative in nature with no modification to plant systems or components.
                                                                          ~urry Monthly Operating Report No. 96-12 Page 16 of 22 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTHNEAR:      December, 1996 O-ICM-EH-CAB-001 Instrument Corrective Maintenance                                                      12-12-96 (Safety Evaluation No. 96-156)
Therefore, an unreviewed safety question does not exist. Updated Final Safety Analysis Report Change (Safety Evaluation 96-163) 12-19-96 Currently, UFSAR Section 10.3.7.3 contains a statement indicating the non-safety related turbine generator DC bearing oil pump is required to function during a LOCA or loss of station power. Additionally, Section 10.3.7.4 contains a statement that the DC bearing oil pump will be tested on a monthly basis. Changes to the UFSAR Section 10.3.7.3 will state the DC bearing oil pump is designed to function during a loss of station power. Section 10.3.7.4 will change the frequency of DC oil pump testing from "monthly" to "periodically." Although the turbine generator DC bearing oil pump is designed to operate during a loss of station power, there is no design basis assumption that requires it to be operable during a LOCA or loss of station power. The testing frequency is governed by industry good practice and insurance carrier requirements.
Instrument Corrective Maintenance Procedure O-ICM-EH-CAB-001, "EHC System Diagnostic Checks," was revised to provide instructions for a procedurally controlled temporary test lead. This will allow the collection of test data using a recorder during the Unit 2 ramp down to investigate a possible signal problem with the governor valve control system.
There are no Technical Specification or design basis assumption requirements for the monthly testing of the pump. Therefore, an unreviewed safety question does not exist.
Should the governor valves begin to open, the valve position limiting circuit would act to limit the power increase. Should the valve limiter fail, the resultant load increase is still bounded by the current safety analyses. The physical limit on steam flow through all governor valves wide open (105%) is bounded by the analyzed step load increase safety analysis limit (116%). Should a step load decrease occur, the plant response would be within the current design requirements and the reactor protection system would function as required. Therefore, an unreviewed safety question does not exist.
. . ' SE 96-167 SE 96-0051 ~urry Monthly Operating Report No. 96-12 Page 15 of 22 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR:
1(2)-NSP-SD-001  Engineering Surveillance Procedure                                                    12-16-96 (Safety Evaluation No. 96-162)
December, 1996 Safety Evaluation 12-20-96 (Safety Evaluation No. 96-167) This safety evaluation assesses continued Unit 2 power operation with a single Unit 2 RCP~1 C flange bolt preload stretch below the minimum required by the vendor. The flange bolts provide a structural connection between the flange and the pump casing and provide adequate preload and compression to the gasketed joint. The bolt has full thread engagement which meets the structural requirements.
Engineering Surveillance Procedure 1(2)-NSP-SD-001, "Optimum Feedwater Heater Level Test," provides instructions for determining/calculating the optimum water level in the shell side of feedwater heaters 1A, 1B, 3A, 3B, 4A, 4B, 5A, 5B. This will maximize the efficiency of the feedwater heaters, increasing overall plant efficiency.
However, with the bolt preload below the required minimum some leakage may occur at the casing joint. A temporary modification was installed to monitor the flange area using a camera. The probability of a rapid propagation type failure is not credible based on an evaluation performed by the vendor. The RC System pressure boundary will continue to accommodate the temperatures and pressures attained under all expected modes of station operations or anticipated transients, as well as maintain integrity without catastrophic rupture. Therefore, an unreviewed safety question does not exist. Safety Evaluation 12-20-96 (Safety Evaluation No. 96-0051) This safety evaluation assesses the continued storage of TN-32 Cask No.1 on the ISFSI pad with a pinhole leak in a weld. The weld connects the outer shell to the body of the cask. The cask is to remain on the ISFSI pad until appropriate procedures can be developed for the repair of the pinhole leak. The function of the weld is to attach the outer skin to the cask body. The outer skin encloses the resin boxes which provide the primary neutron shielding for the cask. The presence of the pinhole could potentially allow the contents of the atmosphere inside the resin chamber to escape as the cask reaches equilibrium temperature.
This test will affect the efficiency of the feedwater heaters, but will not affect the operation of the heaters. The heaters will operate as required, but with different setpoints for liquid level. Therefore, an unreviewed safety question does not exist.
The gases given off by the resin during heatup could include carbon dioxide, carbon monoxide and other hydrocarbons.
SE 96-160        Safety Evaluation                                                                      12-16-96 (Safety Evaluation No. 96-160)
Gas samples taken from the leakage site determined that no radioisotopes were present and that the primary constituents of the sample were nitrogen and oxygen in the percentages that would indicate that the leaking gas was air. No helium was detected and a smear taken of the area was not contaminated.
Safety evaluation 96-160 was performed to assess the acceptability of continued usage of the procedure O-OSP-RM-002 to check source the Component Cooling Radiation Monitors in accordance with Technical Specification requirements, although the methodology differs from that stated in the UFSAR. This condition will continue until June 1997 when the Main Control Room Radiation Monitoring Cabinet portion of the Design Change is installed.
The release of a small amount of these gases will not result in any detrimental environmental or radiological conditions.
The evaluation establishes the acceptability of the current method of source checking the Component Cooling Water Radiation Monitors and does not affect any safety related equipment. Therefore, an unreviewed safety question does not exist.
Therefore, an unreviewed safety question does not exist.
 
O-ICM-EH-CAB-001 1 (2)-NSP-SD-001 SE 96-160 ~urry Monthly Operating Report No. 96-12 Page 16 of 22 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTHNEAR:
.. L
December, 1996 Instrument Corrective Maintenance (Safety Evaluation No. 96-156) 12-12-96 Instrument Corrective Maintenance Procedure O-ICM-EH-CAB-001, "EHC System Diagnostic Checks," was revised to provide instructions for a procedurally controlled temporary test lead. This will allow the collection of test data using a recorder during the Unit 2 ramp down to investigate a possible signal problem with the governor valve control system. Should the governor valves begin to open, the valve position limiting circuit would act to limit the power increase.
                          -                                                  ~urry Monthly Operating Report No. 96-12 Page 17 of 22 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: December, 1996 O-IMP-BR-001  Instrument Maintenance Procedure                                                  12-19-96 (Safety Evaluation No. 96-166)
Should the valve limiter fail, the resultant load increase is still bounded by the current safety analyses.
Instrument Maintenance Procedure O-IMP-BR-001, "Monitoring of Boron Recovery Tank During Reactor Coolant System Drain Down Evolutions," provides instructions to connect a calibrated 250 ohm resistor in series in the Boron Recovery Tank (BRT) level instrumentation loop. This will allow a chart recorder to be connected across the resistor to allow accurate monitoring of RCS inventory during RCS draining evolutions.
The physical limit on steam flow through all governor valves wide open (105%) is bounded by the analyzed step load increase safety analysis limit (116%). Should a step load decrease occur, the plant response would be within the current design requirements and the reactor protection system would function as required.
The system is passive and its characteristics will be unchanged. The "Channel Operation and Accuracy" Section of the affected tank's level calibration procedure will be completed once the resistor is installed. The BRT high and low level alarms, which are not safety related, will be unaffected by this activity. Therefore, an unreviewed safety question does not exist.
Therefore, an unreviewed safety question does not exist. Engineering Surveillance Procedure (Safety Evaluation No. 96-162) 12-16-96 Engineering Surveillance Procedure 1 (2)-NSP-SD-001, "Optimum Feedwater Heater Level Test," provides instructions for determining/calculating the optimum water level in the shell side of feedwater heaters 1A, 1 B, 3A, 3B, 4A, 4B, 5A, 5B. This will maximize the efficiency of the feedwater heaters, increasing overall plant efficiency.
O-AP-23.01    Abnormal Procedure                                                                  12-19-96 (Safety Evaluation No. 96-165)
This test will affect the efficiency of the feedwater heaters, but will not affect the operation of the heaters. The heaters will operate as required, but with different setpoints for liquid level. Therefore, an unreviewed safety question does not exist. Safety Evaluation 12-16-96 (Safety Evaluation No. 96-160) Safety evaluation 96-160 was performed to assess the acceptability of continued usage of the procedure O-OSP-RM-002 to check source the Component Cooling Radiation Monitors in accordance with Technical Specification requirements, although the methodology differs from that stated in the UFSAR. This condition will continue until June 1997 when the Main Control Room Radiation Monitoring Cabinet portion of the Design Change is installed.
Abnormal Procedure O-AP-23.01, "Rapid RCS Cooldown," was revised to modify the current practice of borating to Cold Shutdown boron prior to initiating a cooldown and blocking Safety Injection to a method of concurrent borations and cooldown. In addition, this change increases the current administrative Reactor Coolant System (RCS) cooldown rate from 50 °F/hr to 75 °F/hr while above the Low Temperature Overpressure Mitigation System {LTOPs) enabling temperature of 350 °F. Below the LTOPs enabling temperature of 350 °F, the current administrative cooldown rate of 50 °F/hr is still
The evaluation establishes the acceptability of the current method of source checking the Component Cooling Water Radiation Monitors and does not affect any safety related equipment.
                  .. applicable.
Therefore, an unreviewed safety question does not exist.   
The proposed changes do not alter the design or principles of operation of the CVCS or any associated safety related system. Therefore, the probability of the malfunction of equipment important to safety is not increased, and no new or unique equipment malfunction scenarios are created. Since the CVCS is not relied on for accident mitigation, the consequences of the CVCS malfunction has not increased. The exception is when the plant is aligned to Safety Injection and the Charging Pumps are considered High Head Safety Injection Pumps. Inadvertent boron dilution by addition of primary grade water to the RCS is addressed in the UFSAR and this analysis remains bounding.
.. L O-IMP-BR-001 O-AP-23.01
The severity of an inadvertent dilution with the proposed changes would be less severe than the bounding analysis. Therefore, an unreviewed safety question does not exist.
-~urry Monthly Operating Report No. 96-12 Page 17 of 22 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR:
 
December, 1996 Instrument Maintenance Procedure (Safety Evaluation No. 96-166) 12-19-96 Instrument Maintenance Procedure O-IMP-BR-001, "Monitoring of Boron Recovery Tank During Reactor Coolant System Drain Down Evolutions," provides instructions to connect a calibrated 250 ohm resistor in series in the Boron Recovery Tank (BRT) level instrumentation loop. This will allow a chart recorder to be connected across the resistor to allow accurate monitoring of RCS inventory during RCS draining evolutions.
                                                        ~urry Monthly Operating Report
The system is passive and its characteristics will be unchanged.
. j L
The "Channel Operation and Accuracy" Section of the affected tank's level calibration procedure will be completed once the resistor is installed.
No. 96-12 Page 18 of 22 TESTS AND EXPERIMENTS THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: December, 1996 None During the Reporting Period
The BRT high and low level alarms, which are not safety related, will be unaffected by this activity.
 
Therefore, an unreviewed safety question does not exist. Abnormal Procedure 12-19-96 (Safety Evaluation No. 96-165) Abnormal Procedure O-AP-23.01, "Rapid RCS Cooldown," was revised to modify the current practice of borating to Cold Shutdown boron prior to initiating a cooldown and blocking Safety Injection to a method of concurrent borations and cooldown.
                                                                                ~urry Monthly Operating Report
In addition, this change increases the current administrative Reactor Coolant System (RCS) cooldown rate from 50 °F/hr to 75 °F/hr while above the Low Temperature Overpressure Mitigation System {L TOPs) enabling temperature of 350 °F. Below the L TOPs enabling temperature of 350 °F, the current administrative cooldown rate of 50 °F/hr is still .. applicable.
.,..                                                                                                No. 96-12 I,                                                                                         Page 19 of 22 CHEMISTRY REPORT MONTHNEAR:  December, 1996 Unit No. 1                   Unit No. 2 Primarv Coolant Analysis          Max.        Min.      Avg. Max. Min.         Avg.
The proposed changes do not alter the design or principles of operation of the CVCS or any associated safety related system. Therefore, the probability of the malfunction of equipment important to safety is not increased, and no new or unique equipment malfunction scenarios are created. Since the CVCS is not relied on for accident mitigation, the consequences of the CVCS malfunction has not increased.
Gross Radioactivity, &#xb5;Ci/ml          9.55E-1    4.97E-2    7.21 E-1 4.10E-1  2.27E-3      1.44E-1 Suspended Solids, ppm                sO.D10      so.010      so.010    2.5  so.010        0.389 Gross Tritium, &#xb5;Ci/ml                3.30E-1    2.38E-1    2.85E-1  6.32E-1  1.73E-1      4.00E-1 1131, &#xb5;Ci/ml                          1.15E-2    8.07E-3    9.43E-3 9.36E-5  1.15E-5      4.65E-5 113111133                              0.41        0.23        0.29    0.11    0.06        0.08 Hydrogen, cc/kg                        40.1        31.2        36.6    31      1.7          16.6 Lithium, oom                            1.67        1.24        1.53    3.69    0.10          1.43 Boron - 10, ppm*                        47.4        28.4        37.6  346.7    192.1        289.6 Oxygen, (DO), ppm                    s0.005      s0.005      s0.005    6.0  s0.005        0.18 Chloride, ppm                          0.004      <0.001      0.002  0.008    0.002        0.004 pH at 25 deqree Celsius                7.30        6.78        6.98    6.81    4.79          5.61
The exception is when the plant is aligned to Safety Injection and the Charging Pumps are considered High Head Safety Injection Pumps. Inadvertent boron dilution by addition of primary grade water to the RCS is addressed in the UFSAR and this analysis remains bounding.
* Boron - 10 = Total Boron x 0.196 Comments:
The severity of an inadvertent dilution with the proposed changes would be less severe than the bounding analysis.
None
Therefore, an unreviewed safety question does not exist.
 
.. .. j L ~urry Monthly Operating Report No. 96-12 Page 18 of 22 TESTS AND EXPERIMENTS THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR:
        '    '.                              e                                    ~urry Monthly Operating Report I.
December, 1996 None During the Reporting Period 
No. 96-12 Page 20 of 22 FUEL HANDLING UNITS 1 & 2 MONTH/YEAR: December, 1996 New or Spent                  Number of                                           New or Spent Fuel Shipment Date Stored or  Assemblies    Assembly        ANSI      Initial  Fuel Shipping Number      Received    per Shipment    Number        Number  Enrichment  Cask Activity Spent Fuel Cask TN-32-01      12/18/96          32          N40          NOANSI    2.5560 6P2          LM05YN    3.6070 N44          NOANSI    2.5560 N46          NOANSI    2.5560 N33          NOANSI    2.5560 D02          LM007P    3.3250 D25          LM007D    3.3250 D39          LM0075    3.3250 2E8          LMODEP    2.5933 N34          NOANSI    2.5560 D31          LM0084    3.3250 D05          LM008E    3.3250 D14          LM007U    3.3250 D41          LMOOCA    3.3250 D50          LM0073    3.3250 N42          NOANSI    2.5560 N38          NOANSI    2.5590 D06          LM008F    3.3250 D49          LM007G    3.3250 D43          LM007J    3.3250 V17          LM041K    2.9060 6P4          LM05YR    3.6070 N39          NOANSI    2.5560 2E7          LMODFH    3.6028 D33          LM008K    3.3250 D46          LMOOCD    3.3250
.,.. I, CHEMISTRY REPORT MONTHNEAR:
 
December, 1996 Unit No. 1 Primarv Coolant Analysis Max. Min. Avg. Gross Radioactivity, &#xb5;Ci/ml 9.55E-1 4.97E-2 7.21 E-1 Suspended Solids, ppm sO.D10 so.010 so.010 Gross Tritium, &#xb5;Ci/ml 3.30E-1 2.38E-1 2.85E-1 1131, &#xb5;Ci/ml 1.15E-2 8.07E-3 9.43E-3 113111133 0.41 0.23 0.29 Hydrogen, cc/kg 40.1 31.2 36.6 Lithium, oom 1.67 1.24 1.53 Boron -10, ppm* 47.4 28.4 37.6 Oxygen, (DO), ppm s0.005 s0.005 s0.005 Chloride, ppm 0.004 <0.001 0.002 pH at 25 deqree Celsius 7.30 6.78 6.98
      ' ' .                                                                   ~Surry Monthly Operating
* Boron -10 = Total Boron x 0.196 Comments:
                                                                                                  . Report No. 96-12
None ~urry Monthly Operating Report No. 96-12 Page 19 of 22 Unit No. 2 Max. Min. Avg. 4.10E-1 2.27E-3 1.44E-1 2.5 so.010 0.389 6.32E-1 1.73E-1 4.00E-1 9.36E-5 1.15E-5 4.65E-5 0.11 0.06 0.08 31 1.7 16.6 3.69 0.10 1.43 346.7 192.1 289.6 6.0 s0.005 0.18 0.008 0.002 0.004 6.81 4.79 5.61 
"*. J Page 21 of 22 FUEL HANDLING UNITS 1 & 2 MONTHNEAR: December, 1996 New or Spent                  Number of                                          New or Spent Fuel Shipment Date Stored or  Assemblies    Assembly        ANSI      Initial    Fuel Shipping Number      Received    per Shipment    Number        Number  Enrichment    Cask Activity V19        LM042H    2.9060 N45        NOANSI    2.5560 N41        NOANSI    2.5560 N43        NOANSI    2.5560 6P8        LM009PA    3.6070 N47        NOANSI    2.5560
' '. .... , . I. New or Spent Fuel Shipment Date Stored or Number Received Spent Fuel Cask TN-32-01 12/18/96 e FUEL HANDLING UNITS 1 & 2 MONTH/YEAR:
 
December, 1996 Number of Assemblies Assembly ANSI per Shipment Number Number 32 N40 NOANSI 6P2 LM05YN N44 NOANSI N46 NOANSI N33 NOANSI D02 LM007P D25 LM007D D39 LM0075 2E8 LMODEP N34 NOANSI D31 LM0084 D05 LM008E D14 LM007U D41 LMOOCA D50 LM0073 N42 NOANSI N38 NOANSI D06 LM008F D49 LM007G D43 LM007J V17 LM041K 6P4 LM05YR N39 NOANSI 2E7 LMODFH D33 LM008K D46 LMOOCD ~urry Monthly Operating Report No. 96-12 Page 20 of 22 New or Spent Initial Fuel Shipping Enrichment Cask Activity 2.5560 3.6070 2.5560 2.5560 2.5560 3.3250 3.3250 3.3250 2.5933 2.5560 3.3250 3.3250 3.3250 3.3250 3.3250 2.5560 2.5590 3.3250 3.3250 3.3250 2.9060 3.6070 2.5560 3.6028 3.3250 3.3250 
tturry Monthly Operating Report No. 96-12 Page 22 of 22 DESCRIPTION OF PERIODIC TEST(S) WHICH WERE NOT COMPLETED WITHIN THE TIME LIMITS SPECIFIED IN TECHNICAL SPECIFICATIONS MONTH/YEAR: December, 1996 None During the Reporting Period}}
** ' ' . "*. J New or Spent Fuel Shipment Date Stored or Number Received FUEL HANDLING UNITS 1 & 2 MONTHNEAR:
December, 1996 Number of Assemblies Assembly ANSI per Shipment Number Number V19 LM042H N45 NOANSI N41 NOANSI N43 NOANSI 6P8 LM009PA N47 NOANSI . R Surry Monthly Operating eport Initial Enrichment 2.9060 2.5560 2.5560 2.5560 3.6070 2.5560 No. 96-12 Page 21 of 22 New or Spent Fuel Shipping Cask Activity 
' .... tturry Monthly Operating Report No. 96-12 Page 22 of 22 DESCRIPTION OF PERIODIC TEST(S) WHICH WERE NOT COMPLETED WITHIN THE TIME LIMITS SPECIFIED IN TECHNICAL SPECIFICATIONS MONTH/YEAR:
December, 1996 None During the Reporting Period}}

Latest revision as of 23:38, 2 February 2020

Monthly Operating Repts for Dec 1996 for Surry Power Station Units 1 & 2.W/970110 Ltr
ML18152A404
Person / Time
Site: Surry  Dominion icon.png
Issue date: 12/31/1996
From: Fanguy M, Mason M, Sarver S
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
97-020, 97-20, NUDOCS 9701220318
Download: ML18152A404 (23)


Text

  • ~

l -*----. .. t..,

VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 January 10, 1997 United States Nuclear Regulatory Commission Serial No.97-020 Attention: Document Control Desk NURPC Washington, D.C. 20555 Docket Nos. 50-280 50-281 License Nos. DPR-32 DPR-37 Gentlemen:

VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION UNITS 1 AND 2 MONTHLY OPERATING REPORT Enclosed is the Monthly Operating Report for Surry Power Station Units 1 and 2 for the month of December 1996.

If you have any questions or require additional information, please contact us.

Very truly yours, S. P. Sarver, Acting Manager Nuclear Licensing and Operations Support Enclosure cc: U. S. Nuclear Regulatory Commission Region II 101 Marietta Street, N.W.

Suite 2900 Atlanta, Georgia 30323 Mr. R. A. Musser NRC Senior Resident Inspector Surry Power Station

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VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION MONTHLY OPERATING REPORT REPORT No. 96-12 Approved:

~S)G_{l Station Manager

tl'8urry-Monthly Operating Report No. 96-12 Page 2 of 22 TABLE OF CONTENTS Section Page Operating Data Report - Unit No. 1 ............................................................................................................................ 3 Operating Data Report - Unit No. 2 ............................................................................................................................ 4 Unit Shutdowns and Power Reductions - Unit No. 1 .................................................................................................. 5 Unit Shutdowns and Power Reductions - Unit No. 2 .................................................................................................. 6 Average Daily Unit Power Level - Unit No. 1 ............................................................................................................. 7 Average Daily Unit Power Level - Unit No. 2 ............................................................................................................. 8 Summary of Operating Experience - Unit No. 1 ......................................................................................................... 9 Summary of Operating Experience - Unit No. 2 ......................................................................................................... 9 Facility Changes That Did Not Require NRC Approval ............................................................................................ 10 Procedure or Method of Operation Changes That Did Not Require NRC Approval. ................................................ 16 Tests and Experiments That Did Not Require NRC Approval .................................................................................. 18 Chemistry Report ..................................................................................................................................................... 19 Fuel Handling - Unit No. 1 ........................................................................................................................................ 20 Fuel Handling - Unit No. 2 ........................................................................................................................................ 20 Description of Periodic Test(s) Which Were Not Completed Within the Time Limits Specified in Technical Specifications ....................................................................................................................... 22

- Surry Monthly Operating Report No. 96-12 Page 3 of 22 OPERATING DATA REPORT Docket No.: 50-280 Date: 01/01/97 Completed By: D. K. Mason Telephone: (804) 365-2459

1. Unit Name: ........................................................... Surry Unit 1
2. Reporting Period: ................................................ . December, 1996
3. Licensed Thermal Power (MWt): ......................... . 2546
4. Nameplate Rating (Gross MWe): ........................ . 847.5
5. Design Electrical Rating (Net MWe): ................... . 788
6. Maximum Dependable Capacity (Gross MWe): .. . 840
7. Maximum Dependable Capacity (Net MWe): ...... . 801
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
9. Power Level To Which Restricted, If Any (Net MWe):
10. Reasons For Restrictions, If Any:

This Month YTD Cumulative

11. Hours In Reporting Period ............................... 744.0 8784.0 210624.0
12. Number of Hours Reactor Was Critical ........... 744.0 8784.0 146834.7
13. Reactor Reserve Shutdown Hours .................. 0.0 0.0 3774.5
14. Hours Generator On-Line ................................ 744.0 8784.0 144531.0
15. Unit Reserve Shutdown Hours ........................ 0.0 0.0 3736.2
16. Gross Thermal Energy Generated (MWH) ...... 1892818.6 22237651.3 338635443.8
17. Gross Electrical Energy Generated (MWH) ..... 633235.0 7395635.0 110972818.0
18. Net Electrical Energy Generated (MWH) ......... 610120.0 7137776.0 105593749.0
19. Unit Service Factor .......................................... 100.0% 100.0% 68.6%
20. Unit Availability Factor. .................................... 100.0% 100.0% 70.4%
21. Unit Capacity Factor (Using MDC Net) ............ 102.4% 101.4% 64.5%
22. Unit Capacity Factor (Using DER Net) ............ 104.1% 103.1% 63.6%
23. Unit Forced Outage Rate ................................ 0.0% 0.0% 15.2%
24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):

Refueling, March 6, 1997, 37 Days

25. If Shut Down at End of Report Period, Estimated Date of Start-up: N/A
26. Unit In Test Status (Prior to Commercial Operation):

FORECAST ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION

  • - Surry Monthly Operating Report No. 96-12 Page 4 of 22 OPERATING DATA REPORT Docket No.: 50-281 Date: 01-01-97 Completed By: D. K. Mason Telephone: {804) 365-2459
1. Unit Name: .......................................................... . Surry Unit 2
2. Reporting Period: ................................................ . December, 1996
3. Licensed Thermal Power (MWt): ......................... . 2546
4. Nameplate Rating (Gross MWe): ........................ . 847.5
5. Design Electrical Rating (Net MWe): ................... . 788
6. Maximum Dependable Capacity (Gross MWe): .. . 840
7. Maximum Dependable Capacity (Net MWe): ...... . 801
8. If Changes Occur in Capacity Ratings {Items Number 3 Through 7) Since Last Report, Give Reasons:
9. Power Level To Which Restricted, If Any (Net MWe):
10. Reasons For Restrictions, If Any:

This Month YTD Cumulative

11. Hours In Reporting Period ............................... 744.0 8784.0 207504.0
12. Number of Hours Reactor Was Critical ........... 502.5 7572.7 143075.6
13. Reactor Reserve Shutdown Hours .................. 0.0 0.0 328.1
14. Hours Generator On-Line ................................ 493.6 7541.7 141097.8
15. Unit Reserve Shutdown Hours ........................ 0.0 0.0 0.0
16. Gross Thermal Energy Generated (MWH) ...... 1238394.8 18939202.8 331474256.8
17. Gross Electrical Energy Generated (MWH) ..... 415495.0 6295155.0 108450799.0
18. Net Electrical Energy Generated (MWH) ......... 401148.0 6081464.0 103191879.0
19. Unit Service Factor .......................................... 66.3% 85.9% 68.0%
20. Unit Availability Factor ..................................... 66.3% 85.9% 68.0%
21. Unit Capacity Factor (Using MDC Net) ............ 67.3% 86.4% 63.7%
22. Unit Capacity Factor (Using DER Net) ............ 68.4% 87.9% 63.1%
23. Unit Forced Outage Rate ................................ 0.0% 1.7% 12.5%
24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
25. If Shut Down at End of Report Period, Estimated Date of Start-up: N/A
26. Unit In Test Status (Prior to Commercial Operation):

FORECAST ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION

- Surry Monthly Operating Report No. 96-12 Page 5 of 22 UNIT SHUTDOWN AND POWER REDUCTION (EQUAL To OR GREATER THAN 20%)

REPORT MONTH: December, 1996 Docket No.: 50-280 Unit Name: Surry Unit 1 Date: 01-02-97 Completed by: M. J. Fanguy Telephone: (804) 365-2155 (1) (2) (3) (4) (5)

Method Duration of LER . System _Component Cause & Corrective Action to Date Type Hours Reason Shutting No. Code Code Prevent Recurrence Down Rx None During the Reporting Period (1) (2) (3)

F: Forced REASON: METHOD:

S: Scheduled A - Equipment Failure (Explain) 1 - Manual B Maintenance or Test 2 - Manual Scram C Refueling 3 - Automatic Scram D Regulatory Restriction 4 - Other (Explain)

E Operator Training & Licensing Examination F Administrative G Operational Error (Explain)

(4) (5)

Exhibit G - Instructions for Preparation of Data Entry Sheets Exhibit 1 - Same Source for Licensee Event Report (LER) File (NU REG 0161)

- - Surry-Monthly Operating Report No. 96-12 Page 6 of 22 UNIT SHUTDOWN AND POWER REDUCTION

{EQUAL To OR GREATER THAN 20%}

REPORT MONTH: December, 1996 Docket No.: 50-281 Unit Name: Surry Unit 2 Date: 01-02-97 Completed by: M. J. Fanguy Telephone: (804) 365-2155 (1) (2) (3) (4) (5)

Method Duration of LER No. System Component Cause & Corrective Action to Date Type Hours Reason Shutting Code Code Prevent Recurrence Down Rx 12/12/96 s 250.4 B 3 96-006 SJ NA Scheduled maintenance outage to repair the letdown line (had automatic Rx trip from 11 % power due to steam flow/feed flow mismatch with low level on "A" SG).

(1) (2) (3)

F: Forced REASON: METHOD:

S: Scheduled A Equipment Failure (Explain) 1 - Manual B Maintenance or Test 2 - Manual Scram C Refueling 3 - Automatic Scram D Regulatory Restriction 4 - Other (Explain)

E Operator Training & Licensing Examination F Administrative G Operational Error (Explain)

(4) (5)

Exhibit G - Instructions for Preparation of Data Entry Sheets Exhibit 1 - Same Source for Licensee Event Report (LER) File (NU REG 0161)

- - Surry Monthly Operating

. Report No. 96-12 Page 7 of 22 AVERAGE DAILY UNIT POWER LEVEL Docket No.: 50-280 Unit Name: Surry Unit 1 Date: 01-05-97 Completed by: J. D. Kilmer Telephone: (804) 365-2792 MONTH: December, 1996 Average Daily Power Level Average Daily Power Level Day (MWe - Net) Day (MWe - Net) 824 17 821 2 824 18 819 3 813 19 819 4 821 20 813 5 822 21 802 6 826 22 799 7 824 23 815 8 824 24 820 9 821 25 823 10 824 26 820 11 823 27 822 12 825 28 823 13 820 29 823 14 820 30 824 15 822 31 824 16 822 INSTRUCTIONS On this format, list the average daily unit power level in MWe - Net for each day in the reporting month. Compute to the nearest whole megawatt.

_____J

~urry Monthly Operating Report J No. 96-12 Page 8 of 22 AVERAGE DAILY UNIT POWER LEVEL Docket No.: 50-281 Unit Name: Surry Unit 2 Date: 01-05-97 Completed by: John D. Kilmer Telephone: (804) 365-2792 MONTH: December, 1996 Average Daily Power Level Average Daily Power Level Day (MWe - Net) Day (MWe - Net) 822 17 0 2 821 18 0 3 824 19 0 4 826 20 0 5 827 21 0 6 827 22 0 7 828 23 203 8 828 24 818 9 827 25 825 10 827 26 826 11 828 27 826 12 801 28 825 13 5 29 825 14 0 30 825 15 0 31 825 16 0 INSTRUCTIONS On this format, list the average daily unit power level in MWe - Net for each day in the reporting month. Compute to the nearest whole megawatt.

. .urry Monthly Operating Report No. 96-12 Page 9 of 22

SUMMARY

OF OPERATING EXPERIENCE MONTHNEAR: December, 1996 The following chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents.

UNIT ONE:

12/01/96 0000 The reporting period began with the unit operating at 100% power, 850 MWe.

12/03/96 0925 Start power reduction to change out E/P controller for 1-FW-FCV-1478.

1017 Stopped power reduction at 90%, 770 MWe.

1206 Started power increase.

1345 Stopped power increase at 100%, 850 MWe.

12/31/96 2400 The reporting period ended with the unit operating at 100% power, 855 MWe.

UNIT Two:

12/01/96 0000 The reporting period began with the unit operating at 99% power, 850 MWe.

12/03/96 1538 Unit returned to 100% power, Computer calorimetric operable after failed Feedwater RTD replaced.

12/12/96 2102 Started power reduction in preparation for planned outage to repair the letdown line.

12/13/96 0235 Auto Reactor Trip from 11 % power due to steam flow/feed flow mismatch with low steam generator water level in the "A" steam generator.

12/23/96 0255 Commence Reactor Startup.

0348 Reactor critical.

1243 Unit on line, start power increase.

12/24/96 1548 Stopped power increase at 100%, 858 MWe.

12/31/96 2400 The reporting period ended with the unit operating at 100% power, 855 MWe.

-urry Monthly Operating Report No. 96-12 Page 10 of 22 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: December, 1996 FS 96-44 Updated Final Safety Analysis Report Change 12-02-96 (Safety Evaluation 96-150)

Section 14.3.2 of the UFSAR discusses the rupture of a main steam pipe. Questions have been raised about what is meant by the term "main steam lines."

This change adds information to clarify what is meant by the term "main steam lines."

Since this change is clarification of existing information only, no change to the meaning or intent of the UFSAR will be made. Therefore, an unreviewed safety question does not exist.

TM S2-96-28 Temporary Modification 12-3-96 (Safety Evaluation No.95-005 Rev.1)

Temporary Modification (TM) S2-96-28 installed a replacement resistance temperature device (RTD) in the local temperature indicator thermowell to provide the Unit 2 Steam Generator (SG) "8" inlet feedwater temperature.

The local temperature indicator thermowell is of the same design as the main RTD thermowell, except for length. An evaluation of this difference concluded, based on a comparison of previous temperature data, that a reliable and accurate indication of the SG "B" inlet feedwater temperature can be obtained. This modification did not reduce the Technical Specifications margin of safety. Therefore, an unreviewed safety question does not exist.

FS 96-47 - Updated Final Safety Analysis Report Change 12-5-96 (Safety Evaluation 96-154)

Currently, a note in UFSAR Table 6.2-2 and Section 6.2.2.1.1 states "any of the listed motor operated valves will actuate a combination light and alarm when one or more SIS valves are out of position." This does not accurately reflect actual plant control room indication, since not all of the SIS valves listed will actuate the "SIS Valves Out Of Position" alarm.

A review of the SI Design Basis Document and the applicable General Design Criteria for control room indication did not indicate any specific requirement for all SIS valves listed in Table 6.2-2 or those implied in Section 6.2.2.1.1 to actuate an alarm when out of position.

Sufficient monitoring exists to ensure that the SI valves are in their correct positions.

Therefore, an unreviewed safety question does not exist.

FS 96-49 Updated Final Safety Analysis Report Change 12-5-96 (Safety Evaluation 96-152)

Due to limited space, a change to the UFSAR is required to allow storage of QA records offsite at an approved facility.

Records will continue to be stored in accordance with the applicable ANSI commitments.

This change is administrative in nature with no modification to plant systems or components. Therefore, an unreviewed safety question does not exist.

.,,urry Monthly Operating Report No. 96-12 Page 11 of 22 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/VEAR: December, 1996 FS 96-41 Updated Final Safety Analysis Report Change 12-5-96 (Safety Evaluation 96-153)

This UFSAR change moves the stated numerical value of the auxiliary feedwater flow for the licensing basis Loss Of Normal Feedwater {LONF) event from Section 10.3.5.3 to Section 14.2.11.1.3 where the other analysis assumptions are located. The statement in Section 10.3.5.3 will be changed from "a minimum of 500 gpm of auxiliary feedwater flow

to "adequate auxiliary feedwater flow."

This change is administrative in nature with no modification to plant systems or components. Therefore, an unreviewed safety question does not exist.

FS 96-54 Updated Final Safety Analysis Report Change 12-5-96 (Safety Evaluation 96-155)

This UFSAR change updates Section 3.2.1 to be consistent with the current plant configuration. When the plant configuration was changed in 1984, Section 6.2 Safety Injection System and Section 14.3.2 accident analysis were updated but Section 3.2.1 was overlooked.

This UFSAR change updates Section 3.2.1 for consistency and has no physical impact on any plant system or component. Therefore, an unreviewed safety question does not exist.

DCP 95-023 Design Change Package 12-5-96

  • * (Safety Evaluation 95-129)

Design Change Package 95-023 replaced existing fire pump 1-FP-P-3 with a pump which meets the specified design requirements and provides the required pressure and flow capacity. Therefore, an unreviewed safety question does not exist.

SE 96-0021 Safety Evaluation 12-11-96 (Safety Evaluation 96-0021)

The NRC has approved the TN-32 Dry Storage Cask Topical Safety Analysis Report and a Surry ISFSI Technical Specification amendment for the use of this cask. This safety evaluation is performed to incorporate the use of the TN-32 storage cask into the Surry ISFSI Safety Analysis Report, Environmental Report and License Application.

The design and operation of the TN-32 cask is similar to that of the four cask designs already approved for use at the Surry ISFSI. There is no reduction in the margin of safety as defined in the basis for any Technical Specification. The current design basis for the Surry ISFSI was evaluated and remains bounding. Therefore, an unreviewed safety question does not exist.

e Surry Monthly Operating Report No. 96-12 Page 12 of 22 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: December, 1996 SE 96-0031 Safety Evaluation 12-11-96 (Safety Evaluation 96-0031)

This safety evaluation is performed to allow the revision of the ISFSI Safety Analysis Report for the storage of burnable poison rod assemblies and thimble plugging devices with the spent fuel in dry storage casks at the Surry ISFSI. The NRC issued a draft Standard Review Plan for Dry Cask Storage Systems which indicated that the:storage of "non-fuel core components" or "control assemblies" in dry storage casks is allowed, if they are described in the cask Topical Safety Analysis Report and included in the structural and shielding analyses.

The casks have been analyzed and it has been determined that the margin of safety has not been reduced by the storage of these core components since the cask and basket stresses remain below the allowable values during a cask end drop or tipover event.

Additionally, the existing surface dose rate limits in Technical Specification 3.3 still apply

- to ensure compliance with the dose rate limits for the ISFSI perimeter fence and nearest resident. Therefore, an unreviewed safety question does not exist.

SE 96-0041 Safety Evaluation 12-11-96 (Safety Evaluation 96-0041)

This safety evaluation assesses the as-built conditions of ISFSI Surry Pad 2 to determine whether this pad meets the criteria established by the NRC in their Safety Evaluation Report (SER) for cask drops or tipover of the Transnuclear TN-32 cask. A review of the pad design criteria was performed. The results of the review determined that the pad meets the criteria established by the NRC SER.

This change is administrative in nature with no modification to plant systems or components. Therefore, an unreviewed safety question does not exist.

SE 96-161 Safety Evaluation 12-11-96 (Safety Evaluation 96-161)

This safety evaluation assesses the update to the Small Break Loss of Coolant Accident (SBLOCA) analysis which is being incorporated into the licensing analysis basis for Surry Units 1 and 2.

The reanalysis of the SBLOCA was performed using Westinghouse LOCA-ECCS SBLOCA Evaluation Model. The analytical techniques are in full compliance with 10CFR50, Appendix K. The evaluation model is an approved methodology in the COLR list. This reanalysis used conservative assumptions with respect to existing limits and plant capabilities. The analysis results show that the emergency core cooling system will meet the acceptance criteria in 10CFR50.46. Therefore, an unreviewed safety question does not exist.

e .

  • Surry Monthly Operating Report

.. " No. 96-12 Page 13 of 22 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTHIYEAR: December, 1996 FS 96-59 Updated Final Safety Analysis Report Change 12-12-96 (Safety Evaluation 96-158)

Currently, UFSAR Sections 4.1.2.6 and 4.2.7.1 reference humidity indication as a method of monitoring containment coolant leakage. In 1978, the containment humidity monitoring instrumentation was abandoned in place.

Primary coolant system leakage is most readily detected by increased makeup requirements and by c secondary coolant system leak. Therefore, an unreviewed safety question does not exist.

FS 96-53 Updated Final Safety Analysis Report Change 12-12-96 (Safety Evaluation 96-157)

Currently, UFSAR Section 4.3.4.2 contains a statement "Two additional bottles charged to 2200 psig are connected to the system but isolated as spares" may lead to misinterpretation of the requirements associated with maintaining ready spares. A revision is needed to clarify current operating practices associated with the pressurizer PORV backup air supply system. The change will state "The two bottles that are not aligned to the manifold are initially fully charged and used as installed spare bottle capacity. The intent is to reduce the time required to reestablish bottle pressure when a low pressure alarm occurs with the unit at load. Instead of changing out bottles, the spare bottles need only be valved in." The intent of this change is to minimize the radiation exposure personnel would receive changing depleted bottles during power operations.

The backup air bottle pressure limits are set by the low temperature overpressure mitigating system, based on the assumption that no operator action is required for ten minutes. The air supply should be capable of providing 100 cycles. Two high pressure bottles are normally valved in with each bottle capable of 115 cycles at 1000 psig. The low pressure backup air annunicator alarms at 1000 psig. Therefore, an unreviewed safety question does not exist.

SE 96-158 Safety Evaluation 12-16-96 (Safety Evaluation No.96-159)

This safety evaluation assesses the impact of the "B" Circulating Water (CW) Pump being out of service for greater than 30 days. The purpose of the pump is to provide the water required to condense the turbine exhaust steam and supply water to the Service Water System by transferring water from the James River into a common intake canal for Units 1 and 2.

There are four CW pumps for each unit. The minimum requirement per Technical Specification (TS) 3.14 to support plant operation is two CW pumps. The TS requirement is satisfied and adequate canal level is maintained by the remaining operable CW pumps.

Therefore, an unreviewed safety question does not exist.

.,,urry Monthly Operating Report No. 96-12 Page 14 of 22 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: December, 1996 TM 82-96-030 Temporary Modification 12-17-96 (Safety Evaluation No.96-113 Rev. 1)

This Temporary Modification (TM) adds spray shields to protect the RCP flange studs from boric acid spray and reduce the amount of boric acid spray being drawn into the RCP motor. Additionally, this TM will provide remote monitoring of the RCP flange from the Main Control Room by the installation of a camera and lights in the "C" RCP Loop Room.

The spray shields will not affect the original configuration of the Reactor Coolant System or the loading on the primary loop piping supports. The shields will be secured in order to prevent them from becoming missiles during postulated earthquakes or high energy line breaks. The camera has no ties to existing station protection or control systems. The installation of equipment by this TM will not create an unreviewed safety question as described in 10CFR50.59. Therefore, an unreviewed safety question does not exist.

FS 96-55 Updated Final Safety Analysis Report Change 12-19-96 (Safety Evaluation 96-164)

UFSAR Section 9.9.1.3 is being revised to delete some details on specific times when actions would be taken prior to the arrival of a hurricane on site and the specified hurricane wind speed. UFSAR Section 9.10.4.18 will be revised to reflect the Circulating Water (CW) isolation valves as safety-related. This Section incorrectly identifies the valves as non safety-related.

The details removed from Section 9.9.1.3 are not vital to the hurricane actions. Important actions as described in Technical Report 0032 will remain in the UFSAR. The CW isolation valves that were described as non safety-related were installed and maintained as safety-related. These changes are administrative in nature with no modification to plant systems or components. Therefore, an unreviewed safety question does not exist.

FS 96-58 Updated Final Safety Analysis Report Change 12-19-96 (Safety Evaluation 96-163)

Currently, UFSAR Section 10.3.7.3 contains a statement indicating the non-safety related turbine generator DC bearing oil pump is required to function during a LOCA or loss of station power. Additionally, Section 10.3.7.4 contains a statement that the DC bearing oil pump will be tested on a monthly basis. Changes to the UFSAR Section 10.3.7.3 will state the DC bearing oil pump is designed to function during a loss of station power.

Section 10.3.7.4 will change the frequency of DC oil pump testing from "monthly" to "periodically."

Although the turbine generator DC bearing oil pump is designed to operate during a loss of station power, there is no design basis assumption that requires it to be operable during a LOCA or loss of station power. The testing frequency is governed by industry good practice and insurance carrier requirements. There are no Technical Specification or design basis assumption requirements for the monthly testing of the pump. Therefore, an unreviewed safety question does not exist.

~urry Monthly Operating Report No. 96-12 Page 15 of 22 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: December, 1996 SE 96-167 Safety Evaluation 12-20-96 (Safety Evaluation No.96-167)

This safety evaluation assesses continued Unit 2 power operation with a single Unit 2 RCP~1 C flange bolt preload stretch below the minimum required by the vendor. The flange bolts provide a structural connection between the flange and the pump casing and provide adequate preload and compression to the gasketed joint. The bolt has full thread engagement which meets the structural requirements. However, with the bolt preload below the required minimum some leakage may occur at the casing joint. A temporary modification was installed to monitor the flange area using a camera.

The probability of a rapid propagation type failure is not credible based on an evaluation performed by the vendor. The RC System pressure boundary will continue to accommodate the temperatures and pressures attained under all expected modes of station operations or anticipated transients, as well as maintain integrity without catastrophic rupture. Therefore, an unreviewed safety question does not exist.

SE 96-0051 Safety Evaluation 12-20-96 (Safety Evaluation No. 96-0051)

This safety evaluation assesses the continued storage of TN-32 Cask No.1 on the ISFSI pad with a pinhole leak in a weld. The weld connects the outer shell to the body of the cask. The cask is to remain on the ISFSI pad until appropriate procedures can be developed for the repair of the pinhole leak.

The function of the weld is to attach the outer skin to the cask body. The outer skin encloses the resin boxes which provide the primary neutron shielding for the cask. The presence of the pinhole could potentially allow the contents of the atmosphere inside the resin chamber to escape as the cask reaches equilibrium temperature. The gases given off by the resin during heatup could include carbon dioxide, carbon monoxide and other hydrocarbons. Gas samples taken from the leakage site determined that no radioisotopes were present and that the primary constituents of the sample were nitrogen and oxygen in the percentages that would indicate that the leaking gas was air. No helium was detected and a smear taken of the area was not contaminated. The release of a small amount of these gases will not result in any detrimental environmental or radiological conditions. Therefore, an unreviewed safety question does not exist.

~urry Monthly Operating Report No. 96-12 Page 16 of 22 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTHNEAR: December, 1996 O-ICM-EH-CAB-001 Instrument Corrective Maintenance 12-12-96 (Safety Evaluation No.96-156)

Instrument Corrective Maintenance Procedure O-ICM-EH-CAB-001, "EHC System Diagnostic Checks," was revised to provide instructions for a procedurally controlled temporary test lead. This will allow the collection of test data using a recorder during the Unit 2 ramp down to investigate a possible signal problem with the governor valve control system.

Should the governor valves begin to open, the valve position limiting circuit would act to limit the power increase. Should the valve limiter fail, the resultant load increase is still bounded by the current safety analyses. The physical limit on steam flow through all governor valves wide open (105%) is bounded by the analyzed step load increase safety analysis limit (116%). Should a step load decrease occur, the plant response would be within the current design requirements and the reactor protection system would function as required. Therefore, an unreviewed safety question does not exist.

1(2)-NSP-SD-001 Engineering Surveillance Procedure 12-16-96 (Safety Evaluation No.96-162)

Engineering Surveillance Procedure 1(2)-NSP-SD-001, "Optimum Feedwater Heater Level Test," provides instructions for determining/calculating the optimum water level in the shell side of feedwater heaters 1A, 1B, 3A, 3B, 4A, 4B, 5A, 5B. This will maximize the efficiency of the feedwater heaters, increasing overall plant efficiency.

This test will affect the efficiency of the feedwater heaters, but will not affect the operation of the heaters. The heaters will operate as required, but with different setpoints for liquid level. Therefore, an unreviewed safety question does not exist.

SE 96-160 Safety Evaluation 12-16-96 (Safety Evaluation No.96-160)

Safety evaluation 96-160 was performed to assess the acceptability of continued usage of the procedure O-OSP-RM-002 to check source the Component Cooling Radiation Monitors in accordance with Technical Specification requirements, although the methodology differs from that stated in the UFSAR. This condition will continue until June 1997 when the Main Control Room Radiation Monitoring Cabinet portion of the Design Change is installed.

The evaluation establishes the acceptability of the current method of source checking the Component Cooling Water Radiation Monitors and does not affect any safety related equipment. Therefore, an unreviewed safety question does not exist.

.. L

- ~urry Monthly Operating Report No. 96-12 Page 17 of 22 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: December, 1996 O-IMP-BR-001 Instrument Maintenance Procedure 12-19-96 (Safety Evaluation No.96-166)

Instrument Maintenance Procedure O-IMP-BR-001, "Monitoring of Boron Recovery Tank During Reactor Coolant System Drain Down Evolutions," provides instructions to connect a calibrated 250 ohm resistor in series in the Boron Recovery Tank (BRT) level instrumentation loop. This will allow a chart recorder to be connected across the resistor to allow accurate monitoring of RCS inventory during RCS draining evolutions.

The system is passive and its characteristics will be unchanged. The "Channel Operation and Accuracy" Section of the affected tank's level calibration procedure will be completed once the resistor is installed. The BRT high and low level alarms, which are not safety related, will be unaffected by this activity. Therefore, an unreviewed safety question does not exist.

O-AP-23.01 Abnormal Procedure 12-19-96 (Safety Evaluation No.96-165)

Abnormal Procedure O-AP-23.01, "Rapid RCS Cooldown," was revised to modify the current practice of borating to Cold Shutdown boron prior to initiating a cooldown and blocking Safety Injection to a method of concurrent borations and cooldown. In addition, this change increases the current administrative Reactor Coolant System (RCS) cooldown rate from 50 °F/hr to 75 °F/hr while above the Low Temperature Overpressure Mitigation System {LTOPs) enabling temperature of 350 °F. Below the LTOPs enabling temperature of 350 °F, the current administrative cooldown rate of 50 °F/hr is still

.. applicable.

The proposed changes do not alter the design or principles of operation of the CVCS or any associated safety related system. Therefore, the probability of the malfunction of equipment important to safety is not increased, and no new or unique equipment malfunction scenarios are created. Since the CVCS is not relied on for accident mitigation, the consequences of the CVCS malfunction has not increased. The exception is when the plant is aligned to Safety Injection and the Charging Pumps are considered High Head Safety Injection Pumps. Inadvertent boron dilution by addition of primary grade water to the RCS is addressed in the UFSAR and this analysis remains bounding.

The severity of an inadvertent dilution with the proposed changes would be less severe than the bounding analysis. Therefore, an unreviewed safety question does not exist.

~urry Monthly Operating Report

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No. 96-12 Page 18 of 22 TESTS AND EXPERIMENTS THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: December, 1996 None During the Reporting Period

~urry Monthly Operating Report

.,.. No. 96-12 I, Page 19 of 22 CHEMISTRY REPORT MONTHNEAR: December, 1996 Unit No. 1 Unit No. 2 Primarv Coolant Analysis Max. Min. Avg. Max. Min. Avg.

Gross Radioactivity, µCi/ml 9.55E-1 4.97E-2 7.21 E-1 4.10E-1 2.27E-3 1.44E-1 Suspended Solids, ppm sO.D10 so.010 so.010 2.5 so.010 0.389 Gross Tritium, µCi/ml 3.30E-1 2.38E-1 2.85E-1 6.32E-1 1.73E-1 4.00E-1 1131, µCi/ml 1.15E-2 8.07E-3 9.43E-3 9.36E-5 1.15E-5 4.65E-5 113111133 0.41 0.23 0.29 0.11 0.06 0.08 Hydrogen, cc/kg 40.1 31.2 36.6 31 1.7 16.6 Lithium, oom 1.67 1.24 1.53 3.69 0.10 1.43 Boron - 10, ppm* 47.4 28.4 37.6 346.7 192.1 289.6 Oxygen, (DO), ppm s0.005 s0.005 s0.005 6.0 s0.005 0.18 Chloride, ppm 0.004 <0.001 0.002 0.008 0.002 0.004 pH at 25 deqree Celsius 7.30 6.78 6.98 6.81 4.79 5.61

None

' '. e ~urry Monthly Operating Report I.

No. 96-12 Page 20 of 22 FUEL HANDLING UNITS 1 & 2 MONTH/YEAR: December, 1996 New or Spent Number of New or Spent Fuel Shipment Date Stored or Assemblies Assembly ANSI Initial Fuel Shipping Number Received per Shipment Number Number Enrichment Cask Activity Spent Fuel Cask TN-32-01 12/18/96 32 N40 NOANSI 2.5560 6P2 LM05YN 3.6070 N44 NOANSI 2.5560 N46 NOANSI 2.5560 N33 NOANSI 2.5560 D02 LM007P 3.3250 D25 LM007D 3.3250 D39 LM0075 3.3250 2E8 LMODEP 2.5933 N34 NOANSI 2.5560 D31 LM0084 3.3250 D05 LM008E 3.3250 D14 LM007U 3.3250 D41 LMOOCA 3.3250 D50 LM0073 3.3250 N42 NOANSI 2.5560 N38 NOANSI 2.5590 D06 LM008F 3.3250 D49 LM007G 3.3250 D43 LM007J 3.3250 V17 LM041K 2.9060 6P4 LM05YR 3.6070 N39 NOANSI 2.5560 2E7 LMODFH 3.6028 D33 LM008K 3.3250 D46 LMOOCD 3.3250

' ' . ~Surry Monthly Operating

. Report No. 96-12

"*. J Page 21 of 22 FUEL HANDLING UNITS 1 & 2 MONTHNEAR: December, 1996 New or Spent Number of New or Spent Fuel Shipment Date Stored or Assemblies Assembly ANSI Initial Fuel Shipping Number Received per Shipment Number Number Enrichment Cask Activity V19 LM042H 2.9060 N45 NOANSI 2.5560 N41 NOANSI 2.5560 N43 NOANSI 2.5560 6P8 LM009PA 3.6070 N47 NOANSI 2.5560

tturry Monthly Operating Report No. 96-12 Page 22 of 22 DESCRIPTION OF PERIODIC TEST(S) WHICH WERE NOT COMPLETED WITHIN THE TIME LIMITS SPECIFIED IN TECHNICAL SPECIFICATIONS MONTH/YEAR: December, 1996 None During the Reporting Period