ML12102A043: Difference between revisions
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{{#Wiki_filter:4/6/2012Fort Calhoun Station Public Meeting with the Nuclear Regulatory Commission April 4, 2012 DAVIDBANNISTER OPENINGREMARKSFortCalhounStation VicePresident&ChiefNuclearOfficer 4/6/2012 PerformanceInitiatives*IntegratedPerformanceImprovementPlan*PlantStatus*In depthReviews*Look Ahead 4/6/2012 RONSHORTINTEGRATEDPERFORMANCEIMPROVEMENTPLANSTATUSFortCalhounStationRecoveryManager 4/6/2012 4/6/2012IntegratedPerformanceImprovementPlan 4/6/2012 4/6/2012 Systematicapproachtoperformanceimprovement-fourphases 4/6/2012AnalysisEvaluatesignificanceandtrendsIdentifyfundamentalperformancedeficienciesImplementcorrectiveaction FlooddamagerepaircompleteFloodinglessonslearnedincludedinplantproceduresRemainingissuesaddedtoIPIP 4/6/2012 | |||
*4160/480voltAC*125voltDC/EmergencyBatteries*HighPressureSafetyInjection 4/6/2012 | |||
*Selectionbasedonnuclearsafetysignificance | |||
*Sixkeyattributesaddressed-Design-EquipmentPerformance | |||
-ConfigurationControl-ProcedureQuality-HumanPerformance | |||
-EmergencyResponseOrganizationReadiness 4/6/2012 | |||
*Reviewofprocessesforfindingandfixingproblems*Tenassessmentareas-Auditsandoversight-HistoricalDataReviewandtrending 4/6/2012 | |||
*Areasoffocus:-Survey-Interviews:One on oneandfocusgroups-Observationsanddocumentreviews*Conductedbyrecognizedexperts*ResultsdiscussedwithNRCandatafuturepublicmeeting 4/6/2012 | |||
*ScopeResolutionofdesignandprogramissues:-Vendormanuals-Equipmentservicelife-Degraded/nonconformingconditions | |||
-Vendordesignchanges 4/6/2012 Summary*IntegratedImprovementplanestablished | |||
*Staffingandresourcesinplace*Workhasbegun*Progressisbeingmade 4/6/2012 WOODYGOODELLCORRECTIVEACTIONPROGRAMFortCalhounStation DivisionManager 4/6/2012 | |||
*ImprovedCAPcultureKeytoStationimprovementComprehensiveprogramimprovementTrainingbeingcompleted 4/6/2012 4/6/2012*Enhancedmanagementinvolvement | |||
*Reinforcingbehaviors*Multidisciplinaryscreeningteam*Establishednewpositions 4/6/2012*SafetyCultureAssessmentwillrefineactions*Behavioralchangestaketime*Seeingimprovements | |||
*Futurestate MIKEPROSPERO PLANTSTATUSFortCalhounStationPlantManager 4/6/2012 21 4/6/2012 June2011March2012August2011August2011 PlantStatus 4/6/2012 June2011March2012 LookingDowntheAccessRoadtowardsthePlant PlantStatus 4/6/2012 June2011March2012ViewofPlantfromAccessBridge PlantStatus 4/6/2012 June2011March2012WalkwayExitingthePlant PlantStatus 4/6/2012 June2011March2012ViewofRiverfromPlant PlantStatus 4/6/2012 FloodCleanupActivities PlantStatus*Plantincoldshutdown*Safecondition*Maintenanceandtestingactivitiesinprogress 4/6/2012 PlantStatus*MeteorologicalTower-Outofserviceduetoflooding-ReceivedweatherinformationfromothersourcesOperational 4/6/2012 PlantStatus*Electrical equipment restorationFire damaged electrical equipment repairedTestedRe-energizedReturned to normal electrical alignment 4/6/2012RestoredSwitchgear1B4A LessonsLearnedProceduralGuidanceUpgraded FORTCALHOUNSTATIONFCSG 63,"EstablishingIncidentCommand"implementedFCSG 64,"ExternalFloodingofSite"implemented OMAHAPUBLICPOWERDISTRICTBusinessContinuityPlanupdatedtoincorporatelessonslearned LessonsLearned AbnormalOperatingProcedureEnhancedAOP 01,"ActsofNature"updatedwithenhancedfloodingactions. | |||
LessonsLearnedEPIPTSC 2,"CatastrophicFloodingPreparations"updated LessonsLearned ACPowerReliabilityReEvaluatedbasedonFloodingEventLengthNewmethodtotransferdieselfuelduringflooding LessonsLearned BuildingandFloorPenetrationsSealedandCertifiedApproximately375penetrations(electricalconduit,pipingruns,etc.)weresealedandcertified LessonsLearned BelowGroundSurveysConductedNosignificantimpactsidentified todate FloodReadinessIntakestructure*Evaluatingequipmentclassification | |||
*Changedoperatingprocedures | |||
*Actionsneededtoprotectthesluicegatesandmotoroperatedvalvesfromriverdebrisduringaflood*Interimcompensatorymeasures 4/6/2012 PlantStatus PublicWarningSirens*101Sirens*SeverallostpowerduringfloodSirensoperable*RecentSirenOutage NRCInspectionReadiness*Actionstoimproveinspectionreadiness-Detailedselfassessments 4/6/2012 NRCInspectionReadiness*Actionstoimproveinspectionreadiness-Seniormanagementledchallengeboards 4/6/2012 | |||
*TriennialFireProtectionInspectionConductedLastWeek*Firstoftwoweeksofinspection(willbebackApril9 th)*WorkingonitemsidentifiedNRCInspectionReadiness 4/6/2012 NRCInspectionReadiness*EmergencyPlanningInspectionConductedLastWeekEvaluatedExercisewithStatesandCounties 4/6/2012"TheNuclearRegulatoryCommissionconcludedthattheoverallEmergencyPlanningOrganizationperformancecontinuedtoprovideconfidenceinFortCalhoun'sabilitytoimplementthemajorelementsoftheemergencyplanandprotectthehealthandsafetyofthepublic."SeniorInspector,NRCRegionIV JOHNHERMANELECTRICALFIREFortCalhounStation DivisionManagerEngineering 4/6/2012 480VoltLoadCenter 4/6/2012 480VoltLoadCenter 4/6/2012 LoadCenterwithBreaker 4/6/2012 Event*June7,2011-Electricalfaultcausedafirein480voltloadcenter1B4A-Firedamagerequiredcompletereplacementofloadcenter1B4A-Nootherloadcentersweredamagedbythefire 4/6/2012 Event*Sootfromthefirecausedsupplybreaker1B3Atotriponovercurrent-Breakerwasresetandpowerrestoredto1B3A-Therewasnodamagetoloadcenter1B3A 4/6/2012 Priorities | |||
*Safety*Quality*Timeliness 4/6/2012 4/6/2012 LookingDowntheAccessRoadtowardsthePlantElevatedWalkwaystogetaroundplant ResponseActivities | |||
*FireoccurredonTuesday,June7,2011*AforensicengineeringcompanywasonsitetobeginfireinvestigationbyFriday*Demolitionworkcouldnotbeginuntilfireinvestigationwascomplete 4/6/2012 ResponseActivities | |||
*Replacementelectricalequipmenthadtobecustombuilttofittheexistingequipment*Twooptionsconsidered: | |||
-Buildtheentireloadcenteroffsite-Rebuildinplaceonesite 4/6/2012 Duetoflooding,materialstorebuildonsitehadtobebroughtinviabarge ResponseActivities | |||
*Workhadtobeperformedinseriestoensurenomorethanoneadditionalloadcenterwasremovedatatime*Engineeringdesignpackage*1B3Arootcauseanalysis 4/6/2012 ResponseTimeline*6/7/11Fireevent*6/10/11Engineeringworkstarted*7/23/11Demolitionandreconstructionworkstarted*8/29/11Floodlevelbelow1004'msl-siterecoverystarted*9/12/11Rootcauseanalysisforfirecompleted*10/27/11Reconstructionworkfinished*12/9/11Extentofconditionworkcompleted*2/17/12Engineeringworkcompleted*3/5/121B4Aloadcenterenergizedfortesting 4/6/2012 LessonsLearned*Followingthefire,theFortCalhounStation:-Actedpromptlytoinvestigatethefire-Determinedthecause-Begantheengineeringwork-Procurenewelectricalequipment 4/6/2012 LessonsLearned*TimelycompletionofEOCwork*Timelycompletionofdesignpackage*Appropriateresourcesallocated 4/6/2012 RootCauseAnalysisTerminology | |||
*DirectCause-thephysicalconditionthatcreatedthefailure*RootCause thesituationthatallowedthephysicalconditiontoexist,ifcorrectedwouldhavepreventedtheeventfromoccurring 4/6/2012 RootCauseAnalysisTerminology | |||
*ContributingCause-increasesthelikelinessorseverityofanoccurrence*ExtentofCondition-describesotherequipmentthatcouldhavethesamephysicalconditionthatledtothefailure*ExtentofCause-describeshowtherootcausecouldimpactotherequipmentandprocesses 4/6/2012 CurrentRootCauseAnalysis*Directcauseofthefireinloadcenter1B4A-Highresistanceelectricalconnectionfailed*Directcauseofthe1B3Abreakertrip-Overcurrentcondition 4/6/2012CircuitBreakerFinger&Stab Bus tiebreakerand1B3Asupplybreakerbothtripped 4/6/2012 480VoltLoadCenter 4/6/2012 1B3ABreaker*Thetwobreakerswereremovedfromtheplantandtestedtogetheratthetestingfacility 4/6/2012 1B3ABreakerJumper 4/6/2012 1B3ABreaker*Designchangeproceduresdonotprovideguidancetoevaluatetheimpactofunuseddesignfeatures*Trainingnotprovidedonuniquefeaturesofnewequipment 4/6/2012 CorrectiveActions*Demolitionandclean upafterthefire*Fabricationandreconstructionof1B4A*Extentofconditioninvestigationsandrepairsonother480VACcircuitbreakers*Removehardenedgrease 4/6/2012 CorrectiveActions 4/6/2012 CorrectiveActionsProcedureswerechangedtoincludespecificguidanceonidentifyingcriticalcharacteristicsExpandedtherequirementsforresearchingoperatingexperienceduringdesignprocessMoredetailedinstructionsforcleaningbreakerstabs 4/6/2012 CorrectiveActionsReviewofinprogressmodificationsReviewofpreviouslycompletedmodifications(inprogress)Newthermographyprocedureforinvestigatingunusual"odors"Qualityauditofequipmentsupplier 4/6/2012 CorrectiveActionsVerifiedotherjumpersinstalledcorrectlyIdentifiedotherequipmentsuppliedby samevendor 4/6/2012 4/6/2012 DAVIDBANNISTERLOOKAHEADANDCLOSINGREMARKSFortCalhounStation VicePresident&ChiefNuclearOfficer 4/6/2012}} |
Revision as of 05:27, 2 August 2018
ML12102A043 | |
Person / Time | |
---|---|
Site: | Fort Calhoun |
Issue date: | 04/04/2012 |
From: | Omaha Public Power District |
To: | NRC/RGN-IV/DRP |
References | |
Download: ML12102A043 (70) | |
Text
4/6/2012Fort Calhoun Station Public Meeting with the Nuclear Regulatory Commission April 4, 2012 DAVIDBANNISTER OPENINGREMARKSFortCalhounStation VicePresident&ChiefNuclearOfficer 4/6/2012 PerformanceInitiatives*IntegratedPerformanceImprovementPlan*PlantStatus*In depthReviews*Look Ahead 4/6/2012 RONSHORTINTEGRATEDPERFORMANCEIMPROVEMENTPLANSTATUSFortCalhounStationRecoveryManager 4/6/2012 4/6/2012IntegratedPerformanceImprovementPlan 4/6/2012 4/6/2012 Systematicapproachtoperformanceimprovement-fourphases 4/6/2012AnalysisEvaluatesignificanceandtrendsIdentifyfundamentalperformancedeficienciesImplementcorrectiveaction FlooddamagerepaircompleteFloodinglessonslearnedincludedinplantproceduresRemainingissuesaddedtoIPIP 4/6/2012
- 4160/480voltAC*125voltDC/EmergencyBatteries*HighPressureSafetyInjection 4/6/2012
- Selectionbasedonnuclearsafetysignificance
- Sixkeyattributesaddressed-Design-EquipmentPerformance
-ConfigurationControl-ProcedureQuality-HumanPerformance
-EmergencyResponseOrganizationReadiness 4/6/2012
- Reviewofprocessesforfindingandfixingproblems*Tenassessmentareas-Auditsandoversight-HistoricalDataReviewandtrending 4/6/2012
- Areasoffocus:-Survey-Interviews:One on oneandfocusgroups-Observationsanddocumentreviews*Conductedbyrecognizedexperts*ResultsdiscussedwithNRCandatafuturepublicmeeting 4/6/2012
- ScopeResolutionofdesignandprogramissues:-Vendormanuals-Equipmentservicelife-Degraded/nonconformingconditions
-Vendordesignchanges 4/6/2012 Summary*IntegratedImprovementplanestablished
- Staffingandresourcesinplace*Workhasbegun*Progressisbeingmade 4/6/2012 WOODYGOODELLCORRECTIVEACTIONPROGRAMFortCalhounStation DivisionManager 4/6/2012
- ImprovedCAPcultureKeytoStationimprovementComprehensiveprogramimprovementTrainingbeingcompleted 4/6/2012 4/6/2012*Enhancedmanagementinvolvement
- Reinforcingbehaviors*Multidisciplinaryscreeningteam*Establishednewpositions 4/6/2012*SafetyCultureAssessmentwillrefineactions*Behavioralchangestaketime*Seeingimprovements
- Futurestate MIKEPROSPERO PLANTSTATUSFortCalhounStationPlantManager 4/6/2012 21 4/6/2012 June2011March2012August2011August2011 PlantStatus 4/6/2012 June2011March2012 LookingDowntheAccessRoadtowardsthePlant PlantStatus 4/6/2012 June2011March2012ViewofPlantfromAccessBridge PlantStatus 4/6/2012 June2011March2012WalkwayExitingthePlant PlantStatus 4/6/2012 June2011March2012ViewofRiverfromPlant PlantStatus 4/6/2012 FloodCleanupActivities PlantStatus*Plantincoldshutdown*Safecondition*Maintenanceandtestingactivitiesinprogress 4/6/2012 PlantStatus*MeteorologicalTower-Outofserviceduetoflooding-ReceivedweatherinformationfromothersourcesOperational 4/6/2012 PlantStatus*Electrical equipment restorationFire damaged electrical equipment repairedTestedRe-energizedReturned to normal electrical alignment 4/6/2012RestoredSwitchgear1B4A LessonsLearnedProceduralGuidanceUpgraded FORTCALHOUNSTATIONFCSG 63,"EstablishingIncidentCommand"implementedFCSG 64,"ExternalFloodingofSite"implemented OMAHAPUBLICPOWERDISTRICTBusinessContinuityPlanupdatedtoincorporatelessonslearned LessonsLearned AbnormalOperatingProcedureEnhancedAOP 01,"ActsofNature"updatedwithenhancedfloodingactions.
LessonsLearnedEPIPTSC 2,"CatastrophicFloodingPreparations"updated LessonsLearned ACPowerReliabilityReEvaluatedbasedonFloodingEventLengthNewmethodtotransferdieselfuelduringflooding LessonsLearned BuildingandFloorPenetrationsSealedandCertifiedApproximately375penetrations(electricalconduit,pipingruns,etc.)weresealedandcertified LessonsLearned BelowGroundSurveysConductedNosignificantimpactsidentified todate FloodReadinessIntakestructure*Evaluatingequipmentclassification
- Changedoperatingprocedures
- Actionsneededtoprotectthesluicegatesandmotoroperatedvalvesfromriverdebrisduringaflood*Interimcompensatorymeasures 4/6/2012 PlantStatus PublicWarningSirens*101Sirens*SeverallostpowerduringfloodSirensoperable*RecentSirenOutage NRCInspectionReadiness*Actionstoimproveinspectionreadiness-Detailedselfassessments 4/6/2012 NRCInspectionReadiness*Actionstoimproveinspectionreadiness-Seniormanagementledchallengeboards 4/6/2012
- TriennialFireProtectionInspectionConductedLastWeek*Firstoftwoweeksofinspection(willbebackApril9 th)*WorkingonitemsidentifiedNRCInspectionReadiness 4/6/2012 NRCInspectionReadiness*EmergencyPlanningInspectionConductedLastWeekEvaluatedExercisewithStatesandCounties 4/6/2012"TheNuclearRegulatoryCommissionconcludedthattheoverallEmergencyPlanningOrganizationperformancecontinuedtoprovideconfidenceinFortCalhoun'sabilitytoimplementthemajorelementsoftheemergencyplanandprotectthehealthandsafetyofthepublic."SeniorInspector,NRCRegionIV JOHNHERMANELECTRICALFIREFortCalhounStation DivisionManagerEngineering 4/6/2012 480VoltLoadCenter 4/6/2012 480VoltLoadCenter 4/6/2012 LoadCenterwithBreaker 4/6/2012 Event*June7,2011-Electricalfaultcausedafirein480voltloadcenter1B4A-Firedamagerequiredcompletereplacementofloadcenter1B4A-Nootherloadcentersweredamagedbythefire 4/6/2012 Event*Sootfromthefirecausedsupplybreaker1B3Atotriponovercurrent-Breakerwasresetandpowerrestoredto1B3A-Therewasnodamagetoloadcenter1B3A 4/6/2012 Priorities
- Safety*Quality*Timeliness 4/6/2012 4/6/2012 LookingDowntheAccessRoadtowardsthePlantElevatedWalkwaystogetaroundplant ResponseActivities
- FireoccurredonTuesday,June7,2011*AforensicengineeringcompanywasonsitetobeginfireinvestigationbyFriday*Demolitionworkcouldnotbeginuntilfireinvestigationwascomplete 4/6/2012 ResponseActivities
- Replacementelectricalequipmenthadtobecustombuilttofittheexistingequipment*Twooptionsconsidered:
-Buildtheentireloadcenteroffsite-Rebuildinplaceonesite 4/6/2012 Duetoflooding,materialstorebuildonsitehadtobebroughtinviabarge ResponseActivities
- Workhadtobeperformedinseriestoensurenomorethanoneadditionalloadcenterwasremovedatatime*Engineeringdesignpackage*1B3Arootcauseanalysis 4/6/2012 ResponseTimeline*6/7/11Fireevent*6/10/11Engineeringworkstarted*7/23/11Demolitionandreconstructionworkstarted*8/29/11Floodlevelbelow1004'msl-siterecoverystarted*9/12/11Rootcauseanalysisforfirecompleted*10/27/11Reconstructionworkfinished*12/9/11Extentofconditionworkcompleted*2/17/12Engineeringworkcompleted*3/5/121B4Aloadcenterenergizedfortesting 4/6/2012 LessonsLearned*Followingthefire,theFortCalhounStation:-Actedpromptlytoinvestigatethefire-Determinedthecause-Begantheengineeringwork-Procurenewelectricalequipment 4/6/2012 LessonsLearned*TimelycompletionofEOCwork*Timelycompletionofdesignpackage*Appropriateresourcesallocated 4/6/2012 RootCauseAnalysisTerminology
- DirectCause-thephysicalconditionthatcreatedthefailure*RootCause thesituationthatallowedthephysicalconditiontoexist,ifcorrectedwouldhavepreventedtheeventfromoccurring 4/6/2012 RootCauseAnalysisTerminology
- ContributingCause-increasesthelikelinessorseverityofanoccurrence*ExtentofCondition-describesotherequipmentthatcouldhavethesamephysicalconditionthatledtothefailure*ExtentofCause-describeshowtherootcausecouldimpactotherequipmentandprocesses 4/6/2012 CurrentRootCauseAnalysis*Directcauseofthefireinloadcenter1B4A-Highresistanceelectricalconnectionfailed*Directcauseofthe1B3Abreakertrip-Overcurrentcondition 4/6/2012CircuitBreakerFinger&Stab Bus tiebreakerand1B3Asupplybreakerbothtripped 4/6/2012 480VoltLoadCenter 4/6/2012 1B3ABreaker*Thetwobreakerswereremovedfromtheplantandtestedtogetheratthetestingfacility 4/6/2012 1B3ABreakerJumper 4/6/2012 1B3ABreaker*Designchangeproceduresdonotprovideguidancetoevaluatetheimpactofunuseddesignfeatures*Trainingnotprovidedonuniquefeaturesofnewequipment 4/6/2012 CorrectiveActions*Demolitionandclean upafterthefire*Fabricationandreconstructionof1B4A*Extentofconditioninvestigationsandrepairsonother480VACcircuitbreakers*Removehardenedgrease 4/6/2012 CorrectiveActions 4/6/2012 CorrectiveActionsProcedureswerechangedtoincludespecificguidanceonidentifyingcriticalcharacteristicsExpandedtherequirementsforresearchingoperatingexperienceduringdesignprocessMoredetailedinstructionsforcleaningbreakerstabs 4/6/2012 CorrectiveActionsReviewofinprogressmodificationsReviewofpreviouslycompletedmodifications(inprogress)Newthermographyprocedureforinvestigatingunusual"odors"Qualityauditofequipmentsupplier 4/6/2012 CorrectiveActionsVerifiedotherjumpersinstalledcorrectlyIdentifiedotherequipmentsuppliedby samevendor 4/6/2012 4/6/2012 DAVIDBANNISTERLOOKAHEADANDCLOSINGREMARKSFortCalhounStation VicePresident&ChiefNuclearOfficer 4/6/2012