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{{Adams | |||
| number = ML20217B698 | |||
| issue date = 04/21/1998 | |||
| title = Insp Rept 50-382/98-06 on 980201-0321.Violations Noted.Major Areas Inspected:Operations,Maint & Engineering | |||
| author name = Harrell P | |||
| author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) | |||
| addressee name = | |||
| addressee affiliation = | |||
| docket = 05000382 | |||
| license number = | |||
| contact person = | |||
| document report number = 50-382-98-06, 50-382-98-6, NUDOCS 9804230113 | |||
| package number = ML20217B670 | |||
| document type = INSPECTION REPORT, NRC-GENERATED, TEXT-INSPECTION & AUDIT & I&E CIRCULARS | |||
| page count = 21 | |||
}} | |||
See also: [[see also::IR 05000382/1998006]] | |||
=Text= | |||
{{#Wiki_filter:l | |||
4 | |||
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ENCLOSURE 2 | |||
U.S. NUCLEAR REGU'ATORY COMMISSION | |||
REGION IV | |||
. Docket No.: 50-382 | |||
License No.: NPF-38 | |||
Report No.: 50-382/98-06 | |||
Licensee: Entergy Operations, Inc. | |||
Facility: Waterford Steam Electric Station, Unit 3 | |||
Location: Hwy.18 | |||
Killona, Louisiana | |||
Dates: February 1 through March 21,1998 | |||
Inspectors: J. M. Keeton, Resident inspector | |||
D. R. Lanyi, Resident inspector, Region 11 | |||
Accompanied By: J. C. Edgerly, Resident inspector Trainee | |||
M. A. Kotzalas, NRC Headquarters intern | |||
Approved By: P. H. Harrell, Chief, Project Branch D | |||
ATTACHMENT: Supplemental Information | |||
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9804230113 980421 | |||
PDR ADOCK 05000382 | |||
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EXECUTIVE SUMMARY | |||
Waterford Steam Electric Station, Unit 3 | |||
NRC Inspection Report 50-382/98-06 | |||
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This routine, announced inspection included aspects of operations, maintenance, engineering i | |||
and plant support activities. The report covers a 7-week period of resident inspection. ! | |||
Ooerations I | |||
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- The licensed operators performed in a professional manner and demonstrated excellent | |||
knowledge and understanding of the safety consequences of the loss of instrument | |||
power event (Section 01.1). | |||
. In general, control room activities were conducted in a very good manner (Section 01.2). | |||
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Inattentiveness to licensed duties by a senior reactor operator resulted in a noncited | |||
violation of Technical Specification (TS) shift-manning requirements when both the shift | |||
superintendent (SS) and the control room supervisor (CRS) were absent from the control | |||
room for 1 minute 38 seconds (Section O4.1). | |||
Maintenance | |||
+ The performance of the check valve leakage surveillance adequately tested the valves. | |||
The inspectors noted good procedural compliance and good questioning attitudes by all | |||
of the operations personnelinvolved in the test (Section M1.1). | |||
* The inspectors determined that the emergency feedwater turbine-driven pump | |||
surveillance was performed in accordance with approved procedures. The operators | |||
were knowledgeable about the test (Section M1.2). | |||
. Valve CVC-103 did not properly perform all its design functions during an event. A | |||
violation resulted because testing was not performed after completion of maintenance | |||
(Section M1.3). | |||
- Personnel failed to implement broad, effective corrective actions following the spent fuel | |||
pool overflow event. Specifically, a violation was identified because the licensee failed to | |||
review the stop nut adjustment on similar valves since the stop nut adjustment was | |||
considered a contributing factor to the overflow of the spent fuel pool (Section M2.1). | |||
- - _ . _ _ - | |||
- Engineers had been responsive to the need for developing a technical failure mechanism | |||
for a plant protective system relay (Section E1.1). | |||
* An engineer inappropriately operated equipment in the plant without the SS or CRS | |||
knowledge or concurrence. This was a repeat of a similar occurrence within the last | |||
2-years, and this issue is being treated as a violation (Section E5.1). | |||
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The engineering review and the revised procedures for control of volatile organic | |||
compounds (VOC) was acceptable. This issue is being treated as a noncited violation | |||
(Section E8.1). | |||
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Reoort Details | |||
) | |||
Summary of Plant Status | |||
During this inspection period, the plant operated at essentially 100 percent power. | |||
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1. Operations | |||
01 Conduct of Operations (71707) | |||
01.1 Loss of Static Uninterruotible Power Sucolv (SUPS) B | |||
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a. Insoection Scoce (71707) | |||
The inspectors observed the control room operators during the response to a loss of ) | |||
SUPS B, the activities involved in prioritizing recovery of power to the SUPS B | |||
distribution panel, and recovery of plant instruments required for continued plant | |||
operation. | |||
b. Observations and Findinas | |||
On February 4,1998, SUPS B failed and caused a loss of electrical power to | |||
instrumentation required for continued plant operation. The CRS entered | |||
Procedures OP-901-112, " Charging or Letdown Malfunction," and OP-901-312, " Loss of | |||
Vital Instrument Bus." The inspectors observed the CRS directing licensed operators in | |||
accordance with the applicable off-normal procedures. The SS directed the shift | |||
technical advisor to verify which TS were in effect and to track time clocks associated | |||
with the action statements in effect. Additionallicensed operators reported to the control | |||
room to assist the shift crew as necessary. | |||
Investigation of the cause of the trip revealed that the SUPS B inverter had blown fuses. | |||
The power to Distribution Panel PDP3918, which is supplied by SUPS B, was restored | |||
! by energizing the bypass power supply approximately 15 minutes after the SUPS | |||
l tripped. The order of restoration of loads had been priontized using the basic guidance | |||
l in Procedure OP-901-312, and field reports from nuclear plant operators verified that the | |||
loads being restored had not been affected. The inspectors reviewed the off-normal | |||
procedures used during recponse to the transient and noted that the guidelines were | |||
very general in that the procedure required the operators to develop the detailed | |||
restoration plan ad hoc. The operators demonstrated an excellent knowledge and | |||
understanding of the safety consequences of the event. | |||
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All components powered from Distribution Panel PDP3918 had been restored within | |||
approximately 3 hours. All TS action requirements were exited, except for TS 3.8.3.1, | |||
which required the SUPS bus to be energized from the inverter within 24 hours. All TS | |||
action statements had been satisfied within the required time limits. The SUPS B | |||
inverter was repaired and returned to service within 24 hours. | |||
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The inspectors discussed the off-normal procedure weaknesses with the Operations | |||
Manager and Operations Superintendent. They agreed to review the procedures and the | |||
actual activities required for event mitigation for potential procedure enhancement. | |||
c. Conclusions | |||
The licensed operators performed in a professional manner and demonstrated excellent | |||
- knowledge and understanding of the safety consequences of the loss of instrument | |||
power event. | |||
O1.2 . Control Room Observations | |||
a. Insoection Scooe (71707) | |||
in addition to routine daily control room observations, on March 11 and 12,1998, the J | |||
Inspectors observed control room activities including accet.s control, operator conduct, | |||
general operator knowledge, and shift tumover, | |||
b. . Observations and Findinas | |||
The inspectors reviewed Administrative Procedures OP-100-001, Revision 14, " Duties | |||
and Responsibilities of Operators on Duty," and OP-100-007, Revision 13, " Shift | |||
Tumover," to determine the requirements for the conduct of control room activities. The | |||
inspectors determined that the observed operations crews were generally meeting these | |||
requirements. | |||
The inspectors noted that control room access controls were good. The layout of the | |||
control room naturally funneled personnel into the SS office or to the entrance of the , | |||
control room proper. This arrangement minimized personnel congregating in the rear of 1 | |||
the control room. Also, extraneous conversations were maintained in the enclosed office | |||
space behind the control room, which minimized distractions to the operators. The i | |||
inspectors also noted that the CRS only allowed entrance to personnel requiring control I | |||
room access for a work- and business-related activity. ) | |||
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The inspectors observed several hours of licensed operator activity and noted the l | |||
following: | |||
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. The operation staff's conduct was professional. | |||
. The operators were generally attentive to plant status and indicators. | |||
. Excellent communications were observed among the crew whenever one of the | |||
- crew members left the control room area. Not only did the operators inform their | |||
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partner and the CRS, but they also informed the SS. The inspectors did observe | |||
the SS and the CRS brief each other on plant changes whenever one of them | |||
retumed to the control room. | |||
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Control room command function was clearly delineated, including any changes in | |||
emergency response responsibilities. | |||
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Alarm and annunciator response by the operators was very good. Without fail, | |||
l the annunciators were acknowledged in an appropriate amount of time. The | |||
! alarm was announced to the CRS and/or SS, and shift supervision acknowledged | |||
the alarm and ensured appropriate actions were taken. | |||
. . During shift tumovers, operators followed the requirements in | |||
Procedure OP-100-007. The shift meeting was especially useful in providing the . | |||
appropriate information to all key members of the shift. The CRS was able to | |||
, coordinate conflicting maintenance and surveillance activities that had been | |||
l previously scheduled. | |||
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c. Conclusions 1 | |||
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in general, control room activities were conducted in a very good manner. | |||
03 Operations Procedures and Documentation | |||
O3.1 Station Loo Procedures Observations (71707) | |||
The inspectors observed that with the computer logging process, the station log can be | |||
modified anytime within the 12-hour shift. The editing can be accomplished without | |||
appropriately identifying whether a modification was editorial or whether it should have | |||
been identified as a corrected entry or late entry. The logging procedure in Operating ) | |||
Instruction 01-004-000, Revision 25, " Operations Narrative and Shift Logs," implied that I | |||
the log was not final until printed at the end of the shift, and that only changes made after | |||
that time would be subject to identifying as a late or corrected entry. | |||
The inspectors have implemented an ongoing review of this issue. An inspection | |||
followup item has been opened to continue review of this issue (50-382/9806-01). | |||
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04 Operator Knowledge and Performance | |||
04.1 Loss of Control Room Command Function | |||
a. Insoection Scoce (71707) | |||
The inspectors reviewed the documentation of circumstances, reviewed the statements | |||
of the supervisors, and interviewed operations personnel regarding a loss of control room | |||
command function. | |||
b. Ohtervations and Findinos | |||
On February 15,1998, with the reactor stable at 100 percent power, the CRS had | |||
notified the SS that he was leaving the control room to get lunch. The SS had | |||
acknowledged the CRS. The SS had been engrossed in an electrical problem, which he | |||
was discussing with an electrician. He accompanied the electrician out of the control | |||
room to the relay room without notifying the remaining control room operators. One of | |||
the licensed operators noticed that neither the CRS nor the SS was in the control room | |||
and went to the lunch room to tell the CRS that the SS had also left the control room. | |||
The CRS reentered the control room and paged the SS to tell him that they had violated | |||
the TS control room manning requirements, as both the SS and the CRS had been | |||
absent from the control room for 1 minute 38 seconds. | |||
Condition Report 98-0222 had been issued immediately following the incident. Also, | |||
personnel statements had been written by the CRS and SS. Review of these documents | |||
revealed no further pertinent information. | |||
A root cause determination was performed by the licensee and it found that the incident | |||
was an isolated human error. The inspectors agreed with this evaluation based on a | |||
review of the documentation and interviews with the individuals who were involved. | |||
Immediate corrective actions included counseling of the SS, issuance of a daily | |||
instruction reminding the control room staff of the procedural and TS requirements, and | |||
discussion of the incident at the next SS/CRS meeting. The long-term corrective actions | |||
identified involved enhanced training during scheduled requalification and additional | |||
management observations. Completion of the long-term actions will be verified during | |||
review of Licensee Event Report (LER) 50-382/98-002. | |||
TS 6.2.2.b states, in part, that at least one licensed operator shall be in the control room | |||
when fuelis in the reactor. In addition, while the reactor is in MODE 1,2,3, or 4, at least | |||
one licensed Senior Operator shall be in the control room. | |||
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TS Table 6.2-1 contains a note that states, in part, that during any absence of the shift | |||
supervisor from the control room while the unit is in MODE 1,2, 3, or 4, an individual, | |||
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other than the shift technical advisor, with a valid senior operator license shall be | |||
j designated to assume the control room command function. ) | |||
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Operating Procedure OP-100-001, " Duties and Responsibilities of Operators on Duty," l | |||
l Step 5.4.1.4, states, in part, that before leaving the control room for tours, | |||
troubleshooting, or other reasons; operators, shift superintendents, or control room | |||
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supervisors should inform the remaining control room operating staff of their intended | |||
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activities and the approximate duration of these activities. Additionally, they shall verify { | |||
that the control room command function remains appropnately delineated. l | |||
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; Failure to adhere to these TS and procedural requirements demonstrates inattentiveness | |||
to licensed duties by a senior licensed operator. However, this licensee-identified and | |||
corrected violation is being treated as a noncited violation consistent with Section Vll.B.1 | |||
of the NRC Enforcement Policy. Specifically, the violation was identified by the licensee, | |||
it was not willful, actions taken as a result of a previous violation should not have | |||
corrected this problem, and appropriate corrective actions were completed by the | |||
licensee (50-382/9806-02). | |||
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l c. Conclusions | |||
Inattentiveness to licensed duties by a senior reactor operator resulted in a noncited | |||
violation of TS control room staffing requirements when both the SS and the CRS were | |||
l absent from the control room for 1 minute 38 seconds. | |||
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08 Mhscellaneous Operations issues (92901) | |||
l 08.1 (Closed) Violation S0-382/9704-01: Failure to comply with working-hour limitations for | |||
j operations personnel. | |||
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Between February 1 and March 1,1997, the licensee failed to implement the | |||
j requirements of TS 6.2.2.e and Procedure UNT-005-005, " Working Hour Policy for | |||
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Nuclear Safety-Related Work." Working-hour policy guidelines had been exceeded in | |||
several instances without proper approval. | |||
The inspectors reviewed the corrective actions described in the LER and verified | |||
that: (1) the operations, maintenance, radiation protection, and site support department | |||
personnel had been briefed on the root cause of the event and resultant corrective | |||
actions; (2) Revision 5 to Procedure UNT-005-005 had been implemented to clarify the | |||
working-hour policy; (3) the quality assurance department incorporated evaluation of | |||
organizational compliance with the working-hour policy into its audit program; and (4) the | |||
quality assurance department audited the operations and health physics departments | |||
and found these departments to be in compliance with the working-hour policy | |||
guidelines. | |||
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The inspectors concluded, based on verification of these actions, that the licensee j | |||
appropriately addressed this violation. | |||
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08.2 (Closed) LER 50-382/96-01* Control Room Ventilation Valve Leakage. X | |||
l It was identified that the control room normal ventilation isolation valves were leaking | |||
during operation of the emergency filtration system. Assuming a single failure, this | |||
leakage could have resulted in a single individual exceeding the 30 Rem thyroid j | |||
exposure limit in 10 CFR Part 50, Appendix A, Criterion 19 and Standard Review 4 | |||
Plan 6.4, Section 11.6. The cause of the leakage was determined to be debris that had | |||
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accumulated inside the valve disc region and prevented the valves from fully closing. | |||
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The inspectors reviewed the root cause analysis and corrective actions and determined i | |||
them to be appropriate. Long term corrective actions included: (1) establishing an | |||
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18-month frequency for leak rate checkirig the isolation dampers, (2) developing a j | |||
procedure with an administrative limit of 8 scfm to leak rate test the isolation valves, and | |||
(3) reviewing the testing configuration for the control room pressure test to ensure | |||
compliance with all licensing documents. | |||
i The implementation of these corrective actions are discussed in NRC Inspection | |||
l Report 50-382/96-21 and found to be fully satisfactory. | |||
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08.3 (Closed) LER 50-382/97-012; Programmatic Breakdown of Overtime Program. | |||
! The corrective actions for this LER are the same as the corrective actions for NRC | |||
Violation 50-382/9704-01, discussed in Section 08.1 of this report. , | |||
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l 08.4 (Closed) LER 50-382/97-018: Dropped New Fuel Assembly. | |||
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During Refueling Outage 8, a new fuel assembly became disengaged from the spent fuel | |||
handling tool and dropped approximately 5 inches. The assembly came to rest at a 40 ; | |||
i angle against the side of the spent fuel pool. No other fuel assemblies were damaged ; | |||
and no spent fuel pool liner leakage was detected. The root cause of the event was j | |||
determined by the licensee to be human error. j | |||
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l The inspectors reviewed the root cause analysis and considered it to be thorough and | |||
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representative of a good self-assessment. Corrective actions included a revision to the ' | |||
l refueling procedure, training, and removal of several environmental distractions. These | |||
l are described in NRC Inspection Report 50-382/97-08. | |||
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Based on the review completed by the inspectors, it was determined that the licensee | |||
had taken the appropriate actions to address this issue. i | |||
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11. Maintenance | |||
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! M1 Conduct of Maintenance (61726,62707) | |||
l The inspectors observed all or portions of the following surveillances: | |||
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OP-903-119 Secondary Auxiliaries Quarterly Valve Tests | |||
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OP-903-046 Emergency Feed Pump Operability Check | |||
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OP-903-068 Emergency Diesel Generator and Subgroup Relay Train B | |||
Operability Test | |||
Additionally, the inspectors observed portions of Work Authorization 01167398, which | |||
was issued to troubleshoot Control Element Assembly 14 to determine why it slipped | |||
l approximately 5 inches while moving it. | |||
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l The inspectors found the conduct of these maintenance and surveillance activities to be | |||
l good. All activities observed were performed with an appropriate authorization package | |||
j or test procedure. The inspectors observed supervisors monitoring job progress. | |||
M1.1 Quarterly Surveillance of Comoonent Coolino Water (CCW) Makeuo System Check l | |||
j Valves | |||
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a. Insoection Scoce (61726) l | |||
l The inspectors observed portions of Surveillance Procedure OP-903-119, Revision 4, | |||
" Secondary Auxiliaries Quarterly IST Valve Tests." The operators performed the | |||
applicable sections to leak test various CCW makeup water check valves. | |||
j b. Observations and Findinas | |||
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On March 12,1998, the operators performed a quarterly leak check on two CCW | |||
makeup system check valves. The procedure required securing CCW Makeup Pump B | |||
for a portion of the test. Not only did the operators declare CCW Makeup System B out | |||
of service, but also those loads sen/ed by the system. Therefore, the cascading TS | |||
action statements for securing CCW System B, Emergency Diesel Generator B, and | |||
Essential Chiller B were entered. | |||
The briefing for the evolution was thorough, covered the details of the test, expected | |||
responses, and personnel responsibilities. All appropriate personnel were present and | |||
actively involved in the briefing. The CRS made it clear to the crew that this was not an | |||
evolution to be rushed. When the operators arrived on station to perform the | |||
surveillance, they found the spent resin transfer cask being moved from the minus | |||
35-foot level. The operators and the CRS made the conservative decision to wait for the | |||
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cask to be lifted from the area prior to beginning work. Their concern was leaving the i | |||
CCW makeup system in a degraded state if there were problems with lifting the cask. l | |||
The inspectors observed the operators perform the surveillance. The operators properly | |||
followed the procedure, recorded all required information, and appeared knowledgeable j | |||
in their tasks. They exhibited good three-part communications between each other and ) | |||
the control room. Peer checking was also properly used to ensure that the right i | |||
component was being operated and they used appropriate cleanliness controls. | |||
The inspectors noted that while the CRS was reviewing the procedure and drawings in | |||
preparation for the brief, he noted that a simple addition of a drain line installed on the | |||
nonsafety-related portion of the piping would, in the future, prevent the necessity of | |||
securing Makeup Pump B and cause entrance into cascading TS. The CRS contacted | |||
the system engineer who would look into the matter further. | |||
c. Conclusions l | |||
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The performance of the check valve leakage surveillance adequately tested the valves. I | |||
Very good procedural compliance and questioning attitudes by all of the operations l | |||
personnel involved in the test was noted. | |||
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M 1.2 Emeraency Feedwater (EFW) Pumo AB Surveillance Observation ' | |||
a. Insoection Scoce (61726) | |||
On March 12,1998, the inspectors observed the EFW Pump AB surveillance. The | |||
surveillance was performed using Surveillance Procedure OP-903-046, Revision 14, | |||
" Emergency Feed Pump Operability Check." | |||
b. Observations and Findinos | |||
The operators performed a routine run and overspeed trip check of EFW Pump AB. The | |||
inspectors were present for the pretest briefing and for the majority of the test. The | |||
briefing was performed by a licensed operator and contained the appropriate precautions | |||
and limitations. However, the operator stated that the crew was familiar with the | |||
procedure and he would not review it step by step. One of the nonficensed operators | |||
asked several pertinent questions about the procedure. These questions, in combination | |||
with the rest of the information presented, made the briefing information complete. | |||
I The inspectors observed a licensed operator starting the EFW pump from the control | |||
! room. The operator exhibited good control of the evolution. The inspectors noted that | |||
the procedure was in constant use in the control room. The operators used good | |||
three-part communication among each other and with the operators in the field. | |||
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The inspectors observed the pump operate from the minus 35-foot level of the reactor | |||
auxiliary building. Besides the operators and system engineer, there were several | |||
mechanics in the area with measuring equipment. One of the operators was surprised | |||
by the number of mechanics assigned to the job since they had not been present for the | |||
briefing in the control room. The inspectors spoke to the system engineer about the | |||
mechanics. The system engineer stated that he had been working on gathering pump | |||
data for some time. The inspectors noted that the mechanics worked well together in | |||
gathering the required data. | |||
The inspectors observed the overspeed trip test of the pump. The operators then | |||
restored the pump to service. No problems were noted with this portion of the test. ; | |||
Procedure adherence by the operators was good. The inspectors asked several l | |||
questions about the pump operation. The inspectors found the nonlicensed operators l | |||
knowledge level good. | |||
c. Conclusions | |||
The surveillance test of the EFW turbine-driven pump was very good. The operators | |||
were knowledgeable about the test. | |||
M1.3 Postmaintenance Testina of Valve CVC-103 | |||
a. Observations and Findinas | |||
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In September 1997, SUPS SB failed as a result of an internal fault. Failure of SUPS SB | |||
resulted in a loss of power to a number of components, one of which was | |||
Valve CVC-103. All other components responded as designed without any problems. | |||
Valve CVC-103 is installed in the letdown line and serves as a containment isolation | |||
valve for the line. As such, it is required to close to prevent flow from the reactor coolant | |||
system to the auxiliary building in the event of a line break outside containment. | |||
When power from SUPS SB was lost, Valve CVC-103 closed, but the valve did not fully | |||
shut, which allowed flow through the valve of approximately 25 gpm. Another valve in | |||
the letdown line was shut to stop the flow. | |||
Licensee personnel made a containment entry to inspect the valve to verify there was no | |||
physical damage to the valve. After verifying no damage occurred, the licensee | |||
inspected the valve stem travel stop nut and noted that it appeared to be misadjusted. | |||
The stop nut was adjusted and a subsequent leak test performed. The test results | |||
indicated no further leakage through the valve. | |||
During review of this issue by the inspectors, it was noted that maintenance had been | |||
performed on Valve CVC-103, and no postmaintenance test had been performed to | |||
verify that the valve could perform its intended function of isolating letdown flow. | |||
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The failure to provide instructions to specify postmaintenance testing of Valve CVC-103 | |||
is a violation of TS 6.8.1 (50-382/9806-03). | |||
b. Conclusions | |||
Valve CVC-103 did not properly perform all of its design functions because testing was | |||
not performed after completion of maintenance. | |||
M2 Maintenance and Material Condition of Facilities and Equipment | |||
M2.1 Soent Fuel Pool (SFP) Overflow Corrective Action Followuo | |||
a. Insoection Scooe (62702) | |||
The inspectors assessed the adequacy of the licensee's corrective actions pursuant to a | |||
SFP overflow event that occurred in May 1997. ' | |||
b. Observations and Findinas | |||
On May 21,1997, approximately 5000 gallons of radioactive water had overflowed from | |||
the SFP into the fuel handling building (FHB). The licensee had estimated that | |||
approximately 2500 gallons was contained in the FHB railroad bay and that between 230 | |||
and 1850 gallons had escaped outside the FHB through the railroad bay doors, where it | |||
had contaminated a large area of asphalt and gravel within the protected area and the | |||
storm drain system. The remainder of the spilled fluid was captured in the reactor | |||
auxiliary building sump and waste systems. Condition Report (CR) 97-1284 had been | |||
initiated and an event review team was convened on May 21 to investigate the event. | |||
The event review team had concluded that the spill had been the result of a combination | |||
of tagging and communication errors, which had resulted in dead-heading of a | |||
purification pump, combined with a leaking SFP purification isolation valve. The | |||
investigation revealed that the travel stop nuts on SFP isolation Valve FS-345 (a | |||
manually-operated diaphragm valve) had been incorrectly positioned %-inch lower than | |||
required by the valve technical manual. The mispositioning occurred during a | |||
maintenance activity in May 1992, when reach rods were installed per Design | |||
Change (DC) 3211. DC 3211 had required the travel stop nuts to be removed; however, | |||
neither DC 3211 nor the associated work authorization had contained specific | |||
instructions as to the required position for the travel stop nuts upon replacement. This | |||
resulted in the valve not fully blocking flow when it indicated shut. The licensee had | |||
taken soil and liquid samples to determine if any reportable releases to the environment | |||
had occurred and concluded that 10 CFR Part 20 limits had not been exceeded. | |||
I | |||
l- -11- | |||
! | |||
! | |||
! The event review team had determined that isolation Valve FS-345 and four other | |||
diaphragm valves had extension stems installed per DC 3211, as required. These | |||
valves were checked and the travel stop nuts were adjusted. The licensee had not | |||
inspected any other diaphragm valves. | |||
On February 2,1998, the inspectors performed an inspection of travel stop nuts on other | |||
diaphragm valves in the FHB and noted the following deficiencies: ) | |||
i | |||
l Valve Condition | |||
FS-1058 - Fuel Pool Pump B Discharge Drain No travel stop lock nut | |||
! | |||
l FS-210 - Refueling Canal Drain Pump Discharge Loose travel stop lock nut | |||
FS-212 - Refueling Canal Drain Pump Discharge Drain No travel stop lock nut | |||
i s | |||
FS-214 - Refueling Canal Drain Pump Discharge No travel stop lock nut | |||
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isolation to Fuel Pool | |||
The inspectors notified the licensee of the above conditions. The licensee initiated i | |||
l CR 98-0146 to address the identified deficiencies. At the end of this inspection period, { | |||
the licensee was in the process of inspecting approximately 800 other diaphragm valves l | |||
installed in the plant. | |||
l When the event team identified that the stop nut on Valve FS-345 was incorrectly | |||
installed, the team incorrectly limited the population of other potentially affected valves to | |||
l those modified per DC 3211. No effort was made by the licensee to inspect other similar ] | |||
' | |||
valves to determine the full scope of the stop nut misadjustment problem. As a result, full l | |||
and effective evaluation did not occur for the hardware deficiencies on the relatively large | |||
population of valves. | |||
The failure to promptly identify and correct the travel stop nut deficiencies, after having i | |||
' | |||
attributed the misadjustment as a contributing factor to a SFP overflow event, is a | |||
violation of Criterion XVI (50-382/9806-04). | |||
l c. Conclusiong | |||
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The scope of the corrective actions identified after the SFP overflow event was j | |||
l | |||
i inadequate because other similiar diaphragm valves were not deficiencies. This is a l | |||
violation of Criterion XVI. | |||
1 | |||
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. | |||
-12- | |||
111. Engl.neerina | |||
E1 Conduct of Engineering (37551) | |||
E1.1 Enaineerina Evaluation of Delaved Reactor Trio Breaker (RTB) Ooenina | |||
a. Insoection Scoce (37551) | |||
The inspectors reviewed enginecring activities associated with evaluating the delayed | |||
opening of RTB 2. | |||
b. Observations and Findinas | |||
On February 8,1998, while performing Procedure OP-903-107, " Plant Protection System | |||
Functional Test," RTB 2 opened 15 seconds after the trip signal was initiated. RTB 6, | |||
which is designed to open concurrently, did respond and open immediately. RTB 2 was | |||
declared inoperable and both breakers were left in the tripped position to comply with | |||
TS 3.3.1-13, Action 5. CR 98-0182 was written to address the issue. Electrical | |||
maintenance technicians determined that the K2 relay had failed. The relay was | |||
replaced, the breakers retested satisfactorily, and the RTBs were declared operable. | |||
The K2 relay was a Potter & Brumfield MDR Model 170-1 with Date Code 9416. A | |||
generic issue related to these relays was reported in NRC Inspection | |||
Report 50-382/98-02, Section M2.1. Inspection Followup Item 50-382/9802-01 was | |||
opened to track the status of the action plan to identify, evaluate, and replace MDRs prior | |||
to failure. The inspectors determined that this relay had failed before the program had | |||
been effectively implemented. | |||
The K2 MDR relay was sent to Combustion Engineering in Windsor, Connecticut, for | |||
failure analysis. The failure was determined to most likely be caused by a slight | |||
misalignment of the shaft and top end bell. This condition caused excessive wear, a | |||
buildup of wear materials, and binding of the shaft, which prevented full rotation. Glass | |||
fiber contamination was also discove ed (in the grease) and may have been a | |||
contributor. | |||
A review of the relay history for the plant protective system indicated that the K2 relay | |||
had been replaced in April 1997. On that occurrence, RTB 6 had been slow to open. | |||
Failure analysis had indicated that hardened grease, mechanical binding, and grease | |||
contamination had contributed to that failure. CR 97-0787 had been initiated. | |||
The inspectors questioned the engineer to determine if they had checked the other three | |||
relays in the plant protection system to identify the date codes. The response wat, that | |||
they had not checked those relays. After checking the other relays, the date codes found | |||
were: K1 - 9404; K3 - 9345; and K4 - 9416. Relay K2 had been replaced with Date | |||
Code 9730. The inspectors asked if these relays were going to be replaced because | |||
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their date codes were part of those of originalindustry concem. The reply was that they | |||
would not be replaced unless they failed. The justification was that each relay was | |||
tested quarterly. | |||
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The inspectors found that the engineers had been responsive to the need for providing | |||
root cause determination. Tne technical approach and understanding of the mechanical | |||
problems were good. | |||
c. Conclusions . | |||
Engineers had been responsive to the need for developing a technical failure mechanism | |||
for plant protective system relays. | |||
] | |||
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l E5 Engineering Staff Training and Qualification | |||
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E5.1 Ooeration of EFW Pumo AB without Control Room Concurrence | |||
a. Insoection Scooe (37551) | |||
, | |||
The inspectors reviewed the licensee's findings and corrective actions related to this l | |||
l issue. 1 | |||
I | |||
b. Observations and Findinas l | |||
On March 5,1998, an engineer determined that he had been operating equipment in the | |||
plant without the SS or CRS knowledge or concurrence. He had been partially stroking j | |||
EFW Turbine Governor Valve MS-417 by moving the stem approximately % inch for the ! | |||
purpose of detecting stem binding. The engineer wrote CR 98-0333 to address the i | |||
issue, which involved operation of equipment in the plant without the consent of the l | |||
control room staff. l | |||
This activity constituted a violation of Procedure OP-100-001," Duties and | |||
Responsibilities of Operators on Duty," Section 5.8.1.3, which stated, in part, that | |||
l operational activities performed locally in the plant to support overall plant operating | |||
activities must take place under the direction of or with the concurrence of the SS/CRS. | |||
This was a repeat of Violation 50-382/9605-02. The !!censee had taken immediate steps | |||
to stress proper conduct of any operations with plant personnel. Long-term corrective | |||
actions had not been finalized (50-382/9806-05). | |||
c. Conclusions ; | |||
! | |||
An engineer inappropriate!y operrated equipment in the plant without the SS or CRS l | |||
knowledge or concurrence. | |||
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E8 Miscellaneous Engineering issues (92903) | |||
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E8.1 (Closed) Unresolved item 50-382/9704-04: Failure to have a procedure addressing | |||
VOCs in areas serviced by engineered safety features (ESF) filtration units. | |||
NRC Inspection Report 50-382/97-04 identified two issues that remained unresolved | |||
pending additionalinput from the licensee and a response from the Office of Nuclear | |||
Reactor Regulation (NRR). The first issue identified a failure to have a procedure that | |||
specifically limited the amount of VOCs in an area that could adversely affect | |||
safety-related ventilation charcoal adsorbers. The second issue involved use of a | |||
waiting period in lieu of performing testing following painting in an area served by | |||
charcoal filters. This issue was referred to NRR for resolution. | |||
The inspectors performed a detailed review of the procedure that had been revised in | |||
response to the first issue. Procedure PMC-002-007, " Installation Procedure | |||
Maintenance and Construction Painting," limits the amount of VOCs in the areas that | |||
would affect ventilation charcoal filters. A detailed engineering review was performed to | |||
evaluate the amount of VOCs it would require in a given area to inhibit adsorption in the | |||
charcoal filter to the extent that it could not perform its safety function. Engineering | |||
Request Response ER-W3-97-0040, "VOC Limits for Insulation Cement and Painting in | |||
ESF Areas," dated April 11,1997, provided conservative calculations showing the | |||
maximum VOC loadings in critical areas. The procedure further reduces the amount of | |||
VOC allowed in any critical area to less than that shown in the engineering evaluation. | |||
The response from NRR was in a letter to Mr. Jerrold D. Dewease from | |||
Jack N. Donohew, SUBJECT: "lNTERPRETATION OF FILTRATION UNIT | |||
FREQUENCY-OF-TESTING REQUIREMENTS SPECIFIED IN THE TECHNICAL | |||
SPECIFICATIONS AND REGULATORY GUIDE 1.52 FOR ARKANSAS NUCLEAR | |||
ONE, UNITS 1 AND 2, GRAND GULF NUCLEAR STATION, UNIT 1, RIVER BEND | |||
STATION, AND WATERFORD 3 STEAM ELECTRIC STATION (TAC NOS. M98367, | |||
M98368, M98369, M98370, AND M98371)," dated September 11,1997. The oveiall | |||
conclusion of the issued response was that the licensee had the responsibility to define | |||
the criteria based on a well-documented, sound, and conservative technical basis. The | |||
letter stated that the staff considered that a painting, fire, or chemical release was not | |||
communicating with a ventilation system only if the ventilation system is not in operation | |||
and the isolation dampers for the system are closed and leaktight thereby preventing air | |||
from passing through the filters. | |||
The inspectors determined that the engineering review and the procedure appropriately | |||
addressed this unresolved issue and the licensee was in full compliance with NRC | |||
regulations. This licensee-identified and corrected violation is being treated as a | |||
i noncited violation consistent with Section Vll.B.1 of the NRC Enforcement Policy. | |||
Specifically, the violation was identified by the licensee, it was not willful, actions taken as | |||
a result of a previous violation should not have corrected this problem, and appropriate | |||
corrective actions were completed by the licensee (50-382/9806-06). | |||
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E8.2 (Closed) LERs 50-382/97-007-00 and 50-382/97-007-01: Refueling Water Storage I | |||
' | |||
Pool (RWSP) Level Indication inaccuracies and Discovery of Additional Refueling Water | |||
Storage Pool Instrument Uncertainty | |||
The licensee discovered that the analytical limit for tha RWSP level instrument was | |||
exceeded due to an inadequate design of the level transmitter reference leg. The low | |||
side of each RWSP level transmitter was vented to an area filtered by the controlled | |||
l ventilation area system, whereas the high side was connected to the RWSP. Operation | |||
of the controlled ventilation area system caused indicated RWSP level to differ from | |||
actuallevelin the nonconservative direction. This would have resulted in a recirculation | |||
actuation signal being generated below the TS allowed value. , | |||
l | |||
The inspectors determined that adequate corrective actions were implemented, dunng l | |||
Refueting Outage 8, in that a design change was initiated to reroute the reference legs | |||
for the RWSP level instruments back to the RWSP. This change eliminated any i | |||
ventilation system interactions. The corrective actions are discussed in NRC Inspection | |||
l Reports 50-382/97-12 and 50-382/97-27. | |||
! | |||
! Based on reviews performed by the inspectors, it was concluded that the licensee had | |||
' | |||
taken the appropriate actions to address this issue. | |||
! | |||
l IV. Plant Suncort | |||
! | |||
F8 Miscellaneous Fire Protection issues (92904) | |||
; F8.1 (Closed) Insoection Followuo item 50-382/9708-08: Reactor coolant pump (RCP) oil fill | |||
i administrative controls. | |||
There was no separate oil collection system under the remote fill lines for the RCP lube | |||
oil system. This condition did not meet 10 CFR Part 50, Appendix R, requirements. The | |||
licensee recognized that their system did not meet Appendix R requirements and | |||
submitted an exemption request (Letter W3F1-97-0021, February 10,1997). The letter | |||
addressed administrative controls that would be implemented if the licensee had to use | |||
the RCP remote lube oil fill lines. The inspectors concluded that the controls were | |||
generally adequate, except for monitoring levelin the reservoirs. The licensee did not | |||
have a formal reservoir volume versus indicated level curve for either the upper or lower | |||
RCP oil reservoir. The licensee informed the inspectors that they would generate formal | |||
curves for both the upper and lower reservoir. | |||
t The inspectors verified that volume versus level curves for both the upper and lower | |||
' | |||
RCP oil reservoirs were incorporated into Volume 1 of the RCP vendor technical manual. | |||
The actions taken by the licensee to address this issue were acceptable. , | |||
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V. Manaaement Meetinas | |||
l X1 Exh Meeting Summary | |||
The inspectors presented the inspection results to members of licensee management on | |||
March 20,1998. The licensee acknowledged the findings presented. | |||
: The inspectors asked the licensee whether any materials examined during the inspection 1 | |||
l should be considered proprietary. No proprietary information was identified. | |||
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9 | |||
ATTACHMENT | |||
SUPPLEMENTAL INFORMATION | |||
PARTIAL LIST OF PERSONS CONTACTED | |||
Licensee | |||
F. J. Drummond, Director Site Support | |||
C. M. Dugger, Vice-President, Operations | |||
E. C. Ewing, Director, Nuclear Safety & Regulatory Affairs | |||
C. Fugate, Operations Superintendent | |||
T. J. Gaudet, Manager, Licensing | |||
J. G. Hoffpauir, Manager, Operations | |||
T. R. Leonard, General Manager, Plant Operations | |||
G. D. Pierce, Director of Quality | |||
D. W. Vinci, Superintendent, System Engineering | |||
A. J. Wrape, Director, Design Engineering | |||
INSPECTION PROCEDURES USED | |||
IP 37551 Engineering | |||
IP 61726 Surveillance Observation | |||
IP 62702 Maintenance Program | |||
IP 71707 Plant Operations | |||
IP 92901 Followup - Operations | |||
IP 92903 Followup - Engineering | |||
IP 92904 Followup - Plant Support | |||
ITEMS OPENED. CLOSED. AND DISCUSSED | |||
Ooened | |||
50-382/9806-01 IFl Station logkeeping procedures (Section O3.1) , | |||
50-382/9806-02 NCV Loss of control room command function (Section 04.1) | |||
50-382/9806-03 VIO Postmaintenance Testing of Valve CVC-103 (Section M1.3) | |||
50-382/9806-04 VIO Corrective Actions for Diaphragm Valves (Section M2.1) | |||
\ .. . | |||
. - __ -_______ -_ | |||
. | |||
.- | |||
-2- | |||
50-382/9806-05 VIO Operation of EFW Pump AB without control room concurrence | |||
(Section E5.1) J1 | |||
50-382/9806-06 NCV Failure to have procedure addressing VOCs in areas serviced by i | |||
ESF filtration units (Section E8.1) | |||
Closed l | |||
I | |||
50-382/9806-02- NCV Loss of control room command function (Section 04.1) | |||
50-382/9704-01 VIO Failure to comply with working-hour limitations for operations | |||
personnel (Section 08.1). | |||
50-382/96-011 LER Control Room Ventilation Valve Leakage (Section 08.2) | |||
50-382/97-012 LER Programmatic Breakdown of Overtime Program (Section 08.3). | |||
50-382/97-018 LER Dropped New Fuel Assembly (Section 08.4) | |||
. | |||
50-382/9704-04 URI Failure to have a procedure addressing VOCs in areas serviced by | |||
ESF filtration units (Section E8.1). | |||
l | |||
50-382/9806-06 NCV Failure to have a procedure addressing VOCs in areas serviced by | |||
ESF filtration units (Section E8.1). | |||
50-382/9708-08 IFl RCP oil fill administrative controls (Section F8.1). | |||
l | |||
50-382/97-007-00 LER RWSP Level Indication inaccuracy (Section E8.2) | |||
50-382/97-007-01 LER RWSP Level Indication inaccuracy (Section E8.2) | |||
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Discussed | |||
None | |||
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-3- | |||
1 | |||
LIST OF ACRONYMS USED | |||
CCW component cooling water | |||
CR condition report | |||
CFR Code of Federal Regulations | |||
CRS control room supervisor | |||
DC design change | |||
EFW emergency feedwater | |||
ESF engineered safety features | |||
FHB fuel handling building | |||
gpm gallons per minute | |||
LER licensee event report | |||
NRC Nuclear Regulatory Commission | |||
NRR Office of Nuclear Reactor Regulation | |||
MDR motor-driven relay | |||
RCP reactor coolant pump | |||
RTB reactor trip breaker | |||
RWSP refueling water storage pool | |||
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SFP spent fuel pool | |||
SS shift superintendent | |||
SUPS station uninterruptible power supply | |||
TS Technical Specifications | |||
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VOC volatile organic compound | |||
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! | |||
}} |
Latest revision as of 06:26, 2 February 2022
ML20217B698 | |
Person / Time | |
---|---|
Site: | Waterford |
Issue date: | 04/21/1998 |
From: | Harrell P NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) |
To: | |
Shared Package | |
ML20217B670 | List: |
References | |
50-382-98-06, 50-382-98-6, NUDOCS 9804230113 | |
Download: ML20217B698 (21) | |
See also: IR 05000382/1998006
Text
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4
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ENCLOSURE 2
U.S. NUCLEAR REGU'ATORY COMMISSION
REGION IV
. Docket No.: 50-382
License No.: NPF-38
Report No.: 50-382/98-06
Licensee: Entergy Operations, Inc.
Facility: Waterford Steam Electric Station, Unit 3
Location: Hwy.18
Killona, Louisiana
Dates: February 1 through March 21,1998
Inspectors: J. M. Keeton, Resident inspector
D. R. Lanyi, Resident inspector, Region 11
Accompanied By: J. C. Edgerly, Resident inspector Trainee
M. A. Kotzalas, NRC Headquarters intern
Approved By: P. H. Harrell, Chief, Project Branch D
ATTACHMENT: Supplemental Information
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9804230113 980421
PDR ADOCK 05000382
G PDR
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EXECUTIVE SUMMARY
Waterford Steam Electric Station, Unit 3
NRC Inspection Report 50-382/98-06
I
This routine, announced inspection included aspects of operations, maintenance, engineering i
and plant support activities. The report covers a 7-week period of resident inspection. !
Ooerations I
l
- The licensed operators performed in a professional manner and demonstrated excellent
knowledge and understanding of the safety consequences of the loss of instrument
power event (Section 01.1).
. In general, control room activities were conducted in a very good manner (Section 01.2).
-
Inattentiveness to licensed duties by a senior reactor operator resulted in a noncited
violation of Technical Specification (TS) shift-manning requirements when both the shift
superintendent (SS) and the control room supervisor (CRS) were absent from the control
room for 1 minute 38 seconds (Section O4.1).
Maintenance
+ The performance of the check valve leakage surveillance adequately tested the valves.
The inspectors noted good procedural compliance and good questioning attitudes by all
of the operations personnelinvolved in the test (Section M1.1).
- The inspectors determined that the emergency feedwater turbine-driven pump
surveillance was performed in accordance with approved procedures. The operators
were knowledgeable about the test (Section M1.2).
. Valve CVC-103 did not properly perform all its design functions during an event. A
violation resulted because testing was not performed after completion of maintenance
(Section M1.3).
- Personnel failed to implement broad, effective corrective actions following the spent fuel
pool overflow event. Specifically, a violation was identified because the licensee failed to
review the stop nut adjustment on similar valves since the stop nut adjustment was
considered a contributing factor to the overflow of the spent fuel pool (Section M2.1).
- - _ . _ _ -
- Engineers had been responsive to the need for developing a technical failure mechanism
for a plant protective system relay (Section E1.1).
knowledge or concurrence. This was a repeat of a similar occurrence within the last
2-years, and this issue is being treated as a violation (Section E5.1).
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The engineering review and the revised procedures for control of volatile organic
compounds (VOC) was acceptable. This issue is being treated as a noncited violation
(Section E8.1).
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Reoort Details
)
Summary of Plant Status
During this inspection period, the plant operated at essentially 100 percent power.
I
1. Operations
01 Conduct of Operations (71707)
01.1 Loss of Static Uninterruotible Power Sucolv (SUPS) B
1
'
a. Insoection Scoce (71707)
The inspectors observed the control room operators during the response to a loss of )
SUPS B, the activities involved in prioritizing recovery of power to the SUPS B
distribution panel, and recovery of plant instruments required for continued plant
operation.
b. Observations and Findinas
On February 4,1998, SUPS B failed and caused a loss of electrical power to
instrumentation required for continued plant operation. The CRS entered
Procedures OP-901-112, " Charging or Letdown Malfunction," and OP-901-312, " Loss of
Vital Instrument Bus." The inspectors observed the CRS directing licensed operators in
accordance with the applicable off-normal procedures. The SS directed the shift
technical advisor to verify which TS were in effect and to track time clocks associated
with the action statements in effect. Additionallicensed operators reported to the control
room to assist the shift crew as necessary.
Investigation of the cause of the trip revealed that the SUPS B inverter had blown fuses.
The power to Distribution Panel PDP3918, which is supplied by SUPS B, was restored
! by energizing the bypass power supply approximately 15 minutes after the SUPS
l tripped. The order of restoration of loads had been priontized using the basic guidance
l in Procedure OP-901-312, and field reports from nuclear plant operators verified that the
loads being restored had not been affected. The inspectors reviewed the off-normal
procedures used during recponse to the transient and noted that the guidelines were
very general in that the procedure required the operators to develop the detailed
restoration plan ad hoc. The operators demonstrated an excellent knowledge and
understanding of the safety consequences of the event.
l
All components powered from Distribution Panel PDP3918 had been restored within
approximately 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />. All TS action requirements were exited, except for TS 3.8.3.1,
which required the SUPS bus to be energized from the inverter within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. All TS
action statements had been satisfied within the required time limits. The SUPS B
inverter was repaired and returned to service within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
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The inspectors discussed the off-normal procedure weaknesses with the Operations
Manager and Operations Superintendent. They agreed to review the procedures and the
actual activities required for event mitigation for potential procedure enhancement.
c. Conclusions
The licensed operators performed in a professional manner and demonstrated excellent
- knowledge and understanding of the safety consequences of the loss of instrument
power event.
O1.2 . Control Room Observations
a. Insoection Scooe (71707)
in addition to routine daily control room observations, on March 11 and 12,1998, the J
Inspectors observed control room activities including accet.s control, operator conduct,
general operator knowledge, and shift tumover,
b. . Observations and Findinas
The inspectors reviewed Administrative Procedures OP-100-001, Revision 14, " Duties
and Responsibilities of Operators on Duty," and OP-100-007, Revision 13, " Shift
Tumover," to determine the requirements for the conduct of control room activities. The
inspectors determined that the observed operations crews were generally meeting these
requirements.
The inspectors noted that control room access controls were good. The layout of the
control room naturally funneled personnel into the SS office or to the entrance of the ,
control room proper. This arrangement minimized personnel congregating in the rear of 1
the control room. Also, extraneous conversations were maintained in the enclosed office
space behind the control room, which minimized distractions to the operators. The i
inspectors also noted that the CRS only allowed entrance to personnel requiring control I
room access for a work- and business-related activity. )
i
The inspectors observed several hours of licensed operator activity and noted the l
following:
l
. The operation staff's conduct was professional.
. The operators were generally attentive to plant status and indicators.
. Excellent communications were observed among the crew whenever one of the
- crew members left the control room area. Not only did the operators inform their
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partner and the CRS, but they also informed the SS. The inspectors did observe
the SS and the CRS brief each other on plant changes whenever one of them
retumed to the control room.
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Control room command function was clearly delineated, including any changes in
emergency response responsibilities.
,
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Alarm and annunciator response by the operators was very good. Without fail,
l the annunciators were acknowledged in an appropriate amount of time. The
! alarm was announced to the CRS and/or SS, and shift supervision acknowledged
the alarm and ensured appropriate actions were taken.
. . During shift tumovers, operators followed the requirements in
Procedure OP-100-007. The shift meeting was especially useful in providing the .
appropriate information to all key members of the shift. The CRS was able to
, coordinate conflicting maintenance and surveillance activities that had been
l previously scheduled.
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c. Conclusions 1
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in general, control room activities were conducted in a very good manner.
03 Operations Procedures and Documentation
O3.1 Station Loo Procedures Observations (71707)
The inspectors observed that with the computer logging process, the station log can be
modified anytime within the 12-hour shift. The editing can be accomplished without
appropriately identifying whether a modification was editorial or whether it should have
been identified as a corrected entry or late entry. The logging procedure in Operating )
Instruction 01-004-000, Revision 25, " Operations Narrative and Shift Logs," implied that I
the log was not final until printed at the end of the shift, and that only changes made after
that time would be subject to identifying as a late or corrected entry.
The inspectors have implemented an ongoing review of this issue. An inspection
followup item has been opened to continue review of this issue (50-382/9806-01).
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04 Operator Knowledge and Performance
04.1 Loss of Control Room Command Function
a. Insoection Scoce (71707)
The inspectors reviewed the documentation of circumstances, reviewed the statements
of the supervisors, and interviewed operations personnel regarding a loss of control room
command function.
b. Ohtervations and Findinos
On February 15,1998, with the reactor stable at 100 percent power, the CRS had
notified the SS that he was leaving the control room to get lunch. The SS had
acknowledged the CRS. The SS had been engrossed in an electrical problem, which he
was discussing with an electrician. He accompanied the electrician out of the control
room to the relay room without notifying the remaining control room operators. One of
the licensed operators noticed that neither the CRS nor the SS was in the control room
and went to the lunch room to tell the CRS that the SS had also left the control room.
The CRS reentered the control room and paged the SS to tell him that they had violated
the TS control room manning requirements, as both the SS and the CRS had been
absent from the control room for 1 minute 38 seconds.
Condition Report 98-0222 had been issued immediately following the incident. Also,
personnel statements had been written by the CRS and SS. Review of these documents
revealed no further pertinent information.
A root cause determination was performed by the licensee and it found that the incident
was an isolated human error. The inspectors agreed with this evaluation based on a
review of the documentation and interviews with the individuals who were involved.
Immediate corrective actions included counseling of the SS, issuance of a daily
instruction reminding the control room staff of the procedural and TS requirements, and
discussion of the incident at the next SS/CRS meeting. The long-term corrective actions
identified involved enhanced training during scheduled requalification and additional
management observations. Completion of the long-term actions will be verified during
review of Licensee Event Report (LER) 50-382/98-002.
TS 6.2.2.b states, in part, that at least one licensed operator shall be in the control room
when fuelis in the reactor. In addition, while the reactor is in MODE 1,2,3, or 4, at least
one licensed Senior Operator shall be in the control room.
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TS Table 6.2-1 contains a note that states, in part, that during any absence of the shift
supervisor from the control room while the unit is in MODE 1,2, 3, or 4, an individual,
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other than the shift technical advisor, with a valid senior operator license shall be
j designated to assume the control room command function. )
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Operating Procedure OP-100-001, " Duties and Responsibilities of Operators on Duty," l
l Step 5.4.1.4, states, in part, that before leaving the control room for tours,
troubleshooting, or other reasons; operators, shift superintendents, or control room
l
supervisors should inform the remaining control room operating staff of their intended
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activities and the approximate duration of these activities. Additionally, they shall verify {
that the control room command function remains appropnately delineated. l
i i
- Failure to adhere to these TS and procedural requirements demonstrates inattentiveness
to licensed duties by a senior licensed operator. However, this licensee-identified and
corrected violation is being treated as a noncited violation consistent with Section Vll.B.1
of the NRC Enforcement Policy. Specifically, the violation was identified by the licensee,
it was not willful, actions taken as a result of a previous violation should not have
corrected this problem, and appropriate corrective actions were completed by the
licensee (50-382/9806-02).
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l c. Conclusions
Inattentiveness to licensed duties by a senior reactor operator resulted in a noncited
violation of TS control room staffing requirements when both the SS and the CRS were
l absent from the control room for 1 minute 38 seconds.
!
08 Mhscellaneous Operations issues (92901)
l 08.1 (Closed) Violation S0-382/9704-01: Failure to comply with working-hour limitations for
j operations personnel.
l
Between February 1 and March 1,1997, the licensee failed to implement the
j requirements of TS 6.2.2.e and Procedure UNT-005-005, " Working Hour Policy for
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Nuclear Safety-Related Work." Working-hour policy guidelines had been exceeded in
several instances without proper approval.
The inspectors reviewed the corrective actions described in the LER and verified
that: (1) the operations, maintenance, radiation protection, and site support department
personnel had been briefed on the root cause of the event and resultant corrective
actions; (2) Revision 5 to Procedure UNT-005-005 had been implemented to clarify the
working-hour policy; (3) the quality assurance department incorporated evaluation of
organizational compliance with the working-hour policy into its audit program; and (4) the
quality assurance department audited the operations and health physics departments
and found these departments to be in compliance with the working-hour policy
guidelines.
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The inspectors concluded, based on verification of these actions, that the licensee j
appropriately addressed this violation.
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08.2 (Closed) LER 50-382/96-01* Control Room Ventilation Valve Leakage. X
l It was identified that the control room normal ventilation isolation valves were leaking
during operation of the emergency filtration system. Assuming a single failure, this
leakage could have resulted in a single individual exceeding the 30 Rem thyroid j
exposure limit in 10 CFR Part 50, Appendix A, Criterion 19 and Standard Review 4
Plan 6.4, Section 11.6. The cause of the leakage was determined to be debris that had
l
accumulated inside the valve disc region and prevented the valves from fully closing.
1
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The inspectors reviewed the root cause analysis and corrective actions and determined i
them to be appropriate. Long term corrective actions included: (1) establishing an
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18-month frequency for leak rate checkirig the isolation dampers, (2) developing a j
procedure with an administrative limit of 8 scfm to leak rate test the isolation valves, and
(3) reviewing the testing configuration for the control room pressure test to ensure
compliance with all licensing documents.
i The implementation of these corrective actions are discussed in NRC Inspection
l Report 50-382/96-21 and found to be fully satisfactory.
1
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08.3 (Closed) LER 50-382/97-012; Programmatic Breakdown of Overtime Program.
! The corrective actions for this LER are the same as the corrective actions for NRC
Violation 50-382/9704-01, discussed in Section 08.1 of this report. ,
I
l 08.4 (Closed) LER 50-382/97-018: Dropped New Fuel Assembly.
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During Refueling Outage 8, a new fuel assembly became disengaged from the spent fuel
handling tool and dropped approximately 5 inches. The assembly came to rest at a 40 ;
i angle against the side of the spent fuel pool. No other fuel assemblies were damaged ;
and no spent fuel pool liner leakage was detected. The root cause of the event was j
determined by the licensee to be human error. j
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l The inspectors reviewed the root cause analysis and considered it to be thorough and
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representative of a good self-assessment. Corrective actions included a revision to the '
l refueling procedure, training, and removal of several environmental distractions. These
l are described in NRC Inspection Report 50-382/97-08.
I
Based on the review completed by the inspectors, it was determined that the licensee
had taken the appropriate actions to address this issue. i
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11. Maintenance
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! M1 Conduct of Maintenance (61726,62707)
l The inspectors observed all or portions of the following surveillances:
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OP-903-119 Secondary Auxiliaries Quarterly Valve Tests
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OP-903-046 Emergency Feed Pump Operability Check
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OP-903-068 Emergency Diesel Generator and Subgroup Relay Train B
Operability Test
Additionally, the inspectors observed portions of Work Authorization 01167398, which
was issued to troubleshoot Control Element Assembly 14 to determine why it slipped
l approximately 5 inches while moving it.
l
l The inspectors found the conduct of these maintenance and surveillance activities to be
l good. All activities observed were performed with an appropriate authorization package
j or test procedure. The inspectors observed supervisors monitoring job progress.
M1.1 Quarterly Surveillance of Comoonent Coolino Water (CCW) Makeuo System Check l
j Valves
! 4
a. Insoection Scoce (61726) l
l The inspectors observed portions of Surveillance Procedure OP-903-119, Revision 4,
" Secondary Auxiliaries Quarterly IST Valve Tests." The operators performed the
applicable sections to leak test various CCW makeup water check valves.
j b. Observations and Findinas
l
On March 12,1998, the operators performed a quarterly leak check on two CCW
makeup system check valves. The procedure required securing CCW Makeup Pump B
for a portion of the test. Not only did the operators declare CCW Makeup System B out
of service, but also those loads sen/ed by the system. Therefore, the cascading TS
action statements for securing CCW System B, Emergency Diesel Generator B, and
Essential Chiller B were entered.
The briefing for the evolution was thorough, covered the details of the test, expected
responses, and personnel responsibilities. All appropriate personnel were present and
actively involved in the briefing. The CRS made it clear to the crew that this was not an
evolution to be rushed. When the operators arrived on station to perform the
surveillance, they found the spent resin transfer cask being moved from the minus
35-foot level. The operators and the CRS made the conservative decision to wait for the
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cask to be lifted from the area prior to beginning work. Their concern was leaving the i
CCW makeup system in a degraded state if there were problems with lifting the cask. l
The inspectors observed the operators perform the surveillance. The operators properly
followed the procedure, recorded all required information, and appeared knowledgeable j
in their tasks. They exhibited good three-part communications between each other and )
the control room. Peer checking was also properly used to ensure that the right i
component was being operated and they used appropriate cleanliness controls.
The inspectors noted that while the CRS was reviewing the procedure and drawings in
preparation for the brief, he noted that a simple addition of a drain line installed on the
nonsafety-related portion of the piping would, in the future, prevent the necessity of
securing Makeup Pump B and cause entrance into cascading TS. The CRS contacted
the system engineer who would look into the matter further.
c. Conclusions l
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The performance of the check valve leakage surveillance adequately tested the valves. I
Very good procedural compliance and questioning attitudes by all of the operations l
personnel involved in the test was noted.
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M 1.2 Emeraency Feedwater (EFW) Pumo AB Surveillance Observation '
a. Insoection Scoce (61726)
On March 12,1998, the inspectors observed the EFW Pump AB surveillance. The
surveillance was performed using Surveillance Procedure OP-903-046, Revision 14,
" Emergency Feed Pump Operability Check."
b. Observations and Findinos
The operators performed a routine run and overspeed trip check of EFW Pump AB. The
inspectors were present for the pretest briefing and for the majority of the test. The
briefing was performed by a licensed operator and contained the appropriate precautions
and limitations. However, the operator stated that the crew was familiar with the
procedure and he would not review it step by step. One of the nonficensed operators
asked several pertinent questions about the procedure. These questions, in combination
with the rest of the information presented, made the briefing information complete.
I The inspectors observed a licensed operator starting the EFW pump from the control
! room. The operator exhibited good control of the evolution. The inspectors noted that
the procedure was in constant use in the control room. The operators used good
three-part communication among each other and with the operators in the field.
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The inspectors observed the pump operate from the minus 35-foot level of the reactor
auxiliary building. Besides the operators and system engineer, there were several
mechanics in the area with measuring equipment. One of the operators was surprised
by the number of mechanics assigned to the job since they had not been present for the
briefing in the control room. The inspectors spoke to the system engineer about the
mechanics. The system engineer stated that he had been working on gathering pump
data for some time. The inspectors noted that the mechanics worked well together in
gathering the required data.
The inspectors observed the overspeed trip test of the pump. The operators then
restored the pump to service. No problems were noted with this portion of the test. ;
Procedure adherence by the operators was good. The inspectors asked several l
questions about the pump operation. The inspectors found the nonlicensed operators l
knowledge level good.
c. Conclusions
The surveillance test of the EFW turbine-driven pump was very good. The operators
were knowledgeable about the test.
M1.3 Postmaintenance Testina of Valve CVC-103
a. Observations and Findinas
i
In September 1997, SUPS SB failed as a result of an internal fault. Failure of SUPS SB
resulted in a loss of power to a number of components, one of which was
Valve CVC-103. All other components responded as designed without any problems.
Valve CVC-103 is installed in the letdown line and serves as a containment isolation
valve for the line. As such, it is required to close to prevent flow from the reactor coolant
system to the auxiliary building in the event of a line break outside containment.
When power from SUPS SB was lost, Valve CVC-103 closed, but the valve did not fully
shut, which allowed flow through the valve of approximately 25 gpm. Another valve in
the letdown line was shut to stop the flow.
Licensee personnel made a containment entry to inspect the valve to verify there was no
physical damage to the valve. After verifying no damage occurred, the licensee
inspected the valve stem travel stop nut and noted that it appeared to be misadjusted.
The stop nut was adjusted and a subsequent leak test performed. The test results
indicated no further leakage through the valve.
During review of this issue by the inspectors, it was noted that maintenance had been
performed on Valve CVC-103, and no postmaintenance test had been performed to
verify that the valve could perform its intended function of isolating letdown flow.
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The failure to provide instructions to specify postmaintenance testing of Valve CVC-103
is a violation of TS 6.8.1 (50-382/9806-03).
b. Conclusions
Valve CVC-103 did not properly perform all of its design functions because testing was
not performed after completion of maintenance.
M2 Maintenance and Material Condition of Facilities and Equipment
M2.1 Soent Fuel Pool (SFP) Overflow Corrective Action Followuo
a. Insoection Scooe (62702)
The inspectors assessed the adequacy of the licensee's corrective actions pursuant to a
SFP overflow event that occurred in May 1997. '
b. Observations and Findinas
On May 21,1997, approximately 5000 gallons of radioactive water had overflowed from
the SFP into the fuel handling building (FHB). The licensee had estimated that
approximately 2500 gallons was contained in the FHB railroad bay and that between 230
and 1850 gallons had escaped outside the FHB through the railroad bay doors, where it
had contaminated a large area of asphalt and gravel within the protected area and the
storm drain system. The remainder of the spilled fluid was captured in the reactor
auxiliary building sump and waste systems. Condition Report (CR) 97-1284 had been
initiated and an event review team was convened on May 21 to investigate the event.
The event review team had concluded that the spill had been the result of a combination
of tagging and communication errors, which had resulted in dead-heading of a
purification pump, combined with a leaking SFP purification isolation valve. The
investigation revealed that the travel stop nuts on SFP isolation Valve FS-345 (a
manually-operated diaphragm valve) had been incorrectly positioned %-inch lower than
required by the valve technical manual. The mispositioning occurred during a
maintenance activity in May 1992, when reach rods were installed per Design
Change (DC) 3211. DC 3211 had required the travel stop nuts to be removed; however,
neither DC 3211 nor the associated work authorization had contained specific
instructions as to the required position for the travel stop nuts upon replacement. This
resulted in the valve not fully blocking flow when it indicated shut. The licensee had
taken soil and liquid samples to determine if any reportable releases to the environment
had occurred and concluded that 10 CFR Part 20 limits had not been exceeded.
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! The event review team had determined that isolation Valve FS-345 and four other
diaphragm valves had extension stems installed per DC 3211, as required. These
valves were checked and the travel stop nuts were adjusted. The licensee had not
inspected any other diaphragm valves.
On February 2,1998, the inspectors performed an inspection of travel stop nuts on other
diaphragm valves in the FHB and noted the following deficiencies: )
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l Valve Condition
FS-1058 - Fuel Pool Pump B Discharge Drain No travel stop lock nut
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l FS-210 - Refueling Canal Drain Pump Discharge Loose travel stop lock nut
FS-212 - Refueling Canal Drain Pump Discharge Drain No travel stop lock nut
i s
FS-214 - Refueling Canal Drain Pump Discharge No travel stop lock nut
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isolation to Fuel Pool
The inspectors notified the licensee of the above conditions. The licensee initiated i
l CR 98-0146 to address the identified deficiencies. At the end of this inspection period, {
the licensee was in the process of inspecting approximately 800 other diaphragm valves l
installed in the plant.
l When the event team identified that the stop nut on Valve FS-345 was incorrectly
installed, the team incorrectly limited the population of other potentially affected valves to
l those modified per DC 3211. No effort was made by the licensee to inspect other similar ]
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valves to determine the full scope of the stop nut misadjustment problem. As a result, full l
and effective evaluation did not occur for the hardware deficiencies on the relatively large
population of valves.
The failure to promptly identify and correct the travel stop nut deficiencies, after having i
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attributed the misadjustment as a contributing factor to a SFP overflow event, is a
violation of Criterion XVI (50-382/9806-04).
l c. Conclusiong
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The scope of the corrective actions identified after the SFP overflow event was j
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i inadequate because other similiar diaphragm valves were not deficiencies. This is a l
violation of Criterion XVI.
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111. Engl.neerina
E1 Conduct of Engineering (37551)
E1.1 Enaineerina Evaluation of Delaved Reactor Trio Breaker (RTB) Ooenina
a. Insoection Scoce (37551)
The inspectors reviewed enginecring activities associated with evaluating the delayed
opening of RTB 2.
b. Observations and Findinas
On February 8,1998, while performing Procedure OP-903-107, " Plant Protection System
Functional Test," RTB 2 opened 15 seconds after the trip signal was initiated. RTB 6,
which is designed to open concurrently, did respond and open immediately. RTB 2 was
declared inoperable and both breakers were left in the tripped position to comply with
TS 3.3.1-13, Action 5. CR 98-0182 was written to address the issue. Electrical
maintenance technicians determined that the K2 relay had failed. The relay was
replaced, the breakers retested satisfactorily, and the RTBs were declared operable.
The K2 relay was a Potter & Brumfield MDR Model 170-1 with Date Code 9416. A
generic issue related to these relays was reported in NRC Inspection
Report 50-382/98-02, Section M2.1. Inspection Followup Item 50-382/9802-01 was
opened to track the status of the action plan to identify, evaluate, and replace MDRs prior
to failure. The inspectors determined that this relay had failed before the program had
been effectively implemented.
The K2 MDR relay was sent to Combustion Engineering in Windsor, Connecticut, for
failure analysis. The failure was determined to most likely be caused by a slight
misalignment of the shaft and top end bell. This condition caused excessive wear, a
buildup of wear materials, and binding of the shaft, which prevented full rotation. Glass
fiber contamination was also discove ed (in the grease) and may have been a
contributor.
A review of the relay history for the plant protective system indicated that the K2 relay
had been replaced in April 1997. On that occurrence, RTB 6 had been slow to open.
Failure analysis had indicated that hardened grease, mechanical binding, and grease
contamination had contributed to that failure. CR 97-0787 had been initiated.
The inspectors questioned the engineer to determine if they had checked the other three
relays in the plant protection system to identify the date codes. The response wat, that
they had not checked those relays. After checking the other relays, the date codes found
were: K1 - 9404; K3 - 9345; and K4 - 9416. Relay K2 had been replaced with Date
Code 9730. The inspectors asked if these relays were going to be replaced because
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their date codes were part of those of originalindustry concem. The reply was that they
would not be replaced unless they failed. The justification was that each relay was
tested quarterly.
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The inspectors found that the engineers had been responsive to the need for providing
root cause determination. Tne technical approach and understanding of the mechanical
problems were good.
c. Conclusions .
Engineers had been responsive to the need for developing a technical failure mechanism
for plant protective system relays.
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l E5 Engineering Staff Training and Qualification
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E5.1 Ooeration of EFW Pumo AB without Control Room Concurrence
a. Insoection Scooe (37551)
,
The inspectors reviewed the licensee's findings and corrective actions related to this l
l issue. 1
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b. Observations and Findinas l
On March 5,1998, an engineer determined that he had been operating equipment in the
plant without the SS or CRS knowledge or concurrence. He had been partially stroking j
EFW Turbine Governor Valve MS-417 by moving the stem approximately % inch for the !
purpose of detecting stem binding. The engineer wrote CR 98-0333 to address the i
issue, which involved operation of equipment in the plant without the consent of the l
control room staff. l
This activity constituted a violation of Procedure OP-100-001," Duties and
Responsibilities of Operators on Duty," Section 5.8.1.3, which stated, in part, that
l operational activities performed locally in the plant to support overall plant operating
activities must take place under the direction of or with the concurrence of the SS/CRS.
This was a repeat of Violation 50-382/9605-02. The !!censee had taken immediate steps
to stress proper conduct of any operations with plant personnel. Long-term corrective
actions had not been finalized (50-382/9806-05).
c. Conclusions ;
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An engineer inappropriate!y operrated equipment in the plant without the SS or CRS l
knowledge or concurrence.
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E8 Miscellaneous Engineering issues (92903)
1
E8.1 (Closed) Unresolved item 50-382/9704-04: Failure to have a procedure addressing
VOCs in areas serviced by engineered safety features (ESF) filtration units.
NRC Inspection Report 50-382/97-04 identified two issues that remained unresolved
pending additionalinput from the licensee and a response from the Office of Nuclear
Reactor Regulation (NRR). The first issue identified a failure to have a procedure that
specifically limited the amount of VOCs in an area that could adversely affect
safety-related ventilation charcoal adsorbers. The second issue involved use of a
waiting period in lieu of performing testing following painting in an area served by
charcoal filters. This issue was referred to NRR for resolution.
The inspectors performed a detailed review of the procedure that had been revised in
response to the first issue. Procedure PMC-002-007, " Installation Procedure
Maintenance and Construction Painting," limits the amount of VOCs in the areas that
would affect ventilation charcoal filters. A detailed engineering review was performed to
evaluate the amount of VOCs it would require in a given area to inhibit adsorption in the
charcoal filter to the extent that it could not perform its safety function. Engineering
Request Response ER-W3-97-0040, "VOC Limits for Insulation Cement and Painting in
ESF Areas," dated April 11,1997, provided conservative calculations showing the
maximum VOC loadings in critical areas. The procedure further reduces the amount of
VOC allowed in any critical area to less than that shown in the engineering evaluation.
The response from NRR was in a letter to Mr. Jerrold D. Dewease from
Jack N. Donohew, SUBJECT: "lNTERPRETATION OF FILTRATION UNIT
FREQUENCY-OF-TESTING REQUIREMENTS SPECIFIED IN THE TECHNICAL
SPECIFICATIONS AND REGULATORY GUIDE 1.52 FOR ARKANSAS NUCLEAR
ONE, UNITS 1 AND 2, GRAND GULF NUCLEAR STATION, UNIT 1, RIVER BEND
STATION, AND WATERFORD 3 STEAM ELECTRIC STATION (TAC NOS. M98367,
M98368, M98369, M98370, AND M98371)," dated September 11,1997. The oveiall
conclusion of the issued response was that the licensee had the responsibility to define
the criteria based on a well-documented, sound, and conservative technical basis. The
letter stated that the staff considered that a painting, fire, or chemical release was not
communicating with a ventilation system only if the ventilation system is not in operation
and the isolation dampers for the system are closed and leaktight thereby preventing air
from passing through the filters.
The inspectors determined that the engineering review and the procedure appropriately
addressed this unresolved issue and the licensee was in full compliance with NRC
regulations. This licensee-identified and corrected violation is being treated as a
i noncited violation consistent with Section Vll.B.1 of the NRC Enforcement Policy.
Specifically, the violation was identified by the licensee, it was not willful, actions taken as
a result of a previous violation should not have corrected this problem, and appropriate
corrective actions were completed by the licensee (50-382/9806-06).
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E8.2 (Closed) LERs 50-382/97-007-00 and 50-382/97-007-01: Refueling Water Storage I
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Pool (RWSP) Level Indication inaccuracies and Discovery of Additional Refueling Water
Storage Pool Instrument Uncertainty
The licensee discovered that the analytical limit for tha RWSP level instrument was
exceeded due to an inadequate design of the level transmitter reference leg. The low
side of each RWSP level transmitter was vented to an area filtered by the controlled
l ventilation area system, whereas the high side was connected to the RWSP. Operation
of the controlled ventilation area system caused indicated RWSP level to differ from
actuallevelin the nonconservative direction. This would have resulted in a recirculation
actuation signal being generated below the TS allowed value. ,
l
The inspectors determined that adequate corrective actions were implemented, dunng l
Refueting Outage 8, in that a design change was initiated to reroute the reference legs
for the RWSP level instruments back to the RWSP. This change eliminated any i
ventilation system interactions. The corrective actions are discussed in NRC Inspection
l Reports 50-382/97-12 and 50-382/97-27.
!
! Based on reviews performed by the inspectors, it was concluded that the licensee had
'
taken the appropriate actions to address this issue.
!
l IV. Plant Suncort
!
F8 Miscellaneous Fire Protection issues (92904)
- F8.1 (Closed) Insoection Followuo item 50-382/9708-08
- Reactor coolant pump (RCP) oil fill
i administrative controls.
There was no separate oil collection system under the remote fill lines for the RCP lube
oil system. This condition did not meet 10 CFR Part 50, Appendix R, requirements. The
licensee recognized that their system did not meet Appendix R requirements and
submitted an exemption request (Letter W3F1-97-0021, February 10,1997). The letter
addressed administrative controls that would be implemented if the licensee had to use
the RCP remote lube oil fill lines. The inspectors concluded that the controls were
generally adequate, except for monitoring levelin the reservoirs. The licensee did not
have a formal reservoir volume versus indicated level curve for either the upper or lower
RCP oil reservoir. The licensee informed the inspectors that they would generate formal
curves for both the upper and lower reservoir.
t The inspectors verified that volume versus level curves for both the upper and lower
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RCP oil reservoirs were incorporated into Volume 1 of the RCP vendor technical manual.
The actions taken by the licensee to address this issue were acceptable. ,
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V. Manaaement Meetinas
l X1 Exh Meeting Summary
The inspectors presented the inspection results to members of licensee management on
March 20,1998. The licensee acknowledged the findings presented.
- The inspectors asked the licensee whether any materials examined during the inspection 1
l should be considered proprietary. No proprietary information was identified.
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9
ATTACHMENT
SUPPLEMENTAL INFORMATION
PARTIAL LIST OF PERSONS CONTACTED
Licensee
F. J. Drummond, Director Site Support
C. M. Dugger, Vice-President, Operations
E. C. Ewing, Director, Nuclear Safety & Regulatory Affairs
C. Fugate, Operations Superintendent
T. J. Gaudet, Manager, Licensing
J. G. Hoffpauir, Manager, Operations
T. R. Leonard, General Manager, Plant Operations
G. D. Pierce, Director of Quality
D. W. Vinci, Superintendent, System Engineering
A. J. Wrape, Director, Design Engineering
INSPECTION PROCEDURES USED
IP 37551 Engineering
IP 61726 Surveillance Observation
IP 62702 Maintenance Program
IP 71707 Plant Operations
IP 92901 Followup - Operations
IP 92903 Followup - Engineering
IP 92904 Followup - Plant Support
ITEMS OPENED. CLOSED. AND DISCUSSED
Ooened
50-382/9806-01 IFl Station logkeeping procedures (Section O3.1) ,
50-382/9806-02 NCV Loss of control room command function (Section 04.1)
50-382/9806-03 VIO Postmaintenance Testing of Valve CVC-103 (Section M1.3)
50-382/9806-04 VIO Corrective Actions for Diaphragm Valves (Section M2.1)
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50-382/9806-05 VIO Operation of EFW Pump AB without control room concurrence
(Section E5.1) J1
50-382/9806-06 NCV Failure to have procedure addressing VOCs in areas serviced by i
ESF filtration units (Section E8.1)
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50-382/9806-02- NCV Loss of control room command function (Section 04.1)
50-382/9704-01 VIO Failure to comply with working-hour limitations for operations
personnel (Section 08.1).
50-382/96-011 LER Control Room Ventilation Valve Leakage (Section 08.2)
50-382/97-012 LER Programmatic Breakdown of Overtime Program (Section 08.3).
50-382/97-018 LER Dropped New Fuel Assembly (Section 08.4)
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50-382/9704-04 URI Failure to have a procedure addressing VOCs in areas serviced by
ESF filtration units (Section E8.1).
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50-382/9806-06 NCV Failure to have a procedure addressing VOCs in areas serviced by
ESF filtration units (Section E8.1).
50-382/9708-08 IFl RCP oil fill administrative controls (Section F8.1).
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50-382/97-007-00 LER RWSP Level Indication inaccuracy (Section E8.2)
50-382/97-007-01 LER RWSP Level Indication inaccuracy (Section E8.2)
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Discussed
None
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LIST OF ACRONYMS USED
CCW component cooling water
CR condition report
CFR Code of Federal Regulations
CRS control room supervisor
DC design change
ESF engineered safety features
FHB fuel handling building
gpm gallons per minute
LER licensee event report
NRC Nuclear Regulatory Commission
NRR Office of Nuclear Reactor Regulation
MDR motor-driven relay
RCP reactor coolant pump
RTB reactor trip breaker
RWSP refueling water storage pool
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SFP spent fuel pool
SS shift superintendent
SUPS station uninterruptible power supply
TS Technical Specifications
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VOC volatile organic compound
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