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| {{#Wiki_filter:**0 PS~G | | {{#Wiki_filter:**0 PS~G Public Service Electric and Gas Company 80 Park Place Newark, N.J. 07101 Phone 201 /622-7000 March 23, 1978 |
| * Public Service Electric and Gas Company 80 Park Place Newark, N.J. 07101 Phone 201 /622-7000 March 23, 1978
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| ~" | | ~" |
| *.o | | *.o |
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| Sincerely yours, Original Signed f_. P. Librizzi F. P. Librizzi General Manager - | | Sincerely yours, Original Signed f_. P. Librizzi F. P. Librizzi General Manager - |
| Electric Production CC: Director, Office of Inspection and Enforcement (30 copies) | | Electric Production CC: Director, Office of Inspection and Enforcement (30 copies) |
| Director, Office of Management Information and Program Control | | Director, Office of Management Information and Program Control 7809500:35 The Energy People 95*2001 300M 1C* 0 |
| ,----- - - - - - - -
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| 7809500:35 The Energy People 95*2001 300M 1C* 0 | |
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| Occurrence Date: | | Occurrence Date: |
| Facility: | | Facility: |
| 78-16/03L J/23/78 2/23/78 | | 78-16/03L J/23/78 2/23/78 Salem Generating Station Public Service Electric & Gas Company Hancock's Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE: |
| * Salem Generating Station Public Service Electric & Gas Company Hancock's Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:
| |
| Quadrant Power Tilt Ratio Greater than 1.02 CONDITIONS PRIOR TO OCCURRENCE: | | Quadrant Power Tilt Ratio Greater than 1.02 CONDITIONS PRIOR TO OCCURRENCE: |
| Operational Mode 1 Reactor power decreased from 100% to 70% | | Operational Mode 1 Reactor power decreased from 100% to 70% |
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| LICENSEE EVENT REPO. | | LICENSEE EVENT REPO. |
| c'owNTROL BLOCK: ~--~----...._~_ _,J Q (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) | | c'owNTROL BLOCK: ~--~----...._~_ _,J Q (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) |
| ,. "
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| 7 8 I9 N IJ LICENSEE I s I GCOOE I s l 1 14IG)IIS o I ol - I o Io I oI o I o I - I o I o25101264 I 1LICENSE LICENSE NUMBER I i 11 I i 10157 C,o.T TYPE JO I 58I 0 CON'T | | 7 8 I9 N IJ LICENSEE I s I GCOOE I s l 1 14IG)IIS o I ol - I o Io I oI o I o I - I o I o25101264 I 1LICENSE LICENSE NUMBER I i 11 I i 10157 C,o.T TYPE JO I 58I 0 CON'T |
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| !At 1315 hours following a 30% loop reduction quadrant power t i l t ratio | | !At 1315 hours following a 30% loop reduction quadrant power t i l t ratio |
| [TIIJ I was determined to be 1. 027. Action Statements for LCD 3. 2. 4 implemented.! | | [TIIJ I was determined to be 1. 027. Action Statements for LCD 3. 2. 4 implemented.! |
| []]3J !Action Statement terminated at 1345 hours with QPT ratio less than 1.02.1 CIT!] | | [))3J !Action Statement terminated at 1345 hours with QPT ratio less than 1.02.1 CIT!] |
| 7 8 9. s SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUB CODE suacoDE | | 7 8 9. s SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUB CODE suacoDE |
| [ill] | | [ill] |
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[Table view] Category:Licensee Event Report (LER)
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[Table view] |
Text
- 0 PS~G Public Service Electric and Gas Company 80 Park Place Newark, N.J. 07101 Phone 201 /622-7000 March 23, 1978
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Dear Mr. Grier:
LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 78-16/03L Pursuant to the requirements of Salem Generating Station Unit No. 1 Technical Specifications, Section 6.9.1.9.b, we are submitting Licensee Event Report for Reportable Occurrence 78-16/03L. This report is required within thirty (30) days of the occurrence.
Sincerely yours, Original Signed f_. P. Librizzi F. P. Librizzi General Manager -
Electric Production CC: Director, Office of Inspection and Enforcement (30 copies)
Director, Office of Management Information and Program Control 7809500:35 The Energy People 95*2001 300M 1C* 0
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_-,- Report Number:
Report Date:
Occurrence Date:
Facility:
78-16/03L J/23/78 2/23/78 Salem Generating Station Public Service Electric & Gas Company Hancock's Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:
Quadrant Power Tilt Ratio Greater than 1.02 CONDITIONS PRIOR TO OCCURRENCE:
Operational Mode 1 Reactor power decreased from 100% to 70%
DESCRIPTION OF OCCURRENCE:
At 1315 hours0.0152 days <br />0.365 hours <br />0.00217 weeks <br />5.003575e-4 months <br /> following a .30% load reduction the Power Range Channel 1 deviation alarm was received in the Control Room. Quadrant Power Tilt Ratio was determined to be 1.027 on N-41 upper. Technical Specification 3.2.4 Action Statement a.2 was implemented. At 1345 hours0.0156 days <br />0.374 hours <br />0.00222 weeks <br />5.117725e-4 months <br /> Action Statement for LCO 3.2.4 was terminated with QPT calculation less than 1.02. QPT calculations continued for 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. All calculations were less than 1.02.
DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:
The cause of this occurrence was the load reduction which resulted in flux oscillations resulting in the Quadrant Power Tilt Ratio exceeding 1.02.
ANALYSIS. OF OCCURRENCE:
Technical Specification Action Statement for LCO 3.2.4 states that ...
With the Quadrant Power Tilt Ratio determined to exceed 1.02 but< 1.09:
Within 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />s:
a) Either reduce the Quadrant Power Tilt Ratio to within its limit, or b) Reduce Thermal Power at least 3% from Rated Thermal Power for each 1% of indicated Quadrant Power Tilt Ratio in excess of 1.0 and similarly reduce the Power Range Neutron Flux-High Trip Setpoints within the next 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.
Verify that the Quadrant Power Tilt Ratio is within its limit within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> after exceeding the limit or reduce Thermal Power to less than 50% of Rated Thermal Power within the next 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> and reduce the Power Range Neutron Flux-High Trip setpoints to < 55% of Rated Thermal Power within the next 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.
LER 78-16/03L ~ Identify and correct the cause of the out of limit condition prior to increasing Thermal Power; subsequent Power Operation above 50%
of Rated Thermal power may proceed provided that the Quadrant Power Tilt Ratio is verified within its limit at least once per hour for 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> or until verified acceptable at 95% or greater Rated Thermal Power.
The Quadrant Power Tilt Ratio was reduced to within its limits within thirty minutes therefore no further action was required.
CORRECTIVE ACTION:
This occurrence is considered to be normal following a large load change. No long term corrective action is planned.
FAILURE DATA:
N/A Prepared by T. L. Spencer Manage~ - Salem Generating Station SORC Meeting No.* 14-78
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LICENSEE EVENT REPO.
c'owNTROL BLOCK: ~--~----...._~_ _,J Q (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
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7 8 I9 N IJ LICENSEE I s I GCOOE I s l 1 14IG)IIS o I ol - I o Io I oI o I o I - I o I o25101264 I 1LICENSE LICENSE NUMBER I i 11 I i 10157 C,o.T TYPE JO I 58I 0 CON'T
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- ~~~~~ LJJ© I o I s ! o! o I oI 2 I 7 I 2 \GI o I 2 I 2 60 61 DOCKET NUMBER 68 69 I3I EVENT DATE 7 I a IG) I;p I1 I 2 I 3 I 1 I a IG) 74 7 REPORT DATE BO EVENT DESCRIPTION ANO PROBABLE CONSEQUENCES @
!At 1315 hours0.0152 days <br />0.365 hours <br />0.00217 weeks <br />5.003575e-4 months <br /> following a 30% loop reduction quadrant power t i l t ratio
[TIIJ I was determined to be 1. 027. Action Statements for LCD 3. 2. 4 implemented.!
[))3J !Action Statement terminated at 1345 hours0.0156 days <br />0.374 hours <br />0.00222 weeks <br />5.117725e-4 months <br /> with QPT ratio less than 1.02.1 CIT!]
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J2 ACTION FUTURE EFFECT SHUTDOWN (::;:'.;\ ATTACHMENT NPRC-4 PRIME COMP. COMPONENT TAl<EN ACTION ON PL.ANT METHOD HOURS Id SUBMITTED FORM :;us. SUPPLIER MANUFACTURER W@W@ LU@
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4J I z I9 J9 I9 CAUSE DESCRIPTION ANO CORRECTIVE ACTIONS @
.u:::m ]This occurrence was the result of a 30% load reduction which resulted CIIIJ !in QPT ratio exceeding 1. 02. This is an exvected occurrence and no o:JJJ 1corrective action is planned.
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v:::J METHOOOF (.;:;\
STATUS '4 POWER OTHER STATUS DISCOVERY DISCOVERY OESCRIPTlON ~
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45 46 BC ACTIVITY CONTENT Q\
RELEASED OF REl.EASE AMOUNT OF ACTIVITY ~ LOCATION CF RELEASc @
GE] lz.J@ W@I N/A N/A 8 9 10 11 44 45 PERSONNEL EXPOSURES r:::;::..,
NUMBER ~TYPE DESCRll'TlON 82] I o I o I o lW@.____N-'/_A_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ __
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NUMBER DESCRIPTION~
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TYPE DESCRIPTION '-::)
~ W@ N/A 1 a 9 10 PUBLICITY (';;";\
ISSUEOQ OESC1'11P'TION ~
NRC USE ONLY ITEJ 8 L.z.J6 ll IC N/A I I I I ! II 1 I I I 68 69 2 NAME OF PREPARER _ _ _T __._L_._s_o.,..e_n_c_e~r ________ (609)365-7000 Salen Ex:
PHONE:
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