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{{#Wiki_filter:**0        PS~G
{{#Wiki_filter:**0        PS~G Public Service Electric and Gas Company 80 Park Place Newark, N.J. 07101  Phone 201 /622-7000 March 23, 1978
* Public Service Electric and Gas Company 80 Park Place Newark, N.J. 07101  Phone 201 /622-7000 March 23, 1978
                                                                                             ~"
                                                                                             ~"
                                                                                             *.o
                                                                                             *.o
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Sincerely yours, Original Signed f_. P. Librizzi F. P. Librizzi General Manager -
Sincerely yours, Original Signed f_. P. Librizzi F. P. Librizzi General Manager -
Electric Production CC:    Director, Office            of Inspection and Enforcement          (30 copies)
Electric Production CC:    Director, Office            of Inspection and Enforcement          (30 copies)
Director, Office            of Management Information and          Program Control
Director, Office            of Management Information and          Program Control 7809500:35 The Energy People 95*2001 300M 1C* 0
                                                            ,----- - - - - - - -
7809500:35 The Energy People 95*2001 300M 1C* 0


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Occurrence Date:
Occurrence Date:
Facility:
Facility:
78-16/03L J/23/78 2/23/78
78-16/03L J/23/78 2/23/78 Salem Generating Station Public Service Electric & Gas Company Hancock's Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:
* Salem Generating Station Public Service Electric & Gas Company Hancock's Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:
Quadrant Power Tilt Ratio Greater than 1.02 CONDITIONS PRIOR TO OCCURRENCE:
Quadrant Power Tilt Ratio Greater than 1.02 CONDITIONS PRIOR TO OCCURRENCE:
Operational Mode 1 Reactor power decreased from 100% to 70%
Operational Mode 1 Reactor power decreased from 100% to 70%
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LICENSEE EVENT REPO.
LICENSEE EVENT REPO.
c'owNTROL BLOCK:            ~--~----...._~_ _,J Q                                          (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
c'owNTROL BLOCK:            ~--~----...._~_ _,J Q                                          (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
      ,.                                                                                "
  ~
  ~
7        8 I9 N IJ LICENSEE I s I GCOOE  I s l 1 14IG)IIS o I ol - I o Io                      I oI o I o I - I o I o25101264 I 1LICENSE LICENSE NUMBER I i 11    I i 10157 C,o.T TYPE JO I 58I 0 CON'T
7        8 I9 N IJ LICENSEE I s I GCOOE  I s l 1 14IG)IIS o I ol - I o Io                      I oI o I o I - I o I o25101264 I 1LICENSE LICENSE NUMBER I i 11    I i 10157 C,o.T TYPE JO I 58I 0 CON'T
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                 !At 1315 hours following a 30% loop reduction quadrant power t i l t ratio
                 !At 1315 hours following a 30% loop reduction quadrant power t i l t ratio
[TIIJ I was determined to be 1. 027. Action Statements for LCD 3. 2. 4 implemented.!
[TIIJ I was determined to be 1. 027. Action Statements for LCD 3. 2. 4 implemented.!
[]]3J !Action Statement terminated at 1345 hours with QPT ratio less than 1.02.1 CIT!]
[))3J !Action Statement terminated at 1345 hours with QPT ratio less than 1.02.1 CIT!]
7        8    9.                                                                                                                                                                              s SYSTEM              CAUSE                CAUSE                                                            COMP.          VALVE CODE                CODE            SUBCODE                      COMPONENT CODE                      SUB CODE        suacoDE
7        8    9.                                                                                                                                                                              s SYSTEM              CAUSE                CAUSE                                                            COMP.          VALVE CODE                CODE            SUBCODE                      COMPONENT CODE                      SUB CODE        suacoDE
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Latest revision as of 01:00, 17 March 2020

LER 1978-016-03 for Salem Unit 1 Excessive Tilt Ratio of Quadrant Power
ML19031B168
Person / Time
Site: Salem  PSEG icon.png
Issue date: 03/23/1978
From: Librizzi F
Public Service Electric & Gas Co
To: Grier B
NRC/IE, NRC Region 1
References
LER 1978-016-03
Download: ML19031B168 (4)


Text

    • 0 PS~G Public Service Electric and Gas Company 80 Park Place Newark, N.J. 07101 Phone 201 /622-7000 March 23, 1978

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Dear Mr. Grier:

LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 78-16/03L Pursuant to the requirements of Salem Generating Station Unit No. 1 Technical Specifications, Section 6.9.1.9.b, we are submitting Licensee Event Report for Reportable Occurrence 78-16/03L. This report is required within thirty (30) days of the occurrence.

Sincerely yours, Original Signed f_. P. Librizzi F. P. Librizzi General Manager -

Electric Production CC: Director, Office of Inspection and Enforcement (30 copies)

Director, Office of Management Information and Program Control 7809500:35 The Energy People 95*2001 300M 1C* 0

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I

_-,- Report Number:

Report Date:

Occurrence Date:

Facility:

78-16/03L J/23/78 2/23/78 Salem Generating Station Public Service Electric & Gas Company Hancock's Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:

Quadrant Power Tilt Ratio Greater than 1.02 CONDITIONS PRIOR TO OCCURRENCE:

Operational Mode 1 Reactor power decreased from 100% to 70%

DESCRIPTION OF OCCURRENCE:

At 1315 hours0.0152 days <br />0.365 hours <br />0.00217 weeks <br />5.003575e-4 months <br /> following a .30% load reduction the Power Range Channel 1 deviation alarm was received in the Control Room. Quadrant Power Tilt Ratio was determined to be 1.027 on N-41 upper. Technical Specification 3.2.4 Action Statement a.2 was implemented. At 1345 hours0.0156 days <br />0.374 hours <br />0.00222 weeks <br />5.117725e-4 months <br /> Action Statement for LCO 3.2.4 was terminated with QPT calculation less than 1.02. QPT calculations continued for 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. All calculations were less than 1.02.

DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:

The cause of this occurrence was the load reduction which resulted in flux oscillations resulting in the Quadrant Power Tilt Ratio exceeding 1.02.

ANALYSIS. OF OCCURRENCE:

Technical Specification Action Statement for LCO 3.2.4 states that ...

With the Quadrant Power Tilt Ratio determined to exceed 1.02 but< 1.09:

Within 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />s:

a) Either reduce the Quadrant Power Tilt Ratio to within its limit, or b) Reduce Thermal Power at least 3% from Rated Thermal Power for each 1% of indicated Quadrant Power Tilt Ratio in excess of 1.0 and similarly reduce the Power Range Neutron Flux-High Trip Setpoints within the next 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.

Verify that the Quadrant Power Tilt Ratio is within its limit within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> after exceeding the limit or reduce Thermal Power to less than 50% of Rated Thermal Power within the next 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> and reduce the Power Range Neutron Flux-High Trip setpoints to < 55% of Rated Thermal Power within the next 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.

LER 78-16/03L ~ Identify and correct the cause of the out of limit condition prior to increasing Thermal Power; subsequent Power Operation above 50%

of Rated Thermal power may proceed provided that the Quadrant Power Tilt Ratio is verified within its limit at least once per hour for 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> or until verified acceptable at 95% or greater Rated Thermal Power.

The Quadrant Power Tilt Ratio was reduced to within its limits within thirty minutes therefore no further action was required.

CORRECTIVE ACTION:

This occurrence is considered to be normal following a large load change. No long term corrective action is planned.

FAILURE DATA:

N/A Prepared by T. L. Spencer Manage~ - Salem Generating Station SORC Meeting No.* 14-78

~----~--~----~~-

N l).c-:~.lHH*1.366 (7*17?

LICENSEE EVENT REPO.

c'owNTROL BLOCK: ~--~----...._~_ _,J Q (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

~

7 8 I9 N IJ LICENSEE I s I GCOOE I s l 1 14IG)IIS o I ol - I o Io I oI o I o I - I o I o25101264 I 1LICENSE LICENSE NUMBER I i 11 I i 10157 C,o.T TYPE JO I 58I 0 CON'T

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~~~~~ LJJ© I o I s ! o! o I oI 2 I 7 I 2 \GI o I 2 I 2 60 61 DOCKET NUMBER 68 69 I3I EVENT DATE 7 I a IG) I;p I1 I 2 I 3 I 1 I a IG) 74 7 REPORT DATE BO EVENT DESCRIPTION ANO PROBABLE CONSEQUENCES @

!At 1315 hours0.0152 days <br />0.365 hours <br />0.00217 weeks <br />5.003575e-4 months <br /> following a 30% loop reduction quadrant power t i l t ratio

[TIIJ I was determined to be 1. 027. Action Statements for LCD 3. 2. 4 implemented.!

[))3J !Action Statement terminated at 1345 hours0.0156 days <br />0.374 hours <br />0.00222 weeks <br />5.117725e-4 months <br /> with QPT ratio less than 1.02.1 CIT!]

7 8 9. s SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUB CODE suacoDE

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20 SEQUENTIAL OCCURRENCE REPORT REVISION

{.:;'\ LE A *AO CV ENT YE.1'.R REPORT NO. CODE TYPE

  • NC.

~ REPORT NUMB EB I7 I 8I 21 22 l.=:=J 23 I o 11 I 6 I 24 26 27 I oI 3I 2S :29 LlJ JO L=1 31 w

J2 ACTION FUTURE EFFECT SHUTDOWN (::;:'.;\ ATTACHMENT NPRC-4 PRIME COMP. COMPONENT TAl<EN ACTION ON PL.ANT METHOD HOURS Id SUBMITTED FORM :;us. SUPPLIER MANUFACTURER W@W@ LU@

JJ J4 JS W

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37 010 I 010 40 I W@

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4J I z I9 J9 I9 CAUSE DESCRIPTION ANO CORRECTIVE ACTIONS @

.u:::m ]This occurrence was the result of a 30% load reduction which resulted CIIIJ !in QPT ratio exceeding 1. 02. This is an exvected occurrence and no o:JJJ 1corrective action is planned.

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7 8 9 B FACILITY f:iQ\

v:::J METHOOOF (.;:;\

STATUS '4 POWER OTHER STATUS DISCOVERY DISCOVERY OESCRIPTlON ~

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U:J I 0 I 7 I 0 l@I 9 . 10 12 l'J N/A 44 LJiJ~~I_...Q=P~T'--'r=-=a~t~i~o"--~c~a~l~c~u==l~a~t~i~o~n:.:-~~~~~~

45 46 BC ACTIVITY CONTENT Q\

RELEASED OF REl.EASE AMOUNT OF ACTIVITY ~ LOCATION CF RELEASc @

GE] lz.J@ W@I N/A N/A 8 9 10 11 44 45 PERSONNEL EXPOSURES r:::;::..,

NUMBER ~TYPE DESCRll'TlON 82] I o I o I o lW@.____N-'/_A_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ __

7 B 9 11 12 lJ PERSONNEL. INJURIES (;"":;\

NUMBER DESCRIPTION~

~ I 0 I 0 I 0 I@

1 a g 11 L.OSS OF OR DAMAGE TO F.C.CILITY '4J' N A

~12:-------__,_~------------------------------~

TYPE DESCRIPTION '-::)

~ W@ N/A 1 a 9 10 PUBLICITY (';;";\

ISSUEOQ OESC1'11P'TION ~

NRC USE ONLY ITEJ 8 L.z.J6 ll IC N/A I I I I ! II 1 I I I 68 69 2 NAME OF PREPARER _ _ _T __._L_._s_o.,..e_n_c_e~r ________ (609)365-7000 Salen Ex:

PHONE:

528