ML19031A896

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LER 1978-022-01 for Salem Unit 1 Seismic Test Results for NEMA 12 Enclosures
ML19031A896
Person / Time
Site: Salem  PSEG icon.png
Issue date: 04/17/1978
From: Librizzi F
Public Service Electric & Gas Co
To: Grier B
NRC/IE, NRC Region 1
References
LER 1978-022-01
Download: ML19031A896 (4)


Text

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Public Service Electric and Gas Company 80 Park Place Newark, N.J. 07101 Phone 201 /622-7000 April 17, 1978 Mr. Boyce H. Grier

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Director of USNRC S:'. '°

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Dear Mr. Grier:

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0 LICENSE NO. DPR-70 (.0 0

DOCKET NO. 50-272 REPORTABLE OCCURRENCE 78-22/0lT Pursuant to the requirements of Salem Generating Station Unit No. 1 Environmental Technical Specifications, Section 6.9.1.8.i, we are submitting*Licensee Event Report for Reportable Occurrence 78-22/0lT. This report is required within fourteen (14) days of the occurrence.

Sincerely yours, F. P. Librizzi General Manager -

Electric Production CC: Director, Office of Inspection and Enforcement (40 copies)

Director, Office of Management Information and

( 3 copies) Program control REGul/lIO~fy DUC1{tI .fl.LE tOrY The Energy People 95-2001 300M 10*7*

Report Number: 78-22/0lT Report Date: 4/17/78 Occurrence Date: 4/4/78 Facility: Salem Generating Station Public Service Electric & Gas Company Hancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:

Reactor Coolant Low Flow Protection Seismic Qualification Deficiency CONDITIONS PRIOR TO OCCURRENCE:

N/A DESCRIPTION OF OCCURRENCE:

During a review of seismic test data for NEMA 12 panel enclosures, it was found that a transmitter manufactured by Fischer and Porter, Model No. 10B2496, was used in a NEMA 12 enclosure for monitoring reactor coolant flow. This transmitter had a high output deviation during the seismic test which exceeded acceptable tolerances. This transmitter in the noted application provides a low flow signal to the solid state protection system for reactor trip. The tra~smitters' high output deviation during a seismic event could prevent it from performing its required function. This is only applicable if. the reactor coolant low flow condition occurs in coincidence with a seismic event. Test reports indicate that the transmitter output returns to normal following the seismic disturbance.

DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:

The Fischer and Porter 10B2496 transmitter experienced the high out-put deviation during the seismic test due to vibratory motion of the instrument mounting plate within the NEMA 12 enclosure. The sub-panel mounting plate was not stiff enough to adequately support the heavy lOB2496 transmitter. As a result, this transmitter was subjected to high vibration levels which caused its output to be offset in the upscale direction during the test. Subsequent inspection and cali-bration checks showed no damage or significant shift in transmitter accuracy.

LER 78-22/0lT ANALYSIS OF OCCURRENCE:

Sufficient diversity exists for protection against loss of reactor coolant flow transients to overcome the failure of one protection system parameter. However, if the cause of a loss in reactor coolant flow is not electrical in nature, the reactor coolant low flow transmitters are especially important. With the previously described condition existing, the low reactor coolant flow reactor trip may not have been initiated during a seismic everit if needed within the time limitations imposed by the Technical Specifications. Eventually, the overtemperature ~T reactor trip and/or the low reactor coolant flow reactor trip (when the seismic disturbance had subsided) would be initiated.

CORRECTIVE ACTION:

The installation of a unistrut to stiffen the sub-panel mounting plate in the NEMA 12 panel and enlarging the instrument mounting bracket will correct the output deviation of the transmitter to within acceptable tolerances during a seismic event. Confirmatory seismic tests have been performed demonstrating this design. This change will be incorporated in accordance with DCR ED-0357. Panel modifications will be completed prior to the unit returning to service from the present outage.

FAILURE DATA:

N/A

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Prepared by T. L. Spencer

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Manager -*Salem Generating Statior SORC Meeting No. 22-78

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e NRC FORM 366 U.S. NUCLEAR REGULATUAY COMMISSION *.77 l LICENSEE EVENT REPORT

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I During review of seismic test results for NEMA 12 enclosures, it was C£:ID 1determined that Fischer & Porter 10B2496 transmitters utilized in reacto~

~ 1coolant low flow monitoring, had a high output deviation during seismic CQ:ITI 1test. This high output deviation causes inoperability during seismic

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8 9 ao FACILITY METHOD OF STATUS  % POWER OTHER STATUS DISCOVERY DISCOVERY DESCRIPTION @

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NAMEOFPREPARER--~~~~-~*--L-.....___s_o ___e~n~c;;;...;;;e~r'--~~~~~~ P~ONE: (609)365-7000 Salen ~xt.~

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